ML18086B314

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Notice of Violation from Insp on 811124-1231
ML18086B314
Person / Time
Site: Salem  PSEG icon.png
Issue date: 02/02/1982
From: Starostecki R
NRC OFFICE OF INSPECTION & ENFORCEMENT (IE REGION I)
To:
Shared Package
ML18086B313 List:
References
50-272-81-29, 50-311-81-29, NUDOCS 8202190323
Download: ML18086B314 (2)


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APPENDIX A NOTICE OF VIOLATION Public Service Electric and Gas Company Salem Nuclea~ Generating Station, Units l and 2 e

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Docket Nos. 50-272; 50-311 License Nos. DPR-70; DPR-75 As a result of the inspection conducted on November 24 - December 31, 1981, and in accordance with the Interim Enforcement Policy, 45 FR 66754 (October 7, 1980), the following violations were identified:

A..

10 CFR 50.59 authorizes changes 'in the facility and proe!3dures provided these changes do not constitute an unreviewed safety question~ 10 CFR 50.59 further requires that the licensee maintain on record a written safety evaluation which provides the basis for this detennination *

. Contrary to the above, (1)

On several occasions during 1981, the licensee repaired leaking tubes in Containment Fan Coil Units by applying a metal-epoxy filler compound to the leak area.

No safety evaluation was made to provide a basis for acceptability of this repair. The FSAR describes copper-nickle fan coil tubes.

(2)

On November 19, 1981, the licensee declared CFCU 22 operable with a known 0.5 gpm service water leak from the motor cooler.

No written safety evalu-ation was made to provide the basis for this determination. The FSAR de*

scribes the cooling coil tubes as completely closed within the containft1ent.

This is a Severity Leve*l nt Violation (Supplement I) applicable to DPR-70 and DPR-75.

B.

Technical Specification 6.8. l requires that written.. procedures be established~

implemented, and maintained for. surveillance activities and for those activities listed in Appendix A to Regulatory Guide L33.

Contrary to the above, (1)

On December 14, 1981, there was no surveillance procedure to assure com-pliance with Technical Specification 3.6.2.2. The procedure in use, SP(O) 4.6.2.2(b), Containment Systems - Spray Additive Unit No. 2, did not spec-ify the upper limits of level and NaOH concentration as dictated by Tech-nical Specification 3.6.2.2.

(2)

On December 13, 1981, a technician failed to follow procedure PD-3.6.014, Ion Exchanger Resin Refilling, in that the resin fill valve was not closed prior to plaCing Deborating Demineralizer 11 in service. This procedure is required by Regulatory Guide l.33

  • OFFlCE~

SURNAME..

. -*.------*--~

'. 8202190323 820202

' ~********** ********************* ********************* ********************* *********************

DATE~ PDR ADOCK 05000272 I

~~- G PDR*

NRCFORM318110/80lNRCM0240 OFFICIAL RECORD COPY

-il USGPO: 1980-329*824

Appendix A 2

(3)

As of December 31, 1981, the licensee had not provided an emergency in-struction for loss of pressure control, specifically, loss of pressurizer heaters. This procedure is required by Regulatory Guide 1.33.

This is a Severity Level V Violation (Supplement I} applicable to DPR-70 and DPR-75.

Pursuant to the provisions of 10 CFR 2.201, Public Service Electric and Gas Company is hereby required to submit to this office within thirty days of the date of this Notice, a written statement or explanation in reply, including: (1) the corrective steps which have been taken and the results achieved; (2) corrective steps which will be taken to avoid further violations; and (3) the date when full compliance will be achieved. Under the authority of Section 182 of the Atomic Energy Act of 1954, as amended, this response shall be submitted under oath or affirmation. Where GCl.Bia good cause is shown, consideration will be gi~*

en 1

ng your_ respons time

  • Date FEB 2 1982

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..:~xu:_,

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Ricnard W. Starost

, irector Division of Resid t

~ Project Inspection OFFICE~

. SURNAME. * ** ************* * ****.**** * ***************** : ********************* **************: ******.********* ; ************** * ****************** *******************'*.

DATE.

NRC.FORM 318 110/801 NRCM-0240

  • OFFICIAL RECORD COPY

>> USGPO: l980-329*824