LER-1979-004, /01T-0 on 790226:during Containment Insp After Outage,Weld Leak Discovered on Controlled bleed-off Line on Reactor Coolant Pump RC-3C.Caused by Vibration Induced Fatigue.Repairs Performed |
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| 2851979004R01 - NRC Website |
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60 61 OOCKET NUMSER 68 69 EVENT OATE 74 75 REPORT D ATE 80 EVENT DESCRIPTION AND PROBABLE CONSEQUENCES h o 2 l During containment inspection following a unit outage a veld leak vas discovered I
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I en the controlled bleed-off line on Reactor Coolant Pump RC-30.
The leak rate l
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Ioisi Specification 2.1.h leakage limits. The unit was placed in a hot shutdown l
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10 11 12 13 18 19 20 SEQU ENTI AL OCCUNRENCE REPORT REVISION ggq po EVENT YEAR REPORT NO.
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33 34 35 36 31 40 di 42 43 44 47 CAUSE DESCRIPTION AND CORRECTIVE ACTIONS 1 o l The veld failu e oc~ ~ad d"a % vibration induced fatione.
Retair was I
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vas successfully hydroed in accordance with an approved procedure.
EEAR FC-Tb-63 3
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% POWER OTHER STATUS OIS O RY DISCOVERY OESCRIPTION NA l
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,ERSCNNE L IN3u' RIES NUMBER OESCRIPTION l
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8 9 11 12 LOSS OF OR DAMAGE TO FACILITY TYPE CESCRIPTION l
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D. Jones /R. Andrevs PHONE:
NAME OF PREPARER
LER 79-00h C=aha Public Power District Fort Calhoun Station Unit No.1 Docket No. 05000285 Attachment No. 1 Analysis of Occurrence / Safety Analysis The reactor coolant system leak experienced was well within Tech-nical Specification 2.1.h, hence, a limiting condition for operation was not violated.
Since this failure did result in " abnormal degradation" of the reactor coolant pressure boundary and was not the result of packing or gasket leakage, it has been classified as a reportable occurrence.
The leakage experienced was less that 0.2 gym and did not contribute to any detectable increase in containment activity or dev point.
Since all activity released was confined to the containment structure, the health and safety of the public was not endangered by this occurrence.
LER 79-00h C=aha Public Power District Fort Calhoun Station Unit No.1 Docket No. 05000285 Attachment No. 2
Corrective Action
1.
Prior to plant startup, the veld failure on RC-3C controlled bleed-off line was repaired.
2.
EIAR 76-50 was submitted as a result of two previous failures of this type on RC-3C over two years ago.
Controlled bleed-off line restraint was evaluated at that time and all required restraints were verified to be properly installed.
EEAR FC-78-63 has been submitted to investigate vibration on Reactor Coolant Pump RC-3C which is inducing vibration on the controlled bleed-off piping.
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., s LER 79-00h Omaha Public Power District Fort Calhoun Station Unit No. 1 Docket No. 05000285 Attachment No. 3 Failure Data This is the third instance where veld leakage has occurred on Reactor Coolant Pump RC-3C controlled bleed-off line.
