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Category:LICENSEE EVENT REPORT (SEE ALSO AO
MONTHYEARML17292B7421999-07-20020 July 1999 LER 99-001-00:on 990628,ESF Signal Closed All Eight MSIVs While Plant Was Shutdown.Caused by Failure of Relay RPS-RLY-K10D.Subject Relay Was Replaced & Tested on 990630. with 990720 Ltr ML17292B4451998-10-27027 October 1998 LER 98-012-01:on 980715,failure to Comply with Requirements of TS SR 3.8.4.7 Was Noted.Caused by Inadequate Work Practices.Training Session Was Held with Personnel.With 981027 Ltr ML17284A7561998-09-0303 September 1998 LER 98-013-00:on 980805,ESF Actuations Were Noted Due to Deenergization of Vital Electrical Bus SM-8.Caused by Inadequate Direction in Troubleshooting Plan.Will Conduct Training for Engineering Personnel.With 980903 Ltr ML17284A7571998-09-0202 September 1998 LER 98-014-00:on 980807,completion of TS 3.8.1.F Required Shutdown Due to Inoperability of EDG-2 Was Noted.Caused by Degraded Voltage Regulator for DG-2.Replaced Voltage Regulator & Associated Scrs.With 980902 Ltr ML17284A7551998-09-0202 September 1998 LER 98-015-00:on 980808,discovered Reactor Coolant Pressure Boundary Leak During Shutdown Conditions.Caused by Leakage from Socket Weld (Fwb 63) on Elbow Connection.Failed Piping Connection Was Replaced.With 980902 Ltr ML17284A7311998-08-17017 August 1998 LER 98-012-00:on 980716,determined That 24-month SR 3.8.4.7 Had Not Been Fulfilled within Specified Frequency.Caused by Inadequate Work Practices.License Requested & Received Enforcement Discretion Re Battery Svc test.W/980817 Ltr ML17284A7121998-07-23023 July 1998 LER 98-006-01:on 980520,discovered Discrepancies in Low Voltage Bus Calculations During Review of 10CFR50,App R Calculations for High Impedance Faults.Caused by Inadequate Work Practices.Implemented Procedural Changes ML17284A6951998-07-17017 July 1998 LER 98-011-00:on 980617,ECCS Pump Room Flooding Was Noted Due to FP Sys Pipe Break.Caused by Inadequate Design of FP Sys.Detailed Review of FP Sys Design Was Conducted. W/980717 Ltr ML17284A6961998-07-15015 July 1998 LER 98-010-00:on 980615,TS Required Shutdown Due to Inoperability of TIP Sys Isolation Valve Was Noted.Caused by Improper Installation of TIP Tubing.Reattached Affected Tubing & Inspected Other TIP tubing.W/980715 Ltr ML17284A6731998-07-0101 July 1998 LER 98-009-00:on 980606,nuclear Steam Supply Shutoff Sys Group 3 & 4 Isolations During Testing Was Noted.Caused by Procedural Deficiency.Counseled Individuals Involved in preparation.W/980701 Ltr ML17284A6651998-06-24024 June 1998 LER 98-007-00:on 980530,inadvertent Full Scram & Division 1 ECCS Injection Was Noted.Caused by Failure to Meet Mgt Work Practice Expectation When Encountering Deficient Procedure. Incident Review Board Convened to Review event.W/980624 Ltr ML17284A6641998-06-24024 June 1998 LER 98-008-00:on 980531,inadvertent Full Scram During RPV Leak Testing in Mode 4 Was Noted.Caused by Change in Mgt Techniques.Revised Procedures to Take Into Account Addl Water Head in Pressure Sensing lines.W/980624 Ltr ML17284A6631998-06-19019 June 1998 LER 98-006-00:on 980520,discovered Discrepancies in Low Voltage Bus Calculations During Review of App R Calculations for High Impedance Fault Analysis.Caused Indeterminate. Implemented Procedural Changes Involving Operator Action ML17284A6551998-06-0404 June 1998 LER 98-005-00:on 980506,potential for Failure of RHR Sys Valve to Close on Isolation Signal Was Noted.Caused by Design Deficiency.Caution Tag Was Placed on RHR-V-40 Control Switch to Inform Plant Operators of limitation.W/980604 Ltr ML17284A6421998-06-0101 June 1998 LER 98-004-00:on 980502,determined That Primary Containment Penetration Overcurrent Protection Does Not Meet Reg Guide 1.63 Requirements.Caused by Inadequate Design Changes. Installed Addl Fuse in RHR-MO-9 circuit.W/980601 Ltr ML17292B3281998-04-0909 April 1998 LER 98-002-00:on 980311,reactor Scram & Plant Transient Occurred,Due to Failed Closed Main Steam Isolation Valve. Caused by Loss of Pneumatic Actuating Supply Pressure. Problem Evaluation Request Written for Failure of MS-V-22D ML17292B3291998-04-0909 April 1998 LER 98-003-00:on 980311,WNP-2 Experienced SCRAM Signal as Result of Low Rpv.Caused by Less than post-SCRAM Operational Strategy for Resetting SCRAM Signal in Conditions.Changes in post-SCRAM Operational Strategy implemented.W/980409 Ltr ML17292B2661998-03-0404 March 1998 LER 98-001-00:on 980203,automatic Start of HPCS EDG Was Noted.Caused by Operator Error.Operations Crew Stabilized Plant at Approximately 75% Reactor Power & Investigation of Event Was initiated.W/980304 Ltr ML17292B1111997-11-10010 November 1997 LER 97-011-00:on 971010,HPCS Battery Charger Failed.Caused by Failure of a Phase Firing Control Circuit Board Due to Aging During 7 Yrs of Use.Hpcs Sys Was Immediately Declared inoperable.W/971110 Ltr ML17292B1151997-11-0707 November 1997 LER 97-010-00:on 970906,discovered That TS SR 3.4.5.1 for Identified Portion of RCS Total Leakage Would Not Be Able to Perform within Time Limits of SR 3.0.2.Caused by Inadequate Methods.Method of Meeting SR 3.4.5.1 Established ML17292B0641997-09-24024 September 1997 LER 97-004-01:on 970327,plant Operators Manually Scrammed Reactor as Required by TS Due to Indication of Entry Into Region a of power-to-flow Map.Caused by Inadequate Attention to Detail.Established Event Evaluation teams.W/970924 Ltr ML17292B0241997-08-18018 August 1997 LER 97-009-00:on 970717,discovered Error in Recently Performed Inservice Testing procedure,OSP-TIP/IST-R701. Caused by Procedure Inadequacy.Plant Procedure OSP/TIP/IST-R701 Will Be changed.W/970818 Ltr ML17292B0291997-08-15015 August 1997 LER 97-008-00:on 970716,wire Seal Used to Lock Containment Instrument Air Pressure Control valve,CIA-PCV-2B,found Not Intact.Cause of