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LER-1979-037, /01T-0 on 790612:GE Review of Class IE Drywell Equipment Per IE Bulletin 79-01 Found Incomplete Documentation of Limit Switches on MSIV B21-F022 A,B,C & D. Caused by Changed Requirements.New Switch Ordered |
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| 3211979037R01 - NRC Website |
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8 60 61 COCK ET NUM6ER bd b3 EVENT OATE J4 75 HEPORT OATE 80 EVENT oESCRIPT3oN AND PROBABLE CONSEGUENCES h i2 l Ouring the 1979 refueling outage a General Electric review of Class IE drvwell equio-J I ment in response to IEB 79-01, indicated that the limit switches on main -steam isola- [
is l tion valves B21-F022 A. B. C, and D did not have a comolete temoerature and radiation I 4
I oualification test report document to aualify it to perform under an accident con-I s
I dition. There was no significant effect on olant safety from this event since the' j
s Iworst case failure of these limit switches would only result in a loss of valve positiop 7
lindication on the failed valve or the tricoing of the main steam isolation valves (cont) i a
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JI 40 41 42 43 44 47 CAUSE CESCRIPTICN AND CCRPECTIVE ACTIONS h l At the time of installation, the NAMC0 Model SL3-E2W limit switches were not reauired i o
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The later imolemented IEB i
i l 79-01 requires that all IE equipment in the drywell meet test. qualifications for 17 l accident conditions. A new NAMC0 Model EA-740-8000 limit switch has been ordered and 3
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NAME OF PREPARER
Georgia Power Company E. I. Hatch' Nuclear Plant Baxley, Georgia 31513 Reportable Occurrence No.
50-321-1979-37 Event Description And Probable Consequences Cont.
to the failed closed or safe condition on the failed valve.
Since the outboard MSIVs would still have valve position indication and function normally out of the accident environment,.there would still be a re-i dundant main steam isolation valve' with valve position indication.
This is a non-repetitive occurrence.
Cause Description And Corrective Actions Cont.
limit switches.
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NARRATIVE
REPORT 0
LER 79-037-01-T-0 F
On June 12, 1979, during the 1979 refueling outage a General Electric Company review of Class IE electrical equipment in' the drywell, in response to IE Bulletin 79-01, indicated that the limit switches on main steam isolation valves 821-F022 A, B, C, and D did not have a complete temperature and radiation qualification test report to qual-y ify it to perform under an accident condition.
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There was no significant effect on plant safety from this event since the worst case failure of these limit switches would only result in a j
loss of valve position indication on the failed valve or the tripping of the main steam isolation valves to the failed closed or safe condi-U tion on the failed valve.
Since the outboard MSIVs would still have valve position indication and function normally out of the accident en-E vironment there would still be a redundant main steam isolation valve with valve position indication that would function normally.
At the time of the installation, the NAMCO Model SL3-82W limit switches were not required to have environmentally qualified test report docu-ments.
The later implemented NRC IES 79-01 requires that all IE equipment j
in the drywell meet test qualifications for accident conditions.
A new NAMCO model EA-740-8000 limit switches has been ordered and it will be installed at the first scheduled cold shutdown upon receipt of the new limit switches.
