ML18033B591
| ML18033B591 | |
| Person / Time | |
|---|---|
| Site: | Browns Ferry |
| Issue date: | 12/17/1990 |
| From: | Kellogg P, Patterson C NRC OFFICE OF INSPECTION & ENFORCEMENT (IE REGION II) |
| To: | |
| Shared Package | |
| ML18033B589 | List: |
| References | |
| 50-259-90-33, 50-260-90-33, 50-296-90-33, NUDOCS 9012280320 | |
| Download: ML18033B591 (79) | |
See also: IR 05000259/1990033
Text
UNITED STATES
NUCLEAR REGULATORY COMMISSION
REGION II
101 MARIETTASTREET, N.IN.
ATLANTA,GEORGIA 30323
Report Nos.:
50-259/90-33,
50-260/90-33,
and 50-296/90-33
Licensee:
Valley Authority
6N 38A Lookout Place
1101 Market Street
Chattanooga,
TN
.37402-2801
Docket Nos.:
50-259,
50-260,
and 50-296
License Nos.:
and
Facility Name:
Browns Ferry Units 1, 2,
and
3
Inspection at Browns Ferry Site near Decatur,
Inspection
Conducted:
October
16 - November
16,
1990
Inspector:
C. A.
i
Accompanied
by:
E.
W.
K.
G.
E.
p.
B.
M.
inator
Christnot,
Resident
Inspector
Bearden,
Resident
Inspector
Ivey, Resident
Inspector
Humphrey,
Resident
Inspector
Lea, Reactor
Inspector
Taylor, Reactor Inspector
Collins,
NRC Consultant
Branch, Sr. Resident
Inspector
Da e Signed
Approved by:
Inspec
>on
grams,
TVA Projects Division
SUMMARY
It'te i ne
Scope:
This routine resident inspection
included surveillance observation,
maintenance
observation,
MIC,
operational
safety
verification, modifications,
post
modification testing,
SPOC,
restart
test
program,
reportable
occurrences,
actions
on
previous
inspection
findings,
TMI action
items,
Bulletins
and
Generic Letters,
ATWS, restart
assessment,
and
gA activities.
0
9012280320
901217
ADQCK 05000259
6
0
0
Results:
A Violation with
three
examples
was
identified for failure to
make
and
50.73 reports,
paragraph
5.
The licensee
made
a decision at
the time of occurrence
of each
event not to report the item.
One example
was
reported
10
days
after
the
event
after
the
inspector
questioned
the
reportability.
The other
examples
have not been reported.
This violation is
similar to
a violation contained
in
IR 89-27.
The
licensee
not
being
conservative
in meeting the reporting requirements
of 10 CFR 50.72
and 50.73.
A URI was identified concerning failure to maintain configuration control in
the
CS system after the system
SPOC,
paragraph
5.
The inspector i4entified two
electrical
disconnected
on
the
CS testable
check
75-54
valve disc
position indicator.
A URI was identified for failure to control design
by allowing an unqualified
cable installation,
paragraph
6..
The licensee installed several
thousand feet
of unjacketed
cable
in
EQ modifications.
Also, another
type of cable
previously identified
as
not suitable for
EQ modifications
was installed.
Problems
have
been
identified with
Power
Stores
control
and
issuance
of
materials.
An IFI was identified for hardware activities
delayed
but not approved
by
Senior
Management,
paragraph
8.
The Plant Manager approves all
SPOC deferrals
and exceptions.
Other methods
are
used to defer work which are not approved.
These
methods
are refer red to as work arounds,
break the tie,
and punchlist.
An IFI was identified for review of the licensee's
QA control process
related
to calculations,
paragraph
11.,
Two different versions of a
QA recor'd for the
same calculation were supplied to the inspector during the inspection.
An IFI
was identified for
RPS/ARI diversity during the
ATWS inspection,
paragraph
14.
This is
a generic industry issue
and not
a restart
item.
Except
for this
item the licensee
has
adequately
met the requirements
of the
rule.
A recent
negative
trend
was identified in
QA activities,
paragraph
16.
The
total
number of CAQRs/PRDs increased.
The number of delinquent
CAQRs increased
from 33 to
51 in one month.
Two
CAQRs were closed out prematurely.
Two more
examples
of
bypassed
holdpoints
were
identified
and
are
considered
additional
examples of Violation 259, 260, 296/90-27-03.
Two more
examples
of Violation 259,
260, 296/90-29-01
concerning
performance
of work activities without
an
adequate
hold order clearance
boundary
were
identified, paragraph
16.
REPORT
DETAILS
Persons
Contacted
Licensee
Employees:
'*0. Zeringue, Site
Director'L.
Myers, Plant Manager
- M. Her rell, Operations
Manager
J. Rupert, Project Engineer
R. Johnson,
Modifications Manager
- B. McKinney, Technical
Support Manager
R. Jones,
Operations
Superintendent
A. Sorrell, Maintenance
Manager
G. Turner, Site equality Assurance
Manager
- P. Carier, Site Licensing Manager
- P. Salas,
Compliance Supervisor
J.
Corey, Site Radiological Control Manager
R. Tuttle, Site Security Manager
Other
licensee
employees
or
contractors
contacted
included
licensed
reactor operators,
auxiliary operators,
craftsmen,
technicians,
and public
safety officers;
and quality assurance,
design,
and engineering
personnel.
NRC Personnel;
- C. Patterson,-Restart
Coordinator
- E. Christnot, Resident
Inspector
- h'. Bearden,
Resident
Inspector
- K. Ivey, Resident
Inspector
- G. Humphrey, Resident
Inspector
~Attended exit interview
Acronyms used throughout this report are listed in the last paragraph.
Surveillance
Observation
(61726)
The inspectors
observed
and reviewed the performance of required SIs.
The
inspections
included
reviews
of the
SIs for technical
adequacy
and
conformance
to
TS,
verification of test
instrument
calibration,
observations
of the conduct of testing,
confirmation of proper
removal
from service
and return to service of systems,
and reviews of test data.
The inspectors
also verified that
LCOs were met, testing
was accomplished
by qualified personnel,
and
the
were
completed within the required
frequency.
The following SIs were reviewed during this reporting period:
l
'
n
e
a.
, Calibration of Steam Line Flow Instrumentation.
b.
Core
and Containment
Cooling Systems
Reactor
Low Pressure
Instrument
Channel
8 Calibration, 2-SI-4.2.B-7(B).
c.
4KV Shutdown
Board Undervoltage Start Generator,
1 5 2 SI-4.9.A.4.b.
d.
The performance
of 3-SI-4.9.A.3.a,
Common Accident Signal
Logic was
observed.
This
was
being conducted
to satisfy
PMT requirements
. for several
ECNs.
The inspector
observed
the SI from all'f the work
locations
including the Unit 3 control
room, the Unit 2 auxiliary
instrument
room,
and
both Unit 3
4160V shutdown
board
rooms.
No
deficiencies
were identified with the SI procedure
or the conduct of
the test.,
No violations
or
deviations
were
identified
in
the
Surveillance
Observation
area.
3.
Maintenance
Observation
(62703)
Plant
maintenance
activities
were
observed
and
reviewed for selected
safety-related
systems
and
components
to ascertain
that
they
were
conducted
in accordance
with requirements.
The following items
were
considered
during
these
reviews:
LCOs
were
met, activities
were
accomplished
using
approved
procedures,
functional testing
and calibra-
tions were performed prior to returning components
or systems
to service,
gC
records
were maintained,
activities
were
accomplished
by qualified
personnel,
parts
and materials
used were properly certified, proper tagout
clearance
procedures
were
followed,
and
radiological
controls
were
implemented
as required.
Work documentation
(MR,
WR,
and
WO) was
reviewed to determine
the status
of outstanding
jobs
and to assure
that priority was assigned
to'quipment.
maintenance
which might affect plant safety.
The inspectors
observed
the
following maintenance activities during this reporting period:
0
a ~
Electrical
Cable Splices
The
inspector
reviewed activities
in progress,to
replace
non-
environmentally qualified electrical
cable
splices
with qualified
splices.
This work was
performed
per
MR C031646
and dealt with
Raychem
terminations
on
Rosemont
seals
that
had
been
installed
to seal
the jackets
of TVA field cables.
The inspected
splice
was
located inside Junction
Box 106B inside the Unit 2 reactor building.
The inspector
observed
that the work activities were performed
per
the steps
in the procedure
and that
a
gC inspector
was monitoring the
work in progress.
No discrepancies
were noted during the inspector 's
review of the activities.
l
'
b.
Calibration of Steam Line Flow Instrumentation
Maintenance
activities to investigate
and repair false indications
of main steam line flow were observed
by the inspector.
This effort
consisted
of a "troubleshoot
and repair activity" of the Unit 2 main
steam
line
"B" flow indication
instrumentation.
However,
the
instructions
specified
that if. any
work efforts
outside
of the
instrument
and
loop calibrations
were required,
an
MR was to
be
generated
for those activities.
The inspector
noted that the
MR was originally issued
in October of
1989.
The instruments
could not be calibrated at that, time because
of calibration
procedure
problems.
The calibration
procedure
was
revised
and calibration of the transmitter
was in the
process
of
being re-performed.
Procedure
steps
were performed in the specified
order.
Proper authorizations
were obtained prior to the beginning
of
work activities.
No deficiencies
were
noted
during
the
review of this work.
C.
Overcurrent Trip Device
The inspector received
information that
a type EC-2A overcurrent trip
device
that
had
been
sent
to
GE Atlanta for refurbishment
was
impacted
by
The
licensee
issued
CARR
BFP
900365,
documenting that the trip unit subcomponents
did not conform to the
vendor
assembly
drawing.
The inspector
inspected
the trip device
and
noted
that
the
following from Attachment I,
Supplement
I applied:
COMPONENT
Magnetic structure
pole-piece
laminations
ORIGINAL GE
)
Fastened
with
rivets
REFURBISHED
Fastened
with split
pins (also called
roll-pins)
EC-2A dashpot fasteners
Riveted to frame
Bolted to frame with
nuts
and machine
screws
It was also
noted that the
NO block, catalog part or drawing number,
on the
name plate
was
stamped
instead of printed.
The inspector will
monitor the licensee's
activities in dispositioning the
CARR.
No violations or deviations
were identified in the maintenance
observation
area.
4.
Microbiological Induced Corrosion
The inspectors
reviewed
the status
of the licensee's
MIC program dealing
with the
raw water
systems
at
BFNP.
This
consisted
of reviewing
correspondence
between
the Commission
and the licensee
associated
with GL 89-13
and the activities that were on-going.
The
licensee's
respondse
to
was
a list of activities
and
commitments
in
a letter from Mark 0.
Medford to the
Commission,
dated
March 16,
1990.
The response
addressed
only the
RHRSW and .the
EECW which
serve
to transfer
heat
from safety-related
structures,
systems
and
'components
directly to
the
ultimate
heat
sink
and
included
eight
,commitments.
The
inspectors
reviewed
this
issue
with the
licensee's
personnel
responsible for the
MIC program.
This discussion
involved the licensee's
use of metal
coupons
to establish
corrosion rates
and the evaluation of
inhibitors to
be
used
in these
systems
which also
included
the
system.
In addition,
the licensee
indicated that more than
300 feet of
the
system
has
been
replaced.
The carbon steel
piping in the
two
safety-related
systems,
RHRSW and
EECW, with
a diameter of less
than
4
inches
has
been replaced.
The status
of the
MIC program will be routinely monitored
in future
inspections.
Operational
Safety Verification (71707)
The
NRC inspectors
followed the overall plant status
and any significant
safety matters
related to plant operations.
Daily discussions
were held
with plant management
and various
members of the plant operating staff.
The
inspectors
made
routine visits to the control
rooms.
Inspection
observations
included
instrument
readings,
setpoints
and
recordings,
status
and alignments
systems,
ver ification of onsite
and offsite power
supplies,
emergency
power sources
available for automatic operation,
the
purpose of temporary
tags
on equipment controls
and switches,
alarm status,
adherence
to procedures,
adherence
to
LCOs,
temporary
alterations
in effect, daily journals
and logs,
and control
room manning.
This inspection activity also
included
numerous
informal discussions
with
operators
and'supervisors.
General
plant tour's
were conducted.
Portions of the turbine buildings,
each reactor building, and general. plant areas
were visited.
Observations
included
valve
position
and
system
alignment,
and
hanger
conditions,
instrument
readings,
housekeeping,
power supply
and breaker
alignments,
radiation
and
contaminated
area
controls,
tag controls
on
equipment,
work activities
in progress,
and
radiological
protection
controls.
Informal discussions
were held with selected
plant personnel
in
their functional
areas
during these tours.
a.
10 CFR 50.72 Notifications
During this reporting period,
the licensee
experienced
two unplanned
ESF actuations
which were not reported within the
4 hour4.62963e-5 days <br />0.00111 hours <br />6.613757e-6 weeks <br />1.522e-6 months <br /> time frame
required
by
requires
that
licensee's
notify the
NRC within four hours of any event or condition
that results
in manual
or automatic
actuation
of any
ESF.
Section
1.6.2,
Nuclear
Safety
Systems
and
Engineered
Safeguards,
includes
both
the
and
Secondary
Containment.
The
automatically initiates closure of isolation valves
to seal off all
potential
leakage
paths for radioactive material
to the environs.
The isolation of PCIS components
are zonsidered
ESF actuations.
(1)
On October
20,
1990,
during the transfer of the
38 480V
RMOV
board to its alternate
supply,
the
38
bus
was deenergized;
This was
an expected
occurrence
since the
38
bus
was
on its
alternate
supply transformer
and
a
board transfer
under these
circumstances
results
in
a trip of
RPS circuit protectors
3C1
and
3C2.