Misadjustment of CIA-PCV-2B Unknown.Event Will Be Communicated to Plant employees.W/970815 Ltr ML17292B0201997-08-15015 August 1997 LER 97-S01-00:on 970718,failure to Take Compensatory Measure for Inoperative Microwave Security Zone Occurred. Caused by Personnel Error.Training Will Be Conducted W/ Appropriate Members of Security force.W/970815 Ltr ML17292A9481997-07-23023 July 1997 LER 97-007-00:on 970611,voluntary Rept of Automatic Start of DG-1 & DG-2 Was Experienced.Caused by Undervoltage Condition on Electrical Busses SM-7 & SM-8.Circulating Water Pump CW-P-1C Control Switch Placed in pull-to-lock.W/970723 Ltr ML17292A9201997-06-26026 June 1997 LER 97-006-00:on 970527,non-performance of Surveillance Requirement 3.6.1.3.2 for Blind Fanges,Was Noted.Caused Because Misunderstanding of Intent of Specs.Added Five Structural Assemblies for SP.W/970626 Ltr ML17292A8331997-04-28028 April 1997 LER 97-004-00:on 970327,plant Operators Manually Scrammed Reactor as Required by TS Due to Entry Into Region a of power-to-flow Map Following Planned Trip of Single Mfp. Event Evaluation teams,established.W/970428 Ltr ML17292A8311997-04-28028 April 1997 LER 97-005-00:on 970327,valid Reactor Scram Signal Received Due to Low Water Level Condition During Preparations for SRV Testing.Caused by Risks & Consequences of Decisions Not Completely Identified.Restored Water level.W/970428 Ltr ML17292A8251997-04-21021 April 1997 LER 97-003-00:on 970320,notification of Noncompliance W/Ts as TS SRs for Response Time Testing Were Not Being Met for Specified Instrumentation in Rps,Pcis & Eccs.Requested Enforcement Discretion for One Time exemption.W/970421 Ltr ML17292A7431997-03-20020 March 1997 LER 97-002-00:on 970218,determined That Rod Block Monitor (RBM) Calibr Values Were Not Set IAW Tech Specs.Caused by Calibr Procedures Inadequacies.Revised & re-performed RBM Channel Calibr procedures.W/970330 Ltr ML17292A7401997-03-13013 March 1997 LER 97-001-00:on 970211,reactor Water Cleanup Sys Blowdown Flow Isolation Setpoint Was Slightly Above TS Allowable Valve Occurred Due to Calculation Error.Lds Fss LD-FS-15 LD-FS-16 Were Declared inoperable.W/970313 Ltr ML17292A6641997-01-22022 January 1997 LER 96-009-00:on 961220,miscalculation of Instantaneous Overcurrent Relay Settings Resulted in Inoperability of safety-related Equipment.Caused by Utilization of Inappropriate Design.Testing Was completed.W/970122 Ltr ML17292A6461997-01-0606 January 1997 LER 96-008-00:on 961205,failure to Comply with TS Action Requirement for Emergency Core Cooling Sys Actuation Instrumentation Occurred Due to Unidentified Inoperability Condition.Pmr initiated.W/970106 Ltr ML17292A6371996-12-19019 December 1996 LER 96-007-00:on 961122,electrical Breakers Were Not Seismically Qualified in Test/Disconnect Position.Circuit Breaker Mfg Did Not Consider Raced Out Breaker Position During Testing.Relocated Circuit breakers.W/961217 Ltr ML17292A4121996-08-0808 August 1996 LER 96-006-00:on 960709,average Power Range Monitor Rod Block Downscale Surveillance Not Performed Prior to Entry Into Mode 1.Caused by long-standing Misinterpretation of Requirements of Tss.Procedures revised.W/960808 Ltr ML17292A3801996-07-24024 July 1996 LER 96-004-00:on 960624,plant Was Manually Scrammed by Control Room Personnel Due to Reactor Water Level Transient Experienced During Testing of Digital Feedwater Sys.Caused by Programming Error.Sys Was corrected.W/960724 Ltr ML17292A3771996-07-24024 July 1996 LER 96-005-00:on 960624,determined Missed Surveillance Test Re Channel Check of Average Power Range Monitor.Caused by Inadequate Procedures.Revised Surveillance Procedure Re When APRM Checks Must Be performed.W/960724 Ltr ML17292A3641996-07-12012 July 1996 LER 96-003-00:on 960615,required Surveillance Test Not Performed When Required by TS 3.4.1.3.Caused by Inadequate Procedures.Implementing Surveillance Procedure & Reactor Plant Startup Procedures revised.W/960712 Ltr ML17292A3361996-06-20020 June 1996 LER 96-002-00:on 960504,critical Bus SM-8 Lost Power When Supply Breaker 3-8 Tripped.Caused by Personnel Error. Operators Counselled & Procedures revised.W/960620 Ltr ML17292A2861996-05-24024 May 1996 LER 96-001-00:on 960425,inadvertent ESF Actuations Occurred Due to Tripping of Temporary Power Supply to IN-3.Caused by Personnel Error.Operations Restored to IN-3 Loads & Reset ESF actuations.W/960524 Ltr ML17291B0891995-10-19019 October 1995 LER 95-011-00:on 950919,failed to Comply W/Ts SR for RCIC Sys Due to Analysis Deficiency That Resulted in Inadequate Surveillance Test Procedure.Surveillance Procedure Revised to Correct deficiency.W/951019 Ltr ML17291A9021995-07-0707 July 1995 LER 95-010-00:on 950609,HPCS DG Declared Inoperable Due to Discovery That TS Test Method Incomplete.Caused by Inadequate Testing Procedure.Test Procedure for HPCS DG Reviewed & Special Test Procedures written.W/950707 Ltr ML17291A9031995-07-0707 July 1995 LER 95-009-00:on 950607,inadvertent MSIV Closure Occurred During Surveillance Test Due to Poor Communication Between Test Team.Determined That MSIV Closure Not Valid Because Closure Not Triggered by Plant conditions.W/950707 Ltr ML17291A8501995-06-0808 June 1995 LER 95-006-01:on 950405,reactor Scram Occurred During Surveillance Testing Due to Protective Sys Relay Failure. Replaced Failed Relay Before Plant Startup ML17291A8101995-05-12012 May 1995 LER 95-008-00:on 940125,TS Wording Lead to Potential TS Violation.Caused by Lack of Clarity in Ts.Submitted Improved TS for Plant to Provide Addl clarity.W/950512 Ltr ML17291A7841995-05-0505 May 1995 LER 95-007-00:on 950222,emergency Diesel Start Occurred Due to Voltage Transient on BPA Grid.Confirmation Was Received at 17:51 H That Disturbance Had Originated in BPA Grid ML17291A7801995-05-0404 May 1995 LER 95-006-00:on 950405,main Turbine