ML18094A320

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Insp Repts 50-272/89-01 & 50-311/89-01 on 890131-0320. Violations Noted.Major Areas Inspected:Resident Safety Insp of Operations,Radiological Controls,Surveillance Testing, Maint,Emergency Preparedness,Security & Engineering Support
ML18094A320
Person / Time
Site: Salem  PSEG icon.png
Issue date: 03/29/1989
From: Swetland P
NRC OFFICE OF INSPECTION & ENFORCEMENT (IE REGION I)
To:
Shared Package
ML18094A317 List:
References
50-272-89-01, 50-272-89-1, 50-311-89-01, 50-311-89-1, NUDOCS 8904130148
Download: ML18094A320 (22)


See also: IR 05000272/1989001

Text

Report No.

.License

Licensee:

Facility:

Dates:

Inspectors:

Approved:

U. S. NUCLEAR REGULATORY COMMISSION

REGION I

50-272/89-01

50-311/89-01

DRP-70

DRP-75

Public Service Electric and Gas Company

P. 0. Box 236

Hancocks Bridge, New Jersey 08038

Salem Nuclear Generating Station - Units 1 and 2

January 31, 1989 - March 20, 1989

Kathy Halvey Gibson, Senior Resident Inspector

Noel F. Dudley, Project Engineer

Steve M. Pindale, Resident Inspector

Peter W. Kelley, Resident Inspector

Specialist

P. D. Swetland, Chief, Projects Section 2B

Inspection Summary:

Inspection 50-272/89-01; 311/89-01 on January 31, 1989 - March 20, 1989

Areas Inspected:

Resident safety inspection of the following areas:

operations, radiological controls, surveillance testing, maintenance,

emergency preparedness, security, engineering/technical support, safety

assessment/assurance of quality, and review of licensee event reports.

Results:

Two violations were identified during the report period involving 3

examples of failure to follow procedures which resulted in inadvertent safety

system actuation (paragraph 2) and the failure to correct or prevent

,

recurrence of licensee identified nonconformances with regard to material

control (paragraph 8).

~904130148 890329

PDR

ADOCK 05000272

Q

PDC

1.

DETAILS

SUMMARY OF OPERATIONS

Unit 1 operated at 100% power until February 6, 1989, when the reactor

tripped during performance of a surveillance test.

The unit returned to

power operations on February 8.

On February 15, 1989, a controlled

shutdown was commenced to effect repairs to a component cooling water

leak inside containment.

On February 18, 1989, with the unit critical at

lOE-8 amps, the reactor tripped as a result of an error made during

surveillance testing.

The unit returned to power on February 18, 1989

and remained at full power for the remainder of the inspection period.

Unit 2 operated at 100% power until February 5, 1989, when the reactor

tripped due to loss of both steam generator feedpumps.

The unit returned

to service on February 8.

On March 3, 1989, discretionary enforcement

was granted by the NRC to extend the Technical Specification Action

Statement time limit for containment spray header inoperability for the

licensee to replace a leaking spool piece on No. 21 CS header.

The CS

header was returned to service on March 7, 1989.

On March 12, 1989 a

reactor trip and safety injection ~ccur~ed as a result of the failure of

10 vital instrument bus.

The unit returned to service on March 13, 1989.

2.

OPERATIONS

(71707, 93702)

2.1

Inspection Activities

On a daily basis throughout the report period, the inspectors verified

that the facility was operated safely and in conformance with regulatory

requirements.

Public Service Electric and Gas (PSE&G) Company management

control was evaluated by direct observation of activities, tours of the

facility, interviews and discussions with personnel, independent

verification of safety system status and Limiting Conditions for

Operation, and review of facility records.

These inspection activities

were conducted in accordance with NRC inspection procedure 71707.

The

inspectors performed 334 hours0.00387 days <br />0.0928 hours <br />5.522487e-4 weeks <br />1.27087e-4 months <br /> of normal and backshift inspection

including deep backshift and weekend tours of the facility on February 10

(9:30 p.m.-2:30 a.m.), March 5 (6:30 a.m.-1:30 p.m.), March 12 (9:30

a.m.-10:30 a.m.).

2.2 Inspection Findings and Significant Plant Events

2.2.1

A.

Un-it 1

On February 6, 1989, during performance of a channel functional

test on No. 14 steam generator (SG) steam pressure channel I,

the reactor tripped due to No. 14 SG steam flow - feed flow

mismatch coincident with low SG level. Plant systems responded

to the trip as designed and the unit was stabilized in Mode 3

(hot shutdown).

On February 8, 1989 the unit returned to power

operation.

8.

2

Steam flow for each SG is sensed by two steam flow channels

which are density compensated utilizing the electrical signal

from corresponding steam pressure channels.

Either of the two

compensated steam flow channels for each SG may be selected by

the reactor operator (RO) for input to the SG water level control

circuitry.

In performing the functional test, the I&C technician

engaged the test switch upon which the corresponding steam flow

signal decreased to zero causing the SG water level control

circuitry to respond closing No. 14 SG feedwater control valve

(14BF19) which reduced feedwater flow to No. 14 SG.

The low

feedwater flow resulted in No. 14 SG reaching the low level

setpoint (25%) and the steam flow - feed flow mismatch signal

since the steam flow bistable had been tripped making up the

input to the reactor protection system.

Licensee investigation

determined that in preparing to perform the functional test, the

channel I steam flow bistable had been tripped, however the RO

at the controls failed to switch to the alternate steam flow

channel (II) in accordance with procedures.

The inspector reviewed the I&C surveillance procedure, No. 14

SG Steam Pressure Channel Functional Test, discussed the event

with operations personnel and determined that failure to switch

to the alternate steam flow channel constitutes an apparent

violation of T.S. 6.8.1 in that surveillance test procedures

for safety systems were not followed.

(50-272/89-01-01)

On February 7, 1989, the licensee performed a surveillance test

on the reactor coolant pump breaker status indication to the

reactor protection system.

The surveillance for Nos. 11 and 12

RCP 1 s were completed satisfactorily.