The deenergized
bus
caused
anticipated isolations
of ventilation
systems
(PCIS
Group
6)
and
the outboard
system isolation valves
(PCIS Group 3).
Followup investigation
revealed
that
RWCU valve
3'-FCV-69-1,
inboard isolation valve,
had also closed.
The closure of this
valve was not anticipated
in association
with the deenergization
of
bus
38.
Further investigation
revealed that the valve
had closed
due to
a blown fuse
(16A-F60C) in conjunction with
the
38
bus deenergization.
The unplanned
closure of this
ESF valve should
have
been reported
to the
NRC with 4 hours4.62963e-5 days <br />0.00111 hours <br />6.613757e-6 weeks <br />1.522e-6 months <br />
as
an
unanticipated
ESF actuation.
The licensee
reported
this
event to the
Hg Duty Officer as
an unplanned
ESF actuation
on
October 30,
1990.
(2)
On November 4,
1990,
the Refueling Floor fan motors tripped and
the Refuel
Zone ventilation isolated
on all three units for no
apparent
reason.
During investigation of the isolation, it was
discovered
that
a Refueling Floor static pressure
switch relay
(1-PDS-64-618/D)
was isolated
and would not reset.
The static
pressure
switches
are currently supplied
power from a temporary
transformer that is supplying
IKC bus
B.
This temporary
power
supply
was
installed
to facilitate modification
work in
progress.
The Refuel
Zone ventilation is part of PCIS group
6
which is
an
ESF.
This event should
have
been reported
to the
NRC within 4 hours4.62963e-5 days <br />0.00111 hours <br />6.613757e-6 weeks <br />1.522e-6 months <br />
as
an unanticipated
ESF actuation.
This
event
had not been reported at the end of this reporting period.
From discussions
with licensee
management,
the inspectors
determined
that
poor interpretations
of questions
and
answers
from NUREG-1022,
Licensee
Event Report
System,
and
Supplement
1, were the
cause for
the failure to make the required reports.
The first example
was not
reported
until
ten
days
following the
event.
The
licensee
lk
management
had
been
made
aware of the event reportability concerns
of the resident
inspectors
within days of the event.
The During an
exit meeting
on
November 2,
1990,
the inspectors
also. provided the
licensee
with
a letter
from
NRR to
Region II stating
the
NRC
position for reporting
ESF actuations.
This was prior to the second
two events.
In both
cases
the licensee
decided
against
reporting
the events.
These
incidences
for failure to report unplanned
ESF actuations
are
two examples
of Violation 259,
260,
296/90-33-01,
Failure
to" Make
and 50.73 Reports.
10 CFR 50.73 Reportability
On September
27,
1990, the
A 480V Diesel Auxiliary Board was returned
to its
normal
power supply,'ausing
a
loss of the security
card
reading
system.
In anticipation of the
power loss,
BFNP Security
personnel
locked all vital doors in order to maintain plant security.
The locked doors
caused
the patrolling fire watch to miss the hourly
check .in the
A 4160V Shutdown
Board
Room.
The last check
was
made at
7:55 p.m.
and the
room was not checked
again until 9:30 p.m.
TS section 3.11.A. l.b requires
that
a patrolling fire watch
be
established
whenever
the fire detection
instrumentation listed in TS
Table
3. 11.A is inoperable.
Table 3.11.A, item number 36, requires
, that
the
duct
detector
'in the
A 4160V
Shutdown
Board
Room
be
The table also lists the function of the detector
as being
"actuate
damper".
The patrolling fire watch
was
established
by
Attachment
F 890-0990 since
the duct detector failed 1-SI-4. 11.A.1,
Semi
Annual
Smoke
Detector
Functional
Test,
steps
7.8.1.5. 1
and
7.8. 1.5.2,
because
the dampers
were inoperable.
10 CFR 50.73(a)(2)(i)(B) requires that
a
LER be submitted within 30
days after the discovery of any operation or condition prohibited by
the plant's
TS.
The failure to perform
a patrolling fire watch
required
by the
TS should
have
been
reported to the
NRC by a
LER.
The failure to submit
a
LER on this event is the .third example of
Violation 259,
260,
296/90-33-01,
Failure to Make
and
50.73 reports.
In addition to'he
10 CFR 50.73 reporting concerns,
the inspector
noted that the actuation of the dampers
by the duct detector
were not
included
as
acceptance
criteria in the SI.
Steps
7.8. 1.5.1
and
7.8. 1.5.2 verify that the
actuate
but do not include
"AC"
next to the individual steps.
This could result in the duct detector
being considered
even
when it cannot
perform the
TS stated
function.
The licensee's
action
on this issue will be reviewed
as
part of the violation followup.
1J
ff
co
Drywell Tour
On November
14,
1990,
the inspectoi
toured the Unit 2 drywell.
The
licensee
has
established
a
drywell
work completion
program
in
preparation for closing the drywell when the unit returns to service.
Each
Wednesday
the drywell is toured
by various licensee
personnel"as
part of the work completion
program.
The inspector
noted
progress
had
been
made
but much work remained.
The inspector
discussed
his
observations
with the
drywell
work completion
supervisor.
The
supervisor
was quite
knowledgeable
of the items identified
on the
tour and plans to correct the items.
One
item of concern
was
identified
by
the
inspector.
Two
unterminated
electrical
on
CS testable
check valve 75-54 were
identified.
The leads
were to a magnetic
valve position indicator.
No
work
was
in progress
on
the
valve.
Hold order
tags
or
deficiency
tags
were
not in place.
The
CS system
was previously
returned
to service
with the
completion
of the
system
.SPOC
on
October
14,
1990.
This system
was under status
control or configura-
tion management
control.
The inspector discussed
this item with the
system engineer
and
no work was in progress
on the valve.
The reason
for the disconnected
was not known.
cwork had been
performed
on
the valve but was
completed
on October 30,
1990.
This item will be
identified
as
URI 260/90-33-02,
Failure to Maintain Configuration
Control
on
Core
Spray
System After System
SPOC.
The
licensee
initiated an incident investigation for the item.
One violation was identified in the,Operational
Safety Verification Area.
6.
Modifications (37700,
37828)
The inspectors
maintained
cognizance of modification activities to support
the restart
of Unit 2.
This included
reviews of scheduling
and work
control, routine meetings,
and observations
of field activities.
a ~
Breaker Installation
The inspector monitored the licensee's
activities in the installation
of
DCN 7161A, Instrumentation
and Control
Power
Buses for all three
units.
The specific activities observed
involved the termination of
the
new power cables
and installation of the
power feed breakers
on
'he
480V shutdown
boards.
The activities also involved the removal
of the temporary
power feeds to the buses.
The safety assessment
for
this modification indicated that
GE type
AK 6A 15/25 series circuit
breakers
were to be used for the
IRC bus feeder breakers
on the 480V
shutdown
boards.
The licensee
installed type
AK 6A 15/25 series for
the Unit 2 IEC buses
and type AK 2A 15/25 series for the
ISC buses
on
the Units
1 and 3.
Additional review by
NE indicated that the type
AK 2A breakers
were
an acceptable
substitute for the type
AK 6A.
The
inspector
also
observed
circuit breaker
testing
and
adjustments
required
by this
modification.
All observed
activities
were
Cl
10
controlled
by approved
procedures.
QC inspectors
were
observed
performing verifications.
Modifications,
NE,
and
system
engineers
were observed actively providing expertise
as
needed.
b.
Cable Installation
The licensee
informed
the
inspector
that during
a cable splicing
activity under
DCN
W14589
the field personnel
questioned
the.
suitability of installing
an
unjacketed
type
PX cable
in
an
modification.
An initial review by the licensee
indicated that the
cable
was
the wrong type.
The correct cable should
have
been
type
PXJ.
This item was also identified as impacting
DCN W11053;
Additional
reviews
indicated
that
in
June
1990,
a
problem with
electrical
cable
procurement
was identified.
Recurrence
control for
these
problems
was
the
issuance
of QDCN
Q 13819A which contained
a
list of cable qualified for Class
1 structures.
The
QDCN was sent to
the Maintenance,
Modifications,
and
Power Stores
group.
The type
PX
was
issued
by power stores
personnel
after distribution of the
QDCN
and the type
PX was not on the approved list.
The description
on the
bill of material identified type
PXJ cable, but the cable identified
as type
PX was issued for the installation instead.
Other
cable mark
letters manufactured
under the
same contract
number were
shown
on the
approved list.
The issue cler k did not have the list available
and
because
of the
urgency
for the cable,
issued
the cable
because
the
clerk could remember
the contract
number being
on the list.
These additional
reviews involving the
QDCN and power stores activity
also indicated
problems with the use of Anaconda supplied cable in 10 CFR 50.49 application.
NE
by memorandum restricted this type of
cable
from Class
1 structures
and
ordered its
removal
from the
nuclear
inventory.
Two DCNs,
H6910
and
W1073,
were
issued
by
NE
which specified
Anaconda cable.
The following installations resulted
from all the above:
implementation activities for DCN/ECN 10017A installed
700 feet
of PX cable
implementation activities for DCN/ECN W14589 installed
1100 feet
of PX cable
implementation activities for DCN/ECN W11053 installed
2200 feet
of PX cable
implementation
activities
for
DCN/ECN
P5136,
a
Unit
3
modification, installed
470 feet of PX cable,
and
implementation activities for DCN/ECN H6910 install
500 feet of
Anaconda cable.
J
11
An additional
item identified
by the
licensee
was that
advanced
authorized
FDCNs
F15025
and
F15101
changed
the
type of cable
to be
used for
DCN/ECNs
M10017A and
W14589.
These
AAFDCNs specified
PX cable
instead
of
PXJ cable.
The licensee
at the
end of this
reporting
period
was
removing
the
type
PX cable
and replacing it
with
type
PXJ.
The
item
is
identified
as
URI 259,
260,
296/90-33-03,
Failure
to Control
Design
in Allowing Unqualified
Cable Installation.
Cable Pulling Calculation
\\
The
inspector
reviewed
cable
pulling calculation
ED-N2057-88114.
This calculation
was for system
75.
Some existing cables
had to
be'eplaced
due
to fire damage
in the drywell.
The purpose
of the
calculation
was to provide
an evaluation
and analysis of conduit and
cable configuration to ensure
the installation requirements
of both
cable
and conduit related
to the
cable installation
were
met or
exceeded.
The inspector
reviewed the calculation
performed for each
cable
and conduit.
The pull tension
was calculated for each section
of the
conduit installation
accounting
for bends,
inclines,
and
angles.
The inspector
sampled
the mathematics
and found
no errors.
Calculations
of the pull tension,
side wall pressure,
bend radius,
and training radius
were performed
and
compared to allowable values.
All of the
requirements
were met.
The calculation
was
signed
as
being checked
by another engineer.
No discrepancies
were noted.
RPS Circuit Protector Modifications
In the
Browns Ferry design,
the
power supplies
are not Class
lE
electrical
systems.
Therefore,
redundant
Class
1E circuit protectors
were required for isolatiol between
each of the
power supplies
and
the
associated
RPS distribution
buses.
The circuit protectors
monitor
the
power
supply.
If abnormal
voltage
or
an
underfrequency
condition is detected,
the circuit protectors
actuate
to isolate
the Class
1E
RPS equipment
from the power source.
Since the installation of circuit protectors
in 1984, there
have
been
numerous
incidences
of
bus de-energization
and resulting
LERs.
The licensee
created
a task force in March
1989 to evaluate
the
numerous cir cuit protector de-energization
events.
Concerns with the
circuit protector
relaying
setpoints
were
identified
by that
evaluation.
The setpoints of the circuit protector relays were found
to
have insufficient margin with respect
to the
normal
operating
voltage of the system.
This allowed little room for drift of either
the relay setpoints
or the output voltage of the associated
MG sets.
Also, time delay relays
should
have allowed the circuit protectors
to
reset for short duration voltage
spikes without
ESF actuation.
In
addition,
the
large
deadband
on the reset
action of the circuit
protectors
prevented
resetting
when
the
MG set
output
voltage
returned to normal.
'
12
From system
design
reviews
and engineering
analysis,
TVA determined
that
the circuit protector
setpoints
should
be
changed
and other
system
changes
should
be
made.
TVA approved
design
changes
to
implement the following:
( I)
Add or lengthen
the circuit protector relays
time delay to trip.
A three
second
time delay
was established
for both
normal
and
'lternate
supplies
in all three Units.
(2)
Replace
the
5 percent
deadband
relays in Units I/3 with newer
one percent
deadband
models.
Unit 2 already
had the
one percent
deadband
models.
(3)
Revise
the circuit protector relay setpoints for undervoltage,
overvoltage,
and underfrequency.
The modifications
removed
excess
conservatism
from the circuit
protector
setpoints
and
should
allow the circuit protectors
to
withstand
a greater
range of voltage
and frequency excursions without
exposing
RPS components
to damage or malfunction.
The changes
should
reduce
the
number of
RPS trips
due to spurious circuit protector
actuation.
An inspector
discussed
the status
of the
and circuit protector
changes
with the
cognizant
system
engineer.
The system
engineer
stated all the modifications
had
been
completed
in Units I/3.
In
Unit 2,
the
addition of the
underfrequency
time delay
and
the
resetting
of the circuit protector
setpoints
have yet to
be
completed.
The licensee
was awaiting approval of TS change
8286 for
revision of the
Unit 2 setpoints.
The
inspector
reviewed
the
completed
modifications
in the plant during the
SPOC preliminary
system
walkdown
which
was
conducted
on
September
20,
1990.
