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Category:LICENSEE EVENT REPORT (SEE ALSO AO
MONTHYEARML17292B7421999-07-20020 July 1999 LER 99-001-00:on 990628,ESF Signal Closed All Eight MSIVs While Plant Was Shutdown.Caused by Failure of Relay RPS-RLY-K10D.Subject Relay Was Replaced & Tested on 990630. with 990720 Ltr ML17292B4451998-10-27027 October 1998 LER 98-012-01:on 980715,failure to Comply with Requirements of TS SR 3.8.4.7 Was Noted.Caused by Inadequate Work Practices.Training Session Was Held with Personnel.With 981027 Ltr ML17284A7561998-09-0303 September 1998 LER 98-013-00:on 980805,ESF Actuations Were Noted Due to Deenergization of Vital Electrical Bus SM-8.Caused by Inadequate Direction in Troubleshooting Plan.Will Conduct Training for Engineering Personnel.With 980903 Ltr ML17284A7571998-09-0202 September 1998 LER 98-014-00:on 980807,completion of TS 3.8.1.F Required Shutdown Due to Inoperability of EDG-2 Was Noted.Caused by Degraded Voltage Regulator for DG-2.Replaced Voltage Regulator & Associated Scrs.With 980902 Ltr ML17284A7551998-09-0202 September 1998 LER 98-015-00:on 980808,discovered Reactor Coolant Pressure Boundary Leak During Shutdown Conditions.Caused by Leakage from Socket Weld (Fwb 63) on Elbow Connection.Failed Piping Connection Was Replaced.With 980902 Ltr ML17284A7311998-08-17017 August 1998 LER 98-012-00:on 980716,determined That 24-month SR 3.8.4.7 Had Not Been Fulfilled within Specified Frequency.Caused by Inadequate Work Practices.License Requested & Received Enforcement Discretion Re Battery Svc test.W/980817 Ltr ML17284A7121998-07-23023 July 1998 LER 98-006-01:on 980520,discovered Discrepancies in Low Voltage Bus Calculations During Review of 10CFR50,App R Calculations for High Impedance Faults.Caused by Inadequate Work Practices.Implemented Procedural Changes ML17284A6951998-07-17017 July 1998 LER 98-011-00:on 980617,ECCS Pump Room Flooding Was Noted Due to FP Sys Pipe Break.Caused by Inadequate Design of FP Sys.Detailed Review of FP Sys Design Was Conducted. W/980717 Ltr ML17284A6961998-07-15015 July 1998 LER 98-010-00:on 980615,TS Required Shutdown Due to Inoperability of TIP Sys Isolation Valve Was Noted.Caused by Improper Installation of TIP Tubing.Reattached Affected Tubing & Inspected Other TIP tubing.W/980715 Ltr ML17284A6731998-07-0101 July 1998 LER 98-009-00:on 980606,nuclear Steam Supply Shutoff Sys Group 3 & 4 Isolations During Testing Was Noted.Caused by Procedural Deficiency.Counseled Individuals Involved in preparation.W/980701 Ltr ML17284A6651998-06-24024 June 1998 LER 98-007-00:on 980530,inadvertent Full Scram & Division 1 ECCS Injection Was Noted.Caused by Failure to Meet Mgt Work Practice Expectation When Encountering Deficient Procedure. Incident Review Board Convened to Review event.W/980624 Ltr ML17284A6641998-06-24024 June 1998 LER 98-008-00:on 980531,inadvertent Full Scram During RPV Leak Testing in Mode 4 Was Noted.Caused by Change in Mgt Techniques.Revised Procedures to Take Into Account Addl Water Head in Pressure Sensing lines.W/980624 Ltr ML17284A6631998-06-19019 June 1998 LER 98-006-00:on 980520,discovered Discrepancies in Low Voltage Bus Calculations During Review of App R Calculations for High Impedance Fault Analysis.Caused Indeterminate. Implemented Procedural Changes Involving Operator Action ML17284A6551998-06-0404 June 1998 LER 98-005-00:on 980506,potential for Failure of RHR Sys Valve to Close on Isolation Signal Was Noted.Caused by Design Deficiency.Caution Tag Was Placed on RHR-V-40 Control Switch to Inform Plant Operators of limitation.W/980604 Ltr ML17284A6421998-06-0101 June 1998 LER 98-004-00:on 980502,determined That Primary Containment Penetration Overcurrent Protection Does Not Meet Reg Guide 1.63 Requirements.Caused by Inadequate Design Changes. Installed Addl Fuse in RHR-MO-9 circuit.W/980601 Ltr ML17292B3281998-04-0909 April 1998 LER 98-002-00:on 980311,reactor Scram & Plant Transient Occurred,Due to Failed Closed Main Steam Isolation Valve. Caused by Loss of Pneumatic Actuating Supply Pressure. Problem Evaluation Request Written for Failure of MS-V-22D ML17292B3291998-04-0909 April 1998 LER 98-003-00:on 980311,WNP-2 Experienced SCRAM Signal as Result of Low Rpv.Caused by Less than post-SCRAM Operational Strategy for Resetting SCRAM Signal in Conditions.Changes in post-SCRAM Operational Strategy implemented.W/980409 Ltr ML17292B2661998-03-0404 March 1998 LER 98-001-00:on 980203,automatic Start of HPCS EDG Was Noted.Caused by Operator Error.Operations Crew Stabilized Plant at Approximately 75% Reactor Power & Investigation of Event Was initiated.W/980304 Ltr ML17292B1111997-11-10010 November 1997 LER 97-011-00:on 971010,HPCS Battery Charger Failed.Caused by Failure of a Phase Firing Control Circuit Board Due to Aging During 7 Yrs of Use.Hpcs Sys Was Immediately Declared inoperable.W/971110 Ltr ML17292B1151997-11-0707 November 1997 LER 97-010-00:on 970906,discovered That TS SR 3.4.5.1 for Identified Portion of RCS Total Leakage Would Not Be Able to Perform within Time Limits of SR 3.0.2.Caused by Inadequate Methods.Method of Meeting SR 3.4.5.1 Established ML17292B0641997-09-24024 September 1997 LER 97-004-01:on 970327,plant Operators Manually Scrammed Reactor as Required by TS Due to Indication of Entry Into Region a of power-to-flow Map.Caused by Inadequate Attention to Detail.Established Event Evaluation teams.W/970924 Ltr ML17292B0241997-08-18018 August 1997 LER 97-009-00:on 970717,discovered Error in Recently Performed Inservice Testing procedure,OSP-TIP/IST-R701. Caused by Procedure Inadequacy.Plant Procedure OSP/TIP/IST-R701 Will Be changed.W/970818 Ltr ML17292B0291997-08-15015 August 1997 LER 97-008-00:on 970716,wire Seal Used to Lock Containment Instrument Air Pressure Control valve,CIA-PCV-2B,found Not Intact.Cause of Misadjustment of CIA-PCV-2B Unknown.Event Will Be Communicated to Plant employees.W/970815 Ltr ML17292B0201997-08-15015 August 1997 LER 97-S01-00:on 970718,failure to Take Compensatory Measure for Inoperative Microwave Security Zone Occurred. Caused by Personnel Error.Training Will Be Conducted W/ Appropriate Members of Security force.W/970815 Ltr ML17292A9481997-07-23023 July 1997 LER 97-007-00:on 970611,voluntary Rept of Automatic Start of DG-1 & DG-2 Was Experienced.Caused by Undervoltage Condition on Electrical Busses SM-7 & SM-8.Circulating Water Pump CW-P-1C Control Switch Placed in pull-to-lock.W/970723 Ltr ML17292A9201997-06-26026 June 1997 LER 97-006-00:on 970527,non-performance of Surveillance Requirement 3.6.1.3.2 for Blind Fanges,Was Noted.Caused Because Misunderstanding of Intent of Specs.Added Five Structural Assemblies for SP.W/970626 Ltr ML17292A8331997-04-28028 April 1997 LER 97-004-00:on 970327,plant Operators Manually Scrammed Reactor as