ML18153C923

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Insp Repts 50-280/91-37 & 50-281/91-37 on 911201-920104. Violations Noted.Major Areas Inspected:Plant Operations, Maint,Surveillance,Design Change Review & Actions on Previous Insp Findings
ML18153C923
Person / Time
Site: Surry  Dominion icon.png
Issue date: 01/29/1992
From: Branch M, Frederickson P, Tingen S, York J
NRC OFFICE OF INSPECTION & ENFORCEMENT (IE REGION II)
To:
Shared Package
ML18153C921 List:
References
50-280-91-37, 50-281-91-37, NUDOCS 9203090261
Download: ML18153C923 (14)


See also: IR 05000280/1991037

Text

Report Nos.:

UNITED STATES

NUCLEAR REGULATORY COMMISSION

REGION II

101 MARIETTA STREET, N.W.

-ATLANTA, GEORGIA 30323

50-280/91-37 and 50-281/91-37

Licensee:

Virginia Electric and Pow~r Compiny

5000 Dominion Boulevard

Glen Allen, VA

23060

Docket Nos.:

50-280 and 50-281

Facility Name:

Surry 1 and 2

License Nos.:

DPR-32 and DPR-37

through January 4, 1992

S. G. Tingen, Resident Insector

"

Approved by: ' f~ \\I l-v..v t "-1.,__

Scope:

P. E. Fredrickson, Section hief

Division of Reactor Projects

SUMMARY

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Date Signed

l -L.~ -'1 '2.

Date Signed

/-'2...<:?-'Ja..

Date Signed

} ~ J-p\\ - "I L--'

Date Signed

This routine resident inspection was conducted on site in the areas of plant

operations, plant maintenance, plant surveillance, design change review, and

action on previous inspection findings.

During the performance of this

inspection, the resident inspectors conducted review of the licensee's*

backshift or weekend operations on December 20, 24, 28, and 29, 1991, and

January 2, 1992.

Results:

In the engineering and technical support area, the licensee's failure to

request NRC relief to continue plant operations without repairing a leaking-

weld joint on the ASME Class 2 letdown line is identified as a violation

(paragraph 4.c).

In the operations functional area, Technical Specifications did not clearly

indicate operability requirements for the charging pump intermediate seal

9203090261 920203

PDR

ADOCK 05000280

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PDR

2.

-coolers; however the inspectors concluded that the seal coolers were being

properly operated (paragraph 3.b).

In the operational functional area, the operators response to the January 2

runback and manua 1 reactor trip due to two dropped rods is cons i_dered a

strength.

However, the magnitude_ of the turbine run back cha 11 enged 'the

operators ability to maintain the unit at power during the transient (paragraph

3 .c).

-

The January 2 Unit 1 manual reactor trip, which occurred after 379 days of

continuous operation, * resulted from improper control of trouble shooting

activities and is considered a weakness (paragraph 3.c).

The cause or dropped rod [: .. 5 on Unit 1 was attributed to degradation of the CRD -

coil stack. This sam~ type of failure also resulted in a forced outage on Unit

2 in August, 1991 due to degradation of the CRD coil stack for rod D-4 and may

be indicative of.~quipment failures due to aging (paragraph 3.c).

In the surveillance area, the missed TS surveillance was determined to have

occurred prior to the implementation of corrective action violation 280/91-06-01

and therefore an additional violation is not appropriate (paragraph 6.a):

1.

Persons Contacted

Licensee Employees

REPORT DETAILS

R. Allen, Supervisor, Shift Operations

  • M. Bowling, Manager Nuclear Licensing and Programs
  • W. Benthall, Supervisor, licensing

R. Bilyeu, Licensing Engineer*

D. Christian, Assi~tant Station Manager

  • J. Downs, Superintendent of Outage and Planning

o.*Erickson, Superintendent of Health Physics

  • R. Gwaltney, Superintendent of Maintenance
  • L. Hartz, Quality Assurance, Corporate Manager
  • M. Kansler, Station Manager

