ML18096A637

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Monthly Operating Rept for Mar 1992 for Salem Unit 1.W/ 920413 Ltr
ML18096A637
Person / Time
Site: Salem PSEG icon.png
Issue date: 03/31/1992
From: Shedlock M, Vondra C
Public Service Enterprise Group
To:
NRC OFFICE OF INFORMATION RESOURCES MANAGEMENT (IRM)
References
NUDOCS 9204210185
Download: ML18096A637 (13)


Text

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OPS~G Public Service Electric and Gas Company P.O. Box 236 Hancocks Bridge, New Jersey 08038 Salem Generating Station April 13, 1992 U.S. Nuclear Regulatory Commission Document Control Desk Washington, DC 20555

Dear Sir:

MONTHLY OPERATING REPORT SALEM NO. 1 DOCKET NO. 50-272 In compliance with Section 6.9.l.6, Reporting Requirements for the Salem Technical Specifications, the original copy of the monthly operating reports for the month of March 1992 are being sent to you.

Average Daily Unit Power Level Operating Data Report Unit Shutdowns and Power Reductions Safety Related Maintenance 10CFR50.59 Evaluations Operating Summary Refueling Information

~c~rely yours, RH:pc

~'~ Salem Operations cc: Mr. Thomas T. Martin Regional Administrator USNRC Region I 631 Park Avenue King of Prussia, PA 19046 Enclosures 8-l-7.R4 T~e i=_n~rgy_i:>e_ople 9204210185 920331 .. - -l 8 95*2189 (10M) 12-89 PDR ADOCK 05000272 R PDR

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AVERAGE DAILY UNIT POWER LEVEL Docket No.: 50-272 Unit Name: Salem #1 Date: 04/10/92 Completed by: Mark Shedlock Telephone: 339-2122 Month March 1992 Day Average Daily Power Level Day Average Daily Power Level (MWe-NET) (MWe-NET) 1 1117 17 1116 2 1116 18 1130 3 1120 19 1130 4 1120 20 1118 5 1121 21 1119 6 1119 22 1119 7 1117 23 1123 8 1121 24 1112 9 1112 25 1122 10 1120 26 1116 11 1089 27 1099 12 1125 28 1126 13 1125 29 1126 14 1125 30 1108 15 1119 31 1118 16 1115 P. 8.1-7 Rl

OPERATING DATA REPORT Docket No: 50-272 Date: 04/10/92 Completed by: Mark Shedlock Telephone: 339-2122 Operating Status

1. Unit Name Salem No. 1 Notes
2. Reporting Period March 1992
3. Licensed Thermal Power (MWt) 3411
4. Nameplate Rating (Gross MWe) 1170
5. Design Electrical Rating (Net MWe) 1115
6. Maximum Dependable Capacity(Gross MWe) 1149
7. Maximum Dependable Capacity (Net MWe) 1106
8. If Changes Occur in Capacity Ratings (items 3 through 7) since Last Report, Give Reason NA
9. Power Level to Which Restricted, if any (Net MWe) N/A
10. Reasons for Restrictions, if any NA This Month Year to Date Cumulative
11. Hours in Reporting Period 744 2184 129337
12. No. of Hrs. Rx. was Critical 744 2184 85784.3
13. Reactor Reserve Shutdown Hrs. 0 0 0
14. Hours Generator On-Line 744 2046.1 83094.0
15. Unit Reserve Shutdown Hours 0 0 0
16. Gross Thermal Energy Generated (MWH) 2538681.6 6964245.6 262461390.8
17. Gross Elec. Energy Generated (MWH) 865740 2335270 87139900
18. Net Elec. Energy Gen. (MWH) 831920 2238572 83015145
19. Unit Service Factor 100 93.7 64.2
20. Unit Availability Factor 100 93.7 64.2
21. Unit Capacity Factor (using MDC Net) 101.1 92.7 58.0
22. Unit Capacity Factor (using DER Net) 100.3 91.9 57.6
23. Unit Forced outage Rate 0 6.3 21. 0
24. Shutdowns scheduled over next 6 months (type, date and duration of each)

Refueling outage scheduled to start 4-4-92 and last 73 days.