However, prior to

restarting No. 13 RCP and contrary to test procedure

SP(0)4.3.l.l.l,

11 Reactor Coolant Pump.Breaker Status

Indication", the reactor operator (RO) failed to defeat the

second level undervoltage (UV) protective relay for C vital

bus.

Defeating the UV relays is required prior to starting

each RCP and is accomplished by pres.sing 3 pushbuttons 1 ocated

on the control room console, one for each vital bus.

The

relays for A and B vital buses were defeated.

As a result of

the UV relay defeat for C vital bus not being energized, when

No. 13 RCP was started, voltage decreased to the 91.6% relay

setpoint and the C vital bus loads were stripped.

No. lC

emergency diesel generator automatically started and closed on

the bus and the blackout loads were then sequenced on to the

bus.

AOP-ELEC.4KV-C

11 Loss of lC 4KV Vital Bus

11 was entered and

C vital bus was restored to normal.

Related systems responded

as designed and this event had no adverse affect on the unit

which was in Mode 3 (hot shutdown).

The inspector r~viewed the

AOP, discussed the event with operations personnel and

determined that this second instance of failure to follow

c.

D.

3

procedures for surveillance procedure "Reactor Coolant Pump

Breaker Status Indication

11 is an apparent violation of T.S.

6.8.1. (50-272/89-01-01)

On February 15, 1989, the licensee commenced a controlled

shutdown from 100% power as a result of a component cooling

water (CCW) leak inside containment.

The leak occurred as

maintenance workers were attempting to tighten a leaking pipe

cap on CCW drain valve 13CC293.

Valve 13CC293 is connected to

the CCW supply to No. 13 reactor coolant pump (RCP).

The drain

piping and valve are 3/4 inch in diameter and the drain line is

unisolable without securing CCW to the RCP.

As the pipe cap

was tightened, the valve sheared off. A plant shutdown was

initiated to facilitate isolation of the leak.

During the

shutdown, makeup was continuously supplied to the CCW system.

Approximately 30,000 gallons of CCW was spilled from the CCW

system to the containment sump.

After the unit was removed

from service, No. 13 RCP was secured, the leak was isolated and

the drain line repaired.

Several maintenance workers were wetted with CCW which contains

potassium chromate.

The workers have undergone medical review

with no adverse results identified.

The licensee hosed down

the affected areas with water to flush the chromated water from*

the floor and piping to the containment sump.

The leakage and

flush water were transferred to the waste holdup tanks (WHUT).

The WHUT is being processed by a vendor using demineralization.

The inspector had no further questions concerning this event.

On February 18, 1989 with the unit critical at lOE-8 amps, the

reactor tripped as a result of an error made during

surveillance testing.

During the performance of procedure

l!C-2.6.025 "lPT-506 First Stage Turbine Impulse Pressure" the

instrument and controls (I&C) technician did not properly

verify by status panel indication that the turbine was latched.

Since the surveillance was attempted with the turbine

unlatched, when the P-7 bistable was tripped as part of the

surveillance procedure, the Reactor Protection System sensed

reactor power greater than 10% with the turbine tripped and

caused a reactor trip. All equipment responded as designed to

the trip.

The inspector reviewed the surveillance procedure

and discussed the event with I&C and operations personnel.

An

instrument and controls technician failed to verify the proper

status of reactor protection system panel lights for turbine

stop valves closed and turbine low oil pressure as specified in

procedure l!C-2. 6*. 025

11 lPT-506 First Stage Turbine Impulse

Pressure' 1 *

The inspector is concerned that the technician

continued with the procedure after recognizing that procedural

instructions were not met and did not consult with the

supervisor and/or operations personnel.

This third instance of

2.2.2

A.

4

failure to properly implement surveillance procedures is an

apparent violation of T.S. 6.8.1 (50-272/89-01-01).

The unit

returned to power on February 19, 1989.

Unit 2

On February 5, 1989, after removing Nos. 23A and 238 circulators

from service for condenser cleaning and circulator repair, No.

22 steam generator feed pump (SGFP) tripped due to low suction

pressure and caused a reactor trip resulting from No. 23 SG

steam flow - feed flow mismatch coincident with low SG level.

Plant systems responded as designed to the trip and the unit was

stabilized in Mode 3.

The inspector discussed the circumstances surrounding the.trip

with operations and engineering personnel and determined the

following.

With both No. 23 condenser circulators and No. 23

heater drain pump out of service, steam flashing occurred in

No. 23 hotwell which caused some cavitation in No. 23

condensate pump and' low suction pressure to the SGFPs ..

In

addition, the licensee determined that the non-safety related

suction pressure trip mechanism for No. 22 SGFP was

electrically degraded such that the as-found trip setpoint was

at 256 psi versus 215 psi, the intended setpoint.

Upon the

trip of No. 22 SGFP, the reactor operator (RO) quickly reduced

power to 67% in an attempt to maintain SG level and avert a

reactor trip, however No. 21 SGFP subsequently tripped for an

unknown reason.

Licensee followup testing with respect to No.

21 SGFP did not reveal any deficiencies.

Following repair of

the No. 22 SGFP suction pressure trip mechanism, testing of No.

21 SGFP and No. 23 condensate pump and reset of three main

steam safeties (discussed later); the unit was returned to

service on February 9, 1989.

The inspector reviewed procedure

AOP-COND-2

11 Loss of Circulating Water and/or Condenser Vacuum

11

which the licensee has upgraded to provide added controls to

ensure proper SGFP suction pressure with circulators and heater

drain pumps out of service.

The inspector had no further

questions regarding the trip.

During plant stabilization following the trip, main steam

safety valve No. 23MS15 lifted.

As a result, reactor coolant

average temperature was reduced from 548 degrees F to 538

degrees F when the valve reseated.

Subsequent testing by the

licensee determined that this valve lifted at 960 psi versus

its required setpoint of '1070 psi.

The licensee tested all 20

main steam safety valves to verify their setpoints and

determined that valve No. 21MS12 was slightly low and 21MS13

was slightly higher than required.

