ML19095A749

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Submit Abnormal Occurrence Report No. AO-S1-75-13 Re Failure of Valve MOV-CS-102B to Function Properly During Periodic Test
ML19095A749
Person / Time
Site: Surry  Dominion icon.png
Issue date: 05/30/1975
From: Stallings C
Virginia Electric & Power Co (VEPCO)
To: Moseley N
NRC/RGN-II
References
Serial No. 538 LER 1975-013-00
Download: ML19095A749 (3)


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Dear Mr. Moseley:

Pursuant to Surry Power Station Technical Specification 6.6.B.1, the Virginia Electric and Power Company hereby submits forty (40) copies of Abnormal Occurrence Report No. AO-:-Sl-75-13.

The substance of this.report has.been reviewed by the Station Nuclear Safety and Operating Committee and wiil be placed on the agenda for the next meeting of the System Nuclear Safety and Operating Committee.

Very truly yours,

v. )/21;-yJkU,;.~

.C. M. Stallings Vice President-Power Supply and Production Operations Enclosures 40 copies of AO~Sl-75-13.

cc: Mr. K. R. Goller l

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LICENSEE EVENT REPORT- AO-Sl-75-13 CONTROL BLocK: I *_ I I I I I [PLEASE PRINT ALL REQUIRED INFORMATION]

1 6 LICENSEE LICENSE EVENT

, NAME LICENSE NUMBER TYPE TYPE

@El 7 8 9 Iv I A I s I Pl sI 114I 15 1°1 °1-1°1 °1°1 °1°1-1° 1°1 25 I26411 I 1 I 1! oI 30 I 01 1 I 31 32 REPORT REPORT CATEGORY TYPE. SOURCE DOCKET NUMBER EVENT DATE REPORT DATE

@EJ CON'T IP j Oj l!J L!:.J Io Is I o I~ I o j 2 I 8j o I jojsj116j7jsj 10 I s I 2 I 2 I1 Is 7 8 57 58 59 60 61 68 69 74 75 80 EVENT DESCRIPTION

@IgJ Valve MOV-CS-102B, Chemical Addition Tank Discharge to RWST, failed to function 7 99!;"-~'--~~~~-----~~~~~~~~~-,-~~.:;._~:__~_:_~~~~~~~~~~....J I

80 I0131 ._I-'p'-r_o-'p'"""e_r_l....:y_d_u_r_i_n...:g::.__a__.:p:....e_r_i_*o_d_i_*c_t_e_s_t_._v_a_l_v_e_M_o_v_-_c_s_-_1_0_2_A_w_a_s_a_v_a_1_*_la_b_l_e_an_d_o,,_p::_e_r:a....,.b..:..*_1_e_a_s_ _.JI 7 8 9 80 jol41 I the redundant valve. The above is contrary to definition of Tech Spec .* 1.0,.I.6. J 7 89!;-~~--------------------------.:_-----~

80 lol51 I....--'(,__Ao-_s_1_-1_s_-_1_;3)~---------------------------__J

__ 1 7rnr.;i8 9 80 iQ..i§ .___ _ _ _ _ _ _ _ _ _ _ _ _ _ _ _ _ _ _ _ _ _ _ _ _ _ _ _ _ _ _ ___J 7 8 9 PRIME 80 SYSTEM CAUSE COMPONENT COMPONENT CODE CODE COMPONENT CODE SUPPLIER MANUFACTURER VIOLATION

@0 ls !c I . lu jvl Alt jvjEjXJ ~ IA 44 I 2 lo lo 47I LBJ 7 8 9 10 11 12 17 43 48 CAUSE DESCRIPTION

~ l Aloyco 6 inch 150 lb stainless steel gate valve with Limitorque operator. Valve I

7 8 9 80

~ l would not open electrically. The valve was opened manually and thereafter cycled I

7 8 9 EE] j electrically. The Limitorque operator was thoroughly checked and found to be (cont'~

7 8 9 80 FACILITY METHOD OF

% POWER OTHER STATUS DISCOVERY DISCOVERY DESCRIPTION EE]

STATUS

~ I1 I O I O12I N/A ~ I N/A.

7 8 9 FORM OF 10 13 44 45 46 80 ACTIVITY CONTENT rn w RELEASED OF RELEASE AMOUNT OF ACTIVITY LOCATION OF RELEASE w I N/A. I N/A 7 8 9 10 11 44 45 80 PERSONNEL EXPOSURES NUMBER TYPE DESCRIPTION

~ 10 I 0101 ~ N/A 7 8 9 11 12 13 80 PERS"ONNEL INJURIES NUMBER DESCRIPTION EEi IO I OI 0111 7 8 9 N/A 1~2--------------------------------------8..JO OFFSITE CONSEQUENCES E::eJ N/ A 7 8 9 80 LOSS OR DAMAGE TO FACILITY TYPE DESCRIPTION

~- ~ .___~~~N_/_A~~~~~~~~~~~~~~~~~~~~~~~~_J 7 8 9 10 80 PUBLICITY E08 9 ~ - -N/A 7 --------------------------------------------1 80 ADDITIONAL FACTORS

~ I This problem will be pursued further with the valve manufacturer.

7 8 9 80 NAME: E. M. Sweeney, Jr. PHONE: (804) 357-3184 GPO 881

  • 667

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e e CAQSE DESCRIPTION (cont'd) operating properly. The operating electrical current values were well within normal parameters. The valve was disassembled but no apparent damage, corrosion, indication of binding or other abnormal condition was observed. The valve was reassembled and tested satisfactorily. There apparently was some small debris in the valve seat area that created the initial problem. Currently no mechanical or electrical problem exists and no further action is contemplated.