T. Kendzia, Supervisor; Safety Engineering

  • J. McCarthy, Superintendent of Operations
  • A. McNeil) Design Engineer
  • J. O'Hanlon, VP Nuclear Operations
  • A. Price, Assi,tant Station Manager
  • R. Scanlan, Licensing
  • E. Smith, Site Quality Assurance Manager
  • T. Sowers~ Superintendent of Engineering

G. Thompson, Supervisor Maintenance Engineering

Other Personnel

NRC Personnel

  • M. Branch, Senior Resident Inspector
  • S. Tingen, Resident Inspector

J. York, Resident Inspector

  • Attended exit interview

Other licen*see employees contacted included control room operators, shift

technical advisors, shift supervisors and other plant personnel.

Acronyms and initialisms used throughout this report are listed in the

last paragraph.

2.

Plant Status

Unit 1 began the reporting period in power operation.

On January 2, day

379 of continuous operation, the unit experienced a turbine runback to

approximately 67 percent power when rod E-5 dropped into the core.

Later

2

in the same day, the unit was manually tripped from approximately 56%

power when rod H-2 {the second rod) dropped into the core.

This trip

is further discussed in paragraph 3.c.

At the end of the inspection

period, the unit was in coJd shut down in order to replace the coil stacks

on rod E-5.

Unit 2 began the reporting period in power operation.

On December 11, the

unit was shutdown in order to repair a reactor coolant leak on the RTD

bypass manifold flow element.

The RTD manifold flow element leak is

discussed further in paragraph 5.b.

On December 17, the unit was

restarted.

Later in the day, the unit experienced an automatic reactor trip from approximately 25% power which is discussed in paragraph 3.a.

The unit was restarted -on December 18, and was at 100% power on

December 19.

The unit was at power at the end of the inspection period,

day 17 of continuous operation.

3.

Operational Safety Verification (71707, 42700, 64704)

The- inspectors conducted frequent tours of the control room to verify

proper staffing, operator attentiven~ss and adherence to approved

procedures.

The inspectors attende*d pl ant status meetings and reviewed

operator logs on a daily basis to verify operations safety and compliance

with TS and to maintain awareness of the overa 11 operation of the

facility.

Iristrumentation and ECCS lineups were periodically reviewed

from control room indication to assess operability.

Frequent plant tours

were concjucted to observe equipment status, .fire protection programs,

radiological work practices, plant security programs and housekeeping.

Deviation reports were reviewed to assure that potential safety concerns

were properly addressed and reporteq.

a.

Licensee 10 CFR 50.72 Reports

On December 10, at 4:22 a~m., the licensee reported to the NRC that

ERFCS had became ;~operable at 3:00 a.m.

The purpose of the ERFCS is

to provide plant monitoring and data acquisition in order to aid .in

the evaluation of the reactor plant's safety status during emerg~ncy

conditions. Jhe ERFCS was reforned to service at 7:30 a.m.

On December 18, at 2:35 a.m., the licensee reported to -the NRC that

at 10:45 p.m. on December 17, Unit 2 experienced an automatic reactor trip from approximately 25% power.

During a reactor startup, SG

levels were being controlled manually.

After 6perato~s transferred

SG level control to automatic, the B MFRV began to oscillate

excessively.

The B SG level control was returned to manual; however,

level in the B SG reached the high level turbine trip*setpoint. This

resulted in a automatic turbine trip followed by an automatic reactor

    • -

3

trip.

The main feed pump tripped and both motor driven AFW pumps

auto started as required~

Also, all rods inserted and SG blowdowri

isolated *as required.

No primary or secondary relief valves lifted

after the reactor trip. Troubleshooting and repair of the B MFRV is

discussed in paragraph 4.d. *

On January 2, at 8:30 p.m., the 1 icensee reported to the NRC that

Unit 1 had experienced a manual reactor trip from 56% power at.4:49

p.m. - The reactor trip is discussed in paragr~ph 3.c.

b.

Operation of Charging Pump Intennediate Seal Coolers

During the previous inspection period, a leak developed in the Unit 2

charging pump intermediate seal. cool er, 2-SW-E-lA.

The .1 eak did not

render the seal cooler inoperable; however, it was an operational

inconvenience because SW was leaking into the CC system.