Required by TS Due to Entry Into Region a of power-to-flow Map Following Planned Trip of Single Mfp. Event Evaluation teams,established.W/970428 Ltr ML17292A8311997-04-28028 April 1997 LER 97-005-00:on 970327,valid Reactor Scram Signal Received Due to Low Water Level Condition During Preparations for SRV Testing.Caused by Risks & Consequences of Decisions Not Completely Identified.Restored Water level.W/970428 Ltr ML17292A8251997-04-21021 April 1997 LER 97-003-00:on 970320,notification of Noncompliance W/Ts as TS SRs for Response Time Testing Were Not Being Met for Specified Instrumentation in Rps,Pcis & Eccs.Requested Enforcement Discretion for One Time exemption.W/970421 Ltr ML17292A7431997-03-20020 March 1997 LER 97-002-00:on 970218,determined That Rod Block Monitor (RBM) Calibr Values Were Not Set IAW Tech Specs.Caused by Calibr Procedures Inadequacies.Revised & re-performed RBM Channel Calibr procedures.W/970330 Ltr ML17292A7401997-03-13013 March 1997 LER 97-001-00:on 970211,reactor Water Cleanup Sys Blowdown Flow Isolation Setpoint Was Slightly Above TS Allowable Valve Occurred Due to Calculation Error.Lds Fss LD-FS-15 LD-FS-16 Were Declared inoperable.W/970313 Ltr ML17292A6641997-01-22022 January 1997 LER 96-009-00:on 961220,miscalculation of Instantaneous Overcurrent Relay Settings Resulted in Inoperability of safety-related Equipment.Caused by Utilization of Inappropriate Design.Testing Was completed.W/970122 Ltr ML17292A6461997-01-0606 January 1997 LER 96-008-00:on 961205,failure to Comply with TS Action Requirement for Emergency Core Cooling Sys Actuation Instrumentation Occurred Due to Unidentified Inoperability Condition.Pmr initiated.W/970106 Ltr ML17292A6371996-12-19019 December 1996 LER 96-007-00:on 961122,electrical Breakers Were Not Seismically Qualified in Test/Disconnect Position.Circuit Breaker Mfg Did Not Consider Raced Out Breaker Position During Testing.Relocated Circuit breakers.W/961217 Ltr ML17292A4121996-08-0808 August 1996 LER 96-006-00:on 960709,average Power Range Monitor Rod Block Downscale Surveillance Not Performed Prior to Entry Into Mode 1.Caused by long-standing Misinterpretation of Requirements of Tss.Procedures revised.W/960808 Ltr ML17292A3801996-07-24024 July 1996 LER 96-004-00:on 960624,plant Was Manually Scrammed by Control Room Personnel Due to Reactor Water Level Transient Experienced During Testing of Digital Feedwater Sys.Caused by Programming Error.Sys Was corrected.W/960724 Ltr ML17292A3771996-07-24024 July 1996 LER 96-005-00:on 960624,determined Missed Surveillance Test Re Channel Check of Average Power Range Monitor.Caused by Inadequate Procedures.Revised Surveillance Procedure Re When APRM Checks Must Be performed.W/960724 Ltr ML17292A3641996-07-12012 July 1996 LER 96-003-00:on 960615,required Surveillance Test Not Performed When Required by TS 3.4.1.3.Caused by Inadequate Procedures.Implementing Surveillance Procedure & Reactor Plant Startup Procedures revised.W/960712 Ltr ML17292A3361996-06-20020 June 1996 LER 96-002-00:on 960504,critical Bus SM-8 Lost Power When Supply Breaker 3-8 Tripped.Caused by Personnel Error. Operators Counselled & Procedures revised.W/960620 Ltr ML17292A2861996-05-24024 May 1996 LER 96-001-00:on 960425,inadvertent ESF Actuations Occurred Due to Tripping of Temporary Power Supply to IN-3.Caused by Personnel Error.Operations Restored to IN-3 Loads & Reset ESF actuations.W/960524 Ltr ML17291B0891995-10-19019 October 1995 LER 95-011-00:on 950919,failed to Comply W/Ts SR for RCIC Sys Due to Analysis Deficiency That Resulted in Inadequate Surveillance Test Procedure.Surveillance Procedure Revised to Correct deficiency.W/951019 Ltr ML17291A9021995-07-0707 July 1995 LER 95-010-00:on 950609,HPCS DG Declared Inoperable Due to Discovery That TS Test Method Incomplete.Caused by Inadequate Testing Procedure.Test Procedure for HPCS DG Reviewed & Special Test Procedures written.W/950707 Ltr ML17291A9031995-07-0707 July 1995 LER 95-009-00:on 950607,inadvertent MSIV Closure Occurred During Surveillance Test Due to Poor Communication Between Test Team.Determined That MSIV Closure Not Valid Because Closure Not Triggered by Plant conditions.W/950707 Ltr ML17291A8501995-06-0808 June 1995 LER 95-006-01:on 950405,reactor Scram Occurred During Surveillance Testing Due to Protective Sys Relay Failure. Replaced Failed Relay Before Plant Startup ML17291A8101995-05-12012 May 1995 LER 95-008-00:on 940125,TS Wording Lead to Potential TS Violation.Caused by Lack of Clarity in Ts.Submitted Improved TS for Plant to Provide Addl clarity.W/950512 Ltr ML17291A7841995-05-0505 May 1995 LER 95-007-00:on 950222,emergency Diesel Start Occurred Due to Voltage Transient on BPA Grid.Confirmation Was Received at 17:51 H That Disturbance Had Originated in BPA Grid ML17291A7801995-05-0404 May 1995 LER 95-006-00:on 950405,main Turbine Trip Occurred During Performance of Surveillance Test Due to Protective Sys Relay Failed.Replaced Failed Relay Before Plant startup.W/950504 Ltr ML17291A7851995-05-0303 May 1995 LER 95-005-00:on 950222,inoperable IRM Had Been Relied Upon to Meet TS Requirements During Reactor Startup.Caused by Lack of Neutron Source to Test Instrumentation. Sys Knowledge Gained Will Be incorporated.W/950503 Ltr ML17291A7071995-03-25025 March 1995 LER 95-004-00:on 950226,malfunction in Main Turbine DEH Control Sys Caused All Four High Pressure Turbine Governor Valves to Rapidly Close.Caused by Blown Fuse.Suspected Faulty Circuit Card replaced.W/950325 Ltr ML17291A7011995-03-20020 March 1995 LER 95-002-00:on 950218,automatic Reactor Scram Occurred. Caused by Erroneous Positioning of Control During Performance of Scheduled Periodic Functional Test.Control repositioned.W/950320 Ltr 1999-07-20
[Table view] Category:RO)
MONTHYEARML17292B7421999-07-20020 July 1999 LER 99-001-00:on 990628,ESF Signal Closed All Eight MSIVs While Plant Was Shutdown.Caused by Failure of Relay RPS-RLY-K10D.Subject Relay Was Replaced & Tested on 990630. with 990720 Ltr ML17292B4451998-10-27027 October 1998 LER 98-012-01:on 980715,failure to Comply with Requirements of TS SR 3.8.4.7 Was Noted.Caused by Inadequate Work Practices.Training Session Was Held with Personnel.With 981027 Ltr ML17284A7561998-09-0303 September 1998 LER 98-013-00:on 980805,ESF Actuations Were Noted Due to Deenergization of Vital Electrical Bus SM-8.Caused by Inadequate Direction in Troubleshooting Plan.Will Conduct Training for Engineering Personnel.With 980903 Ltr ML17284A7571998-09-0202 September 1998 LER 98-014-00:on 980807,completion of TS 3.8.1.F Required Shutdown Due to Inoperability of EDG-2 Was Noted.Caused by Degraded Voltage Regulator for DG-2.Replaced Voltage Regulator & Associated Scrs.With 980902 Ltr ML17284A7551998-09-0202 September 1998 LER 98-015-00:on 980808,discovered