IR 05000280/2019002
| ML19217A072 | |
| Person / Time | |
|---|---|
| Site: | Surry |
| Issue date: | 08/05/2019 |
| From: | Bradley Davis Division Reactor Projects II |
| To: | Stoddard D Virginia Electric & Power Co (VEPCO) |
| Reeder D | |
| References | |
| IR 2019001, IR 2019002 | |
| Download: ML19217A072 (20) | |
Text
August 5, 2019
SUBJECT:
SURRY POWER STATION - NRC INTEGRATED INSPECTION REPORT 05000280/2019002 AND 05000281/2019002; 07200055/2019001
Dear Mr. Stoddard:
On June 30, 2019, the U.S. Nuclear Regulatory Commission (NRC) completed an inspection at Surry Power Station. On July 3, 2019, the NRC inspectors discussed the results of this inspection with Mr. Fred Mladen and other members of your staff. The results of this inspection are documented in the enclosed report.
No NRC-identified or self-revealing findings were identified during this inspection.
The inspectors documented a licensee-identified violation which was determined to be of very low safety significance in this report. The NRC is treating this violation as non-cited violation (NCV) consistent with Section 2.3.2.a of the Enforcement Policy. This letter, its enclosure, and your response (if any) will be made available for public inspection and copying at http://www.nrc.gov/reading-rm/adams.html and at the NRC Public Document Room in accordance with 10 CFR 2.390, Public Inspections, Exemptions, Requests for Withholding.
Sincerely,
/RA/
Bradley J. Davis, Chief Reactor Projects Branch 4 Division of Reactor Projects
Docket Nos. 05000280 and 05000281
07200055
License Nos. DPR-32 and DPR-37
Enclosure:
As stated
Inspection Report
Docket Numbers:
05000280 and 05000281
07200055
License Numbers:
Report Numbers:
05000280/2019002 and 05000281/2019002
07200055/2019001
Enterprise Identifier: I-2019-002-0030
I-2019-001-0124
Licensee:
Virginia Electric and Power Company
Facility:
Surry Power Station
Location:
Surry, VA
Inspection Dates:
April 1, 2019 to June 30, 2019
Inspectors:
L. McKown, Senior Resident Inspector
C. Read, Resident Inspector
S. Monarque, Project Engineer
C. Stancil, Senior Fuel Facility Inspector
Approved By:
Bradley J. Davis, Chief
Reactor Projects Branch 4
Division of Reactor Projects
SUMMARY
The U.S. Nuclear Regulatory Commission (NRC) continued monitoring the licensees performance by conducting a integrated inspection at Surry Power Station in accordance with the Reactor Oversight Process. The Reactor Oversight Process is the NRCs program for overseeing the safe operation of commercial nuclear power reactors. Refer to https://www.nrc.gov/reactors/operating/oversight.html for more information. A licensee-identified non-cited violation is documented in report section 7115
List of Findings and Violations
No findings or violations of more than minor significance were identified.
Additional Tracking Items
Type Issue Number Title Report Section Status LER 05000281/2019-001-00 LER 2019-001-00, Foreign Material in Breaker Contact Causes Pressurizer Power Operated Relief Valve Block Valve Inoperability.
71153 Closed
PLANT STATUS
Unit 1 operated at or near rated thermal power for the entire inspection period.
Unit 2 began the inspection period at rated thermal power. On April 22, 2019, the unit was down powered to 83 percent to repair both high pressure heater drain pumps. The unit was returned to rated thermal power on April 25, 2019, and remained at or near rated thermal power for the remainder of the inspection period.
INSPECTION SCOPES
Inspections were conducted using the appropriate portions of the inspection procedures (IPs) in effect at the beginning of the inspection unless otherwise noted. Currently approved IPs with their attached revision histories are located on the public website at http://www.nrc.gov/reading-rm/doc-collections/insp-manual/inspection-procedure/index.html. Samples were declared complete when the IP requirements most appropriate to the inspection activity were met consistent with Inspection Manual Chapter (IMC) 2515, Light-Water Reactor Inspection Program - Operations Phase. The inspectors performed plant status activities described in IMC 2515 Appendix D, Plant Status and conducted routine reviews using IP 71152, Problem Identification and Resolution. The inspectors reviewed selected procedures and records, observed activities, and interviewed personnel to assess licensee performance and compliance with Commission rules and regulations, license conditions, site procedures, and standards.
