05000321/LER-1979-017-03, /03L-1 on 790227:variations in Speed of HPCI Turbine Occurred During Test.Caused by Turbine Control Loop Failure.Controls Calibrated & Actuator Determined to Be Inoperable.Actuator Was Replaced

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/03L-1 on 790227:variations in Speed of HPCI Turbine Occurred During Test.Caused by Turbine Control Loop Failure.Controls Calibrated & Actuator Determined to Be Inoperable.Actuator Was Replaced
ML19282C511
Person / Time
Site: Hatch Southern Nuclear icon.png
Issue date: 03/26/1979
From: Nix R
GEORGIA POWER CO.
To:
NRC OFFICE OF INSPECTION & ENFORCEMENT (IE REGION II)
Shared Package
ML19282C505 List:
References
LER-79-017-03L-02, LER-79-17-3L-2, NUDOCS 7903300255
Download: ML19282C511 (1)


LER-1979-017, /03L-1 on 790227:variations in Speed of HPCI Turbine Occurred During Test.Caused by Turbine Control Loop Failure.Controls Calibrated & Actuator Determined to Be Inoperable.Actuator Was Replaced
Event date:
Report date:
3211979017R03 - NRC Website

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