05000265/LER-1979-020-03, /03L-0:on 790919,three Grinnell Hydraulic Snubbers Found to Have Empty Reservoirs.Caused by Excess Leakage Through Defective Gaskets.Snubbers Repaired by Installing New Oil Resevoirs and Seals

From kanterella
(Redirected from ML19254F018)
Jump to navigation Jump to search
/03L-0:on 790919,three Grinnell Hydraulic Snubbers Found to Have Empty Reservoirs.Caused by Excess Leakage Through Defective Gaskets.Snubbers Repaired by Installing New Oil Resevoirs and Seals
ML19254F018
Person / Time
Site: Quad Cities Constellation icon.png
Issue date: 10/15/1979
From: Kan S
COMMONWEALTH EDISON CO.
To:
NRC OFFICE OF INSPECTION & ENFORCEMENT (IE REGION III)
Shared Package
ML19254F014 List:
References
LER-79-020-03L-04, LER-79-20-3L-4, NUDOCS 7911050357
Download: ML19254F018 (1)


LER-1979-020, /03L-0:on 790919,three Grinnell Hydraulic Snubbers Found to Have Empty Reservoirs.Caused by Excess Leakage Through Defective Gaskets.Snubbers Repaired by Installing New Oil Resevoirs and Seals
Event date:
Report date:
2651979020R03 - NRC Website

text

.

NRC FORM 366 U. S. P.UCLE AR Rt;GUL ATOR'. i;OMMISSION (7 77)

'~

LICENSEE EVENT REPORT CONTROL BLOCK: l l

l l

l l lh (PLEASE PRINT OR TYPE ALL REQUInED INFORMATIONI i

e ll ll Q lA lD l2 l@l 0 l 0 l 0 l - l 0 l Ol 0l -l 0 0l0l@l4l1l1l1l1l@l l

l@

o 1

7 8 9 LICENSEE COOE 14 15 UCENSE NOV6ER 25 26 LICENSE TYPE 40 57 4 A T 58 CON'T

"'" "' l L l@l 01510 l 01012 6 15 l@l_0 19 11 l9 l7 lo l@ l 0l1l517l9l@

O 1

3a gc

?

8 60 61 DOCKET NUMBER 68 63 E w ENT DATE 74 75 REPORT DATE B0 EVENT DESCRIPTION AND PROBABLE CONSEQUENCES h l, An in plant insoect ion of accessible Grinnell Hydraulic Sni t,Oers..ms performed in I

o 2

g,3

accordance with procedure QTS 180-1.

The snuobers on the RHR Shutdown Cooling l

g, g Supply, Main Steam Line Drains, and RCIC Steam Supply were found to have empty l

fluid reservoirs. Work.aquests were initiated to initiate repairs.

Operable j

o s!l i snubbers were in close proximity to the defective snubbers, and the Steam Drains t, l

o e

[o 7

l SDC lines were isolated at the time.

l 0

8 I

7 9 9 60 SYSTEM

CAUSE

CAUSE COYP.

VALVE CODE CCOE SUBCODE COVPONENT CODE SUSCC CE SUSCCCE

[ Xl Xl@ l El@ lB l@ l S l U l P l 0 l R l T l@ lD l@ l Zl@

o 3

7 C

9 13 11 12 13 18 19 20 SE QUE NTI AL OCCUAAENCE RECORT REVISION LER RO EVENTYiAR REPORT NO, CCCE TYPE NO.

@ aiP,g l217 l9 l

[-- l l0 2 0l l/l 1013 l lLl d

0l 22 23 24 26 27 28 23 30 31 32 7 KEN A T ON O PLANT V

HOURS SB iT i FOR 8.

SLPPL1 UAN FACTLRER l A [gl34Zl@

lZl@

l Zj@

j 0l0l0l0l lNl@

lN l@

l Al@

Gl 215 l 7l@

33 35 36 31 40 4'

42 43 44 47 CAUSE DESCRIPTION AND CORRECTIVE ACTIONS h l All three snubbers had empty reservoirs due to excess leakace through defective l

i O

gaskets. The snubbers were recaired by installing new oil reservoirs and seals.

y The reservoi rs were filled and reinspected.

The snubbers were declared operable i

l within the Tech Spec 3.6.l.2. 72-hour limit.

I 3

i 4

1 1

7 8 9 80 STA S

%FOWER

/ OTHER STATUS DISCO RY OlSCOVERY DESCRIPTION 1 s lE l@ l0 l 517 l@l NA l

l8l@l Routine Test / Inspection l

ACTIVITY CO TENT RELEASED OF RELEASE AMOUNT OF ACTIVITY LOCATION CF RELE ASE

@ l Z l@l NA l

l NA l

1 6

7 8 3 to 11 44 45 80 PERSONNEL EXPOSLRES C E SCR'PTIC N NUV8EA TY8E @l dI010l0l@l l

NA l

i PERSCNNE L INJURIES oESCR,fiO.@

NusaER L'_Ltj l 0 l 0 0l@l NA l

7 d 3 11 12 30 LCSS OF OR DAVAGE TO FACILITY 1267 2b4 iTgi

" ' = " ' " ' ~

i NA e

7 4 s 10 80 hkl 8,

'SSLEf@DE CR'PTfCN lN NA l

ll llllltillIII 2

o 8 3 to 68 69 dJ 1 309-654-2241 ext. 174 2

N AVE C ' 'nEDARER PHONE.