ML18101A827

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Insp Repts 50-272/95-10 & 50-311/95-10 on 950507-0623.No Violations Noted.Major Areas Inspected:Operations, Radiological Controls,Maint,Surveillances,Security, Engineering,Techincal Support,Safety Assessment & Qv
ML18101A827
Person / Time
Site: Salem  
Issue date: 07/13/1995
From: Jason White
NRC OFFICE OF INSPECTION & ENFORCEMENT (IE REGION I)
To:
Shared Package
ML18101A825 List:
References
50-272-95-10, 50-311-95-10, NUDOCS 9507210061
Download: ML18101A827 (21)


See also: IR 05000272/1995010

Text

Report Nos.

License Nos.

Licensee:

Facility:

Dates:

Inspectors:

Approved:

U. S. NUCLEAR REGULATORY COMMISSION

REGION I

50-272/95-10

50-311/95-10

DPR-70

DPR-75

Public Service Electric and Gas Company

P~o. Box 236

Hancocks Bridge, New Jersey 08038

Salem Nuclear Generating Station

May 7, 1995 - June 23, 1995

C. S. Marschall, Senior Resident Inspector

J. G. Schoppy, Resident Inspector

T. H. Fish, Resident Inspector

K. S. Kolaczyk, Operations

neer

L. L. Scholl, Reactor Ery_g;: eer

A. E. Finkel

eni or

act

gi

Inspection Summary*

. ;:;"-

~

This inspection report documents inspections to assure public health and

safety during day and back shift hours of station activities, including:

operations, radiological controls, maintenance, surveillances, security,

engineering, technical support, safety assessment and quality verification.

The Executive Summary delineates the inspection findings and conclusions .

9507210061 950714

PDR

ADOCK 05000272

nnn

EXECUTIVE SUMMARY

Salem Inspection Reports 50-272/95-10; 50-311/95-10

May 7, 1995 - June 23, 1995

OPERATIONS

{Module 71707)

Based on preliminary assessment, operators

responded effectively to a Salem Unit 2 trip on June 7.

Operators failed to

fully consider the implications and the risk associated with their actions to

render an enti.re service water bay inoperable, instead of just removing

control power from the affected component. Operators appropriately assessed

emergency diesel generator (EDG) operability after operation with essentially

no fuel to one of the EDG cylinders.

-1*

Ineffective corrective action in response to failures of Residual Heat Removal

(RHR) pump minimum recirculation flow valves resulted in operation of Salem

Unit 2 from February 9, 1995 until June 7, 1995 with both trains of RHR

inoperable.

In addition, when plant staff recognized the degraded conditions

on June 6, they performed an incomplete and incorrect operability

determination for the valve associated with the no. 22 RHR pump.

The

incorrect operability determination, endorsed by the plant management

personnel, demonstrated weaknesses in the plant staff's ability to perform

operability determinations .

The plant staff did not identify that the December 1994 failure of a supply

fan for safety-related switchgear placed Salem Unit 1 at variance with

conditions stated in the Updated Final Safety Analysis Report (UFSAR).

Further, when a second switchgear supply fan failed on May 12, 1995, plant

staff did not recognize that they operated the plant in an unanalyzed

condition.

As a result, the safety related switchgear could have failed under

design basis accident conditions. Plant staff did not take the appropriate

action to shut the plant down until May 16, 1995.

MAINTENANCE/SURVEILLANCE

(Modules 61726, 62703)

Plant staff responded

appropriately to Hagan module fuse configuration issues and implemented a

comprehensive Hagan module fuse inspection program.

Technician inattention to

detail contributed to Maintenance returning IC EDG to service with a cylinder

fuel pump inadvertently left out of service. Operations failure to ensure the

fuel system was reset, as required by procedure, resulted in reduced emergency

diesel generator reliability. Despite extensive troubleshooting and

installation of a modification, maintenance staff continued to experience

recurrent problems due to a safeguard equipment control auto test fault.

Plant staff did not determine the cause, take ade~uate corrective action, or

preclude recurrence of three leak rate test failures for the Salem Unit 1

outer airlock door.

The plant staff initiated an Incident Report after the

third failure, in response to questions by the inspector, and discovered that

the airlock gasket was deformed, not merely dirty as had been supposed by the

organization due to inadequate root cause performance.

i i

ENGINEERING (Module 71707)

Based on their identified probable cause, system

engineering correctly evaluated the effect of mis-operation of the output

breaker on EOG operability. However, they did not rigorously investigate and

evaluate other less probable, but more safety consequential causes of the

diesel generator output breaker failure.

Design engineering installed new design high-speed circulating water traveling

screen motors without detecting an inherent design problem.

Consequently, an

operator work-around was devised relative to the manual operation of the

screen in lieu of designed automatic operation.

The action challenged the

licensee's ability to affect event-free operation.

In addition, design

engineering failed to adequately analyze and evaluate the recurring motor

failures prior to returning them to automatic operation.

Engineering thoroughly assessed the consequences of operating IC EOG with

essentially no fuel to one cylinder and provided operations a reasonable basis

for declaring the emergency diesel generator operable.

Engineering's auxiliary feedwater pump cavitation calculations were found to

be technically adequate.

The licensee appropriately identified the cause for installing incorrect

internals in the Salem Unit 2 PORVs, and took appropriate corrective action.

PLANT SUPPORT (Module 71707) The Radiation Protection staff took comprehensive

measures to prevent the recurrence of the problems involving entry into high

radiation areas.

SELF ASSESSMENT/QUALITY VERIFICATION (Module 71707)

In 1992, the licensee

identified cyclic impact noises coming from an RHR pump discharge valve.

Although they took some corrective actions in 1993, they did not determine the

cause or thoroughly evaluate the potential effects on the operability of the

valve and its affect on the RHR system.

In response to inspector concerns on

this matter, the licensee performed an acceptable operability determination

that provided reasonable assurance of the valve's ability to function and

committed to inspect the valve to confirm the conclusion during the current

outage.

Notwithstanding, the inspector determined that, in 1992, the licensee

failed to take timely and appropriate corrective action in response to

identification of the degraded condition.

Engineering conducted an acceptable root cause determination for recurrent

jacket water instrument line leakage that affected one or more of the

emergency diesel generators.

In view of several similar failures that

occurred since February 1992, the inspector determined that the licensee

previously failed to determine root cause and effect lasting corrective

action.

i i i

TABLE OF CONTENTS

EXECUTIVE SUMMARY .

