ML18086B315

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IE Insp Repts 50-272/81-29 & 50-311/81-29 on 811124-1231. Noncompliance Noted:Failure to Provide Surveillance Procedure to Assure Compliance W/Tech Spec 3.6.2.2 & to Follow Procedure PD-3.6.014,ion Exchanger Resin Refilling
ML18086B315
Person / Time
Site: Salem  PSEG icon.png
Issue date: 01/22/1982
From: Greenman E, Hill W, Norrholm L
NRC OFFICE OF INSPECTION & ENFORCEMENT (IE REGION I)
To:
Shared Package
ML18086B313 List:
References
50-272-81-29, 50-311-81-29, NUDOCS 8202190327
Download: ML18086B315 (24)


See also: IR 05000272/1981029

Text

U. S. NUCLEAR REGULATORY COMMISSION

OFFICE OF INSPECTION AND ENFORCEMENT

(DCS Numbers - see

attached sheet)

Report Nos.

Docket Nos.

License Nos.

Licensee:

50-272/81-29

50-311/81-29

50-272

50-311

DPR-70

DPR-75

REGION I

Public Service Electric and Gas Company

80 Park Plaza

Newark, New Jersey

07101

Faci 1 i ty Name: _ _...;S;.;;;a..:..l e.:;.;.m~N~uc.::...l;.;:e;.:;a.:...r....;G:.:.;:e;.:.;n;.;;;;.er:.....;a:;.;t:...:i.;.:.ngil--,;;.S;...;:t;.;;;;.a..;;.t1.:...:* o;.:.;n:__-....:U:..:.n:.;.i~ts.::.......;:1:......::.a:...:.;nd;;;_..;;2:__

Inspection At: __

H_a_nc_o_c_k_s_B.....;.r.....;.i_dg.._e_.,:......;..;,Ne.;;..;w.;;.._;;,J~e""'"rs"-e""'y _________ _

1981

Inspectors:

W. ~-)li-1~, Jr., e~iden_t R~ac.tor Inspecto".'

Approved By: (Ji~

.

(\\.~E.G. Greenman, Chief, Reactor Projects Sectfon No.* 2A,

'i!S

Projects Branch No. 2, DRPI

Inspection Summary:

JAN 1 3 1982

  • date

JAN 1 3 1982

date

J.O.N 2 2 1982

date

Inspections on November 24 - December 31, 1981 (Combined Report Numbers 50-272/81-29

and 50-311/81-29)

Unit 1 Areas Inspected: Routine inspections by the resident inspectors of plant

operations including tours of the facility; conformance with Technical Specifi-

cations and operating parameters; log and record reviews; IE Circular review;

reviews of licensee events; and followup on previous inspection items.

The

inspection involved 85 inspector hours by the resident NRC inspectors.

Results:

Two items of noncompliance were identified (Failure to establish, im-

plement, and maintain procedures~- paragraphs 2, 8, and 12; and, failure to perform

a safety evaluation - paragraph 7)~

Unit 2 Areas Insaected:

Routine inspections by the resident inspectors of plant

operations inclu ing tours of the facility; conformance with Technical Specifi-

cations and operating parameters; log and record reviews; IE Circular:" review;

review of licensee events; and followup on previous inspection items.

The

inspection involved 91 inspector hours by the resident NRC inspectors.

Results:

Two items of noncompliance were identified (Failure to establish, im-

plement, and maintain procedures - paragraph 12; and, failure to perform a safety

evaluation - * p*ara:grapfr. 17) *

  • 1
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( 8202190327 820202

.PDR ADOCK 05000272
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REPORT NOS. 50-272/81-29 and 50-311/81-29

DCS NUMBERS

050272-810831

050272-810928

050272-810902

050272-810909

050272-810908

050272-810918

050272-810918

050272-810922

050272-810929

050272-811020

050272-810930

050272-811028

050272-811008

050272-811107

050272-811106

050272-811017

050272-811022

050272-811019

050272-811021

050272-811021

050272-811025

050272-811026

050272-811117

050272-811029

050272-811029

050272-811125

050272-811129

050272-811106

050272-811106

050272-811106

050272:;811213

050311-810901

050311-810901

050311-810903

050311-810906

050311-810907

050311-810915

050311-810918

050311-811006

050311-810918

050311-810924

050311-811004

050311-811009

050311-8°11006

050311-811026

050311-811022

050311-811028

050311-811028

050311-811119

050311-811127

050311-811107

050311-811110

050311-811215

050311-811217

050311-811218

\\

DETAILS

1. Persons Contacted

J. Driscoll, Assistant General Manager - Salem Operations

L. Fry, Operations Manager

J. Gallagher, Maintenance Manager

H. Midura, General Manager - Salem Operations

L. Miller, Technical Manager

J. 0

1Connor, Radiation Protection Engineer

F. Schnarr, Reactor Engineer

R. Silverio, Assistant to the General Manager

J. Stillman, Station QA Engineer

The inspector also interviewed other licensee personnel during the course

of the inspections including management, clerical, maintenance, operations,

perfonnance and quality assurance personnel.

2. Status of Previous Inspection Items

(Closed} Unresolved Item (311/81-13-04} Volume calculations for containment

sump level instruments.

The inspector reviewed a document entitled,

Design Calculation No. S-C-A900-MDC-006, Revision 1, Developmental

Chronology of Previous Containment Flooding Calculations, Units

1 and 2, dated October 8, 1981.

Included in this review were com-

putation sheets dating back to 1976.

The inspector confirmed that,

based on containment dimensions, and allowing for reactor, accumu-

lator, piping, structural steel, concrete, and PRT volumes, a

flood volume of 600,000 gallons will reach an elevation of 85

1-6"

or less. Therefore the installed level measuring capacity of 86

1

is adequate for the purpose.

The inspector had no further questions

on this item.

