ML18152A227

From kanterella
Jump to navigation Jump to search
Insp Repts 50-280/89-28 & 50-281/89-28 on 890903-30.One Noncited Violation Noted.Major Areas Inspected:Plant Operations,Maint & Surveillance,Plant Startup from Refueling,Ler Review & Inspector Identified Items
ML18152A227
Person / Time
Site: Surry  Dominion icon.png
Issue date: 11/01/1989
From: Fredrickson P, Holland W, Larry Nicholson, York J
NRC OFFICE OF INSPECTION & ENFORCEMENT (IE REGION II)
To:
Shared Package
ML18152A228 List:
References
50-280-89-28, 50-281-89-28, NUDOCS 8911140119
Download: ML18152A227 (20)


See also: IR 05000280/1989028

Text

Report Nos.:

UNITED STATES

NUCLEAR REGULATORY COMMISSION

. REGION 11

101 MARIETTA STREET, N.W.

ATLANTA, GEORGIA 30323

50-280/89-28 and 50-281/89-28

Licensee:

Virginia Electric and Power Company

5000 Dominion Boulevard

Glen Allen, VA

23060

Oocket'Nos.:

50-280 and 50-281

Faci 1 ity Name:

Surry- 1 and 2

License Nos.:

DPR-32 and DPR-37

Inspection Conducted:

September 3 - 30, 1989

Accompanying Inspector: M. S. Lewis, Project Engineer, DRP

, ... , s

I

-

Approved by:

  • 1,

.

eA...A....,1/)

..*.

Scope:

P .. E. Fredrickson, Sect"bn Chief

Division of Reactor Protects

SUMMARY

/I /1 le?

Da& ITgned

This routine resident inspection was conducted on site in the areas of plant

operations,

plant maintenance,

plant surveillance,

plant

startup

from

refueling, evaluation of licensee self assessment capability, licensee event

report review, and followup on inspector identified items.

Certain tours were conducted on backshifts or weekends.

Backshift or weekend

tours were conducted on September 3, 4, 10, 15, 16, 17, 20, 23, 24, 28, and 30.

Results:

During this inspection period, one non-cited violation was identified for

failure to provide an adequate procedure for restoration of safety-rela_ted

valves following periodic testing (paragraph 3.a).

In addition, a licensee

8911140119 891101

PDR

ADOCK 05000280

Q

PNU

2

identified non-cited violation was noted for failure to provide adequate

procedures for filling *evolutions associated with the service water system

(paragraph 9).

A weakness in operator control of the electro-hydraulic control system at low

powers was noted. This weakness contributed to a Unit 2 reactor trip (paragraph

3.a). Strengths were noted with regards to the licensee 1 s management review of

Unit 2 restart readiness (paragraph 4) .

1.

Persons Contacted

Licensee Employees

REPORT DETAILS

  • W. Bentha 11 , Supervisor, Licensing
  • R. Bilyeu, Licensing Engineer

R. Blount, Superintendent of Technical Services

D. Christian, Assistant Station Manager

D. Erickson, Superintendent of Health Physics

  • E. Grecheck, Assistant Station Manager

iM. Kansler, Station Manager

T. Kendzia, Supervisor, Safety Engineering

J. McCarthy, Superintendent of Operations

G. Miller, Licensing Coordinator, Surry

J. Ogren, Superintendent of Maintenance

T. Sowers, Superintendent of Engineering

  • E. Smith, Site Quality Assurance Manager
  • Attended exit interview

Other licensee employees contacted included control room operators, shift

technical advisors, shift supervisors and other plant personnel.

On September 19, 1989, one of the Commissioners of the Nuclear Regulatory

Commission, Dr. Kenneth C. Rogers, visited the Surry Power Station for a

familiarization tour, to meet with licensee management and staff, and to

review the current status of the station.

Commissioner Rogers was

accompanied by the following personnel:

J. Stohr, Director, DRSS, Region II

M. Lewis, Project Engineer, DRP, Region II

NRC Resident Inspectors

The

Commissioner

met

with

the resident inspectors, was

given a

presentation on the status of the station by licensee management, met with

selected station personnel, and was taken on a tour of the station

including the turbine building, control room, training simulator, and the

independent spent fuel storage installation.

Acronyms and initial isms used throughout this report are listed in the

last paragraph.

2.

Plant Status

Unit 1 began the reporting period at power.

The unit operated at power

for the duration of the inspection period .

2

Unit 2 began the reporting period in cold shutdown. After completion of

all work which was required prior to leaving cold shutdown, the unit

commenced heatup above 200 degrees Fon September 10.

The unit continued

with the startup sequence in accordance with procedures and was critical

on September 16, 1989.

During initial approach to criticality, the unit

was manually tripped due to improper control rod bank overlap.

This

problem is further discussed in paragraph 3.a.

Physics testing was

conducted on September 16 and 17, and the unit was connected to the

turbine generator on September 18.

However, during electrical checkouts

in preparation for connecting to the grid, the unit tripped from 14%

power.

This trip is further discussed in paragraph 3.a. After completion

of repairs to a generator relay, the unit was restarted late on

September 18 and connected to the grid on September 19.

However, during

initial turbine load1ng, the unit tripped from approximately 23% power on

low SG level in

11 8

11 SG.

This trip is further discussed in paragraph 3.a.

The unit was restarted on September 19 and was connected to the grid later

that evening.

The unit was operated at up to 40% power until September 22

when the turbine was taken off line for balancing due to vibration

problems.