To prevent

the CC expansion tank from overflowing, operators were routinely

having to drain the CC expansion tank.

The seal cooler was then

isolated by shutting the manual SW and CC valves on the inlet and

outlet lines.

The redundant intennediate seal cooler 2-SW-E-lB was

aligned for operation.

The inspectors questioned the operability of

the isolated intermediate seal cooler and were infonned that the seal

tooler was considered operable becaus~ operators could valve the seal

cooler in if required. Also, the.inspectors were infonned that it is

a nonnal con.figuration to operate with one intermediate seal cooler *

operating and SW secured to the other redundant intennediate. seal

cooler and that operator manual action has always b~en fequired to place

the alternate redundant intermediate seal cooler in service.

The

inspectors were infonned that during design base LOCA containment

sump recirculation mode of operation, radiation levels in the area of

the intennediate seal coolers would prohibit operators from entering

.

the area.

TS 3.3.A.7.c requires that two charging pump intermediate seal

coolers be operable when a unit is critical.

TS 3.13.B.3 requires

that one charging pump intermediate seal cool~r be operating and the

spare charging *pump intermediate seal cooler be operable when reactor

coolant exceeds a temperature of 3_50F and a pressure of 450 psig.

TSs J.3.B.7 and 3.13.B.4.b state that one charging pump intermediate

seal cooler or other passive component may be but of service provided

the system may still operate at 100% capacity and repairs are

completed within 48 hours5.555556e-4 days <br />0.0133 hours <br />7.936508e-5 weeks <br />1.8264e-5 months <br />.

Section 9.4.3.4 of the FSAR st~tes that

two full-capacity charging pump intermediate seal coolers are

installed in eich unit to provide 100% redundancy for the charging

pump cooling water system.

This section of the FSAR does not

describe operation of the system with SW or CC iso*lated to the

intennediate seal coolers; however, the FSAR system diagram doesshow

the inlet valve to one of the s~al coolers as shut.

.

c.

4

The inspectors requested NRC staff assistance. in detennining

operability of a charging pump* intermediate seal cooler when SW

and/or CC was secured.

The staff concluded that TSs and FSAR did not

  • clearly specify how the system was required to operate and should be

changed to reflect what is actually required. Also, the staff review

of the system design requirements indicated that only one inter-

m~diate seal cooler per unit is required and that the iecond seal

cooler in each unit was the equivalent of a spare *.

During this inspection period, the licensee replaced the Unit 2

charging pump* intermediate seal cooler with the tube leak, and

changed the method of operation of the seal coolers by aligning SW to

both seal coolers in each unit.

At the end of the inspection

period, the seal coolers were operating with SW and CC flowing

through the coolers.

The licensee has initiated a study to evaluate

the need for the charg,ng pump intermediate seal coolers.

Past

operating experience indicates that operation without these coolers

does not adversely effect charging pump performance.

Unit 1 Reactor Runback and Manual Trip

At 7:54 a.m. on January 2, rod E-5 dropped into the core resulting in

a turbi_ne runback from 820 MWe to 335 MWe.

This was approximately~

60 percent turbine runback.

Reactor power decreased from iOO percent

to approximately 67 percent.

Operators considered that the magnitude

of this runback was excessive.

The licensee was investi~ating the

cause of the excessive turbine run back.

The inspectors cone l uded

that the magnitude of the turbine runback challenged the operators

ability to maintain the unit at power during the transient.

At 4: 49 p_.m. on January 2, Surry Unit 1 .was manually tripped from 56

. percent power when rod H-2 dropped during attempted rod motion.

Earlier on the same day rod E-5 had also dropped and was still on the.

bottom of the core when the sec_ond rod dropped.

With two dropped

rods, abnormal operating procedure O-AP-1.00 requires tht reactor to

be manually tripped.

During the transient the AMSAC system actuated

on low SG levels, and it tripped the rod drive MG set breakers.

.