REACTOR SAFETY
71111.01 - Adverse Weather Protection
Summer Readiness Sample (IP Section 03.01) (1 Sample)
- (1) The inspectors evaluated summer readiness prior to the onset of seasonal hot temperatures for plant ventilation systems, vital equipment checks, and temporary equipment installation on May 13, 2019.
71111.04 - Equipment Alignment
Partial Walkdown Sample (IP Section 03.01) (5 Samples)
The inspectors evaluated system configurations during partial walkdowns of the following systems/trains:
- (1) Unit 1 Turbine Driven Auxiliary Feedwater system on April 18, 2019.
- (2) Emergency Service Water Pumps 1-SW-P-1A and -1C protected equipment on April 29, 2019.
(3)
- 2 and #3 Emergency Diesel Generators (EDG) during testing of the #1 EDG on June 24, 2019.
- (4) Unit 2 Reactor Trip and Bypass Trip Breaker Partial Alignment on June 25, 2019.
- (5) Unit 1 Charging Operating pump trains during overhaul of the 'C' Charging Pump on June 28, 2019.
71111.04S - Equipment Alignment
Complete Walkdown Sample (IP Section 03.02) (1 Sample)
- (1) The inspectors evaluated system configurations during a complete walkdown of the fire protection system on May 31, 2019.
71111.05Q - Fire Protection
Quarterly Inspection (IP Section 03.01) (6 Samples)
The inspectors evaluated fire protection program implementation in the following selected areas:
- (1) Mechanical Equipment Rooms 3 and 4 Smoke Detector Test, 1-SW-263, Appendix R Isolation Valve on May 3, 2019.
- (2) Inadequate step in procedures 0-AP-13.00 and 0-FCA-7.00 which failed to isolate Mechanical Equipment Room (MER) 3 from MER 5 following a fire or flood in MER 3 on May 8, 2019.
- (3) AAC diesel generator building on March 16, 2019.
- (4) Auxiliary Building Elev. 45 ft on May 31, 2019.
- (5) Fuel Building on May 31, 2019.
- (6) Unit 2 Emergency Switchgear Room on June 12, 2019.
71111.11Q - Licensed Operator Requalification Program and Licensed Operator Performance
Licensed Operator Performance in the Actual Plant/Main Control Room (IP Section 03.01) (2 Samples)
- (1) The inspectors observed and evaluated licensed operator performance in the Control Room during a Unit 2 down power from 100 percent to 83 percent reactor power to support high pressure heater drain pump maintenance on April 22, 2019.
- (2) The inspectors observed and evaluated licensed operator performance in the Control Room when raising Unit 2 power from 83 percent to 100 percent reactor power following high pressure heater drain pump maintenance on April 25, 2019.
Licensed Operator Requalification Training/Examinations (IP Section 03.02) (1 Sample)
- (1) The inspectors observed and evaluated a scenario in which a toxic gas was released and multiple fission product barriers failed on June 18, 2019.
71111.12 - Maintenance Effectiveness
Quality Control (IP Section 02.02) (1 Sample)
The inspectors evaluated maintenance and quality control activities associated with the following equipment performance activities:
- (1) Emergency Service Water Pump 1-SW-P-1B Replacement and Testing, Work Order
===38077550701 and 0-MCM-0114-01, April 30 - May 3, 2019.
Routine Maintenance Effectiveness Inspection (IP Section 02.01)===
The inspectors evaluated the effectiveness of routine maintenance activities associated with the following equipment and/or safety significant functions:
- (1) Inspection and Overhaul of Unit 1, 1-SW-268 check valve on April 10, 2019.
- (2) Charging pump bearings and seals preventative maintenance effectiveness review on June 17, 2019.
- (3) Maintenance Rule structural inspections of the fire pump house and evaluations of cracks in block walls on June 18, 2019.
71111.13 - Maintenance Risk Assessments and Emergent Work Control
Risk Assessment and Management Sample (IP Section 03.01) (7 Samples)
The inspectors evaluated the risk assessments for the following planned and emergent work activities:
- (1) Unit 1 and Unit 2 intake canal level probe testing on April 10, 2019.