TABLE OF CONTENTS .

I.O

SUMMARY OF OPERATIONS .

2.0

3.0

4.0

OPERATIONS

. . . . . . . . . . . . . . . . . . . . . . . . .

2.I

Operator Response to the Salem Unit 2 Trip

...... .

2.2

Service Water Operability

........ .

2.3

Operation of IC EDG with a Latched Fuel Pump Rack ..

2.4

Inoperable Salem Unit 2 Residual Heat Removal (RHR) pumps

2.5

Salem Unit I Degraded Switchgear Ventilation System

MAINTENANCE AND SURVEILLANCE

. . . . . . . . . . .

3.I

MAINTENANCE . . . . . . . . . . . . . . . . . . .

. ....

3.2

Hagan Module Fuses .............. .

3.3

Emergency Diesel Generator (EDG) Maintenance .. .

3.4

Safeguard Equipment Control (SEC) Troubleshooting .... .

3.5

SURVEILLANCE ..................... .

3.6

Inadequate Corrective Action of Salem Containment Airlock

ENGINEERING . . . . . . . . . . . . . . .

o

4.I

Emergency Diesel Generator Output Breaker .....

4.2

Circulating Water (CW) Traveling Screen Motors ..

4.3

Operation of IC EDG with a Latched Fuel Pump Rack

4.4

Auxiliary Feed Pump Cavitation . . . .

. ...... .

5.0

PLANT SUPPORT ............. .

5.I

Radiological Controls ....... .

i i

iv

I

I

I

2

3

3

5

7

7

7

8

9

9

IO

IO

IO

11

I2

I2

I4

I4

6.0

Self Assessment and Quality Verification . . . . . . . . . . .

14

6.1

Historical Problem Identification and Resolution at Salem

14

7.0

REVIEW OF REPORTS AND OPEN ITEMS

7.1

Licensee Event Reports

8.0

EXIT INTERVIEWS/MEETINGS ... .

8.I

Resident Exit Meeting ....... .

8.2

Specialist Entrance and Exit Meetings

8.3

Salem Management Changes ..... .

iv

I6

I6

I7

I7

I7

I7

-

DETAILS

1.0

SUMMARY OF OPERATIONS

Unit 1 began the period operating at 48% power to support modifications to the

steam generator feed pumps.

Operators began raising power on May 14, 1995.

On May 16, with the unit at 95% power, operators entered Technical

Specification 3.0.3 and began a plant shutdown, due to inoperable switchgear

ventilation supply fans.

The operators put the plant in Mode 5 (Cold

Shutdown) on May 17, where it remained through the end of the reporting

period.

Unit 2 began the period at 100% power.

On May 7, 1995, operators reduced

power to 88% due to the loss of moisture separator reheater drain tank level

indications.

On May 8, with the no. 238 circulating water pump out of service

for maintenance, operators reduced power to 78% due to high temperatures in

the no. 23A circulating water traveling screen motor.

On May 11, operators

increased power to 90%.

Maintenance on the no. 21 heater drain pump and

level swings in no. 2B heater drain tank level prevented a further power

increase until May 15, when operators returned Unit 2 to 100% power.

On

May 25, operators reduced power to 88% due to circulating water pump

unavailability and anticipated loss of an additional circulating water pump.

On May 30, operators returned Unit 2 to 100% power.

On June 3, operators

reduced power to 90% due to an extended outage of no. 238 circulating water

pump and unreliability of circulating water traveling screen motors.

On June

4, operators returned Unit 2 to 100% power.

On June 7, Unit 2 operators

commenced a shutdown required by Technical Specification 3.0.3 due to the

inoperability of both trains of residual heat removal (RHR).

During the shutdown, Unit 2 experienced an automatic reactor trip from 10%

power due to a 500 kV breaker failure and subsequent loss of two of the four

operating reactor coolant pumps.

On June 8, operators placed Unit 2 in mode 5

and maintained it in that condition for the remainder of the inspection

period.

2.0

OPERATIONS

The inspectors evaluated PSE&G's management control by direct observation of

activities, tours of the facilities, interviews and discussions with

personnel, independent verification of safety system status and Technical

Specification compliance, and review of facility records. The inspectors

performed normal and back-shift inspections, including 7 hours8.101852e-5 days <br />0.00194 hours <br />1.157407e-5 weeks <br />2.6635e-6 months <br /> of deep back-

shift inspections.

2.1

Operator Response to the Salem Unit 2 Trip

Based on preliminary assessment, operators responded effectively to a Salem

Unit 2 trip on June 7. *

On June 7, during a Salem Unit 2 shut down required by Technical Specification 3.0.3, a reactor trip resulted from spurious protective relay actuation on the

500 kV ring bus.

With the plant at 10 percent power, the protective relaying

caused loss of the 4160 volt buses supplying power to the nos. 23 and 24

- ..

2

reactor coolant pumps.

As a result, the reactor tripped, from low reactor

coolant system flow with reactor power greater than or equal to 10 percent.

The protective relaying also caused loss of power to other plant equipment

including the control air compressors.

The vital bus transfer to its

alternate source of offsite power occurred successfully, and the emergency air

compressors started and restored air pressure. All plant equipment functioned

as designed in response to the existing conditions.

The inspectors concluded

that the operators responded appropriately to the trip. Salem management

convened a Significant Event Response Team (SERT) to review operator action

and plant response to the trip. The SERT had not completed its review at the

conclusion of the inspection period. The inspectors will review the completed

SERT findings when they become available, as a matter of routine NRC

inspection activities.

2.2

Service Water Operability.

The inspector noted that operators unnecessarily rendered a service water bay

inoperable while waiting for post-maintenance testing of a service water pump.

Operators failed to fully consider the increased risk of unnecessarily

maintaining a service water bay inoperable, instead of merely removing control

po.wer from the affected service water pump breaker.

At 04:51 a.m. on May 26, 1995, operators restored 125 VDC control power to the

no. 25. service water (SW) pump breaker while waiting for a post-maintenance

test on the SW pump.

At the time, the operators considered the no. 25 SW pump

inoperable but available.

The operators recognized that the restoration of

control power to the pump would set-up a condition that would cause the no. 2C

safeguard equipment control (SEC) system to attempt to start the no. 25 SW

pump in the event of a loss of offsite power (LOP); and that if the no. 25 SW

pump breaker failed to close, the 2C SEC would attempt to start the 26 SW

pump, in accordance with design.