Several equipment problems occurred, they included; 1) erratic IR NIS

indication on both channels,. 2) SG PORV~ did not respond to demand,

and 3) several indication and control related problems associated

with the turbine EHC and valve position system occurred. *

The licensee's trouble shooting determined that it would be necessary

to go to cold shutdown to replace the CRD coil *stack for dropped rod

E75.

This same type of failure also resulted in a forced outage on

Unit 2 in August, 1991, due to degradation of the CRD coil stack for

rod D-4.

During the Unit 1 1990 fa 11 refue 1 i ng outage, the CRD

stationary coil on rod K-10 was also identified as degraded and was

replaced.

The licensee has requested Westinghouse to perform failure

analyses for rods D-4 and E-5 degraded coil stacks in order to

determine if these equipment failures w'ere due to aging *. * The cause

5

of dropped rod H-2 was attributed to the removal of a CRD movable.

coil fuse during the troubleshooting* of rod E-5 and this fuse was

common to the movable coils associated with both of the rods

involved.

When rod motion was attempted on rod H-2 for delta-flux

control, the H-2 rod dropped when its stationary coil was deenergized

with the movable coil not bei.ng energized because of the *removed

fuse.

The pre-planned troubleshooting package did not recognize that

the fuse being pulled to isolate rod E-5 also effected rod H-2 as

well.

Because of this failure to recognize the tie betweE!n the two

rods, operational restrictions on rod motion were not implemented and

~~sulted. in dropping of the second rod and placing the plant in an

unanalyzed condition. The relationship of the fuse to other rods was

not intuitively obvious and this may have contributed to the *

confusion on the pait of the parties involved with planning of the

troubleshooting activities.

However, the resulting transient*

challenged the operating crew and resulted in the plant being in an

unanalyzed condition not protected by automatic equipment actuation.

The troubleshooting activities associated with this activity is

considered a weakness.

The licensee is currently in~estigating the eq~ipment problems noted

above and will correct them as well as accompl.ish other repairs prior

to returning the unit to power.

The inspectors are following the

licensee corrective actions and will review the post trip report

prior to the unit returning to power.

Operator performance during the Unit 1 reactor runback and trip and

the Unit 2 reactor shutdown, startup and trip was good.

Although

operators were frequently challenged, they continued to safely

operate the plant without making any significant errors.

When

operator errors do occur, the cause of the errors are aggressively

pursued and corrected.

For example, on November 20, 1991, a valve

sequencing error occurred when an opera tor returned a turbine

building instrument air tank to service following maintenance.

This

event was thoroughly investigated by the 1 icensee and was attributed

to an inadequate prejob brief. -As a result, the operations

department strengthened prejob briefs.

~ithin the areas inspected, no violations were identified.

4.

Maintenance Inspections (62703, 42700, 71500)

During the reporting period, the inspectors reviewed maintenance

activities to assure compliance with the .appropriate procedures~

The following maintenance activities were reviewed.

a.

Visual Inspection of CW Expansion Joints

During the NRC .exit meeting on November 21, 1991, the 1 icensee

corrrnitted in part to visually inspecting the condenser outlet

6

waterbox rubber EJs. * An engineering work request (EWR No.91-139)

was written to cover this work.

TMs *EwR stated that soft and spongy

areas, thin or exposed areas, cracking, leaking, and-bulging areas

needed to be reported and evaluated.

During a previous inspection period, the inspectors observed the

visual examination of the B waterbox outlet EJ for Unit 1. There was

some bulging; concavity, sponginess, and 1i near separations foun_d

during the internal visual examination.

Examination of the outer

surfaces of the EJ revealed spongy areas, several thinned areas, an

area where the outer ply was separated (almost one quadrant in .

lerigth) and exposing two metal reenforcing rings.

On~ ~f the rings

had rusted approximately halfway through the -diameter.

-

As a result of this inspection on Unit 1, the licensee decided to

inspect the same B waferbox on Unit 2.

Visual inspection of the

inside of this joint revealed only three* tears that exposed the

fabric.

The external inspection revealed a number of soft spots but

only one area approximately five inches long where the metal

reenforcing ring was exposed.

As a result of these inspections and

discussions with the vendor, the licensee concluded that significant

degradation to these EJs had occurred.