- (2) Unit 1 and Unit 2 emergent offsite power switching activities planned during emergency service water pump maintenance on April 18, 2019.
- (3) Unit 2 downpower to 83%, high pressure heater drain pump replacement, and removal of floor grating for access to EOP components on April 22, 2019.
- (4) Unit 1 and 2 emergency service water pump replacement week of April 29, 2019.
- (5) Unit 2 reactor coolant pump underfrequency testing on May 31, 2019.
- (6) Unit 1 emergent online troubleshooting of high pressure feedwater heater '1B' moisture separator drain tank normal level control valve erratic operation on June 12, 2019.
- (7) Unit 1 and Unit 2 transportation of a dry storage cask to ISFSI pad and insertion into a horizontal storage module on June 13, 2019.
71111.15 - Operability Determinations and Functionality Assessments
Operability Determination or Functionality Assessment (IP Section 02.02) (6 Samples)
The inspectors evaluated the following operability determinations and functionality assessments:
- (1) CR1122159, Degraded Rebar and Concrete Associated with 1-SW-P-1B Pump Floor Slab, on April 30, 2019.
- (2) CR1122689, High Vibrations on 1-SW-P-1B, 'B' Emergency Service Water Pump, on May 7, 2019.
- (3) CR1073491, operability impact of silt deposits in intake canal on ultimate heat sink
- (4) CR1124848, Main Control Room Chiller '4A' Failure to Start, first attempted start since 2017 on June 11, 2019.
- (5) CR1125718, Delayed Undervoltage Light during Unit 2 Train 'A' Reactor Protection Logic Testing on June 25, 2019.
- (6) CR112529, Failure to complete diagnosis of fire due to performance of parallel Time Critical Operator Actions in AP-48.00, Fire Protection - Operations Response, on June 26, 2019.
71111.18 - Plant Modifications
Temporary Modifications and/or Permanent Modifications (IP Section 03.01 and/or 03.02) (1 Sample)
The inspectors evaluated the following temporary or permanent modifications:
- (1) Temporary Modifications for 1-SW-P-1B Pump Heavy Lifts: Fuel Oil Line Jumper and Flood Protection Restoration.
71111.19 - Post-Maintenance Testing
Post Maintenance Test Sample (IP Section 03.01) (7 Samples)
The inspectors evaluated the following post maintenance tests:
(1)1-PT-41.1, Component Cooling Water (CC) Pumps Performance Test after replacement of the 1A CC pump seals and motor refurbishment on April 2, 2019.
(2)2-OSP-TM-001, Turbine Inlet Valve Freedom Test, after cam adjustment of the Unit 2
- 4 Turbine Stop Valve, on April 24, 2019.
- (3) Post Maintenance Testing of Unit 1, 1-SW-268 check Valve on April 10, 2019.
(4)0-OPT-SW-008, Emergency Service Water Pump 1-SW-P-1B Comprehensive Test after replacement of the 1-SW-P-1B pump on May 3 and 6, 2019.
(5)0-OP-AAC-001, AAC Diesel Generator Operation, on June 13, 2019 following 3-year and 6-year preventative maintenance packages.
(6)2-PT-8.1, Reactor Protection Logic Test following swapping leads on the Channel 1 Overtemperature Delta Temperature Relay 2-RP-RLY-TC412CXA, on June 26, 2019.
(7)0-OPT-SW-002, Emergency Service Water Pump 1-SW-P-1B Periodic Test following packing gland failure on June 23, 2019.
71111.22 - Surveillance Testing
The inspectors evaluated the following surveillance tests:
FLEX Testing (IP Section 03.02)
- (1) Annual testing of the following FLEX equipment from June 10 through June 24, 2019:
- 1-FP-P-4, Portable Backup Diesel Fire Pump
- 0-BDB-P-1, Beyond Design Basis (BDB) High Capacity Pump
- 0-BDB-GEN-1B, BDB 40kW 120/240VAC Diesel Generator
- 0-BDB-GEN-1C, BDB 40kW 120/240VAC Diesel Generator
Inservice Testing (IP Section 03.01) (1 Sample)
- (1) 1-OPT-CS-002, Containment Spray System Test, on April 15, 2019.