No
deficiencies
were identified.
The completion of the
RPS circuit
protector modifications
and
TS
changes
are
being
followed by IFI
90-20-03
(see
paragraph
11.d).
No violations or deviations
were identified in the Modifications area.
7.
Post Modification Testing
(37828)
The inspector
observed
and reviewed
the licensee's
activities in the
area.
This included discussions
with system engineers,
Test Directors,
and
supervisors.
The specific
areas
observed
and
reviewed
were
as
follows:
PMT-196D,
EECW Flow Verification.
This test was performed to verify
that
the
EECW to
RCW systems
crossconnect
will supply at least
900
gpm of water flow from the
EECW to the
RBCCW heat exchanger
2A in
case of a loss of RCW.
Part of the acceptance
criteria
was to set
the travel
stops
on the crossconnect
valve 2-FCV-67-50 such that at
least
900
gpm flows through the valve with only the north header of
the
EECW operating
and just two pumps
on the header.
The licensee
S
!'
13
experienced difficulty with adjusting
the valve travel
stops
due to
fluctuating pressures
when the crossconnect
valve opened.
The system
engineer
informed the inspector that the
BFNP design engineers
would
be informed of the
TD and would be requested
to change
the pressure
setting at which the valve opens
and closes.
PMT-BF-268.006, Test of RHR Valve 2-MOV-74-53A,
RHR Inboard Injection
Valve.
This test
involved testing for proper operation of the
inboard injection valve from the Control
Room, local station
and from
RMOV Board
2D.
The test
was adequately 'performed
using
an approved
procedure
and
by
a qualified Test Director.
When control of the
valve
was shifted to the
RMOV Board
and tested
in the Appendix
R
configuration,
the valve indicated
both
open
and closed at the local
station
and at the
RMOV Board
2A.
This valve
had
been previously
tested
after
the Appendix
R modification
and
had tested
satisfac-
torily.
However,
a
new modification W10017A,
known
as
the black
snake
issue,
changed
out
an
unqualified
control
cable.
This
modification
used
an
"As Constructed
Drawing"
and
consequently
a
wiring error
was inserted
into the control wiring.
This item was
corrected
and the valve tested satisfactory.
The inspector will continue
to monitor the licensee's
activities in the
Post Modification Testing area.
No violations
or deviations
were identified in the
Post Modification
Testing area.
8.
System Pre-Operability Checklist
(71707)
a 4
Systems
Returned
to Service
The
inspectors
continued
to monitor the licensee's
activities to
evaluate
and
upgrade
both plant
equipment
and
documentation
as
necessary
to
insure
that
plant
systems
are
in compliance
with
applicable
standards
and
commitments
to support their
required
functions.
As of November
15,
1990,
20 of the
35 systems
required to
support
fuel re-load
had
been
completed
and
35 of the
80 systems
required to support plant operation
were completed.
Those
systems
reviewed
by the inspectors
during this reporting period
are listed as follows:
(1)
Raw Cooling Water
(System
24)
The inspector
reviewed
the completed
SCL
and
SPAE package for
this system.
The checklist
was completed
October 5, 1990.
Six
deferrals
were
taken for this
system.
The inspector
reviewed
the completed
package
and
each of the defer rais.
There
was
a
logical basis for each of the deferrals.
Most of the items were
deferrals
because
the
ECN was not being closed
as work was not
complete for other systems.
14
(2)
(3)
(4)
(5)
(6)
(7)
Normal Ventilation System
(System
30)
The inspector
performed
a walkdown on portions of this system
on
November
5,
1990.
Plant
areas
included
the
rooms
and
radwaste
building.
One
item
was identified to the
system
"engineer.
The
DG 3A exhaust
fan local controller contained
no
identification label to identify the junction box.
Other labels
were in place for 3B, 3C,
and
3D.
No other items were noted.
Station Drainage
(System
40)
The
SCL was completed
on August 8,
1990.
The inspector
reviewed
the completed checklist with the system engineer
on August 13,
1990,
and identified no deficiencies.
Breathing Air (System
49)
The
SCL was
completed
on July 3,
1990.
The inspector
reviewed
the
completed
checklist with the
system
engineer
on July 6,
1990,
and identified no deficiencies.
Sodium Hypochlorite (System
50)
The
SCL
was
completed
on
November
8,
1990.
An inspector
accompanied
the
system
engineer
on the final walkdown for this
system
on
November
6,
1990.
No major work activities
were
identified.
The
inspector
reviewed
the
completed
SCL
on
November
13,
1990,
and
identified
no deficiencies.
The
inspector
noted that
no exceptions
or deferrals
were taken for
this system.
DG 120V
DC Distribution (System 57-1)
The inspector
reviewed
the
package for the
system.
The
was
completed
on October,7,
1990.
The inspector
observed
the following:
ECN/DCNs were identified; primary and critical
drawings
were verified;
PMs identified
by the
system
engineer
were in periodicity; and system hold orders
cleared
except for
the
DG logic power.
These
breakers
were open
and tagged
due to
continuing
System
82, Diesel
Generators,
work activities.
The
inspector
noted
one
minor deficiency
in that
primary
and
critical
drawing
3-C196C11017,
Revision
2 carried
the
wrong
title in the
package.
This item was discussed
with system
engineering.
250V
DC Distribution (System 57-3)
The inspector
observed
the following:
Battery Board
1 battery
was recently replaced with a new upgraded battery; Battery Board
2 battery
was replaced
during this outage
and
was not upgraded;
Battery
Board
3 battery
is
near
the
end of life and
is
0
15
(s)
(9)
(IO)
scheduled
to
be
replaced
during the Unit
2 cycle
6 outage;
Battery, Board
4 battery is
a balance of plant battery
and is not
scheduled for replacement;
and the Control
Power Battery for the
4KV Shutdown
Board
B is scheduled
to be replaced prior to Unit 2
restart
and will not be upgraded.
Additional information supplied
by the licensee, indicated
the
total
amount of
DC power available for station blackout will be
raised
from three to four hours.
This increased
duration is
based
on the present
configuration of the system,
a change
to
the load shed procedures,
and
an ongoing calculation revision.
Secondary
Containment
(System
64 C)
An inspector
accompanied
the
systems
engineer
on
a portion of a
preliminary
walkdown
on
November
16,
1990.
Members
of
operations
and maintenance
groups
were also present.
Only minor
work items
and
housekeeping
were identified.
This system is
currently scheduled for SPOC completion
on December 5, 1990.
Primary/Secondary
Containment Isolation
(System
64 D)
The
inspector
accompanied
the
system
engineer,
Plant Manager,
Technical
Support
Manager,
and others
on the final walkdown of
this
system.
Plant
areas
toured
included
the auxiliary
instrument
room, control
room,
and reactor building.
No major
deficiencies
were identified and all items
were
documented
on
the final walkdown
check
sheet.
The inspector
reviewed
the
system
boundaries
with the system engineer.
The boundaries
were
stated
in
a
memorandum
from the
Project
Engineer
to
the
Technical
Support
Manager.
The boundaries
were
the drywell
pressures
transmitter,
panel
annunication,
and
panel
internal
components.
Further review of this system will occur
when the system
SPOC scheduled
for November
16,
1990.
Emergency
Equipment Cooling Water (System
67)
On
November
1,
1990,
the
inspector
accompanied
the
system
engineer
on
a portion of the final walkdown of this system.
The
inspector
went into the shutdown
board
room chiller room located
above
the Unit
3
rooms
and four of the
RHRSW discharge
tunnels.
The
walkdown
was effective in identifying material
problems.
The inspector
noted that
housekeeping
items
were
previously identified
on the preliminary walkdown but were not
corrected
prior to the final walkdown.
This was discussed
with
plant
management.
Also,
the
inspector
questioned
the
consistency
of support installation
on the piping in the
discharge
tunnels.
Design engineering
reviewed the supports
on
the piping
and
determined
that
the
inconsistency
was
due to
Units
1
and
3 piping not presently
being part of the support
program.
Some
sections
of the piping for Units
1 and'
have
been
cut
and
a blank flange installed until those units are
prepared for operation.
This resolved
the inspector's
question
and no other items were identified.
Reactor
Water Cleanup
System
(System
69)
The
SPOC for this system
was completed
on October 23,
1990.
The
inspector
reviewed
the completed
package.
There
was
one
exception
and
two deferrals
against this system.
The exception
was for
a
TS
change
scheduled
for January 5,
1991.
The change
involved installation of
a
10 CFR 50.49 qualified
break
detection
system.
One deferral
involved installation of thermal
overload heaters.
The work for System 69'as
complete but the
DCN was
not closed
due to outstanding
work on other'ystems.
The second deferral
was
a
PMT which required the system to be at
operating
temperature
and pressure.
The inspector
concluded
the
exception
and deferral
could
be justified.
Control
Rod Drive (System
85)
The
was
completed for this
system
and
reviewed
by the
inspector.
The inspector
accompanied
the systems
engineer
and
those
representing
the plant staff
on
a final. walkdown of the
system
and found the equipment
in good condition.
Eight items
deferred
in the
package
were reviewed
and determined to be
acceptable
for system completion.
Ho'Id orders,
temporary alterations,
and configuration control
documentation
were also reviewed.
It was determined that at the
time of system
completion,
each
had
been
evaluated .and
accepted.
In addition,
drawings
were
reviewed
and
previous
deficiencies
were found to have
been
incorporated.
There were
no deficiencies
noted after
SPOC completion.. The completed
for this system
was evaluated
to be acceptable.
b.
Options for System Return to Service
Over the last four reporting periods,
the inspector
has
made
numerous
observations
of the
SPOC activities.
Based
on these
observations,
the
inspector
has
concluded
that
the
licensee
has
two options
available for returning system to service,
as follows:
Option A
This option involves completing
the work prior to turning the
system
over to operations.
This
means
correcting
hardware
deficiencies
and performing
adequate
testing.
A system to be
turned
over to operations
should
have
hardware
deficiencies
C
4
t
0
17
corrected
either
by modification activities
or maintenance
activities
and post modification/maintenance
testing performed.
2.
Option
B
Deferral/Exception.
If a deficiency cannot
be corrected
then
a
deferral
or
an exception
is written.
As of this reporting
period
the
20
systems
which
have
completed
the
process
contain
60 deferrals,
and
10 exceptions.
Break the tie, work arounds,
and punchlist items are also being
generated
during the
SPOC process.
These options should produce
deferrals or,exceptions if not corrected
by the completion of
the
SPOC process.
The inspector
has
observed
that all of the
above
methods
can
be
applied in stages
of the
SPOC process.
The licensee's
SPOC process
requires
that all
Deferr als/Exceptions
be
approved
by the Plant
Manager.
It was
noted
by the inspector that the break the tie, the
work around,
or the punchlist
methods
do not require
individual
approval
by Senior
Management.
This item is identified as IFI 259,
260,
296/90-33-04,
Hardware Activities Delayed
but not approved
by
Senior Management.
One example of senior management
involvement occurred
when System 32,
Control Air, was
being divided into two systems.
System
32 would be
SPOCed
and
a
new system
32A, Drywell Control Air would
be
SPOCed
later.
This is the
break
the tie method.
Site Management
became
aware of this
and directed
middle
management
to
the entire
system
as originally planned.
Another example
noted involved System
9, Control
Bay Panels.
Thils system
was originally established
to
check
the control
panels
to ensure
adequacy
of configuration
and
verify the
HEDs
from
CRDR.
The inspector
was
informed that this
system
would
no longer
be
a
SPOC system,
and consequently
there will
be one less
system to
SPOC before fuel load.
No violations or deviations
were identified in the
SPOC area.
9.
Restart Test Program
(70400)
The inspector
reviewed
the licensee's
BFP 890772P in which
RTP Test
Exceptions
were
reviewed.
The
reviewed
were
those
which
were
classified for equipment
performance
or hardware
issues.
The results of
this review indicated that
11 corrective actions
were necessary
such as:
provide
the required
documentation
to ensure
that the appropriate
design
output documentation
has
been
issued;
evaluate
each listed
TE against the
issued
design output document;
and document all discrepancies
which relate
to any failure to satisfactorily
complete
the required testing or which
affect the acceptability of test results.
18
The inspector
noted that this review consisted
of TEs from 39
RTP test
'rocedures.
A total of
16
from
9
RTP test
procedures
required
additional
review due to inadequate
documentation.
The documentation
was
required for two reasons:
The
TEs did not provide clear and complete exception descriptions
or
failed
to
provide
adequate
disposition
documentation
within the
package.
The
TEs did not provide adequate
documen'tation
that all disposition
was coordinated
through other organizations.
The
licensee
discussed
these
16 TEs'n
depth
and
provided
necessary
documentation for adequate
disposition of each
item.
Based
on this
review
and
previous
observations,
the
inspector
has
concluded
that
the
licensee
conducted
the
RTP test
procedures
in
an
approved,
controlled
and
adequate
manner
and that
TEs were adequately
addressed.
Additional
RTP reviews
and observations
will be
documented
under the licensee's
Power Ascension
Program.
10.
Reportable
Occurrences
(92700)
The
LERs listed
below
were
reviewed
to determine if the information
provided
met
NRC
requirements.
The
determinations
included
the
verification of compliance
with
TS
and
regulatory
requirements,
and
addressed
the
adequacy
of the event description,
the corrective actions
taken,
the
existence
of potential
generic
problems,
compliance
with
reporting
requirements,
and
the relative
safety
significance of each
event.
Additional in-plant reviews
and discussions
with plant personnel,
as appropriate,
were conducted.
0
a
~
(CLOSED)
Main Steam Relief Valves Actuating Outside of
Technical Specification Setpoint
Because of Pilot Disc Sticking.