The turbine was pl aced back on line on September 23; however,

the vibration problems continued and the unit was operated at 40% power

until September 28 when the turbine was again taken off line for

additional balancing.

The turbine balancing was completed and the unit

was preparing to return to power operations when the inspection period

  • ended._

3.

Operational Safety Verification (71707 & 42700)

a.

Daily Inspections

The inspectors conducted daily inspections in the following areas:

control

room staffing, access, and operator behavior;

operator

adherence to approved procedures, TS, and LCOs; examination of panels

containing instrumentation and other RPS elements to determine that

required channels are operable; and review of control room operator

logs, operating orders, plint deviation reports, tagout logs, jumper

logs, and tags on components to verify compliance with approved

. procedures.

On September 11, the inspectors were informed of a condition in which

the Unit 2 LHSI pump, 2-SI-P-lA, was operated for approximately 3

minutes witho~t*a suction flowpath.

Investigation by the operators

determined that-a manually operated pump suction valve (2-SI-57) was

shut.

Review of the configuration status logs and valve lineups for

restart of the un.it indicated that the valve was open.

Additional

reviews by the oper~ti6ns department determined that Type C leakage

testing in accordance with periodic test 2-PT-16.4 for containment

penetration 60 had been performed after the system valve lineups.

The test, which was performed on September 4, shut the valve for

3

testing, then required that the valve be reopened in the restoration

portion of the test.

However, the restoration step of the periodic

test required that valves which were positioned for testing be

returned to their required position without specifically listing each

affected valve.

The step did require independent verification;

however, it a 1 so necessitated that the operators review the entire

procedure to determine which valves needed to be repositioned.

After

completion of a review of the valves that were repositioned by

2-PT-16.4, it was discovered that one additional valve was not in its

correct position.

The inspectors and 1 i censee management discussed the use of the

PT-16.4

series

procedures

in

their

present

condition.

The

discussions focused on procedure use after unit valve lineups for

startup had been completed.

The inspectors were informed that use of

these procedures in their current condition would not be allowed

without requiring that additional

valve

by

valve

lineups be

accomplished and documented as a part of the valve restoration

process .. A 1 though the inspectors concluded that the valve 1 i neup

problem was caused in part by the operators 1 failure to follow

~rocedures, an

additional

contributor was

inadequate procedure

concerning the lack of specific valve restoration requirements.

Additional reviews concluded that the safety significance of this

problem was minimal due to the fact that the pump was not required to

be operable during the time frame that the valve was out of position

and additional critical valve lineups during the startup process

would have discovered the problem.

Failure to provide an adequate

procedure for restoration of safety-related valves following periodic

testing is a violation (NCV 281/89-28-01).

However, the violation is

not being cited because the criteria specified in Section V.G of the

Enforcement Policy were satisfied.

The inspectors specifically focused on Unit 2 restart activities

during the earlier part of the inspection period.

Inspection was

increased during the heatup and return to criticality of the unit.

The inspectors focused on the startup controlling procedures and

noted that greater operator attention was being placed on completion

of procedures prior to commencing the next sequential procedure than

had been displayed during the Unit 1 startup in July 1989.

Also

noted was proper verifications of initial condition steps prior to

commencing the performance section of the procedures.

However, the

inspectors believed that the operations procedures were still not

written in a manner which would provide for the best possible aid to

operators during the startup evolutions.

The inspectors consider

that these procedures should be upgraded in a priority manner

consistent with usage.

This concern was discussed with licensee

management and they agreed to review the priority assigned to these

upgrades.

The inspectors will review this area as part of the

procedure upgrade program review.

4

On

September 16,

the inspectors were conducting a backshift

inspection of the Unit 2 startup and witnessed a problem with the rod

control bank overlap system.

During rod withdrawal to criticality,

the

118

11 control bank was reading 15 st~s out when the

11A

11 control

rod bank was reading 103 steps out. This constitutes a bank overlap

of 88 steps versus the expected 128 steps.

The RO stopped rod motion

and contacted the SRO.

A decision was made to trip the rods in and

initiate troubleshooting by the instrument technicians. A four hour

notification was

made

to the

NRC at 1458 hours0.0169 days <br />0.405 hours <br />0.00241 weeks <br />5.54769e-4 months <br />.

Subsequent

troubleshooting failed to identify and/or repeat the problem and the

reactor was taken critical at 1950 hours0.0226 days <br />0.542 hours <br />0.00322 weeks <br />7.41975e-4 months <br />.

No abnormal conditions

were noted in the contra 1 rod bank overlap system during the

subsequeni pull to criticality.

The

inspectors witnessed the

operator actions in the control room during this time frame and

considered them to be appropriate.

On September 18, 1989 at 1042 hours0.0121 days <br />0.289 hours <br />0.00172 weeks <br />3.96481e-4 months <br />, Unit 2 tripped from 14% reactor

power.

The inspectors were in the control room at the time of the

trip and observed operator actions.

At the time of the trip, the RO

was

placing the generator voltage

regulator

in

service

in

preparations for connecting the main generator to the electrical

grid. While increasing generator voltage, the operator received a

generator backup relay trip alarm, indicating: that the Unit 2

generator had tri*pped.

The generator trip initiated a turbine trip

and

subsequent reactor trip.

Following the reactor trip, the

inspectors noted that Tavg decreased to less than 530 degrees F.

All

safety systems responded as required and the inspectors noted that

operator actions following the reactor trip were adequate.

On September 18, the licensee held a post trip review meeting with

those operators involved.