Reactor Coolant Pressure Boundary Leak During Shutdown Conditions.Caused by Leakage from Socket Weld (Fwb 63) on Elbow Connection.Failed Piping Connection Was Replaced.With 980902 Ltr ML17284A7311998-08-17017 August 1998 LER 98-012-00:on 980716,determined That 24-month SR 3.8.4.7 Had Not Been Fulfilled within Specified Frequency.Caused by Inadequate Work Practices.License Requested & Received Enforcement Discretion Re Battery Svc test.W/980817 Ltr ML17284A7121998-07-23023 July 1998 LER 98-006-01:on 980520,discovered Discrepancies in Low Voltage Bus Calculations During Review of 10CFR50,App R Calculations for High Impedance Faults.Caused by Inadequate Work Practices.Implemented Procedural Changes ML17284A6951998-07-17017 July 1998 LER 98-011-00:on 980617,ECCS Pump Room Flooding Was Noted Due to FP Sys Pipe Break.Caused by Inadequate Design of FP Sys.Detailed Review of FP Sys Design Was Conducted. W/980717 Ltr ML17284A6961998-07-15015 July 1998 LER 98-010-00:on 980615,TS Required Shutdown Due to Inoperability of TIP Sys Isolation Valve Was Noted.Caused by Improper Installation of TIP Tubing.Reattached Affected Tubing & Inspected Other TIP tubing.W/980715 Ltr ML17284A6731998-07-0101 July 1998 LER 98-009-00:on 980606,nuclear Steam Supply Shutoff Sys Group 3 & 4 Isolations During Testing Was Noted.Caused by Procedural Deficiency.Counseled Individuals Involved in preparation.W/980701 Ltr ML17284A6651998-06-24024 June 1998 LER 98-007-00:on 980530,inadvertent Full Scram & Division 1 ECCS Injection Was Noted.Caused by Failure to Meet Mgt Work Practice Expectation When Encountering Deficient Procedure. Incident Review Board Convened to Review event.W/980624 Ltr ML17284A6641998-06-24024 June 1998 LER 98-008-00:on 980531,inadvertent Full Scram During RPV Leak Testing in Mode 4 Was Noted.Caused by Change in Mgt Techniques.Revised Procedures to Take Into Account Addl Water Head in Pressure Sensing lines.W/980624 Ltr ML17284A6631998-06-19019 June 1998 LER 98-006-00:on 980520,discovered Discrepancies in Low Voltage Bus Calculations During Review of App R Calculations for High Impedance Fault Analysis.Caused Indeterminate. Implemented Procedural Changes Involving Operator Action ML17284A6551998-06-0404 June 1998 LER 98-005-00:on 980506,potential for Failure of RHR Sys Valve to Close on Isolation Signal Was Noted.Caused by Design Deficiency.Caution Tag Was Placed on RHR-V-40 Control Switch to Inform Plant Operators of limitation.W/980604 Ltr ML17284A6421998-06-0101 June 1998 LER 98-004-00:on 980502,determined That Primary Containment Penetration Overcurrent Protection Does Not Meet Reg Guide 1.63 Requirements.Caused by Inadequate Design Changes. Installed Addl Fuse in RHR-MO-9 circuit.W/980601 Ltr ML17292B3281998-04-0909 April 1998 LER 98-002-00:on 980311,reactor Scram & Plant Transient Occurred,Due to Failed Closed Main Steam Isolation Valve. Caused by Loss of Pneumatic Actuating Supply Pressure. Problem Evaluation Request Written for Failure of MS-V-22D ML17292B3291998-04-0909 April 1998 LER 98-003-00:on 980311,WNP-2 Experienced SCRAM Signal as Result of Low Rpv.Caused by Less than post-SCRAM Operational Strategy for Resetting SCRAM Signal in Conditions.Changes in post-SCRAM Operational Strategy implemented.W/980409 Ltr ML17292B2661998-03-0404 March 1998 LER 98-001-00:on 980203,automatic Start of HPCS EDG Was Noted.Caused by Operator Error.Operations Crew Stabilized Plant at Approximately 75% Reactor Power & Investigation of Event Was initiated.W/980304 Ltr ML17292B1111997-11-10010 November 1997 LER 97-011-00:on 971010,HPCS Battery Charger Failed.Caused by Failure of a Phase Firing Control Circuit Board Due to Aging During 7 Yrs of Use.Hpcs Sys Was Immediately Declared inoperable.W/971110 Ltr ML17292B1151997-11-0707 November 1997 LER 97-010-00:on 970906,discovered That TS SR 3.4.5.1 for Identified Portion of RCS Total Leakage Would Not Be Able to Perform within Time Limits of SR 3.0.2.Caused by Inadequate Methods.Method of Meeting SR 3.4.5.1 Established ML17292B0641997-09-24024 September 1997 LER 97-004-01:on 970327,plant Operators Manually Scrammed Reactor as Required by TS Due to Indication of Entry Into Region a of power-to-flow Map.Caused by Inadequate Attention to Detail.Established Event Evaluation teams.W/970924 Ltr ML17292B0241997-08-18018 August 1997 LER 97-009-00:on 970717,discovered Error in Recently Performed Inservice Testing procedure,OSP-TIP/IST-R701. Caused by Procedure Inadequacy.Plant Procedure OSP/TIP/IST-R701 Will Be changed.W/970818 Ltr ML17292B0291997-08-15015 August 1997 LER 97-008-00:on 970716,wire Seal Used to Lock Containment Instrument Air Pressure Control valve,CIA-PCV-2B,found Not Intact.Cause of Misadjustment of CIA-PCV-2B Unknown.Event Will Be Communicated to Plant employees.W/970815 Ltr ML17292B0201997-08-15015 August 1997 LER 97-S01-00:on 970718,failure to Take Compensatory Measure for Inoperative Microwave Security Zone Occurred. Caused by Personnel Error.Training Will Be Conducted W/ Appropriate Members of Security force.W/970815 Ltr ML17292A9481997-07-23023 July 1997 LER 97-007-00:on 970611,voluntary Rept of Automatic Start of DG-1 & DG-2 Was Experienced.Caused by Undervoltage Condition on Electrical Busses SM-7 & SM-8.Circulating Water Pump CW-P-1C Control Switch Placed in pull-to-lock.W/970723 Ltr ML17292A9201997-06-26026 June 1997 LER 97-006-00:on 970527,non-performance of Surveillance Requirement 3.6.1.3.2 for Blind Fanges,Was Noted.Caused Because Misunderstanding of Intent of Specs.Added Five Structural Assemblies for SP.W/970626 Ltr ML17292A8331997-04-28028 April 1997 LER 97-004-00:on 970327,plant Operators Manually Scrammed Reactor as Required by TS Due to Entry Into Region a of power-to-flow Map Following Planned Trip of Single Mfp. Event Evaluation teams,established.W/970428 Ltr ML17292A8311997-04-28028 April 1997 LER 97-005-00:on 970327,valid Reactor Scram Signal Received Due to Low Water Level Condition During Preparations for SRV Testing.Caused by Risks & Consequences of Decisions Not Completely Identified.Restored Water level.W/970428 Ltr ML17292A8251997-04-21021 April 1997 LER 97-003-00:on 970320,notification of Noncompliance W/Ts as TS SRs for Response Time Testing Were Not Being Met for Specified Instrumentation in Rps,Pcis & Eccs.Requested Enforcement Discretion for One Time exemption.W/970421 Ltr ML17292A7431997-03-20020 March 1997 LER 97-002-00:on 970218,determined That Rod Block Monitor (RBM) Calibr Values Were Not Set IAW Tech Specs.Caused by Calibr Procedures Inadequacies.Revised & re-performed RBM Channel Calibr procedures.W/970330 Ltr ML17292A7401997-03-13013 March 1997 LER 97-001-00:on 970211,reactor Water Cleanup Sys Blowdown Flow Isolation Setpoint Was Slightly Above TS Allowable Valve Occurred Due to Calculation Error.Lds