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| 05000285/LER-1979-001, Forwards LER 79-001/01T-0 | Forwards LER 79-001/01T-0 | | | 05000285/LER-1979-001-01, /01T-0 on 790118:during Check of Diesel Driven Fire Pump,Engine Cooling Fluid Boiled Out of Holding Tank. Diesel Engine Cooling Sys Refilled & Manual Isolation Valve Found Closed.Valve Opened & Fire Pump Returned to Svc | /01T-0 on 790118:during Check of Diesel Driven Fire Pump,Engine Cooling Fluid Boiled Out of Holding Tank. Diesel Engine Cooling Sys Refilled & Manual Isolation Valve Found Closed.Valve Opened & Fire Pump Returned to Svc | | | 05000285/LER-1979-002-03, /03L-0 on 790117:reactor Protective Sys for Axial Power Distribution Channel a Trip Setpoint Fluctuated Nonconservatively.Caused by Bell & Howell Potentiometer Module Part 384612/001 Failure | /03L-0 on 790117:reactor Protective Sys for Axial Power Distribution Channel a Trip Setpoint Fluctuated Nonconservatively.Caused by Bell & Howell Potentiometer Module Part 384612/001 Failure | | | 05000285/LER-1979-002, Forwards LER 79-002/03L-0 | Forwards LER 79-002/03L-0 | | | 05000285/LER-1979-003, Forwards LER 79-003/03L-1 | Forwards LER 79-003/03L-1 | | | 05000285/LER-1979-003-03, /03L-1 on 790127:during Containment Pressure Release,Containment Air Monitor Readings Were Abnormally Low.Caused by Closed Isolation Valves.Containment Ventilation Valves Were Closed & Pressure Valves Opened | /03L-1 on 790127:during Containment Pressure Release,Containment Air Monitor Readings Were Abnormally Low.Caused by Closed Isolation Valves.Containment Ventilation Valves Were Closed & Pressure Valves Opened | | | 05000285/LER-1979-004-01, /01T-0 on 790226:during Containment Insp After Outage,Weld Leak Discovered on Controlled bleed-off Line on Reactor Coolant Pump RC-3C.Caused by Vibration Induced Fatigue.Repairs Performed | /01T-0 on 790226:during Containment Insp After Outage,Weld Leak Discovered on Controlled bleed-off Line on Reactor Coolant Pump RC-3C.Caused by Vibration Induced Fatigue.Repairs Performed | | | 05000285/LER-1979-004, Forwards LER 79-004/01T-0 | Forwards LER 79-004/01T-0 | | | 05000285/LER-1979-005-03, /03L-0 on 790226:at 15% Power C Channel Loss of Load Trip Did Not Annunciate.Caused by Bistable Multivibrator Set to 18.1%.Bistable Reset & Surveillance Test Performed | /03L-0 on 790226:at 15% Power C Channel Loss of Load Trip Did Not Annunciate.Caused by Bistable Multivibrator Set to 18.1%.Bistable Reset & Surveillance Test Performed | | | 05000285/LER-1979-005, Forwards LER 79-005/03L-0 | Forwards LER 79-005/03L-0 | | | 05000285/LER-1979-007-01, /01T-3:on 800305,during Review Required by IE Bulletin 79-01,Barksdale Pressure Switch Not Found Environmentally Qualified.Caused by Switch Not Being Properly Specified for Intended Svc.Switch Will Be Upgraded | /01T-3:on 800305,during Review Required by IE Bulletin 79-01,Barksdale Pressure Switch Not Found Environmentally Qualified.Caused by Switch Not Being Properly Specified for Intended Svc.Switch Will Be Upgraded | | | 05000285/LER-1979-008, Forwards LER 79-008/03L-0 | Forwards LER 79-008/03L-0 | | | 05000285/LER-1979-008-03, /03L-0 on 790321:during Normal Operation,Loop Safety Injection Valve Failed to Open from Lockout Relay Activation.Caused by Dirty Auxiliary Interlock Switch. Switch Cleaned | /03L-0 on 790321:during Normal Operation,Loop Safety Injection Valve Failed to Open from Lockout Relay Activation.Caused by Dirty Auxiliary Interlock Switch. Switch Cleaned | | | 05000285/LER-1979-013-03, /03L-0 on 790625:during Normal Operation,Hot Leg Temp Indications C/TI-122H Failed Low.Caused by Power Supply Failure Due to Blown Fuse.Ge/Mac Power Supply Model GR700 Replaced & Sys Returned to Normal | /03L-0 on 790625:during Normal Operation,Hot Leg Temp Indications C/TI-122H Failed Low.Caused by Power Supply Failure Due to Blown Fuse.Ge/Mac Power Supply Model GR700 Replaced & Sys Returned to Normal | | | 05000285/LER-1979-013, Forwards LER 79-013/03L-0 | Forwards LER 79-013/03L-0 | | | 05000285/LER-1979-014, Forwards LER 79-014/01T-0 | Forwards LER 79-014/01T-0 | | | 