The inspector noted that if the operators had not restored control power to

the no. 25 SW pump, 2C SEC would have started the operable no. 26 SW pump,

directly in response to a LOP.

However, as a result of making the no. 25 SW

pump available with restored control power, an SEC actuation under accident

conditions could result in 2C SEC closing the no. 25 SW pump breaker before

the pump was demonstrated as operable by post-maintenance testing.

In such

condition, the pump may not have been able to perform its intended function.

In such case, the potential existed for not having any pumps in the affected

SW bay that would start in response to a LOP.

When this matter was brought to the attention of the operating personnel, the

operators reacted initially by considering the SW bay inoperable and

appropriately entering Technical Specification 3.7.4. while continuing to wait

for the performance of a post-maintenance test that was planned for the next

shift.

The next morning, the inspector questioned the advisability of the operators

rendering the entire SW bay ino~erable while waiting for a post-maintenance

test for a single pump.

The Operations Manager concluded that the decision to

render the entire SW bay inoperable was inappropriate and unnecessary.

.(

3

Subsequently, the operations manager took prompt action to ensure the

operating shift removed breaker control power for the affected SW pump until

maintenance was prepared to perform the post-maintenance test.

The inspector determined that the operators failure to consider the

implications of their approach a contributor to the potential for rendering a

portion of SW unable to respond to a LOP; and demonstrated a weakness in

understanding and assessing aggregate risk.

2.3

Operation of lC EDG with a Latched Fuel Pump Rack

Operators appropriately considered the emergency diesel generator (EOG)

inoperable after operation with essentially no fuel to one of the EOG

cylinders. Later,-they appropriately declared the EOG operable after review

of information provided by system engineering.

On June 15, during a surveillance of IC EOG, operators identified abnormally

low no. 4R cylinder exhaust temperature (165 °F).

Normal cylinder exhaust

temperatures for a loaded EOG range from 860 to 960 °F.

Subsequently, a

maintenance supervisor found the 4R cylinder fuel pump latched, essentially

eliminating fuel flow to the 4R cylinder.

The supervisor unlatched the fuel

pump, returned the cylinder to service, and operators completed the EOG

surveillance run with no apparent degradation in engine performance.

Following the surveillance, the Senior Nuclear Shift Supervisor (SNSS)

declared the EOG inoperable pending engineering evaluation of running the EOG

with no fuel to cylinder 4R.

On June 16, engineering provided operations with

information indicating the EOG had not experienced damage.

The SNSS declared

the EOG operable.

(Sections 3.3 and 4.3 pertain)

2.4

Inoperable Salem Unit 2 Residual Heat Removal (RHR) pumps

Ineffective corrective action in response to failures of Residual Heat Removal

(RHR) pump minimum recirculation flow valves resulted in operation of Salem

Unit 2 from February 9, 1995 until June 7, 1995 with both trains of RHR

inoperable.

In addition, when plant staff recognized the degraded conditions

on June 6, they performed an incomplete and incorrect operability

determination for the valve associated with the no. 22 RHR pump.

The

incorrect operability determination, endorsed by the plant engineering and

operations management, demonstrated fundamental weaknesses in the plant

staff's ability to perform operability determinations.

On January 26, 1995, as operators decreased flow from no. 22 RHR pump into the

reactor vessel, the RHR minimum recirculation flow bypass valve (22HR29)

failed to open.

Operators noted that, as flow decreased, the valve did not

open at 500 gpm, as expected.

At 200 gpm flow, operators manually opened the

motor operated valve (MOV).

In consultation with the system engineer,

operators manually stroked 22RH29 to verify manual operation of the valve.

They initiated a work order stating that the valve failed to open

automatically, but considered the valve operable without any basis.

On

February 9, 1995, the minimum recirculation flow bypass valve (21HR29) also

failed to open automatically in response to a low flow condition. However,

4

since the operators were able to stroke the valve manually, they continued to

considered the component operable without any other basis. Notwithstanding, a

work order to investigate and repair was initiated.

No significant priority

was assigned to the work orders. Consequently, the actions became part of the

licensee's work order backlog even though the work orders described an

operability concern.

On June 6, 1995, during a review of open safety related work orders, plant

staff identified that the work orders for the 21 and 22 RH29 valves identified

unresolved degraded conditions potentially affecting RHR pump operability.

Plant staff noted that for certain loss of coolant accidents (LOCAs) the RHR

pumps would start but would not immediately inject into the reactor coolant

system (RCS) due to elevated system pressure. Those conditions would require

that the 21 and 22 RH29 valves open to assure adequate flow through the RHR

pumps to prevent pump failure due to over-heating or excessive vibration.

With the plant at full power, operators started the nos. 21 and 22 RHR pumps

individually with the RH29 valves closed.

The 22RH29 opened in response to

the low RHR flow; the 21RH29 valve failed to open.

The operators, with

management concurrence, declared the no. 21 RHR pump inoperable.

However,

with no other basis than this single functional test, the operators continued

to consider the no. 22 RHR pump operable.

On June 7, 1995, the inspectors questioned the basis for operability of

22RH29.

In response to the inspector's questions, the General Manager

confirmed that the plant engineering and operations management considered

22RH29 operable based solely the functional test and engineering assurance.

When challenged by the inspector, neither the general manager nor the

engineering or operations staff could provide the basis for this operability

determination.

Follow-up revealed that the plant operations and engineering

managers assumed that the system engineer, in response to the 22RH29 failure

on January 26, 1995, had engineering assurance that permitted him to conclude

that the valve was operable at that time.

On June 7, the managers considered the single functional test as sufficient

reasonable assurance of operability to arbitrarily established a deadline of

5:00 p.m. to supply further basis for a positive operability determination for

22RH29.

However, at 6:27 p.m. on June 7, engineering was unable to provide a

rationale for operability. Subsequently, the operations organization declared

the no. 22 RHR pump inoperable, and commenced a Unit 2 shutdown, as required

by Technical Specification 3.0.3.

In summary, the inspector found that the plant staff did not identify a root

cause for either 22RH29 or 21RH29 functional failures in January and February,

1995. Though operability of the RHR system was recognized as an issue, no

basis for operability was ever established, and no significant priority was

assigned to work efforts to investigate and resolve the matters.

Consequently, the issues remained unresolved until June 7, when the licensee

finally determined that neither valve could be considered operable.

Following

shutdown of Unit 2, the licensee still unable to demonstrate the proper

functioning of the valves, confirming that both trains of the RHR system were

inoperable since January/February 1995, during which time the plant was at

5

full power.