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| 05000366/LER-1979-001, Forwards LER 79-001/03L-0 | Forwards LER 79-001/03L-0 | | | 05000366/LER-1979-001-03, /03L-0 on 781229:in Cold Shutdown While Performing HNP-2-3154,reactor Water Level Instrument Switch 1 Was Found Inoperative Due to Broken Foot, & Switch 3 Actuated at 122.2 in H2O Input | /03L-0 on 781229:in Cold Shutdown While Performing HNP-2-3154,reactor Water Level Instrument Switch 1 Was Found Inoperative Due to Broken Foot, & Switch 3 Actuated at 122.2 in H2O Input | | | 05000321/LER-1979-001, Forwards LER 79-001/03L-0 | Forwards LER 79-001/03L-0 | | | 05000321/LER-1979-001-03, /03L-0 on 790109:during Steady State Power at 2400 Mwt,Plant Personnel Inadvertently Opened Both Doors of Reactor Bldg 130-ft Airlock R106.For Reasons Unknown,Switch Which Allows Defeat of Interlock Was Operated | /03L-0 on 790109:during Steady State Power at 2400 Mwt,Plant Personnel Inadvertently Opened Both Doors of Reactor Bldg 130-ft Airlock R106.For Reasons Unknown,Switch Which Allows Defeat of Interlock Was Operated | | | 05000321/LER-1979-002, Forwards LER 79-002/03L-0 | Forwards LER 79-002/03L-0 | | | 05000321/LER-1979-002-03, /03L-0 on 790111:during Normal Operation,Hpci Steam Supply valves,E41-F002 & E41-F003,automatically Isolated Due to Equipment Room High Differential Temp & Cold Outside Air Flowing Across Inlet Air Temp Elements | /03L-0 on 790111:during Normal Operation,Hpci Steam Supply valves,E41-F002 & E41-F003,automatically Isolated Due to Equipment Room High Differential Temp & Cold Outside Air Flowing Across Inlet Air Temp Elements | | | 05000366/LER-1979-002, Forwards LER 79-002/03L-0 | Forwards LER 79-002/03L-0 | | | 05000366/LER-1979-002-03, /03L-0 on 791231:in Cold Shutdown While Performing HNP-2-3456,overvoltage Trip Setpoint for Reactor Protection Sys Motor Generator Set B Was Found at 133.5 Volts Alternating Current.Caused by Setpoint Drift | /03L-0 on 791231:in Cold Shutdown While Performing HNP-2-3456,overvoltage Trip Setpoint for Reactor Protection Sys Motor Generator Set B Was Found at 133.5 Volts Alternating Current.Caused by Setpoint Drift | | | 05000321/LER-1979-003-03, /03L-0 on 790114:during Normal operation,hi-flow Alarm Occurred on Stack Effluent Radiation Monitor.Sample Pump Was Found Not Running.Restart Failed,As Did Spare Pump. Caused by Failure of Operating Pump Carbon Valves | /03L-0 on 790114:during Normal operation,hi-flow Alarm Occurred on Stack Effluent Radiation Monitor.Sample Pump Was Found Not Running.Restart Failed,As Did Spare Pump. Caused by Failure of Operating Pump Carbon Valves | | | 05000321/LER-1979-003, Forwards LER 79-003/03L-0 | Forwards LER 79-003/03L-0 | | | 05000366/LER-1979-003, Forwards LER 79-003/03L-0 | Forwards LER 79-003/03L-0 | | | 05000366/LER-1979-003-03, /03L-0 on 790102:in Cold Shutdown While Performing HNP-2-3173 on Reactor Pressure Switch 2B21-N021C,setpoint Found Above 600 Psig for Switch No 2.Caused by Switch Setpoint Drift | /03L-0 on 790102:in Cold Shutdown While Performing HNP-2-3173 on Reactor Pressure Switch 2B21-N021C,setpoint Found Above 600 Psig for Switch No 2.Caused by Switch Setpoint Drift | | | 05000321/LER-1979-004-03, /03L-0 on 790119:during Performance of Procedure HNP-1-3302,armature Winding of HPCI Injecting Valve Motor (E41-F006) Burned When Valve Was Opening.Minor Internal Disorder Probably Led to Overheat | /03L-0 on 790119:during Performance of Procedure HNP-1-3302,armature Winding of HPCI Injecting Valve Motor (E41-F006) Burned When Valve Was Opening.Minor Internal Disorder Probably Led to Overheat | | | 05000366/LER-1979-004, Forwards LER 79-004/03L-0 | Forwards LER 79-004/03L-0 | | | 05000366/LER-1979-004-03, /03L-0 on 790104:review of HNP-2-3610-0 (RHR Pump Operability) Data Sheet Revealed Pump Delta Requirements Not Met.Caused by Personnel Error Resulting from New Procedures | /03L-0 on 790104:review of HNP-2-3610-0 (RHR Pump Operability) Data Sheet Revealed Pump Delta Requirements Not Met.Caused by Personnel Error Resulting from New Procedures | | | 05000321/LER-1979-004, Forwards LER 79-004/03L-0 | Forwards LER 79-004/03L-0 | | | 05000366/LER-1979-005-03, /03L-0 on 790103:under Frequency Trip