The inspectors attended the meeting, and

questioned the licensee with regards to the lower than expected Tavg

after the trip. The licensee concluded that the cooldown was nor~al

for the reactor conditions at hand, i.e. cool feedwater due to no

extraction steam, 210 gpm blowdown from the SGs, and no fuel decay

heat.

Licensee investigations on that same day revealed that the

generator trip was caused by an electrical problem in the generator

backup relay.

The relay was replaced and the unit was returned to

criticality. A four hour notification was made to the NRC at 1351

hours on September 18.

On September 19, 1989 at 0051 hours5.902778e-4 days <br />0.0142 hours <br />8.43254e-5 weeks <br />1.94055e-5 months <br />, Unit 2 tripped from 23% reactor

power on low low level in the

118

11

SG.

After the trip, required

safety systems performed as designed.

Both motor driven AFW pumps

auto started and SG levels were recovered into the normal bands.

A

four hour notification of the trip ~as made to the NRC at 0120 on

September 19.

b.

5

During discussions with the inspectors, the licensee attributed the

ca~se of the reactor trip to operator error in the operation of the

EHC turbine control system combined with a sensitive manual feedwater

control system.

Prior to the trip, feedwater to the SGs was being

controlled manually.

Just prior to the trip one operator was

attempting to establish AFW regulating valve control while another

operator was raising turbine load.

The operator controlling the

turbine increased load faster than normal, causing a temperature

decrease in the RCS ~nd subsequent closing of the SG steam dumps at a

low Tavg of 540 degrees F.

SG levels began to oscillate as a result

of increased load and subsequent steam dump closures.

Because of the

sensitive feedwater control

system, the operator was unable to

control the SG levels in the required band. Subsequently, a low low

level in the

11 8

11 SG initiated the reactor trip.

The Operations Superintendent described to the inspectors the proper

operator actions in increasing load for the reactor conditions at

hand, and stated that the turbine 1 oad 1 imi ter should have been

increased in a more controlled manner.

Discussions with the training

department personnel indicated that only specific steps in the

startup procedure are emphasized during training.

The specific

requirement associated with deliberate bumping up of turbine load

limiter at low powers appeared to be addressed in start~p procedure

2-0P-2. 2 .1,

Turbine -

Generator Startup to

20~6.

This event

demonstrated a weakness in operator control of the EHC system at low

powers.

Weekly Inspections

The inspectors conducted weekly inspections in the following areas:

verification of operability of selected ESF systems by valve

alignment, breaker positions, condition of equipment or component,

and operabi 1 i ty of instrumentation and support items es sent i a 1 to

system actuation or performance.

Plant tours were

conducted which

included observation of general

plant/equipment conditions, fire

protection and preventative measures, control of activities in

progress, radiation protection controls, physical security controls,

plant housekeeping conditions/cleanliness, and missile hazards.

The

inspectors routinely monitored the temperature of the AFW pump

discharge piping to ensure increases in temperature were being

properly monitored and evaluated by the licensee.

c.

Biweekly Inspections

The inspectors conducted biweekly inspections in the following areas:

verification review and walkdown of safety-related tagouts in effect;

review of sampling program (e.g., primary and secondary coolant

samples, boric acid tank samples, plant liquid and gaseous samples);

6

observation of control room shift turnover; review of implementation

of the plant problem identification system; verification of selected

portions of containment isolation lineups; and verification that

-notices to workers a re posted as re qui red by 10 CFR 19.

d.

Other Inspection Activities

Inspections included areas in the Unit 1 and 2 cable vaults, vital

battery rooms, steam safeguards areas, emergency switchgear rooms,

diesel generator rooms, control room, auxiliary building, Unit 2

containment, cable penetration areas, independent spent fuel storage

facility, low level intake structure, and the safeguards valve pit

and pump pit areas. RCS leak rates were reviewed to ensure that

detected or suspected leakage fro~ the

system was

recorded,

investigated, and evaluated; and that appropriate actions were taken,

if required.

The inspectors routinely independently calculated RCS

leak rates using the NRC Independent Measurements Leak Rate Program

(RCSLK9).

On a regular basis, RWPs were reviewed and specific work

activities were monitored to assure they were being conducted per the

RWPs.

Selected radiation protection instruments were periodically

checked, and equipment operability and calibration frequency were

verified.

~-

Physical Security Program Inspections

In the course of monthly activities, the inspectors included a review

of the 1 icensee' s physical security program.

The performance of

various shifts of the security force was observed in the conduct of

daily activities to include: protected and vital .areas access

controls;

searching of personnel, packages and -v_ehicles;

badge

issuance and retrieval; escorting of visitors; and patrols and

compensatory posts.

f.

Licensee 10 CFR 50.72 Reports

(1)

On September 3, 1989, the licensee made a report in accordance

with 10 CFR 50.72 concerning an inadvertent ESF actuation.

The

event, which was an auto start of the No.3 EOG, occurred during

the securing of the EOG in accordance with normal procedures.

The diesel had previously been running as a part of special test

ST-241, ESF Actuation with Instantaneous Undervoltage on the

Unit 2

11J

11 Bus.

The inadvertent restart was traced to a loose

connection on the terminal block of the Hi

Hi

CLS signal

circuitry.

Because of this loose terminal, the Hi Hi CLS signal

remai~ed locked in after the test and could not be reset.

This

condition resulted in the EOG auto start after returning the

diesel to the standby condition by placing the EOG selector

switch in auto. After identification of the problem, the loose

terminal was tightened, the Hi Hi CLS signal was reset and the

EOG was properly secured and placed in standby.