All other valves tested

satisfactorily.

Valves 23MS15, 21MS12 and 13 were adjusted to

their proper values.

The inspector notes that the main steam

5

safety valves were lift tested and set at the vendor's shop

during the August 1988, refueling outage.

In addition, valve

23MS15 lifted prematurely at 1000 psi (vs 1070 psi) on November

18, 1988 with the unit in Mode 3 and was subsequently reset by

the licensee.

Licensee investigation into the cause of the

discrepant setpoints has been inconclusive.

Licensee discussions

with the vendor indicate that valve setpoint drift does occur,

but infrequently.

The inspector is concerned that valve 23MS15

has exhibited setpoint drift twice and to this point cannot be

explained by the vendor or licensee.

The inspector will continue

to follow licensee actions relative to monitoring and resolution

of the apparent setpoint drift.

8.

On March 3, 1989, the licensee identified two pinhole thru wall

leaks on No. 21 containment spray (CS) header piping between

the inboard and outboard containment isolation valves.

The

leaks were about 1/2

11 apart on the outside radius of a 10

degree bend in a 4 ft. long spool piece.

The piping material

is 8" schedule 10, 304 stainless steel.

The header was

immediately isolated by the licensee.

To ensure containment

integrity a blank flange was installed at the valve 21CS6

location inside containment, where a flanged spool piece had

been previously installed in place of the 21CS6.

Technical

Specification Action Stat~ment (TSAS) 3.6.2.1 was entered which

allows one containment spray header to be out of service for 72

hours before a plant shutdown is required.

After evaluating

repair methods and the low safety consequences of extending the

out of service period (the redundant CS header and 5 containment

fan coil units were operable), the licensee requested and NRC

granted discretionary enforcement to extend the 72 hour8.333333e-4 days <br />0.02 hours <br />1.190476e-4 weeks <br />2.7396e-5 months <br /> TSAS by

96 hours0.00111 days <br />0.0267 hours <br />1.587302e-4 weeks <br />3.6528e-5 months <br /> with the condition that the redundant containment spray

header and all 5 containment fan coil units remain operable.

The leaking spool piece was replaced by ~ flanged spool piece

and No. 21 CS header was returned to service on March 7, 1989.

The licensee's evaluation of the cause and extent of the leak,

and the applicability of the problem to similar piping configu-

rations on the Nos. 21 and 22 headers consisted of the following

tests:

1.

Visual walkdown of piping.

A darkening or discoloration

of the leaking spool piece was noted.

Similar discoloration

was noted on 2 additional bends in the No. 21 CS header and

on 1 bend in the No. 22 CS header.

2.

Ultrasonic testing (UT) was performed on the four darkened

bend locations.

Results on the leaking spool piece showed

indications of 9 pitting areas on the top (10 o'clock to 2

o'clock) section of the leaking pipe.

The other three bend

c.

3.

4.

6

areas showed baseline noise at the top portion of the p1p1ng

which the licensee stated is indicative of a rough surface.

No other indications of pitting were observed.

Radiography of the failed spool piece revealed several

small hairline cracks in the area of the two thru wall

holes.

The radiography results and visual observation of

the inside of the spool piece after it was cut out, did

not support the UT

results of 9 pit areas.

Radiography

of the other three areas showed no indications.

Metallography performed by Westinghouse on the failed

spoolpiece indicated a small area of sensitization in the

immediate area of the thruwall cracks.

The failure

mechanism has been attributed to intergranular stress

corrosion cracking resulting from borated stagnant water

in the sensitized piping.

A visual walkdown of Unit 1 CS p1p1ng did not identify any

similar areas of concern.

The licensee stated that the Unit 1

piping contains mitered welds rather than bends in the pipes as

in Unit 2.

The licensee is evaluating a surveillance plan for other areas

where stagnant borated water IGSCC may be of concern such as

hot and cold leg safety injection piping, BIT outlet piping and

various sample piping.

The inspector is following licensee

actions in this regard.

On March 12, 1989, a reactor trip and safety injection

occurred.

The inspector responded to the site and determined

the following concerning the transient.

The initiating event

was the failure of the 10 vital instrument bus inverter due to

a loose control power fuse.

The loss of the 10 inverter

resulted in Channel IV inputs to the reactor protection system

(RPS) being made up.

In addition, the steam generator feed

pump master controller is powered from the 10 vital instrument

bus, and upon failure of the inverter the feedpump controller

reduced the two main feedpumps to idle speed.

The reduction in

feedwater flow resulted in steam generator steam flow/feed flow

mismatch and coincident with steam generator low level (Channel

IV input), the reactor trip occurred.

When a reactor trip occurs, high steamline flow signals result

since some steam flow is present in the steamlines and the

steam flow bistables reset to their no-load value upon a

3.

3.1

7

reactor trip signal.

High steamline flows coincident with a

low steam pressure (Channel IV inputs - 2 of 4) caused by the

loss of lD inverter made up the logic for safety injection

(SI) actuation.

Plant systems responded as expected to the trip and SI.

The SI

was terminated 27 minutes after initiation, when the operators

had completed diagnostics and reached the appropriate SI

termination step in EOP-TRIP-1.

During this time the

pressurizer filled and a power operated relief valve (2PR2)

cycled sev~ral times to relieve the pressure.

Valve 2PR2 was

subsequently isolated (block valve 2PR7 closed) due to leakage

apparently caused by passing steam and water through the valve.

The licensee does not plan to repair the valve at this time.

The inspector observed the subsequent reactor startup on March

13, 1989.

No inadequacies were identified.

RADIOLOGICAL CONTROLS (71707, 83750, 92701, 92702)

Inspection Activities

PSE&G 1 s compliance with the radiological protection program was verified

on a periodic basis.

These inspection activities were conducted in

accordance with NRC inspection procedure 71707.

In addition, the inspector reviewed licensee planning and preparation in

the area of radiological controls for the upcoming Unit 1 refueling

outage.

