ML19221B727

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Integrated Inspection Report 05000445/2019002 and 05000446/2019002
ML19221B727
Person / Time
Site: Comanche Peak  Luminant icon.png
Issue date: 08/09/2019
From: O'Keefe N
NRC/RGN-IV/DNMS/NMSB-B
To: Peters K
Vistra Operations Company
References
IR 2019002
Download: ML19221B727 (34)


See also: IR 05000445/2019002

Text

August 9, 2019

Mr. Ken Peters

Senior Vice President and Chief Nuclear Officer

VISTRA Operations Company, LLC

P.O. Box 1002

Glen Rose, TX 76043

SUBJECT:

COMANCHE PEAK NUCLEAR POWER PLANT, UNITS 1 AND 2 -

INTEGRATED INSPECTION REPORT 05000445/2019002 AND

05000446/2019002

Dear Mr. Peters:

On June 30, 2019, the U.S. Nuclear Regulatory Commission (NRC) completed an inspection at

Comanche Peak Nuclear Power Plant, Units 1 and 2. On July 2, 2019, the NRC inspectors

discussed the results of this inspection with Mr. Tom McCool and other members of your staff.

A telephonic re-exit was conducted on July 31, 2019, with Mr. Tom McCool and other members

of your staff to discuss a change in characterization on one finding. The results of this

inspection are documented in the enclosed report.

Three findings of very low safety significance (Green) are documented in this report. Each of

these findings involved violations of NRC requirements. Additionally, one Severity Level IV

violation without an associated finding is documented in this report. We are treating these

violations as non-cited violations (NCVs) consistent with Section 2.3.2.a of the Enforcement

Policy.

If you contest the violations or significance or severity of the violations documented in this

inspection report, you should provide a response within 30 days of the date of this inspection

report, with the basis for your denial, to the U.S. Nuclear Regulatory Commission, ATTN:

Document Control Desk, Washington, DC 20555-0001; with copies to the Regional

Administrator, Region IV; the Director, Office of Enforcement; and the NRC Resident Inspector

at Comanche Peak.

If you disagree with a cross-cutting aspect assignment in this report, you should provide a

response within 30 days of the date of this inspection report, with the basis for your

disagreement, to the U.S. Nuclear Regulatory Commission, ATTN: Document Control Desk,

Washington, DC 20555-0001; with copies to the Regional Administrator, Region IV; and the

NRC Resident Inspector at Comanche Peak.

K. Peters

2

This letter, its enclosure, and your response (if any) will be made available for public inspection

and copying at http://www.nrc.gov/reading-rm/adams.html and at the NRC Public Document

Room in accordance with 10 CFR 2.390, Public Inspections, Exemptions, Requests for

Withholding.

Sincerely,

/RA by CYoung for/

Neil F. O'Keefe Chief

Reactor Projects Branch B

Docket Nos. 05000445 and 05000446

License Nos. NPF-87 and NPF-89

Enclosure:

As stated

cc w/ encl: Distribution via LISTSERV

K. Peters

3

COMANCHE PEAK NUCLEAR POWER PLANT, UNITS 1 AND 2 - INTEGRATED

INSPECTION REPORT 05000445/2019002 AND 05000446/2019002 - DATED AUGUST 9,

2019

DISTRIBUTION:

DISTRIBUTION:

SMorris, RA

MShaffer, DRA

AVegel, DRP

MHay, DRP

RLantz, DRS

GMiller, DRS

DCylkowski, RC

DDodson, RIV/OEDO

VDricks, ORA

JWeil, OCA

MOBanion, NRR

AMoreno, RIV/CAO

BMaier, RSLO

RKellar, IPAT

JJosey, DRP

RAlexander, DRP

PJayroe, DRP/IPAT

MHerrera, DRMA

AAthar, DRP

LReyna, DRP

R4Enforcement

DOCUMENT NAME: CP2019002-RP-JEJ

ADAMS ACCESSION NUMBER: ML19221B727

X SUNSI Review

ADAMS:

Non-Publicly Available

X Non-Sensitive

Keyword:

By:BKT

X Yes No

X Publicly Available

Sensitive

NRC-002

OFFICE

SRI/DRP/B

RI/DRP/B

RI/DRP/B

AC/DRS/EB1

C/DRS/EB2

C/DRS/OB

NAME

JJosey

AAthar

RKumana

GGeorge

NTaylor

GWerner

SIGNATURE

/RA/

/RA/

/RA/

/RA/

/RA/

/RA by

COsterholtz

for/

DATE

08/05/2019

07/31/2019

07/31/2019

08/05/2019

08/02/2019

08/01/2019

OFFICE

C:CRS/RCB

C:DNMS/RIB

TL/IPAT

C:DRP/B

NAME

MHaire

GWarnick

RKellar

NOKeefee

SIGNATURE

/RA/

/RA/

/RA/

/RA/

DATE

07/31/2019

08/01/2019

8/01/2019

08/08/2019

FFICIAL RECORD COPY

Enclosure

U.S. NUCLEAR REGULATORY COMMISSION

Inspection Report

Docket Numbers:

05000445 and 05000446

License Numbers:

NPF-87 and NPF-89

Report Numbers:

05000445/2019002 and 05000446/2019002

Enterprise Identifier: I-2019-002-0011

Licensee:

VISTRA Operations Company, LLC

Facility:

Comanche Peak Nuclear Power Plant, Units 1 and 2

Location:

Glen Rose, TX 76043

Inspection Dates:

March 17, 2019 to June 30, 2019

Inspectors:

R. Alexander, Senior Project Engineer

I. Anchondo-Lopez, Reactor Inspector

A. Athar, Resident Inspector

B. Baca, Health Physicist

L. Carson, Senior Health Physicist

N. Hernandez, Operations Engineer

J. Josey, Branch Chief

R. Kumana, Senior Resident Inspector

B. Larson, Senior Operations Engineer

Approved By:

Neil F. O'Keefe, Chief

Reactor Projects Branch B

Division of Reactor Projects

2

SUMMARY

The U.S. Nuclear Regulatory Commission (NRC) continued monitoring the licensees

performance by conducting a integrated inspection at Comanche Peak Nuclear Power Plant,

Units 1 and 2 in accordance with the Reactor Oversight Process. The Reactor Oversight

Process is the NRCs program for overseeing the safe operation of commercial nuclear power

reactors. Refer to https://www.nrc.gov/reactors/operating/oversight.html for more information.

List of Findings and Violations

Failure to Report a Change in Medical Condition of a Licensed Operator

Cornerstone

Significance

Cross-Cutting

Aspect

Report

Section

Not Applicable

NCV 05000446,05000445/2019002-

01

Open

Not Applicable

71111.11B

The NRC identified a Severity Level IV non-cited violation (NCV) of 10 CFR 55.25,

"Incapacitation Because of Disability or Illness," for the licensees failure to notify the NRC

within 30 days of a change in a licensed operators medical condition.

Failure to Evaluate a Change to the Facilities AC Power System

Cornerstone

Significance

Cross-Cutting

Aspect

Report

Section

Mitigating

Systems

Green

NCV 05000446/2019002-02

Open/Closed

None (NPP)

71111.15

The inspectors identified a Green non-cited violation of 10 CFR Part 50, Appendix B, Criterion

III, Design Control, associated with the licensees failure to assure that a design change met

regulatory requirements for sharing of systems among units. Specifically, the licensee

performed a change to the facility to allow the inclusion of Unit 1 specific safety-related loads

on common panels XEC 2-1 and XEC 1-1 but failed to verify that there would be no adverse

effect on the performance of safety functions if these unitized loads were powered from

Unit 2.

Inadequate Operability Evaluation of Control Room Air Conditioning Unit X-01

Cornerstone

Significance

Cross-Cutting

Aspect

Report

Section

Mitigating

Systems

Green

NCV 05000446/2019002-03

Open/Closed

[H.11] -

Challenge the

Unknown

71152

The inspectors identified a Green non-cited violation of 10 CFR Part 50, Appendix B, Criterion

V, Instructions, Procedures, and Drawings, associated with the licensees failure to follow

the requirements of Station Procedure STI-422.01, Operability Determination and

Functionality Assessment Program. Specifically, on December 15, 2018, control room air

conditioning (CRAC) Unit X-01 tripped due to a low lube oil condition caused by freon

absorption in the oil. Operations personnel subsequently declared CRAC X-01 operable and

placed it back in service without understanding the cause of the trip or establishing a

reasonable expectation for operability of the unit.