Surveillance Tests (other) (IP Section 03.01) (4 Samples)
(1)2-OPT-SI-005, Low Head Safety Injection (LHSI) Pump Test, on April 12, 2019.
(2)2-OPT-EG-001Q, Number 2 Emergency Diesel Generator Quarterly/Monthly Load Test, on April 8, 2019.
(3)0-NSP-CW-006, Canal Level Probe Removal, Inspection and Cleaning, on April 10, 2019.
(4)1-OPT-CH-002, Charging Pump Operability and Performance Test for 1-CH-P-1B, on May 16, 2019.
71114.06 - Drill Evaluation
Drill/Training Evolution Observation (IP Section 03.02) (1 Sample)
The inspectors evaluated:
- (1) The inspectors evaluated a licensee emergency planning drill from the control room simulator on June 18, 2019. The drill involved a toxic gas release and the failure of multiple fission product barriers resulting in a General Emergency declaration.
Select Emergency Preparedness Drills and/or Training for Observation (IP Section 03.01) (1 Sample)
- (1) The inspectors evaluated a licensee emergency planning drill at the Corporate Emergency Response Center in Glen Allen, VA, on April 11, 2019. The drill involved an earthquake within 200km of Surry which resulted in an Alert declaration due to a hazardous atmosphere at the low level intake structure. The drill also involved aftershocks which resulted in a loss of fuel clad barrier and eventually a large break loss of coolant accident, which ultimately resulted in a General Emergency declaration.
OTHER ACTIVITIES - BASELINE
===71151 - Performance Indicator Verification
The inspectors verified licensee performance indicators submittals listed below:
BI01: Reactor Coolant System (RCS) Specific Activity Sample (IP Section 02.10)===
- (1) Unit 1 (April 1, 2018 through March 31, 2019)
- (2) Unit 2 (April 1, 2018 through March 31, 2019)
BI02: RCS Leak Rate Sample (IP Section 02.11) (2 Samples)
- (1) Unit 1 (April 1, 2018 through March 31, 2019)
- (2) Unit 2 (April 1, 2018 through March 31, 2019)
MS05: Safety System Functional Failures (SSFFs) Sample (IP Section 02.04) (2 Samples)
- (1) Unit 1 (April 1, 2018 through March 31, 2019)
- (2) Unit 2 (April 1, 2018 through March 31, 2019)
71152 - Problem Identification and Resolution
Annual Follow-up of Selected Issues (IP Section 02.03) (2 Samples)
The inspectors reviewed the licensees implementation of its corrective action program related to the following issues:
- (1) Challenges to operator performance including operator work arounds, burdens and challenges; main control room deficiencies and distractions; and night/standing orders on April 4, 2019.
- (2) Loss of Configuration Control of Surry Unit 1 Outside Recirculation Spray Pump 01-RS-P-2B Recirculation Isolation Valve 1-RS-6 due to degraded Stem to Disc Interface (CR1114023) on June 24, 2019.
Semiannual Trend Review (IP Section 02.02) (1 Sample)
- (1) The inspectors reviewed the licensees corrective action program for potential adverse trends in scheduling and completion of items added and removed from the equipment reliability top 10 focus items list that might be indicative of a more significant safety issue on June 26, 2019.