Fss LD-FS-15 LD-FS-16 Were Declared inoperable.W/970313 Ltr ML17292A6641997-01-22022 January 1997 LER 96-009-00:on 961220,miscalculation of Instantaneous Overcurrent Relay Settings Resulted in Inoperability of safety-related Equipment.Caused by Utilization of Inappropriate Design.Testing Was completed.W/970122 Ltr ML17292A6461997-01-0606 January 1997 LER 96-008-00:on 961205,failure to Comply with TS Action Requirement for Emergency Core Cooling Sys Actuation Instrumentation Occurred Due to Unidentified Inoperability Condition.Pmr initiated.W/970106 Ltr ML17292A6371996-12-19019 December 1996 LER 96-007-00:on 961122,electrical Breakers Were Not Seismically Qualified in Test/Disconnect Position.Circuit Breaker Mfg Did Not Consider Raced Out Breaker Position During Testing.Relocated Circuit breakers.W/961217 Ltr ML17292A4121996-08-0808 August 1996 LER 96-006-00:on 960709,average Power Range Monitor Rod Block Downscale Surveillance Not Performed Prior to Entry Into Mode 1.Caused by long-standing Misinterpretation of Requirements of Tss.Procedures revised.W/960808 Ltr ML17292A3801996-07-24024 July 1996 LER 96-004-00:on 960624,plant Was Manually Scrammed by Control Room Personnel Due to Reactor Water Level Transient Experienced During Testing of Digital Feedwater Sys.Caused by Programming Error.Sys Was corrected.W/960724 Ltr ML17292A3771996-07-24024 July 1996 LER 96-005-00:on 960624,determined Missed Surveillance Test Re Channel Check of Average Power Range Monitor.Caused by Inadequate Procedures.Revised Surveillance Procedure Re When APRM Checks Must Be performed.W/960724 Ltr ML17292A3641996-07-12012 July 1996 LER 96-003-00:on 960615,required Surveillance Test Not Performed When Required by TS 3.4.1.3.Caused by Inadequate Procedures.Implementing Surveillance Procedure & Reactor Plant Startup Procedures revised.W/960712 Ltr ML17292A3361996-06-20020 June 1996 LER 96-002-00:on 960504,critical Bus SM-8 Lost Power When Supply Breaker 3-8 Tripped.Caused by Personnel Error. Operators Counselled & Procedures revised.W/960620 Ltr ML17292A2861996-05-24024 May 1996 LER 96-001-00:on 960425,inadvertent ESF Actuations Occurred Due to Tripping of Temporary Power Supply to IN-3.Caused by Personnel Error.Operations Restored to IN-3 Loads & Reset ESF actuations.W/960524 Ltr ML17291B0891995-10-19019 October 1995 LER 95-011-00:on 950919,failed to Comply W/Ts SR for RCIC Sys Due to Analysis Deficiency That Resulted in Inadequate Surveillance Test Procedure.Surveillance Procedure Revised to Correct deficiency.W/951019 Ltr ML17291A9021995-07-0707 July 1995 LER 95-010-00:on 950609,HPCS DG Declared Inoperable Due to Discovery That TS Test Method Incomplete.Caused by Inadequate Testing Procedure.Test Procedure for HPCS DG Reviewed & Special Test Procedures written.W/950707 Ltr ML17291A9031995-07-0707 July 1995 LER 95-009-00:on 950607,inadvertent MSIV Closure Occurred During Surveillance Test Due to Poor Communication Between Test Team.Determined That MSIV Closure Not Valid Because Closure Not Triggered by Plant conditions.W/950707 Ltr ML17291A8501995-06-0808 June 1995 LER 95-006-01:on 950405,reactor Scram Occurred During Surveillance Testing Due to Protective Sys Relay Failure. Replaced Failed Relay Before Plant Startup ML17291A8101995-05-12012 May 1995 LER 95-008-00:on 940125,TS Wording Lead to Potential TS Violation.Caused by Lack of Clarity in Ts.Submitted Improved TS for Plant to Provide Addl clarity.W/950512 Ltr ML17291A7841995-05-0505 May 1995 LER 95-007-00:on 950222,emergency Diesel Start Occurred Due to Voltage Transient on BPA Grid.Confirmation Was Received at 17:51 H That Disturbance Had Originated in BPA Grid ML17291A7801995-05-0404 May 1995 LER 95-006-00:on 950405,main Turbine Trip Occurred During Performance of Surveillance Test Due to Protective Sys Relay Failed.Replaced Failed Relay Before Plant startup.W/950504 Ltr ML17291A7851995-05-0303 May 1995 LER 95-005-00:on 950222,inoperable IRM Had Been Relied Upon to Meet TS Requirements During Reactor Startup.Caused by Lack of Neutron Source to Test Instrumentation. Sys Knowledge Gained Will Be incorporated.W/950503 Ltr ML17291A7071995-03-25025 March 1995 LER 95-004-00:on 950226,malfunction in Main Turbine DEH Control Sys Caused All Four High Pressure Turbine Governor Valves to Rapidly Close.Caused by Blown Fuse.Suspected Faulty Circuit Card replaced.W/950325 Ltr ML17291A7011995-03-20020 March 1995 LER 95-002-00:on 950218,automatic Reactor Scram Occurred. Caused by Erroneous Positioning of Control During Performance of Scheduled Periodic Functional Test.Control repositioned.W/950320 Ltr 1999-07-20
[Table view] Category:TEXT-SAFETY REPORT
MONTHYEARML17284A9001999-10-31031 October 1999 Rev 0 to COLR 99-15, WNP-2 Cycle 15,COLR GO2-99-177, LER 99-S01-00:on 990903,failure to Take Compensatory Measure within Required Time Upon Failure of Isolation Zone Microwave Unit,Was Noted.Caused by Personnel Error.Provided Refresher Training on Compensatory Measures.With1999-10-0101 October 1999 LER 99-S01-00:on 990903,failure to Take Compensatory Measure within Required Time Upon Failure of Isolation Zone Microwave Unit,Was Noted.Caused by Personnel Error.Provided Refresher Training on Compensatory Measures.With ML17284A8941999-09-30030 September 1999 Monthly Operating Rept for Sept 1999 for WNP-2.With 991012 Ltr ML17284A8801999-08-31031 August 1999 Monthly Operating Rept for Aug 1999 for WNP-2.With 990910 Ltr ML17284A8691999-07-31031 July 1999 Monthly Operating Rept for July 1999 for WNP-2.With 990813 Ltr ML17292B7421999-07-20020 July 1999 LER 99-001-00:on 990628,ESF Signal Closed All Eight MSIVs While Plant Was Shutdown.Caused by Failure of Relay RPS-RLY-K10D.Subject Relay Was Replaced & Tested on 990630. with 990720 Ltr ML17292B7271999-06-30030 June 1999 Monthly Operating Rept for June 1999 for WNP-2.With 990707 Ltr ML17292B6961999-05-31031 May 1999 Monthly Operating Repts for May 1999 for WNP-2.With 990608 Ltr ML17292B6641999-04-30030 April 1999 Monthly Operating Rept for Apr 1999 for WNP-2.With 990507 Ltr ML17292B6391999-03-31031 March 1999 Monthly Operating Rept for Mar 1999 for WNP-2.With 990413 Ltr ML17292B5871999-02-28028 February 1999 Monthly Operating Rept for Feb 1999 for WNP-2.With 990311 Ltr ML17292B5571999-01-31031 January 1999 Monthly Operating Rept for Jan 1999 for WNP-2.With 990210 Ltr ML17292B5621999-01-31031 January 1999 Rev 1 to COLR 98-14, WNP-2 Cycle 14 Colr. ML17292B5341999-01-15015 January 1999 Part 21 Rept Re Incorrect Modeling of BWR Lower Plenum Vol in Bison.Defect Applies Only to Reload Fuel Assemblies Currently in Operation at WNP-2.BISON Code Model for WNP-2 Has Been Revised to Correct Error ML17292B5331999-01-15015 January 1999 Part 21 Rept Re XL-S96 CPR Correlation for SVEA-96 Fuel. Defect Applies Only to WNP-2,during Cycles 12,13 & 14 Operation.Evaluations of Defect Performed by ABB-CE ML17292B4791998-12-31031 December 1998 Washington Public Power Supply Sys 1998 Annual Rept. with 981215 Ltr ML17292B5351998-12-31031 December 1998 Monthly Operating Rept for Dec 1998 for WNP-2.With 990112 Ltr ML17292B5741998-12-31031 December 1998 WNP-2 1998 Annual Operating Rept. with 990225 Ltr ML17284A8231998-11-30030 November 1998 Monthly Operating Rept for Nov 1998 for WNP-2.With 981207 Ltr ML17284A8081998-10-31031 October 1998 Monthly Operating Rept for Oct 1998 for WNP-2.With 981110 Ltr ML17292B4451998-10-27027 October 1998 LER 98-012-01:on 980715,failure to Comply with Requirements of TS SR 3.8.4.7 Was Noted.Caused by Inadequate Work Practices.Training Session Was Held with Personnel.With 981027 Ltr ML17284A7831998-09-30030 September 1998 Monthly Operating Rept for Sept 1998 for WNP-2.With 981007 Ltr ML17284A7491998-09-10010 September 1998 WNP-2 Inservice Insp Summary Rept for Refueling Outage RF13 Spring,1998. ML17284A7561998-09-0303 September 1998 LER 98-013-00:on 980805,ESF Actuations Were Noted Due to Deenergization of Vital Electrical Bus SM-8.Caused by Inadequate Direction in Troubleshooting Plan.Will Conduct Training for Engineering Personnel.With 980903 Ltr ML17284A7571998-09-0202 September 1998 LER 98-014-00:on 980807,completion of TS 3.8.1.F Required Shutdown Due to Inoperability of EDG-2 Was Noted.Caused by Degraded Voltage Regulator for DG-2.Replaced Voltage Regulator & Associated Scrs.With 980902 Ltr ML17284A7551998-09-0202 September 1998 LER 98-015-00:on 980808,discovered Reactor Coolant Pressure Boundary Leak During Shutdown Conditions.Caused by Leakage from Socket Weld (Fwb 63) on Elbow Connection.Failed Piping Connection Was Replaced.With 980902 Ltr ML17284A7681998-08-31031 August 1998 Monthly Operating Rept for Aug 1998 for WNP-2.With 980915 Ltr ML17284A7311998-08-17017 August 1998 LER 98-012-00:on 980716,determined That 24-month SR 3.8.4.7 Had Not Been Fulfilled within Specified Frequency.Caused by Inadequate Work Practices.License Requested & Received Enforcement Discretion Re Battery Svc test.W/980817 Ltr ML17284A7261998-07-31031 July 1998 Monthly Operating Rept for July 1998 for WNP-2.W/980810 Ltr ML17284A7121998-07-23023 July 1998 LER 98-006-01:on 980520,discovered Discrepancies in Low Voltage Bus Calculations During Review of 10CFR50,App R Calculations for High Impedance Faults.Caused by Inadequate Work Practices.Implemented Procedural Changes ML17284A6951998-07-17017 July 1998 LER 98-011-00:on 980617,ECCS Pump Room Flooding Was Noted Due to FP Sys Pipe Break.Caused by Inadequate Design of FP Sys.Detailed Review of FP Sys Design Was Conducted. W/980717 Ltr ML17284A6961998-07-15015 July 1998 LER 98-010-00:on 980615,TS Required Shutdown Due to Inoperability of TIP Sys Isolation Valve Was Noted.Caused by Improper Installation of TIP Tubing.Reattached Affected Tubing & Inspected Other TIP tubing.W/980715 Ltr ML17284A6731998-07-0101 July 1998 LER 98-009-00:on 980606,nuclear Steam Supply Shutoff Sys Group 3 & 4 Isolations During Testing Was Noted.Caused by Procedural Deficiency.Counseled Individuals Involved in preparation.W/980701 Ltr ML17284A6751998-06-30030 June 1998 Ro:On 980617,flooding of RB Northeast Stairwell with Consequential Flooding of Two ECCS Pump Rooms.Caused by Inadequate Fire Protection Sys Design.Pumped Out Water from Affected Areas to Point Below Berm Areas of Pump Rooms ML17284A6641998-06-24024 June 1998 LER 98-008-00:on 980531,inadvertent Full Scram During RPV Leak Testing in Mode 4 Was Noted.Caused by Change in Mgt Techniques.Revised Procedures to Take Into Account Addl Water Head in Pressure Sensing lines.W/980624 Ltr ML17284A6651998-06-24024 June 1998 LER 98-007-00:on 980530,inadvertent Full Scram & Division 1 ECCS Injection Was Noted.Caused by Failure to Meet Mgt Work Practice Expectation When Encountering Deficient Procedure. Incident Review Board Convened to Review event.W/980624 Ltr ML17284A6631998-06-19019 June 1998 LER 98-006-00:on 980520,discovered Discrepancies in Low Voltage Bus Calculations During Review of App R Calculations for High Impedance Fault Analysis.Caused Indeterminate. Implemented Procedural Changes Involving Operator Action ML17284A6551998-06-0404 June 1998 LER 98-005-00:on 980506,potential for Failure of RHR Sys Valve to Close on Isolation Signal Was Noted.Caused by Design Deficiency.Caution Tag Was Placed on RHR-V-40 Control Switch to Inform Plant Operators of limitation.W/980604 Ltr ML17284A6421998-06-0101 June 1998 LER 98-004-00:on 980502,determined That Primary Containment Penetration Overcurrent Protection Does Not Meet Reg Guide 1.63 Requirements.Caused by Inadequate Design Changes. Installed Addl Fuse in RHR-MO-9 circuit.W/980601 Ltr ML17284A6491998-05-31031 May 1998 Rev 0 to COLR 98-14, WNP-2,Cycle 14 Colr. ML17292B4031998-05-31031 May 1998 Monthly Operating Rept for May 1998 for WNP-2.W/980608 Ltr ML17292B3921998-04-30030 April 1998 Monthly Operating Rept for Apr 1998 for WNP-2.W/980513 Ltr ML17292B3291998-04-0909 April 1998 LER 98-003-00:on 980311,WNP-2 Experienced SCRAM Signal as Result of Low Rpv.Caused by Less than post-SCRAM Operational Strategy for Resetting SCRAM Signal in Conditions.Changes in post-SCRAM Operational Strategy implemented.W/980409 Ltr ML17292B3281998-04-0909 April 1998 LER 98-002-00:on 980311,reactor Scram & Plant Transient Occurred,Due to Failed Closed Main Steam Isolation Valve. Caused by Loss of Pneumatic Actuating Supply Pressure. Problem Evaluation Request Written for Failure of MS-V-22D ML17292B3371998-03-31031 March 1998 Monthly Operating Rept for Mar 1998 for WNP-2.W/980409 Ltr ML17292B2641998-03-0404 March 1998 Performance Self Assessment,WNP-2. ML17292B2661998-03-0404 March 1998 LER 98-001-00:on 980203,automatic Start of HPCS EDG Was Noted.Caused by Operator Error.Operations Crew Stabilized Plant at Approximately 75% Reactor Power & Investigation of Event Was initiated.W/980304 Ltr ML17292B2911998-02-28028 February 1998 Monthly Operating Rept for Feb 1998 for WNP-2.W/980313 Ltr ML17284A7971998-02-17017 February 1998 Rev 28 to Operational QA Program Description, WPPSS-QA-004.With Proposed Rev 29 ML17292B3591998-02-12012 February 1998 WNP-2 Cycle 14 Reload Design Rept. 1999-09-30
[Table view] |
Text
ACCELERATED DESI'RIBUYION DEMONSTRATION SYSTEM REGULATORY INFORMATION DISTRIBUTION SYSTEM (RIDS)
ACCESSION NBR:8803230003 DOC.DATE: 88/03/14 NOTARIZED: NO DOCKET FACIL:50-397 WPPSS Nuclear Project, Unit 2, Washington Public Powe 05000397 AUTH. NAME AUTHOR AFFILIATION DAVISON,W.S. Washington Public Power Supply System POWERS,C.M. Washington Public Power Supply System RECIP.NAME RECIPIENT AFFILIATION
SUBJECT:
LER 88-006-00:on 880213,low reactor pressure vessel level reactor protective sys actuation.
W/8 ltr.