Unit 2 shutdown on June 7, 1995.

Power operation of the Salem

Unit 2 for prolonged periods with both trains of RHR inoperable is an apparent

violation.

2.5

Salem Unit 1 Degraded Switchgear Ventilation System

The plant staff did not identify that the December 1994 failure of a supply

fan for safety related switchgear placed Salem Unit 1 at variance with

conditions stated in the Updated Final Safety Analysis Report (UFSAR).

Further, when a second switchgear supply fan failed on May 12, 1995, plant

staff still failed to recognize that they had operated the plant in an

unanalyzed condition.

The inspector identified that in such condition, the

safety related switchgear could have failed under design basis accident

conditions. Plant staff did not take the appropriate action to shut the plant

down until May 16, 1995.

The UFSAR, section 9.4.6, states that the switchgear ventilation system is

designed for continuous operation to maintain safe levels of temperature and

cleanliness in the 64' and 84' switchgear rooms as well as the 78' lower

electrical penetration and 100' upper electrical penetration rooms.

The

UFSAR, section 9.4.6.2.2 further states that the ventilation system consists,

in part, of three 50 percent capacity fans to supply filtered air through

supply ducts, with two of the three supply fans operating and the third as a

standby.

The switchgear ventilation system supplies cooling to all safety

related 4160V, 460V, and 230V switchgear.

On December 11, 1994, the no. 12 control area switchgear supply fan motor

breaker tripped on overload due to mechanical failure of the motor bearings.

Plant staff wrote work order (WO) 941211094 to investigate and correct the

condition. However, the fan remained unrepaired due to the lack of available

parts (the fan motors were obsolete).

On May 12, 1995, with Salem Unit 1 at power, the no. 13 control area

switchgear supply fan motor tripped on overload.

Plant staff initiated a Work

Order (950512188).

On May 14, 1995, at 7:00 p.m., operators completed an

initial operability determination.

The determination concluded that the

switchgear remained operable based on the expectation that ambient outside air

temperature would remain less than the design assumption of 95°F, that.low

initial temperatures in the affected areas would limit the rate of temperature

rise from the onset of an accident permitting timely restoration of at least

one fan before reaching the design inside air temperature limit of 105°F.

Engineering considered the limit of 105°F to be a long term reliability

concern.

On May 15, 1995, system engineering provided a memorandum to operations

documenting their basis for concluding that the switchgear ventilation

remained operable.

The memorandum stated that the switchgear ventilation was

designed to maintain switchgear ambient air temperature within 65°F - 105°F,

but did not state that the UFSAR indicated that the fans were 50 percent

capacity, that two were assumed to be running, and the third fan was expected

to be available in standby.

The memorandum described the assumption that all

of the Unit 1 exhaust fans were available when, in fact, one of six was out of

6

service due to parts problems.

System engineering also assumed that a fan

could be restored within 72 hours8.333333e-4 days <br />0.02 hours <br />1.190476e-4 weeks <br />2.7396e-5 months <br />, even though some of the components were

obsolete.

For compensatory measures, engineering advised operations to rely

on the Unit 2 switchgear exhaust fans, and proposed that the fire doors

between Unit 1 and Unit 2 switchgear rooms be propped open to allow Unit 2 to

serve as a source of outside air for Unit 1.

The memorandum did not address

the affect of reduced ventilation on Unit 2, or evaluate the condition

relative to fire protection requirements and the existing Appendix R analyses.

To accommodate this proposal, engineering's memorandum suggested that

operations disable the C02 automatic function for the 84' switchgear rooms.

The memorandum further stated that the ambient switchgear temperatures were

acceptable assuming that the ambient temperatur~ did not exceed 80°F.

Operations received the memorandum on the evening of May 15.

In the morning

on May 16, the assistant operations manager noted that the predicted high

ambient temperature for the day was expected to exceed 80°F.

Subsequently,

the operations organization rejected engineering's proposal as unacceptable.

Design engineering began a 10CFR50.59 evaluation to determine if the

switchgear could be accepted as meeting the design basis cooling assumptions

in its present condition. Later in the afternoon of May 16, design

engineering informed operations that they had determined that operation with

only one switchgear supply fan constituted an Unreviewed Safety Question .

Subsequently, the design engineering organization initiated a effort to

develop a Justification for Continued Operation (JCO).

The operations

organization set a deadline of 9:00 p.m. on May 16, to have the JCO, or to

begin to initiate plant shutdown.

Shortly after 9:00 p.m. on May 16,

operations initiated a plant shutdown after it became evident that the

engineering organization would not be able to prepare a JCO on schedule.

At 11:10 p.m., design engineering completed the JCO.

It relied on use of

Unit 2 switchgear ventilation supply fans, specified daytime temperatures to

be less than or equal to 80°F and nighttime temperatures to be less than or

equal to 60°F.

The JCO was based on the proposition that the fire doors

between Units 1 and 2 would be blocked open, and that the automatic operation

of the C02 fire suppression system would be disengaged.

The JCO concluded

that Unit 1 could be safely shut down with loss of the third switchgear

ventilation supply fan, provided that the ambient air temperature limitations

and the blocked open fire door conditions were met.

The Salem Operations

Review Committee reviewed the JCO and rejected it at approximately 2:30 a.m.

on May 17.

In summary, the licensee's response to the December 11, 1994 failure of the

no. 12 switchgear supply fan failed to evaluate switchgear operability or the

effect on the design basis assumptions (as requir~d by 10CFR50.59).

The plant

staff did not recognize that they did not meet design basis assumptions

specified in the UFSAR.

As a result, they did not promptly obtain repair or

replacement parts for the disabled components.

Further, they did not

recognize that the design basis assumption of 95°F ambient air temperature

assumed that there were at least two operating supply fans.

The engineering

analysis to support operability relied on Unit 2 equipment for operability of

Unit 1 systems, yet assumed that Unit 2 would be unaffected by a loss of

offsite power affecting Unit 1, even though the last two switchyard problems

7

that perturbed offsite power affected the vital buses for both units. System

engineering's memorandum to the operations organization failed to specify and

an engineering basis for concluding that Unit 2 ventilation would provide

adequate motive force for both units. Also, the memorandum failed to provide

an evaluation of the affect of propping fire doors open and disabling

automatic functions of C02 systems.