Trip Occurred During Performance of Surveillance Test Due to Protective Sys Relay Failed.Replaced Failed Relay Before Plant startup.W/950504 Ltr ML17291A7851995-05-0303 May 1995 LER 95-005-00:on 950222,inoperable IRM Had Been Relied Upon to Meet TS Requirements During Reactor Startup.Caused by Lack of Neutron Source to Test Instrumentation. Sys Knowledge Gained Will Be incorporated.W/950503 Ltr ML17291A7071995-03-25025 March 1995 LER 95-004-00:on 950226,malfunction in Main Turbine DEH Control Sys Caused All Four High Pressure Turbine Governor Valves to Rapidly Close.Caused by Blown Fuse.Suspected Faulty Circuit Card replaced.W/950325 Ltr ML17291A7011995-03-20020 March 1995 LER 95-002-00:on 950218,automatic Reactor Scram Occurred. Caused by Erroneous Positioning of Control During Performance of Scheduled Periodic Functional Test.Control repositioned.W/950320 Ltr 1999-07-20
[Table view] Category:RO)
MONTHYEARML17292B7421999-07-20020 July 1999 LER 99-001-00:on 990628,ESF Signal Closed All Eight MSIVs While Plant Was Shutdown.Caused by Failure of Relay RPS-RLY-K10D.Subject Relay Was Replaced & Tested on 990630. with 990720 Ltr ML17292B4451998-10-27027 October 1998 LER 98-012-01:on 980715,failure to Comply with Requirements of TS SR 3.8.4.7 Was Noted.Caused by Inadequate Work Practices.Training Session Was Held with Personnel.With 981027 Ltr ML17284A7561998-09-0303 September 1998 LER 98-013-00:on 980805,ESF Actuations Were Noted Due to Deenergization of Vital Electrical Bus SM-8.Caused by Inadequate Direction in Troubleshooting Plan.Will Conduct Training for Engineering Personnel.With 980903 Ltr ML17284A7571998-09-0202 September 1998 LER 98-014-00:on 980807,completion of TS 3.8.1.F Required Shutdown Due to Inoperability of EDG-2 Was Noted.Caused by Degraded Voltage Regulator for DG-2.Replaced Voltage Regulator & Associated Scrs.With 980902 Ltr ML17284A7551998-09-0202 September 1998 LER 98-015-00:on 980808,discovered Reactor Coolant Pressure Boundary Leak During Shutdown Conditions.Caused by Leakage from Socket Weld (Fwb 63) on Elbow Connection.Failed Piping Connection Was Replaced.With 980902 Ltr ML17284A7311998-08-17017 August 1998 LER 98-012-00:on 980716,determined That 24-month SR 3.8.4.7 Had Not Been Fulfilled within Specified Frequency.Caused by Inadequate Work Practices.License Requested & Received Enforcement Discretion Re Battery Svc test.W/980817 Ltr ML17284A7121998-07-23023 July 1998 LER 98-006-01:on 980520,discovered Discrepancies in Low Voltage Bus Calculations During Review of 10CFR50,App R Calculations for High Impedance Faults.Caused by Inadequate Work Practices.Implemented Procedural Changes ML17284A6951998-07-17017 July 1998 LER 98-011-00:on 980617,ECCS Pump Room Flooding Was Noted Due to FP Sys Pipe Break.Caused by Inadequate Design of FP Sys.Detailed Review of FP Sys Design Was Conducted. W/980717 Ltr ML17284A6961998-07-15015 July 1998 LER 98-010-00:on 980615,TS Required Shutdown Due to Inoperability of TIP Sys Isolation Valve Was Noted.Caused by Improper Installation of TIP Tubing.Reattached Affected Tubing & Inspected Other TIP tubing.W/980715 Ltr ML17284A6731998-07-0101 July 1998 LER 98-009-00:on 980606,nuclear Steam Supply Shutoff Sys Group 3 & 4 Isolations During Testing Was Noted.Caused by Procedural Deficiency.Counseled Individuals Involved in preparation.W/980701 Ltr ML17284A6651998-06-24024 June 1998 LER 98-007-00:on 980530,inadvertent Full Scram & Division 1 ECCS Injection Was Noted.Caused by Failure to Meet Mgt Work Practice Expectation When Encountering Deficient Procedure. Incident Review Board Convened to Review event.W/980624 Ltr ML17284A6641998-06-24024 June 1998 LER 98-008-00:on 980531,inadvertent Full Scram During RPV Leak Testing in Mode 4 Was Noted.Caused by Change in Mgt Techniques.Revised Procedures to Take Into Account Addl Water Head in Pressure Sensing lines.W/980624 Ltr ML17284A6631998-06-19019 June 1998 LER 98-006-00:on 980520,discovered Discrepancies in Low Voltage Bus Calculations During Review of App R Calculations for High Impedance Fault Analysis.Caused Indeterminate. Implemented Procedural Changes Involving Operator Action ML17284A6551998-06-0404 June 1998 LER 98-005-00:on 980506,potential for Failure of RHR Sys Valve to Close on Isolation Signal Was Noted.Caused by Design Deficiency.Caution Tag Was Placed on RHR-V-40 Control Switch to Inform Plant Operators of limitation.W/980604 Ltr ML17284A6421998-06-0101 June 1998 LER 98-004-00:on 980502,determined That Primary Containment Penetration Overcurrent Protection Does Not Meet Reg Guide 1.63 Requirements.Caused by Inadequate Design Changes. Installed Addl Fuse in RHR-MO-9 circuit.W/980601 Ltr ML17292B3281998-04-0909 April 1998 LER 98-002-00:on 980311,reactor Scram & Plant Transient Occurred,Due to Failed Closed Main Steam Isolation Valve. Caused by Loss of Pneumatic Actuating Supply Pressure. Problem Evaluation Request Written for Failure of MS-V-22D ML17292B3291998-04-0909 April 1998 LER 98-003-00:on 980311,WNP-2 Experienced SCRAM Signal as Result of Low Rpv.Caused by Less than post-SCRAM Operational Strategy for Resetting SCRAM Signal in Conditions.Changes in post-SCRAM Operational Strategy implemented.W/980409 Ltr ML17292B2661998-03-0404 March 1998 LER 98-001-00:on 980203,automatic Start of HPCS EDG Was Noted.Caused by Operator Error.Operations Crew Stabilized Plant at Approximately 75% Reactor Power & Investigation of Event Was initiated.W/980304 Ltr ML17292B1111997-11-10010 November 1997 LER 97-011-00:on 971010,HPCS Battery Charger Failed.Caused by Failure of a Phase Firing Control Circuit Board Due to Aging During 7 Yrs of Use.Hpcs Sys Was Immediately Declared inoperable.W/971110 Ltr ML17292B1151997-11-0707 November 1997 LER 97-010-00:on 970906,discovered That TS SR 3.4.5.1 for Identified Portion of RCS Total Leakage