71153 - Followup of Events and Notices of Enforcement Discretion Event Report (IP Section 03.02)
The inspectors evaluated the following licensee event report (LER):
- (1) LER 05000281/2019-001-00, Foreign Material in Breaker Contact Causes Pressurizer Power Operated Relief Valve Block Valve Inoperability (ADAMS accession ML19098A163). The circumstances surrounding this LER are documented in the Results section. (Closed)
OTHER ACTIVITIES
- TEMPORARY INSTRUCTIONS, INFREQUENT AND ABNORMAL
60855.1 - Operation of an Independent Spent Fuel Storage Installation at Operating Plants Operation of an Independent Spent Fuel Storage Installation at Operating Plants
- (1) The inspectors evaluated the licensees independent spent fuel storage installation (ISFSI) cask loadings on June 3, 2019. Specifically, the inspectors observed the following activities:
- Fuel selection and fuel loading
- Heavy load movement of dry shielded canister/transfer cask
- Radiological field surveys
The inspectors evaluated the licensee's ISFSI cask movement and installation into the horizontal storage module on June 13, 2019. Specifically, the inspectors observed the following activities:
- Heavy load movement of transfer cask
- Radiological field surveys
- Transportation of the transfer cask to the ISFSI pad The inspectors evaluated the licensee's ISFSI cask movement and installation into the horizontal storage module on June 20, 2019. Specifically, the inspectors observed the following activities:
- Radiological field surveys
- Transportation of the transfer cask to the ISFSI pad
- Installation of the transfer cask into the horizontal storage module
The inspectors evaluate the following program changes:
- Revision of procedure 0-OP-FH-072, NUHOMS 32 PTH Dry Shielded Canister Loading and Unloading, Revisions 28 and
INSPECTION RESULTS
Licensee-Identified Non-Cited Violation 71153 This violation of very low safety significance was identified by the licensee and has been entered into the licensee corrective action program and is being treated as a non-cited violation, consistent with Section 2.3.2 of the Enforcement Policy.
Violation: Surry Technical Specification 6.4.A.7 states, in part, that detailed written procedures with appropriate check-off lists and instructions shall be provided for conditions that include: preventive or corrective maintenance operations which would have an effect on the safety of the reactor. Surry Technical Specification 6.4.D states, in part, that procedures described in section 6.4.A shall be followed. These requirements were implemented, in part, by WO38102324301 and procedure MA-AA-102, Foreign Material Exclusion. Contrary to the above, on November 7, 2018, the licensee failed to follow the written procedures and instructions for breaker preventive maintenance of a unit 2 pressurizer power operated relief valve (PORV) block valve 2-RC-MOV-2536 including foreign material closeout, which resulted in a nylon brush bristle lodged in the valve breaker stationary closed contactor assembly and inoperability of the associated PORV block valve from December 4, 2018, to January 29, 2019. The pressurizer PORV block valves are active reactor coolant system boundary valves which provide the operators with the ability to detect a stuck-open safety or relief valve and to isolate a stuck-open PORV. The licensee reported the operation prohibited by Technical Specifications to the NRC on April 1, 2019, as Licensee Event Report 50-281/2019-001-00, Foreign Material in Breaker Contact Causes Pressurizer Power Operated Relief Valve Block Valve Inoperability.
Significance: Green. The failure to prevent foreign material from affecting operation of PORV block valve 2-RC-MOV-2536 was a performance deficiency (PD). The inspectors assessed the significance of the finding using IMC 0609 Attachment 4, Initial Characterization of Findings, Table 2, dated October 7, 2016, and the finding was determined to adversely affect the Barrier Integrity cornerstone under the active components of boundary (valve, seals) area to measure. Specifically, the pressurizer PORV block valve was not available to provide the operators with the ability to detect a stuck-open safety or relief valve and to isolate a stuck-open PORV. An independent bounding risk analysis was performed by a regional senior reactor analyst in accordance with NRC Inspection Manual Chapter 0609 Appendix A. The analysis assumed a non-recoverable failure to operate of the 2-RC-MOV-2536 block valve with no common cause impact for a period of 57 days. The analysis determined that the increase in core damage frequency due to the PD was less than 1E-7/year, a Green finding of very low safety significance.
Corrective Action References: CR1113030
EXIT MEETINGS AND DEBRIEFS
The inspectors verified no proprietary information was retained or documented in this report.
- On July 3, 2019, the inspectors presented the integrated inspection results to Mr. Fred Mladen and other members of the licensee staff.
DOCUMENTS REVIEWED
Inspection
Procedure
Type
Designation
Description or Title
Revision or
Date
60855.1
Miscellaneous
Loading for Surry
Spent Fuel Pool
05/28/2019
S1-OP-19-03
Fuel Handling Report
Procedures
0-OP-FH-072
NUHOMS 32 PTH Dry Shielded Canister Loading and
Handling
HP-1061.500
NUHOMS Spent Fuel Cask Preparation/Loading and
Transport to ISFSI
Calculations
ME-12152
Loss of Ventilation in the Cable Vault and Tunnel
Corrective Action
Documents
CR1118627
Calculation provides elevated temperature at DBA with loss
of ventilation.