(Closed} Unresolved Item (311/81-11-03} Surveillance for battery powered

emergency lights. The inspector reviewed procedure M4B, Emergency

Lighting Equipment Test and Inspection - Battery Units, Revision

0, dated December 16, 1981.

The procedure is conducted annually

and scheduled by Inspection Order.

The inspector had no further

questions.

(Closed} Unresolved Item (311/80'-16-03} Operator walkthrough of core thenno-

couple readout when over range. Since identification of this

issue, the licensee has stationed instrument and control techni-

cians on operating shifts and has prepared procedure PD-14.3.010,

Extended Range Reading of Incore Thennocouples.

The inspector

reviewed the procedure, which has been field-tested, and confirmed

that the actions necessary to detennine core thermocouple tempera-

tures in the event of computer failure are within the capability

of shift personnel. The inspector had no further questions on

this item.

3

(Closed) Unresolved Item (272/81-05-02) Definition of pressurizer operability

when heater groups become inoperable.

Amendment 39 to Facility

Operating License DPR-70 established two 150 KW groups of heaters-

as the minimum required in Modes 1, 2, and 3. The basis for this

minimum is the requirement to sustain natural circulation. Oper-

ational experience indicates that this heater capacity may be

insufficient to maintain pressure control during power operation.

Further review by the inspector identified no operating or emergency

procedure which addresses loss of heater capacity. Technical

Specification 6.8.1, which includes Regulatory Guide 1.33 Appendix

A by reference, requires a procedure for malfunctions of the

pressure control system. This item is resolved as noncompliance

with Technical Specification 6.8.1 (272/81-29-01).

(Closed) Noncompliance (272/80-10-02) Failure to meet the reporting require-

ments of 10 CFR 50 Appendix J.

By letter dated July 8, 1980, the

licensee provided an addendum to the CILRT report which includes

the Type C testing performed.

In addition, the licensee has con-

solidated responsibilities for leak rate testing to preclude recur-

rence of this item.

The inspector had no further questions.

lClosed) Unresolved Item (272/80-10-03) Acceptance of 1979 CILRT results.

In the July 8, 1980 addendum to the CILRT report, the licensee

revised the analysis to account for water inventory changes.

The

inspector concluded that the evaluation was adequate and the re-

vised analysis of test results met applicable acceptance criteria.

This item is resolved as acceptable.

(Closed) Unresolved Item (272/81-01-04) Identification of erroneous control

room instrumentation. The inspector reviewed the implementation

of an Operations Directives Manual procedure whereby instrumentation

which has failed or does not correspond in a channel check is de-

clared inoperable, entered in Log 13, and is identified with a

strip of translucent red tape. The system is effective in identi-

fying those instruments which would provide incorrect information

to the operator.

Based on continuing observation, the inspector

also confirmed that, in the case of reactor trip or ESF instrumen-

tation, the appropriate Technical Specification Action Statement

is also invoked.

The inspector had no further questions on this

item.

(Closed)

Open Item (311/79-30-01) Confirmation that alarm setpoints are

conservative with respect to Technical Specifications. The licensee

has concluded a review which verified that existing alarm setpoints

are consistent with Technical Specification limits.

Some minor

procedure changes resulted from this review.

The inspector had no

questions on this item.

(Closed)

(Closed)

4

Unresolved Item (272/80-31-02) Alarm setpoint for C02 system low

pressure. The Technical Specification minimum for the C02 system

is 285 psig. The alarm had been set at 275 psig and the procedures

were consistent with the as-built configuration. The licensee

has completed a design change to modify the setpoint to 290 and

the procedures have been changed accordingly. The inspector had

no further questions.

Unresolved Item (272/80-31-03) Console Alarm procedures for water

treatment system.

The alarm procedures in both units have been

changed to refer to other station procedures rather than Technical

Specification 3.7.1.7, which has been deleted.

The inspector had

no further questions on this item.

(Closed) Unresolved Item (272/80-20-02) Weight testing of miscellaneous

fuel handling (rigging) equipment. Maintenance Procedure M2Q,

Revision 0, dated August 28, 1981, provides requirements for con-

trol, inspection, testing, and maintenance of general rigging

equipment (cables, slings, shackles, etc.). This procedure provides

acceptable guidance for maintenance of general rigging equipment.

The inspector confirmed adherence to this procedure during receipt

and storage of new fuel .

(Closed} Unresolved Item (272/80-23-03) Field change to Spent Fuel Handling

Tool.

Design Changes lEC 1286 and 2EC 1299 were issued to describe

the modifications to the Spent Fuel Handling Tool.

The design

change packages were acceptable and satisfied the licensee's require-

ment for implementing engineering changes.

  • , ;i.

(Closed) Unresolved Item {272/81-01-05) Air flow check/calibration of the

AMS-2 Airborne radiation monitor. Procedure RP 9.021 Calibration

of AMS-2 (Revision 1, dated April 8, 1981) has been revised to

include a check of the air flow through the AMS-2 radiation monitor.

(Closed} Unresolved Item (272/81-14-03) Fire Protection Dampers.

The licensee

provided the test{~ results of the remaining 13 dampers. All of the

dampers were tested satisfactorily. The inspector had no further

questions.

{Closed) Unresolved Item {311/81-10-02) Supervisor ... f:feview of ,~s*urveillances.

Following the observation of periodic surveillances over the past

several months, the inspector concluded that the licensee's super-

visors provide an adequate independent review of the completed

surveillance procedures.

(Closed) Unresolved Item (311/81-10-03) Annunciator Alarm.* The hinged

covers above the test switches in equipment racks 11 and 31 were

replaced. These covers were necessary to contact a microswitch to

clear annunciator alarms B-18 and B-26.

The alarms are working

properly now.

i

' I

'

I

I

I

I

(Closed)

SITE

5

Unresolved Item (311/81-19-02) Identify units of measure for control

room radiation monitors.