Wyle Laboratories
notified Browns Ferry
on
December
14,
1988, that
two of three
Unit
1 Target
Rock
MSRV tested
did not meet
the
acceptance
criteria specified
in
TS.
The
two valves failed to
actuate
within one
percent
(11 psig) of their setpoints.
Wyle
Laboratories
investigated
the
problems
and
determined
that
the
setpoint drift was
due to sticking of the pilot disc in combination
with inadequate
clearance
between
the pilot rod
and liner in the
labyrinth seal.
Wyle refurbished
these
valves
as necessary
to assure
that each would actuate within TS requirements.
The inspector
reviewed
the closure
package for this
LER, reviewed
plant procedures,
Plant SIs,
and interviewed plant personnel.
O-SI-4.6.D.1
is
the controlling
document
used for verifying the
setpoint
of the
Completion
of this
SI satisfies
the
requirements
of TS 4.6.G. 1.
Documentation
indicates that all Unit 2
valves
have
been
tested
by Wyle Laboratories.
The licensee
has
19
written
PN R08672 to have the setpoints
verified for all Unit I and
Unit 3
NSRVs
as required
by O-SI-4.6.D. 1.
Continued
implementation
of 'present
plant
procedures
should
ensure
that
the
TS's
NSRV
setpoint requirements
are met.
(CLOSED)
ESF Actuation
Caused
by Fault
on "8" Phase
Shunt Reactor of 500
KV Union Transmission
Line.
On
December
28,
1989,
a Unit 2 half scram occurred
when the Unit 2
2A bus
tripped,
resulting
in
an
ESF actuation.
The event
occurred
during
an attempt
by plant personnel
to flush debris
from
the
HPFP system automatic
deluge valve, which resulted in a full flow
fire protection
discharge
onto
the
500
KV shunt
reactors
while
energized.
The licensee
issued
LER 50-259/89-28
to document
the
events
leading to the
ESF actuation,
the results/consequences
of the
actuation,
and corrective action provided.
The inspector
reviewed
the licensee
closure
package
and associated
documentation.
The licensee
identified the root cause of the event
as
personnel
error
in the
LER.
The
licensee
also
identified
unreliable
equipment,
in the final event report,
as the
second
root
cause
that
contributed
to
the
event.
The
licensee
performed
appropriate
corrective actions
to properly re-align the
ESF systems
which actuated.
The license
provided counseling
to the personnel
responsible for the
error,
and provided reinforcement
in initial training for all fire
protection
personnel.
DCNs were
issued
to modify the
RPS circuit
protector underfrequency trip circuitry to make't less vulnerable to
and
to replace
the deluge
system
valves
as
necessary.
The
licensee
performed
appropriate
evaluations
to determine
the
effect of the
system
spray
on the shunt reactor,
and performed
sufficient tests
to assure
that the shunt reactor functions properly.
(CLOSED)
ESF Actuation
Caused
by Design Oversight-
Water Intrusion in
ATU Panels.
On June I, 1990, during
an air test
on the
HPFP system,
an unplanned
ESF actuation occurred.
The actuation
was
a result of water from the
HPFP system in cable
spreading
room
A dripping onto the
ECCS analog
trip units in the Unit 2 auxiliary instrument
room in the elevation
below the
spreading
room.
The water dripping
on the
ATU panels
caused circuit cards
in the
ATUs to generate
spurious
signals
which
resulted
in unnecessary
start of EECW pump Al and emergency
DGs A, C,
and
D.
Additional review by the licensee
indicated that an'ATWS/ARI
trip also
occurred
and if the plant were not in its present
system
lineup, additional
equipment actuation
would have occurred.
The
cause
of the event
was
a design oversight.
The design of the
seismic
gap is such that water from the cable spreading
room in the
elevation
above
the Unit 2 auxiliary instrument
room leaked directly
20
d.
onto the
ATU cabinets.
This effect has
the potential
to cause
the
ATU cards
to short and,initiate
erroneous,
signals
to various
equipment.
The inspector
reviewed the licensee's
corrective
actions
which stated
that
a technical
assessment
of the safety aspects'f
intrusion of
water into the
ATU panels
and the design of the seismic
gap slip
joint to insure water tightness will be performed.
The inspector
also
noted that IFI 259,
260,
296/90-'18-01,
Interaction of ATU and
Seismic
Gap,
was initiated to review the results of the licensee
activities
in this
area.
This
LER is closed
based
on reviews
generated
by the IFI.
(CLOSED)
De-energization
of
Bus
Caused
by
Inadequate
Design of Circuit Protector
Setpoint.
(CLOSED)
De-energization
of
Bus
by Alternate
Supply Circuit Protector
Operations
Caused
by Inadequate
Design of
Protector Setpoints.
On January
26,
1990, in Unit 3, and
on July 20, 1990, in Unit 1, the
de-energization
of
buses
occurred
due
to the tripping of
associated
circuit protectors.
In
each
case,
unplanned
actuations
occurred.
These
two events
are further examples
of the
licensee's
continuing
problems
with the
RPS circuit protector
setpoints.
As
a result of previous trips
and
LERs,
the licensee
developed
a detailed
plan to resolve
these, problems.
These
two
events
occurred
before
the licensee's
corrective
actions
could
be
completed.
The
inspector
reviewed
the
LERs
and verified that they met the
requirements
of
This issue
has
been followed on
an
ongoing
basis
by the resident
inspectors.
All modifications
have
been
completed for Units
1
5 3.
The majority of the physical
work
has
been
completed
and the license
is awaiting the
issuance
of TS
amendments
for completions
of the modifications
in Unit 2.
A
detailed
status of this issue
is given in paragraph
6.d.
No further
deficiencies
or concerns
were identified for these
LERs.
11.
Action on Previous
Inspection
Findings
(92701,
92702)
a
~
(OPEN)
IFI
50-259,260,296/86-05-07,
Reactor
Building Isolation
Radiation Monitor
This
item dealt
with the
question
of
how long
the radiation
monitoring channels for the reactor
zone
and the refueling zone could
remain inoperable
during
a surveillance
before the channel
had to be
tripped or declared
Note
11 to
TS Table 3.2.a states
that
a
channel
may
be
for
up to four
hours
for
surveillance
without placing
the trip
system
in
the
tripped
condition.
Note
22 to
TS
Table 4.2.a
states
that
one
channel
Cl
~,
21
may
be administratively
bypassed
for a period not to exceed
24 hours2.777778e-4 days <br />0.00667 hours <br />3.968254e-5 weeks <br />9.132e-6 months <br />
for functional testing
and calibration.
A followup of this IFI was conducted
and documented
in IR 89-19.
As
a result of additional
discrepancies
that arose during that followup
coupled with the original issue
had not been resolved,
IFI 86-05-07
was left open.
As indicated
in
IR 89-19, for the
purpose
of
eliminating
concerns
over
time
periods,
the
licensee
revised
procedures
2-SI-4.2.A-10FT,
"Reactor Building Ventilation Radiation
Monitors
RM-90-140,141,142,143
Instrument
Functional
Test"
and
2-SI-4.2.a. 10,
"Reactor
Building
and
Refuel
Floor Ventilation
Radiation
Monitor Calibration
and
Functional
Test"
to place trip
systems
in the tripped condition at the beginning of the tests.
This
- approach
however
was later judged
inadequate
in that it introduced
other
TS associated
with the unavailability of the drywell and torus
analyzers
due to the
Group VI isolation signal that results
from the SI's
systems
being tripped.
As stated
in IR 89-19 followup,
the inspector considered
the changes
to the SIs
as incomplete in that
they still did not clarify how long
a Reactor
Building radiation
monitor is allowed
by TS to remain inoperable for surveillances.
Based
on
a current
review of the
issue,
a clear
and
unambiguous
position
on the original question
raised
by IFI 86-05-07 regarding
how long
a Reactor
Building radiation monitor is allowed
by TS to
remain
inoperable for sur'veillances,
has
not
been developed.
Step
3.4 in Section
3.0,
"Precautions
and Limitations" in addition to
a
CAUTION note preceding
Step 7.4.5 in each of the following procedures
alerts
the
user to the notion that
a
TS
LCO "may result" if the
particular monitor being tested is out of service for more than four
hours,
and requires
the individual to notify the
SOS if it becomes
apparent that the four hour time limit will be exceeded:
2-SI-4.2.A-9(A)
2-SI-4.2.A-9(B)
2-SI-4.2.A-10(A)
2-SI-4.2.A-10(B)
Rev.3
Rev.3
Rev.4
Rev.4
The
ambiguity "of the
"may result"
wording utilized in these-
procedures,
permits
the inference that allowable outage
times other
than
the four hour provision of Note
11 to TS Table 3.2.a
(such
as
may
be afforded
by Note
22 to
TS Table 4.2.a)
are available to the
SOS in making an operability determination.
The inspector
was unable
to find
any
programmatic
documentation
defining
usage
and/or
restrictions
on the
usage of "administrative
bypass" in the context
of Note
22 to
TS Table 4.2.a.
Consequently,
the original
TS
inconsistency
between
Note
11 to
TS Table 3.2.a
and Note 22 to TS
Table 4.2.a,
covered
by IFI 86-05-07,
has not been resolved.
Additional deficiencies
identified in IR 89-19 followup and their
current status
are:
i
22
Deficiency:
TS Table 3.2.a -- Unit
2
Notes
(2), (5),
and
(13)
are not
attached
to any item in the table.
Resolution:
TS Amendment
Request
8288 submitted
by TVA on 10/30/90,
revises
Table 3.2.a to add
Note (13) next to "Instrument Channel
- High
Radiation
Line Tunnel". Additionally, Notes
(2) and
(5) have
been deleted.
Deficiency:
Paragraph
6.2 of SI
4.2.A-10FT,
which describes
acceptance
criteria, is not accurate.
Resolution:
This paragraph
has
been modified to replace
"and" by "and/or"
thereby correcting the inaccuracy.
Deficiency:
SI 4.2.A Data Tables
7-1408,
1418,
142B,
143B should denote
the
value of the downscale trip as
an acceptance
criteria since the
downscale trip is
a
TS function.
Resolution:
The following procedures
containing
the
above referenced
tables
were reviewed
by the inspector
during the current follow-up to
IFI 86-05-07:
2-SI-4.2.A-9(A)
Rev.3
2-SI-4.2.A-9(B)
Rev.3
2-SI-4.2.A-10(A)
Rev.4
2-SI-4.2.A-10(B)
Rev.4
Each
of- the
referenced
tables
provides
the. information for downscale
trips.
Based
on this review and recognizing that the
TS do not establish
a downscale trip setpoint
as they do for the upscale trip, the inspector
considers
that the additional
concerns
contained
in the deficiency
have
been adequately
addressed
by the referenced
procedures.
b.
(CLOSED) IFI 89-16-12,
Followup
on Compensatory
Actions
Due to the
Inability to Perform
10 CFR Part 50 Appendix J Testing
on Containment
Check
Valves74-705,
706,
829,
830,
and
75-580A,
580B,
581A,
and
5818.
The inability of the licensee
to perform Appendix J testing
on the
above
valves
was identified in IR 89-16.
Because
these
valves
can
not
be Appendix
J tested, it is necessary
to close valves75-582
A
and
B when primary'ontainment
is required.
The inspectors
noted in
the report that the
licensee
was
aware of this
problems
and
an
evaluation of the corrective actions
was in process.
23
The inspector
reviewed
the licensee's
corrective action,
both short
ter'm and
long term.
The short term res'olution
included
a change to
the
"Core
Spray
System
Operating
Instructions".
The
procedure
presently
requires
that
be charged
using the
head
tank
when
primary
containment
is
required.
The
inspector
reviewed
the
associated
plant drawings
and verified that this alignment
would
provide the necessary
water to charge
the
CS system
and assure
that
the necessary
valves are closed
when primary containment is required.
The licensee
has issued'a
OCR to provide long term corrective action.
The inspector
reviewed
the
DCR and discussed
its details with the
responsible
system
engineer.
The
requested
changes
adequately
addressed
the
concerns
identified in
IR 89-16.
The licensee
has
established
90-0407
as
a tracking
number for this item.
The design
is scheduled
for completion in 1992
and implementation in 1993.
Any
further inspection
in this area will be conducted
under the routine
inspection
program.
(CLOSED) IFI 259,
260, 296/89-17-05,
Followup on
ATWS Modifications.
This
item
was
closed
during
the
ATWS inspection
discussed
in
paragraph
14 of this IR.
(CLOSED)
IFI 259,
260,
296/89-27-03,
Verification That
DG Output
Breakers
Recharge
in 2.5 Seconds
or Less.
The ihspector
reviewed
the yearly surveillance
instruction for all
eight
BFNP
and noted that step 7.12 of the SIs required that the
DG output
breakers
be tested
to verify that they recharge
in 2.5
seconds
or less.
(OPEN)
IFI 259,
260,
296/90I 20-03,
RPS Circuit Protector
Trip Level
Setpoints
and Surveillance.
This item concerns
the inconsistency of surveillance
requirements for
RPS circuit protector
setpoints
between
the
TS for all three units at
BFNP.
Because
of these
inconsistencies
and
numerous
RPS circuit
protector trips, the licensee
revised
the setpoints
and submitted
a
TS revision
to establish
consistent
setpoints
and
surveillance
requirements
for all three
BFNP units.
Change
request
8286
was
submitted
to the
NRC
on June 4,
1990.
Issuance
of the
TS change
request
and implementation 'of the
new setpoints will resolve the
circuit protector
issues
for
BFN Unit 2.
The
TS change also included
new requirements
for Unit
1
and Unit 3.