03/19/2019
Corrective Action
Documents
Resulting from
Inspection
CR1124184
Unit 1 upper cable vault ventilation O.O.S. and high
temperature
05/30/2019
Procedures
0-OSP-ZZ-003
Hot Weather Preparation
Drawings
113E244A
Reactor Protection System Reactor Trip Matrices - Surry
Power Station - Unit 2
Miscellaneous
1-19-SW-00010
Safety Tagout of 1-SW-P-1B
April 30,
2019
Procedures
0-OP-SW-002A
Emergency Service Water System Alignment
1-OP-CH-002
Charging Pump A Operations
1-OP-CH-003
Charging Pump B Operations
1-OPT-FW-003
Turbine Driven Auxiliary Feedwater Pump 1-FW-P-2
2-PT-8.1
Reactor Protection System Logic (for Normal Operations)
Corrective Action
Documents
CR1086466,
CR1091946,
CR1092279,
CR1116987,
CR1121992,
CR1123110,
CR1123469
Drawings
11448-FB-2A
Fire Protection - Arrangement, Surry Power Station
Inspection
Procedure
Type
Designation
Description or Title
Revision or
Date
11448-FB-3A
Yard, Water & Fire Protection Lines, Surry Power Station -
Unit 1
11448-FB-47A
Flow/Valve Operating Numbers Diagram, Fire Protection &
Domestic Water System, Surry Power Station - Unit 1
Miscellaneous
Module
NCRODP-6-S-6-
S
Nuclear Control Room Operator Development Program
Surry Power Station: Fire Protection System
10/06/2017
SDBD-SPS-FP
System Design Basis Document for Fire Protection System
Procedures
0-AP-48.00
Fire Protection-Operations Response (with 5 attachments)
0-LPT-FP-006
Inspection of Hose Stations and Fire Extinguishers -
RCA/North Yard
0-OP-FP-006
Operation of Fire Protection Systems
1-OP-52.2A
Fire Protection System Alignment
CM-AA-FPA-100
Fire Protection/Appendix R (Fire Safe Shutdown) Program
Drawings
11548-FE-51R
Wiring Diagram Internal and External Fire Protection Panel,
Surry Power Station, Unit 2
Procedures
0-FCA-7.00
Limiting Mechanical Equipment Room 3 or Fire
71111.05Q Drawings
11448-FM-071D
Flow/Valve Operating Numbers Diagram Circulating and
Service Water System Surry Power Station Unit 1
11548-FM-071A
Flow/Valve Operating Numbers Diagram Circulating and
Service Water System Surry Power Station Unit 2
103
Engineering
Changes
Standing Order
SO-19-002
Alternative Method to provide Flood Isolation of MER 3
May 2, 2019
Fire Plans
0-FS-FP-225
Alternate AC Diesel Room - Construction Site Elev. 35 Feet
Procedures
0-AP-13.00
Turbine Building or MER 3 Flooding
0-EPM-0901-05
Mechanical Equipment Rooms 3 and 4 Smoke Detector Test
0-FS-FP-162
Auxiliary Building Elevation 45 Feet - 10 Inches
0-FS-FP-163
Fuel Building Elevation 6 Feet - 10 Inches and 15 Feet - 10
Inches
0-FS-FP-164
Fuel Building Elevation 27 Feet - 6 Inches and 45 Feet - 10
Inches
0-FS-FP-225
Alternate AC Diesel Room
Work Orders
204187733
Mechanical Equipment Room 3 and Mechanical Equipment
Room 4 Smoke Detector Test
Inspection
Procedure
Type
Designation
Description or Title
Revision or
Date
204187733
Mechanical Equipment Rooms 3 and 4 Smoke Detector Test
71111.11Q Corrective Action
Documents
CR1125393
Last minute EP Inject Message Request
Miscellaneous
EAL Matrix
Surry Power Station Emergency Action Level Matrix
Procedures
2-OP-CH-007
Blender Operations
2-OP-TM-005
Unit Ramping Operations
Corrective Action
Documents
CR1122082,
CR1122157,
CR1122159,
CR1122199,
CR1122272,
CR1122337
Engineering
Evaluations
S-PMTE-2002-
011
Replace the mechanical seals on 1/2-CH-P-1A/B/C
9/11/2002
S-PMTE-2005-
0355
PM to replace mechanical seals
10/19/2005
Procedures
0-MCM-0109-01
Charging Pump Overhaul
0-MCM-0114-01
Emergency Service Water Pump Maintenance