Would Not Be Able to Perform within Time Limits of SR 3.0.2.Caused by Inadequate Methods.Method of Meeting SR 3.4.5.1 Established ML17292B0641997-09-24024 September 1997 LER 97-004-01:on 970327,plant Operators Manually Scrammed Reactor as Required by TS Due to Indication of Entry Into Region a of power-to-flow Map.Caused by Inadequate Attention to Detail.Established Event Evaluation teams.W/970924 Ltr ML17292B0241997-08-18018 August 1997 LER 97-009-00:on 970717,discovered Error in Recently Performed Inservice Testing procedure,OSP-TIP/IST-R701. Caused by Procedure Inadequacy.Plant Procedure OSP/TIP/IST-R701 Will Be changed.W/970818 Ltr ML17292B0291997-08-15015 August 1997 LER 97-008-00:on 970716,wire Seal Used to Lock Containment Instrument Air Pressure Control valve,CIA-PCV-2B,found Not Intact.Cause of Misadjustment of CIA-PCV-2B Unknown.Event Will Be Communicated to Plant employees.W/970815 Ltr ML17292B0201997-08-15015 August 1997 LER 97-S01-00:on 970718,failure to Take Compensatory Measure for Inoperative Microwave Security Zone Occurred. Caused by Personnel Error.Training Will Be Conducted W/ Appropriate Members of Security force.W/970815 Ltr ML17292A9481997-07-23023 July 1997 LER 97-007-00:on 970611,voluntary Rept of Automatic Start of DG-1 & DG-2 Was Experienced.Caused by Undervoltage Condition on Electrical Busses SM-7 & SM-8.Circulating Water Pump CW-P-1C Control Switch Placed in pull-to-lock.W/970723 Ltr ML17292A9201997-06-26026 June 1997 LER 97-006-00:on 970527,non-performance of Surveillance Requirement 3.6.1.3.2 for Blind Fanges,Was Noted.Caused Because Misunderstanding of Intent of Specs.Added Five Structural Assemblies for SP.W/970626 Ltr ML17292A8331997-04-28028 April 1997 LER 97-004-00:on 970327,plant Operators Manually Scrammed Reactor as Required by TS Due to Entry Into Region a of power-to-flow Map Following Planned Trip of Single Mfp. Event Evaluation teams,established.W/970428 Ltr ML17292A8311997-04-28028 April 1997 LER 97-005-00:on 970327,valid Reactor Scram Signal Received Due to Low Water Level Condition During Preparations for SRV Testing.Caused by Risks & Consequences of Decisions Not Completely Identified.Restored Water level.W/970428 Ltr ML17292A8251997-04-21021 April 1997 LER 97-003-00:on 970320,notification of Noncompliance W/Ts as TS SRs for Response Time Testing Were Not Being Met for Specified Instrumentation in Rps,Pcis & Eccs.Requested Enforcement Discretion for One Time exemption.W/970421 Ltr ML17292A7431997-03-20020 March 1997 LER 97-002-00:on 970218,determined That Rod Block Monitor (RBM) Calibr Values Were Not Set IAW Tech Specs.Caused by Calibr Procedures Inadequacies.Revised & re-performed RBM Channel Calibr procedures.W/970330 Ltr ML17292A7401997-03-13013 March 1997 LER 97-001-00:on 970211,reactor Water Cleanup Sys Blowdown Flow Isolation Setpoint Was Slightly Above TS Allowable Valve Occurred Due to Calculation Error.Lds Fss LD-FS-15 LD-FS-16 Were Declared inoperable.W/970313 Ltr ML17292A6641997-01-22022 January 1997 LER 96-009-00:on 961220,miscalculation of Instantaneous Overcurrent Relay Settings Resulted in Inoperability of safety-related Equipment.Caused by Utilization of Inappropriate Design.Testing Was completed.W/970122 Ltr ML17292A6461997-01-0606 January 1997 LER 96-008-00:on 961205,failure to Comply with TS Action Requirement for Emergency Core Cooling Sys Actuation Instrumentation Occurred Due to Unidentified Inoperability Condition.Pmr initiated.W/970106 Ltr ML17292A6371996-12-19019 December 1996 LER 96-007-00:on 961122,electrical Breakers Were Not Seismically Qualified in Test/Disconnect Position.Circuit Breaker Mfg Did Not Consider Raced Out Breaker Position During Testing.Relocated Circuit breakers.W/961217 Ltr ML17292A4121996-08-0808 August 1996 LER 96-006-00:on 960709,average Power Range Monitor Rod Block Downscale Surveillance Not Performed Prior to Entry Into Mode 1.Caused by long-standing Misinterpretation of Requirements of Tss.Procedures revised.W/960808 Ltr ML17292A3801996-07-24024 July 1996 LER 96-004-00:on 960624,plant Was Manually Scrammed by Control Room Personnel Due to Reactor Water Level Transient Experienced During Testing of Digital Feedwater Sys.Caused by Programming Error.Sys Was corrected.W/960724 Ltr ML17292A3771996-07-24024 July 1996 LER 96-005-00:on 960624,determined Missed Surveillance Test Re Channel Check of Average Power Range Monitor.Caused by Inadequate Procedures.Revised Surveillance Procedure Re When APRM Checks Must Be performed.W/960724 Ltr ML17292A3641996-07-12012 July 1996 LER 96-003-00:on 960615,required Surveillance Test Not Performed When Required by TS 3.4.1.3.Caused by Inadequate Procedures.Implementing Surveillance Procedure & Reactor Plant Startup Procedures revised.W/960712 Ltr ML17292A3361996-06-20020 June 1996 LER 96-002-00:on 960504,critical Bus SM-8 Lost Power When Supply Breaker 3-8 Tripped.Caused by Personnel Error. Operators Counselled & Procedures revised.W/960620 Ltr ML17292A2861996-05-24024 May 1996 LER 96-001-00:on 960425,inadvertent ESF Actuations Occurred Due to Tripping of Temporary Power Supply to IN-3.Caused by Personnel Error.Operations Restored to IN-3 Loads & Reset ESF actuations.W/960524 Ltr ML17291B0891995-10-19019 October 1995 LER 95-011-00:on 950919,failed to Comply W/Ts SR for RCIC Sys Due to Analysis Deficiency That Resulted in Inadequate Surveillance Test Procedure.Surveillance Procedure Revised to Correct deficiency.W/951019 Ltr ML17291A9021995-07-0707 July 1995 LER 95-010-00:on 950609,HPCS DG Declared Inoperable Due to Discovery That TS Test Method Incomplete.Caused by Inadequate Testing Procedure.Test Procedure for HPCS DG Reviewed & Special Test Procedures written.W/950707 Ltr ML17291A9031995-07-0707 July 1995 LER 95-009-00:on 950607,inadvertent MSIV Closure Occurred During Surveillance Test