3

Failure to Provide Adequate Procedure Results in a Reactor Trip

Cornerstone

Significance

Cross-Cutting

Aspect

Report

Section

Initiating Events

Green

NCV 05000446/2019002-04

Open/Closed

[H.12] - Avoid

Complacency

71153

The inspectors reviewed a Green, self-revealing non-cited violation of 10 CFR Part 50,

Appendix B, Criterion V, Instructions, Procedures, and Drawings, associated with the

licensees failure to establish adequate procedural guidance for operators checking for

buzzing relays. This resulted in a feedwater isolation to steam generator 2-04 and operators

inserting a manual reactor trip. The licensee entered this issue into the corrective action

program as Condition Report CR-2019-001949.

Additional Tracking Items

Type

Issue Number

Title

Report Section

Status

LER

05000446,05000445/2

019-001-00

LER 2019-001-00 for

Comanche Peak Nuclear

Power Plant (CPNPP),

Units 1 and 2, LTOP Power

Operated Relief Valve

(PORV) Setpoint.

71153

Closed

LER

05000446/2019-001-

00

LER 2019-001-00 For

Comanche Peak Nuclear

Power Plant (CPNPP) Unit 2,

Manual Reactor Trip Due to

Feedwater Isolation Valve

Closure.

71153

Closed

4

PLANT STATUS

Unit 1 began this inspection period in coast down at 91 percent rated thermal power. The unit

coasted down until April 20, 2019, when the unit was shut down to commence a refueling

outage. On May 26, 2019, the unit began a reactor startup and reached rated thermal power on

May 31, 2019. The unit remained at or near rated thermal power for the remainder of the

inspection period.

Unit 2 operated at or near rated thermal power for the entire inspection period.

INSPECTION SCOPES

Inspections were conducted using the appropriate portions of the inspection procedures (IPs) in

effect at the beginning of the inspection unless otherwise noted. Currently approved IPs with

their attached revision histories are located on the public website at http://www.nrc.gov/reading-

rm/doc-collections/insp-manual/inspection-procedure/index.html. Samples were declared

complete when the IP requirements most appropriate to the inspection activity were met

consistent with Inspection Manual Chapter (IMC) 2515, Light-Water Reactor Inspection

Program - Operations Phase. The inspectors performed plant status activities described in

IMC 2515 Appendix D, Plant Status and conducted routine reviews using IP 71152, Problem

Identification and Resolution. The inspectors reviewed selected procedures and records,

observed activities, and interviewed personnel to assess licensee performance and compliance

with Commission rules and regulations, license conditions, site procedures, and standards.

REACTOR SAFETY

71111.01 - Adverse Weather Protection

External Flooding Sample (IP Section 03.04) (1 Sample)

(1)

The inspectors evaluated readiness to cope with external flooding associated with

Squaw Creek Reservoir level reaching 776.5 feet.

Impending Severe Weather Sample (IP Section 03.03) (1 Sample)

(1)

The inspectors evaluated readiness for impending adverse weather conditions for

severe thunderstorms on March 17, 2019.

71111.04 - Equipment Alignment

Partial Walkdown Sample (IP Section 03.01) (4 Samples)

The inspectors evaluated system configurations during partial walkdowns of the following

systems/trains:

(1)

Unit 2, train B station service water (protected under defense-in-depth strategy-03) on

May 1, 2019

(2)

Unit 1, centrifugal charging pump 1-02 while pump 1-01 was out of service on

June 11, 2019

5

(3)

Unit 2, motor drive auxiliary feedwater pump 2-02 while pump 2-01 was out of service

on June 13, 2019

(4)

Unit 2, reactor coolant system leakage detection instrumentation on June 24, 2019

71111.04S - Equipment Alignment

Complete Walkdown Sample (IP Section 03.02) (1 Sample)

(1)

The inspectors evaluated system configurations during a complete walkdown of the

service water intake and ultimate heat sink system on June 24, 2019.

71111.05Q - Fire Protection

Quarterly Inspection (IP Section 03.01) (5 Samples)

The inspectors evaluated fire protection program implementation in the following selected

areas:

(1)

fire zones 2SA1B and 2SA2A, Unit 2, safeguards building 773' elevation on May 28,

2019

(2)

fire zone AA21a, auxiliary building elevation 790' CCW HX room and hallway area

outside of room on May 14, 2019

(3)

fire zone AA21b, auxiliary building elevation 810' hallways on June 21, 2019

(4)

fire zone SB2c, auxiliary building elevation 773 on June 25, 2019

(5)

fire zone SB4, auxiliary building 773 elevation on June 26, 2019

71111.07A - Heat Sink Performance

Annual Review (IP Section 02.01) (1 Sample)

The inspectors evaluated readiness and performance of:

(1)

Unit 1, diesel generator 1-01 jacket water heat exchanger

71111.08P - Inservice Inspection Activities (PWR)

PWR Inservice Inspection Activities Sample (IP Section 03.01) (1 Sample)

(1)

The inspectors verified that the reactor coolant system boundary, steam generator

tubes, reactor vessel internals, risk-significant piping system boundaries, and

containment boundary are appropriately monitored for degradation and that repairs

and replacements were appropriately fabricated, examined and accepted by

reviewing the following activities from April 29 to May 3, 2019:

03.01.a - Nondestructive Examination and Welding Activities.

6

The inspectors directly observed or reviewed records of the following

Nondestructive activities:

1. Ultrasonic Examination

a. Weld TBX-2-2501-29, Report Number 1RF20-UT-018, Elbow-to-Pipe

in Residual Heat Removal System

b. Weld TBX-2-2501-34, Report Number 1RF20-UT-028, Tee-to-Pipe in

Residual Heat Removal System

c. Weld TBX-1-1100-3, Report Number RV-ISI 2019, Reactor Vessel

Intermediate to Lower Shell weld

d. Weld TBX-1-1100-4, Report Number RV-ISI 2019, Reactor Vessel

Lower Shell to Bottom Head weld

e. Weld TBX-1-1100-7, Report Number RV-ISI 2019, Reactor

Vessel Upper Shell Longitudinal Weld

f. Weld TBX-1-4100-1, 2, Report Number SE-338-01 , Hot Leg One

Reactor Vessel Nozzle to Safe End and Safe End to Pipe

g. Weld TBX-1-4100-14, 13, Report Number SE-293-01 , Cold Leg One

Reactor Vessel Nozzle to Safe End and Safe End to Pipe

h. Weld TBX-1-4200-14, 13, Report Number SE-247-01 , Cold Leg Two

Reactor Vessel Nozzle to Safe End and Safe End to Pipe

i.

Weld TBX-1-4300-1, 2, Report Number SE-158-01 , Hot Leg Three

Reactor Vessel Nozzle to Safe End and Safe End to Pipe

j.

Weld TBX-1-4200-1, 2, Report Number SE-202-01 , Hot Leg Two

Reactor Vessel Nozzle to Safe End and Safe End to Pipe

k. Weld TBX-1-4300-14, 13, Report Number SE-113-01 , Cold Leg Three

Reactor Vessel Nozzle to Safe End and Safe End to Pipe

l.

Weld TBX-1-4400-14, 13, Report Number SE-67-01 , Cold Leg Four

Reactor Vessel Nozzle to Safe End and Safe End to Pipe

m. Weld TBX-1-4400-1, 2, Report Number SE-158-01 , Hot Leg Four

Reactor Vessel Nozzle to Safe End and Safe End to Pipe

2. Magnetic Particle Examination

a. Weld TBX-2-2301-H4, Report Number 1RF20-MT-002, Pipe Welded

Attachment in Feedwater System

3. Liquid Penetrant Examination

a. Weld TBX-2-2568-H28, Report Number 1RF20-PT002, Pipe Welded

Attachment in Safety Injection System

4. Visual Examination

a. Weld TBX-2-2568-H28, Report Number 1RF20-VT-055, Pipe Dual

Struts in Safety Injection System

03.01.b - Pressurized-Water Reactor Vessel Upper Head Penetration Examination

Activities were not required this outage.

03.01.c - Pressurized-Water Reactor Boric Acid Corrosion Control Activities.

The inspector reviewed five boric acid corrosion evaluations and associated

corrective actions contained in condition report 2019-03234.

7

03.01.d - Pressurized-Water Reactor Steam Generator Tube Examination Activities

were not required this outage.

Identification and Resolution of Problems:

The inspector reviewed 16 notifications that dealt with inservice inspections issues

and found that items were entered into the corrective action program at the

appropriate level and addressed correctly.

71111.11B - Licensed Operator Requalification Program and Licensed Operator Performance

Licensed Operator Requalification Program (IP Section 03.04) (1 Sample)

(1)

Biennial Requalification Written Examinations

The inspectors evaluated the quality of the licensed operator biennial requalification

written examination administered on May 29, 2019.

Annual Requalification Operating Tests

The inspectors evaluated the adequacy of the facility licensees annual requalification

operating test.