Setpoint Found at 54.1HZ for Motor Generator Set A.Caused by pre-op Test on Sys.Surveillance Test HNP-2-3456 Contains Setpoint More Conservative than Tech Specs | /03L-0 on 790103:under Frequency Trip Setpoint Found at 54.1HZ for Motor Generator Set A.Caused by pre-op Test on Sys.Surveillance Test HNP-2-3456 Contains Setpoint More Conservative than Tech Specs | | | 05000366/LER-1979-005, Forwards LER 79-005/03L-0 | Forwards LER 79-005/03L-0 | | | 05000321/LER-1979-005, Forwards LER 79-005/03L-0 | Forwards LER 79-005/03L-0 | | | 05000321/LER-1979-005-03, /03L-0 on 790118:while Performing HNP-1-350-M,TDR G31-R616D Failed to Actuate at Its Setting of 15-s.Two-h Time Limit Exceeded W/Sys Down for Repair.Caused by Loose Screw on Diaphragm,Resulting in Component Failure | /03L-0 on 790118:while Performing HNP-1-350-M,TDR G31-R616D Failed to Actuate at Its Setting of 15-s.Two-h Time Limit Exceeded W/Sys Down for Repair.Caused by Loose Screw on Diaphragm,Resulting in Component Failure | | | 05000366/LER-1979-006, Forwards LER 79-006/03L-0 | Forwards LER 79-006/03L-0 | | | 05000366/LER-1979-006-03, /03L-0 on 790102:reactor Pressure Instrument Ft&C, Relay 2B21-K34A Failed to Operate W/Actuation of 2B21-N021A. Caused by Open Coil | /03L-0 on 790102:reactor Pressure Instrument Ft&C, Relay 2B21-K34A Failed to Operate W/Actuation of 2B21-N021A. Caused by Open Coil | | | 05000321/LER-1979-006, Forwards LER 79-006/03L-0 | Forwards LER 79-006/03L-0 | | | 05000321/LER-1979-006-03, /03L-0 on 790122:during Normal Startup,Reactor Operated Above 1% for Over 24-h W/O Critical Mass Peaking Factor Being Calculated.Caused by Computer Limitations for Low Power Operation | /03L-0 on 790122:during Normal Startup,Reactor Operated Above 1% for Over 24-h W/O Critical Mass Peaking Factor Being Calculated.Caused by Computer Limitations for Low Power Operation | | | 05000321/LER-1979-007, Forwards LER 79-007/03L-0 | Forwards LER 79-007/03L-0 | | | 05000321/LER-1979-007-03, /03L-0 on 790120:reactor Core Isolation Cooling Min Flow Valve (E51-F019) Failed to Close Automatically. Caused by Failure of Open Limit Switch,Resulting in Damage to Valve Operator & Torque Switch | /03L-0 on 790120:reactor Core Isolation Cooling Min Flow Valve (E51-F019) Failed to Close Automatically. Caused by Failure of Open Limit Switch,Resulting in Damage to Valve Operator & Torque Switch | | | 05000321/LER-1979-008-03, /03L-0 on 790121:reactor Max Cooling Rate Exceeded Due to Injection of Condensate Feedwater Into Reactor Vessel During Slowdown.Caused by Pressure Decreasing Below Condensate Booster Pump Discharge Pressure | /03L-0 on 790121:reactor Max Cooling Rate Exceeded Due to Injection of Condensate Feedwater Into Reactor Vessel During Slowdown.Caused by Pressure Decreasing Below Condensate Booster Pump Discharge Pressure | | | 05000366/LER-1979-008, Forwards LER 79-008/03L-0 | Forwards LER 79-008/03L-0 | | | 05000366/LER-1979-008-03, /03L-0 on 790110:reactor Core Isolation Cooling Steam Line Differential Pressure Low Switch Found to Actuate at 119 in H2O & High Switch at +122 in H2O.Caused by Switch Setpoint Drift | /03L-0 on 790110:reactor Core Isolation Cooling Steam Line Differential Pressure Low Switch Found to Actuate at 119 in H2O & High Switch at +122 in H2O.Caused by Switch Setpoint Drift | | | 05000321/LER-1979-008, Forwards LER 79-008/03L-0 | Forwards LER 79-008/03L-0 | | | 05000366/LER-1979-009-03, /03L-0 on 790111:low Switch & High Switch of 2E51-NO18 Operated Contrary to Tech Specs.Caused by Switch Setpoint Drift.Corrected by Performance of HNP-2-5202 Procedure | /03L-0 on 790111:low Switch & High Switch of 2E51-NO18 Operated Contrary to Tech Specs.Caused by Switch Setpoint Drift.Corrected by Performance of HNP-2-5202 Procedure | | | 05000366/LER-1979-009, Forwards LER 79-009/03L-0 | Forwards LER 79-009/03L-0 | | | 05000321/LER-1979-009, Forwards LER 79-009/03L-0 | Forwards LER 79-009/03L-0 | | | 05000321/LER-1979-009-03, /03L-0 on 790123:during Normal Operation,While