7

  • (2)

On September 8, 1989, the licensee made a report in accordance

with 10 CFR 50.72 concerning an inadvertent a_ctuation of ESF

components on Unit 2 during performance of surveillance testing

on flood control circuitry. The testing was not associated with

ESF circuitry and the closure signal was not an ESF signal ..

However, the two valves that inadvertently closed were. ESF

components.

The problem was traced to a fault in a relay for

the flood control circuitry.

The

relay problem will be

corrected after completion of the investigation and procurement

of required parts.

(3)

On September 11 , 1989, the licensee made a report in accordance

with 10 CFR 50.72 concerning an ESF component actuation.

The

actuation was the closing of the containment instrument air

isolation valves due to a containment radiation monitor alarm.

The cause of the radiation monitor alarm was attributed to a

natural isotope buildup inside containment after pressure was

reduced in preparation for startup.

Sampling and no increase in

RCS leakage confirmed this conclusion. A setpoint change to the

radiation monitor was accomplished to allow for natural isotope

buildup.

(4)

On September 16, 1989, the licensee made a report in accordance

with 10 CFR 50.72 concerning an ESF component actuation.

The

actuation was the closing of one of the containment isolation

valves for the suction of the containment instrument air

compressor due to an* apparent loss of power to the valve

solenoid.

No valid ESF signal was present.

The licensee was

conducting an investigation into the cause of this problem when

the report period ended.

An

LER wi 11 be prep a red for this

event.

(5)

On September 16, 1989, the licensee made a report in accordance

with 10 CFR 50.72 concerning a manual trip of the Unit 2 reactor

during startup.

The licensee stated that during withdrawal of

the control banks for approach to criticality, _the operators

noticed an improper bank overlap between the A and B control

banks.

The startup was stopped and a manual reactor trip was

accomplished at the direction of the Operations Superintendent.

This event is further discussed in paragraph 3.a.

(6)

On September 18, 1989, the licensee made a report in accordance

with 10 CFR 50.72 concerning an automatic reactor trip of Unit 2

from

14% power.

The cause was a generator trip causing a

turbine trip which resulted in the reactor trip.

All safety

systems operated as designed.

This event is further discussed

in paragraph 3.a.

8

(7)

On September 19, 1989, the* licensee made a report in accordance

with 10 CFR 50.72 concerning an automatic reactor trip from 23%

power due to a low low level in the

11 8

11 SG.

All safety systems

operated as designed.

This event is further discussed in

paragraph 3.a.

(8)

On September 19. 1989, the licensee made a report in accordance

with 10 CFR 50.72 concerning a pipe which penetrates the Unit 2

containment being classified in *an unanalyzed condition from a

containment integrity standpoint.

The pipe was determined to be

suspect during a review of an existing pipe design.

The review

concluded that the support for the pipe was connected to both

the auxiliary building and the reactor building, which did not

allow for proper movement in a seismic event.

Corrective action

was. taken to disconnect the pipe support from one of the

buildings.

In addition, a licensee inspection determined that

the same condition did not exist on the other unit.

The cause

of the event was due to inadequate design review during

installation in the early 1980s.

This issue is discussed in

greater detail in paragraph 5.c.

Within the areas inspected, one non-cited violation was identified.

4.

Operaticinal Readiness Assurance Program Review - Unit 2 (7171P)

On September 4, 1989. the inspectors monitored the continuation of the

licensee

1 s management review of the functional areas associated with the

return to opera't ion of

Un it 2.

These funct i ona 1 areas inc 1 uded

operations, maintenance, surveillance, engineering, radiological controls,

safety assessment and QA.

The management team involved in these reviews

included the Station Manager, the two Assistant Station Managers, and the

Quality Assurince Manager.

The reviews were similar to those accomplished

for Unit 1 restart, and consisted of the appropriate supervisors of each

functional area discussing the restart readiness of their responsible

areas.

The inspectors _noted that one problem was .identified in the

l{censing area with regards to verification of the Unit 2 containment sump

cleanliness in accordance with a recent revision to TS.

Accordingly, a

decision was made to open up and reinspect the containment sump, resulting

in the unit restart schedule being

delayed.

This activity is further

discussed in paragraph 5.b.

After the completion of each review area, a list of action items was

generated.

The 1 icensee management al so discussed the status of unit

readiness prior to changing plant conditions and authorized each plant

condition change.

The inspectors monitored the licensee

1 s actions in this

area and believes that all restart issues* were adequately addressed. This

is considered an area of strength in the licensee

1 s performance.

  • -

9

On August 31, 1989, the licensee sent a letter to the NRC which formally

documented the resolution of the CAL items that were identified in a

letter from the NRC dated March 9, 1989.

In their letter, the licensee

reviewed the status of each item and listed each outstanding action to be

completed prior to Unit 2 criticality.

The NRC sent a. letter to the

licensee on September 8, 1989 concurring with the completion status of

each CAL item for Surry Unit 2 restart.

The residents reviewed the

licensee 1 s letter and verified completion of the items prior to Unit 2

restart.

Within the areas inspected, no violations or deviations were identified.

5.

Maintenance Inspections (62703 & 42700)

During the reporting period, the inspectors reviewed maintenance

activities to

assure

compliance

with

the appropriate

procedures.

Inspection areas included the following:

a.