25. If shutdown at end of Report Period, Estimated Date of Startup:

NA 8-l-7.R2

UNIT SHUTDOWN AND POWER REDUCTIONS REPORT MONTH MARCH 1992 DOCKET NO. 50-272 UNIT NAME Salem #l DATE 04/10/92 COMPLETED BY Mark Shedlock TELEPHONE 339-2122 METHOD OF SHUTTING LICENSE DURATION DOWN EVENT SYSTEM COMPONENT CAUSE AND CORRECTIVE ACTION NO. DATE TYPE 1 (HOURS) REASON 2 REACTOR REPORT # CODE 4 CODE 5 TO PREVENT RECURRENCE 1 2 3 4 5 F: Forced Reason Method: Exhibit G - Instructions Exhibit 1 - Same S: Scheduled A-Equipment Failure (explain) 1-Manual for Preparation of Data Source B-Maintenance or Test 2-Manual scram Entry Sheets for Licensee C-Refueling 3-Automatic Scram Event Report CLER) File D-Requlatory Restriction 4-Continuation of (NUREG-0161)

E-Operator Training & License Examination Previous Outage F-Administrative 5-Load Reduction G-Operational Error (Explain) 9-0ther H-Other (Explain)

e SAFETY RELATED MAINTENANCE e

DOCKET NO: 50-272 MONTH: - MARCH 1992 UNIT NAME: SALEM 1 DATE: APRIL 10, 1992 COMPLETED BY: J. FEST TELEPHONE: (609)339-2904

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WO NO UNIT EQUIPMENT IDENTif ICATION 900615143 1 RADIATION MONITOR 1R12A FAILURE DESCRIPTION: FAULTY CHECK SOURCE - INSPECT &

REPAIR 911104131 1 1C DIESEL GENERATOR FAILURE DESCRIPTION: AIR START REGULATOR VALVE DID NOT FAIL OPEN - INVESTIGATE 920113138 1 RADIATION MONITOR 1R12A FAILURE DESCRIPTION: DETECTOR CONNECTION HAS BARE CONDUCTOR - REPAIR 920129157 1 #15 CONTAINMENT FAN COIL UNIT (CFCU)

FAILURE DESCRIPTION: 14 CFCU WATER HAMMER -

TROUBLESHOOT & REWORK 920228132 1 1C DIESEL GENERATOR FAILURE DESCRIPTION: 1C D/G SUSPECTED CLOG IN STARTING AIR - INVESTIGATE & CORRECT 920317126 1 12 CHARGING PUMP ROOM COOLER FAILURE DESCRIPTION: 12 CHARGING PUMP ROOM COOLER DOES NOT WORK IN AUTOMATIC -

INVESTIGATE 920323134 1 15 SERVICE WATER PUMP FAILURE DESCRIPTION: 15 SW PUMP HIGH VIBRATION -

INVESTIGATE

10CFR50.59 EVALUATIONS e

DOCKET NO: 50-272 MONTH: - MARCH 1992 UNIT NAME: SALEM 1 DATE: APRIL 10, 1992 COMPLETED BY: J. FEST TELEPHONE: (609)339-2904 The following items were evaluated in accordance with the provisions of the Code of Federal Regulations 10CFR50.59. The Station Operations Review Committee has reviewed and concurs with these evaluations.

ITEM

SUMMARY

A. Design Change Packages (DCP}

DCP# lEC-3133 Pkg. 1 "Replacement of Steam Generator Blowdown System Maintenance Isolation Valves (11-14GB3}" - The purpose of this design change is to replace the existing steam generator blowdown system maintenance isolation valves (11-14GB3} with new valves for better reliability. Also, the design package modifies five pipe supports inside the containment and four pipe supports in the mechanical penetration area. (Inside Containment: lC-BDA-43, lC-BDS-34, 35, lC-BDG-123, 124, Outside Containment:

lP-BDA-95, 97, 98, 99}. The replacement valve with a higher pressure rating and the modified support designs provide an improved pressure retaining boundary and the improved design of the new valve minimizes the leakage through the GB3 valves during maintenance of the steam generator blowdown system isolation valves (GB4). This change does not alter the original design intent or the modes of operation or function for which the steam generator blowdown system is currently analyzed. Therefore, the margin of safety basis for the Technical Specification will not be affected.