The
new setpoints
are
already in place in those units.
All other
aspects
of the
RPS circuit protector
concerns
have
been
resolved
(see
paragraph
6.d).
The inspector
reviewed the licensee's
upgraded
SI for Unit 2,
2-SI-4. 1.B-16
"RPS Circuit Protector
Calibration/FT",
and verified that it included the setpoints
which
were
submitted
in the
TS
change.
The
SI will remain
under
administrative
hold until the
TS change
has
been
issued
by the
NRC.
This item will remain
open pending the issuance
of the
TS revision by
the
NRC
and
the
change
of the setpoints
for the Unit
2 circuit
protectors.
f.
(CLOSED)
IFI 259,
260,
296/90-25-03,
Documenting
and Controlling
. Clearances.
This item relates
to the difficulties encountered
by the licensee
in
determining
which equipment
clearance
numbers
were associated
with
work activities being reviewed
by the inspector.
The licensee
believes
that the current hold order tracking
system
provides
the necessary
information for operations
to manage
the hold
order
process.
The licensee
indicated that several
sorting fields
are currently available including the following:
system
people
on the hold order
expected
date of the hold order release
working group requesting
the hold order
The licensee
has further stated'hat
to create
another field to sort
by the
WO or
PN would not be especially beneficial
and there
are
no
plans
now to implement
a computerized
tracking system that would tie
the activity to the clearance
number.
During the followup of this
open item, the inspector
reviewed Site
Director
Standard
Practices
7.6.2,
"Maintenance
Management
System-Planning
Work Orders"
(Rev.
10)
and
SDSP
14.9,
"Equipment
Clearance
Procedure".
The following aspects
were noted:
Appendix
B,
"Work Order
Form" to
SDSP 7.6.2 presently
provides
for the documentation
of the hold order
number
on space
18 of
the form.
Section
6. 1 of
SDSP
14.9 currently states
that
no work shall
begin
on equipment
to
be
included
in
a clearance
until the
clearance
has
been
issued
to the
person
responsible
for the
work..
Based
on
the
above
the
inspector
considers
that
an
adequate
programmatic correlation exists
between
hold order
numbers
and the
activities covered
by work orders.
g.
(CLOSED)
259,
260,
296/89-06-05,
Inadequate
Calibration
of
Instrumentation
Required for TS Surveillance Testing.
Previously
an inspector identified that
some calibration instructions
used
to calibrate
instruments
necessary
to meet
system operability
requirements.
wi 11
not
be
upgraded prior to Unit 2 restart.
During
the inspection,
several
calibration instructions
were
found to
be
0
25
inadequate
and
the
inspector
was
concerned
that
the
inadequate
instructions
could affect
system
operability
following Unit
2
restart.
The inspector
held discussions
with licensee
personnel
concerning
the
'completion of calibration instruction upgrades.
In the
NPP Volume 3,
TYA committed to prioritize the
procedures
to be upgraded prior to
restart
using
information similar to that
used for
a
PRA.
The
licensee
established
a list of maintenance
procedures
to be completed
prior to restart
based
on this priorit'ization.
The
inspector
reviewed
the list and
noted
there
were only a few remaining which
were not upgraded.
The licensee
stated that the few remaining
ones
would be upgraded prior to Unit 2 restart.
The inspector identified
no further concerns.
(CLOSED)
URI 260/89-16-06,
Evaluation of Unsupported
Piping Spans
For
Pump Suction Pressure
Instrument
During inspection
89-16,
the
team identified that the approximately
15 foot and
17 foot span of unsupported
1/2 inch schedule
80 piping
for the
2C and
2A
pump suction instrumentation
appeared
to exceed
the piping code in place during Brown's Ferry construction.
The licensee's
review of this issue
involved determining what program
would
have
corrected
or evaluated
this condition.
The licensee
determined
that
the piping in question
was qualified
under
the
attribute
walkdown portion of the
small
bore piping program.
To
resolve
the question
about
whether
the
span
was acceptable
per the
piping code,
the licensee
provided the following information:
The piping
was
designed
and installed to the requirements
of
USAS B31. 1.0-1967,
"Code for Pressure
Piping-Power Piping".
Section
121. 1.4,
"Hanger
Spacing"
of B31.1.0
requires
that
supports
for piping
be
spaced
to prevent
excessive
sag
or
bending
and shear stresses
in the piping.
Mhere calculation are
not made,
suggested
maximum spacing of supports for standard
and
heavier pipe are provided in included tables.
Table
121. 1.4,
which
addressed
1-inch to
24
inch piping,
suggested
that support spacing for 1-inch piping be
a maximum of
7 feet for water service.
The
licensee
indicated
that
the
suggested
table
values
were not
utilized during construction,
and that is why the small
bore program
was
implemented
to
evaluate
the
actual
configuration
through
walkdowns utilizing acceptance
criteria that
had
been
established
through bounding calculations.
To ensure
the adequacy of the small
program evaluation,
which had
been previously completed for the
piping sections
in question,
and to ensure that the above piping code
requirements
were
implemented,
the licensee
rigorously analyzed
the
26
piping in question.
This analysis
was to ensure
that the actual
stresses
were within those
allowed, by the piping code.
The analysis
was
documented
by calculation
CD-Q2075-900468
which
evaluated
the
instrument
piping for all four of the
pump suction
lines in
question.
The licensee
performed
a worse case analysis for the
2D
pump suction line
which they determined
to involve the
longest
unsupported
span.
The inspector
reviewed
the results of the previous
walkdown
as well
as
the
results
of
the
rigorous
analysis
performed
by
the
calculation
noted
above.
The
review of the
walkdown
package
indicated
that
the
small
program did not evaluate
sag
as
an
attribute
,in the walkdown.
The licensee
indicated that sag for the
small
instrument
lines
was evaluated
during the resolution of the
instrument
slope
issue.
Additionally, the inspector
discussed
the
lack of a piping sag verification for small
had accepted
the
program in
Volume 3, Supplement
1.
Sag
is not
a mandatory
code requirement for piping supports
design
and is
in most cases
bounded
by the piping stress
analysis.
Regarding
the
rigorous
analysis,
the
licensee's
calculation
CD-Q2075-900468
(a
QA document)
that
was
presented
to the inspector
in the closure
package
contained
information that was different from
an identical calculation that
was latter presented
to the inspector.
Specifically,
identical
revisions
with the
same
RIM
number
contained different information on page
5 as to what instrument line
was analyzed.
The original calculation in the closure
package
tied
the four analysis
problems
numbers
to the respective
pump.
The
latter
calculation
aligned
the
calculation
problem
numbers
to
different
pumps.
Statements
from the
two calculations
are provided
for clarification.
Closure
package calculation stated,
"Four similar
problems
2-75-814-1-17,21,22,24
are
branched
out from 16" suction
of
pumps
2A,28,2C,
and
2D, respectively.
Only the worst
case,
i.e.,
problem
17 is analyzed
to confirm that the piping is
properly
supported ...."
However,
the calculation
presented
on
November 8,
1990 stated,
"Four similar problems 2-75-814-1-22,21,24,
17 are
branched
out from 16" suction
pumps
2A, 2B, 2C,
and
2D, respectively.
Only the worst case, i.e.,
problem
17 is
Analyzed to confirm that the piping is properly supported'...."
It is
be apparent
from, the two versions
that the worst case
problem
analyzed (i.e.,
17) could
have
been either
the suction
instrument
piping for the
2A or the
2D pump,
depending of the version of the
calculation reviewed.
The inspector
reviewed the actual installation
and determined that the suction line for the
2D pump appeared
to be
worst case
based
on the unsupported
length..
The inspector.
requ'ested
that the licensee
determine
the cause for the different versions of a
QA record.
The licensee
determined that the official record
was the
one that
was provided to the inspector during the inspection
and not
the
one that
was
provided
in the closure
package.
The licensee
27
provided
the following explanation
based
on their investigation of
the calculation discrepancies:
'uring the calculation review and approval
process
the reviewer
noted that the problem to pump correlation
was incorrect and it
was
changed
on the official copy.
'he calculation
was sent to RIMs for distribution
(The process
takes
approximately
4 weeks).
'he licensing organization
requested
an expedited
copy for the
closure
package.
'he engineering
organization
got a copy of the cover sheet
from
the
RIMs group and attached it to an in-house
copy of the
'alculation
that
had not been
changed
to correct the error that
was discovered
during the review and approval
process.
The inspector discussed
the following concerns
with the licensee:
(1)
With the long delay in issuing the
RIMs copy of calculations it
appears
that any revisions
during that time frame would be made
to uncontrolled copies of the calculation.
(2)
The
process
that allow attaching
a cover sheet to an in-house
document
is
a weakness
in the record distribution process
and
should
be evaluated.
(3)
Information being provided to the
NRC needs
to be factual
and
complete
Review of the licensee
gA control
process
in the
above
areas
is
identified as IFI 50-260/90-33-05.
(OPEN)
50-260/89-16-07,
Need
to
Perform
ASME Section
XI
Inspections
On Valve Operator Supports
During inspection
89-16 the
team questioned
ISI SI-4.6.G regarding
the failure to include
valve operator
supports
in the
American
Society of Mechanical
Engineers
Boiler and Pressure
Vessel
Code
(ASME
Code) Section
XI program.
The ISI group advised
the team -that valve
operators
were not included in the ISI program because
they were not
pressure
boundary
component
supports.
Contrary
to this,
the
licensee's
Engineering
Department
advised
the
team
that
valve
operator
supports
are
designed
either
to maintain
pipe
pressure
boundary
integrity
(pipe
stress)
or to
assure
valve
operation
(seismic
oualification).
The
team
noted
that
the
system
contained
valve operator
supports
that were not in the ISI program.
On December
15,
1989, the ISI group proposed
a corrective action plan
to review all drawings, identify all required
valve supports,
and
I
0
28
perform
a baseline
examination of the identified supports
to
Code Section
XI requirements
prior to restart.
The
inspector's
review of
the
licensee's
corrective
actions
associated
with resolving this
URI indicated that the licensee
had
changed
their
proposed
corrective
action.
Specifically,
the
licensee's
gA ISI group reevaluated
the requirements
of Section
XI of
the
ASME Boiler
and
Pressure
Vessel
Code,
1974
summer of 1975
Addendum edition,
which is
the current
code of record for
BFNP
Unit 2.
This reevaluation
indicated
that
the
licensee
no longer
believed
that
the
code
required
inspection
of supports
which
connected
to valve operators.
The licensee's
did indicate
in the
issue
closure
package
that they were planning to implement the
1986
revision of the
code during the next
10 year interval
and that the
newer code specifically requires
inspection of intervening elements.
The inspector's
review of the
1974 edition of Section
XI determined
that sections
IWB for Class
1 and
IWC for Class
2, requires
in Tables
and
IWC-2520 that the support
components
be inspected..The
tables specifically require that the area to be inspected
include the
support
components
that
extend
from the piping, valve,
and
pump
attachment
to
and
including
the
attachment
to the
supporting
structure.
-The licensee
had interpreted
that this requirement
did
not apply to valve
operator
supports
even if the
operator
is
supporting
the valve
and 'piping system.
The inspector
has discussed
the licensee's
interpretation with NRR and Regional
NRC staff and the
NRC does
not concur with the licensee's
position.
The requirements
to inspect
supports
are
to
ensure
pressure
boundary
integrity
and to eliminate
supports
that serve this
purpose
does
not comply
with code requirements.
The inspector
met with licensee site senior management
on November 8,
1990 to discuss
the licensee's
position.
The licensee
agreed that
the supports
logically should
be inspected.
However, the licensee
pointed
out that their
program that
was
submitted
to the
NRC in
July 1977
and for concurrence
in November
1981
never
intended
to
inspect the type of supports
in question.
Nevertheless,
the licensee
proposed
to include the supports
in their program
and
perform the
baseline
inspection
before plant restart.
Follow up inspections
of
the licensee
resolution of this issue will be tracked
by this item
remaining open.
(CLOSED) Violation 259,260,296/88-28-01,
Failure
to Control
and
Correct
Known Drawing Discrepancies
(CLOSED)
Violation
259,260,296/90-14-04,
Failure
to
Implement
Drawings
and Procedures.
The program description for handling drawing discrepancies
at
BFNP is
found in SDSP 9. 1, "Processing
Drawing Discrepancies".
The detailed
handling
of drawing
discrepancies
within Nuclear
Engineering
is
.
'I
0
29
described
in
BFEP
Process
Instruction
87-,70,
"Processing
Drawin'g
Discrepancies"
which is
a subtier
document of SDSP 9.1.
The following discussion
centers
around
VIO 90-14-04
since
the
corrective action originally implemented
as
a result of VIO 88-28-01
when coupled with the corrective action taken for 90-14-04 satisfies
the original concerns
associated
with VIO 88-28-01.
During the
NRC inspection
conducted
from April 16 - May 18,
1990,
and
documented
in IR 90-14,
two examples of failure to implement drawings
and procedures
were. identified by the inspector
.
In their July
13,,
1990
response
to the Violation the
licensee
attributed
the
cause
of
example
one
to
inadequate
procedural
controls.
IR 90-14 previously documented
the inspector's
review of
the
licensee's
completed
incident
investigation
( II-B-90-504)
associated
with this
example
and determined
that inadequacies
had
existed in the implementation of SRN G-38-69.
The
SRN was
signed
out April 6,
1990,
as "effective immediately" yet
it did not arrive at
BFNP Document Control until April 26,
1990, at
which time it was
given
a
due
date
of
May 27,
1990 for site
implementation.