Low Head Safety Injection Pump 2-SI-P-18 Repairs

During this inspection period, the inspector monitored the progress

and reviewed the documentation associated with the repair of the Unit

2 LHSI pump 18.

The pump repairs were required as a result of a high

vibration condition that occurred during performance of a routine

periodic test.

The licensee decided to disassemble, inspect, and

repair the pump in order to correct the condition which was

contributing to the high vibration.

The disassembly, inspection, and repair of the pump were accomplished

on work order 3800084712.

Actua 1 pump work was accomp 1 i shed in

accordance

with

maintenance

procedure

MMP-C-SI-090,

Removal,

Disassembly, Inspection, Repair, Reassembly, and Reinstallation of

Low Head Safety Injection Pump.

The inspector reviewed the completed

work package and specifically focused on foreign material exclusion

controls during reinstallation of the pump.

The inspector noted that

prior to reinstallation of the pump in its container, a visual

cleanliness inspection was made of this location by a QC inspector.

The inspector verified that pump container cleanliness was documented

by the QC inspector in the comp 1 eted procedure.

In *addition, the

inspector noted that the procedure required appropriate cleanliness

to be

maintained during all work evolutions.

The

inspector

specifically reviewed several material control accountability sheets

for different shifts accomplishing work.

The inspector believes that

the procedure documented adequate repair and

foreign material

exclusion control for the repair of ~-SI-P-18.

b.

Review of the Unit 2 Containment Sump Closeout Activities

During this inspection period, the licensee conducted a closeout

inspection of the Unit 2 containment sump.

This inspection was

accomplished in order to satisfy a TS amendment that was issued on

10

August 28, 1989.

The _amendment required that a visual inspection of

the containment sump be accomp 1 i shed at 1 east once each refue 1 i ng

period and/or after major

maintenance activities.

The

sump

inspection was accomplished in accordance with Design Change 88-02-2,

Revisions 54, 55, 56, and 57, which were reviewed by the inspectors.

An inspection was conducted in this area during a containment tour.

The inspector specifically focused on the foreign material exclusion

requirements of the procedure. It was noted that the procedure

required a confined entry and tool control be implemented prior to

removing blanks over pump suctions and/or any time a screen assembly

was not in place.

The inspector verified that the foreign material

controls were documented in accordance with requirements whenever

action steps removing screens and/or blanks were accomplished.

The

inspection of the containment sump identified foreign objects from

the suction piping of one outside recirculation spray pump (one piece

of wire) and one LHSI pump (2 rags).

Deviation reports weie written

for the foreign objects and evaluation of each object concluded that

pump operability would not have been affected.

The

inspector

reviewed the deviation reports and discussed them with engineering

personnel. It was concluded

that this maintenance activity was

accomplished in accordance with required procedures.

c.

Seismic Support Repair

On September 19, 1989, the licensee made a report in accordance with

10

CFR

50.72 describing a pipe which penetrates the Unit 2

containment being classified in an unanalyzed condition from a

containment integrity standpoint.

One of the supports for the pipe

had hanger members connected on both the auxiliary building and the

reactor building surfaces.

The potential exists that both of these

buildings could move at different rates or distances during a seismic

event, and since it is uncertain how the hanger will respond, an

unanalyzed condition was identified.

The inspectors reviewed field

change AW to EWR 88-309, Repair to Miscellaneous Hangers.

This field

change required removal of the hanger member which was attached to

the reactor building wall (member RC-19.lA).

The inspectors also

discussed the removal .of this member with maintenance personnel

. performing the task.

Field change AY to EWR 88-309 documents that calculation SE0-1486 was

performed to demonstrate the acceptability of the modified support

with a new brace and base plate attached to the auxiliary building

floor.

Results of the calculation are that the interim condition of

the support, with the member to the reactor building wa 11 removed,

was acceptable, i.e. meets interim seismic requirements.

Although

the inspectors did not review the calculations, the inspector's

review of the EWR which documents that the calculations, along with

the witnessing of part of the hanger modification, allowed the

11

inspectors to arrive at the conclusion that the problem had been

properly addressed.

An engineering walkdown was performed to ensure

that the corresponding piping in Unit 1 did not have a similar

condition.

No discrepancies were found.

d.

Feedwater Isolation Valve Repair

On

September 15,

1989,

the inspectors observed a maintenance

electrician changing the wiring of a motor on Unit 2 feedwater

isolation valve MOV-FW-254C.

The work was being performed in

accordance with EWR 89-466, Eva 1 uate MI

Va 1 ves, and work order 3800085719.

A quality maintenance organization inspector was also

observing the work.

The inspectors reviewed the EWR, the work order,

and the work in progress, and found no problems.

Within the areas inspected, no violations or deviations were identified.

6.

Surveillance Inspections (61726 & 42700)

During the reporting period, the inspectors reviewed various surveillance

activities to assure compliance with the appropriate procedures as

fo 11 ows:

Test prerequisites were met.

Tests were performed in accordance with approved procedures.

Test procedures appeared to perform their intended function.

Adequate coordination existed among personnel involved in the test.

Test data was properly collected and recorded.

Inspection areas included the following:

a.

Special Test 2-ST-245

On September 3, 1989, the inspector witnessed selected portions of

the performance of special test 2-ST-245, ESF Actuation with Delayed

Under Voltage (UV) (5 Min) - J Bus.

The purpose of the test was to

functionally check the sequencing of loads onto emergency bus 2J

following the injection of an ESF signal.

An undervoltage signal was

injected greater than 5 minutes after the initial ESF signal to

verify that the required loads tripped off the emergency bus and were

re-sequenced back onto the emergency bus in the required manner.