Areas reviewed were as follows:

organization and staffing

training and qualification of radiation protection personnel and

radiation workers

ALARA; including source term reduction

oversight of contractor personnel

planning and work package review by radiological controls personnel

work scope and knowledge of work scope by radiological control

personnel

hot particle control

management support of radiological controls

incorporation of lessons learned from previous outages

licensee efforts to address radiological controls weakness

previously identified by the NRC

radwaste volume reduction

use of engineering control to minimize use of respiratory equipment

protection

8

3.2 Inspection Findings

The licensee appeared to be providing adequate planning and preparation

for the upcoming outage.

Special emphasis was being placed on efforts to

preclude recurrence of weaknesses in the implementation of the

radiological controls program identified during the last outage at Unit

2.

At the time of this inspection, licensee radiological controls

personnel indicated that planning and preparation for outage work tasks

were about 70% complete.

Licensee personnel indicated they were somewhat

behind in do~umentation of work packages, but they believed most work

packages would be completed by the start of the outage.

3.3 Followup on Open Items

A.

B.

(Closed) Violation 272/88-16-01; Post Accident Sampling System (PASS)

equipment not properly maintained, procedures not properly implemented

or issued in a timely manner.

The inspector verified that the licensee

has developed a prioritization system for ensuring timely completion

of PASS work orders.

Refer to Unresolved Item 272/88-16-06.

The

inspector verified that chemistry personnel retraining on procedure

implementation has been conducted.

Corrective actions for this

violation appear to be adequate.

This item is closed.

(Closed) Unresolved Item 272/88-16-02; Ensure capability of obtaining

backup samples.

The inspector reviewed Engineering Memo (EM)89-005

dated February 17, 1989 which delineates a project scope proposal for

backup grab sampling capability for PASS in-line monitored parameters.

The EM states that modification and upgrades to the PASS panel,

chemistry laboratory and equipment, procedures and training are

required to be able to obtain grab samples for pH, chloride, hydrogen

and boron.

The inspector concludes that implementation of the EM

proposal would satisfy T.S. and NUREG-0737 requirements.

Integrated

dose estimates will be calculated as part of the design change package.

The NRC recognizes that failure to provide backup sampling and

analysis capability for PASS in-line monitored parameters is a

deviation from NUREG-0737, Item II.B.3 and license conditions.

However, inspector review of previous correspondence between PSE&G

and the NRC concerning this issue leads to a conclusion that PSE&G

informed the NRC and implemented what they thought was an alternate

method (i.e. timely instrument repair) for meeting the intent of

NUREG-0737 requirements relative to backup sampling capability.

The

licensee was not informed by the NRC of the unacceptability of their

position.

Since being informed of the deficiency in Inspection

Report 272/311/88-16, the licensee is in the process of developing

an action plan as discussed previously to resolve the issue.

Since

it is reasonable that PSE&G did not know that their position would

not meet the intent of NUREG-0737 requirements and acceptable

corrective actions are planned by the licensee, enforcement action

will not be taken.

c.

D.

E.

F.

9

The inspector noted that the EM estimates complete implementation in

1990, while the licensee's response dated October 19, 1988 estimates

backup grab sampling capability implementation by December 1989.

The licensee should keep the NRC informed as to any changes in the

completion date as the design change package is developed.

The

inspector will follow licensee activities in this regard to ensure

timely implementation.

This item is closed.

(Closed) Unresolved Item 272/88-16-03; Proper control and testing of

the PASS area radiation monitor (ARM).

The inspector verified that

calibration and testing of ARM 2R52 is acceptable and that the

instrument has been added to the Radiation Monitor System manual.

This item is closed.

(Closed) Unresolved Item 272/88-16-04; Verify completion of PASS

sample valve maintenance.

Maintenance on PASS sample valves is

complete.

This item is cl~sed.

(Closed) Unresolved Item 272/88-16-05; Hydrogen comparison results

between the reactor coolant system (RCS) and PASS samples are not

consistent.

The inspector verified that licensee equipment and

calibration procedure upgrades have improved consistency in RCS and

PASS hydrogen results.

This item is closed.

(Closed) Unresolved Item 272/88-16-06; Implement provisions to

ensure PASS availability with support systems isolated.

Initial

inspector review determined that the licensee's response to this

item was unacceptable.

In further discussion with the licensee, the

inspector clarified the concern to radiation protection and

licensing* personnel.

Subsequentl~ the licensee dev~loped

administrative controls to ensure that timely action is taken by

Operations and Chemistry personnel to maintain the PASS operable

when support systems are taken out of service.

The administrative

controls include an operations procedure for tracking PASS support

system and PASS availability, chemistry notification, and

establishing time requirements for restoration; establishment of

work order priority for PASS components; and development of

proceduralized alternatives for each PASS support system.

The

inspector reviewed a memo dated February 23, 1989 entitled "Post

Accident Sampling System-Priority and Operability" from the Salem

General Manager to the station managers delineating the

administrative controls and directing implementation within 60 days.

The inspector determined that the administrative controls appear to

be acceptable in ensuring PASS operability.

The inspector will

monitor licensee implementation and the effectiveness of this

program in future inspections.

This item is closed.

'.

G.

10

(Closed) Violation 311/88-25-01; Personnel did not adhere to

radiation protection procedures as required by Technical

Specification 6.11.

The licensee satisfactorily implemented the

corrective actions outlined in the March 10, 1989 letter to NRC.

This item is closed.

H.

(Closed) Unresolved Item 311/88-25-02; NRC to review dosimetry

record system, exposure control methods, and exposure limits.

Inspector review indicated that the licensee reviewed previous

personnel exposure results which were possibly subject to

interpretation errors.

No unusual exposures were identified.

The

licensee revised exposure control method~ to provide computer flags

for unusual exposures.

The licensee clarified exposure limits for

the areas between the knee and ankle.

This item is closed.

I.

(Closed) Unresolved 272/88-18-02; 311/88-18-02; NRC to review

licensee control of access to the Seal Table Rooms.

Keys to the

rooms were left in the doors to the rooms in containment and removed

when containment was opened for general access.