Administration of an Annual Requalification Operating Test

The inspectors evaluated the effectiveness of the facility licensee in administering

requalification operating tests required by 10 CFR 55.59(a)(2) and that the facility

licensee is effectively evaluating their licensed operators for mastery of training

objectives.

Requalification Examination Security

The inspectors evaluated the ability of the facility licensee to safeguard examination

material, such that the examination is not compromised.

Remedial Training and Re-examinations

The inspectors evaluated the effectiveness of remedial training conducted by the

licensee, and reviewed the adequacy of re-examinations for licensed operators who

did not pass a required requalification examination.

Operator License Conditions

The inspectors evaluated the licensees program for ensuring that licensed operators

meet the conditions of their licenses.

Control Room Simulator

The inspectors evaluated the adequacy of the facility licensees control room

simulator in modeling the actual plant, and for meeting the requirements contained in

10 CFR 55.46.

8

Problem Identification and Resolution

The inspectors evaluated the licensees ability to identify and resolve problems

associated with licensed operator performance.

71111.11Q - Licensed Operator Requalification Program and Licensed Operator Performance

Licensed Operator Performance in the Actual Plant/Main Control Room (IP Section 03.01)

(2 Samples)

(1)

The inspectors observed and evaluated licensed operator performance in the control

room during Unit 1 shutdown on April 20, 2019.

(2)

The inspectors observed and evaluated licensed operator performance in the control

room during Unit 1 startup on May 26, 2019.

Licensed Operator Requalification Training/Examinations (IP Section 03.02) (1 Sample)

(1)

The inspectors observed and evaluated a simulator-based loss of coolant accident

scenario on June 24, 2019.

71111.12 - Maintenance Effectiveness

Routine Maintenance Effectiveness Inspection (IP Section 02.01) (1 Sample)

The inspectors evaluated the effectiveness of routine maintenance activities associated with

the following equipment and/or safety significant functions:

(1)

Radiation monitors on June 27, 2019.

71111.13 - Maintenance Risk Assessments and Emergent Work Control

Risk Assessment and Management Sample (IP Section 03.01) (5 Samples)

The inspectors evaluated the risk assessments for the following planned and emergent work

activities:

(1)

Unit 1, risk mitigating actions associated with insulation removal on the residual

heat removal system on March 18, 2019

(2)

Unit 1, risk mitigating actions associated with Train B EDG system outage window on

April 22, 2019

(3)

Risk mitigating actions associated with spent fuel pool cooling (after Unit 1

fuel offload) on May 1, 2019

(4)

Unit 1, diesel generator 1-02 cylinder liner and piston emergent replacement on

May 15, 2019

(5)

Unit 1, high energy line break damper testing on May 23, 2019

9

71111.15 - Operability Determinations and Functionality Assessments

Operability Determination or Functionality Assessment (IP Section 02.02) (6 Samples)

The inspectors evaluated the following operability determinations and functionality

assessments:

(1)

Units 1 and 2, CRAC X-01 trip on low load on April 8, 2019

(2)

Unit 1, operability of safety systems with power supply panel XEC 2-1 aligned to

Unit 2 on May 9, 2019

(3)

Unit 2 motor drive auxiliary feedwater pump exceeded alert range for vibrations on

May 10, 2019

(4)

Units 1 and 2, potential tornadic missiles due to storage locations on May 28, 2019

(5)

Unit 1, train B EDG exhaust relief valve doghouse insulation worn through on May 30,

2019

(6)

Control room air conditioning calculation did not evaluate heat load from

panel CPX-ECPRCV-13 on June 13, 2019

71111.18 - Plant Modifications

Temporary Modifications and/or Permanent Modifications (IP Section 03.01 and/or 03.02)

(3 Samples)

The inspectors evaluated the following temporary or permanent modifications:

(1)

common service water tunnel sump modification on April 15, 2019

(2)

mechanical stress introduction project on May 22, 2019

(3)

power operated relief valve setpoint changes on May 24, 2019

71111.19 - Post-Maintenance Testing

Post Maintenance Test Sample (IP Section 03.01) (7 Samples)

The inspectors evaluated the following post maintenance tests:

(1)

Unit 1, low temperature over pressure protection setpoint change on April 15, 2019

(2)

Unit 1, diesel generator 1-02 following cylinder liner and piston emergent replacement

on April 29, 2019

(3)

Unit 1, replace oil return trap on control room air conditioning unit X-01, work order 5615078 on May 5, 2019

(4)

Unit 1, work order 5505638, replace regulator on valve 1-8825 on May 6, 2019

10

(5)

Unit 1, work order 5754670, replace solid state protection switch S809 on May 9,

2019

(6)

Unit 1, diesel generator 1-01 following turbocharger replacement on May 13, 2019

(7)

Unit 1, work order 5515877, component cooling water supply valve 1-HV-4515-MO

on May 24, 2019

71111.20 - Refueling and Other Outage Activities

Refueling/Other Outage Sample (IP Section 03.01) (1 Sample)

(1)

The inspectors evaluated 1RF20 activities from March 19 to May 26, 2019.

71111.22 - Surveillance Testing

The inspectors evaluated the following surveillance tests:

Containment Isolation Valve Testing (IP Section 03.01) (1 Sample)

(1)

Unit 1, safety injection check valves 1-8956A and 1-8956B on May 23, 2019

Inservice Testing (IP Section 03.01) (1 Sample)

(1)

Unit 1, OPT-503A stroke time test of valve 1-HV-4168 on May 12, 2019

Surveillance Tests (other) (IP Section 03.01) (4 Samples)

(1)

Unit 1, OPT-417A turbine driven auxiliary feedwater pump control panel load shed

test on March 20, 2019

(2)

power operated relief valve testing following setpoint changes on April 10, 2019

(3)

Unit 2, train A RHR surveillance, OPT-203B on May 15, 2019

(4)

Unit 2, train A integrated test surveillance on May 16, 2019

71114.06 - Drill Evaluation

Select Emergency Preparedness Drills and/or Training for Observation (IP Section 03.01)

(1 Sample)

(1)

The inspectors evaluated an emergency preparedness drill on June 26, 2019

11

RADIATION SAFETY

71124.01 - Radiological Hazard Assessment and Exposure Controls

Contamination and Radioactive Material Control (IP Section 02.03) (1 Sample)

The inspectors evaluated licensee processes for monitoring and controlling contamination

and radioactive material.

(1)

The inspectors evaluated licensee processes for monitoring and controlling

contamination and radioactive material. The inspectors verified the following sealed

sources are accounted for and are intact:

Well Source, 2,178 Curies of Cs-137

HP-60193-XSS, 3.3. Curies Am-241(Be)

HP-60265-XSS, 2.0 Curies Pu-238

HP-60250-XSS, 1.06 Curies Cs 137

High Radiation Area and Very High Radiation Area Controls (IP Section 02.05) (1 Sample)

(1)

The inspectors evaluated risk-significant high radiation area and very high radiation

area controls.

Instructions to Workers (IP Section 02.02) (1 Sample)

The inspectors evaluated instructions to workers including radiation work permits used to

access high radiation areas.

(1)

The inspectors evaluated instructions to workers including radiation work permits

used to access high radiation areas:

Radiation work packages

Mechanical Stress Improvement Process (MSIP): RWPs 2019-2604, 2605, 2606, &

2607

Cavity Decontamination: RWP 2019-1607

Westinghouse Refueling & Support: RWPs 2019-1600 & 1601

Scaffolding Support: RWPs 2019-1215 & 1606

Electronic alarming dosimeter alarms

There were no alarms that occurred during the period of this inspection.

12

Labeling of containers

Cavity Decontamination, 55-gallon drum loaded with contaminated mop heads and

radwaste: 5/1/19

Rad Vault Container - 16 loaded with spent radwaste filters; 5/1/19

Unit-1 Volume Control Tank Room stored with seven 55-gallon drums of radwaste:

5/3/19

Radiation Worker Performance and Radiation Protection Technician Proficiency (IP

Section 02.06) (1 Sample)

(1)

The inspectors evaluated radiation worker performance and radiation protection

technician proficiency.

Radiological Hazard Assessment (IP Section 02.01) (1 Sample)

The inspectors evaluated radiological hazards assessments and controls.