0-MCM-0417-52
William Powell Swing Check Valve Inspection and Overhaul
Model 2342
VPAP-1001
Quality Control (QC) Inspection Program
Work Orders
38077550701
Emergency Service Water Pump 1-SW-P-1B Replacement
and Testing
April 30,
2019
38103275045
0-NSP-BS-005 1825 Day Freq. PT: Monitoring of Structures
11/26/2018
Corrective Action
Documents
CR1124809
High pressure feedwater heater '1B' moisture separator
drain tank normal level control valve erratic operation
06/12/2019
Miscellaneous
Radiological Risk Screening Worksheet for NUHOMS cask
campaign
dated
2/25/2019
Schedulers Risk
Evaluation for
Surry Power
Station
April 10,
2019
Inspection
Procedure
Type
Designation
Description or Title
Revision or
Date
Schedulers Risk
Evaluation for
Surry Power
Station
April 18,
2019
Procedures
0-DRP-049
Time Critical Operator Actions
Work Orders
204199267
Corrective Action
Documents
CR1122509,
CR1122600,
CR1122662,
CR1122689
1-SW-P-1B High Vibrations
CR1124848
Main Control Room Chiller '4A' Failure to Start, first
attempted start since 2017
06/11/2019
CR112529
Failure to complete diagnosis of fire due to performance of
parallel Time Critical Operator Actions
06/26/2019
CR1125718
Delayed Undervoltage Light during Unit 2 Train A Reactor
Protection Logic Testing
06/25/2019
Operability
Evaluations
Engineering Logs
1-SW-P-1B ESW Pump high vibrations.
May 7, 2019
Station Narrative
Log Follow-ups
for CR1122159
Degradation of 1-SW-P-1B Foundation Rebar and Concrete
Degradation
May 1 and 2,
2019
Procedures
Calculations
CE-2056
Surry Emergency Service Water Pump Heavy Load Rigging
& Load Drop Evaluation for 01-SW-P-1A, 01-SW-P-1B, &
01-SW-P-1C
Engineering
Changes
S1-17-155
Emergency Service Water Pump Fuel Oil Line Jumper
SU-19-00112
Emergency Service Water Pump House Flood Protection
Restoration Following Postulated Load Drop of 1-SW-P-1B
Engineering
Evaluations
ETE-SU-2019-
0008
Emergency Service Water Pump NUREG-0612 Heavy Load
Requirements
ETE-SU-2019-
1007
Repair Disposition for 1-SW-P-1B Pump Pit Plate
Corrective Action
Documents
CR1121088
Interlock switch for 2-MS-TV-4 found out of adjustment.
April 17,
2019
Inspection
Procedure
Type
Designation
Description or Title
Revision or
Date
CR1122502,
CR1122504,
CR1122558,
CR1122559,
CR1122572,
CR1122744
Pushbutton start needs reset, throttle linkage repair, 1-SW-
P-1B packing leakage, fuel filter leak, loose base plate bolts
Drawings
11448-FM-072D
Flow/Valve Operating Numbers Diagram Component
Cooling Water System, Sheets 1 and 2
and 37
respectively
Procedures
0-MCM-0107-01
Component Cooling Pump Maintenance
0-MCM-0417-52
William Powell Swing Check Valve Inspection and Overhaul
Model 2342
0-OP-AAC-001
AAC Diesel Generator Operation
0-OPT-SW-002
Emergency Service Water Pump 1-SW-P-1B
0-OPT-SW-008
Emergency Service Water Pump 1-SW-P-1B
Comprehensive Test
1-PT-18.8
Charging Pump Service Water Performance
1-PT-41.1
Component Cooling Water Pumps Performance Test
2-OSP-TM-001
Turbine Inlet Valve Freedom Test
2-PT-8.1
Reactor Protection System Logic (for Normal Operations)
Work Orders
38103680975
38103680975
Unit 2 Turbine Stop Valve Interlock Verification
38103711862
and
38103401882
204192362
204199804
06/26/2019
Corrective Action
Documents
CR1120556,
CR1120552
Corrective Action
Documents
Resulting from
Inspection
CR1120807
Non-ISI elevated vibes Point 9
CR1120821
1-CS-115 externally leaking by
CR1120834
1-CS-PP-1B Pump seal drain boric acid accumulation.
