05000285/LER-1978-005-03, /03L-1 on 780214:CH-1C Charging Pump Was Out for Maint on Leaking End Cap.Crack in Valve Block Noted.Pump Not Inoperable & Returned to Svc.Crack Due to Heavy Usage & Excessive Vibration.New Block Installed 790105

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/03L-1 on 780214:CH-1C Charging Pump Was Out for Maint on Leaking End Cap.Crack in Valve Block Noted.Pump Not Inoperable & Returned to Svc.Crack Due to Heavy Usage & Excessive Vibration.New Block Installed 790105
ML19270F374
Person / Time
Site: Fort Calhoun 
Issue date: 01/29/1979
From: David Jones, Stevens J
OMAHA PUBLIC POWER DISTRICT
To:
NRC OFFICE OF INSPECTION & ENFORCEMENT (IE REGION IV)
Shared Package
ML19270F369 List:
References
LER-78-005-03L, LER-78-5-3L, NUDOCS 7902060319
Download: ML19270F374 (1)


LER-1978-005, /03L-1 on 780214:CH-1C Charging Pump Was Out for Maint on Leaking End Cap.Crack in Valve Block Noted.Pump Not Inoperable & Returned to Svc.Crack Due to Heavy Usage & Excessive Vibration.New Block Installed 790105
Event date:
Report date:
2851978005R03 - NRC Website

text

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