Additionally, when design engineering concluded that operation with a single

supply fan constituted an unreviewed safety question, Salem management failed

to recognize that they could not support continued plant operation, since

design engineering had clearly told them that they were operating the plant

outside of the design basis. Although it could have been more timely,

operations finally took control, established a deadline, and acted in the

absence of engineering support of switchgear operability. Engineering's

rationale as documented in their memorandum to operations and in the proposed

JCO was dubious and based on invalid assumptions.

The SORC appropriately

rejected the JCO, however, plant management's judgement to consider a JCO,

after being informed that the design basis assumptions could not be met, is

questionable.

3.0

MAINTENANCE AND SURVEILLANCE

3.1

MAINTENANCE

The inspectors observed portions of the following safety-related maintenance

to determine if the licensee conducted the activities in accordance with

approved procedures, Technical Specifications, and appropriate industrial

codes and standards.

The inspector observed portions of the following activities:

Work Order(WO) or Design

!ln.i1

Change Package CDCP)

Description

Salem 1

WO 991027004

RCP Seal Inspection

Salem 1&2

WO 950524250

Hagan Module Fuse Inspection

Salem 1

WO 95012247

Emergency Diesel Generator no.

IC periodic maintenance

The inspectors observed that the plant staff performed the maintenance

effectively within the requirements of the station maintenance program.

3.2

Hagan Module Fuses

Plant staff responded appropriately to Hagan module fuse configuration issues

and implemented a comprehensive Hagan module fuse inspection program.

Between May 20 and May 21, 1995, Unit 1 Instrument and Controls technicians

identified at least six incorrect fuses installed in Hagan modules.

The

modules, used in safety-related and non-safety related applications, provide a

8

I20 VAC output that energizes or de-energizes downstream relays. The fuses.

protect the signal input to the Hagan modules, the power supplies, and the -

output to the relays.

The licensee identified two fuse misapplications: I) incorrect voltage ratings

(installed 32 V or I25 V ratings vs. specified 250 V), and 2) incorrect fuse

current ratings (installed .2A vs. specified SA; and installed SA vs.

specified .2A).

On May 23, the licensee initiated a program to inspect all

Hagan module fuses installed in both Salem units. The inspection placed

priority on safety-related systems, but included non-safety related systems.

At the end of the inspection period, Unit I technicians completed_ inspection

of approximately 350 of II39 fuses, with approximately IO percent of the fuses

found to be incorrect. Unit 2 technicians completed inspection of

approximately 440 of II33 fuses, with approximately 5 percent of the fuses

found to be incorrect.

Salem management expected to complete inspections of safety-related systems by

the end of July. They had not yet determined the completion date for

inspections of the remaining non-safety system modules.

NRC inspectors will

continue to follow-up on the licensee's resolution of this configuration

control problem.

3.3

Emergency Diesel Generator (EOG) Maintenance

Technician inattention to detail contributed to Maintenance returning IC EOG

to service with a cylinder fuel pump inadvertently left out of service. The

inspector also discovered that operations failed to insure the emergency

diesel generator fuel rack linkage had been properly repositioned following a

surveillance. Although this did not render the diesel inoperable, it reduced

reliability of the emergency diesel generator.

Both matters represent

examples of failure to follow procedures.

As described in Section 2.3, maintenance technicians inadvertently left

cylinder 4R fuel pump latched after completing compression checks on IC EOG.

The licensee determined that technicians failed to comply with the procedure

SC.MO-ST.OG-0003, Eighteen Month Diesel Engine Inspection Maintenance, step

5.I5.8.G, which requires the technicians to unlatch the fuel pump rack and

allow the rack to return to its normal position following compression pressure

checks on the cylinder.

The inspectors concluded technician inattention to detail contributed to the

fuel pump rack being left latched, and resulted in operators running the EOG

without fuel to the cylinder.

Failure to correctly implement the maintenance

procedure is an example of failure to follow procedures.

At 5:55 a.m. on May I6, I995, operations declared the 2C emergency diesel

generator (EOG) operable after completing a surveillance. At approximately

IO:OO a.m. on May I6, the inspector discovered the 2C EOG fuel rack linkage

was not in the open position. The shift supervisor appropriately restored the

fuel rack linkage to the correct position.

In addition, operations ensured

that the fuel rack was properly lubricated and functional.

9

The licensee determined that an equipment operator's failure to follow

procedural requirements for EOG restoration was the root cause. Step 5.3.45

of S2.0P-ST.DG-0003, 2C Diesel Generator Surveillance Test, required EOG

restoration in accordance with Attachment 6. Attachment 6 to S2.0P-ST.DG-0003

required positioning of the fuel rack linkage to the open position.

Engineering determined that the incorrectly positioned fuel rack did not

affect emergency diesel generator operability since hydraulic pressure would

be expected to automatically open the fuel racks during the starting sequence.

The inspector verified that operations successfully tested the automatic

feature on December 4, 1994, during S2.0P-ST.DG-0021, 2C Diesel Generator Hot

Restart Test.

The inspector concluded that Attachment 6 to procedure S2.0P-

ST.DG-0003 provided a redundant means to assure open fuel racks prior to

diesel starts. The licensee's failure to adhere to S2.0P-ST.DG-0003 step

5.3.45 and procedure SC.MD-ST.DG-0003 step 5.15.8.G, as discussed above,

constitutes an apparent violation of Technical Specification 6.8.1.

(VIO 50-272&311/95-10-02)

3.4

Safeguard Equipment Control (SEC) Troubleshooting

Despite extensive troubleshooting and installation of a modification, the

maintenance organization has been unsuccessful in preventing recurrence of

safeguard equipment control auto test faults.

Previous inspection reports (NRC Inspection Reports 50-272&311/94-31,

50-272&311/94-35, and 50-272&311/95-02) documented recurring problems with

Unit 1 SEC power supplies, particularly frequent Automatic Test Insertion

(ATI) test faults and spurious alarms.

To address the problems, the licensee

installed modified SEC power supplies on May 22 and made improvements to

reduce electromagnetic interference.

The licensee also planned modifications

to the ATI card to reduce sensitivity to noise.

On June 13 and June 20, the IA SEC again experienced ATI test faults.

Initial

analysis indicated that the new power supplies had degraded.

At the end of

the inspection period, the licensee continued to troubleshoot the power

supplies.

3.5

SURVEILLANCE

The inspectors performed detailed technical procedure reviews, observed

surveillances, and reviewed completed surveillance packages. The inspectors

verified that plant staff performed surveillance tests in accordance with

approved procedures, Technical Specifications and NRC regulations.