A justification for continued

operation (no. C-91-0006 dated November 29, 1991) was completed by

the licensee *and reviewed by the inspectors.

The licensee decided to inspect the remaining six EJs (three for each

unit) and has modified the bottom periphery of the existing EJ

shields.

This modification was designed to reduce the flow from

approximately 13,000 gpm to approximately 3,000 gpm or less from a

ruptured expansion joint. The inspectors followed the inspections of

the remaining expansion joints and noted that there were varying

degrees of degraded conditions similar to those found on the first

two EJ inspected.

The most degraded condition was found on the first

joint inspected, 1 B.

The 2 A EJ was in the best condition with just

a shallow linear area.

Documentation showed that this joint was

replaced in 1981.

The inspectors reviewed the licensee modificatioh to the EJ shields

and verified that the modification was completed on all eight joints

{4 per unit).

The inspectors did note that the rubber seal used in

the modification ~as torn in several areas on most of the installa-

tions.

The licensee indicated that the rubber seal was not rel,ied

upon in their calculation for the amount *Of water that would pass

through the opening.

The licerisee

1s flow calculation was based on an

opening of 1/8 inch around the circumference of the expansion joint~

The inspectors consider that the iicensee improvements in this area

should reduce the amount of flow below the original value considered

in the initial !PE assumptions and the flow from a failed EJ should

be limited to the capacity of the TB sump pumps.

7

b.

Repair of Leak on a Unit 2 RTD Manifold Flow Element

The licensee made a Unit 2 containment entry on December 3, 1991, in

order to 1 oca te the source of a gradua 11 y increasing 1 ea k.

Additional entries and insulation removal identified the leak to be

on flow element 2-RC-FE-2492.

A threaded plug used to close one of

the unused openings on the flange was leaking.

A Code case, N-3,

cla.rifying the Code of record for Surry B 31.1-1955, stated that

screwed connections in which threads provide the only seal shall not**

be penni tted in nuclear piping sys terns.

Therefore this threaded

connection did not meet the requirement of the original construction

Code.

The licensee di_d not immediately recognize t,he need to submit*

a ~equest for. relief from the ASME Code Requirements of Section XI,

1980 Edition, Winter 1980 Addendum.

However, after discussions with

the NRC staff, the licensee submitted a request for relief and cited

the requirements of 10 CFR 50.55a(g)(6)(i) which in part states, that

the Commission will evaluate determinations of impracticality, and

may

grant reli~f and may

impose alternate req~irements.

Additionally, the residents referenced the.licensee to the guidance

in Generic.Letters 90-05 and 91-18

which discusses situations of

this nature .

c.

Repair of Leak on Unit 1 Letdown Line

On December 13 the licensee noted a step change in the unidentified

RCS leakage on Unit 1.

The PT-10 , rea~tor coolant leakage, (TITLE)

. test results indicated that leakage had increased from approximately

0.2 gpm to approximately 0.37 gpm.

This value was still well below

the TS limits of 1.0 gpm unidentified leakage.

In accordance with

the requirements of PT-10 the licensee increased the leakage

monitoring activity and attempted to locate the source of the

leakage.

The 1 icensee made several containment entries and noted

leakage at a welded joint on the eves letdown line.

The licensee.

made plans to isolate, drain, and repair weld the joint in accordance

with station procedures.

During the attempts to isolate and drain the line for weld repairs

the licensee noted that the isolation valves were leakihg past their

seats.

The amount of leakage that was being funneled with a

partially opened drain valve was above the TS limit of 1 gpm and the

licens*ee entered the TS LCO action.

The licensee exited the LCO

action after the dr~in valve was reclosed and the RCS leakage was

verified as being within the TS l.imits.

During the period of time

that letdown was isolated the excess letdown system was being used.

The 1 i censee did not want to utilize* the excess 1 et down system for an

extend~d period since there was RCS to CC system leakage in the heat

exchanger and this leakage was causing the CC system activity to

increase.

On December 20 the 1 icensee returned the Unit 1 letdown

system to service without repairing the leak on* the welded ASME class

2 piping system.