The licensee
acknowledged
in their response
that the source
document
implementation
program
had failed to process
the change
covered
by
SRN G-38-69 in the timeframe necessary
to support the ongoing field
activities.
As corrective
action,
NEP-5.1,
"Design Output",
was
revised
to
provide
an
administrative
control
program for the
processing
of "effective immediately" changes.
Under this revision to
NEP-5. 1, the inspector
confjirmed that the Chief Discipline Engineer/
Project
Engineer
is
now required
to provide to the affected site
directors
approved
copies of any specification, revision, or
SRN when
implementation
date is "effective immediately" or is not supported
through the normal controlled copy distribution.
In the case of example
82, the licensee
attributed the Violation to
personnel
error.
As
a result of the system engineer's
review of the
PDD that
was written to address
the difference
between
the field
wiring and the plant drawing, the decision
was
made to reconnect
the
wiring in
accordance
with
the
plant
drawing.
However,
this
dispositioning
of the
PDD failed
to consider
the effect
the
reconnection
would have
on the control logic for the
4160V shutdown
board.
Details
associated
with the inadvertent
diesel
generator start were
documented
in
which
was
subsequently
reviewed
and
closed out in IR 90-27.
30
As corrective aetio'n,
the
system engineering
personnel
involved with
the event
have
been
counseled
and instructed
on the
importance of
performing
thorough
technical
evaluations
of
PDDs. Additionally,
Revision
10
to site
procedure
SDSP
9.1,
"Processing
Drawing
Discrepancies",
has
been
issued
to require
independent
verification
on
PDD resolutions.
Section
7.0 of SDSP 9.1 assigns
an "Independent
Verifier" to review and concur with
PDD disposition
and categoriza-
tion.
A block requiring independent verification of PDD disposition
and categorization
has
been
added to Attachment A, "Potential
Drawing
Discrepancy
Flow Process"
of
SDSP 9.1,
downstream
of the
system
engineer's
det'ermination of the
method for dispositioning
the
PDD.
Finally, Form SDSP-17,
"Potential
Drawing Discrepancy
Form", has
been
modified to require
a signature
by the independent verifier, the date
- signed,
and the individual's extension
number.
Based
on
the
above,
the
inspector
determined
that
the
concerns
associated
with the
referenced
violations
have
been
adequately
addressed.
(CLOSED) YIO 50-260/89-16-04,
Inadequate
Procedure.
The
issue
that
was identified by the
NRC
as
the first example,
involved inadequate
instructions
in procedure
2-0I-75 which directed
valve manipulation that allowed post accident
water to
be directed
outside
the
containment
boundary.
The
licensee
response
dated
April 9,
1990,
indicated that the
OI in question
was revised to note
that the resetting of PCIS
and that restoration of keep-fill water
would be controlled by procedure
2-AOI-100-1.
The inspector
reviewed revision
16 of 2-OI-75 which added
caution
about contacting chemistry for special
caution
on opening containment
isolation valves.
This
same
revision indicated in step
7.1 that
resetting
of
and
restoration
of keep-fill water
would
be
controlled
per
procedure
2-AOI-100-1,
"Reactor
Abnormal'perating
Instruction."
The
inspector
reviewed
2-AOI-100-1
and
verified that instruction
on operating
the valves
and resetting
the
PCIS signal
were included.
However, the licensee failed to insert
a
caution
about
hazards
associated
with diverting post accident water
outside
the containment
boundary.
The licensee
subsequently
revised
2-AOI-lOO-I to include the caution note.
Regarding
example
2 of VIO 260/89-15-04,
the licensee's
calculation
(MD-f2075-890109)
determined
that
the
flow valve specified
in
procedure "2-SI-4.5.A. 1.D (1)
was incorrect.
Revision
19 of the SI
corrected
the values
and referenced
the calculation.
The inspector
also
reviewed
the
CCRIS
system
to ensure
that there
was
a cross
reference
from the calculation
to the
SI to ensure
that if the
calculation*changed
the procedure
would be reviewed.
(OPEN) Violation 259,
260, 296/89-17-01,
Failure to Comply With the
Requirements 'of 10 CFR 50.59
31
This violation involved the processing
of DCN H3858A,
ECN P7113,
and
DCN
HO166A, which modified the facility as
described
in the
without
a written safety
evaluation
to provide
the
basis
for
determining that an unreviewed safety question
was not being created.
The licensee
responded
to the Violation by letter dated
September ll,
,
1989.
The
NRC accepted
the licensee's
response.
by letter
dated
October
2,
1989.
The
licensee
committed
to
provide
safety
evaluations for the three
DCN/ECNs identified in the violation and to
review change
packages
closed
between
January
1988 and April 1989 in
support of the next
FSAR annual
update.
The inspector
reviewed the safety evaluation
provided for the three
change
packages
identified in the violation.
They appeared
to
be
adequate.
However,
the
licensee
committed
to review all
ECN/DCN
packages
completed
between
January
1988
and April 1989.
The
inspector
questioned
the basis for the review beginning in January
1988 versus
,the date
on which screening
reviews
were permitted.
The inspector
reviewed the
SWEC procedure
for
FSAR verification and determined that
although all
DCN/ECNs closed during this time period were reviewed,
they were first screened
for
FSAR impact.
If none was'ound,
the
packages
were not further reviewed.
The purpose of this commitment to review all
ECN/DCNs closed
during
that
time period (or the period during which inadequate
screening
reviews
may
have
been
performed)
was
to find any
packages
which
should
have contained
a safety evaluation
but did not.
However, the
inspection
determined that if ECN/DCNs did not affect the
FSAR, they
were
not reviewed for adequate
50.59 evaluations.
The inspector
expressed
this concern to the licensee,
and it was confirmed (I) that
the January
1988 date
was
based
on the
FSAR update
schedule
and (2)
that
the first screening
criteria
used
by their
update
contractor
was
impact
on the
FSAR, therefore,
packages
which would
not impact the
UFSAR were
not reviewed for 50.59
adequacy.
The
inspector
does not believe that the corrective action
was adequate
to
identify the type of problem cited in this violation.
After the
above
review the inspector
evaluated
several
additional
screening
reviews for other modification
performed
in
1988
time
frame.
The inspector identified similar problems to those described
in the violation.
Although the inspector did not identify any items
that constituted
an
unreviewed
safety
question it could not
be
ascertained
from the
screening
review. that
the
licensee
had
an
adequate
written basis
for their determination.
The
SWEC review
relied
on
a review of the entire design
change
package
and not just
the screening
form.
The inspector
discussed
the findings of this
sample
review with the licensee
and the licensee
indicated in the
exit interview that they
may
sample
some of the screening
review
forms that
were
excluded
from the
SWEC review.
The
inspector
32
informed
the
license
that this
item
wi 11
remain
open
pending
additional
reviews of screening
forms by the
NRC.
(CLOSED)
VIO 259,260,296/89-27-04,
Failure to Report
as
Required
by
During the
NRC inspection
conducted
from June
16 - July 15,
1989,
three
examples of a failure to submit
a
LER within 30 days after the
discovery of an event,
as required
by
were identified
by the inspectors.
These
examples
formed
the
bases
for Violation
50-259,
260,
296/89-27-04
transmitted
to the
licensee
on August 8,
1989 in
IR
89-27.
In their
September
21,
1989,
response
to the
VIO, the
licensee
admitted violation
example
83 but expressed
the belief that
the
events
covered
by examples
81 and
b'2 were not reportable
pursuant
to
Based
on the information provided in the licensee's
response,
the
denial of example
81 was accepted
by
NRC Region II in a letter to the
licensee
on
November
16,
1989.
Irrespective
of the original
uncertainty regarding
the reportability of Example
81 pursuant to 10 CFR 50.73
the
licensee
did identify it as
a condition adverse
to
quality
and
issued
CARR
BFP 880702
thereby formalizing root cause
identification and corrective
action plan development.
In reference
to the reportability of example
P2, the
NRC Region II
November
16,
1989 letter advised
the licensee that the
NRR technical
staff would be reviewing the licensee's
position and that the results
of their evaluations
would be communicated
to the licensee
once they
became available.
Notification of these results
was
made
by
NRC Region II in a letter
dated
November
2,
1990.
This letter
provided
the
NRC staff's
conclusions
there
was insufficient basis
available to support
TVA's
engineering
judgement
that
the
postulated
relay failure scenario
would only trip one diesel
generator
and that therefore,
the ability
of some
systems
to fulfill their safety functions
was indeterminate
during certain
plant
accident
conditions
and
should
have
been
reported in accordance
with 10 CFR 50.73.
The letter also noted that TVA's commitment to install
an additional
lockout relay prior to restart of Unit 2 as stated
in the voluntary
LER (89-09) that
was
submitted after the
30 day requirement,
was
adequate
corrective action for the conditions described
in LER 89-09.
The
inspector
confirmed
in the field that installation of the
additional
lockout relay is complete
and is being tracked
by Design
Change
Notice
DCN 8W6909A.
Post modification testing
remains
to be
done prior to final package
closeout.
4
,
33
Regarding
example
b'3,
the licensee's
September
21,
1989
response
stat'ed
that although
TVA initially identified potential
equipment
area
cooler air flow problems
on
May 25,
1989,
no
LER was submitted
within thirty days
of
May
25
because
at that
time
TYA had
not
determined, that
a
strong possibility existed
that the plant
had
previously operated at power with the degraded
flow rates.
As TVA's investigation continued into the possible
causes
of degraded
flow, they discovered
on July
12,
1989, that'he grill/registers
mounted at the
end of each
room, cooler duct =were partially closed,
restricting air flow.
Sine'e
as their condition indicated
a long term
degradation,
TVA then
concluded
that this condition
could
have
existed
during operation
and it was
then that
the
reportabi lity aspect
was= formally recognized.
LER 50-259/89018
was
later submitted
on August ll, 1989.
In this
LER the root cause
of the
problem
was attributed to the
inexistence of a procedure/program
to periodically measure
flow rates
through
room coolers.
As
a result of the lack of a procedure
and the
attendant
lack of historical
data,
the licensee
had
been
unable to
readily determine if the air flow had deteriorated
over time or if
there
had
been
a step
change
in air flow.
The inspector
confirmed that
Technical
Instruction TI-134,
"Core
Spray
and Residual
Heat
Removal
Room Coolers Air Flow Verification"
was
developed
and
issued for Units
1 and
3 on November
21
1989
and
for Unit 2 on August 24 1989.
Of the three
examples
cited in the original violation, examples
hl
and
b'2 had
been
the subject of an initial 10 CFR 50.72 report
on the
part of the licensee.
The licensee's
subsequent
reviews would result
in their judgement
that the conditions
were
not reportable
under
In their response
to the violation,
TVA made
a commitment to advise
the
NRC by letter within 30 days in cases
where
a four hour report
will not require
a
10 CFR 50.73 report.
Based
on the
above
discussion,
the inspector
determined
that the
concerns
associated
with the referenced violation, as modified by the
NRC
Region II November
16,
1989 letter,
have
been
adequately
addressed.
(CLOSEO) Violation 259,
260, 296/90-14-05,
Failure to Implement. the
Independent Verification Requirements
for a Temporary Alteration.
During
the
review of activities
performed
under
associated
with the determination
and retermination
of cables
in
conduit 3ES-1676-IB,
discrepancies
in the documentation
of the work
activities were identified by the inspector
independent verification
of the wire lifting activities
as required
by STD-10. 1.5s,
"Control
34
of Temporary Alterations"
and
PMI 8.1,
"Temporary Alteration," had
not
been
performed
before
conducting
high potential testing of low
voltage cable in accordance
with special test ST-90-01.
TVA Standard
STD-10.1.53
and PMI-8.1 require independent verification
for both lifting and relanding of electrical wires.
Both of these
documents
include wire lifts as
an example of a temporary alteration.
In their July
13,
1990,
response,
the
licensee
attributed
the
violation to personnel
error for failing 'to follow procedures.
Also,
the format of the data
sheets
being utilized for the -"determinating".
activities is listed in their response
as
a contributing factor in
that the test of the procedure
requires
two signatures,
yet the data
sheets
only provide one block for both signatures.
The inspector
reviewed
the following documents
and records
provided
by the licensee
to support completed corrective actions
in this area:
(1)
MIA-1.3, "General
Requirements
for Modifications" (Rev. 3)
(a)
Definitions
have
been
incorporated
in Section
4 of the
procedure
to address
First Party Verification, Second Party
Verification, and Independent Verification.
(b)
Duties
and responsibilities
in the area of "verification"
have
been
incorporated
in Section
5 of the procedure for
craftsmen,
foremen,
"and responsible
engineers"
(c)
Attachment
B to
the
procedure
has
been
modified
to
encompass
guidance
on independent verification requirements
associated
with the data sheet.
(2)
MIA-3.3, "Cable Terminating
and Splicing for Cables
Rated
up to
15,000 Volts" (Rev. 9)
The "Cable/Mire Life and Reland
Data Sheet"
was revised in Rev.
8 of this procedure
to add
a block for independent verification,
initialing, and dating.
Also,
an asterisk
was
added to the data
sheet
denoting,
"Independent
Verification (IV) required for
SDSP-3. 15".
(3)
Training
on Independent
Verification and the changes
to MAI 1.3
and 3.3 for individuals in the modifications organization
who
are designated
to perform IV.
(a)
A lesson
plan titled, "Verifications
Performed
During
Modifications Activities" was
developed
and
presented
to
personnel
performing
IV activities.
Course
attendance
sheets
were
examined
and
a
review
was
conducted
of a
July 17,
1990, scenario
issued
by the Modifications Manager
and containing
a listing of individuals
who
had received.
I
35
the training and
who meet the site criteria for personnel
performing
I.V.