Due to Poor Communication Between Test Team.Determined That MSIV Closure Not Valid Because Closure Not Triggered by Plant conditions.W/950707 Ltr ML17291A8501995-06-0808 June 1995 LER 95-006-01:on 950405,reactor Scram Occurred During Surveillance Testing Due to Protective Sys Relay Failure. Replaced Failed Relay Before Plant Startup ML17291A8101995-05-12012 May 1995 LER 95-008-00:on 940125,TS Wording Lead to Potential TS Violation.Caused by Lack of Clarity in Ts.Submitted Improved TS for Plant to Provide Addl clarity.W/950512 Ltr ML17291A7841995-05-0505 May 1995 LER 95-007-00:on 950222,emergency Diesel Start Occurred Due to Voltage Transient on BPA Grid.Confirmation Was Received at 17:51 H That Disturbance Had Originated in BPA Grid ML17291A7801995-05-0404 May 1995 LER 95-006-00:on 950405,main Turbine Trip Occurred During Performance of Surveillance Test Due to Protective Sys Relay Failed.Replaced Failed Relay Before Plant startup.W/950504 Ltr ML17291A7851995-05-0303 May 1995 LER 95-005-00:on 950222,inoperable IRM Had Been Relied Upon to Meet TS Requirements During Reactor Startup.Caused by Lack of Neutron Source to Test Instrumentation. Sys Knowledge Gained Will Be incorporated.W/950503 Ltr ML17291A7071995-03-25025 March 1995 LER 95-004-00:on 950226,malfunction in Main Turbine DEH Control Sys Caused All Four High Pressure Turbine Governor Valves to Rapidly Close.Caused by Blown Fuse.Suspected Faulty Circuit Card replaced.W/950325 Ltr ML17291A7011995-03-20020 March 1995 LER 95-002-00:on 950218,automatic Reactor Scram Occurred. Caused by Erroneous Positioning of Control During Performance of Scheduled Periodic Functional Test.Control repositioned.W/950320 Ltr 1999-07-20
[Table view] Category:TEXT-SAFETY REPORT
MONTHYEARML17284A9001999-10-31031 October 1999 Rev 0 to COLR 99-15, WNP-2 Cycle 15,COLR GO2-99-177, LER 99-S01-00:on 990903,failure to Take Compensatory Measure within Required Time Upon Failure of Isolation Zone Microwave Unit,Was Noted.Caused by Personnel Error.Provided Refresher Training on Compensatory Measures.With1999-10-0101 October 1999 LER 99-S01-00:on 990903,failure to Take Compensatory Measure within Required Time Upon Failure of Isolation Zone Microwave Unit,Was Noted.Caused by Personnel Error.Provided Refresher Training on Compensatory Measures.With ML17284A8941999-09-30030 September 1999 Monthly Operating Rept for Sept 1999 for WNP-2.With 991012 Ltr ML17284A8801999-08-31031 August 1999 Monthly Operating Rept for Aug 1999 for WNP-2.With 990910 Ltr ML17284A8691999-07-31031 July 1999 Monthly Operating Rept for July 1999 for WNP-2.With 990813 Ltr ML17292B7421999-07-20020 July 1999 LER 99-001-00:on 990628,ESF Signal Closed All Eight MSIVs While Plant Was Shutdown.Caused by Failure of Relay RPS-RLY-K10D.Subject Relay Was Replaced & Tested on 990630. with 990720 Ltr ML17292B7271999-06-30030 June 1999 Monthly Operating Rept for June 1999 for WNP-2.With 990707 Ltr ML17292B6961999-05-31031 May 1999 Monthly Operating Repts for May 1999 for WNP-2.With 990608 Ltr ML17292B6641999-04-30030 April 1999 Monthly Operating Rept for Apr 1999 for WNP-2.With 990507 Ltr ML17292B6391999-03-31031 March 1999 Monthly Operating Rept for Mar 1999 for WNP-2.With 990413 Ltr ML17292B5871999-02-28028 February 1999 Monthly Operating Rept for Feb 1999 for WNP-2.With 990311 Ltr ML17292B5571999-01-31031 January 1999 Monthly Operating Rept for Jan 1999 for WNP-2.With 990210 Ltr ML17292B5621999-01-31031 January 1999 Rev 1 to COLR 98-14, WNP-2 Cycle 14 Colr. ML17292B5341999-01-15015 January 1999 Part 21 Rept Re Incorrect Modeling of BWR Lower Plenum Vol in Bison.Defect Applies Only to Reload Fuel Assemblies Currently in Operation at WNP-2.BISON Code Model for WNP-2 Has Been Revised to Correct Error ML17292B5331999-01-15015 January 1999 Part 21 Rept Re XL-S96 CPR Correlation for SVEA-96 Fuel. Defect Applies Only to WNP-2,during Cycles 12,13 & 14 Operation.Evaluations of Defect Performed by ABB-CE ML17292B4791998-12-31031 December 1998 Washington Public Power Supply Sys 1998 Annual Rept. with 981215 Ltr ML17292B5351998-12-31031 December 1998 Monthly Operating Rept for Dec 1998 for WNP-2.With 990112 Ltr ML17292B5741998-12-31031 December 1998 WNP-2 1998 Annual Operating Rept. with 990225 Ltr ML17284A8231998-11-30030 November 1998 Monthly Operating Rept for Nov 1998 for WNP-2.With 981207 Ltr ML17284A8081998-10-31031 October 1998 Monthly Operating Rept for Oct 1998 for WNP-2.With 981110 Ltr ML17292B4451998-10-27027 October 1998 LER 98-012-01:on 980715,failure to Comply with Requirements of TS SR 3.8.4.7 Was Noted.Caused by Inadequate Work Practices.Training Session Was Held with Personnel.With 981027 Ltr ML17284A7831998-09-30030 September 1998 Monthly Operating Rept for Sept 1998 for WNP-2.With 981007 Ltr ML17284A7491998-09-10010 September 1998 WNP-2 Inservice Insp Summary Rept for Refueling Outage RF13 Spring,1998. ML17284A7561998-09-0303 September 1998 LER 98-013-00:on 980805,ESF Actuations Were Noted Due to Deenergization of Vital Electrical Bus SM-8.Caused by Inadequate Direction in Troubleshooting Plan.Will Conduct Training for Engineering Personnel.With 980903 Ltr ML17284A7571998-09-0202 September 1998 LER 98-014-00:on 980807,completion of TS 3.8.1.F Required Shutdown Due to Inoperability of EDG-2 Was Noted.Caused by Degraded Voltage Regulator for DG-2.Replaced Voltage Regulator & Associated Scrs.With 980902 Ltr ML17284A7551998-09-0202 September 1998 LER 98-015-00:on 980808,discovered Reactor Coolant Pressure Boundary Leak During Shutdown Conditions.Caused by Leakage from Socket Weld (Fwb 63) on Elbow Connection.Failed Piping Connection Was Replaced.With 980902 Ltr ML17284A7681998-08-31031 August 1998 Monthly Operating Rept for Aug 1998 for WNP-2.With 980915 Ltr ML17284A7311998-08-17017 August 1998 LER 98-012-00:on 980716,determined That 