This leak did not meet the Code* requirements in

IWA-5250 of Section XI of the ASME Code, and the licensee did not

d.

8

submit a request for relief from Section XI as required by 10 CFR

50.55a(g)(6)(i).

No engineering evaluation was perfonned to

determine the extent of the defect. _ Further guidance for obtaining

relief i's provided in Generic *Letter 90-05.

This is identified as

the Violation 280/91-37,.0l, Failure to Follow the Requirements of

10 CFR 50.SSa(g).

-

On December 24, the licensee isolated the 'effected line using a

manual valve in ~ddition to the isolation v~lve which had excessive

seat leakage during the first attempt.

The licensee completed the

weld repairs on Dec~mber 26, and the system was returned to service

on December 27.

The licensee did not agree with the inspectors findings as noted in

the violation above.

The licensee's stated position was that the RCS

leakage* TS apply to situations of identified leakage found during

plant operations.

The inspectors referred the licensee to GL 91-18

which provides

NRC guidance on requirements associated with

operability and ensuring the* functional capability of a *system or

component.

Section 6.15 of the guidance, titled Operational Leakage*

speciftes the NRC's position on leakage identified during operations

as well as during ISI inspections.

The NRC's 'guidance specifies that

upon discovery of leakage from Class 1, 2 or 3 component pressure

boundary, the licensee should declare the component inoperable.

Additionally, the guidance further indicates that section IWA-5250 of

ASME section XI would not allow acceptance of a through wall leak and

other sectfons- of the guidance requires the licensee to request NRC

approval for relief_ from code requ-irements.

The licensee position

was discussed with NRC management, as required by the GL guidance,

and it WQS detennined that the licensee was requireed to obtain NRC

relief in order to operate with through-wall defects in ASME Code

Class 2 piping.

Troubleshooting Feedwater Control_Valve 2-FW-FCV-2488

On December 17, Unit 2 was starting back up to power after an outage

to repair RTD bypass instrument leak discussed in Paragraph 4~b.,

when the B feedwater regulating valve started oscillating open and

closed.

This resulted in -a rise in the level in the B steam

generator, a turbine trip, and a reactor trip;

The inspectors observed the troubleshooting on this valve using work

order no. 38000121938 and procedure 2-PT-2.34, Functional Testing of

Main Feedwater Regulating and Bypass Valves, dated July 29, 1989.

The licensee replaced the valve positioner and ran several regulatof

pressure versus valve movement curves for all three valves., These

curves are still undergoing analysis by the maintenance engineering

group.

In addition, the inspectors observed the replacement of the

packing for this va 1 ve using the same work order and procedure

0-MCM-0412-05,

Chesteron R~pack Without Lantern Rings, dated

October 10, 1991.

No deficiencies were noted.

9

Within the areas inspected, one violation was identified (Paragraph 4.c).

5.

Design Change Review

During several of the Unit 1 outage planning meetings the licensee has

indicated that the RTD bypass manifolds will be removed during the

upcoming February, 1992 Unit 1 refueling outage.

The licensee's proposed

modification is needed since the bypass manifolds have historically been

contributors to personnel exposure and have resu 1 ted in severa 1 forced

plant shutdowns and mode changes due to system leakage.

The licensee's

proposed design change 91-05-1, describes the modifications of the piping

as well as the electrical systems that are necessary_to process the signal

from the new RTDs which are being installed directly in the thermowells

mounted in the hot and cold legs of the RCS.

  • T.he inspector's review of the 1 icensee proposed RTD bypass manifold

elimination per design change 91-05-1 identified several concerns.

The

concerns i.nvol ved changes in the equipment time response character, sti cs

as well as the acceptability of perfonning this modification under the 10

CFR 50.59 umbrella without prior NRC approval. * The licensee's proposed

modification contained a statement that the response time. used by

Westinghouse in the Surry accident analysis for OT and OP delta-T trips is

six seconds.

The proposed modification also states that the response time

for the new narrow range RCS temperatu~e measurement system will be held

to this 1 imi t.

Since the Surry TS was silent on equipment time response, the* inspector

reviewed FSAR chapter 14 accident analysis to detennine if a time response

for OT and OP delta-T was specified.