The radiation monitors indicated in the

control room have labels attached below the meter face.

These

labels indicate the radiation units for each meter.

3. Shift Logs and Operating Records

a. The inspector reviewed the following plant procedures to determine the

licensee established requirements in this area in~:preparation for a

review of selected logs and records.

AP-5, Operating Practices, Revision 11, August 13, 1981;

--

AP-6, Incident Reports and Reportable Occurrences, Revision 7,

October 8, 1981;

AP-13, Control of Lifted Leads and Jumpers, Revision 4, February

11, 1980;

Operations Directive Manual; and,

AP-15, Safety Tagging Program*, Revision 1, November 21, 1980.

b.

Shift logs and operating records were reviewed to verify that:

Control room log sheet entries are filled out and initialled;

Auxiliary log sheets are filled out and initialled;

Log entries involving abnormal cond1tions provide sufficient detail

to communicate equipment status, lockout status, correction and

restoration;

Log book reviews are being conducted by the staff;

Operating orders do not conflict with Technical Specification

requirements;

Incident reports detail no violation of Technical Specification LCO

or reporting requirement; and,

Logs and records were maintained in accordance with Technical

Specifications and the procedures in 3.a above.

6

c. The review included examination of the following plant shift logs

and operating records and discussions with licensee personnel:

Log No. 1 - Control Room Daily Log, November 24 - December 31, 1981

Log No. 6 - Primary Plant Log, November 24 - December 31, 1981

Log No. 7 - Secondary Plant Log, November 24 - December 31, 1981

Log No. 8 - Unavailable Equipment Status Log, November 24.-

December 31, 1981

Night Orders, November 24 - December 22, 1981

Lifted Lead and Jumper Log - All active

Tagging Requests - All active

Nonconfonnance Reports for November 1981

The inspector had no questions relative to logs reviewed during this

inspection period.

4. Plant Tour

a.

During the course of the inspections, the inspector made observations

and conducted multiple tours of plant areas, including the following;

(1)

Control Room (daily)

(2)

Relay Rooms

(3)

Auxiliary Building

(_4)

Vital Switchgear Rooms

(5)

Turbine Building

(6)

Yard Areas

(7)

Radwaste Building

(_8)

Penetration Areas

(9)

Control Point

(10) Site Perimeter

(_11) Fuel Handling Building

(12) Guard House

7

b.

The following detenninations were made:

Monitoring instrumentation. The inspector verified that selected

instruments were functional and demonstrated parameters within

Technical Specification limits.

Valve positions. The inspector verified that selected valves were

in the position or condition required by Technical Specifications

for the applicable plant mode. This verification included exam-

ination of control board indication and field observation of valve

positions (Charging/Safety Injection, Auxiliary Feedwater, and

Containment Spray Systems).

Radiation Controls.

The inspector verified by observation that

control point procedures and posting requirements were being

followed.

Plant housekeeping conditions. The inspector observed that with

limited exceptions, housekeeping was generally acceptable.

Any *

cluttered or littered areas for which maintenance was not in

progress, was brought to the attention of the plant management or

operating staff.

Fluid leaks.

No fluid leaks were observed which had not been

identified by station personnel and for which corrective action

had not been initiated, as necessary.

Piping vibtation.

No excessive piping vibrations were observed and

no adverse conditions were noted.

Selected pipe hangers and seismic restraints were observed and no

adverse conditions were noted.

Equipment tagging. The inspector selected plant components for

which valid tagging requests were in effect and verified that the

tags were in place and the equipment in the condition specified.

By frequent observation through the inspection, the inspector

verified that control room manning requirements of 10 CFR

50.54

(k) and the Technical Specifications were being met.

In addition,

the inspector observed shift turnovers to verify that continuity of

system status was maintained. The inspector periodically questioned

shift personnel relative to plant conditions and their knowledge of

emergency procedures.

Releases.

On a sampling basis, the inspector verified t.hat appro-

priate documentation, sampling, authorization, and monitoring

instrumentation were provided for effluent releases.

8

Fire protection. The inspector verified that selected fire ex-

tinguishers were accessible and inspected on schedule, that fire

alarm stations were inspected on schedule, that fire alarm stations

were unobstructed and t.hat cardox systems were operable.

Technical Specifications. Through log review and direct observa-

tions during tours, the inspector verified compliance with Technical

Specifications including Limiting Conditions for Operation (LC0

1s).

The following parameters were sampled frequently:

RWST level, BAST

level and temperature, containment temperature, boration flow path,

offsite power, BAST and Accumulator chemistry.

In addition, the

inspector conducted periodic visual checks of protective instrumen-

tation and inspection of electrical switchboards to confirm avail-.

ability of safeguards equipment.

Security.

During the course of these inspections, observations

relative to protected and vital area security were made, including

access controls, boundary integrity, search, escort, and badging.

c. The following acceptance criteria were used for the above items:

Technical Specifications

Operation Directives Manual

Inspector Judgement

d.

During control room reviews, the inspector noted that the Unit 2 Refueling

Water Storage Tank (RWST) temperature was 55-60°F while the Unit 1 RWST

was maintained at 80-850F.

The recirculating pump to the heating water

heat exchanger was in service but the depressed temperature was of con-

cern due to expected cold weather. Technical Specification 3.1.2.6 sets

a minimum temperature of 350F.

Examination of the heat exchanger revealed

that recirculation (RWST) temperatures were identical into and out of the

heat exchanger at approximately 550F.

Heating water exceded 2000F and

the return was at ambient, approximately 700F.

Following the inspector's

expression of concern that the heat exchanger was not functioning, the

licensee determined that the heating water side was fouled with debris.

The heat *exchanger was-cleaned and an RWST temperature of 900F.,established

prior to conclusion of the inspection.

e. The inspector had no further questions relative to tours made during this

inspection.

9

5.