Performing Maint on Reactor Water Cleanup Pumps,Personnel Unable to Sample Primary Coolant Every 4-h.Caused by Stopped Up Redundant Sample Line | /03L-0 on 790123:during Normal Operation,While Performing Maint on Reactor Water Cleanup Pumps,Personnel Unable to Sample Primary Coolant Every 4-h.Caused by Stopped Up Redundant Sample Line | | | 05000321/LER-1979-010-03, /03L-0 on 790124:during Normal pre-conditional Ramp,Determined That a Reactor Coolant Chemistry Sample Could Not Be Obtained.Caused by Both Reactor Water Cleanup Pumps Being Inoperable & Primary Sample Line Clogged | /03L-0 on 790124:during Normal pre-conditional Ramp,Determined That a Reactor Coolant Chemistry Sample Could Not Be Obtained.Caused by Both Reactor Water Cleanup Pumps Being Inoperable & Primary Sample Line Clogged | | | 05000321/LER-1979-010, Forwards LER 79-010/03L-0 | Forwards LER 79-010/03L-0 | | | 05000366/LER-1979-010, Forwards LER 79-010/03L-0 | Forwards LER 79-010/03L-0 | | | 05000366/LER-1979-010-03, /03L-0 on 790117:in Cold Shutdown,While Performing HNP-2-3820,switches 2B21-N301 F,H & L Did Not Actuate.Caused by Switch Diaphragm Failure | /03L-0 on 790117:in Cold Shutdown,While Performing HNP-2-3820,switches 2B21-N301 F,H & L Did Not Actuate.Caused by Switch Diaphragm Failure | | | 05000321/LER-1979-011, Forwards LER 79-011/03L-0 | Forwards LER 79-011/03L-0 | | | 05000366/LER-1979-011, Forwards LER 79-011/03L-0 | Forwards LER 79-011/03L-0 | | | 05000366/LER-1979-011-03, /03L-0 on 790117:during Normal Startup Test & Reactor in Cold Shutdown,Review of HNP-2-3160 (RHR Pump Operability) Revealed Required Flow Not Being Met.Caused by Procedural Error by Personnel | /03L-0 on 790117:during Normal Startup Test & Reactor in Cold Shutdown,Review of HNP-2-3160 (RHR Pump Operability) Revealed Required Flow Not Being Met.Caused by Procedural Error by Personnel | | | 05000321/LER-1979-011-03, /03L-0 on 790124:while in Cold Shutdown,Both Doors of Reactor Bldg Were Opened,Violating Secondary Containment. Bracket Into Which Dead Bolt Projects Was Bent,Preventing Interlock from Functioning.Bracket Was Repaired | /03L-0 on 790124:while in Cold Shutdown,Both Doors of Reactor Bldg Were Opened,Violating Secondary Containment. Bracket Into Which Dead Bolt Projects Was Bent,Preventing Interlock from Functioning.Bracket Was Repaired | | | 05000366/LER-1979-012, Has Been Voided | Has Been Voided | | | 05000321/LER-1979-012-03, /03L-0 on 790124:during Shutdown,High Pressure of 200 to 300 Psig Existed in RHR Heat Exchangers.Caused by Slow Leak Past E11-F015A Valve | /03L-0 on 790124:during Shutdown,High Pressure of 200 to 300 Psig Existed in RHR Heat Exchangers.Caused by Slow Leak Past E11-F015A Valve | | | 05000321/LER-1979-012, Forwards LER 79-012/03L-0 | Forwards LER 79-012/03L-0 | | | 05000366/LER-1979-013, Forwards LER 79-013/03L-0 | Forwards LER 79-013/03L-0 | | | 05000321/LER-1979-013-01, /01X-1 on 790131:scram Received on Intermediate Range Monitor Hi-Hi Trip at Notch 26 of Rod 42-15.Caused by Notches Being Withdrawn Past Point Required to Achieve Criticality.Procedures Revised | /01X-1 on 790131:scram Received on Intermediate Range Monitor Hi-Hi Trip at Notch 26 of Rod 42-15.Caused by Notches Being Withdrawn Past Point Required to Achieve Criticality.Procedures Revised | | | 05000366/LER-1979-013-03, /03L-0 on 790125:while in Refuel Mode,Control Rod & Control Rod Drive Removal Was Begun Before Performing one- Rod Out Refueling Interlock Operability Test.Caused by Omission of This Step in Procedure.Procedure to Be Revised | /03L-0 on 790125:while in Refuel Mode,Control Rod & Control Rod Drive Removal Was Begun Before Performing one- Rod Out Refueling Interlock Operability Test.Caused by Omission of This Step in Procedure.Procedure to Be Revised | | | 05000321/LER-1979-013, Foward LER 79-013/01X-1 | Foward LER 79-013/01X-1 | | | 05000321/LER-1979-014, Forwards LER 79-014/03L-0 | Forwards LER 79-014/03L-0 | |
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