(4)
ASSP-3. 15, "Independent Verification" (Rev 6)
As
a result of the licensee's
independent verification generic
impact evaluation,
Rev.
6 to SDSP-3.15
was issued
September
27,
1990.
This
version
clarified
the
differences
between
"Independent
Verification" and
Second
Party Verification".
A
statement
was
added
to indicate that
an "independent verifier"
was to authorized to make configuration changes.
Also, Standard
STD-10. 1.15,
"Independent
Verification,"
was
added
to
the
.
references, section of SDSP-3. 15.
The inspector
determined
that the concerns
identified in the
above
inspection report item have
been adequately
addressed.
12.
TMI Action Items
(CLOSED)
260/TMI Action Item II.F.1.2.E,
Suppression
Pool
Water
Level
Monitor.
The
NRC approved
TS Amendment
Number, 125 for Unit 2 on August 19,
1986.
This
amendment
included
TS requirements
for the suppression
pool water
level
wide range monitor.
The instruments
are for the
A and
B channel
respectively,
LI-64-159A and
XR-64-159.
The
inspector
reviewed
the
applicable
SIs for calibration
and functional test of the instruments,
2-SI-4.2.F-20(A)
and 2-SI-4.2.F-20(B).
The
instruments
were installed
under
ECN P0323.
The inspector
reviewed the
ECN and the instruments
were
Eg verified on September
21,
1990.
The inspector toured the control
room
and discussed
operation of the jnstruments with the plant operators.
The
instruments
had
been operable
and operations
were knowledgable
about them.
The inspector
noted that the
B channel
recorder
XR-64-199
had
no units
designation
label.
The
A channel
had units of feet.
This was discussed
with Operations
Management.
The review of the TS,
ECN,
and
instruments
found the item acceptable.
13.
Bulletins and Generic Letters
a ~
(CLOSED for Unit 2 Restart
Only)
Nonconforming
Materials Supplied
by Piping Supplies,
Inc. At Folsom,
and
West Jersey
Manufacturing
Company at Williamstown,
This bulletin
was
issued
May 6,
1988,
to require that
licensees
submit
information
regarding
materials
supplied
by the
subject
companies
and
to request
the
licensee
1)
assure
that materials
comply with
ASME Code
and design specification
requirements
or are
suitable for their intended service,
or 2) replace
such materials.
36
Supplement
1 to the bulletin was
issued
on
. June
15,
1988,
to
1) provide. additional information concerning material
supplied
by the
subject
companies,
2)
reduce
the
scope of the requested
materials
review to only flanges
and fittings, 3) delineate
actions
licensees
are
requested
to take to identify these materials
and to determine
whether
the materials
comply with ASME 'and
ASTM design
and material
specifications,
and
4) clarify what actions
licensees
are
requested
to take
once
they identify material
that
does
not compl'y with the
above material specifications.
Supplement
2 to the bulletin
was
issued
on August 3,
1988,
to
1) modify, the
schedule
for actions
addressees
were
requested
to
perform in the original bulletin and
supplement
1,
and
2), provide
additional
information concerning
materials
supplied
by the subject
companies
and
an
affiliated
company,
Chews
Landing
Metal
Manufacturers
Incorporated
(CLM).
Supplement
2 temporarily suspended
most of the activities'nd
reporting
requirements
requested
by the
original bulletin and supplement
1.
The remaining actions
requested
from full power licensees
by supplement
2 were:
(1)
Maintain documentation
of the specific actions
taken for the
identified materials.
(2)
Retain nonconforming materials until advised further
by the
NRC.
(3)
Report the results of tests of PSI
and
WJM flanges
and fittings
to the
INPO Nuclear Network for dissemination
to the industry.
The licensee
responded
to the bulletin and both supplements
by letter
on August 26,
1988.
The response
provided the information requested
by supplement
2
and
stated
that
TVA had
suspended
work
on the
bulletin.
The
TYA program
and status
given in the response
was
as
follows:
TYA transmitted letters
to 22 intermediate
suppliers
requesting
information
on
WJM or PSI material
supplied to TVA.
TVA had
received
nine responses
from those supplier stating that
no
WJM
or PSI material
had
been furnished to TVA nuclear plants.
Hub, Inc.,
and
Consolidated
Power
Supply
are
intermediate
suppliers
that
had
provided
WJM or
PSI material
to
BFNP.
Specific information necessary
to locate material at
BFNP was
being obtained.
A plan
was
developed
to systematically locate installed
WJM and
PSI materials,
and test
instructions
were written to test
suspect material
once it is located.
A search
of TVA purchasing
records
revealed
that
no direct
contracts
existed with either
WJM or PSI.
37
Through the
use of Nuclear Network,
TVA is maintaining contact
with other utilities to locate,
test,
and qualify suspect
material.
TVA participated
in the
NUMARC effort to
bound
the
issue,
develop
a
data
base
from results of industry test data,
and
establish
methods
to qualify in-place material.
Based
on the suspension
of the bulletin's efforts by Supplement
2 and
the licensee's
response,
this bulletin is resolved for Unit 2 restart
only.
Further followup or closure of this bulletin will be addressed
once the
NRC has
determined
the extent of further actions
and issued
further guidance.
(CLOSED) Units
2 and
3 TI 2515/96,
Drywell Vacuum Breaker Modifica-
tions,
MPA Item D-20 (Generic Letter 83-08).
This item was modification of vacuum breakers
on Mark I containments
In December
1979,
GE issued
SIL No.
321
informing customers
of unanticipated
cycling and
damage
to drywell
vacuum breakers
during
LOCA tests
in a prototype
Mark I containment.
To
assure
that
drywell
vacuum
breakers
would
be
capable
of
withstanding
chugging
and
condensation
oscillation
loads;
Generic Letter 83-08 requested
licensees
of Mark I containments
to perform
plant-unique calculations
to determine
the structural
adequacy of the
drywell vacuum breakers.
The
NRC in
a letter to TVA dated
November
25,
1986 issued
a safety
evaluation
report accepting
TVA's proposed modifications.
In TVA's
letter of January
29,
1987,
the progress
on the modifications
were
given as follows:
Unit
1 - No work started
Unit 2 - Complete
Unit 3 - Complete
The inspector
reviewed
ECN P0684
and workplans
2114-85 (Unit 2)
and
13130 (Unit 3).
It was found that the hinge arm, the hinge pin, and
the
hinge
arm to pallet bolts
could
become
overstressed.
The
licensee
decided to remedy the situation
by using different materials
for these
parts to increase
their allowable stress limits.
By using
316 stainless
steel for the hinge arms,
303 stainless
steel for the
hinge'ins
and
A193
GR
B6 material for hinge
arm to pallet bolts,
proper safety margins were thus restored.
The inspector
reviewed
WP 2114-84 in the
permanent
record
storage
area
and verified the correct material
was
used.
The material
selection
was verified
by
a
gC holdpoint.
This fulfills the
inspection
requirements
of the TI.
C
38
(CLOSED Unit
2 Only) TI 2500/020,
Revision
2, Inspection
to Determine
Compliance with ATWS Rule,
10 CFR 50.62, Unit 2.
This
item
had
been
reviewed
during
an earlier
inspectio'n
IR 259,
260,
296/89-17,
when
the inspector
determined
that the
ongoing modification
work was not yet complete.
The
inspectors
reviewed
engineering
design
documents
and
inspected
the
installed modifications
associated
with Unit 2
The licensee
modified the existing
SLCS and
RPT systems
and
added the ARI
system.
In addition,
the licensees
ATWS programs
were reviewed to assess
the implementation of training, plant procedures,
and the effectiveness
of
quality "controls
used
during design,
installation
and testing of ATWS
systems.'.
System
The
was modified to allow for the
use of Boron-10 enriched
pentaborate.
This
option meets'0
CFR
50.'62
(C)(4)
requirements
for the
and
was
approved
by the
NRC in safety
evaluation report dated
September
2,
1988.
TS amendments
154,
150,
and
125 concerning
these matters
have
been
issued for Units 1, 2, and
3 respectively.
The inspectors verified that surveillance
procedures
have
been
approved
and
issued
to implement the
new
TS surveillance
requirements.,
A review of Unit
2
completed
surveillance,
data
indicated satisfactory
results.
The trending of chemistry analysis
for
Boron-10
enrichment
showed
stable
chemistry
conditions.
Chemistry personnel
handle
boron addition and analysis.
The licensee
has
procedures
which establishes
.guidel,ines
for the
procurement,
receipt
inspection
and
sampling
the
drums
of enriched
pentaborate.
The
inspectors
noted
that
the
enriched"
pentaborate
drums
are
kept in segregated
storage
in a warehouse
at
the site.
b.
Alternate
Rod Injection System
The licensee
ATWS design
associated
with the ARI system
and
RPT were
submitted to
dated
March 1, July 15,
and August 4,
1988.
NRC safety evaluation report dated
January
22,
1989 approved
the plant specific design for Browns Ferry Units 1, 2, and 3.
The
purpose
of the
ARI system
is to initiate
a reactor
independent
of the
RPS.
The protective
action
can
be initiated
manually using switches
from the main control
room, or automatically
when inputs of low reactor
vessel
water level or high reactor vessel
pressure
(two out of
two logic) trip setpoints
are
reached.
Following an
ARI initiation signal,
the control air supply to the
HCUs is blocked
by energizing
a 3-way valve
and depressurizing
the
air lines to the individual
valve
by energizing
two-way ARI
39
vent valves.
Opening
the individual scram valves results in control
rods
being inserted.
Once the ARI system is initiated it can not be
immediately reset
because
of a
30 second
time delay.
This ensures
that protective action
goes
to completion..
The ARI system
redundant
two out of two trip logic combined with placing the bypass
switch in
test'osition
allows for maintenance,
testing,
and calibration during
power operation.
Surveillance
instructions
2-SI-4.2.B-ATU (A), (B),
(C), and (D)'are in place to conduct monthly functional test of each
ARI/RPT channel initiating logic.
Alarm and annunciator
windows are
provided to indicate
when
ATWS system is being tested
or when
an
has
been initiated.
The
inspectors
identified that
system
valves
(8)
are
not
scheduled
to
be functionally tested
following the post modification
testing
(PMT-184).
Following discussion of this matter the licensee
initiated
a
change
to incorporate
a functional test of ARI system
valves
in 2-SI-4. 1.A. 1.
The test
is to
be
conducted
during
refueling outages.
The inspectors
informed licensee
management
that
the testing
should
be initiated
though
the
SRI system
logic with
requirements
to verify that all ARI system
valves
go to their
positions.
The
ARI system
is required
to start
rod
inward motion wi'thin 15
seconds
of initiation and
be completed within 25 seconds
from ARI
initiation.
Test
data
taken
during
Post Modification Test
184
indicated
that
approximate
by
14 control
rods
exceeded
the
rod
injection motion start time of 15 seconds
(ie 15.2 to 18.0 seconds).
Rod injection completion
times
met the
acceptance
criteria of 25
seconds.
The
licensee
performed
plant specific
analysis
and
justification review using
GE documents
and
changed
the rod motion
start
time acceptance
criteria to
19 seconds.
Although these
time
extensions
were
not
reviewed
in the
SER,
similar reviews
and
approvals
have
been
made
by
NRR for other
BWRs.
Based
on the review
of
completed
PMT-184
test
results,
licensee's
analysis
and
discussions
with NRR, the inspectors
determined that the
ARI system
function times are acceptable.
To comply with the
ATWS rule, the ARI/RPT system is required to have
components
diverse
from those of the
RPS.
Presently,
the diversity
between
the
ARI/RPT system
and the
RPS is not acceptable
as
both
systems utilize Rosemont
ATUs.
This concern
was identified in the
SER.
The licensee
had taken
the
s position
on diversity, ie,
waiting on appeal
of NRC's position.
The staff recently replied to
the owner's
group
and denied
the appeal.
The licensee
informed the
inspectors
that their current
schedule
provides for replacement of
the
ARI/RPT system
ATUs with
GE models
during cycle
6 refueling
outage.
The licensee
stated
that
a letter concerning
the schedule
for GE Model installation would be sent to the
NRC.
The inspectors
discussed
this
issue with
NRR personnel
and determined that it was
not
a restart
issue.
This will be tracked
as
IFI 260/90-33-06,
RPS/ARI Diversity.
Additionally 259, 260, 296/89-17-05 is closed.
40
co
d.
Recirculation
Pump Trip System
The
RPT system
implemented at Browns Ferry is similar to, that used at
the Monticello.
The
RPT initiates from the
same
two out of two logic
as the'RI
system.
A spare trip coil in the "End-of Cycle
Breakers" is used
and
a trip signal will open
one of the two ATWS/RTP
breakers
in series
for
each
recirculation
pump.
Surveillance
instructions
are
in place
to perform monthly test
on the
ARI/RPT
channel
logic 2-SI-4.2.B-ATU (A), (B), (C),
and
(D) and
a once
per
cycle test of the channel
logic including the tripping of the
RPT end
of cycle breakers
(2-SI-4.2-B-71).
Generic Letter 85-06 provided guidance
concerning
(}A requirements
to
be
used during the implementation of the
ATWS 'rule.
The inspectors
reviewed
gA records
(gA audits,
inspection
reports,
work plan hold
points,
procurement
records,
and
acceptance
test results)
which
indicated that gA/gC was active in all the proces'ses
for implementing
the
ATWS rule.
In addition, the inspectors verified that an on-going
program is in place
(NIZAM, Part I, Section
1.3) which identifies
those
management
controls for maintaining the
ATWS equipment.