0 TITLE: 50.73 Licensee Event Report (LER), Incident Rpt,Qetc.
DISTRIBUTION CODE: IE22D COPIES RECEIVED:LTR ( ENCL SIZE:
NOTES 8 RECIPIENT ID PD5 LA CODE/NAME COPIES LTTR ENCL RECIPIENT ID CODE/NAME COPIES LTTR ENCL
/
1 1 PD5 PD 1 1 A SAMWORTH,R 1 1 INTERNAL: ACRS MICHELSON 1 1 ACRS MOELLER 2 2 AEOD/DOA 1 1 AEOD/DS P/NAS 1 1 AEOD/DSP/ROAB 2 2 AEOD/DSP/TPAB 1 1 ARM/DCTS/DAB 1 1 DEDRO 1 1 NRR/DEST/ADS7E4 1 0 NRR/DEST/CEB8H7 1 1 NRR/DEST/ESB 8D 1 1 NRR/DEST/XCSB7A 1 1 NRR/DEST/MEB9H3 1 1 NRR/DEST/MTB 9H 1 1 NRR/DEST/PSB8D1 1 1 NRR/DEST/RSB 8E 1 1 NRR/DEST/SGB 8D 1 1 NRR/DLPQ/HFB10D 1 1 NRR/DLPQ/QAB10A 1 1 NRR/DOEA/EAB11E 1 1 NRR/DREP/RAB10A 1 . 1 NRR/DREP/RPB10A 2 2 NRR DR SIB9Al 1 1 NRR/PMAS/ILRB12 1 1 E L 02 1 1 RES TELFORD,J 1 1 RES/DE/EIB 1 1 RES/DRPS DIR 1 1 RGN5 FILE 01 1 1 EXTERNAL: EG&G GROH, M 4 4 FORD BLDG HOY,A 1 1 H ST LOBBY WARD 1 1 LPDR 1 1 NRC PDR 1 1 NSXC HARRIS,J 1 1 NSIC MAYS,G 1 1 S
j A
TOTAL NUMBER OF COPXES REQUIRED: LTTR 45 ENCL 44
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- N I NRC Form 388 U.S. NUCLEAR AEGULATOAYCOMMISSION (843)
APPROVED OMB NO. 31500104 LICENSEE EVENT REPORT (LER) EXPIAES: 8/31/BS FACILITYNAME (Il DOCKFT NUMBER (2) PAGE I3)
Washington Nuclear Plant - Unit 2 0 5 0 0 0 9 7 ] pF 0 "t.oA'Reactor Pressure Vessel Level Reactor Protective System Actuation EVENT DATE (5) LER NUMBER IS) REPOAT DATE (7) OTHEA FACILITIES INVOLVED (8)
MONTH OAY YEAR YEAR 'SEC VENT I AL &8 ttEVtetGN I'ACILITYNAMES DOCKET NUMBER(SI Na NUMBER OrX NVMSSII MONTH OAY YEAR 0 5 0 0 0 8 8 8 0 0 0 0 0 0 5 0 0 0 OPERATING THIS REPORT IS SUBMITTED PURSUANT T0 THE REDUIAEMENTB DF 10 cFR gt fcercb one or metr of ter follorffnp) l11 MODE (8) 3 20.402(It) 20.405(c) 50.73(e) (1) Dr) 73.71Dt)
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LEYEL 0 0 20A05(s) l1) (El 50M(c)(2) 50.73(a)(21(r8) OTHER ISpeclfy In Abstract below entf In Trit, HAC Form 20.405(al(1)(N) 50.73(el l2) (I) 50.73(el(2)(r(II) IA) 3$ 6AJ 10A05(e) H l(lr) 50.73(s l(2) (8 I 50.73(sl(2)(rl8) (Bl 20.405(e) (1)(r) 50.73(s)(2)(IIII 50,73(s) 12)(x I LICENSEE CON'TACT FOR THIS LER (12I NAME TELEPHONE NUMB'ER AREA CODE W.S. Davison, Compliance Engineer 50 3 7- 501 COMPLETE ONE LINE FOA EACH COMPONENT FAILURE DESCAISEO IN THIS REPOAT (13)
E t 2726 tpt' rI:gP CAUSE SYSTEM COMPONENT MANUFAC EPORTABLE MANUFAC. EPORTABLE TURER TO NPADS CAUSE SYSTEM COMPONENT TURER TO NPRDS L B 4 0 NO SUPPLEMENTAL REPOAT EXPECTED l14) MONTH DAY YEAR EXPECTED SUBMISSION DATE US)
YES flfyrt, romplrte EXPECTED $ (I84IISSIOIY OA TEI NO ABSl'AACT ILlmlt to 1400 tptcet, I.r., rpptoxlmetety flftrrn tlnplerprrr typrwrlttrn linn) (18)
Following a manual scram initiated due to high reactor coolant conductivity problems on February 13, 1988, a series of Reactor Pressure Vessel (RPV) level transients resulted in an actual low RPV Level Reactor Protective System actuation. The low level condition was initiated by loss of the only running Reactor Feedwater (RFW) Pump and was directly caused by opening the Startup Flow Control Valve while RFW System pressure was 250 psig lower than RPV pressure. This resulted in establishing a previously unrecognized diversion flowpath of reactor coolant from the Reactor Water Cleanup System backward through the Startup Flow Control Valve and to the IIain Condenser Hotwell via the Long Cycle Cleanup Flow Control Valve. The root cause of the event was determined to be procedural inadequacy. Plant procedures did not give adequate guidance to the operator to ensure that the RFW System would be operated correctly during situations in which RPV pressure is higher than Reactor Feedwater System pressure.
Corrective Actions consisted of:
IIodifying the RFW Speed Control System to eliminate undesirable speed ramp characteristics, modification of operating procedures to add suficient guidance for RFW System operations, evaluation of the need for Simulator Training, required reading of this LER, evaluation of RPV level management policy and repair of the condensate pump minimutt flow control valve. During the event all manual and automatic safety system responses occurred as designed. This event posed no threat to the safety of Plant personnel or the public.
i' 8803230003 8803i4 PDR ADOCK 05000397 S DCD I V
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-0 NRC FAIIII SSSA U.S. NUCLEAR REOULATORY COMMISSION (0431 LICENSEE EVENT REPORT ILER) TEXT CONTINUATION APPROVEO OMS NO. 3(50M104 EXPIRES: 8/31/88 PACILI'TY NAME (ll COCKET NUMSER (SI LER NUMSER (SI PACE (31 SI<~ SSCVSNTIAL M? IIS V IS IO N NVMSSII NVMSSII Washington Nuclear Plant TEXT ////IIS/S SFSCS /S nPCkeC Plant Conditions VSP ~ - Unit A/RC fe/III3//SAT/ ( Ill 2 0 s 0 0 0 3 9 006 0 0 2oF 0
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A P=T a) Power Leve I - OX
~ I' b) Plant Hode - 3 (Hot Shutdown)
Event Descri tion On February 13, 1988, at 1655 hours0.0192 days <br />0.46 hours <br />0.00274 weeks <br />6.297275e-4 months <br />, the reactor was r(Ianually scrammed from 35 percent reactor power due to rapidly increasing coolant conductivity. An automatic Reactor Protective System (RPS) actuation occurred 21 minutes later due to an actual low Reacto Pressure Vessel (RPV) water level condition following transients initiated by the operating Reactor Feed Pump speed controller during the process of plant shutdown.
Prior to the time of the Low RPV Water Level RPS actuation, the plant was in the Hot Shutdown (Plant Hode 3) condition with RPV level and pressure being maintained using Reactor Feed Pump IA (RFW-P-IA) and the Hain Turbine Bypass Valves (BPV),
The sequence of events occurred as follows, with time zero at 1655 hours, 50 seconds:
o Time 0 minutes, 0 seconds - About 2 minutes after receiving the report from plant c emsstry that hotwe I conductivity was very high and the sample was cloudy, the reactor was manually scrammed at approximately 35 percent power. The rapid increase in reactor coolant conductivity to I micro-mho per centimeter was later determined to be due to ruptured tubes in the condenser.
o Time 0 minutes, 23 seconds - Reactor Feed Pump IB (RFW-P-IB) was shut down as part of the reactor scram recovery action, leaving RFW-P-IA in service.
o Time 2 minutes, 9 seconds - RFW-P-IA automatic turbine speed control circuit decreased to zero demand initiating an automatic shift to speed lockup. The speed lockup feature is designed to hold the feed turbine RPH constant at its last value. Instead, pump speed began to increase rapidly.
o Time 2 minutes, 18 seconds - RFW-P-IA turbine speed reached 3500 RPH (about 60 percent pumping capacity). At this point, RPV level was increasing at a rate o about 50 inches per minute.
o Time 2 minutes, 40 seconds - RFW-P-IA was tripped by the reactor operator as RPV leve increased through +51 inches. An automatic trip would have occurred at +54.5 inches.