The inspector reviewed the test procedure to ensure that initial

conditions and testing prerequisite steps were performed.

Selected

pretest briefings by the test directors were monitored to evaluate

personnel

kn owl edge and understand;'ng of the re qui red tasks. The

inspector monitored test conduct from ESF signal initiation through

12

UV signal initiation and finally through test restoration. It was

noted that the test was controlled in an adequate manner and that

test discrepancies were identified to the test directors for proper

resolution.

No discrepancies were noted.

b.

Steam Dump Control System Valves

On September 10, 1989, the inspector reviewed test documentation

for calibration 63. Steam Dump Control System, and observed the

testing of three of the steam dump valves.

The inspector observed

the position of valves TCV-MS-2058, TCV-MS-2068, and TCV-MS-2088 as

the

information

was

bei~g

relayed to

other

instrumentation

technicians for a valve position verification.

Documentation was

complete and the test results indicated a proper position and

functioning of the three valves.

No discrepancies were noted.

c.

Control Rods

On September 15, 1989, the in specters witnessed hot rod testing of

the Unit 2 rods in accordance with periodic test 2-PT-7.2, Hot Rod

Drops.

This test measured the drop time for each of the 48 control

rods from fully wi thdra.wn to dashpot entry.

The in specter reviewed

the test procedure, witnessed control of testing from the control

room, and reviewed selected timing traces to independently verify

that the drop time was within the 2.4 seconds allowed by TS.

d.

Containment Spray System

On September 17, 1989, the inspector reviewed test documentation for

periodic test 2-PT-17.1, Containment Spray System, for spray pumps

2-CS-P-lA, wh-ich was tested on September 1, 1989, and spray pump

2-CS-P-18, which was tested on August 1, 1989.

Documentation was

complete and both pumps were considered operable.

e.

Inside Recirculation Spray Pumps

f.

On September 17, 1989, the inspector reviewed test documentation for

periodic test 2-PT-17.2, Containment Inside Recirculation Spray Pumps

Test, for inside recirculation spray pumps 2-RS-P-lA*and 18, which

were tested on August 28, 1989.

Documentation was complete and both

pumps were considered operable.

Condenser

On September 18, 1989, the inspectors witnessed licensee personnel

performing leakage tests on

the 8ntt 2 condenser.

Procedure

2-MOP-36.5, Secondary Plant Air Inleakage Inspection Procedure, was

being used.

The inspectors observed the planned release of helium

gas at five joints on the condenser during the testing.

Since the

condenser was under a partial vacuum, a leak at any of these joints

13

would enter into the condenser and later exit through the air ejector

line (elapsed time approximately one to two minutes). A helium leak

detector was placed in the air ejector line. The inspectors reviewed

part of the procedure, observed the release of the helium gas, and

observed the monitoring at the leak detector.

No discrepancies were

noted.

Within the areas inspected, no violations or deviations were identified.

7.

Plant Startup from Refueling

(71711)

During this inspection period, the inspectors witnessed testing and

monitored activities associated with periodic test 2-PT-28.11, Startup

Physics Testing. This procedure was the controlling procedure for several

of the tests that were required to be performed at low power levels

following refueling. The inspectors witnessed pretest briefings, verified

that specified conditions were met, and witnessed selected portions of the

following tests:

Reactivity Computer Accuracy Determination

This test determines the reliability range of the reactivity computer that

is used in subsequent testing by inserting and withdrawing control rods to

subtract or add reactivity.

The computer was determined to be accurate

within the range of plus 45 pcm and minus 43 pcm.

No discrepancies were

noted.

Isothermal Temperature Coefficient

This test involves measuring the MTC by determining the effects of plant

temperature changes on reactivity while maintaining constant rod position

and boron concentration.

The MTC was determined to be -3. 47 pcm/F.

No

discrepancies were noted.

Rod Swap Reference Bank Measurement

This test allows for measurement of the rod worth (pcm) of the reference

bank (control bank B) when fully inserted from 225 steps tb O steps.

No

discrepancies were noted.

Integral Rod Worth Measurements Using the Rod Swap Technique

This test allows for determination of the differential rod worth of the

reference bank (control bank B) when each of the remaining rod banks is

fully inserted from 225 to O steps.

The inspector witnessed selected

portions of this test when control bank

11 C

11 was the test bank.

No.

discrepancies were noted .

Within the areas inspected, no violations or deviations were noted.

14

8.

Evaluation of Licensee Self-Assessment Capability

On September 21, 1989, resident inspectors from Surry and North Anna, and

the NRC project engineer for Virginia Power plants visited the corporate

offices at Innsbrook Technical Center in Richmond, Virginia.

The visit

included discussions associated with the scheduling of current projects,

discussions

with

nuclear operations management,

discussions with

engineering management, and overviews of ongoing activities in the

emergency planning, nuclear operations support, quality assurance and

licensing areas.

Although the schedule did not provide for detailed

review of any area, it was apparent that the licensee had many new

programs in progress.

These new programs were in various stages of

preparation and/or development.

The inspectors concluded that additional

inspection time in the corporate offices to focus on specific programmatic

enhancements was warranted and additional inspection activities will be

scheduled as implementation of the new programs progress.

9.

Licensee Event Report Review

(92700)

The inspectors reviewed the LER 1 s listed below to ascertain whether NRC

reporting requirements were being met and to determine appropriateness of

the corrective actions. The inspector's review also 1ncluded followup on

implementation of corrective action and review of licensee documentation

that all required corrective actions were co~plete.