The inspector reviewed the following surveillances:

Unit

Salem 1

Salem 2

Salem 2

Procedure no.

Sl.RE-ST.ZZ-0002

S2.0P-ST.RC-0008

S2.IC-FT.RCP-0068

10

Test

Shutdown Margin Calculation

' Reactor Coolant System Water Inventory

Balance

Containment Pressure Protection Channel 2

The inspectors observed that plant staff did the surveillances safely, and

that the tests were effective in confirming operability of the associated

systems.

3.6

Inadequate Corrective Action of Salem Containment Airlock

Plant staff failed to determine the cause, take adequate corrective action, or

otherwise preclude recurrence of three successive leak rate test failures for

the Salem Unit 1 outer airlock door.

Although plant staff initiated an

Incident Report after the third failure, in response to questions by the

inspector the plant staff discovered that the airlock gasket was deformed as

opposed to their initial presumption that dirt in the seal area was the cause

of the recurrent test failures .

On March 6, 1995, the Salem Unit 1 100 foot elevation outer airlock door

failed a routine leak rate test. Plant staff cleaned the gasket with Maselin

(oil impregnated) cloth and satisfactorily completed the retest. They

concluded that dirt on the gasket had caused excessive leakage during the

first test.

On May 3, 1995, the outer airlock door again failed a routine

surveillance. Plant staff again cleaned the gasket, and satisfactorily

retested the door.

On May 8, 1995, the door again failed surveillance, and

plant staff again cleaned the gasket with a Maselin cloth, and satisfactorily

retested the door.

Though the plant staff wrote an Incident Report, they considered the airlock

door operable for purposes of containment integrity.

The inspectors

questioned the adequacy of the corrective action, the basis for operability,

and the licensee's ability to preclude recurrence.

In response,

the licensee

thoroughly inspected the gaskets, and found one of the two gaskets

sufficiently deformed to cause the excessive leakage.

The licensee replaced

the damaged gasket and successfully retested the door.

The inspectors concluded that the licensee had not adequately determined the

cause of the airlock failure on March 6, May 3, and May 8, 1995, with the

result that they took inadequate corrective action in each instance.

4.0

ENGINEERING

4.1

Emergency Diesel Generator Output Breaker

System engineering performed a thorough operability evaluation based on their

identified most probable cause of recurring unsuccessful diesel generator

output breaker operation. However, the inspector determined that engineering

11

did not rigorously investigate other potential causes that were factors in, or

contributed to, a previous similar diesel generator breaker failure, and other

related breaker failure events. The inspector noted that engineering readily

dismissed other possible causes with more safety consequence.

On June 2, 1995, the 4KV emergency diesel generator (EOG) output breaker

failed to close on the first attempt while performing Sl.OP-ST.DG-0002, 18

Diesel Generator Surveillance Test.

The licensee experienced similar failures

on May 15, 1995, and March 1, 1995, on the lC EOG and the 2A EOG respectively.

In all cases, the breaker closed on the second attempt.

In each case, the

licensee attributed the failures to the Qperator improperly timing the attempt

to close the 4KV breaker.

Engineering concluded that the operators must not

have satisfied the synchronization permissive required to effect breaker

closure. Operations concluded that the breaker failures, that occurred during

diesel paralleling, affected only the test portion of the EOG breaker closing

circuit.

The inspector determined that plant engineering performed a thorough analysis

of the affect on operability of a faulty synchronization permissive circuit.

The inspector also noted that on April 12, 1994, engineering determined that

increased contact resistance in position switch 52HL caused successive breaker

failures on March 29, 1994.

The inspector also found that plant engineering

did not fully consider potential intermittent failures of relays and contacts

in the synchronization permissive circuit and the safeguard equipment control

(SEC) EOG starting circuit. Although they concluded that 52HL caused the

failure in March 1994, engineering did not consider increased 52HL contact

resistance as a cause for the failures in March, May, and June 1995.

In

addition, engineering did not evaluate other failures of similar 4KV breakers.

The licensee previously attributed four previous failures of 4KV breakers to

close on the first attempt to dirty, pitted or misaligned permissive switch

contacts.

The inspector determined that engineering's recommended corrective actions

were appropriate if the cause of the breaker failing to close was confirmed to

be associated with mis-synchronization.

The inspector noted, however, that

the licensee did not specifically confirm synchronization as the cause, nor

investigate other possible causes.

4.2

Circulating Water (CW) Traveling Screen Motors

Design engineering installed new design high-speed circulating water traveling

screen motors that resulted in an operator work-around (i.e., required manual

screen operation) and had the potential to challenge event-free operations.

In addition, design engineering failed to adequately analyze and evaluate the

recurring motor failures prior to returning them to automatic operation.

The licensee installed new CW traveling screen motors designed to operate in

low speed automatic operation, with automatic speed increases (2nd, 3rd, and

4th speeds) in response to increasing traveling screen differential pressures.

Shortly after installation, the licensee observed extremely high CW traveling

screen motor temperatures while operating the motors in low speed automatic

operation.

On May 3 and May 6, motor failures occurred due to overheating.

I2

On May 8, Unit 2 operators reduced reactor power to 78% due to high

temperatures on the no. 23A CW traveling screen motor while the no. 238 CW

pump was out of service for maintenance.

Based on engineering

recommendations, operations placed the screen motors in manual and in 2nd

speed to reduce the potential for overheating.

Engineering determined that poor workmanship and insufficient end-turn winding

insulation caused the motor failures. Engineering had two of the motors

rewound and properly insulated. Prior to making this modification to all new

motors, however, engineering recommended that operations place all motors back

in low speed automatic operation. Engineering based the recommendation on a

grease and bearing evaluation and on motor desi~n specifications. Despite the

failures experienced, engineering determined that the motors should have

performed as designed.

On May I7, operators placed all the traveling screen

motors in low speed automatic operation.

On May 25, operators reduced power

to 88% due to an overheating failure of no. 23A traveling screen motor and

anticipated loss of additional motors due to overheat. Subsequently,

operations returned the motors to 2nd speed manual operation.

4.3

Operation of lC EDG with a Latched Fuel Pump Rack

Engineering thoroughly assessed the consequences of operating IC EDG with

essentially no fuel to one cylinder and provided operations a reasonable basis

for declaring the emergency diesel generator operable.