(SORC 92-033}

DCP# lEC-3145 Pkg. 1 "Installation of Permanent Rigging System for Maintenance of Unit 1" - The purpose of this design change is to install permanent rigging system (lifting lugs and supplemental steel) for maintenance of the Unit 1 Steam Driven Auxiliary Feed Pump and Turbine, which allows removal and transport of the Pump and Turbine components, at EL. 84' - O" of Auxiliary Building of Unit 1.

The enclosure will be modified to provide a removable panel. A bolted panel was chosen, versus a door, to prevent door control problems.

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10CFR50.59 EVALUATIONS e

DOCKET NO: 50-272 MONTH: - MARCH 1992 UNIT NAME: SALEM 1 DATE: APRIL 10, 1992 COMPLETED BY: J. FEST TELEPHONE: (609)339-2904 (Cont'd)

ITEM

SUMMARY

The modified opening in the enclosure wall is being assigned a penetration seal number to ensure the seal will not be breached without engineering review and the establishment of proper compensatory actions. The rigging devices related to the proposed design change and the proposed safe load path do not create the possibility of an accident of a different type than already evaluated in the SAR. A load drop evaluation was performed and concluded that this drop could not cause any accident that is important to plant safety. ( SORC 92-033)

DCP# lEC-3132 Pkg. 1 "Removal of Old and Installation of New NUKON Insulation" - The purpose of this change is to remove existing metallic reflective insulation and install blanket type NUKON insulation with stainless steel jacketing on the pressurizer vessel, vessel top head and loop seal piping enclosures. This DCP will also install blanket type NUKON insulation on the bottom head without jacketing. The loop seal piping enclosures will be removed and replaced with a new structure.

The vessel area covered by loop seal piping enclosure will not be insulated. UFSAR Section 6.3.2.2 discusses the possibility of insulation material being dislodged and blocking the containment sump screens. An ECCS Safety Analysis (CD P-501) for Salem per USNRC Regulatory Guide 1.82, revision 1 was performed considering the NUKON insulation being installed by this DCP. The analysis concludes that the NUKON insulation system will meet the requirements of the Reg. guide when installed in Salem 1 containment. Therefore, the consequences of a malfunction of equipment important to safety will not be increased.

(SORC 92-031)

DCP# lEC-3112 Pkg. 1 "Installation of Monitoring Enhancements" - The purpose of this change is to install monitoring enhancements to provide early warning of loss of Decay Heat Removal (DHR) capabilities. This modification will; 1.) Provide at least two independent continuous RCS level indications whenever the RCS is in a reduced inventory condition, and


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I 10CFR50.59 EVALUATIONS e

DOCKET NO: 50-272 I

I I

I MONTH: - MARCH 1992 UNIT NAME: SALEM 1 I DATE: APRIL 10, 1992 I I

COMPLETED BY: J. FEST I TELEPHONE: (609)339-2904 I (Cont'd)

ITEM

SUMMARY

2.) Provide capability to monitor the residual Heat Removal (RHR) system performance. The parameters identified for this function are: a.)

RHR Pump Discharge Flow; b.) RHR Pump Discharge Pressure; c.) RHR Pump Suction Pressure; d.) RHR Pump Motor Current, and e.) Mid-Loop Operation core exit thermocouple setpoint. The changes are designed to safety related criteria and the functional design and safety criteria of interface systems are unaffected. (SORC 92-031)

DCP# lEC-3099 Pkg. 1 "Replacement of 57 Rosemount Electronic Transmitters" - The purpose of this change is to replace 57 Rosemount electronic transmitters with new transmitters having improved performance under harsh environmental conditions. The transmitters are: 4 Pressurizer Pressure; 3 Pressurizer Level; 12 Steam Generator; 8 Steam Generator Steam Flow; 12 Steam Generator Pressure; 4 Steam Generator Wide Range Level; 12 Reactor Coolant Flow; 2 Reactor Coolant Pressure. The new transmitters are seismically and environmentally qualified for the installed locations. The tubing and valving arrangements will be standardized for all transmitters of the same type. Where space is available, differential pressure transmitters will be equipped with calibration volume chambers. These chambers allow calibration with pneumatic signals without the incursion of air into the transmitters or impulse tubing. The modification also replaces the electronics assemblies on 16 Rosemount transmitters in accumulator level (8) and pressure (8) service.