Review of Periodic and Special Reports

Upon receipt, periodic and special reports submitted by the licensee

pursuant to Technical Specifications 6.9.1 and 6.9.2 were reviewed by

the inspector.

This review included the following considerations:

The report included the information required to be reported by

NRC requirements;

Test results and/or supporting information were consistent with

design predictions and performance specifications;

Planned corrective action was adequate for resolution of identified

problems; and,

~

Determination whether any information in the report should be

classified as an abnormal occurrence.

Within the scope of the above, the following periodic reports were reviewed

by the inspector:

Unit 1 Monthly Operating Report - Octobe*r and November 1981

Unit 2 Monthly Operating Report - October and November 1981

No unacceptable conditions were identified.

6. .IE Circular Followup

a.

For the IE Circulars listed below, the inspector verified that the

Circular was received by the licensee management, that a review for

applicability was performed, and that if the circulars were applicable

to the facility, appropriate corrective actions were taken or were

scheduled to be taken.

81-02, Performance of NRG-Licensed Individuals While on Duty.

The licensee's review of this Circular concludes that all

appl i cable information is included in statti1ennAdmi ni strative

Procedure AP-5, Operating Practices Program, Revision 11,

dated August 13, 1981.

81-04, The Role of Shift Technical Advisors and Importance of

Reporting Operational Events.

In a memorandum dated July 30,

1981, the licensee concludes that the concerns identified in

this Circular are also covered by AP-5.

In addition, the

inspector noted that AP-6, Incident Report and Reportable

Occurrence Program, Revision 7, dated October 8, 1981, also

covers the subject in detail.

10

81-05, Self-Aligning Rod End Bushings for Pipe Supports. The

inspector reviewed Safety Evaluation S-C-R600-MSE-112,

Revision 0, dated November 4, 1981, entitled, Spherical

Bearing Disengagement Review for Safety Related Snubbers

Salem Nuclear Generating Station No. 1 and 2 Units.

The

evaluation documents the inspection of all supports subject

to the problem.

With the exception of two, potential for

bushing disengagement was absent.

The two remaining supports

are included in the in-service inspection program.

81-08, Foundation Materials. The licensee reviewed the Circular

for applicability to Salem and$in a memorandum dated July

29, 1981, documented the following information. All seismic

Category 1 structures at Salem are on lean concrete fill

not on compacted soil. Other buildings are on steel piers.

81-12, Inadequate Periodic Test Procedure of PWR Protection System.

The licensee's review of this Circular is documented in a

memorandum dated September 24, 1981. Station surveillance

procedures test b.oth the shunt trip coil and the undervoltage

coil for the reactor trip breakers and post-trip position is

verified at the control console.

The inspector had no questions relative to Circulars reviewed.

7.

Licensee Events

a.

In Office Review of Licensee Event Reports

The inspector reviewed LERs submitted to the NRC:RI office to verify

that details of the event were clearly reported, including the accuracy

of the description of cause and adequacy of corrective action. The

inspector determined whether further information was required from the

licensee, whether generic implicatfons were involved, and whether the

event warranted onsite followup.

The following LERs were reviewed:

UNIT 1

81-83/03L

-

No. 12 Charging Pump Inoperable Due to Oil Cooler

Service Water Leak

81-84/0lT

-

Service Water Leak in Containment - No. 11 Containment

Fan Coil Unit Bottom Primary Coil

81-85/03L

-

No. 12 Charging Pump Inoperable Due to Oil Cooler

Service Water Leak

81-86/03L

-

No. 11 Containment Fan Coil Unit Inoperaole on Two

Occasions Due to Loss of Service Water Flow Indication

11

81-87/04L

-

Impingement of Three Sea Turtles on Circulating Water

Intake Trash Bars

81-88/03L

No. 2 Fire Pump Inoperable Due to Cracked Battery Cable

Clamp

81-89/03L

-

Containment Air Lock Inoperable Due to Damaged Seals -

100

1 Elevation

81-90/03L

-

No. 12 Component Cooling Water Heat Exchanger Inoperable

Due to Failed Dissimilar Metal Drain Line Weld

81-91/03L

-

Pressurizer Level Channel 3 Inoperable - Instrument

Drift

81-92/0lT

-

Service Water Leak in Containment - No. 15 Containment

Fan Coil Unit Secondary Coil

81-93/03L

-

No. 1 Fire Pump Inoperable Due to Broken Fuel Pump

Shaft

81-94/0lT

-

Service Water Leak in Containment - No. 14 Containment

Fan Coil Unit Primary Coils (2)

8l-95/03L

-

Containment Sump Level Monitoring System Inoperable Due

to Auxiliary Alarm Annunciator Failure

81-96/0lT

-

Service Water Leak in Containment - No. 11 and No. 15

Containment Fan Coil Units Primary and Secondary Coils

81-97/0lT

-

Boron Injection Tank Inlet Valves Failed to Fully Open

During Inadvertent Safety Injection

81-98/03L

-

Auxiliary Feedwater Storage Tank Below Minimum Volume

Following Reactor Trip

81-99/03L

-

No. 12 Containment Fan Coil Unit Inoperable Due to Loss

of Service Water Flow Indication

81-100/03L -

Intennediate Range Nuclear Instrumentation Channel 1

Inoperable Due to Failed High Voltage Power Supply

81-101/03L -

Pressure Decrease Below DNB Limit For Five Minutes Due

to Operation of Auxiliary Spray Valve

12

81-102/03L -

Failure to Isolate Inoperable PORV In Accordance With

License Amendment 39

81-103/03L -

Intermediate Range Detector N-36 Inoperable Due to

Failed High Voltage Power Supply

81-104/03L -

No. 13 Steam Generator Steam Flow Channel 1 Inoperable -

Instrument Drift

81-105/0lT -

Service Water Leak in Containment - No. 12 Containment

Fan Coil Unit Primary Coil

8l-106/03L -

Penetration Fire Barriers Inoperable - Fire Doors

81-107/03L -

Inadvertent Safety Injection Due to Loss of lA Vital

Instrument Inverter

'