System Engineering assessed the impact of running the EDG with the fuel pump

latched (described in Section 2.3 and 3.4). Engineers evaluated torsional

resonance res~lting from one cylinder not firing, and thermal loading on the

I7 operating cylinders and the non-operating cylinder. They discussed these

issues with the EDG vendor, a consulting firm, and three other utilities.

They also reviewed event reports and industry data to identify other examples

of diesel engines running with a cylinder not firing.

Based on the collective

experience of the engine manufacturer, consultants, other utilities, and broad

industry experience, engineering concluded the IC emergency diesel generator

suffered no damage from running with a fuel pump rack latched.

4.4

Auxiliary Feed Pump Cavitation

The inspector reviewed auxiliary feedwater pump cavitation calculations and

found them to be technically adequate.

The licensing basis of the Salem auxiliary feedwater (AFW) system is described

in section I0.4.7.2.I of the Updated Final Safety Analysis Report (UFSAR).

The AFW system serves as a backup for supplying feedwater to the secondary

side of the steam generators at times when the main feedwater system is not

available, thereby maintaining the heat removal capabilities of the steam

generators.

Each unit is equipped with one turbine-driven and two motor-

driven auxiliary feed pumps.

Steam for the turbine driven pump is taken from

two of the four steam lines upstream of the steam generator stop valves.

The

motor-driven pumps receive power from the 4I60 volt Class IE vital buses.

The

system provides an alternate to the main feedwater system during startup, hot

standby, and also functions as an engineered safeguards system.

In the latter

\\I-

...

13

case, the AFW system is directly relied upon to prevent core damage and

reactor coolant system over pressurization, in the event of transients, such

as loss of feedwater or a secondary system pipe rupture. It also provides a

means for plant cooldown following any plant transient.

The inspector reviewed four auxiliary feedwater cavitation calculations. The

purpose of these calculations was to predict AFW configurations that were

bounded with respect to pump cavitation.

Calculation DOl.6-835, "Limiting Condition for AFW Pump Cavitation Using

Best Estimate Calculations," dated July 27, 1992;

Calculation DOl.6-836, "Best-estimate AFW Pump Cavitation Durinri the

First Ten Minutes of a Split Steam Line Break," dated August 8, 1992;

Calculation S-C-F400-MDC-0225-l, "AFW Flow Rate after Main Steam Line

Break and a Single Active Failure," dated July 10, 1992; and

Calculation lEC-3220, "AFll and AF21 Modification (Trim Replacement),

Package no. l," dated December 15, 1993.

PSE&G 10CFR50.59 Review and Safety Evaluation no. S-O-AF-MSE-0812 dated

September 17, 1992, evaluated the consequences of potential auxiliary

feedwater pump cavitation on Salem's licensing basis by reevaluating the UFSAR

Chapter 15 analyses of steam line break (SLB) and feedwater line break (FWLB)

accidents. The reevaluation (above calculations) conservatively assumed the

turbine driven auxiliary feed pump was not available for mitigation of the SLB

or FWLB events.

Percent cavitation was defined as the percentage reduction in

net positive suction head (NPSH) below that required by the pump during the

design basis event.

The purpose of the safety evaluation was to document that

the postulated worst case of 20% cavitation of one or two auxiliary feed pumps

for 10 minutes or less under postulated SLB and FWLB accident events did not

involve an unreviewed safety question.

The inspectors noted that Byron Jackson Pump Division letter dated August 7,

1992, documented a research test project that was completed by Byron Jackson

in 1967.

The purpose of this test (Byron Jackson Test Curve and Data no. T-

28925-1, dated 21 June 1967) was to determine if extreme cavitation conditions

over a period of time would cause pump seizure, bearing failure, and loss of

pump performance.

The test pump, which was the same model (though a different

size) as Salem's auxiliary feed pump eight-stage DVMX model pump, was selected

to undergo a test program.

The test pump was run for a period of one hour

with 20% cavitation (i.e., available NPSH was equal to 80 percent of what was

required) and there was no appreciable pump noise increase nor bearing

temperature rise. Further, the tested pump resumed its normal performance

after one hour of cavitation.

PSE&G has analyzed 23 postulated cases of main steam line and feedwater line

break accident scenarios. The worst case, a postulated FWLB, has concluded

that one motor-driven auxiliary feed pump and is expected to cavitate 3%

(available NPSH of 97%) at two minutes into the accident, and 19% at the end

of 10 minutes when the faulted loop was isolated by the operator.



Y-

14

Simultaneously, the turbine driven auxiliary feed pump is expected to cavitate

in the range of 4-16% from six minutes into the accident until the faulted

loop is isolated.

In above scenario, both pumps were postulated to cavitate

less than 20% for less than ten minutes.

Based on the Byron Jackson research

pump test, PSE&G concluded that the Salem auxiliary feed pump performance,

with less than 20% cavitation for less than 10 minutes, would not affect pump

performance. Therefore, PSE&G concluded that these conditions were acceptable

and do not involve an unreviewed safety question.

5.0

PLANT SUPPORT

5.1

Radiological ~ontrols

In response to previously identified problems with control of entry into high

radiation areas, the radiation protection (RP) staff made significant changes

to the process for entry into the radiologically controlled area (RCA).

The

changes included positive measures to insure that RP technicians inform each

person entering the RCA of the radiologically conditions in the specific areas

entered by the workers.

The RP staff also revised the Radiation Work Permits

to require that each radiation worker read and sign a summary of the problems

with control of entry into the high.radiation areas.

The inspectors concluded

that the RP staff took comprehensive measures to prevent recurrence of the

problems with entry into high radiation areas.

6.0

Self Assessment and Quality Verification

6.1

Historical Problem Identification and Resolution at Salem

A.

In 1992, the licensee identified cyclic impact noises coming from a

Residual Heat Removal (RHR) pump discharge valve. Although they took

some corrective actions in 1993, they did not determine the cause or

thoroughly evaluate the potential effects on the operability of the

valve and the RHR system until the problem resurfaced in 1995.

The

inspector identified a loss of RHR capability scenario that the licensee

had not considered.

In response, the licensee performed an acceptable

operability determination and committed to thoroughly inspect the

suspect valves during the current outage.

The inspector also determined

that Salem plant staff performed an acceptable operability determination

in response to a lB Emergency Diesel Generator (EOG) jacket water leak

on June 1, 1995.

However, the licensee did not adequately address

previous similar failures that had occurred since February 1992.

Although Salem staff recently took appropriate corrective action, these

two recurring problems demonstrate that previous inadequacies in root-

cause and corrective action determination sontinue to impact current

plant operations.