24-month SR 3.8.4.7 Had Not Been Fulfilled within Specified Frequency.Caused by Inadequate Work Practices.License Requested & Received Enforcement Discretion Re Battery Svc test.W/980817 Ltr ML17284A7261998-07-31031 July 1998 Monthly Operating Rept for July 1998 for WNP-2.W/980810 Ltr ML17284A7121998-07-23023 July 1998 LER 98-006-01:on 980520,discovered Discrepancies in Low Voltage Bus Calculations During Review of 10CFR50,App R Calculations for High Impedance Faults.Caused by Inadequate Work Practices.Implemented Procedural Changes ML17284A6951998-07-17017 July 1998 LER 98-011-00:on 980617,ECCS Pump Room Flooding Was Noted Due to FP Sys Pipe Break.Caused by Inadequate Design of FP Sys.Detailed Review of FP Sys Design Was Conducted. W/980717 Ltr ML17284A6961998-07-15015 July 1998 LER 98-010-00:on 980615,TS Required Shutdown Due to Inoperability of TIP Sys Isolation Valve Was Noted.Caused by Improper Installation of TIP Tubing.Reattached Affected Tubing & Inspected Other TIP tubing.W/980715 Ltr ML17284A6731998-07-0101 July 1998 LER 98-009-00:on 980606,nuclear Steam Supply Shutoff Sys Group 3 & 4 Isolations During Testing Was Noted.Caused by Procedural Deficiency.Counseled Individuals Involved in preparation.W/980701 Ltr ML17284A6751998-06-30030 June 1998 Ro:On 980617,flooding of RB Northeast Stairwell with Consequential Flooding of Two ECCS Pump Rooms.Caused by Inadequate Fire Protection Sys Design.Pumped Out Water from Affected Areas to Point Below Berm Areas of Pump Rooms ML17284A6641998-06-24024 June 1998 LER 98-008-00:on 980531,inadvertent Full Scram During RPV Leak Testing in Mode 4 Was Noted.Caused by Change in Mgt Techniques.Revised Procedures to Take Into Account Addl Water Head in Pressure Sensing lines.W/980624 Ltr ML17284A6651998-06-24024 June 1998 LER 98-007-00:on 980530,inadvertent Full Scram & Division 1 ECCS Injection Was Noted.Caused by Failure to Meet Mgt Work Practice Expectation When Encountering Deficient Procedure. Incident Review Board Convened to Review event.W/980624 Ltr ML17284A6631998-06-19019 June 1998 LER 98-006-00:on 980520,discovered Discrepancies in Low Voltage Bus Calculations During Review of App R Calculations for High Impedance Fault Analysis.Caused Indeterminate. Implemented Procedural Changes Involving Operator Action ML17284A6551998-06-0404 June 1998 LER 98-005-00:on 980506,potential for Failure of RHR Sys Valve to Close on Isolation Signal Was Noted.Caused by Design Deficiency.Caution Tag Was Placed on RHR-V-40 Control Switch to Inform Plant Operators of limitation.W/980604 Ltr ML17284A6421998-06-0101 June 1998 LER 98-004-00:on 980502,determined That Primary Containment Penetration Overcurrent Protection Does Not Meet Reg Guide 1.63 Requirements.Caused by Inadequate Design Changes. Installed Addl Fuse in RHR-MO-9 circuit.W/980601 Ltr ML17284A6491998-05-31031 May 1998 Rev 0 to COLR 98-14, WNP-2,Cycle 14 Colr. ML17292B4031998-05-31031 May 1998 Monthly Operating Rept for May 1998 for WNP-2.W/980608 Ltr ML17292B3921998-04-30030 April 1998 Monthly Operating Rept for Apr 1998 for WNP-2.W/980513 Ltr ML17292B3291998-04-0909 April 1998 LER 98-003-00:on 980311,WNP-2 Experienced SCRAM Signal as Result of Low Rpv.Caused by Less than post-SCRAM Operational Strategy for Resetting SCRAM Signal in Conditions.Changes in post-SCRAM Operational Strategy implemented.W/980409 Ltr ML17292B3281998-04-0909 April 1998 LER 98-002-00:on 980311,reactor Scram & Plant Transient Occurred,Due to Failed Closed Main Steam Isolation Valve. Caused by Loss of Pneumatic Actuating Supply Pressure. Problem Evaluation Request Written for Failure of MS-V-22D ML17292B3371998-03-31031 March 1998 Monthly Operating Rept for Mar 1998 for WNP-2.W/980409 Ltr ML17292B2641998-03-0404 March 1998 Performance Self Assessment,WNP-2. ML17292B2661998-03-0404 March 1998 LER 98-001-00:on 980203,automatic Start of HPCS EDG Was Noted.Caused by Operator Error.Operations Crew Stabilized Plant at Approximately 75% Reactor Power & Investigation of Event Was initiated.W/980304 Ltr ML17292B2911998-02-28028 February 1998 Monthly Operating Rept for Feb 1998 for WNP-2.W/980313 Ltr ML17284A7971998-02-17017 February 1998 Rev 28 to Operational QA Program Description, WPPSS-QA-004.With Proposed Rev 29 ML17292B3591998-02-12012 February 1998 WNP-2 Cycle 14 Reload Design Rept. 1999-09-30
[Table view] |
Text
REGULATORY INFORMATION DISTRIBUTION SYSTEM (RIDS)
CESSION NBR:9412210161 DOC.DATE: 94/12/12 NOTARIZED: NO DOCKET ACIL:50-397 WPPSS Nuclear Project, Unit 2, Washington Public Powe 05000397 AUTH. NAME AUTHOR AFFILIATION FOLEY,C.J. Washington Public Power Supply System PARRISH,J.V. Washington Public Power Supply System RECIP.NAME RECIPIENT AFFILIATION
SUBJECT:
LER 94-020-00:on 941111,postulated that MCR fire could induce hot short that could result in spurious closure of MO CI valve CIA-V-20.Caused by inadequate analysis.Continous fire watch established for area.W/941212 ltr.
DISTRIBUTION CODE: IE22T COPIES RECEIVED LTR t ENCL t SIZE: S TITLE: 50.73/50.9 Licensee Event Report (LER), Incident Rpt,-etc.
NOTES RECIPIENT COPIES RECIPIENT COPIES ID CODE/NAME LTTR ENCL ID CODE/NAME LTTR ENCL PD4-2 PD 1 1 CLIFFORD,J 1 1 INTERNAL: ACRS 1 1 AEO~DS+DJRAB 2 2 AEOD/SPD/RRAB 1 1 ~FXZZ CENSER 02 1 1 NRR/DE/ECGB 1 1 RRR/DE/EELB 1 1 NRR/DE/EMEB 1 1 NRR/DISP/PIPB 1 1 NRR/DOPS/OECB 1 1 NRR/DRCH/HHFB 1 1.
NRR/DRCH/HICB 1 1 NRR/DRCH/HOLB 1 1 NRR/DRSS/PRPB 2 2 NRR/DSSA/SPLB 1 1 NRR/DSSA/SRXB 1 1 RES/DSIR/EIB 1 1 RGN4 FILE 01 1 1 EXTERNAL: L ST LOBBY WARD 1 1 LITCO BRYCE,J H 2 2 NOAC MURPHY,G.A 1 1 NOAC POORE,W. 1 1 NRC PDR 1 1 NUDOCS FULL TXT 1 1 YOTE TO ALL"RIDS" RECIPIENTS:
PLEASE IIELP I'S TO RFDUCE O',KSTE! CONTACT'I'l!E DQCI. XIEiTCOi'TROI.
DESk, ROOXI Pl-37 (EX I: 304-~OS3 ) TO I;LfhflbKTE 5'OI.'lI XAifLFIIOif DIS'I'RIIIO'I'IOiLIS'I'S I'OR DOCI'Nfl i'I'S YOl')Oi"I'I I'.Ii!