81-108/0lT -

Service Water Leak in Containment - No. 14 Containment

Fan Coil Unit Primary Coil

81-109/0lT -

Service Water Leak in Containment - No. 12 Containment

Fan Coil Unit Primary Coil

81-110/03L -

Inadvertent Safety Injection Due to Loss of lA Vital-

Instrument Inverter

81-111/03L -

No. 11 Containment Fan Coil Unit Inoperable Due to

~

'*

--

81-112/03L

Open Breaker Trip Shutter

-

Auxiliary Feedwater Storage Tank Low Level Following

Reactor Trip

UNIT 2

81-97/03L

81-98/03L

81-99/03L

-

Individual Rod Position - 2D2 - Inoperable

Individual Rod Position Indication - 1D4, 1D3, 2D2,

and 2D3 - Inoperable

-

No. 23 Containment Fan Coil Unit Inoperable Due to

Loss of Service Water Flow Indication

81-100/03L -

No. 22 Reactor Coolant Loop Flow Channel 2 Inoperable

Due to Transmitter Failure

81-101/03L -

Radiation Monitor 2R12A Inoperable Due to Failure of

Battery Pack

13

81-102/0JL -

No. 22 Reactor Coolant Loop Flow Channel 2 Inoperable

Due to Transmitter and Equalizing Valve Assembly

Failure

81-103/0JL -

No. 24 Containment Fan Coil Unit Inoperable Due to

Loss of Service Water Flow Indication

81-104/0lT -

Failure.to Comply With Operating License Condition

Relating to Cable Fire Wrapping

81~105/03L -

No. 21 Steam Generator Level Channel 2 Inoperable Due

to Loss of Calibration

81-106/03L

Isolation Damper 2CAA4 Inoperable Due to Lack of

Lubrication

81-107/03L -

Trip of 2B Diesel Generator Due to High Jacket Water

Temperature

81-108/03L -

Individual Rod Position Indication - 2Cl and 2D2 -

Inoperable

81-109/03L -

2A Safeguards Equipment Control Inoperable

  • *

81-110/03L -

No. 21 and 23 Containment Fan Coil Units Inoperable

Due to Loss of Service Water Flow Indication

81-lll/03L -

Reactor Coolant System Pressure and Tavg Below DNB

Limits For Five Minutes Due to Over-Boration

81-112/03L -

Containment Air Lock Inoperable - 100' Elevation

81-ll3/03L -

Containment Spray Additive Tank High Level

81-114/0lT -

Service Water Leak in Containment - No. 22 Containment

Fan Coil Unit Motor Cooler

81-115/0lT -

Service Water Leak in Containment -*No. 24 Containment

Fan Coil Unit

  • .--

81-ll6/03L -

No. 22 Charging Pump Inoperable Due to Broken Impeller

Shaft

81-117/03L -

No. 21 and 22 Containment Fan Coil Units Inoperable

Due to Failed Limit Switch and Loss of Service Water

Flow Indication

_,

14

b.

Onsite Licensee Event Followup _

(1)

For those LERs selected for onsite followup (denoted by asterisks

in detail paragraph 7), the inspector verified the reporting require-

ments of Technical Specifications and Regulatory Guide 1.16 had been

met, that appropriate corrective action had been taken, that the event

was reviewed by the licensee as required by AP-4 and 6, and that con-

tinued operation b,f the facility was conducted in accordance with

Technical Specification limits. The following findings relate to the

LERs reviewed on site:

UNIT 1

81-84/0lT

81-92/0lT

81-94/0lT

81-96/0lT

81-105/0lT

81-108/0lT

81-109/0lT

Each of these events details a service water leak in

containment due to a Containment Fan Coil Unit (CFCU)

tube pinhole leak, typically 0.5 to 1.0 gpm.

In each

case, the cooler service water side is isolated to stop

the leak and one of several repair options pursued.

In

some cases, a cooler bundle is isolated by blank flanges.

As discussed in NRC Inspection Report 50-272/81-25, this

procedure_ is acceptable as long as the remaining heat

removal capacity of the unit is within design limits.

Repairs to leaking tubes using brazing techniques have

been successful but only in cases that are accessible

for the process. The majority of the leaks identified

in these LER's were repaired by applying Belzona metal

filler to the outside of the tube at the leak location.

No subsequent failure of a repair made with this metal-

epoxy filler has occurred. All CFCU coils are scheduled

to be replaced with new material at the next outage.

In

attempting to determine the acceptability of the metal

filler repair in this application, the inspector found

no documentation of any evaluation done by the licensee.

Engineering Department concurrence is implied by disposi-

tion of Deficiency Reports which state that the material

is to be employed.

However, no basis for this determina-

tion is provided. Failure to provide written documentation

to justify a maintenance action which constitutes a change

in the facility contributes to noncompliance with 10 CFR

50.59 (272/81-29-04 ' 311/81-29-03}~

81-86/03L

Loss of service water flow indication to Containment Fan

81-99/03L

Coil Units has been a recurring problem.

The licensee

is currently blowing down transmitters weekly to reduce

the adverse effects of silting. Evaluation of alternate

sensing line configurations is underway.

The inspector

had no further questions at this time. These events do

not impede actual availability of service water to cool

the CFCU's.

15

--

81-87/04L

This event report details three occasions on which

endangered or threatened species of sea turtles were

recovered from the plant circulating water system.

By corre~pondence dated December 10, 1981, the licensee

responded to an Office of Nuclear Reactor Regulation

request, dated November 17, 1981, for additional in-

formation on the subject.

The inspector had no further

questions.

--

81-90/03L

This report detailed a service water leak from a Com-

ponent Cooling Heat Exchanger drain line dissimilar

weld.