(1)

The inspectors evaluated radiological hazards assessments and controls. The

inspectors reviewed the following:

Radiological surveys

M-20190501-40: Unit-1 Reactor Bldg. 854 Pressurizer Compartment 5/01/19

M-20190501-63: Unit-1 Reactor Bldg. 877 Pressurizer Compartment 5/01/19

M-20190421-9: AMS-4 Unit-1 Reactor Bldg. Containment 905 4/21/19

M-20190421-35: Reactor Bldg. 808 Trash rack 4/21/19

Risk significant radiological work activities

MSIP Project: RWPs 2019-2604, 2605, 2606, & 2607

Cavity Decontamination: RWP 2019-1607

Westinghouse Refueling & Support: RWPs 2019-1600 & 1601

Scaffolding Support: RWPs 2019-1215 & 2607

Air sample survey records

M-20190430-20: AMS-4 Unit-1 Containment Hatch 4/30/19

M-20190430-21: AMS-4 Unit-1 Containment Equipment Hatch 4/30/19

13

M-20190428-1: AMS-4 Unit-1 Containment 905 4/27/19

Radiological Hazards Control and Work Coverage (IP Section 02.04) (1 Sample)

The inspectors evaluated in-plant radiological conditions during facility walkdowns and

observation of radiological work activities.

(1)

The inspectors evaluated in-plant radiological conditions during facility walkdowns

and observation of radiological work activities.

Radiological work package for areas with airborne radioactivity

RWP 2019-1607 M-20190430-21: AMS-4 Unit-1 Containment Equipment Hatch

4/30/19

Cavity Decontamination: M-20190428-1: AMS-4 Unit-1 Containment 905 4/27/19

Steam Generator-1 Area HEPA Filter: 5/1/19

Unit-1 RHR-B Pump Room: M-201801225-10 12/25/18

71124.03 - In-Plant Airborne Radioactivity Control and Mitigation

Engineering Controls (IP Section 02.01) (1 Sample)

The inspectors evaluated airborne controls and radioactive monitoring.

(1)

Installed ventilation systems

CPNPP Control Room Ventilation System

Unit-1 Containment Ventilation System

Unit-1 Primary Plant Ventilation Exhaust Filter X-16

Unit-1 Primary Plant Ventilation Exhaust Filter X-02

Temporary ventilation system setups

Unit-1 Steam Generator Reactor Bldg. 860 HEPA Filter 4/27/19 to 5/2/19

Unit-1 Refueling Floor 860 HEPA Filter 4/27/19 to 5/2/19

Portable or installed monitoring systems

M-20190430-20: AMS-4 Unit-1 Containment Hatch 4/30/19

M-20190430-21: AMS-4 Unit-1 Containment Equipment Hatch 4/30/19

14

M-20190428-1: AMS-4 Unit-1 Containment 905 4/27/19

Self-Contained Breathing Apparatus for Emergency Use (IP Section 02.03) (1 Sample)

The inspectors evaluated self-contained breathing apparatus program implementation.

(1)

Status and surveillance records for SCBAs

Inspected 3 SCBAs located in the CPNPP Control Room 5/2/19

W.O. 5345020 Surveillance: 10 Units 1 & 2 Primary Assembly SCBAs, 7/10/17

W.O. 5345020 Surveillance: 9 Control Room SCBAs, 7/20/17

SCBA fit for on-shift operators

3 Unit-1 Operation/Control Room Staff:

Reactor Operator Qualification

Operator Crew Qualification

Operations Crew Supervisor

SCBA maintenance check

Inspected 3 SCBAs located in the CPNPP Control Room 5/2/19

W.O. 5345020 Surveillance: 10 Units 1 & 2 Primary Assembly SCBAs, 7/10/17

W.O. 5345020 Surveillance: 9 Control Room SCBAs, 7/20/17

Use of Respiratory Protection Devices (IP Section 02.02) (1 Sample)

The inspectors evaluated the licensees use of respiratory protection devices by:

(1)

Evaluations for the use of respiratory protection

b. RWP 2019-1607: 16 Radiation Protection Technicians (Contractor & CPNPP

Staff)

Respiratory protection use during work activities

b. RWP 2019-1607: 16 Radiation Protection Technicians (Contractor & CPNPP

Staff)

Medical fitness for use of respiratory protection devices

b. Nine Senior Radiation Protection Technicians, ERO Qualified through

February 2020

c. Sixteen Radiation Protection Technicians (Contractor & CPNPP Staff)

Observation of donning, doffing and functional test

Four Westinghouse Refuel Contractors

Two CPNPP Decontamination Staff

Three Unit-1 Operation/Control Room Staff

Respiratory protection device evaluation

Six Gen Tex Pure Flows units

15

Six 3M Versa Flows

Eight Full Face Respirators and associated filter cartridges

Four Self-Contained Breathing Apparatus (SCBA)

OTHER ACTIVITIES - BASELINE

71151 - Performance Indicator Verification

The inspectors verified licensee performance indicators submittals listed below:

BI01: Reactor Coolant System (RCS) Specific Activity Sample (IP Section 02.10) (2 Samples)

(1)

Unit 1 from April 1, 2018 through March 31, 2019

(2)

Unit 2 from April 1, 2018 through March 31, 2019

BI02: RCS Leak Rate Sample (IP Section 02.11) (2 Samples)

(1)

Unit 1 from April 1, 2018 through March 31, 2019

(2)

Unit 2 from April 1, 2018 through March 31, 2019

MS05: Safety System Functional Failures (SSFFs) Sample (IP Section 02.04) (2 Samples)

(1)

Unit 1 from April 1, 2018 through March 31, 2019

(2)

Unit 2 from April 1, 2018 through March 31, 2019

OR01: Occupational Exposure Control Effectiveness Sample (IP Section 02.15) (1 Sample)

(1)

September 30, 2018 - April 30, 2019

PR01: Radiological Effluent Technical Specifications/Offsite Dose Calculation Manual

Radiological Effluent Occurrences (RETS/ODCM) Radiological Effluent Occurrences Sample.

(IP Section 02.16) (1 Sample)

(1)

September 30, 2018 - April 30, 2019

71152 - Problem Identification and Resolution

Annual Follow-up of Selected Issues (IP Section 02.03) (2 Samples)

The inspectors reviewed the licensees implementation of its corrective action program

related to the following issues:

(1)

Unit 2 safety bus undervoltage due to loss of 25 kV loop

(2)

Appendix R emergency lighting

Semiannual Trend Review (IP Section 02.02) (1 Sample)

(1)

The inspectors reviewed the licensees corrective action program for trends that might

be indicative of a more significant safety issue. The inspectors review was focused

on operability evaluations performed by operations department personnel during the

period of December 1, 2018 to June 30, 2019.

16

71153 - Followup of Events and Notices of Enforcement Discretion

Event Report (IP Section 03.02) (2 Samples)

The inspectors evaluated the following licensee event reports (LERs):

(1)

Licensee Event Report 05000446/2019-01, "Manual Reactor Trip Due To Feedwater

Isolation Valve Closure," on June 17, 2019 (ADAMS Accession No. ML19127A143).

The circumstances surrounding this LER are documented in report Section Inspection

Results.

(2)

Licensee Event Report 05000445/2019-01, "LTOP Power Operated Relief

Valve (PORV) Setpoint," on June 28, 2019 (ADAMS Accession No. ML19127A079).

The circumstances surrounding this LER are documented in report Section Inspection

Results.

INSPECTION RESULTS

Observation: Semi-Annual Trend Review

71152

The inspectors review focused on inadequate operability and functionality evaluations and

considered the results of daily inspector corrective action program item screenings during the

period of December 1, 2018 to June 30, 2019.

The inspectors reviewed operability evaluations documented in station condition reports.

During their review the inspectors identified a declining trend associated with operator

knowledge when performing operability and functionality evaluations. Specifically, the

inspectors identified eight examples, including one non-cited violation, of inadequate

operability determinations. Examples are:

TR-2018-5446 identified an issue with a temperature controller for the operations

support center, emergency plan equipment. Operations personnel failed to evaluate

functionality of the equipment despite procedure STI-433.01, Maintaining Equipment

Important to Emergency Response, stating that issues with this equipment required

functionality assessments. This issue could have affected habitability of the

operations support center.

CR-2018-008521 identified that control room air conditioning unit X-01 tripped

following a valid surveillance test start demand due to a low lube oil condition caused

by freon absorption in the oil. Operations personnel subsequently declared

CRAC X-01 operable and placed it back in service without understanding the cause of

the trip or establishing a reasonable expectation for operability of the unit. This could

affect the ability of the machine to perform its safety function of being able to start and

run when needed and had caused an actual failure during the surveillance test.

CR-2019-000324 identified a component on steam generator atmospheric relief

valves as not meeting environmental qualification requirements. Operations

personnel incorrectly determined that the atmospheric relief valves were not required

to be environmentally qualified despite the FSAR stating they were required to

17

function in a harsh environment. This could have resulted in equipment not being

able to function during an event.

CR-2019-001628 identified that an atmospheric relief valve was experiencing leakage.