The seal table room

doors are independently pad locked closed.

The pad lock keys are

issued by radiation protection personnel in accordance with

applicable licensee procedures.

This item is closed.

J .

(Closed) Violation 272/88-18-01; 311/88-18-01; Personnel did not

adhere to radiation protection procedures.

The licensee implemented

the corrective action outlined in their December 22, 1988 letter to

the NRC.

The licensee also implemented the applicable corrective

action outlined in their December 27, 1988 letter to the NRC.

One

item remaining to be completed is the revision of RPlOOl, Radio-

logical Occurrence Investigation, to address root causes for

recurring problems.

The licensee has committed in the letters

above, to complete this revision by April 15, 1989.

Completion of

this revision will be followed in a subsequent inspection.

(311/89-01-02)

This item is closed.

K.

(Closed) Inspection Followup Item (50-272/88-19-01);

The licensee

was to implement enhancements to the post accident gaseous effluent

monitoring program described in their March 6, 1985 letter to the

NRC.

These enhancements included procedure upgrades, additional

personnel training, enhanced documentation and various design

changes.

The licensee satisfactorily implemented these

enhancements.

This item is closed.

4.

SURVEILLANCE TESTING

(61726)

4.1

Inspection Activity

During this inspection ~eriod the inspector performed detailed technical

procedure reviews, witnessed in-progress surveillance testing, and

reviewed completed surveillance packages.

The inspector verified that

the surveillance tests were performed in accordance with Technical

11

Specifications, approved procedures, and NRC regulations.

These

inspection activities were conducted in accordance with NRC inspection

procedure 61726.

The following surveillance tests were. reviewed, with portions witnessed

by the inspector:

Unit 1

SP(0)4.l.2.l(A)

SP(0)4.5.4.2a

lIC-2.6.025

M3Q-2

REM Part III-3

REM Part III-7

Unit 2

2PD-4 .1. 038

SP(0)4.8.1.1.2

2IC-2 .10. 054

2IC-1.4.003

2IC-16.4.046

4.2

Inspection Findings

Reactivity Control Systems - Boration -

Vital Heat Trace

ECCS Subsystems

lPT-506 First Stage Turbine Impulse

Pressure

Reactor Trip and Bypass Breaker

Surveillance Testing

Spent Fuel Pit Drag Test

New Fuel Receipt Inspection

2R24A Seal Water Injection Filter

calibration

A&B Emergency Diesel Generators - 15

minute run

2TE-413A No. 21 RCS Hot Leg Wide Range

RTD

No. 23 Auxiliary Feed pump tachometer

calibration

Reactivity Computer Recorder calibration

On February 22, 1989, the licensee informed the NRC that the Unit 1 "N'

reactor trip bypass breaker undervoltage trip attachment (UVTA) failed

the output force measurement test.

This test measures the margin of

force in addition to the weight of the trip bar that the UVTA is capable

of overcoming.

The maintenance and testing of the reactor trip breaker

(RTB) and UVTA is performed as part of the above six-month preventive

maintenance activity.

As a result of the Salem ATWS event, the licensee

is committed to report any deficiencies identified with the RTBs to the

NRC.

The inspector witnessed licensee investigation of the failure which

12

consisted of reperforming the output force measurement test.

Subsequent

attempts were satisfactory.

As a result, the licensee concluded that

operability of the UVTA was marginal in that test results were not

consistent.

The licensee replaced-the UVTA and maintenance procedure

M3Q-2 was completed successfully.

Similar test failures have occurred in

the past due to installation of a batch of UVTAs with marginal

performance.

Following the Unit 1 refueling outage in April 1989, all

such UVTAs will have been replaced.

The inspector had no further

questions in this area.

5.

MAINTENANCE

(62703)

5.1

Inspection Activity

During this inspection period the inspector observed portions of selected

maintenance activities to ascertain that these activities were conducted

in accordance with approved procedures, Technical Specifications, and

appropriate industrial codes and standards.

These inspections were

conducted in accordance with NRC

in~pection procedure 62703.

Portions of the following activities were observed by the inspector:

Work Order 890106078

871202128

880401319

0092324

890227156

890223083

Procedure

MllE

MllG

Ml4A-4

2IC1.4.003

M3Z

I

M3R

M34-l

MllE

Description

12 Fuel Handling Building

Exhaust Fan - repair

motor vibration.

12SW387 - 12 Component

Cooling Heat Exchanger Service

Water (CCHX SW) inlet valve -

remove and repair.

22SW158 -

RHR pump room

cooler outlet control valve -

replace diaphragm.

lC Diesel Generator (DG)

lube oil heater - replace.

Boric acid filter vent

heat trace shorted -

repair.

23DF66-2C DG fuel oil

relief valve return to day tank

leaks - repair .

870801108(09)

880913131

890224114

890303089

881227094

5.2

Inspection Findings

1. 4. 003

NDWP

M6E

CJP S-89-036

OCR 2SC-02169

CJP S-89-012

13

11&12AF21 - Auxiliary

Feedwater inlet valve to steam

Generator, adjust limits and

measure stroke.

11 CC pump vent line -

seal weld threaded connection.

23 charging pump -

replace blown packing.

21 containment spray

header - replace

defective pipe with flanged spool

piece.

12A CCHX - repair leak. in

weld downstream of SW inlet

valve.

A.

The maintenance activities inspected were effective with respect to

meeting the safety objectives of the maintenance program.

In

particular, the activities associated with the containment spray

piping replacement were well coordinated and well supervised.

B.

The inspector noted that some maintenance workers compile notebooks

containing the work order, procedures, vendor manuals, instrument

Data cards, etc. for their assigned activities.

The inspector

observed that this practice results in an effective, organized

approach in performing the tasks.

6.

EMERGENCY PREPAREDNESS

( 71707)

A.

On March 16, 1989, a security and fire protection drill with regard

to a simulated fire and medical emergency was held onsite with the

Lower Alloways Creek. Fire Department.