Each of the 73 transmitters affected by this modification will be equipped with a qualified electrical connector to facilitate maintenance.

There is no change to the instrument process variable spans. The new transmitters are equal to or better than the previous instruments under all conditions. Verification of the P-11 allowable value, consistent with the setpoint calculation, will continue to ensure that manual block of safety injection is defeated well above the SI actuation allowable value of ~ 1755 psi.

There is no impact on the margin of safety as defined in the basis for any Technical Specification. ( SORC 92-036) I I

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10CFR50.59 EVALUATIONS e

DOCKET NO: 50-272 MONTH: - MARCH 1992 UNIT NAME: SALEM 1 DATE: APRIL 10, 1992 COMPLETED BY: J. FEST TELEPHONE: (609)339-2904 (Cont'd)

ITEM.

SUMMARY

DCP# lEC-3113 Pkg. 1 "Replacement of Lambda Power Supplies and Daisy Chain" - The purpose of this change is to replace two obsolete Lambda power supplies with equivalent Lambda power supplies for all five Rod Control Cabinets in Unit 1 and to replace existing daisy chain neutral wiring between the power supplies in a rod control cabinet with individual neutral wires for each power supply.

The rod control circuits which are powered by the new power supplies are not safety related.

The replacement power supplies are equal to or exceed the existing power supplies in all physical and electrical parameters. The separate neutral wiring from each of these power supplies to the neutral bus will minimize inadvertent tripping of the reactor during changes to any individual power supply when the reactor is at full power. (SORC 92-036)

DCP# lSC-2267 Pkg. 1 "Replacement of Control Electronics Unit in Safeguards Equipment Cabinets" - The purpose of this change is to replace the existing Control Electronics Unit (CEU) in Safeguards Equipment Cabinets (SEC). Add a Test Panel to each of the SECs to facilitate monthly functional tests and 18 month timing tests. Add three undervoltage test switches to each of the SEC cabinets so as to eliminate the need for jumpering during surveillance testing of the 4kV vital buses.

Add a diesel generator start pushbutton (E2) to the existing control panel in the SEC cabinets to facilitate testing. Revise the procedure to be consistent with new CEU and Test Panel operation including normal operation without ATI engaged. The reliability of the SEC system is demonstrated by analysis/test results that ensure the modified equipment will withstand the effects of a seismic event. Reliability is further maintained through the use of MIL-Specification material in the construction of the replacement equipment. The replacement CEUs interface with existing input and output relays. No new interfaces are introduced, therefore, the existing redundancy and diversity are maintained. (SORC 92-036)

10CFR-50. 59 EVALUATIONS e

DOCKET NO: 50-272 MONTH: - MARCH 1992 UNIT NAME: SALEM 1 DATE: APRIL 10, 1992 COMPLETED BY: J. FEST TELEPHONE: (609)339-2904 (Cont'd)

ITEM

SUMMARY

DCP# lEC-3143 Pkg. 1 "Permanent Remote Indication of Unit 1 AFP No.