LERs that identify violations of regulations and that meet the criteria of

10 CFR, Part 2, Appendix C,Section V shall be identified as NCV in the

following closeout paragraphs.

NCVs are considered first-time occurrence

violations which meet the NRC

Enforcement Policy for exemption from

issuance of a Notice of Violation.

These items are identified to allow

for proper evaluations of corrective actions in the event that similar

events occur in the future.

(Closed) LER 280/88-20, Control/Relay Room Chillers and Unit 2 Charging

Pump SW Pumps Air Bound Due to Inadequate Procedure. The issue involved

the tripping of the subject pumps due to an inadequate procedure which was

being used to fill a drained SW line.

The improper filling evolution

resulted in air entry into the SW flowpath to the subject components, and

the resultant binding of the pumps.

Corrective actions included

venting of the SW line and affected pumps and returning them to service.

The inspector reviewed the LER and has monitored additional licensee

corrective actions in this area.

Failure to provide adequate procedure

for filling evolutions associated with the SW system is identified as

NCV

(280/89-28-02).

This LER is closed.

(Closed) LER 280/88-38, Recirculation Spray Heat Exchanger Valve Leakage.

The

is sue involved wetting of the internals of the subject heat

exchangers.

This condition could be detri men ta 1 to the re qui red heat

transfer capability of the heat exchangers.

Corrective actions included

15

draining the heat exchangers and conducting an appropriate inspection and

engineering evaluation of the condition of the drained heat exchangers.

The inspector verified that the inspection and engineering evaluation were

accomplished and necessary corrective actions were completed.

This LER is

closed.

(Closed) LER 280/88-41, Lifting Frames over RHR Pumps not Seismically

Qualified.

The issue involved the licensee's identification of the

subject concern.

Immediate corrective actions included interim bracing of

the frames for potential seismic loading:

Additional corrective actions

included removal of the frames during the outage.

The licensee also

reviewed other potential lifting device problems associated with the

generic concern and corrected these conditions prior to either units 1

restart.

The inspector monitored the licensee's corrective actions in

this area during the outage.

This LER is closed.

(Closed) LER 280/88-45, Failure to Sample Waste Gas Decay Tank Within 24

Hours Due to Failed Pneumatic Control Valve (PCV).

The issue involved

inability to obtain the required sample due to a failure of the sampling

PCV and a misinterpretation by the chemistry technicians that a 25% grace

period in sampling could be applied to this LCO requirement.

Corrective

action included valve repair to obtain the required sample and reinstruc-

tion of station personnel on the TS requirements.

The inspector reviewed

the LER.

A weakness had been 'previously identified by the NRC with

regards to the licensee's failure to correct radiation monitoring

equipment problems in a timely manner. This has resulted in dependence on

grab samples that are required by TS LCOs.

The licensee is currently

reviewing their options for correcting the inoperable monitoring equipment

problems in several areas.

This LER is closed.

10.

Action on Previous Inspection Findings

(92701, 92702)

(Closed) IFI 281/88-51-03, Evaluation of Whip Restraints on Pressurizer

Surge Line.

This item involved the inspection of the Unit 2 pressurizer

surge line as a response for acquiring some of the data required for NRC

Bulletin 88-11, Pressurizer Surge Line Thermal Stratification.

During

this inspection, it was noted that there were several bent rods on whip

restraints, that three of the whip restraint spring hangers were not

installed directly over the surge line, and that several *of the spring

cans were in the bottomed position.

None

of these conditions were

attributed to thermal stratification in the pressurizer surge line, the

topic of to the bulletin. The ceiling attachments were installed out of

position during construction, the bottomed out spring cans were caused by

improper setting, and the slightly bent rods were determined to have been

caused by improper spring can settings:

Engineering determined that the

improper setting restricted the support from freely pivoting (during the

normal expansion of the piping and not due to thermal stratification) and

caused a slight bending of several rods.

Engineering evaluated the

slightly bent rods an_d determined that they would have performed their

16

intended function in this condition.

The inspectors reviewed completed

documentation for re 1 ocat i ng the spring hanger cei 1 i ng attachments

11 2

11

radially outward, replacing the bent hanger rod.s, and properly resetting

the spring hangers.

This area was

also reviewed by a specialist from

Region II during this inspection period, which is documented in Inspection

Report 280, 281/89-29.

This item is closed.

(Closed)

RAI

89-34,

Reactor Operator

License Verification.

This

inspection effort was conducted to determine the 1 i censee methods for

ensuring that a non-qualified operator does not perform a licensed duty.

The inspector selected five licensed operators that have been disqualified

for various reasons and verified that they did not perform licensed duties

during the time they were disqualified.

No problems were noted.

In addition, the inspector interviewed backshift shift supervisors to

ascertain their ability to verify an individual's qualification prior to

assignment to a licensed duty.

The

licensee does not have

an

administrative procedure that requires a check of qualifications prior to

assignment on shift. The integrity of the operator is the defense agaihst

a problem in this area.

The on"'"shift operations management is not

provided with an updated ,tatus of the licensed operators.

The training

department provides a written statement to the Operations Superintendent

subsequent to an operator failing a requalification examination.

At this

point, the Operations Superintendent generally informs both the individual

and his shift supervisor that he is not to assume a licens~d duty.

This

process is done verbally and may not happen if the individual is a

licensed staff employee that does not work directly for operations.

