LER-1979-012, /03L-0 on 790622:nut Inadvertantly Droppoed Into Diesel Generator Winding During Preventive Maint.Outage Time of Generator Extended 20 Minutes Beyond 1.5-h Time Limit. Caused by Personnel Error |
| Event date: |
|
|---|
| Report date: |
|
|---|
| 2651979012R03 - NRC Website |
|
text
NRC FORM 366 U. S. NUCLEAR RECULATORY COMMISSION (7 77)
LICENSEE EVENT REPORT CONTROL BLCCK:
l l
l l
l l
(PLEASE PRINT OR TYPE ALL REQUIRED INFoRMATION) 1 6
l1lLlQ A l D l 2 l@l 0 l 0 l 0 l - l 0 0l0l-l0 C l 0 l@l4 l 1l 1l 1l 1l@l l
l@
o t
7 d 9 LICENSEE CODE 14 15 LICENSE NUMBEH Is
- 6 LICENSE TYPE J0 57 LA T 58 CON'T b1 5%g"j l L l@l 0 l 5 l0 0 l0 l2 l6 15 l@l 0 l 6 l 2 i 2 l 7 l 9 @l 01 71 1l 3i 7 l o l@
I 8
b0 61 DOCK ET NUMB E R 6d 69 EVENT DATE 14 75 REPORT DATE
$0 EVENT DESCRIPTION AND PROBABLE CONSEQUENCES h a
2 l While performing the Unit Two Diesel Generator monthly Oreventive maintenance
_]
l inspection, a nut was inadvertantly dropped into tne diesel generator winding when l
O 3
replacing the brush rigging Cover. The retrieval of the dropped nut extended the g
g
, y 0
s l diesel generator outage time 20 minutes beyond the 1-1/2 hour time limit set by I
Lo 6
i T.s.3.9.E.1.
The 1/2 diesel generator had been tested prior to taking the Unit' Two l diesel generator out of service. The nut was found prior to starting surveillance l
O 7
- requi red by T.S.3.9.E.1.
I 0
g 7
ao 80 SYSTE M
CAUSE
CAUSE COMP.
VALVE COOE CODE SUBCODE COMPONENT CODE SU8 CODE SUSCODE O
9 lEl El@ {@ l C l@ l Gl El Nl F' Rl Al@ l D l@ [Z l@
7 8
9 10 11 12 13 18 19 20 SEQUE NTI AL
( COU A R E NCE LEPCRT R E VISIO N
. EVENT YEAR REPORT NO.
CODE TY'E N O.
h a('g gf po l7l9l l-l lo il l2 l l/l l 013 l lL l l-l l0 l yuOeRT
_ 21 22 23 24 26 2,
23 29 20 31 32 TA EN AC Of ON PL NT T b HOURS S 3 IT O FOR 8
S PPLIE MANUFACTURER lXl@lZl@
Zl@
lZl@
l0 l0 l0 l0 l
[ Nl@
lNl@
lNl@
Gl0l8l0l@
33 34 35 36 3/
40 41 42 43 44 47 CAUSE DESCRIPTION AND CORRECTIVE ACTIONS h g g lThe dropping of the nut was due to human factors. The nut was found and the Unit Two I
li l' 1 L esel gener tor operability surveillance was performed.
di 11 I ? l L_.
I t i l 31 l 1
4 l
l 7
8 4 80
'ST
% POWER
~
OTHER STATUS blS O RY DISCOV6RY DESCRIPTION lC @ l 0 l 0 l 4 l@l l A l@l Operational Event l
NA i
s ACTIVITY CONTENT RELEASEC OF RELEASE AVOUNT OF ACTIVITY LOCATION OF RELEASE
@ l Z l@
NA l
NA l
i s
Z 7
8 9 10 11 a4 45 80 PERSONNEL EXPOSURES NUMBER TYPE O E SCRIPTI O N y l 0 l 0 l 0]@l Z l@l A
l
' PERSONNE L INJURtES NUVBE R OESCRIPTION 0l0l0l@l NA i
4 7
8 9 11 12 BC LOSS OF C A D AM AGE TO F ACILITY TYPE D E SCRIPTION I
9 f
kh 7
d 3 to 80 6SSUE @nE CRIPTION 8
INi l
NA l
llllllll ll l l };
2 o
7 3 J to 63 69 60 5 J. Vahrenwald 309-654-2241 Ext.