Operations personnel incorrectly determined that the leakage did not affect the reactor

despite the FSAR stating that during accident scenarios the atmospheric relief valves

are assumed to be closed. This appeared to place the plant outside accident

analyses and therefore could have affected the licensee's ability to mitigate an

accident.

CR-2019-001830 and CR-2019-001836 identified both surface and pitting corrosion

on service water piping. Operations personnel evaluated the surface corrosion in the

documented operability evaluation but failed to evaluate the pitting corrosion. This

could have affected the structural integrity of the piping system which could have

affected the systems ability to respond to an event.

CR-2019-003498 noted boric acid on a safety related snubber. Operations personnel

failed to evaluate the ability of the component to function in the identified condition.

CR-2019-003672 identified that the fire protection system had experienced a water

hammer event. Operations personnel failed to evaluate the functionality of the piping

for this type of event.

Upon identification of these issues by the inspectors the licensee appropriately entered these

issues into the station's corrective action program.

While the inspectors determined that most of these issues were minor in nature, inspectors

determined that they were the result of operator knowledge gaps with respect to the facility's

licensing basis documented in the FSAR, which is a primary part of the process for assessing

operability and functionality. The inspectors determined that these issues were indicative of a

declining trend associated with operator knowledge when performing operability evaluations.

Failure to Report a Change in Medical Condition of a Licensed Operator

Cornerstone

Severity

Cross-Cutting

Aspect

Report

Section

Not

Applicable

Severity Level IV

NCV 05000446,05000445/2019002-01

Open

Not

Applicable

71111.11B

The NRC identified a Severity Level IV non-cited violation (NCV) of 10 CFR 55.25,

"Incapacitation Because of Disability or Illness," for the licensees failure to notify the NRC

within 30 days of a change in a licensed operators medical condition.

Description:

On August 8, 2018, during a biennial license physical examination for a senior reactor

operator, the designated medical examiner (DME) determined that the individual required a

prescription for corrective lenses; therefore, a condition was required to be added to the

individuals license. The DME further determined that a no solo condition was also required

for a worsening health condition. At that time, the individual was undergoing evaluation and

treatment by his primary care physician. The facility licensee failed to notify the NRC within

30 days of learning of the disability or illness. The inspectors identified this failure to inform

18

the NRC on March 19, 2019, during a sampling review of medical records for individual

license holders.

The inspectors verified, through interviews, that the individual had been wearing the

prescription lenses as prescribed, and that at no time was the individual in solo operation of

the controls, as verified by station log reviews and interviews with various station personnel.

The inspectors also noted that the individual had committed no errors while on shift or been

involved in any operational mishaps or near misses.

Corrective Actions: On March 28, 2019, Comanche Peak Nuclear Power Plant submitted a

letter to the NRC with a revised NRC Form 396, Certification of Medical Examination by

Facility Licensee, that reflected two new license conditions: one for wearing the prescription

lenses and one prohibiting solo operation of the controls. The prescription lens and no solo

conditions were required for fitness-for-duty reasons in accordance with the American

National Standards Institute (ANSI)-3.4-1983, Medical Certification And Monitoring Of

Personnel Requiring Operator Licenses For Nuclear Power Plants,

Corrective Action References: Condition Report CR-2019-002428

Performance Assessment: The inspectors determined this violation was associated with a

minor performance deficiency.

The performance deficiency is minor because a licensing decision was not made due to the

absence of this medical information, and the individual did follow the required restrictions for

the diagnosed medical conditions.

Enforcement: The ROPs significance determination process does not specifically consider

the regulatory process impact in its assessment of licensee performance. Therefore, it is

necessary to address this violation which impedes the NRCs ability to regulate using

traditional enforcement to adequately deter non-compliance.

Severity: The inspectors determined the violation to be a Severity Level IV violation similar to

Example 6.4.d.1.a in the NRC Enforcement Policy. Specifically, the licensee non-willfully

failed to inform the NRC of a change in an operators medical condition, which did not

contribute to the NRC making an incorrect regulatory decision. In addition, the individual

adhered to the ANSI 3.4 requirements for the changes in his medical condition.

Violation: Title 10 CFR 55.25 requires, in part, that if a licensed senior operator develops a

permanent physical condition that causes the licensee to fail to meet the requirements of

10 CFR 55.21, the facility shall notify the Commission within 30 days of learning of the

diagnosis. For conditions where a license condition is required, the facility licensee must

provide medical certification on NRC Form 396, "Certification of Medical Examination by

Facility Licensee." Contrary to the above from August 8, 2018 to March 28, 2019, the

licensee failed to notify the Commission, within 30 days of learning the diagnosis, of a change

in medical condition of a licensed senior operator that developed a permanent physical

condition that caused the licensed senior operator to fail to meet the requirements of

10 CFR 55.21. Specifically, on August 8, 2018, during a biennial license physical for the

senior reactor operator, the DME determined that the individual required conditions on his

license for prescription corrective lenses and a no solo condition, but the NRC did not

receive the revised NRC Form 396 until March 28, 2019.

19

Enforcement Action: This violation is being treated as a non-cited violation, consistent with

Section 2.3.2 of the Enforcement Policy.

Failure to Evaluate a Change to the Facilities AC Power System

Cornerstone

Significance

Cross-Cutting

Aspect

Report

Section

Mitigating

Systems

Green

NCV 05000446/2019002-02

Open/Closed

None (NPP)

71111.15

The inspectors identified a Green non-cited violation of 10 CFR Part 50, Appendix B, Criterion

III, Design Control, associated with the licensees failure to assure that a design change met

regulatory requirements for sharing of systems among units. Specifically, the licensee

performed a change to the facility to allow the inclusion of Unit 1 specific safety-related loads

on common panels XEC 2-1 and XEC 1-1 but failed to verify that there would be no adverse

effect on the performance of safety functions if these unitized loads were powered from

Unit 2.

Description:

While performing status walkdowns on April 1, 2019, the inspectors noted that the licensee

had shifted power supplied to AC buses XEC 2-1 and XEC 1-1 from Unit 1 power to Unit 2

power. Because of previous issues identified with common power buses

(NCV 05000445/2019001-02, Failure to Evaluate a Change to the Facility DC Power

System) the inspectors asked the licensee if there were any Unit 1 specific loads supplied by

these panels, and whether these loads were operable while powered from Unit 2.

The licensee informed the inspectors that there were Unit 1 loads on buses XEC 2-1 and

XEC 1-1 and that since the swap had been done in accordance with an approved procedure,

SOP-607A, 118 VAC Distribution System and Inverters, and the busses were being power

by a safety-related 1E power supply from the other unit, all loads were operable.

Inspectors were concerned that this configuration did not appear consistent with the facility

design requirements and current licensing bases. Of note, 10 CFR 50, Appendix A, General

Design Criterion 5, Sharing of structures, systems, and components, states that structures,

systems, and components important to safety shall not be shared among nuclear power units

unless it can be shown that such sharing will not significantly impair their ability to perform

their safety functions, including, in the event of an accident in one unit, an orderly shutdown

and cooldown of the remaining units.

Inspectors reviewed NUREG-0797, Safety Evaluation Report related to the operation of

Comanche Peak Steam Electric Station, Units 1 and 2 Docket Nos. 50-445 and 50-446,

Supplement 22 and the facilities FSAR and identified the following with regard to sharing

safety systems:

The site was licensed with a commitment to Regulatory Guide (RG) 1.81, Shared

Emergency and Shutdown Electric Systems for Multi-Unit Nuclear Power Plants,

without exceptions.

RG 1.81 contains three regulatory Positions.

o C.1 required that DC systems in multi-unit nuclear power plants should not be

shared.

20

o C.2 covered plants which were under construction before June 1,1973 and

stated that these plants would be reviewed by the NRC on an individual case

basis. This position gave seven criteria that should be satisfied by the

applicant.

o C.3 stated that for multi-unit plants for which a construction permit was issued

on or after June 1, 1973, should have separate and independent onsite

emergency and shutdown electric systems.

The facility submitted their construction permit application for Unit 1 after June 1,

1973.

NUREG-0797, Section 8.3, states that there is no sharing of emergency power

sources between units, which is in accordance with RG 1.81.

FSAR Section 8.3.1.1.9, Sharing of Equipment between Two Units, states, in part,

that nuclear-safety-related loads associated with each unit are powered exclusively

from Class 1E systems of that particular unit and nuclear-safety-related loads

common to both units are powered from Class 1E MCCs and distribution panels which

have supplies from each unit. The inspectors noted that this was no longer true

because there were unit-specific loads on shared panels XEC1-1 and XEC 2-1.