Time 3 minutes, 50 seconds - The RPV level transient crested at +62 inches. At this point, t e decision was made to use the RCIC system as the preferred source for maintaining RPV inventory and cooling down, thus minimizing the use of the hig conductivity water in the condenser hot well as a source of makeup.
Time 5 minutes, 20 seconds - RPV level started to decrease at about 3 inches per minute. T ss ss considered normal level drop immediately after a plant shutdown.
NRC POIIM JSSA 10431 SU.S.OPO.(0884 524.538/455
e US. NUCLEAR REOULATORY COMMISSION NRC Sons 888A (84L))
LICENSEE EVENT REPORT ILER) TEXT CONTINUATION APPROVED OMS NO. 2)50WIOA EXPIRES: 8/SI/8$
SACII.ITY NAME Ill DOCKET NUMSER (21 LER NUMSER (8) PACE (2)
YEAR SEQUENTIAL REVISION NVM TS ~rg NUM CS Washington Nuclear Plant .- Unit 2 o s o o o 0 6 0 0 30F 0 TEXT //I//s/To /Poco /I nywwL ooo //I/o/N//VRC FomI 2/)/)AY/ (17) o Time 6 minutes 15 seconds - The Long Cycle Cleanup Flow Control Valve RFW-FCV-15 was opened to provide a recirculation path from the condensate system filter demineralizers back to the condenser hotwell in an effort to minimize the conductivity increase and to provide condensate pump minimum f'low. Use of this valve resulted in a 70 psig lower than normal feedwater system pressure. Normally, COND-LCV-1 1 would have been used to supply minimum condensate flow. At this point however, COND-LCV-11 was in manual and closed.
o Time 15 minutes, 0 seconds (approximate) - Because the RCIC system suction valve t the Condensate Storage Tank's (CSTs) was closed; deenergized and caution tagged, the only RCIC suction source was the Pressure Suppression Pool. Since depressurization using RCIC would mean discharging suppression pool water to CSTs, the decision was made to realign the RCIC suction to the Condensate Storage Tanks .
prior to starting the RCIC pump.
o Time 15 minutes, 30 seconas (approximate) - The decision was made to start using the condenser hotwel1 as the RPV water source unti 1 the RCIC suction could be realigned.
.o Time 15 minutes, 54 seconds - Startup F'low Control Valve RFW-V-10A was manually opened in preparetion for using the condensate booster pumps to supply feedwater t the RPV. when pressure decreased to within the capability of the pumps. RPV level had dropped into thb normal leveI control range of +35 inches at this point. RPV level immediately began to decrease at approximately 20 inches per minute. (See Figure 1 for Condensate and Reactor Feedwater System lineup).
Time 16 minutes, 9 seconds - The RPV Low Level alarm was received as level decreased through +3 .5 inches.
Time 16 minutes, 55 seconds - The DEH panel operator initiated a 200 psig per minute depressurization ramp with a pressure setpoint of 600 psig. Since the
~
existing setpoint for the DEH .pressure controller was 940 psig and reactor pressure was 840 psig, no BPV movement occurred.
~
o Time 17 minutes, 45 seconds - When RPV level decreased to +18 inches, the Reactor Core Isolation Cooling RCIC) System was started to provide a source of high pressure feedwater to the RPV by injection via the RCIC head spray nozzle.
o Time 17 minutes 55 seconds - The DEH pressure setpoint decrease ramp reached 840 psig, matching reactor pressure. As the setpoint decreased below reactor pressure, the Hain Turbine Bypass Valves automatically positioned to 50 percent open, causing a rapid increase in depressurization rate, which resulted in a rapid RPV level swell transient.
NRC PO/IM $88* ~ U.S.QPO: I OSBBI28.588/855 (841)
NRC Fona 388A U> NUCLEAR REOULATORY COMMISSION (9831 LICENSEE T REPORT (LER) TEXT CONTINUATI APPROVED OM8 NO. 3150M104 EXPIRES: 8/31/88 PACILITY NAME (11 DOCKET NUMSER (21 LER NUMEER (81 PACE (3)
VEAR 3 3 O V 8 N 'T I A L RSVOIQN NVMPSR NVMSSR Washington Nuclear Plant TEXT I/I'uuuu Auutu /u turn@. uuu ~ - Unit
/VRC fcn// 3////43/ (17(
2 0 5 0 0 0 OF o Time 18 minutes, 10 seconds to 18 minutes, 27 seconds - RCIC ingection ana the eve swell transient combined to increase RPY level to the RCIC High RPV Level auto trip setpoint of +54.5 inches, causing an automatic shutdown of the RCIC System. The level increase transient crested at +57.5 inches. RPV level then started to decrease rapidly as a result of BPY osci llations caused by the initial pressure control system reaction to regulate the depressurization rate.
o Time 20 minutes 45 seconds - As RPV level decreased through +19 inches, the RCIC System was restarted to supply high pressure water to the RPV.
o Time 21 minutes 0 seconds - The DEH panel operator changed the depressurization rate to 25 psig per minute as RPV pressure reached approximately 625 psig. RPS automatically actuated when RPV Level reached the +13 inch Low RPV Level RPS actuation setpoint.
o Time 21 minutes, 0 seconds to 21 minutes, 20 seconds - As a result of the pressure ramp rate change, the BPYs repositioned in the Close direction from 50 percent Open to 15 percent Open. As the BPVs closed down, the decrease in the depressurization rate caused RPV level to shrink at a rate greater than the RCIC System could increase RPV level. RPV level started to decrease rapidly.
o Time 21 minutes 30 seconds - The RPV level decrease leveled off at 0 inches as the leve shrink transient dampened.
o Time 21 minutes, 40 seconds - The DEH panel operator changed the pressure setpoint to 550 psig at a rate of 200 psig per minute. This caused the BPYs to begin to open rapidly. RPV level again started to increase rapidly due to the combined effects of level swell and RCIC injection.
o Time 21 minutes 45 seconds - The BPVs reached 100 percent Open position.
o Time 21 minutes 50 seconds - RPV level increased to +54.5 inches and caused the RCIC System to automatically shut down due to again reaching the RCIC High RPV Level automatic trip setpoint.
0 Time 21 minutes, 55 seconds - As RPV pressure reached 550 psig, the DEH pressure control system responded by rapidly closing the BPVs. This initiated a level shrink transient which caused RPV level to decrease rapidly.
o Time 22 minutes 10 seconds - The RCIC System was restarted to supply high pressure water to the RPV. RPV pressure dropped below the discharge pressure of the condensate booster pump, allowing the RFW system to begin to supply water to the RPV.
o Time 24 minutes, 10 seconds - The RPV level decrease transient was arrested at
-4 inches due to the combination of RCIC injection and condensate booster pump supp ly.
o Time 24 minutes, 30 seconds - RpV level increased to above +13 inches, the RPS Low ation set oint.
NRC PORM 3SSA u U.S.GPO; I 9884424 838IA88 0431
.0 NRC Perm ESSA US. NUCLEAR REOULATORY COMMISSION (SSS)
LICENSEE E T REPORT ILER) TEXT CONTINUATI APPROVED OMS NO. S(50&10(
EXPIRES: d/31/SS SAC/SIST NAME Ill DOCKET NUMSER (21 LER NUMSER (Sl PACE (SI Y EAR '53 SSQVSNTIAS IISVISION NI/Meee NUM SN Washington Nuclear Plant - Unit 2 o s o o o 006 00 50F TEXT /// more ooeoe /o r/Orwled, Iree//l/rme//VRC form 2//SA'o/ ((TI o Time 25 minutes 20 seconds - RPV level reached the normal operating level of
+36 inches. Event end.
Further Evaluation and Corrective Action Further Evaluation This incident is being reported as an event which resulted in the automatic actuation of an Engineered Safety Feature per the requirements of 10CFR50. I3(a) (2) (iv) .