The Operations Superintendent stated that he is developing a mechanism,

possibly by issuing drivers-license type cards, of ensuring that an

operator is prohibited from assuming a licensed watch station while he is

unqualified.

The inspectors will continue to monitor the implementation

of the enhanced program that is projected to be developed during the next

several months as a part of their regular inspection program.

11.

Exit Interview

The inspection scope and findings were summarized on October 3, 1989, with

those individuals identified by an asterisk in paragraph 1.

The following

new items were identified by the inspectors during this exit:

One non-cited violation was identified for failure to provide an adequate

procedure for restoration of safety-related valves following periodic

testing (paragraph 3.a) 281/89-28-01.

One licensee identified non-cited violation was identified for failure to

provide adequate procedures for filling evolutions associated with the SW

system (paragraph 9) 280/89-28-02.

17

A weakness in operator control of the EHC system at low powers was noted

which ultimately resulted in a Unit 2 reactor trip (paragraph 3.a).

Strengths were noted with regards to the licensee's management review of

Unit 2 restart readiness (paragraph 4).

The licensee acknowledged the inspection findings with no dissenting

comments.

The

1 icensee did not identify as proprietary any of the

materials provided to or reviewed by the inspectors during this

inspection.

12.

INDEX OF ACRONYMS ANO INITIALISMS

AFW

ANSI

AP

CAD

CAL

cc

ccw

CFR

CLS

cw

DPI

DR

DRP

DRSS

EOG

EHC

EMP

ESF

ESW

EWR

F

GOC

GPM

HP

HX

HPSI

IA

IE

I FI

IOER

IRPI

ISI

LER

LCO

LHSI

LOCA

LOOP

AUXILIARY FEEDWATER

AMERICAN NATIONAL STANDARDS INSTITUTE

ABNORMAL OPERATING PROCEDURE

COMPUTER AIDED DESIGN

CONFIRMATION OF ACTION LETTER

COMPONENT COOLING

COMPONENT COOLING WATER

CODE OF FEDERAL REGULATIONS

CONSEQUENCE LIMITING SAFEGUARD

CIRCULATING WATER

DELTA PRESSURE INDICATORS

DEVIATION REPORT

DIVISION OF REACTOR PROJECTS

DIVISION OF RADIATION SAFETY AND SAFEGUARDS

EMERGENCY DIESEL GENERATOR

ELECTRO-HYDRAULIC CONTROL

ELECTRICAL MAINTENANCE PROCEDURE

ENGINEERED SAFETY FEATURE

EMERGENCY SERVICE WATER

ENGINEERING WORK REQUEST

FARENHEIT

GENERAL DESIGN CRITERIA

GALLONS PER MINUTE

HEALTH PHYSICS

HEAT EXCHANGER

HIGH PRESSURE SAFETY INJECTION

INSTRUMENT AIR

INSPECTION AND ENFORCEMENT

INSPECTOR FOLLOWUP ITEM

INDEPENDENT OFFSITE EVALUATION AND REVIEW

INDIVIDUAL ROD POSITION INDICATION

INSERVICE INSPECTION

LICENSEE EVENT REPORT

LIMITING CONDITIONS OF OPERATION

LOW HEAD SAFETY INJECTION

LOSS OF COOLANT ACCIDENT

LOSS OF OFFSITE POWER

MER3

MDV

MCR

MTC

NCV

NRC

NRR

OP

ORS

PCM

PCV

PI

PM

PSI

PSIG

PT

QA

QC

RAI

RCS

RHR

RG

RO

RPS

RSS

RWP

RWST

SCFM

SER

SG

SI

SNSOC

sov

SPDS

SRO

SW

TAVG

TI

TS

TSC

UFSAR

URI

UV

vs

18

MECHANICAL EQUIPMENT ROOM 3

MOTOR OPERATED VALVE

MAIN CONTROL ROOM

MODERATOR TEMPERATURE COEFFICIENT

NON-CITED VIOLATION

NUCLEAR REGULATORY COMMISSION

NUCLEAR REACTOR REGULATION

OPERATING PROCEDURE

OUTSIDE RECIRCULATION SPRAY

PERCENT MILLI RHO

PNEUMATIC CONTROL VALVE

PRESSURE INDICATOR

PREVENTATIVE MAINTENANCE

POUNDS PER SQUARE INCH

POUNDS PER SQUARE INCH GAUGE

PERIODIC TEST

QUALITY ASSURANCE

QUALITY CONTROL

RESIDENT ACTION ITEM

REACTOR COOLANT SYSTEM

RESIDUAL HEAT REMOVAL

REGULATORY GUIDES

REACTOR OPERATOR

REACTOR PROTECTION SYSTEM

RECIRCULATION SPRAY SYSTEM

RADIATION WORK PERMIT

REFUELING WATER STORAGE TANK

STANDARD CUBIC FEET PER MINUTE

SAFETY EVALUATION REPORT

STEAM GENERATOR

SAFETY INJECTION

. STATION NUCLEAR SAFETY AND OPERATING COMMITTEE

SOLENOID OPERATED VALVE

SAFETY PARAMETER DISPLAY SYSTEM

SENIOR REACTOR OPERATOR

SERVICE WATER

AVERAGE TEMPERATURE OF RCS

TEMPORARY INSTRUCTION

TECHNICAL SPECIFICATIONS

TECHNICAL SUPPORT CENTER

UPDATED FINAL SAFETY ANALYSIS REPORT

UNRESOLVED ITEM

UNDER VOLTAGE

VENTILATION SYSTEM