FULL TEXT CONVERSION REQUIRED TOTAL NUMBER OF COPIES REQUIRED: LTTR 28 ENCL 28
WASHINGTON PUBLIC POWER SUPPLY SYSTEM P.O. Box 968 ~ 3000 George Washington Way ~ Richland, Washington 99352 December 12, 1994 G02-94-277 Docket No. 50-397 Document Control Desk U.S. Nuclear Regulatory Commission Washington, D.C. 20555
Subject:
NUCLEAR PLANT WNP-2, OPERATING LICENSE NPF-21 LICENSEE EVENT REPORT NO.94-020 Transmitted herewith is Licensee Event Report No.94-020 for the WNP-2 Plant. This report is submitted in response to the reporting requirements of 10CFR50.73 and discusses the items of reportability, corrective action taken, and action taken to preclude recurrence.
Should you have any questions or desire additional information, please call me or D.A, Swank at (509) 377-4278.
Sincerely,
,( ~d
. V. Parrish (Mail Drop 1023)
Assistant Managing Director, Operations JVP/CJF/jcs Enclosure CC: LJ Callan, NRC-RIV KE Perkins, Jr., NRC-RIV, Walnut Creek Field Office NS Reynolds, Winston & Strawn NRC Sr. Resident Inspector (Mail Drop 927N, 2 Copies)
INPO Records Center - Atlanta, GA DL Williams, BPA (Mail Drop 399) 9412210161 941212 PDR ADOD'. 05OCi0397 PDR
LICENSEE EVE REPORT (LER)
AGILITY NAME (I) DOCKET UMB R ( ) PAGE (3) ashin ton Nuclear Plant - Unit 2 0 5 0 0 0 3 9 7 I OF 4 (4)
POI'ENTIAL OF SPURIOUS ACTUATION OF PNEUMATIC SUPPLY VALVE'IQ IMPAIR OPERATION OF MAINSTEAM SAFETY RELIEF VALVES EVENT DATE (5) LER NUMBER (6) REPORT DATE (7) OTHER FACILITIES INVOLVED (8)
MONTH OAY YEAR YEAR SEQUENTIAL EV I SION MONTH OAY YEAR FACILITY NAMES CKE HUHB R (5)
HUMBER '<g UMBER 5 0 0 0 1 1 I 1 9 4 9 4 0 2 0 0 0 1 2 1 2 9 4 5000 P ERAT ING HIS REPORT IS SUBMITTED PURSUANT TO THE REQUIREMENTS OF 10 CFR II: (Ch eck one or more of the following) (1 ODE (9)
OWER-LEVEL 0.402(b) 20.405(C) 50.73(a)(2)(iv) 77.71(b)
(10) 0.405(a)(1)(i) 50.36(c)(1) 50.73(a)(2)(v) 73.73(c) 0.405(a)(1)(ii) 50.36(c)(2) 50.73(a)(2)(vii) THER (Specify in Abstract 20.405(a)(1)(iii) 50.73(a)(2)(i) 50.73(a)(2)(viii)(A) claw and in Text, NRC 20.405(a)(1)(iv) 50.73(a)(2)(ii) 50.73(a)(2)(viii)(B) orm 366A) 20.405(a)(1)(v) 50.73(a)(2)(iii) 50.73(a)(2)(x)
LICENSEE CONTACT FOR THIS LER 12 TELEPHOHE HUHBER REA CODE C.J. Foley, Licensing Engineer 0 9 7' - 4 3 2 5 COHPLETE ONE LINE FOR EACH COHPOHEHT FAILURE DESCRIBED IH THIS REPORT (13)
CAUSE SYSTEM COHPOHEHT MANUFACTURER EPORTABLE CAUSE SYSTEH COMPONENT MANUFACTURER REPORTABLE 0 HPRDS V4:: 0 HPRDS NI'Y'".:'I 5<o <,<< &~Pi<
HA SUPPLEMEHTAL REPORT EXPECTED (14) EXPECTED SUBH1SSI OH MONTH DAY YEAR ATE (15)
YES (If yes, complete EXPECTED SUBHISSIOH DATE) NO BlACT On November 11, 1994, WNP-2 was operating at 100% power in Mode 1. An engineer postulated that a Main Control Room fire could induce a hot short that could result in spurious closure of motor-operated containment isolation valve CIA-V-20. This might result in depletion of pneumatic supplies for Main Steam Relief Valves during the interval between evacuation of the Control Room and assumption of plant
'control from remote shutdown panels. No fire actually occurred. The NRC was notified of this event at 1726 (PST) pursuant to 10CFR50.72(b)(2)(iii)(A). Subsequent analysis revealed that the event was due to inadequate analysis rather than a condition that would have prevented maintaining the reactor safely shut down in event of a Control Room fire and should be reported only under 10CFR50.73(a)(2)(iii)(A). The cause of the event was a design deficiency due to lack of adequate consideration of the plant response during the interval between Control Room evacuation due to a fire and assumption of plant control from the remote shutdown panels.
A continuous fire watch was established for the area, and a procedure revised to assure an operator would be immediately prestaged at a remote shutdown panel to transfer control of certain Main Steam Relief Valves from the Control Room to a remote shutdown panel in event of a Control Room fire. A design hange will be implemented to eliminate the problem, and a procedure governing analysis of equipment.
used for safe shutdown after a Control Room fire will be changed to require consideration of on-going plant processes during the interval between Control Room evacuation and assumption of control from remote panels.
LICENSEE EVENT REPORTER)
TEXT CONTINUATIOPP ILITY NAME (I) DOCKET NUMBER (2) LER NUMBER (8) AGE (3) ear umber ev. No.
ashington Nuclea) Plant - Unit 2
\ 0 5 0 0 0 3 9 7 4 20 00 2 OF 4 ITLE (4) P POTENTIAL OF SPURIOUS ACTUATION OF PNEUMATIC SUPPLY VALVE TO IMPAIR OPERATION OF HAIN STEAM SAFETY RELIEF VALVES Event De ri ion On November 11, 1994, WNP-2 was operating at 100% power in Mode 1. As a result of a review of the design and layout of controls and conductors located in the Control Room, an engineer postulated that a fire in the Main Control Room could induce a hot short in a control switch [HS] or an electrical cable [CBLI],
that could result in spurious closure of motor-operated containment isolation valve [ISV] CIA-V-20. This valve provides compressed nitrogen to eighteen accumulators [ACC] inside of primary containment that are associated with the eighteen Main Steam Safety Relief Valves (MSRVs) [SB] [RV]. Spurious closure of this valve could result in the inability to manually activate 3 of 6 MSRVs from a remote location, as could be necessary if the Main Control Room had to be evacuated due to the postulated fire.
'The NRC was notified of this event at 1726 (PST) pursuant to 10CFR50.72(b)(2)(iii)(A).