Temporary repairs were effected by cutting the

pipe, capping and welding.

The inspector confirmed that

this repair was properly dispositioned in Deficiency

Report No. MD 1034 and that a Work Order has been written

to accomplish a permanent repair at the next outage.

The

inspector had no further questions.

--

81-97/0lT

Durn.ng an inadvertent safety injection on November 6, 1981,

Boron Injection Tank inlet valves 1SJ4 and 1SJ5 failed to

open fully. The valves were subsequently opened by remote

operation from the control room.

The initial cause was

attributed to boron precipitate on the valve stems. It

was also determined that the valve operator torque settings

were set at a value of 2 in a recommended range of 2 to

3.5. Corrective action included increasing the torque

setting to 3.

The licensee's evaluation of'this event and

the torque settings on the operators is continuing and will

be included in a supplemental report. It was noted that

the valves functioned normally on an inadvertent safety

injection one week prior to this event. Further investi-

gation showed that the valves had been cycled and met

acceptable stroke times within 30 days of this event. This

item remains unresolved pending completion of the licensee's

evaluation and submission of a supplemental report (272/81-

29-02).

81-101/03L While troubleshooting pressurizer auxiliary spray valve

1CV75, pressurizer pressure decreased below the Technical

Specification DNB limit for a period of less than five

minutes.

The cause was slow operation of the valve due

to an incorrect air operator liftoff pressure in this

application of the valve.

The liftoff pressure was in-

creased and satisfactory operation achieved. The lowest

primary system pressure reached was 2175 psig based on the

inspector's review of plant records.

No other air operated

valves were identified which would be subject to a similar

problem.

The inspector had no further questions on this

event.

--

81-102/03L

--

81-106/03L

--

81-110/03L

--

81-111/03L

16

Amendment 39 to Unit 1 Facility Operating License DPR-70

provided new Technical Specifications for Power Operated

Relief Valves (PORV} and requires that, with one or more

PORV inoperable, all associated block valves be closed

and power removed from the valves. The amendment was

issued on October 8, 1981 and, at that time, the PORV

had been declared inoperable due to leakage and the block

valves closed from the control console.

By October 21,

1981, the license amendment had not been received by

operating personnel and, therefore, the additional require-

ment of removing motive power had not been accomplished.

When the licensee was informed of the new requirement by

the inspector, the power was removed.

After discussions

with station and corporate management, the inspector de-

termined that new procedure*s' will be employed to ensure

timely dissemination of new requirements to operating

personnel. *The inspector had no further questions.

Following surveillance of fire doors, the licensee deter-

mined that several did not meet acceptance criteria. In

accordance with Technical Specifications, fire detectors

were confirmed operable and a fire patrol established.

Due to continuing problems with doors, the patrol is still

in effect at the conclusion of the inspection period.

The

licensee has initiated design change 1 EC-1333 to improve

the serviceability of fire doors and will submit a supple-

mental report. This item is unresolved pending insp~ctor

review of permanent corrective action (272/81-29-05)_.

This inadvertent safety injection is detailed in NRC In-

spection Report 50-272/81-27.

The interaction between

inverter control cabling and cooling fan power leads has

been reduced by rerouting of the cables.

In addition,

administrative controls have been applied to ensure that

no work in the inverters is attempted while the plant is

in a condition susceptible to inadvertent safety system

actuation om loss of an inverter. The inspector had no

further questions.

During the above safety injection, CFCU 11 failed to start

automatically in slow speed.

The cause was determined as

failure of the breaker shutter to close when the breaker

had last been rack,ed in, resulting in automatic trip on

closure. Previous observed practice had included testing

and surveillance following equipment maintenance which

should have detected this condition.

In this particular

case, the unit had been isolated and tagged for elective

maintenance and, before any work started, had been cleared

and declared operable. Since no work had been done, no

operational test was conducted.

17

81-111/03L The licensee, in Operating Memorandum 15, requires an

(Continued} operational test of all safety related pumps following

the removal of tags, whether or not work has been

accomplished on the equipment. This requirement had

not been applied to CFCU's.

Recognizing the potential

of inoperability due to improper rack-in of breakers,

the licensee will include CFCU's in the OM-15 guidance.

This will be confirmed by the inspector(272/81-29-03).

--

81-112/03L Technical Specifications require that Auxiliary Feed-

water Storage Tank level be maintained above 94 percent

UNIT 2

81-98/03L

81-103/03L

81-110/03L 81-117 /03L

81-101/03L

--

81-104/0lT

in Modes 1, 2, and 3. This event is typical of several

in which, following a reactor trip, automatic initiation

of auxiliary feedwater results in decreased tank levels

before manual makeup valves can be opened to supply

demineralized water to the tank.

To alleviate this pro-

blem, the licensee has initiated design changes to provide

a tank leV-~l alarm before the Technical Specification

limit is reached and also to provide remote operation of

the makeup valve from the console. These modifications

will be accomplished during the January outage on Unit 1

and during the next refueling outage on Unit 2. These

actions will be confirmed during followup on a previous

item of noncompliance related to this issue.

These events detail losses of service water flow indi-

cation to Containment Fan Coil Units.

Comments under

Unit 1 LER 81-86 above apply to these events.

On October 28, 1981, the licensee supplemented this LER

to provide additional information. Failure of the radiation

monitor battery pack on loss of power was attributed to a

design error in that too many batteries were installed,

leading to overcharging and internal shorts. The design

modification to reduce the number of batteries has been

accomplished.

Periodic surveillance of the battery power

supply is accomplished during preventive maintenance of

the system by procedure. This problem is not applicable

to Unit 1 which has a different radiation monitoring system.

The inspector had no further questions.

On October 9 and November 18, 1981, the licensee supple-

mented this LER to list all additional areas in which fire

protection cable wrap had not been properly applied. Based

on complete verification by engineers in the field, the

licensee states that all required wrapping to support

alternate shutdown has been completed.