Furthermore, the inspectors noted that in January 2000, the licensee had previously

discovered that they had unit-specific safety-related loads from both Units 1 and 2 on

common panels XEC 1-1 and XEC 2-1 in addition to the previously evaluated shared

systems, contrary to what was described in their FSAR. The licensee entered this design

control issue into the corrective action program as Condition Report CR-2000-000142. As

corrective actions the licensee removed the Unit 2 loads from these common panels, changed

the normal power supply of XEC 2-1 from Unit 2 to Unit 1, left the Unit 1 loads on both of

these common panels, revised the description of their commitment to RG 1.81, and

performed a 10 CFR 50.59 screening for this change.

The inspectors reviewed 50.59 screening document 59SC-2000-000142-02-02 and noted that

as justification for this change the licensee stated, in part;

that the design is controlled such that loads of only Unit 1 are fed from

a common panel and the normal source of power for the panel is

Unit 1the unit specific loads of only one unit are fed from a common

panel and the common panel normal power source is the same unit,

therefore, under normal operation, the interaction between the units for

maintenance and test operation will be no different than what is required

for a common panel. The time when such common panel is aligned to

the units other than the one whose specific loads it feeds will be limited,

any additional interaction needed for maintenance and test activities will

be limited only.

Based on this justification, the licensee concluded that the requirements of RG 1.81,

Regulatory Position C2 were met. Specifically, the sharing of the system is limited between

two units only. A single failure at the system level, due to redundancy for common systems

being maintained the same as for each unit, shall not preclude capability to automatically

supply minimum ESF loads in any one unit and safely shutdown the other unit assuming a

21

loss of off-site power.

The inspectors determined that the licensee inappropriately applied Regulatory Position C.2.

Specifically:

RG 1.81 Regulatory Position C.2 was not applicable to Comanche Peak because their

construction permit application was submitted after June 1, 1973. Also, this position

included the statement that the NRC would review the proposed design for plants

using this set of standards and did not contain an allowance for self-approval.

Comanche Peak was originally evaluated for compliance against regulatory

position C.3, and the licensee failed to properly change their commitment through the

commitment change process.

The licensee failed to document an analysis that demonstrated that such sharing will

not significantly impair their ability to perform their safety functions, including, in the

event of an accident in one unit, an orderly shutdown and cooldown of the remaining

units.

The unit specific loads on the common panels could result in new failure modes for previously

evaluated accidents. For example, non-1E buses 1EB1-2 and 1EB1-3 have shunt trip

isolation devices that receive a signal from a contacts powered from XEC 1-1. The

licensing basis credits these shunt trips as isolation devices between the non-1E and 1E

buses. During a safety injection actuation on Unit 1 with XEC 1-1 being powered from Unit 2

a single failure (loss of power to this bus) would result in the shunt trip devices not actuating

and leaving the non-1E buses aligned to the Unit 1 emergency diesel generators. This

configuration could impact the emergency diesel generators capability to provide adequate

power for safe shutdown. Based on this the inspectors determined that the inclusion of Unit 1

specific safety related loads on common panels XEC 1-1 and XEC 2-1 was a change to the

facility as described in the FSAR. The inspectors also determined that the licensee had failed

to ensure that this change was subject to design control measures commensurate with those

applied to the original design. Specifically, the NRC had reviewed and approved the stations

shared safety-related electrical bus schemes, and in this instance the site had authorized this

change without any review to determine if there were adverse interactions.

The licensee entered this violation into their corrective action program. The licensee

performed an analysis, EV-CR-2019-003684-2, to evaluate the effects on Unit 1 with cross

powered safety loads. This analysis determined that there were potential detrimental effects

associated with cross connecting Unit 1 safety loads to Unit 2 and recommended that these

loads be powered from Unit 1 pending further review.

Corrective Actions: The licensee entered this violation into their corrective action program.

The licensee performed an analysis, EV-CR-2019-003684-2, to evaluate the effects on Unit 1

with cross powered safety loads. This analysis determined that there were potential

detrimental effects associated with cross connecting Unit 1 safety loads to Unit 2 and

recommended that these loads be powered from Unit 1 pending further review.

Corrective Action References: CR-2019-003684

Performance Assessment:

22

Screening: The inspectors determined the performance deficiency was more than minor

because it was associated with the Design Control attribute of the mitigating systems

cornerstone and it adversely affected the cornerstone objective to ensure the availability,

reliability, and capability of systems that respond to initiating events to prevent undesirable

consequences (i.e., core damage).

Significance: The inspectors assessed the significance of the finding using Appendix A, The

Significance Determination Process (SDP) for Findings At-Power.

Cross-Cutting Aspect: Not Present Performance. No cross-cutting aspect was assigned to

this finding because the inspectors determined the finding did not reflect present licensee

performance.

Enforcement:

Violation: Title 10 CFR 50.59 requires, in part, that if the licensee makes changes to the

facility as described in the FSAR without obtaining a license amendment, they must maintain

a written evaluation which provides the basis for determining that the change does not require

a licensee amendment. Contrary to the above, in April 2002, the licensee made a change to

the facility as described in the FSAR without obtaining a license amendment but did not

maintain a written evaluation which provides the basis for determining that the change does

not require a licensee amendment.

Enforcement Action: This violation is being treated as a non-cited violation, consistent with

Section 2.3.2 of the Enforcement Policy.

Inadequate Operability Evaluation of Control Room Air Conditioning Unit X-01

Cornerstone

Significance

Cross-Cutting

Aspect

Report

Section

Mitigating

Systems

Green

NCV 05000446/2019002-03

Open/Closed

[H.11] -

Challenge the

Unknown

71152

The inspectors identified a Green non-cited violation of 10 CFR Part 50, Appendix B,

Criterion V, Instructions, Procedures, and Drawings, associated with the licensees failure to

follow the requirements of station procedure STI-422.01, Operability Determination and

Functionality Assessment Program. Specifically, on December 15, 2018, control room air

conditioning (CRAC) Unit X-01 tripped due to a low lube oil condition caused by freon

absorption in the oil. Operations personnel subsequently declared CRAC X-01 operable and

placed it back in service without understanding the cause of the trip or establishing a

reasonable expectation for operability of the unit.

Description: On December 15, 2018, during the performance of integrated testing CRAC

Unit X-01 tripped due to low lube oil pressure. Operators declared X-01 inoperable and

initiated Condition Report (CR) 2018-008521 to capture this issue in the station's corrective

action program. Operations also requested an evaluation from engineering for the identified

condition.

Engineering documented an evaluation in EV-CR-2018-008521-1 later in the day on

December 15, 2018. This evaluation concluded that CRAC X-01 had tripped due to

refrigerant migration into the oil, and went on to state that the condition did not need to be

corrected because under normal system loading the velocity of the refrigerant traveling

23

through the system and the piping arrangements returns the oil back to the compressors

crankcase (removing the potential for the low pressure condition at the suction of the

compressor). Operators then declared CRAC X-01 operable.

The inspectors subsequently reviewed CR-2018-008521 and the engineering evaluation

documented in EV-CR-2018-008521-1. During their review inspectors questioned the

adequacy of the engineering evaluation and the operability decision with respect to the cause

of the trip being refrigerant migration. Specifically, the safety function of the CRAC units is to

start and run when needed to maintain the control room environment during accidents, and

refrigerant migration occurs when the unit is secured and is caused by differential pressure

between the oil in the compressors crankcase and refrigerant. Inspectors noted that the

CRACs are not continuously in operation and each unit typically runs one CRAC for two

weeks with the other in standby for that period of time, and CRAC X-01 had been secured for

approximately two weeks prior to integrated testing.

The inspectors reviewed Procedure STI-422.01, Operability Determination and Functionality

Assessment Program, and noted that the following definitions are provided for operability

declaration in section 4.15, presumption of operability in section 4.17, and reasonable

expectation of operability in Section 4.18. These definitions establish that: an operability

declaration is a decision made by an SRO on the operating shift crew that there is reasonable

expectation that an SSC can perform its specified safety function; the presumption of

operability is based on the concept that technical specifications are organized and

implemented on the presumption that systems are operable and without information to the

contrary, it is reasonable to assume that once a system or component is established as

operable, it will remain operable with surveillances providing that assurance; and a

reasonable expectation of operability is the expectation that the evidence collected supports

determining that a TS SSC is capable of performing its specified safety function.

Section 6.2.G states, in part, that operability determinations should include the effect or

potential effect of the degraded or non-conforming condition on the affected SSCs ability to

perform the specified safety functions, and whether there is a reasonable expectation of

operability, including the basis for the determination.