FSAR Section 14.2.2 accident

analysis for uncontrolled control-rod assembly withdrawal at power

specified a method of analysis (section 14.2.2.1) which insured that DNBR

was not exceeded during -the accident.

The method of analysis specified

several assumptions and initial conditions that -were made as part of the

analysis. Section 14.2.2.1.3 contains the following statement:

"The reactor trip on high nuclear power is assumed to actuate ~ta

conservative value of 118% of nominal full power.

The delta T trips

include all adverse instrumentation and setpoint errors.

The delay

for trip signal actuation are assumed at their maximum values, that

is, 0.5 sec for the high nuclear power trip and 3.5 sec for the delta

  • Ttrip."

This time response of 3.5 seconds appears to be the value that was assumed

and reviewed as part of the licensing basis for Surry.

To install a

modification that increases this time response to 6 seconds appears to be

a reduction in the margin assumed as the basis for technical specifica-

tions.

Therefore, the modification should be considered an unreviewed

safety question per the requirements* of io CFR 50. 59.

The Surry TS does

not specify system time response and therefore the other provisions .of

lOCFRS0.59 regarding TS changes also was considered by the licensee not to

, apply.

10

The inspecto~s discussed their concerns with.the licensee's nuclear fuel

and analysis engineering group who were perfonning the 10CFR50.59 analysis

for the proposed modification. The NFA representative indicated that they

were perfonning the 50.59 using the guidance of NSAC-125, Guidelines for

10 CFR 50.59 Safety Evaluations.

The NFA representative also indicated

that although the FSAR original safety analysis indicated-a time response

time of 3.5 seconds, the licensee had submitted several reanalyses to the

NRC to support other license amendments and had used a 6 second time

response although the change in time response had not been highlighted.

The licensee indicated that changing the time response of the OT and OP

delta-T trips was not considered a reduction in.margin per 10 CFR 50.59

and therefore the ~edification was not considered an unreviewed safety

  • question and did not require Cof111!1ission approval.

The licensee interprets NSAC~125 as allowing the flexibility of changing

assumptions used in ace i dent analysis as long as the parameter (i.e. DNBR)

is not' exceeded.

This could include setpoints and time response

assumptions that have not been incorporated into a specific TS limit.

This interpretation of reduction_ of margin is different from what has been

previously allowed by the NRC and may not b*e acceptable.

The inspectors have discussed the above issue with the NRC staff. The NRC

staff's review of the proposed Surry modifications conclucled that since

the six seconds c~trently assumed by the licensee's analysis is unchanged

by the modification, a reduction in margin has not oc~urred.

The NRC is

currently modifying their guidance in the area of 10 CFR 50.59 and this

new guidance will address the applications of NSAC-125 as well.

Within the area~ inspected, no violations were identified.

6.

Surveillance Inspections

(61726, 42700)

During the reporting period, the inspectors reviewed surveillance

activities to assure compliance with the appropriate procedure and TS

requirements.

The following surveillance activity was reviewed:

a.

Perodic Test 1-PT-17.1

Station deviation report S-91-1816 reported that during a QA audit of

the ISI program it was identified that l-PT-17.1, Containment Spray

System, missed its 92 days plus 25*percent performance window by 20

days when it was performed on May 14, 1991.

This constitutes a

missed surveillance per the litensee's TS 4.0 since the allowable

grace period between survei 11 ances was exceeded.

The licensee

identified that the PT had been performed on January 1, 1991, and

then was performed ~gain on May 14, 1991.

The frequency of the PT

was changed from monthly to quarterly by PAR 91-118 on January 24,

1991 and an administrative error was made concerning recording the

last time.the PT was performed.

This example of missed surveillance

11

.

,

was similar to two other examples that were sited by Violation no.

280/91-06-01 that was issued after this January, 1991 date.

The

  • corrective action program for that violation was implemented on*

June 1, 1991.

Since the missed PT, l-PT-17.1, occurred before the

corrective action program was implemented, an additional .violation

will not be issued.

Within the areas inspected, no violations were identified.