- 2. The reportable occurrence was an automatic RPS actuation due to an actual low RPV level at 1716 hours0.0199 days <br />0.477 hours <br />0.00284 weeks <br />6.52938e-4 months <br /> on February 13, 1988. The low RPV level event was a result of transients initiated during the follow-up action for the manual scram initiated at 1655 hours.
- 3. The irrnediate cause of the low RPV level RPS actuation was determined to be the opening of the Startup Flow Control Valve RFW-FCV-10A while RPY pressure was 250 psig greater than Reactor Feedwater System pressure. Because the Long Cycle Cleanup Va'lve RFW-FCV-15 had been previously opened to the condenser hotwell, opening RFW-FCV-IOA resulted in a rapid diversion of water inventory from the RPV through the RWCU System backwards through RFW-FCV-IOA to the condenser via RFW-FCV-15 . The cause of this loss was unknown during the event.
The root cause of the low RPV level RPS actuation was determined to be procedura'I deficiency. The Reactor Scram Recovery Procedure did not contain adequate information to properly direct operation of the Reactor Feedwater System during conditions in which RPV pressure is greater than Reactor Feedwater System pressure. This allowed the Startup Flow Contro'l Valve to be opened to inadvertent'ly establish an unrecognized diversion path of reactor coolant from the RPV via RWCU to the condenser hotwell. This diversion flow path was the primary cause for RPV level dropping from +35 inches to the +13 inch RPS actuation setpoint
- 5. The following were evaluated as contributing factors to the event:
o The condensate pump recirculation control valve COND-LCV-11 was inoperable due to high piping vibration experienced during previous use. This valve controls the prefered flowpath of condensate through the condensate filter demineralizers and back to the condenser hotwell when clean up of the feedwater system is desired. Inability to use this cleanup flow path necessitated the use of RFW-FCV-I5, the Long Cycle Cleanup Flow Control Valve. During the event, the use of RFW-FCY-15 provided an unexpected diversion flowpath of water from the RPV via the RWCU System to the condenser hotwell. Normally RWCU flow would return to the RPV via the feedwater in'let piping o During a previous plant refueling and maintenance outage, a design modification to the Reactor Feedwater Pump speed control circuitry was installed to maintain RPV level during a loss of feedwater drive turbine
'ontrol signal.
NRC SOIIM S4SA
- U.S.OPO:ISSIPDS24 SSS/ASS (0421
NRC POIhI 358A UA. NUCLEAR REOULATORY COMMISSION
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The design added a speed lockup feature which would lock in the speed of the Reactor Feedwater Pump during loss of power//'Ioss of signal conditions. This design, however, did not accomplish that objective. As a combined result of calibration inaccuracies, minor system oscillations and insufficient governor control deadband, the governor unit functionea to either increase or decrease turbine speed as a result of minor differences between governor input signal and the lockup signal developed by the feedwater pump control tachometer.
Instead of a speed lock-up for the pump, the circuit functioned during the event to insert a speed increase ramp resulting in a 1700 rpm increase in approximately 9 seconds. This pump speed increase resulted in overfeeding of the RPV and manual trip of the Reactor Feed Pump. The loss of the Reactor Feed Pump resulted in the RPV pressure being greater than Reactor Feedwater System pressure by approximately 250 psig. This unusual pressure differential established the driving head required for flow of RPV water inventory from RWCU through the Startup Flow Control Valve in the reverse direction and to the condenser hotwell via RFW-FCV-15.
o The operation of the BPV's during the event was not coordinated well with the attempt to feed the RPY using the RCIC system. The rapid RPV level increases resulting in the automatic shutdown of the RCIC System were brought about by the effort to expeditiously depressurize the RPV to less than 600 psig in order to use the condensate booster pumps to supply feedwater to the RPY. The depressurization rate initially used and subsequent changes to the rate resulted in rapid BPY movement which caused rapid RPV level shrink and swell =-
transients. The inability to continuously feed the RPV using the RCIC System contributed significantly to the existing level inventory control problem.
- 6. During the initial high RPV level transient resulting in a level of +62 inches at Time 3 minutes, 50 seconds, the ink pen for the Narrow Range RPV Level Recorder (RFW-LR-608) located on the Reactor Control Console vertical 'section, stuck at the high 'limit and stayed there during the remainder of the event.
- 7. All automatic actions which should have been initiated at RPV Level 3 (+13 inches) did occur as designed. The only actual operation of components that occurred were logic relay actuation and repositioning of valves for the reactor scram funtion of the Control Rod Drive (CRD) System. No control rods were actually repositioned since they had been previously inserted fully into the core. Other automatic functions which occurred are:
o Reactor Recirculation Pumps received a signal to automatically shift to slow speed. (15 hertz) operation. This shift did not occur because both pumps were being operated at 15 hertz at the time of the event.
o Nuclear Steam Supply Shutoff System (NS4) Groups 5 and 6 received an isolation signal. No valves or components changed status because they were in the isolation position at the time of the event.
o An Automatic Depressul ization System (ADS) Low RPV Level 3 Confirmation Signal was generated. This is one of two control logic RPV level functions requirea for the ADS initiation of seven Safety Relief Valves.
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Corrective Action
- 1. The Reactor Feedwater Pump Speed Control System has been modified to eliminate the undesirable speed ramp characteristic.
- 2. Narrow Range RPV Level Recorder RFW-LR-608 has been overhau'led, tested and reinstalled in the Reactor Control Console. This recorder is a IIodeI No. 732, manufactured by Bailey Instrument Company, GE tlPL Number C34-R608. WNP-2 is currently pursuing replacement of this type of recorder with a more reliable type.
- 3. Operating procedures have been modified to include additional information concerning control of RPV level during shutdown conditions with RPV pressure greater than feedwater system pressure.
- 4. A study will be conducted to evaluate the need to add this scenario to the Simulator Training Program.
- 5. This LER will be required reading for all licensed operators and will be added to the subject matter list for requalification training.
- 6. An evaluation will be conducted by the Operations Manager to determine the requirement for increased policy guidance concerning methods for improved early management of RPV 'level control options following a reactor scram.
- 7. The condensate pump minimum flow valve COND-LCV-11 will be modified during the upcomming 1988 refueling and maintenance outage to rectify the previously experienced vibration problems.
Safet Si nificance All manual and automatic safety system responses occurred as designed. The Reactor Protective System functioned correctly to respond to the manually initiated reactor scram and to cause an automatic actuation in response to an actual reactor vessel Iow leve'l (Level 3) condition. The faulty RPV narrow range level recorder reading was compensated for by valid readings on the vertical section of the reactor control console from three narrow range RPV level indicators. With the reactor shut down, the significant safety concern is potential uncovering of the fuel. The top of active fuel is located at -161 inches vessel level. Since the level transient was terminated at
-4 inches, more than adequate vessel water inventory remained to assure fuel coverage.
This event posed no threat to the safety of Plant personnel or the public.
Similar Events LER 88-001 reported a previous low RPV level RPS actuation which occurred shortly after a plant shutdown.
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WASHINGTON PUBLIC POWER SUPPLY SYSTEM P.O. Box 968 ~ 3000 George lVashington 11'ay ~
Richland, 1Vashington 99352 Docket No. 50-397 Narch 14, 1988 Document Control~esk U.S. Nuclear ReguTatory Commission Washington, D.C. 20555
Subject:
NUCLEAR PLANT NO. 2 LICENSEE EYENT REPORT HO. 88-06
Dear Sir:
Transmitted herewith is Licensee Event Report Ho. 88-06 for the WHP-2 Plant.
This report is submitted in response to the report requirements of 10CFR50.73 and discusses the items of reportabi lity, corrective action taken, and action taken to preclude recurrence.
Very truly yours, C.tl. Powers (tl/D 927tl)
WHP-2 Plant Nanager CNP:sm
Enclosure:
Licensee Event Report No. 88-06 cc: Nr. John B. Nartin, NRC - Region Y tlr. C.J. Bosted, NRC Site (tl/D 901A)
INPO Records Center - Atlanta, GA tls. Dottie Sherman, AHI Nr. D.L. Williams, BPA (tl/D 399)
P 703 05'8 $ /8