The inspectors determined that the licensee had failed to evaluate the potential effect of

refrigerant migration on CRAC X-01 with respect to its ability to perform its specified safety

function and establish a reasonable expectation of operability. Specifically, the licensee

evaluated the ability of the system to continue running with the condition present but failed to

evaluate the ability to successfully start and reach a stable running condition, despite the fact

that the evaluation was triggered by a failure to successfully start. The inspectors informed

the licensee of their concerns and the licensee initiated CR-2019-005092 to capture this issue

in the stations corrective action program.

Corrective Actions: The licensee performed an operability evaluation which established a

reasonable expectation of operability and is evaluating corrective actions.

Corrective Action References: CR-2019-002092

Performance Assessment:

Performance Deficiency: The failure to evaluate the potential effect of refrigerant migration

on CRAC X-01 with respect to its ability to perform its specified safety function and establish

a reasonable expectation of operability was a performance deficiency.

24

Screening: The inspectors determined the performance deficiency was more than minor

because it was associated with the Equipment Performance attribute of the Mitigating

Systems cornerstone and it adversely affected the cornerstone objective to ensure the

availability, reliability, and capability of systems that respond to initiating events to prevent

undesirable consequences (i.e., core damage). Specifically, the licensee evaluated the issue

enough to understand the physical mechanism that caused of the chiller trip but failed to

evaluate the reason this mechanism was present to the degree that it could create a condition

that resulted in an actual trip.

Significance: The inspectors assessed the significance of the finding using Appendix A, The

Significance Determination Process (SDP) for Findings At-Power.

Cross-Cutting Aspect: H.11 - Challenge the Unknown: Individuals stop when faced with

uncertain conditions. Risks are evaluated and managed before proceeding. Specifically,

operators failed to stop and use all available information to ensure they fully understood the

issue prior to declaring CRAC X-01 operable.

Enforcement:

Violation: Title 10 CFR Part 50, Appendix B, Criterion V, Instructions, Procedures, and

Drawings, requires, in part, that activities affecting quality shall be prescribed by documented

instructions, procedures, or drawings, of a type appropriate to the circumstances and shall be

accomplished in accordance with these instructions, procedures, and drawings.

Procedure STI-422.01, Operability Determination and Functionality Assessment Program, a

procedure that is appropriate to the circumstances of evaluating the operability of

safety-related components, Section 6.2.G requires, in part, that operability determinations

should include the effect or potential effect of the degraded or non-conforming condition on

the affected SSCs ability to perform the specified safety functions, and whether there is a

reasonable expectation of operability, including the basis for the determination.

Contrary to the above, on December 15, 2019, an activity affecting quality was not

accomplished in accordance with procedures appropriate to the circumstances. Specifically,

operations personnel failed to follow the requirements of station procedure STI-422.01,

Operability Determination and Functionality Assessment Program, Section 6.2.G.

Specifically, the licensee failed to evaluate the potential effect of refrigerant migration on

CRAC X-01 with respect to its ability to start with refrigerant in the oil and establish a

reasonable expectation of operability.

Enforcement Action: This violation is being treated as a non-cited violation, consistent with

Section 2.3.2 of the Enforcement Policy.

Failure to Provide Adequate Procedure Results in a Reactor Trip

Cornerstone

Significance

Cross-Cutting

Aspect

Report

Section

Initiating Events

Green

NCV 05000446/2019002-04

Open/Closed

[H.12] - Avoid

Complacency

71153

The inspectors reviewed a Green, self-revealing non-cited violation of 10 CFR Part 50,

Appendix B, Criterion V, Instructions, Procedures, and Drawings, associated with the

25

licensees failure to establish adequate procedural guidance for operators checking

for buzzing relays. This resulted in a feedwater isolation to steam generator 2-04 and

operators inserting a manual reactor trip.

Description:

On March 3, 2019 an operator was checking for buzzing relays as required by the Shift

Manager Daily Activities Log. During these checks the operator heard an audible buzzing

sound and attempted to positively identify exactly which relay was buzzing by touching the

suspected relay to check for vibration. When the operator made contact with the relay they

also inadvertently made contact with the relay plunger which resulted in steam generator 2-04

feedwater isolation valve 2-HV-2137 shutting. When valve 2-HV-2137 shut this resulted in a

loss of main feedwater to steam generator 2-04 which caused an alarm for divergent level

and resulted in operators manually tripping the reactor. The licensee entered this issue in the

stations corrective action program as CR-2019-001949.

The licensee performed an Organizational Effectiveness Investigation and determined that

the cause of this event was that the Shift Manager Daily Activities Log did not provide

adequate guidance to operators for how to safely perform buzzing relay checks. The lack of

adequate guidance resulted in the operator using their own judgement based on their

individual risk perception.

The inspectors reviewed the licensee evaluation and determined that the licensees actions

had determined the cause and the proposed corrective actions appeared to be adequate to

address this issue.

Corrective Actions: The licensees corrective actions for this issue were to remove buzzing

relay checks from the operators responsibilities and perform a risk review of all routine

operations activities to ensure that adequate procedural guidance is provided.

Corrective Action References: CR-2019-001949

Performance Assessment:

Performance Deficiency: The failure to provide adequate procedural guidance on how to

perform buzzing relay checks was a performance deficiency.

Screening: The inspectors determined the performance deficiency was more than minor

because it was associated with the Human Performance attribute of the Mitigating Systems

cornerstone. It adversely affected the cornerstone objective of limiting the likelihood of events

that upset plant stability and challenge critical safety functions during shutdown as well as

power operations because the finding resulted in operators manually tripping the reactor.

Specifically, the inadequate procedure resulted in an operator using their own judgement and

inadvertently touching the relay plunger causing a feedwater isolation to steam

generator 2-04.

Significance: The inspectors assessed the significance of the finding using Appendix A, The

Significance Determination Process (SDP) for Findings At-Power.

Cross-Cutting Aspect: H.12 - Avoid Complacency: Individuals recognize and plan for the

possibility of mistakes, latent issues, and inherent risk, even while expecting successful

outcomes. Individuals implement appropriate error reduction tools. Specifically, the operator

26

used their own judgement to decide to touch a relay based on their individual risk perception

without planning for mistakes or understanding the risk of the activity.

Enforcement:

Violation: Title 10 CFR Part 50, Appendix B, Criterion V, Instructions, Procedures, and

Drawings, states, in part, that activities affecting quality shall be prescribed by documented

instructions, procedures, or drawings, of a type appropriate to the circumstances. Contrary to

the above, on March 3, 2019 the licensee failed to prescribe by documented instructions,

procedures, or drawings appropriate to the circumstances that provided guidance for

operators performing buzzing relay checks. This resulted in a feedwater isolation to steam

generator 2-04 and operators inserting a manual reactor trip.

Enforcement Action: This violation is being treated as a non-cited violation, consistent with

Section 2.3.2 of the Enforcement Policy.

EXIT MEETINGS AND DEBRIEFS

The inspectors verified no proprietary information was retained or documented in this report.

On July 2, 2019, the inspectors presented the quarterly resident inspector inspection

results to Mr. Tom McCool and other members of the licensee staff.

On May 3, 2019, the inspectors presented the Occupational Safety Cornerstone

Inspection IP 71124.01/03 and PI IP 71151 ORS/PRS Exit Meeting to Mr. T. McCool,

Senior Vice President and other members of the licensee staff.

On May 15, 2019, the inspectors presented the Inservice Inspection Exit Meeting to

Dave Goodwin, Director Site Engineering and other members of the licensee staff.

On June 3, 2019, the inspectors presented the Biennial Requalification Inspection to

Gary Struble, Regulatory Affairs Specialist and other members of the licensee staff.

27

DOCUMENTS REVIEWED

Inspection

Procedure

Type

Designation

Description or Title

Revision or

Date

71111.08P Corrective Action

Documents

CR-YYYY-NNNN

2017-12392, 2017-11619, 2017-12371, 2017-12391,

2017-12859, 2018-00318, 2018-02385, 2018-03983,

2018-05224, 2018-08475, 2018-08535, 2019-03374,

2019-00542, 2019-03234, 2019-00211, 2019-05839.