Further details of

this event are provided in NRC Inspection Report~ 50-311/

81-21.

The inspector had no further questions.

18

--

81-106/03L When reviewing this event, the inspector determined that

no periodic lubrication of damper operating gear is per-

fonned because the device is not required to be lubricated

by design.

The licensee is evaluating design modifications

to improve damper operability. Periodic testing provides

necessary assurance of availability of the dampers.

The

LER will be supplemented to provide a more complete dis-

cussion of corrective measures. This item remains unre-

solved (311/81-29-0lf.

--

81-107/03L 28 Diesel Generator tripped on surveillance testing due to

loss of service water to the jacket water cooling system.

The inspector noted that on safeguards start of the diesel

generator, this trip is bypassed and that sufficient time

would be available to restore cooling if the diesel were

required for safeguards loads. The inspector had no

further questions.

--

81-lll/03L During boration of the primary system, an operator permitted

boric acid injection for an extended period such that pres-

sure and temperature went below the Technical Specification

DNB limit for approximately five minutes.

The LER states

that the operator failed to adhere to standard procedure

while, in fact, he failed to follow standard practice.

The procedure calls for close monitoring of rod position

and plant parameters during boration.

Due to the outmotion

rod stop, plant temperature and pressure decreased before

corrective action to secure boron addition could be accomp-

lished. The inspector had no further questions on this

item.

81-114/0lT These events detail service water leaks in containment due

81-115/0lT to leaking Containment Fan Coil Units.

Comments above with

respect to Unit 1 LER 81-84/0lT apply to these events as

well. With regard to LER 81-114/0lT, the inspector noted

that once the leak was isolated, the plant tripped.

In

order to return the plant to Mode 1 operation consistent

with Technical Specification 3.0.4, the Containment Fan

Coil Unit was declared operable with a known 0.5 gpm

service water leak.

No safety evaluation was documented

to validate safety analysis assumptions with regard to

containment integrity and containment water volume.

Since

the service water system operates well in excess of con-

tainment design pressure and since 10 gpm of identified

leakage to containment is pennitted,.a valid safety concern

appears to be absent. However, failure to document this

conclusion and its basi,s- contributes to noncompliance with

10 CFR 50.59 (311/81-29-03}.

19

--

81-116/03L The charging pump impeller shaft sheared in service and

complete replacement was accomplished. Susceptibility

of this series of shafts to failure has been identified

by Westinghouse in a Part 21 report dated August 15,

1977.

In addition, a service bulletin to owners of

susceptible shafts was issued in July 1977. During the

January 1982 outage, both Salem 1 charging pumps will be

fitted with new shafts which have been modified to pre-

vent this type of failure. Both pumps on Unit 2 now

have modified shafts. The inspector had no further

questions on this item.

c. The inspector had no further questions relative to LER

1s reviewed.

8. Operating Events

UNIT 1

At 10:27 p.m. on December 13, after placing Deborating Demineralizer 11 in

service, airborne activity in the Auxiliary Building increased. The maximum

activity measured was 3.5 E-7 uCi/cc (short lived). Investigation determined

that the resin fill valve for the demineralizer had been left open following

resin replacement earlier in the day.

An area approximately 30 feet on a

side was wetted by the resulting spill. The Demineralizer was taken out of

service and isolated within 10 minutes. Plant vent monitor 1Rl6 increased to

approximately 200,000 cpm but did not reach the alarm point which is established

to alarm prior to exceeding the instantaneous release limit. Six individuals

were found to have short lived (Rb88) contamination of their clothing, which

was allowed to decay.

The initial estimate of the release was 2 Ci of noble

gas, which is below the reporting limit of the Environmental Technical Speci-

fications.

Review of the procedure, PD-3.6.014, Ion Exchanger Resin Refilling, Revision

0, indicated that the valve was to be closed following the filling operation.

This failure to follow a procedure contributes to an item of noncompliance

with Technical Specification 6.8.1 (272/81-29-01).

UNIT 2

At~2:32 a.m. on December 15, the reactor tripped from 95 percent power due to

a low level in Steam Generator 24 after a feedwater pump trip. The cause was

not identified. Because of similar trips, the licensee instrumented 51 secon-

dary process parameters.

None of these indicated the problem.

At 8:56 a.m.,

the reactor tripped at 15 percent power due to low water level in 22 Steam

Generator. The low level was caused by personnel error while shifting from

manual to automatic level control during the startup. The unit was returned

to service at 12:25 p.m.

20

Approximately 8:00 p.m. on December 17, the plant tripped from 95 percent

power due to low steam generator level caused by loss of both feed pumps.

The pumps tripped on a valid low suction pressure condition which was

apparently caused by a large reduction in heater drain pump flow.

Operation

resumed at 6:28 a.m. on December 18.

At 7:15 a.m., operator error during

the shift of power supply to the 4KV

11G

11 non-vital electrical bus caused

the loss of 24 Reactor Coolant Pump.* Loss of the RCP caused a reactor trip

from 32 percent power.

The unit was returned to service later that day.

The licensee remained below 75 percent power until the recorded data was

reviewed and heater drain pump control was verified. Several load rejection

tests were subsequently performed but did not cause or reveal the reason

for the recurrent feed pump trips. During these tests the lowest feed

suction pressure reached was 255 psi. The trip set point is 215 psi.

The recurring series of plant trips due to loss of steam generator feed-

water pumps prompted an investigation of secondary system performance

characteristics by the licensee. This investigation included the recording

instrumentation on 51 secondary parameters and on operational relays in

the pump control circuitry. Based on observations during trips and the

series of load rejection tests conducted during the period December 18-24,

the licensee concluded that loss of feedwater suction pressure on load re-

ductions is attributable to instability in heater drain pump flow and an

apparent inability of the condensate system to compensate for the flow

changes.