The
inspectors
reviewed
changes
to Unit
2 operating,
emergency,
abnormal
operating,
and
procedures
and verified that
actions
required
to initiate
and restore
ATWS systems
have
been
incorporated.
The
review of lesson
plans,
written
exams,
and
attendance
records
in the
area of
ATWS modifications
and plant
procedures
indicates
that training for plant operators
has
been
provided.
Simulator training has also
been provided.
Based
on the
above
reviews,
the inspectors
determined that the licensee
has
adequately
met the requirements
for the
ATWS rule for Unit 2. except
for the unresolved diversity issue which is not a restart issue.
15.
Restart
Assessments
a ~
b.
Senior Management
Assessment
for Restart
Team Meeting
The
inspector
attended
a
portion
of
a
meeting
on
November 3,
1990.
The last meeting of SMART was held on August 14,
1990.
The meeting
was attended
by four Vice-Presidents
of TVA and
other
TVA managers.
The meeting
was
conducted
according
to the
agenda
and
using
the
SMART notebooks.
Detailed charts
of
CARR
trends,
WO trends,
etc.,
were
used
during the meeting to gain
an
overall perspective of the plant recovery status.
Licensee
Operational
Readiness
Review Program
(93806)
The
inspector
held
discussions
with licensee
personnel
for the
purpose
of determining
the
status
of the licensee's
Operational
Readiness
Review Program.
r'
C
41
The inspector
was
informed by the licensee
that
Browns Ferry has
an
ongoing
Operational
Readiness
Review
Program
which is intended
to
provide a,review of the state of readiness
by an independent
group of
personnel
with a broad
base of management,
operating,
and technical
experience.
TVA's stated
objective which was provided to the
ORR
team was to review the qualification and motivation of site personnel
and availability of necessary
supporting
resources
for safe
and
reliable testing,
operation
and maintenance
of the unit.
The review
was initially intended
to
be provided
as
a two phase
look with the
first phase
conducted
during May - June,
1989
and the second
phase
in
March 1990.
The
Phase
1 report
was
issued
in June
1989.
Various concerns
were
identified as follows:
Operations
Conduct of operations
not at desired
standards.
Division of responsibilities
in control
room not well defined.
Sensitivity of reactor safety factors not at desired levels.
Actions to
improve supervision
of non-licensed
operators
not
effectively addressed.
Walkdowns
by managers
not effective.
Administrative, operating,
and work procedures
deficient.
Maintenance
Work packages
need
adequate
work instructions for personnel.
Post maintenance
testing
problems.
Management
involvement required to address
PM backlog.
Vendor technical
recommendations
not timely.
Chemistry
PASS procedures,
training,
and lab techniques
need
improvement.
Other
Emergency
preparedness
exercise
lacked
high
standard
of
performance.
Nuclear experience
reviews
and lessons
learned
lack attention.
~ >.
'PA
42
These
concerns
were
reviewed
by
TVA management
personnel
with
a
formal
response
to 0.
D. Kingsley documented
in Vice President,
Nuclear
Power
Production
Memorandum
dated
October
30,
1989.
This
response
outlined the licensee's
corrective action plan in each
area
and
a schedule for improvement.
The Phase
2 review was completed in March 1990.
This second
team was
given similar guidance
to that provided to the first ORR team.
The
purpose
was
to provide
an additional
independent
assessment
of
readiness
and review the status of corrective actions
associated
with
concerns
identified during the
Phase
1 review.
Although the
team
concluded that it was safe to restart
the unit and that various areas
of improvement were noted there
were inconsistencies
in achieving the
standards
of performance
expected
by senior
management
indicating
that corrective actions
associated
with the
Phase
1 review had
been
less
than fully effective.
Additional'concerns identified included:
guality of procedures
lacking.
Maintenance
planning
and
PMs still need attention.
Training effectiveness
affected
by poor communications.
These
new concerns
were reviewed
by TVA management
personnel
with a
formal
response
to the staff documented
in licensee
submittal
dated
October
24,
1990.
This
response
outlined
the
status
of the
licensee's
corrective actions for each of these
concerns
and provided
a schedule for completion.
The licensee
has identified 47 specific
concerns
with
480
related
action
items
which
must
be
closed
associated
with in this
area.
The
licensee
has
established
a
tracking
program
and
assigned
a manager
to follow the progress
of
status
of corrective actions for these
issues.
A biweekly status
.
report is issued.
As of October 31,
1990, the licensee
had completed
closure of 70/ of the concerns
and
93K of the action items.
The licensee
plans to conduct
a Phase
3 review of operations
and work
control.
This final licensee
readiness
review will be
a short
limited review
and is scheduled
to be conducted after Unit 2 core
reload.
Additionally this review is not intended to be
a followup on concerns
identified as part of the
Phase
2 review since that followup is being
performed independently
by NMRG.
The
inspectors will review the licensee's
corrective
actions for
adequacy
for selected
items
identified
during
the
licensee's
Operational
Readiness
Review
Program
during
the
next reporting
period.
~ ~ s
l$
43
16.
QA Activities (35701)
a.
Management
Review Committee
'n inspector attended
portions of a scheduled
meeting of the
MRC held
on November 9,
1990.
The
MRC is intended to provide the proper level
of management
review neccessary
to assign
the correct
the
proper
safety
significance
level
to
any
licensee
identified potential
conditions
adverse
to quality.
During the
meeting
several
new
potential,
CAQRs/PRDs
were discussed.
In each
case
the
items
were
properly classified
as
a
CAQR or
PRD, inactivated
(one Unit 3 item
was placed
on an inactive list i.e. deferred),
or held over until the
next scheduled
meeting for further discussion.
The inspector
noted
an
improvement
in the sensitivity to potential significant issues
compared to the last meeting attended.
The inspector
determined that
the proper safety significance
was assigned
to each item reviewed
by
the committee
and did not disagree with any committee decisions that
occurred during the period that the inspector
was present.
b.
Corrective Action Program
The
inspector
reviewed
the
status
of the
licensee's
program
to
identify potential
adverse
trends
in the corrective action program.
The inspector
determined
that
the licensee
has
continued
to make
progress
in the area'f
reducing
the
number of outstanding
items
tracked
on TROI.
Although this effort is receiving positive results
the
inspector
noted
various
potential
concerns
which
may require
additional attention.
Although the
number of outstanding
items
on TROI has
continued
to increase
a recent
trend
has
indicated that the
combined
number of CAQRs,
PRDs,
and
COTS related
items increased.
Although the
inspectors
had previously identified
an
adverse
trend involving an excessive
number of bypassed
or missed
holdpoints
which resulted
in a recent violation as discribed in
IR 259,
260,
296/90-27,
the inspector
noted that
two recent
CAQRs
have
been
issued
which identify further problems'n this
area.
CAQR
BFP900364
was
identifed
by the Site Quality
Organization
where holdpoints
were
bypassed
during Appendix
R
and cable" tray penetration
work.
CAQR BFP900368
was identifed
by the Site Quality Organization
where holdpoints were bypassed
during
welding activities
on safety-related
piping.
These
constitute
additional
examples
of Violation
259,
260,
296/90-27-03.
The
number of delinquent
CAQRs
has
shown
a slow but gradual
increase
since
May
1990,
an indicator
which should
be of
particular
concern.
The Quality Tracking
and
Improvement-
Level II Trend Report dated October 1,
1990, identified that the
number of CAQRs deliniqunt at the end of the month
had increased
from 33 to 51.'f 69 outstanding significant
CAQRs open
17 were
delinquent.
C
~)s
r
44
During
the
recent
gA audit
on correction
of deficiencies
(BFA90021) Site guality Organization
personnel
identified two
examples
where
CA(Rs received
improper closure.
The two CAgRs
were closed
on Sept.
30,
1990,
by Site equality
Management after
being rejected
by the Site guality Monitoring section
on the
preceding'ay.
Field work was
not complete
at the time of
closure
and
the
CAgRs were not redispositioned
to reflect the
revised
basis for closure.
One of the
CAgRs was closed
without'vidence
being in the
CA(R package
that all corrective actions
were
complete.
This
failure
was
identified
in
PRO
BFA900336021P.
Although the inspectors
previously identified a problem with the
control of work activities
which resulted
in
a violation as
documented
in IR 90-29,
two new examples
have
been identified by
the licensee.
The violation dealt with the licensee's
failure
to adequately
control
work activities
by site maintenance
and
modifications
personnel
in that work was not performed
on plant
equipment within properly defined
clearance
boundries.
Since
that time the licensee identified that work was performed
on the
Unit 2 "B" CS
Room Cooler and the Unit 3 Dilution Air Discharge
Damper Actuator without an approved clearance.
The licensee
has
initiated
incident
investigations
for both of these
recent
event's
which the inspector will review with licensee
personnel
when
complete.
Both of these
events will be
included
as
additional
examples of Violation 260/90-29-01.
Although these
conditions
were discovered
by the licensee
and the
prematurely closed
CAgRs were reopened
and properly dispositioned
the
inspectors
consider all of the above
as
an indicator of a potential
problem with the implementation of the licensee's
corrective action
program.
Furthermore
the staff considers
any examples of premature
closure
of conditions
adverse
to quality or missed/bypassed
gC
holdpoints
as unacceptable.
17.
Exit Interview (30703)
The inspection
scope
and findings were
summarized
on
November
16,
1990
with those
persons
indicated
in paragraph
1
above.
The
inspectors
described
the areas'nspected
and
discussed
in detail
the inspection
findings listed below.
The licensee
did not identify as proprietary any
of the material
provided to or reviewed
by the inspectors
during this
inspection.
Dissenting
comments
were not received
from the licensee.
For
URI 260/89-16-07,
Need to Peform
ASME Section
XI Inspection of Valve
Operator
Supports,
TYA committed
to perform
a .review of drawings
to
identify supports
in question
and to do the following:
c
~>)
r
1)
Add the supports
to the Unit 2 Section
XI program
2)
Perform the baseline
inspection prior to Unit 2 restart
3)
Review the other units
and place
the required
supports
into their
respective
programs prior to Unit 1 or. Unit 3 restart.
Item Number
259,
260, 296/90-33-01
260/90-33-02
259,
260, 296/90-33-03
259, 260, 296/90-33-04
260/90-33-05
259,
260, 296/90-33-06
Descri tion and Reference
VIO, Failure to Make
and 50.73
Reports,
paragraph
5.
URI, Failure to Maintain Configuration
Control
on
Core
Spray
System After System
SPOC,
paragraph
5.
URI, Failure to Control Design in Allowing
Unqualified Cable Installation,
paragraph
6.
IFI, Hardware Activities Delayed But Not
Approved by Senior Management,
paragraph
8.
IFI,
QA Control Process
Related to
Calculation,
paragraph,
11.
IFI, RPS/ARI Diversity, paragraph
14.
Licensee
management
was
informed that
5 LERs,
5 IFIs,
2 URIs,
5 VIOs, and
1 TMI Item were closed.
AOI
ATU
BFEP
BFNP
CAQR
CFR
COTS
DCN
FDCN
Abnormal Operating Instruction
Alternate
Rod Injection
American Society of Mechanical
Engineers
Analog Trip Units
Anticipated Tranisent Without Scram
Browns Ferry Engineering Project,
Browns Ferry Nuclear Power Plant
Condition Adverse to Quality Report
Code of Federal
Regulations
Corrected
on the Spot
Design
Change Notice
Design
Change
Request
Diesel
Generator
Emergency
Core Cooling Systems
Engineering
Change Notice
Emergency
Equipment Cooling Water
Environmental Qualification
Engineered
Safety Feature
Field Design
Change Notice
Final Safety Analysis Report
(tl
'4
GL
GPM
IKC
IFI
IN
IR
KV
LCO
LER
NE
NEP
NOY
NQAM
NRC
NRR'I
ORR
PASS-
PDD
.
PMI
QDCN
RCW
RMOV
SCL
Genera'1
Electric
Generic Letter
Gallons
Per Minute
Hydraulic Control Unit
High Pressure
Fire Protection
Instrument
and Control
Inspector
Followup Item
Information Notice
Institute of Nuclear
Power Operations
Inspection
Report
Inservice Inspection
Kilovolt
Limiting Condition for Operation
Licensee
Event Report
Loss of Coolant Accident
Microbiological Induced Corrosion
Maintenance
Request
Management
Review Committee
Main Safety Relief Valve
Nuclear Engineering
Nuclear Engineering
Procedure
Nuclear Performance
Plan
Nuclear Quality Assurance
Manual
Nuclear Regulatory
Commission
Nuclear Reactor Regulation
Operating Instruction
Operational
Readiness
Review
Post Accident Sampling
System
Primary Containment Isolation System
Potential
Drawing Discrepancy
Preventive
Maintenance
Plant Manager Instruction
Post Maintenance/Modification Test
Problem Reporting
Document
Pounds
Per Square
Inch Guage
Quality Assurance
Quality Control
Quality Design
Change Notice
Reactor Building Closed Cooling Water
Raw Cooling Water
Residual
Heat Removal
Residual
Heat Removal Service
Water
Reactor Motor Operated
Valve
Reactor Protection
System
Recirculation
Pump Trip
Restart Test Program
System Checklist
42
SDSP
SOS
SRN
TD
'TI
TI
TROI
TS
V
Site Director Standard
Practice
Surveillance Instruction
Service Information Letter
Standby Liquid Control System
Shift Operations
Supervisor
System Pre-Operation
Checklist
Specification Revision Notice
Special
Test
Test Deficiency
Test Exception
Technical
Instruction
Temporary Instruction
Three Nile Island
Tracking and Reporting of Open
Items
Technical Specifications
Valley Authority
Unresolved
Item
Volt
Violation
Work Order
Work Request