The NRC was notified by

letter on that date of the planned drill and the licensee's

intention to waive certain security access requirements.

The

inspector discussed the drill scenario and security controls with

the Senior Fire Protection Supervisor and the Nuclear Security

Manager.

The inspector will review the licensee's critique report

of the drill when available.

7.

SECURITY

(71707)

7.1

Inspection Activity

PSE&G's compliance with the security program was verified on a periodic

basis, including adequacy of staffing, entry control, alarm stations, and

physical boundaries.


~- - - -

14

7.2

Inspection Findings

The inspector observed an inconsistency in the method security force

members (SFM) use to verify the integrity of the diesel rooms' personnel

escape hatch latch.

Some SFMs climb the ladder to the hatch and verify

the proper position of the latch, while others shine a flashlight up to

the latch.

The inspector observed that it is difficult to see the latch

from the floor even with a flashlight.

This issue was discussed with the

Nuclear Security Manager who stated that the SFM should climb the ladder

to verify latch integrity and all SFM would be reinstructed to do so.

The inspector will continue to monitor the implementation of the security

program in this regard.

8.

ENGINEERING/TECHNICAL SUPPORT

(35065, 92701)

8.1

Inspection Activity

The inspector conducted an inspection of material storage by reviewing

Quality Assurance (QA) audits, QA surveillances and Storage and Material

Control procedures, and by conducting interviews with management

personnel.

8.2 Inspection Findings

Materials delivered to the rece1v1ng area undergo a receipt inspection,

are classified and are assigned an appropriate shelf life.

Material

Control personnel enter the information into a computer data base and

conduct a put away inspection of the material to verify various

~ttributes such as correct storage bin location, consistent

classification and shelf life with material in the same bin, and properly

completed identification tags.

If any errors are identified during put

away a problem report is prepared.

The problem report is then

dispositioned by the Engineering and Procurement Branch (E+PB).

The

questionable material is tagged with the problem report, but remains in

storage.

No attempt is made to physically segregate the material or to

correct the identified problem until disposition of the problem report is

completed.

Problem reports appear to be dispositioned only if the

nonconforming material is requisitioned.

During issuance of material for maintenance activities, a check is made

that the part number requested on the work order matches the part number

attached to the material.

There is no formal verification of the

material classification, shelf life or the proper disposition of problem

reports applicable to that part number.

In 1987, a new classification system was instituted which created

different classifications for some material.

The licensee has decided

not to review and update the classifications of existing material in

storage which were classified under the old system.

As a result, problem

reports are generated whenever an inconsistent classification of material

15

is identified.

A new shelf life program was also implemented in May 1988

and the shelf lives of all material were evaluated and problem reports

were written for identified inconsistencies.

PSE&G surveillances as early as 1986 identified nonconformances in the

areas of material ~dentification and control, such as incorrect or

inconsistent classifications and shelf lives.

Corrective Action Request

(CAR) MR-87-C-001 was written on these nonconformances in April 1987, and

a letter was sent to the Manager Material Control in July 1987,

identifying a lack of appropriate corrective actions.

Apparently a

management decision was made not to attempt to identify similar

occurrences of the identified problems, not to physically segregate

material and not to establish any compensatory formal controls to prevent

questionable material issuance.

In June 1988, Quality Action Report (QAR) SP-88-QOOl was issued to the

Manager Material Control for failure to correct material identification

and control problems which were identified in February 1988.

In response

to the QAR, problem reports were written for the deficiencies and

submitted to Procurement Engineering for disposition.

There is no record

to indicate that the problem reports were dispositioned or that the

problems were corrected.

Again, no apparent action was taken to

determine similar problems nor to physically segregate material tagged

with problem reports.

The last three Quarterly Reports for 1988 from the Manager Procurement

Quality Assurance to the Manager Material Control requested corrective

actions to be taken to resolve the generic problems underlying the

continued identification of nonconformances.

There was apparently no

response to the Reports nor any actions taken to correct the problem.

In August 1988, Management Action Request (MAR) MA-88-MOOl was issued to

the General Manager of Nuclear Services concerning, in part, problems of

material identification and control.

A corrective action plan was

developed and implemented, however no attempt was made to identify and

correct problems similar to those documented in the MAR or to establish

compensatory controls for material issuance.

In October 1988, QAR MR-88-Q005 was issued to the Manager Material

Control concerning recurring nonconformances in the areas of material

identification and control.

On December 5, 1988 a letter was sent to the

Manager Material Control from the Engineer-QA Material Compliance

requesting an expedited disposition of the QAR since the response was

past due.

The response detailed the actions taken to correct the

documented problems, however no apparent attempt was made to identify and

correct similar problems.

  • .-*:':::

16

From the above QA reports, the inspector concludes that material of mixed

classifications exists in the same bin and that an undetermined amount of

material in the storage areas may be fncorrectly classified.

Due to the recurring licensee identified problems with inventory storage

and control, it appears that corrective actions taken over the last three

years have not precluded the recurrence of problems in these areas nor

have actions been taken to formally control and more closely monitor the

potential for issuance of nonconforming material.

The failure to correct

or prevent recurrence of self identified nonconformances for over a three

year period is considered an apparent violation of 10CFR50 Appendix B

Section XVI.

(50-272/89-01-02)

The licensee 1 s identification of recurring nonconformances is indicative

of adequate Quality Assurance surveillances and audits, however

inadequate steps have been taken to resolve potential nonconformances,

identify root causes and implement corrective actions which prevent or

alleviate recurrence of similar nonconformances.

There are presently over 1400 problem reports that have not bee11

dispositioned.

Approximately 50% of the reports are for shelf life

discrepancies which were identified in June 1988 when the interim shelf

life program was implemented.

Disposition of shelf life discrepancies

are not planned until a new standard for self life is completed later

this year.

No plans exist for reducing the backlog of problem reports.

This is inconsistent with procedure M-ll-P-300, rev 2, Storage and

Handing of Material, which specifies disposition of problem reports in an

expeditious manner.