195 i, N A'.* E O F P R E P A R E R P'4 C N E.
,&M Wisconsin Electnc ecw come 231 W. MICHIGAN, P.O. BOX 2046. MILWAUKEE WI 53201 July 3, 1979 Mr. James Keppler, Regional Director Office of Inspection and Enforcement Region III U. S. NUCLEAR REGULATORY COMMISSION 799 Rooseveit Road Glen Ellyn, Illinois 60137
Dear Mr. Keppler:
DOCKET NOS. 50-266 AND 50-301 MODIFICATION OF THE RESET CIRCUITS IN THE SAFEGUARDS ACTUATION CIRCUITS LICENSEE EVENT REPORT NO. 79-010/01T-0 POINT BEACH NUCLEAR PLANT, UNITS 1 AND 2 Enclosed is Licensee Event Report No. 79-010/01T-0, which, together with this letter, provides a 14 day followup report to our 24 hour2.777778e-4 days <br />0.00667 hours <br />3.968254e-5 weeks <br />9.132e-6 months <br /> written notification of June 20, 1979. The results of our review of the safeguards actuation circuitry of Point Beach Nuclear Plant indicate a finding that may be reportable in accordance with Technical Specification 15.6.9.2.A.9,
" Performance of structures, systems, or components that requires remedial sction or corrective measures to prevent operation in a manner less conservative than that assumed in t.'.
accident analyses in the safety analysis report or technical specifications bases; or,1iscovery during plant life of conditions not specifically considerad in the safety analysis report or technical specifications that require remedial action or corrective measures to prevent the existence or development of an unsafe condition."
As you know, Mr. A. Schwencer's letter dated November 28, 1978, identified a deficiency in the reset circuitry of the Containment Ventilation Isolation circuits at two other plants. The letter requested that we inves-tigate the reset circuitry used at the Point Beach Nuclear Plant in the Containment Ventilation Isolation and other safeguards circuits.
In our letter to Mr. Denton dated January ~ 16, 1979, we indicated that the safeguards reset circuits at Point Beach had the characteristics mentioned in the November 28 letter and that we would analyze the circuits in detail and modify them where necessary. Further, because of the mechanical characteristics of the containment ventilation valves, we conmitted in LER 79-04 to keep the valves closed during power and hot standby operation. A meeting was held at the Point Beach Nuclear ?lant with Mr. J. T. Beard of your Staff on June 5,1979, at which time circuit configurations, requirements, and modifica-tions were further discussen.
Dy
% \\
398 268 c13
\\
p. 9 79072 5 on 7
Mr. James Keppler - Page Two July 3, 1979 We have completed a detailed review of the safeguards actuation circuits at the Point Beach Nuclear Plant. The results of this review indicate that some changes to the circuitry are desirable. Modification requests to effect these changes have been written and are in the review and approval process.
There are four safeguards circuits for which we believe modifications are desirable. These are Safety Injection, Containment Isolation, Containment Ventilation Isolation, and Containment Spray.
The modifications we propose will provide the following circuit characteristics:
1.
MANUAL INPUTS Manual actuation of a safeguards circuit will not be affected by the reset circuitry. Safety Injection has always had this feature. The other three circuits will be modified.
2.
AUTOMATIC INPUTS The Containment Ventilation Isolation circuit will be modified so the reset function will not block an additional automatic signal from activating the circuit. The Safety Injection circuit is designed to sequence a group of protective actions after receipt of an automatic or manual initiation signal.
The Safaty Injection circuit must be reset after initiation in order to operate equipment which was secured or stripped by the safety injection sequence. Should an additional auto-matic signal be generated after reset it is not desirable to resequence che protective actions which have ciready occurred and chance the post accident equipment lineup.
For this reason che Safety Injection circuit will not be modified in this reg:rd. Containment Spray and Containment Isolation do not have multiple automatic inputs and therefore no modifications are necessary.
3.