13 Speed and Turbine Inlet Steam Trap" - The purpose of this change is to provide suitable permanent remote (i.e., external to AFP enclosure indication of Unit 1 AFP No. 13 speed and turbine inlet steam trap drain line temperature as well as AFW discharge piping temperature. This will eliminate operations personnel entry into a high noise/humidity environment to obtain Surveillance Procedure mandated (as well as INPO recommended) AFP performance parameter measurements. This proposal will not affect the operability, availability or capacity of 13 AFP or affect the flow path to any Steam Generator as described in Technical Specification 3/4.7.1.2. Therefore, this modification will not reduce the margin of safety as defined in the basis for any Technical Specification. ( SORC 92-036)

DCP# lEA-1028 Pkg. 1 "Reclassify Piping Specification Piping Schedule SPS53D from Nuclear Class III to Non-Nuclear" -

The purpose of this change is to reclassify piping specification Piping Schedule SPS53D from Nuclear Class III to non-Nuclear. Changes are being made to numerous P&IDs piping class classification tables to incorporate the above changes. Additional piping class break clarifications and corrections are being made as well. The other document updates require to incorporate the above changes are UFSAR, S-C-MPOO-MGS 0001-SPS53 and MMIS. Engineering Evaluation S-C-WD-MEE-0692 documents and accepts the above Nuclear classification changes. The margin of safety for the Technical Specifications is not reduced since the piping class 53D that is being reclassified is already non-safety related and not part of the Technical Specification bases. ( SORC 92-0 36)

10CFR50.59 EVALUATIONS MONTH: - MARCH 1992 DOCKET I:

UNIT NAME:

50-272 SALEM 1 DATE: APRIL 10, 1992 COMPLETED BY: J. FEST TELEPHONE: (609)339-2904 (Cont'd)

ITEM

SUMMARY

B. Procedures and Revisions (Proc)

SC.SA-AP.ZZ-0012(Q) "Technical Specification Surveillance Program" Rev. 15 - This proposal involves a revision to SC.SA-AP.ZZ-0012(Q). The matrix (Attachment 1 &

2) is being revised to identify that Nuclear Site Maintenance will share the responsibility for performing surveillance number 4.8.3.1 with the Maintenance Department. Site Services Maintenance (SSM) will be used as a designator for Nuclear Site Maintenance and is being added to the list of department designators. The revision to the procedure does not change any previously analyzed testing requirement nor does it change any testing method, therefore the proposal cannot reduce the margin of safety as defined in the basis for any Technical Specification. (SORC 92-031)

SP-4 "Security Plan Procedure #4" Rev. 2 - The purpose of this procedure is to revise Security Plan Procedure #4 "The Artificial Island Personnel Access. Program" to describe Security Plan implementation of 10CFR73.56 and assign appropriate responsibility for its implementation based on reorganization of the Site Protection Department to include the Site Access Group. This revision of the procedure does not reduce the margin of safety because: 1.) It provides a more effective method of administrative ~ontrol over the PAP and other related Security Plan and FFD Program elements, and 2.) It establishes an approach to granting site access which is consistent with other licensees methods of implementing 10CFR73. Such consistency of approach ensures the temporary workforce is screened to the same standards applied to PSE&G employees, thereby increasing the overall margin of safety. (SORC 92-036)

SALEM GENERATING STATION MONTHLY OPERATING

SUMMARY

- UNIT 1 MARCH 1992 SALEM UNIT NO. 1 The Unit began the period operating at full power, and continued to operate at full power throughout the entire period.

REFUELING INFORMATION e

DOCKET NO: 50-272 MONTH: - MARCH 1992 UNIT NAME: SALEM 1 DATE: APRIL 10, 1992 COMPLETED BY: J. FEST TELEPHONE: (609)339-2904 MONTH MARCH 1992

1. Refueling information has changed from last month:

YES X NO

2. Scheduled date for next refueling: APRIL 4, 1992
3. Scheduled date for restart following refueling: JUNE 16, 1992
4. a) Will Technical Specification changes or other license amendments be required?:

YES NO NOT DETERMINED TO DATE ~x~~

b) Has the reload fuel design been reviewed by the Station Operating Review Committee?:

YES NO x If no, when is it scheduled?:

5. Scheduled date(s) for submitting proposed licensing action:

N/A

6. Important licensing considerations associated with refueling:
7. Number of Fuel Assemblies:
a. Incore 193
b. In Spent Fuel Storage 656
8. Present licensed spent fuel storage capacity: 1170 Future spent fuel storage capacity: 1170
9. Date of last refueling that can be discharged to the spent fuel pool assuming the present licensed capacity: September 2001 8-1-7.R4