On July 11, 1992, Engineering identified a loud clanking noise internal

to 21RH10, the no. 21 residual heat removal pump discharge gate valve.

On April 16, 1993, maintenance performed an internal valve inspection

for wear and deterioration. Maintenance found two deep wear marks in

the downstream seat of the double-disk wedge gate valve.

Engineering

determined that the defects did not interfere with the valve function

  • '

15

and were not within the "blue-dye" region that d~fines the seating

surface. Maintenance polished the valve seat and operations considered

the valve operable.

The licensee did not perform an operability

determination, root cause evaluation, or thorough potential failure

analysis.

On June 10, 1995, operations identified that 21RH10 made a loud noise

internally and that plant staff identified the same problem in 1992.

Operations, based on discussion with system engineering, determined that

the valve should be opened and inspected, but that the operability of

the no. 21 RHR pump was not effected. Engineering worked to document

the basis for the operability determination.

On June 11, the inspector

questioned the licensee's initial operability determination and

postulated a potential failure modes of the 21RH10 valve, i.e.,

detachment of the valve disk from the stem such that it impedes or

prevents RHR flow through the valve.

The inspector identified that the

licensee's plan to take the no. 22 RHR pump out of service to work on

the 22RH29 valve, coupled with the postulated failure of 21RH10, could

result in a complete loss of all RHR capability.

On June 16, 1995, system engineering and maintenance met with inspectors

to discuss RHlO operability. They concluded that the RHlO valves for

both trains of RHR remained operable based on a search of industry and

Salem data bases. The search revealed with no identified failures where

the disk actually separated from the stem.

In addition, plant staff

concluded that a fatigue induced separation of the disk from the stem

would require multiple failures at the most susceptible failure points.

Plant management stated that they planned to open and inspect 21RH10 to

evaluate the effect of the banging on the valve internals when plant

conditions permitted taking the no. 21 RHR system out of service. The

inspectors concluded that the plant staff was able to demonstrate a

reasonable basis for RHIO operability in this case, based on equipment

history and engineering judgement of the reliability of the valve

design.

The inspectors noted, however, that plant staff did not adequately

determine the root cause of the clanging and evaluate the effect on

operability in 1992 when first identified.

8.

On June 1, 1995, during a surveillance run of no. 18 EOG, the licensee

identified jacket water leaking from a pressure switch instrument pipe

nipple.

The workers secured the EOG to stop the leak and began

troubleshooting.

Laboratory analysis revealed that the nipple cracked completely through

the threaded area due to fatigue caused by vibration.

The licensee

confirmed this conclusion by performing resonance testing on EOG 18.

The testing found that the pressure switch instrument piping was

susceptible to resonance frequency of 90 cycles per second, a harmonic

of EOG steady state speed of 900 rpm (or 15 cycles per second). Similar

resonance testing on all remaining EOGs, including Unit 2, found EOG lC

also susceptible to resonance frequency vibration.

I6

As an interim measure to eliminate the resonance, engineering proposed

to change the length of the instrument tubing.

Engineering recommended

reorienting the tubing and moving the mounting brackets as permanent

solutions. At the conclusion of the inspection period, the licensee had

implemented the interim measure on EOG IC.

The inspector noted that during troubleshooting efforts the licensee

identified two previous pipe nipple failures that resulted in jacket

water leaks. The IC EOG experienced a jacket water leak in February

I992 and the I8 EOG leaked in December I993.

To address those failures

the licensee replaced the nipple on IC, and re-threaded and reinstalled

the nipple on the I8 EDG.

The inspector concluded the corrective

actions for the I992 nipple failure, since they were not based on any

established root cause, did not prevent recurrence of the degraded

condition for the IC or other EDGs.

The inspectors identified that the licensee's failure to thoroughly evaluate

and resolve the anomalous condition of the RHIO valve and to establish a root

cause of the EDG jacket water leakage problems when these conditions were

first apparent continues to result in potential challenges to safe plant

operation. Accordingly, failure to take adequate corrective actions regarding

the pipe nipple failures and resolution of the RHIO anomalous conditions are

considered as apparent violation of IO CFR 50, Appendix 8, Criterion XVI,

Corrective Action.

7.0

REVIEW OF REPORTS AND OPEN ITEMS

7.1

Licensee Event Reports

The inspectors reviewed the following Licensee Event Report {LER) to confirm

that the licensee took the corrective actions stated in the report, responded

to the event adequately, and met regulatory requirements and commitments:

Salem Unit I

Number

LER 95-007

Event Date

May 5, I995

Description

Emergency Diesel

Generators IA, 18,

and IC Paralleled Concurrently to

Electrical Grid {Assessed in NRC

Inspection Report 50-272&311/95-07)

The inspectors determined that the LER listed above did not identify any

violations beyond those previously identified in NRC Inspection Reports, and

considered the LERs closed.

17

Section 6.2 of this report provides details of inoperable Salem Unit 1

switchgear supply fans from December 12, 1994 until May 16, 1995.

As a result

of the inoperable fans, Salem Unit 1 operated in an unanalyzed condition

during that period.

On May 16, 1995, operators completed a shutdown of Salem

Unit 1 required by Technical Specification 3.0.3. However, the inspectors

confirmed that the licensee did not report the unanalyzed condition or the

shutdown required by Technical Specification 3.0.3 within 30 days as required

by 10 CFR 50.73. This is a violation (VIO 50-272&311/95-10-03)

8.0

EXIT INTERVIEWS/MEETINGS

8.1

Resident Exit Meeting

The inspectors met with Mr. J. Summers and other PSE&G personnel periodically

and at the end of the inspection report period to summarize the scope and

findings of their inspection activities.

Based on NRC Region I review and discussions with PSE&G, the inspectors

determined that this report does not contain information subject to 10 CFR 2

restrictions.

8.2

Specialist Entrance and Exit Meetings

Date(s)

5/11-12/95

Subject

EDS FI Foll owup

Inspection

8.3

Salem Management Changes

Inspection

Report No.

50-272 and 311/95-11

Reporting

Inspector

Cheung

PSE&G appointed Elbert (Bert) Simpson as senior vice president-nuclear

engineering, effective June 30, 1995.

Mr. Simpson will replace Stanley

LaBruna.

Mr. Simpson has served for the past two years as vice president-

nucl ear support for Arizona Public Service Company.

Also, the Nuclear

Licensing and Regulation Department was re-organized under the Quality

Assurance and Nuclear Safety Review organization.