A problem report identifies a nonconformance since it identifies a

deficiency in the documentation of material characteristics that render

the quality of the material unacceptable or indeterminate.

In accordance

with ANSI N18.7, Administrative Controls and Quality Assurance for the

Operational Phase of Nuclear Power Plants, the control of- nonconformances

with tags is acceptable, however physical segregation and marking is

preferable.

Due to the backlog of problem reports further consideration

should be given to the preferred method of physical segregation of

nonconforming material.

There is presently material in the storage area which is over two years

old and may be incorrectly classified in accordance with the present

classification system.

The licensee apparently made a decision that

having an unknown number of improperly classified items in the storage

area is acceptable based on the checks made during put away and the

ev~ntual reordering of all_ material.

-

17

There is no formal verification or validation of the correctness of

material classification and shelf life prior to issuance of the material,

even though there is a significant amount of nonconforming material in

mixed storage in the storage areas.

Instances have been i.dentified in

CAR SA-88-C016, issued in August 1988, and in CAR MAR-87-COOS, issued in

May 1987, where material was issued to the maintenance department and the

appropriate material control tags were not issued or not retained with

the work package.

Follow up licensee investigations verified that the

material installed in the facility was properly qualified.

The inspector is concerned that due to the amount of nonconforming

material in the storage area and the lack of formal verification of

material acceptability upon .issuance, there is a significant potential

that nonconforming material could be issued for use in safety grade

equipment.

This issue is considered an unresolved* item.

(272/89-01-03)

8.3

Open Item Followup

A.

(Closed) Unresolved Item No. 272/311/87-35-02:

Review of the

licensee's evaluation and resolution of degraded grid voltage

problems which could affect the operability of safety related

equipment.

After a Power Technology Inc. transient analysis study

identified the degraded grid voltage problems, six circulating water

pump power supplies were shifted from the Salem 13 KV electrical

distribution system to the Hope Creek 13 KV electrical distribution

system to reduce loads on the Salem grid to below the base value

determined by the study.

An EBASCO calculation, which was initially issued in draft form on

July 15, 1987, provides the design basis for the Salem electrical

system.

Based on the calculation, two 600 volt feeder lines at Unit

1 and three lines at Unit 2 were installed from the the vital buses

to the motor control centers in the service water building in order

to reduce the voltage drop.

In December 1987, an analysis was performed, based on the EBASCO

calculations, for the voltage drop from the 230 V vital MCCs to 120

V control power circuits.

Based on the analysis, interposing relays

were added to approximately 48 control circuits to assure their

operability at the expected low voltage conditions.

In October 1988, an Engineering Evaluation was completed by PSE&G

using plant specific equipment responses.

The Evaluation reanalyzed

motor operating conditions for motors whose voltage had fallen below

80% rated voltage in the EBASCO calculation. It was concluded that

adequate voltage would be available to start and run the vital

motors.

In addition field measured voltage drops were compared to

the calculated values to verify the analysis.

18

The licensee is planning on completing major modifications to the

off site power grid for Salem over the next five to seven years.

The modifications are expected to reduce the degraded grid problems

and provide additional flexibility in conducting maintenance on the

equipment in the electrical yard.

The inspector has no further questions on the short term resolution

of the degraded grid voltage concern.

This Item is closed.

B.

(Closed) Inspector Follow Item 272/88-13-01; Containment Electrical

Backup Protection Modifications.

Modifications to add backup

protection devices for Unit 1 penetrations will be completed during

the upcoming refueling outage under Design Change Package lSC-2001.

This item is closed.

9.

SAFETY ASSESSMENT/QUALITY VERIFICATION

(35502, 40500)

9.1

9.2

Inspection Activity

The inspector reviewed the license2 1 s self assessment capabilities

including interviews with supervisory and management personnel from the

following PSE&G Quality Assurance groups: Programs and Audits, On Site

Safety Review Group, and Off Site Safety Review Group.

An inspection. was

made of selected reviews, audits and reports produced by these groups.

They were evaluated based on quality of the review or audit, quality of

the recommendations made, and the implementation and follow-up on the

recommendations.

The SORC process and the licensee's corrective action

tracking system were also reviewed.

Inspection Findings

The inspector reviewed the quality assurance audits performed on Salem

maintenance and operations in 1987 and 1988, corrective action audits

performed in 1987 and 1988, and corrective action follow-up on several QA

initiated action items.

In general the audits were of sufficient depth

to make a meaningful evaluation of the activity inspected.

Open items are followed by the licensee's corrective action tracking

system (now called ATS).

The inspector observed, however, that a

significant number of QA initiated items were listed on ATS as overdue.

Quality Assurance personnel were questioned as to the reason for the

overdue items.

They indicated that there has been a problem in getting

station response to open QA items in the past.

Part of the problem

appears to be due to the large number of items opened on the ATS by

various groups without a priority established.

Discussions with the Vice

President - Nuclear Operations, General Manager - QA/NSR, and the Salem

General Manager, all of whom are fairly recent appointees to these

positions, indicate that they are working to resolve the prioritization

and responsiveness issues.

The inspector has noted a slight improvement

in the number of overdue items on ~he ATS over the past several months.

,.

,

19

Based on management's acceptance of the problem and commitment to

resolution, and the downward trend on overdue items, unresolved item

272/88-16-07 is closed.

However, the inspector will continue to monitor

licensee progress in this area.

The inspector reviewed the Technical Specification required functions of

the Off Site Safety Review group.

The quality of the unresolved safety

question reviews was adequate, although made less useful by being on a

parallel vice series path with SORC.

The audit function of the Salem QA

program was adequate.

The functions of the On Site Safety Review (SRG) group were

reviewed.

Detailed safety system functional reviews, problem area reviews, root

cause investigations, and post trip reports have been produced by this

group alone or in conjunction with other engineering resources.

Inspector review of a sample of these documents determined that they

appear to be thorough and provide meaningful information for management

action.

The inspector noted that this group does not meet the Technical

Specification 6.5.2.2 which requires manning levels of a Manager, On-Site

Safety Review Group (SRG), who is supported by at least four dedicated,

full-time engineers located on site.