SEPARATE RESETS FOR EAC'i TRAIN Separate reset switches will be provided for each train for each circuit.
4.
PHYSICAL ACCESS The reset swi ches will be fitted with clear plastic covers.
t This will pavent inadvertent or accidental operation and will require deliberate operator action to reset the safeguards circuits.
7nn8 vc09 5.
ANNUNCIATION For Containment Isolatico, Containment Ventilation Isolation and Containment Spray, status lights and annunciation will be provided for each circuit in which the reset hold-in feature is retained. The reset hold-in feature may be deleted, eliminating the need for additional lights and annunciation.
Safety. Injection circuits will be provided with status lights and annunciation for each train.
Mr. James Keppler - Page Three July 3, 1979 It is estimated that these modifications will be completed approximately two weeks after final approval of the modification requests and installation procedures. Approvals are expected to require approximately three weeks.
Very truly yours, 9
, %/ y C. W. Fa, Director flaclear Power Department Enclosure
";o i
...,,wo
|
|---|
|
|
| | | Reporting criterion |
|---|
| 05000265/LER-1979-001-03, /03L-0 on 790104:during Monthly Operability Test, Inlet Air Heater on a Standby Gas Treatment Sys Was Found Inoperable.Caused by Setpoint Drift of Flow Switch 1/2-7541-8A | /03L-0 on 790104:during Monthly Operability Test, Inlet Air Heater on a Standby Gas Treatment Sys Was Found Inoperable.Caused by Setpoint Drift of Flow Switch 1/2-7541-8A | | | 05000254/LER-1979-001, Forwards LER 79-001/03L-0 | Forwards LER 79-001/03L-0 | | | 05000265/LER-1979-001, Forwards LER 79-001/03L-0 | Forwards LER 79-001/03L-0 | | | 05000254/LER-1979-001-03, /03L-0 on 790107:high Steam Line Flow Alarm & Automatic Isolation of Reactor Core Isolation Cooling Steam Supply Line Occurred.Caused by Failure of Micro Switch Inside Steam Line High Flow Differential Pressure Switch | /03L-0 on 790107:high Steam Line Flow Alarm & Automatic Isolation of Reactor Core Isolation Cooling Steam Supply Line Occurred.Caused by Failure of Micro Switch Inside Steam Line High Flow Differential Pressure Switch | | | 05000265/LER-1979-002, Forwards LER 79-002/03L-0 | Forwards LER 79-002/03L-0 | | | 05000265/LER-1979-002-03, /03L-0 on 790110:during Routine Insp of Reactor Water Cleanup Pump Rooms,Small Leak Was Found on 2-1205B Cleanup Pump Suction Line.Cause Unknown.Leak Was Isolated & Linear Indication on Flange Ground Out | /03L-0 on 790110:during Routine Insp of Reactor Water Cleanup Pump Rooms,Small Leak Was Found on 2-1205B Cleanup Pump Suction Line.Cause Unknown.Leak Was Isolated & Linear Indication on Flange Ground Out | | | 05000254/LER-1979-002-03, /03L-0 on 790110:during Freon Test,Noted That Freon Penetration Through Charcoal Absorbers Exceeded Tech Spec Max.Caused by One of Charcoal Clamping Levers Not Being Fully Latched | /03L-0 on 790110:during Freon Test,Noted That Freon Penetration Through Charcoal Absorbers Exceeded Tech Spec Max.Caused by One of Charcoal Clamping Levers Not Being Fully Latched | | | 05000254/LER-1979-002, Forwards LER 79-002/03L-0 | Forwards LER 79-002/03L-0 | | | 05000265/LER-1979-003-03, /03L-0 on 790214:during High Temp Isolation Calibr Procedure,Temp Switch TS 2-2373A Was Found to Trip in Excess of Tech Spec Limit.Caused by Setpoint Drift.Switch