Engineering
Changes
SU-13-01025
Implementation of the Beyond Design Basis Diverse and
Flexible Coping Strategies (FLEX) Program
06/16/2014
Inspection
Procedure
Type
Designation
Description or Title
Revision or
Date
Engineering
Evaluations
ETE-CPR-2014-
1002
Site Acceptance Testing (SAT) and Periodic Performance
Verification Testing Acceptance Criteria for BDB FLEX
Strategy Pumps - North Anna 1&2 and Surry 1&2
Procedures
0-MPM-1960-01
Semi-Annual or Annual Test of BDB Flex Equipment
0-NSP-CW-006
Canal Level Probe Removal, Inspection and Cleaning
0-OP-BDB-003
BDB 120/240 VAC Generator Operator Aid
0-OP-BDB-007
BDB High Capacity Pump Operating Aid
1-FSG-1
Long Term RCS Inventory Control
1-FSG-8
Alternate RCS Boration
1-OPT-CH-002
Charging Pump Operability and Performance Test for 1-CH-
P-1B
1-OPT-CS-002
Containment Spray System Test
2-OPT-EG-001
Number 2 Emergency Diesel Generator Monthly Start
Exercise Test
2-OPT-SI-005
LHSI Pump Test
Corrective Action
Documents
CR1125343
SJUN19FS Obj 4 (Notifications) Met with Problem
CR1125452
SJUN19FS Obj 20 (Exercise Conduct) Met with Problem
Procedures
EPIP-1.01
Emergency Manager Controlling Procedure
EPIP-3.06
Corporate Emergency Response Center Activation
EPIP-3.10
CERC Technical Support Controlling Procedure
EPIP-4.36
CERC Accident Assessment Controlling Procedure
71151
Miscellaneous
1Q/2019 Performance Indicators - Surry 1 and 2 - Reactor
Coolant System Leakage
06/25/2019
1Q/2019 Performance Indicators - Surry 1 and 2 - Safety
System Functional Failures
06/25/2019
Unit 2 Control Room Narrative Log, 04/01/2018 - 3/31/2019
1Q/2019 Performance Indicators - Surry 1 and 2 - Reactor
Coolant System Activity
06/25/2019
Unit 1 Control Room Narrative Log, 04/01/2018 - 3/31/2019
Regulatory Assessment Performance Indicator Guideline
Corrective Action
Documents
CA7489560
CR015505,
CR020890,
Inspection
Procedure
Type
Designation
Description or Title
Revision or
Date
CR021127,
CR572210,
CR1044721,
CR1116262, and
CA018234
CR1114023
Corrective Action
Documents
Resulting from
Inspection
CR1121189
Evaluate OPS aggregate impact based on NRC
observations and recommendations.
April 18,
2019
CR1121192
Self assessments for OP-AA-1700 (OAI) not performed from
2011 to 2017.
April 18,
2019
Miscellaneous
Equipment Reliability Top 10 Focus Items
04/23/2019
Equipment Reliability Top 10 Focus Items
01/22/2019
OAI
Units 1 and 2 Operations Aggregate Impact
March 1 and
April 1, 2019
RO Logs
Units 1 and 2 RO Abnormal Status Reports
April 4, 2019
SPS Units 1 and
Technical
Specifications
Amendment
250 and 251
SPS Units 1 and
4.2.7 Leakage
Procedures
0-OP-BR-001
Boron Recovery Tank Transfer to the Surry Radwaste
Facility
1-OP-ZZ-002
Maintenance of Plant Operations
Operations Aggregate Impact
Self-Assessments PIR1074492
Informal Self-Assessment on Surry Power Station's
Operations Aggregate Impact
February
2017
Work Orders
38052036702
Valve 01-CC-573 Replacement
38078187402
Valve 2-CC-322 Replacement
38103686836
Valve 01-BR-145 Bonnet Overhaul
204193252
Actuator / Valve Overhaul