7.

Action on Previous Inspection Findings (92701, 92702)

(Closed) TI 280,281/2500-20, ATWS Mitigation System.

In report no. 90-41,

the inspectors discussed inspection of the newly installed ATWS mitigation

system for Unit 1.

At the end of that inspection the inspectors noted

that after the system was installed and placed in* service several

annunciators for this system were activated.

Subsequence followup

revealed a problem with a defective program logic card.

This problem was*

corrected and the system was returned to service.

The inspectors also

followed the installation of the Unit 2 ATWS mitigation system.

Followup

by the inspectors, including discussions this inspection period with the

sys tern engineer, rev ea 1 no apparent pr.ob l ems with the ins ta 11 ed sys terns

for both units and this TI is considered closed.

Within the areas inspected, no_ vioilations were identified.

8.

Exit Interview

The inspection scope and results were surrmarized on January 8, 1992, with

those individuals identified by an asterisk in paragraph 1.

The following

surrmary of inspection activity was discussed by the inspectors during this

exit.

Item Number

VIO 280/91-37-01

TI 280,281/2500/20

ATWS MITIGATION

SYSTEM

Status

OPEN

CLOSED

Description and Reference

Failure to meet requirements of

Section XI of ASME Code and seek

relief UNDER 10 cfr 50.55{g)(6)(i).

Followup inspections concerning

ATWS Mitigation System

The licensee acknowledged the inspection conclusions.

However, the

licensee indicated that they did not agree with the NRC

1 s interpretation

of the need for ASME code relief to operate with pressure barrier leakage

that would be allowed by their TS.

The licensee's corporate licensing

manager indicated that the utility considered that the NRC's position

represented a Backfit.

Details of the licensee's position on this issue

are discussed in paragraph 4.c.

12

9.

Index of Acronyms and Initial isms

AFW

AUXILIARY FEEDWATER

AMSAC

ATWS MITIGATION SYSTEM ACTUATION CIRCUIT

ASME

AMERICAN SOCIETY OF MECHANICAL ENGINEERS

ATWS

ANTIC I PATED TRANS IT WITHOUT SCRAM

CC

COMPONENT COOLING

CFR

CODE OF FEDERAL REGULATIONS

CRD

CONTROL ROD DRIVE

eves

CHEMICAL AND VOLUME CONTROL SYSTEM

CW

CIRCULATING WATER

DNBR

DEPARTURE NUCLEAR BOILING RATIO

ECCS

EMERGENCY CORE COOLING SYSTEM

EHC

ELECTROHYDRAULIC CONTROL

EJ

EXPANSION JOINT

ERFCS

EMERGENCY RESPONSE FACILITY COMPUTER SYSTEM

EWR

ENGINEERING WORK REQUEST

FSAR

FINAL SAFETY ANALYSIS REPORT

GL

GENERIC LETTER

GPM

GALLONS PER MINUTE

IR

INTERMEDIATE RANGE

!PE

INDEPENDENT PLANT EVALUATION

ISI

INSERVICE INSPECTION

LCO

LIMITING CONDITION OF OPERATION

LOCA

LOSS OF COOLANT ACCIDENT

MFRV

MAIN FEEDWATER REGULATING VALVE

MG

MOTOR GENERATOR

MWe

MEGAWATI ELECTRIC

NFA

NUCLEAR FUEL AND ANALYSIS

NIS

NUCLEAR INSTRUMENTATION SYSTEM

NCV

NON-CITED VIOLATION

NRC

NUCLEAR REGULATORY COMMISSION

OP

OVER PRESSURE

OT

OVER TEMPERATURE

PAR

PROCEDURE ADMINISTRATIVE REVISION

PORV

POWER OPERATED RELIEF VALVE

PT

PERIODIC TEST

RCS

REACTOR COOLANT SYSTEM

RTD

RESISTANCE TEMPERATURE DETECTOR

SG

STEAM GENERATOR

SW

SERVICE WATER

T

TEMPERATURE

TB

TURBINE BUILDING

TI

TEMPORARY INSTRUCTION

TS

TECHNICAL SPECIFICATIONS