Recalibrated & Retested | /03L-0 on 790214:during High Temp Isolation Calibr Procedure,Temp Switch TS 2-2373A Was Found to Trip in Excess of Tech Spec Limit.Caused by Setpoint Drift.Switch Recalibrated & Retested | | | 05000254/LER-1979-003, Forwards LER 79-003/03L-0 | Forwards LER 79-003/03L-0 | | | 05000265/LER-1979-003, Forwards LER 79-003/03L-0 | Forwards LER 79-003/03L-0 | | | 05000254/LER-1979-003-03, /03L-1 on 790119:MSIV Local Leak Rate Showed Seven Valves Leaking Excessively.Causes Unspecified.Valve Stroke Adjusted,Certain Valves Dismantled,Discs & Seats Were Lapped & Machined | /03L-1 on 790119:MSIV Local Leak Rate Showed Seven Valves Leaking Excessively.Causes Unspecified.Valve Stroke Adjusted,Certain Valves Dismantled,Discs & Seats Were Lapped & Machined | | | 05000254/LER-1979-004, Forwards LER 79-004/01T-0 | Forwards LER 79-004/01T-0 | | | 05000254/LER-1979-004-01, /01T-0 on 790122:piece of Control Rod Drive Return Nozzle Thermal Sleeve Retaining Ring Was Missing.Cause Unknown | /01T-0 on 790122:piece of Control Rod Drive Return Nozzle Thermal Sleeve Retaining Ring Was Missing.Cause Unknown | | | 05000265/LER-1979-004-03, /03L-0 on 790211:suction Isolation Valve Mo 2-1001-50 Failed to Close from Control Room.Caused by Failed Circuit Breaker in Valve Motor Control Center. Valve Taken Out of Svc for Repair During Outages | /03L-0 on 790211:suction Isolation Valve Mo 2-1001-50 Failed to Close from Control Room.Caused by Failed Circuit Breaker in Valve Motor Control Center. Valve Taken Out of Svc for Repair During Outages | | | 05000265/LER-1979-004, Forwards LER 79-004/03L-0 | Forwards LER 79-004/03L-0 | | | 05000254/LER-1979-005-03, /03L-0 on 790123:during Unit 1/2 Diesel Generator Monthly Load Test Qos 6600-1,pilot Solenoid Valve to Air Starting Motors Failed & Unit 1/2 Diesel Was Shutdown. Caused by Mechanical Failure of Valve.Valve Was Replaced | /03L-0 on 790123:during Unit 1/2 Diesel Generator Monthly Load Test Qos 6600-1,pilot Solenoid Valve to Air Starting Motors Failed & Unit 1/2 Diesel Was Shutdown. Caused by Mechanical Failure of Valve.Valve Was Replaced | | | 05000254/LER-1979-005, Forwards LER 79-005/03L-0 | Forwards LER 79-005/03L-0 | | | 05000265/LER-1979-005-03, /03L-0 on 790223:2A Recirculation Motor Generator Field Breaker Opened,Causing Flow Mismatch.Caused by Loosening of Coupling Between Main Shaft & Recirculation Motor Generator Set Tachometer.Tachometer Coupling Reset | /03L-0 on 790223:2A Recirculation Motor Generator Field Breaker Opened,Causing Flow Mismatch.Caused by Loosening of Coupling Between Main Shaft & Recirculation Motor Generator Set Tachometer.Tachometer Coupling Reset | | | 05000265/LER-1979-005, Forwards LER 79-005/03L-0 | Forwards LER 79-005/03L-0 | | | 05000254/LER-1979-006-03, /03L-0 on 790125:during Primary Containment Isolation Valve Closure Timing,Valve AO 1-1601-21 Failed to Close in 10 Seconds.Caused by Improper Adjustment of Valve Speed Control from Operational Wear.Control Was Readjusted | /03L-0 on 790125:during Primary Containment Isolation Valve Closure Timing,Valve AO 1-1601-21 Failed to Close in 10 Seconds.Caused by Improper Adjustment of Valve Speed Control from Operational Wear.Control Was Readjusted | | | 05000254/LER-1979-006, Forwards LER 79-006/03L-0 | Forwards LER 79-006/03L-0 | | | 05000254/LER-1979-007, Forwards LER 