Corrective measures initiated by the licensee include operation

witb a heater string bypass valve open to provide an additional condensate

flow path to the feedwater pumps.

The result has been more stable response

from the heater drain pumps and an increase in steady state feedwater suction

pressure, placing the operating pressure further from the trip point. During

full power operation at the end of the inspection period, suction pressure

was between 350-360 psig. These operational modifications appear to provide

an acceptable interim solution. Permanent design solutions are being evaluated.

9.

Nuclear Review Board

The 'inspector reviewed the minutes of Nuclear Review Board (NRB) meetings

81-01 through 81-17, conducted during the period January 25 - November 19,

1981.

The inspector had no questions with respect to the following aspects

re.viewed: meeting frequency, quorum requirements, review material, conclu-

sions reached, designation and qualifications of members, and timeliness of

minutes.

The inspector selected three license change requests submitted during the

interval (LCR

1s 81-01, 81-14, and 81-18) and confirmed that they had received

prior NRB review.

No unacceptable conditions were identified.

10.

21

Fire Protection

Supplement 4 to the Salem Nuclear Generating Station Safety Evaluation Report

(SER), dated April 1980, includes the Fire Protection SER and a listing of

nine modifications yet to be performed.

The licensee stated that all listed

modifications have been completed, except as discussed below.

The inspector

conducted a sampling review of items 27, 29, 32, 33, and 36, and confirmed

that they had been accomplished.

Item 37, dealing with alternative shutdown capability, was reviewed by the

staff in detail in May 1981, and findings from that review were documented

in Supplement 6 to the Safety Evaluation Report, dated May 1981.

Open items

were included in the Salem Unit 2 Full Power Operating license and completion

of these items is discussed in NRC Inspection Reports 50-311/81-11 and 81-13,

and 81-26.

The scope of item 37 has changed since issuance of Appendix R

and as a result of the on site review in May 1981.

The licensee has committed to completion of Appendix R backfit items for

both units, with the exception of certain aspects of III.G,(Safe Shutdown

Capability) for which exemption requests are under review by the staff.

The inspector had no further questions with respect to fire protection modi-

fications at this time.

11.

Maintenance Activities

The inspector observed maintenance activities on the following equipment:

a. 1 Spent Fuel Pool Heat Exchanger - tube leak

b.

21 Main Feed Pump - weld crack in casting plug

c. 11 Component Cooling Heat Exchanger - tube cleaning and inspection

These activities were observed to ascertain the following:

The work was

conducted in accordance with approved procedures, regulatory guides, Technical

Specifications, and industry codes or standards. The following items were

considered during this review; the limiting conditions for operation were met

while components or systems were removed from service; approvals were obtained

prior to initiating the work; activities were accomplished using approved

procedures and were inspected as applicable; functional testing was performed

prior to declaring that particular component as operable; activities were

accomplished by qualified personnel; radiological controls were implemented;

and fire prevention controls were implemented.

No unacceptable conditions were identified *

-

~

22

12. Surveillances

The inspector observed the licensee

1s performance of the following surveillance

procedures:

a. 2 PO 2.6.045 Channel Functional Test

2 LT 529 #22 Steam Generator Level Protection Channel I, Revision

1, December 23, 1981

b.

2 PO 2.6.055 Channel Functional Test

2 LT 539 #23 Steam Generator Level Protection Channel I, Revision

1, November 23, 1981

c. 2 PO 2.6.020 Channel Functional Test

2 LT 459 Pressurizer Level Protection Channel I, Revision 2,

October 5, 1981

During the performance of these tests, the inspector confirmed the following:

Testing was performed in accordance with adequate procedures; test instrumen-

tation was calibrated; limiting conditions for operations were met; removal

and restoration of the affected components were properly accomplished; and,

the test results conformed with Technical Specification and procedural re-

quirements and were reviewed by personnel other than the individual performing

the test. Any deficiencies noted were reviewed and resolved by the personnel

of the responsible department.

The personnel performing the surveillance

activities were knowledgeable of the systems and the test procedures. The

inspector confirmed that these personnel were qualified to perform the tests.

The inspector reviewed surveillance procedure SP(O) 4.6.2.2(b) Containment

Systems - Spray Additive Unit 2, Revision 0, dated April 26, 1979.

The pro-

cedure documents the semiannual determination of spray additive tank level

and NaOH concentration. Acceptance criteria established reflected only the

lower limit of each parameter.

The upper limits which are established by

Technical Specification 3.6.2.2 were not called out in the procedure. The

"as found" values were, in fact, consistent with Technical Specifications.

Failure to establish an adequate surveillance procedure contributes to an

apparent item of noncompliance with Technical Specification 6.8.1.

(272/81-29-01, 311/81-29-02).

The inspector had no further questions regarding the performance of surveillance

activities.

23

13. System Operation and Review

The inspector conducted a walk down of selected portions of plant systems.

The following drawings were used to conduct this review:

a.

Main Steam System (Unit 2) - 205303, Revision 10, dated May

1, 1980

b.

Main Feed System (Unit 2) - 205302, Revision 10, dated May

2, 1980

c. Auxiliary Feed System (Unit 2) - 205336, Revision 6, dated

April 11, 1980

d.

Auxiliary Feed System (Unit 1) - 205236, Revision 1, dated

January 12, 1981

The walk down was conducted to confirm system operability. Included in

this review was an examination of valve positions, seismic restraints and

supports, leaks, local indicators and instrumentation, unusual noise or

vibrations, overheated equipment, and system conformance with "as built"

drawings.

No unacceptable conditions were identified.

14. Unresolved Items

Areas for which more information is required to determine acceptability are

considered unresolved. Unresolved items are contained in Paragraph 7.

15. Exit Interview

At periodic intervals during the course of this inspection, meetings were

held with senior facility management to discuss inspection scope and findings.