05000285/LER-1979-014-01, /01T-0 on 790515:ASCO Solenoid Valves Lacked Sufficient Environ Qualification Data.Caused by Inadequate Specs During Design & Installation Period.Valves Will Be Replaced Following 1980 Refueling Outage | /01T-0 on 790515:ASCO Solenoid Valves Lacked Sufficient Environ Qualification Data.Caused by Inadequate Specs During Design & Installation Period.Valves Will Be Replaced Following 1980 Refueling Outage | | | 05000285/LER-1979-015, Forwards LER 79-015/01T-0 | Forwards LER 79-015/01T-0 | | | 05000285/LER-1979-015-01, /01T-0 on 790511:seismic Support Appeared Inadequate for Component Cooling Water piping-to-containment Cooling & Filtering Unit VA-3A.Analyses Indicated That Clamping piping-to-cooling Unit Will Provide Needed Support | /01T-0 on 790511:seismic Support Appeared Inadequate for Component Cooling Water piping-to-containment Cooling & Filtering Unit VA-3A.Analyses Indicated That Clamping piping-to-cooling Unit Will Provide Needed Support | | | 05000285/LER-1979-016-01, /01T-0 on 790517:testing on First Removed Irradiated Surveillance Capsule Showed Higher than Predicted Nil Ductility Transition Temp New Pressure.Temp Limitation Curves Have Been Developed | /01T-0 on 790517:testing on First Removed Irradiated Surveillance Capsule Showed Higher than Predicted Nil Ductility Transition Temp New Pressure.Temp Limitation Curves Have Been Developed | | | 05000285/LER-1979-016, Forwards LER 79-016/01T-0 | Forwards LER 79-016/01T-0 | | | 05000285/LER-1979-017-03, /03L-0 on 790724:during Normal Operation,D Channel Wide Range Nuclear Instrumentation Failed W/Complete Loss of Power.Caused by Blown Main Power Fuses.Fuses Replaced & Instrumentation Placed in Svc | /03L-0 on 790724:during Normal Operation,D Channel Wide Range Nuclear Instrumentation Failed W/Complete Loss of Power.Caused by Blown Main Power Fuses.Fuses Replaced & Instrumentation Placed in Svc | | | 05000285/LER-1979-017, Forwards LER 79-017/03L-0 | Forwards LER 79-017/03L-0 | | | 05000285/LER-1979-018, Forwards LER 79-018/03L-0 | Forwards LER 79-018/03L-0 | | | 05000285/LER-1979-018-03, /03L-0 on 790724:steam Generator a Pressure Indicator Ccontroller for C Channel Would Not Reset.Caused by Failure of Sigma Meter Integrally Installed Trip Setpoint.Trip Circuit Replaced & Meter Calibr | /03L-0 on 790724:steam Generator a Pressure Indicator Ccontroller for C Channel Would Not Reset.Caused by Failure of Sigma Meter Integrally Installed Trip Setpoint.Trip Circuit Replaced & Meter Calibr | | | 05000285/LER-1979-019-03, /03L-0:on 791005,during Normal Rotation of Component Cooling Water Heat Exchangers,Inlet Valve Would Not Operate from Control Room Remote Switch.Caused by Failed Plastic Piston Assembly in Actuator.Assembly Replaced | /03L-0:on 791005,during Normal Rotation of Component Cooling Water Heat Exchangers,Inlet Valve Would Not Operate from Control Room Remote Switch.Caused by Failed Plastic Piston Assembly in Actuator.Assembly Replaced | | | 05000285/LER-1979-020, Forwards LER 79-020/03L-0 | Forwards LER 79-020/03L-0 | | | 05000285/LER-1979-020-03, /03L-0:on 791031,during Insps of Accessible Piping,Eight Snubbers on Safety Injection Sys Piping Found Inoperable.Caused by Improper Installation of Anchor Bolts. Base Plate Redesigned & Anchor Bolts Reinstalled | /03L-0:on 791031,during Insps of Accessible Piping,Eight Snubbers on Safety Injection Sys Piping Found Inoperable.Caused by Improper Installation of Anchor Bolts. Base Plate Redesigned & Anchor Bolts Reinstalled | | | 05000285/LER-1979-021-21, /21L-0:on 791106,during Insp Required by IE Bulletin 79-14 Re safety-related Piping Sys,Discrepancies Found Between Design Documents & as-built Configuration of Seismic Restraints.Caused by Probable QC Installation Error | /21L-0:on 791106,during Insp Required by IE Bulletin 79-14 Re safety-related Piping Sys,Discrepancies Found Between Design Documents & as-built Configuration of Seismic Restraints.Caused by Probable QC Installation Error | | | 05000285/LER-1979-021, Forwards LER 79-021/21L-0 | Forwards LER 79-021/21L-0 | |
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