79-007/03L-0 | Forwards LER 79-007/03L-0 | | | 05000254/LER-1979-007-03, /03L-0 on 790201:main Steam Line Leak Detection Temp Switches TS 1-261-16A,MTS 1-261-18A & TS 1-261-15C Tripped in Excess of Setpoint.Caused by Instrument Setpoint Drift.Temp Switches Recalibrated | /03L-0 on 790201:main Steam Line Leak Detection Temp Switches TS 1-261-16A,MTS 1-261-18A & TS 1-261-15C Tripped in Excess of Setpoint.Caused by Instrument Setpoint Drift.Temp Switches Recalibrated | | | 05000254/LER-1979-008, Forwards LER 79-008/03L-0 | Forwards LER 79-008/03L-0 | | | 05000254/LER-1979-008-03, /03L-0 on 790202:temp Switch TS-1-1360-15D Had Trip Setpoint in Excess of Tech Spec Limit.Caused by Setpoint Drift.Switch Recalibrated & Satisfactorily Tested | /03L-0 on 790202:temp Switch TS-1-1360-15D Had Trip Setpoint in Excess of Tech Spec Limit.Caused by Setpoint Drift.Switch Recalibrated & Satisfactorily Tested | | | 05000254/LER-1979-009-03, /03L-0 on 790203:bed Plate Drain Valves AO 1-4999-57,58 & 60 Did Not Fully Close.Caused by Corrosion & Failure of Internal Return Springs.Springs Replaced & Valves Satisfactorily Retested | /03L-0 on 790203:bed Plate Drain Valves AO 1-4999-57,58 & 60 Did Not Fully Close.Caused by Corrosion & Failure of Internal Return Springs.Springs Replaced & Valves Satisfactorily Retested | | | 05000254/LER-1979-009, Forwards LER 79-009/03L-0 | Forwards LER 79-009/03L-0 | | | 05000265/LER-1979-009, Forwards LER 79-009/03L-0.Corrects Docket Number of Original Forwarding Ltr | Forwards LER 79-009/03L-0.Corrects Docket Number of Original Forwarding Ltr | | | 05000265/LER-1979-009-03, /03L-0:on 790429,switch Trip Positions Found at Greater than 10% of MSIV Closure.Caused by Failure to Set Field Calibr for Switch Trip Point Limit.Switches Were Adjusted to 10% Closure or Less | /03L-0:on 790429,switch Trip Positions Found at Greater than 10% of MSIV Closure.Caused by Failure to Set Field Calibr for Switch Trip Point Limit.Switches Were Adjusted to 10% Closure or Less | | | 05000254/LER-1979-010-03, /03L-1 on 790205:diesel Fire Pump 1/2A Out of Svc Beyond Tech Spec Limit.Caused by Personnel Error.Pump Returned to Svc | /03L-1 on 790205:diesel Fire Pump 1/2A Out of Svc Beyond Tech Spec Limit.Caused by Personnel Error.Pump Returned to Svc | | | 05000254/LER-1979-010, Forwards LER 79-010/03L-1 | Forwards LER 79-010/03L-1 | | | 05000265/LER-1979-010, Forwards LER 79-010/03L-0 | Forwards LER 79-010/03L-0 | | | 05000265/LER-1979-010-03, /03L-0 on 790514:2A Fuel Pool Radiation Monitor Failed Upscale & Failed Again on 790601 & 02.Caused by Failure of GM-tube in Sensor Conventor Unit.Tube Finally Replaced W/Amperex 18529 | /03L-0 on 790514:2A Fuel Pool Radiation Monitor Failed Upscale & Failed Again on 790601 & 02.Caused by Failure of GM-tube in Sensor Conventor Unit.Tube Finally Replaced W/Amperex 18529 | | | 05000254/LER-1979-011, Forwards LER 79-011/03L-0 | Forwards LER 79-011/03L-0 | | | 05000254/LER-1979-011-03, /03L-0 on 790202:drywell Vent Valve AO 1-1601-23 Closed in Excess of Tech Spec Max Time Limit.Caused by Worn & Leaking Seals on Air Operating pistons.U-cup Piston Seals Replaced | /03L-0 on 790202:drywell Vent Valve AO 1-1601-23 Closed in Excess of Tech Spec Max Time Limit.Caused by Worn & Leaking Seals on Air Operating pistons.U-cup Piston Seals Replaced | | | 05000265/LER-1979-011, Forwards