Presently the on-site Safety Review

Group consists of an onsite safety review engineer assisted by three

engineers.

This issue is unresolved pending NRC review of outstanding

license amendment requests (UNR 50-272/89-01-04).

Station Operations Review Committee (SORC) reviews of engineering design

changes were determined to be adequate.

10.

LICENSEE EVENT REPORT ( LER) AND OPEN ITEM FOLLOWUP

(90712, 92700)

10.1 Review of Licensee Reeorts

The inspector reviewed the fo 11 owing licensee reports for accuracy and

timely submission.

Unit 1 Monthly Operating Report - December, 1988 and January, 1989

Unit 2 Monthly Operating Report - December, 1988 and January, 1989

Unit 1 LER 89-001; On January 4, 1989, an Unusual Event was declared

and a Unit 1 shutdown commenced due to all three groups of

containment fan coil units (CFCU) being inoperable.

This event was

discussed in NRC Inspection Report 50-272/88-24; 311/88-27.

The

inspector had no further questions following review of the LER.

Unit 1 LER 89-003; On January 25, 1989, the licensee identified that

two impaired relay room penetrations had not been addressed in a

Special Report in accordance with Technical Specification (T.S.).

The deficiency is due to inattention to detail in entering computer

data which is used to compile the information for the Special

Reports.

The personnel involved have been counseled.

The inspector

verified that the two impairments have been added to Special Report

88-3-6.

Due to the administrative nature of this problem and small

  • ,

20

safety significance, the inspector has determined that failure to

include the two impairments in a Special Report is a licensee

identified violation of T.S. 3.7.11.a for which no further action is

required. (50-272/89-01-02).

Unit 1 LER 89-004; On January 20, 1989, an Unusual Event was

declared and a reactor shutdown commenced due to the breaker

position input to the reactor trip system for all four reactor

coolant pumps (RCP) being declared inoperable.

This event was

discussed in NRC Inspection Report 50-272/88-24; 311/88-27.

The

i~spector had no further questions following review of the LER.

Unit 1 LER 89-005; On January 27, 1989, both trains of ECCS were

declared inoperable due to unrelated equipment problems.

No. 11

train was inoperable due to No. 12 service water (SW) header being

out of service to effect repairs to No. 12A component cooling water

heat exchanger (CCHX) SW inlet piping.

No. 12 train was inoperable

due to the inoperability of lC diesel generator to repair it's

failed lube oil heater.

A blank flange was installed in 12A CCHX SW

inlet piping to allow 12 SW header to be placed in service within

the two hour T.S. action statement and a plant shutdown was not

required.

The equipment deficiencies have been corrected by the

licensee.

Inspector review of this issue is complete.

Unit 2 LER 89-001; On January 3, 1989, both service water headers

were inoperable due to unrelated equipment problems.

The Unit was

in Mode 4.

Equipment deficiencies were corrected by the licensee

within TSAS requirements and a reduction in mode was not required.

The inspectors review of this issue is complete.

Unit 1 Supplemental Special Report 88-3-6 addresses additional

licensee identified fire barrier penetration seal impairments

discovered as a result of the Penetration Seal Program.

Unit 2 Special Report 88-8;

Inadvertent actuation of the

pressurizer over pressure protection system (POPS).

On October 31, 1988, with Unit 2 in cold shutdown, POPS Channel II

actuated with an indicated pressure of approximately 360 psig, which

is below the actuation set point of 370 psig.

POPS Channel I did

not actuate even though actual pressure was determined to be

approximately 380 psig.

The inspector found the special report to be inadequate to meet the

requirements of Technical Specification action statement 3.4.10.3.c.

The description and the apparent cause of the event did not provide

sufficient details regarding to the components that failed.

The

source of the error in the main control board bezel reading was not

identified by the report as affecting the indication from both

channels or that both sensors were properly calibrated.

The

corrective actions did not include steps that would be implemented

to prevent reoccurrence of the event.

21

After review of the report and discussions with the licensee it

appears that the Channel I POPS comparitor was set above the maximum

Technical Specification set point and therefore rendered the channel

inoperable for an undetermined period of time.

The licensee has not

addressed the cause for the inoperability of the channel, the time

that the channel was inoperable nor what steps would be taken to

preven~ reoccurrence of the inoperability.

Based on the identified deficiencies in the report the licensee was

requested to reevaluate the POPS actuation and provide a supplement

to the Special Report.

This issue is unresolved pending NRC review

of the supplemental report. (UNR 50-311/89-01-01)

Unit 2 Special Report 88-9 des~ribes a non-valid 2C diesel generator

(DG) test failure as a result of a speed relay and alarm reset

switch problem.

The equipment deficiencies were corrected and the

DG tested satisfactorily.

The inspectors review of this occurrence

is complete.

10.2 Reference to Open Items

The following open items from previous inspections were followed up

during this inspection and are tabulated below for cross reference

purposes.

Closed

Closed

Closed

Closed

Closed

Closed

Closed

Closed

Closed

Closed

Closed

Closed

Closed

VIO 272/88-16-01

UNR 272/88-16-02

UNR 272/88-16-03

UNR 272/88-16-04

UNR 272/88-16-05

UNR 272/88-16-06

VIO 311/88-25-01

UNR 311/88-25-02

UNR 272/311/88-18-02

VIO 272/311/88-18-01

IFI 272/88-19-01

UNR 272/311/87-35-02

IFI 272/88-13-01

11.

EXIT INTERVIEW

(30703)

Section 3.3

Section 3.3

Section 3.3

Section 3.3

Section 3.3

Section 3.3

Section 3.3

Section 3.3

Section 3.3

Section 3.3

Section 3.3

Section 8.3

Section 8.3

The inspectors met with Mr. L. Miller and other PSE&G personnel

periodically and at the end of the inspection report period to summarize

the scope and findings of their inspection activities.

Based on Region I review and discussions with PSE&G, it was determined

that this report does not contain information subject to 10 CFR 2

restrictions.