Further Evalu ti n the event that the Main Control Room must be evacuated because of a Control Room fire, the Reactor must be depressurized from remote shutdown panels to permit cooling to be established by Low Pressure Core Injection (LPCI) [BO]. Three MSRVs must be opened from the Remote Shutdown (RSD) panel, and three from the Alternate Remote Shutdown (ARSD) panel, using switches on these panels. MSRV design is such that compressed gas is used to overcome actuator spring forces when the MSRV is opened in either relief or manual mode. Each MSRV is equipped with pneumatic accumulators [TK] to provide the compressed gas. The accumulators are serviced by a compressed nitrogen supply located external to the primary containment. The three MSRVs controlled from the Remote Shutdown (RSD) panel are designed to be part of the Automatic Depressurization System (ADS), the three that may be controlled from the ARSD panel are no'nADS. ADS MSRVs are equipped with two accumulators, a larger one for use only in ADS mode, and a smaller one for use in ordinary relief mode. NonADS MSRVs are equipped with only the smaller sized accumulators for use in ordinary relief mode. The potential spurious closure of motor-operated containment isolation valve CIA-V-20 would isolate the smaller accumulators for all eighteen MSRVs from the external compressed nitrogen supply. During Control Room evacuation, the MSRVs may open cyclically in the relief mode, resulting in rapid depletion of the isolated accumulator for the particular MSRV. The MSRV(s) would then close until Reactor pressure rose to the safety setting, at which level the Reactor pressure is sufiicient to overcome MSRV spring actuator forces. The MSRVs would then reopen, maintaining Reactor pressure at the safety setting level. While Reactor overpressure is thereby prevented, lack of compressed nitrogen in the smaller accumulators would prevent manually opening the three nonADS MSRVs from the ARSD panel, delaying initiation of LPCI. The other three MSRVs are ADS equipped.
The larger ADS accumulators would not be depleted by MSRV cycling in relief mode. Consequently, the ree ADS MSRVs could still be opened from the RSD panel to depressurize the Reactor to enable cooling y LPCI. However, the current commitment requires six MSRVs to be opened to assure depressurization in time to prevent peak fuel cladding temperatures from exceeding approved limits. Consequently, safe shutdown of the Reactor in strict adherence to the currently authorized analysis would be jeopardized if a
'ICENSEE EVENT REPORTER)
TEXT CONTINUATION ILITY NAME (I) OOCKET NUMBER (2) LER NUMBER (8) AGE (3) ear umber ev. No.
ashington'uclear Plant - Unit 2 0 5 0 0 0 3 9 7 4 2 0 0 3 F 4 ITLE (4)
POTENTIAL OF SPURIOUS. ACTUATION OF PNEUMATIC SUPPLY VALVE TO IMPAIR OPERATION OF MAIN STEAM SAFETY RELIEF VALVES fire induced hot short caused spurious closure of the CIA motor-operated containment isolation valve providing compressed nitrogen service to accumulators for the three MSRVs to be opened from the ARSD panel.
V The basic design of the RSD/ARSD panels was established during original construction, at which time a choice was made to control 3 nonADS MSRVs from the ARSD panel. No bases has been found for that choice. However, if 'ADS MSRVs had been chosen for both the RSD and ARSD panels, the situation outlined above would not be possible, because six ADS MSRVs would be available on the remote panels.
This constitutes a design error based on lack of adequate consideration of plant response during the interval between Control Room evacuation and assumption of control from remote shutdown panels. A safe shutdown analysis was performed by the original architect engineer, and was updated by the Supply System in 1990. Consideration was given to the capacity of the accumulators in an analysis in 1988, and again in 1994. However, none of these analyses accurately accounted for the plant response during the time interval between Control Room evacuation and assumption of plant control from the RSD/ARSD panels. This time
'nterval is between 5 and 10 minutes, while accumulator depletion could occur in approximately
.2 minutes if MSRV cycling began immediately upon initiation of a Control Room fire that spuriously losed CIA-V-20. Therefore, the cause of the event was a design deficiency during the original construction phase, resulting from analysis that did not adequately consider the plant response during the time interval intervening between Control Room evacuation due to a fire and assumption of plant control from the remote shutdown panels.
rrective Ac i n A continuous fire watch was immediately initiated to assure early detection of a Main Control Room fire.
The procedure governing safe shutdown for a Control Room fire scenario was changed to require immediate prestaging of an operator to the ARSD panel to transfer control of the three nonADS MSRVs from the Main Control Room to the ARSD panel. This would have the effect of putting those MSRVs on manual control from the ARSD panel, preventing automatically initiated use of the compressed nitrogen in those three accumulators.
To address the lack of consideration of the time interval between Control Room evacuation and assumption of control of the plant from the RSD/ARSD panels, the procedure defining the process to be followed for safe shutdown analyses will be augmented to require explicit consideration of time needed for operators to react to fire conditions. The current design review will be completed to assure no similar problems are present.
'ICENSEE EVENT REPORT/JR)
TEXT CONTINUATION ILITY NANE (I) DOCKET NUNBER (2) LER NUMBER (8) AGE (3) ear Ianber ev. No.
ashington Nuclear Plant - Unit 2 0 5 0 0 0 3 9 7 4 20 00 4 OF 4 ITLE (4)
POTENTIAL OF SPURIOUS ACTUATION OF PNEUMATIC SUPPLY VALVE TO IMPAIR OPERATION OF HAIN STEAM SAFETY RELIEF VALVES A plant design change will be implemented during the refueling outage scheduled for the Spring of 1995 to alter the controls on the ARSD panel such that the existing switches will control three ADS MSRVs instead of three nonADS MSRVs. After implementation, it will be possible to open-a total of six ADS MSRVs from outside the Control Room. This will assure that adequate compressed nitrogen is available to.open these MSRVs from the RSD/ARSD panels under postulated circumstances.
~fi lfi Analysis performed by General Electric (GE) in support of WNP-2 power uprate indicates that reactor depressurization may be effected with 2 MSRVs while maintaining peak fuel clad temperatures (PCT) slightly below 1500'F, the threshold for fuel damage. In this specific case, the core power was not at power uprate conditions, but at approximately 95% of that level. Consequently, the post-SCRAM thermal levels were also at 95% of the level assumed for the GE analysis; this would have the effect of reducing PCl'elow the predictions of the GE analysis. Three ADS MSRVs were actually available to depressurize the reactor for the Control Room fire scenario. The peak fuel cladding temperature would be lower for epressurization for 3 MSRVs than for 2 MSRVs. As a point of reference, the GE analysis also considers 6.MSRV case. The predicted PCT for that case is only 588'F. While no analysis is available for a 3 MSRV case, the two cases'available bound the actual situation. It may therefore be concluded that PCT would not have closely approached the 1500'F threshold for fuel damage if a recovery from an actual Control Room fire had to be effected.
Additionally, the probability of occurrence of Control Room fires that would result in both a Control Room evacuation and concurrent fire damage to the control circuits for valve CIA-V-20 is very low. The event arose from an examination of the possibilities of fire damage to equipment in the Control Room. No actual fire occurred.
Consequently, this event was not safety significant because if a fire had occurred in spite of the very low probability of occurrence of such an event, equipment was available to effect safe shutdown of the plant.
No radioactivity would have been released because the peak fuel cladding temperatures would have been maintained below the threshold of actual fuel damage.
imilar Even LER 94-010 documented inadequate analysis of the effect of a control room fire on circuitry supporting operation of the Residual Heat Removal System when initiated as necessary to safely shut down the plant after a fire.