LER 79-011/03L-0 | Forwards LER 79-011/03L-0 | | | 05000265/LER-1979-011-03, /03L-0 on 790521:three Cables Not Installed in Accordance W/Drawings.Caused by Error in Cable Routing During Initial Const.Reroute of Cables Will Take Place During Nov 1979 Refueling Outage | /03L-0 on 790521:three Cables Not Installed in Accordance W/Drawings.Caused by Error in Cable Routing During Initial Const.Reroute of Cables Will Take Place During Nov 1979 Refueling Outage | | | 05000265/LER-1979-012-03, /03L-0 on 790622:nut Inadvertantly Droppoed Into Diesel Generator Winding During Preventive Maint.Outage Time of Generator Extended 20 Minutes Beyond 1.5-h Time Limit. Caused by Personnel Error | /03L-0 on 790622:nut Inadvertantly Droppoed Into Diesel Generator Winding During Preventive Maint.Outage Time of Generator Extended 20 Minutes Beyond 1.5-h Time Limit. Caused by Personnel Error | | | 05000265/LER-1979-012, Forwards LER 79-012/03L-0 | Forwards LER 79-012/03L-0 | | | 05000254/LER-1979-012, Forwards LER 79-012/03L-0 | Forwards LER 79-012/03L-0 | | | 05000254/LER-1979-012-03, /03L-0 on 790214:air Found Blowing Through Weld on 3/4 Inch Vent Line.Caused by Component Failure.Vent Line Inserted Into Sockolet & re-welded | /03L-0 on 790214:air Found Blowing Through Weld on 3/4 Inch Vent Line.Caused by Component Failure.Vent Line Inserted Into Sockolet & re-welded | | | 05000254/LER-1979-013-03, /03L-0 on 790217:check Valves 1-263-2-31B & 1-263-42A Failed to Check Flow Through Instrument Lines. Caused by Dirt in Valve Internals.Internals Removed,Cleaned & Reassembled | /03L-0 on 790217:check Valves 1-263-2-31B & 1-263-42A Failed to Check Flow Through Instrument Lines. Caused by Dirt in Valve Internals.Internals Removed,Cleaned & Reassembled | | | 05000254/LER-1979-013, Forwards LER 79-013/03L-0 | Forwards LER 79-013/03L-0 | | | 05000265/LER-1979-013, Forwards LER 79-013/03L-0 | Forwards LER 79-013/03L-0 | | | 05000265/LER-1979-013-03, /031-0 on 790712:while Performing Motor Operated Valve Operability Test,Thermal Overload Relay for Pump Suction Valve 1C RHR Tripped & Could Not Be Reopened.Caused by Loose Electrical Connections at Breaker | /031-0 on 790712:while Performing Motor Operated Valve Operability Test,Thermal Overload Relay for Pump Suction Valve 1C RHR Tripped & Could Not Be Reopened.Caused by Loose Electrical Connections at Breaker | | | 05000254/LER-1979-014, Forwards LER 79-014/03L-0 | Forwards LER 79-014/03L-0 | | | 05000265/LER-1979-014, Forwards LER 79-014/03L-0 | Forwards LER 79-014/03L-0 | | | 05000265/LER-1979-014-03, /031-0 on 790723:steam Inlet Valve Mo 2-1301-16 Failed to Close During Reactor Core Isolation Cooling Monthly Valve Operability Test.Caused by Component Failure of Torque Switch on Valve Mo 2-1301-16.Switch Replaced | /031-0 on 790723:steam Inlet Valve Mo 2-1301-16 Failed to Close During Reactor Core Isolation Cooling Monthly Valve Operability Test.Caused by Component Failure of Torque Switch on Valve Mo 2-1301-16.Switch Replaced | | | 05000254/LER-1979-014-03, /03L-0 on 790214:automatic Blowdown Timers Exceeded Tech Spec Limits During Tests.Caused by Instrument Setpoint Drift.One Timer Readjusted,Another Replaced | /03L-0 on 790214:automatic Blowdown Timers Exceeded Tech Spec Limits During Tests.Caused by Instrument Setpoint Drift.One Timer Readjusted,Another Replaced | |
|