Drawings

TBX-1-1100

Inservice Inspection Location Isometric

1

Miscellaneous

CP-201900257

Unit 1 - Third Interval ASME Section XI Inservice Inspection

Program Plan

2

Procedures

MRS-SSP-3498

TBX RV Nozzle to Safe End Weld MSIP Field Service

Procedure

0

STA-737

Boric Acid Corrosion Detection and Evaluation

8

STI-737.01

Boric Acid Corrosion Detection and Evaluation

0

TX-ISI-11

Liquid Penetrant Examination for Comanche Peak Nuclear

Power Plant

5

TX-ISI-302

Ultrasonic Examination of Austenitic Piping Welds

5

TX-ISI-70

Magnetic Particle Examination for Comanche Peak Nuclear

Power Plant

14

TX-ISI-8

VT-1 and VT-3 Visual Examination Procedure

11

WDI-PJF-

1321507-EPP-

001

Examination Program Plan (Scan Plan)

1

71111.11B Corrective Action

Documents

CR-YYYY-NNNN

2017-03868, 2017-03964, 2017-04417, 2017-04499,

2017-04572, 2017-04683, 2017-06489, 2017-07890,

2017-08016, 2017-08672, 2017-09069, 2017-09904,

2017-09915, 2018-03312, 2018-03681, 2018-03745,

2018-03796, 2018-04038, 2018-05098, 2018-05130,

2018-05461, 2018-06369, 2018-07381, 2018-07384,

2018-08504, 2019-00555, 2019-01052, 2019-01240

TR-YYYY-NNNN

2017-03029, 2017-03066, 2017-03068, 2017-03083,

2017-03292, 2017-03770, 2017-05956, 2017-06540,

2017-08662, 2017-07003, 2017-07446, 2017-09096,

2017-12278, 2018-06584, 2018-06280, 2018-06291,

2018-06321, 2018-07045, 2019-01040

28

Inspection

Procedure

Type

Designation

Description or Title

Revision or

Date

Miscellaneous

LORT Cycle 18-5 Simulator Crews

2018 Licensed Operator Requalification Written Exam

Feb 22,

2019

2018 Licensed Operator Requalification Operating Test

Jan 30, 2019

2017-2018 Requalification Operating Test Sample Plan

Mar 11,

2019

2017-2018 Requalification Written Exam Sample Plan

Mar 11,

2019

RO Remedial Exam #1

Feb 28,

2018

SRO Remedial Exam #1

Feb 28,

2018

License Reactivation - 2017-2019

Simulator Differences List

Jan 28, 2019

LL DM.CE

Lessons Learned from Design Modifications and Current

Events Training

Sep 25,

2017

MC-

OPD1.F17.IR4

Cycle 17-6 Design Modifications and Current Events

Feb 20,

2018

SOC-18-03

Simulator Oversight Committee Meeting Minutes

Mar 7, 2018

SOC-18-06

Simulator Oversight Committee Meeting Minutes

Jun 28, 2018

SOC-19-02

Simulator Oversight Committee Meeting Minutes

Feb 5, 2019

Procedures

NTG-104

Nuclear Training Guideline 104 - Implementation

21

ODA-102

Operations Department Administrative Manaual section 102

- Conduct of Operations

27

ODA-407

Operations Department Administrative Manual section 407 -

Procedures Use and Adherence

16

OGPD-13

Operations Guideline 13 - Simulator Training Standards

Jun 27, 2017

OGPD-3

Operations Guideline 3 - Operations Standards and

Expectations

Jun 14, 2018

OGPD-6

Operations Guideline 6 - Operations Department

Performance Management, Monitoring, and Improvement

Jan 7, 2019

SAPT-004

Simulator Annual Performance Test 004 - Core Performance

Test

2

SAPT-1

Simulator Annual Performance Test 1 - Steady State Test

2

29

Inspection

Procedure

Type

Designation

Description or Title

Revision or

Date

SAPT-2

Simulator Annual Performance Test 2 - Transient

Performance Test

2

SAPT-3

Simulator Annual Performance Test 3 - Malfunction Test

2

STA-105

Station Administrative Manual section 105 - Nuclear Training

Department Administration

13

STA-106

Station Procedure 106 - Nuclear Training Records

1

STA-121

Station Procedure 121 - Licensed Operator Physicals and

License Application Process

5

STA-419

Station Procedure 419 - Management Oversight of Training

Programs

15

STA-501

Station Procedure 501 - Nonroutine Reporting

21

STI-214.01

Station Instruction 214.01 - Control of Timed Operator

Actions

1

TRA-204

Training Procedure 204 - Licensed Operator Requalification

Training

18

TRA-206

Training Procedure 206 - Examination Control and

Implementation

0

TRA-207

Training Procedure 207 - Simulator Configuration

Management

0

TRA-208

Training Procedure 208 - Simulator Training

0

TRA-295

Training Procedure 205 - Shift Technical Advisor Training

12

TRI-204.01

Training Instruction 204.01 - Licensed Operator

Requalification Training Processes and Program Reviews

0

TRI-206.02

Training Instruction 206.02 - NRC Requalification Exam

Development Process

0

TRI-206.02

NRC Exam Development Process

0

TRI-206.04

Training Instruction 206.04 - Licensed Operator Requal

Periodic Exams

0

TRI-208.02

Training Instruction 208.02 - Conduct of LORT Simulator

Training

0

71111.15

Corrective Action

Documents

CR-YYYY-NNNN

2000-000142, 2019-003684

Miscellaneous

59SC-2000-

000142-02-02

30

Inspection

Procedure

Type

Designation

Description or Title

Revision or

Date

71124.01

Corrective Action

Documents

IR/TR/CR

2019 - 002448, 002331, 001511, 001117, 001547

2018 - 009060, 009021, 009016, 008400, 00840

Corrective Action

Documents

Resulting from

Inspection

IR-2019

003649, 003650, 003681, 003681

Miscellaneous

1RF20

Cavity Recovery Action Plan for MSIP

2/1/19

DIDCP No.

!RF20-02

Contingency Plan: Containment Closure & Maintaining

Common Area Pressure Boundary

2

RPI-305-2

LHRA/VHRA Key Log

April - May

2019

Procedures

RPI-212

Radioactive Source Control

13

RPI-302

Radiation and Contamination Surveys

1

RPI-303

Radiological Air Sampling

0

RPI-304

Radiological Posting and Labeling

3

RPI-305

Access Controls for High Radiation Areas

3

RPI-629

Radiological Risk Management

5

RPI-700

Sealed Source Leak Testing

13

STA-650

General Health Physics Plan

8

STA-660

Control of High Radiation Areas

18

Radiation

Surveys

M-20190421-29

1-155D-G 1RF20 Initial Entry Survey

M-20190421-35

1-154A/D 1RF20 808' Trash Racks

M-20190421-36

1-154A-D 1RF20 Initial Entry Survey

M-20190421-9

1 905 1RF20 Initial Entry

M-20190423-56

1RF20 (1-155H-K) Post CRUD Burst

M-20190430-33

!RF20 Post Decon of Cavity Floor After Reactor Head Set for

MSIP 1-157

Radiation Work

Permits (RWPs)

RWP 2019-1215

Scaffolding in the RCA

RWP 2019-1600

WEC Refueling

RWP 2019-1604

MSIP Westinghouse

RWP-2019-1607

MSIP Support, Cavity Decon

Self-Assessments EVAL 2018-0006

CPNPP Nuclear Oversight: Work Management/RP

Audit

7/26/18

31

Inspection

Procedure

Type

Designation

Description or Title

Revision or

Date

71124.03

Corrective Action

Documents

IR/TR/CR

2017-009867, 010605, 010692, 010827, 011717, 011762,

012840, 013033, 2018-000842, 001245, 001285, 001859,

003371, 004052, 005228, 006575, 007249, 008342, 008400

2019-000200, 001117, 001421, 001511, 001547, 001622,

001669, 002036, 002128, 002192, 002448

Corrective Action

Documents

Resulting from

Inspection

IR-2019

003680, 003682

Procedures

RPI-115

Alarm Response

10

RPI-303

Radiological Air Sampling

0

RPI-902

Issue and Control of Respiratory Protection

17

RPI-923

Maintenance and Use of Portable HEPA Filter Ventilation

Units

5

SAF-104

Inspection of Respiratory Protection Equipment

(Maintenance & Repair

12

SOP-801A

Containment Ventilation

14

SOP-816

Primary Plant Ventilation Systems

18

STA-652

Radioactive Material Control

21

STA-653

Contamination Control Program

20

STA-802

Control Room Ventilation

13

STI-211.06

Use of Respiratory Protection

1

Self-Assessments EVAL 2018-006

CPNPP Nuclear Oversight: Work Management/RP Audit

7/28/19

71151

Procedures

NGM-710

Management Review Meetings

11/2/18

RPI-629

Radiological Risk Management

5

71152

Calculations

STI-422.01

Operability Determination and Functionality Assessment

Program

23

Corrective Action

Documents

CR-YYYY-NNNN

2018-008521, 2019-000324, 2019-001628, 2019-001830,

2019-001836, 2019-003498, 2019-003672, 2019-005285

TR-YYYY-NNNN

2018-005446

71153

CR-YYYY-NNNN

2019-001949

Miscellaneous

Shift Manager Daily Activities Log