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Category:LICENSEE EVENT REPORT (SEE ALSO AO
MONTHYEARML17292B7421999-07-20020 July 1999 LER 99-001-00:on 990628,ESF Signal Closed All Eight MSIVs While Plant Was Shutdown.Caused by Failure of Relay RPS-RLY-K10D.Subject Relay Was Replaced & Tested on 990630. with 990720 Ltr ML17292B4451998-10-27027 October 1998 LER 98-012-01:on 980715,failure to Comply with Requirements of TS SR 3.8.4.7 Was Noted.Caused by Inadequate Work Practices.Training Session Was Held with Personnel.With 981027 Ltr ML17284A7561998-09-0303 September 1998 LER 98-013-00:on 980805,ESF Actuations Were Noted Due to Deenergization of Vital Electrical Bus SM-8.Caused by Inadequate Direction in Troubleshooting Plan.Will Conduct Training for Engineering Personnel.With 980903 Ltr ML17284A7571998-09-0202 September 1998 LER 98-014-00:on 980807,completion of TS 3.8.1.F Required Shutdown Due to Inoperability of EDG-2 Was Noted.Caused by Degraded Voltage Regulator for DG-2.Replaced Voltage Regulator & Associated Scrs.With 980902 Ltr ML17284A7551998-09-0202 September 1998 LER 98-015-00:on 980808,discovered Reactor Coolant Pressure Boundary Leak During Shutdown Conditions.Caused by Leakage from Socket Weld (Fwb 63) on Elbow Connection.Failed Piping Connection Was Replaced.With 980902 Ltr ML17284A7311998-08-17017 August 1998 LER 98-012-00:on 980716,determined That 24-month SR 3.8.4.7 Had Not Been Fulfilled within Specified Frequency.Caused by Inadequate Work Practices.License Requested & Received Enforcement Discretion Re Battery Svc test.W/980817 Ltr ML17284A7121998-07-23023 July 1998 LER 98-006-01:on 980520,discovered Discrepancies in Low Voltage Bus Calculations During Review of 10CFR50,App R Calculations for High Impedance Faults.Caused by Inadequate Work Practices.Implemented Procedural Changes ML17284A6951998-07-17017 July 1998 LER 98-011-00:on 980617,ECCS Pump Room Flooding Was Noted Due to FP Sys Pipe Break.Caused by Inadequate Design of FP Sys.Detailed Review of FP Sys Design Was Conducted. W/980717 Ltr ML17284A6961998-07-15015 July 1998 LER 98-010-00:on 980615,TS Required Shutdown Due to Inoperability of TIP Sys Isolation Valve Was Noted.Caused by Improper Installation of TIP Tubing.Reattached Affected Tubing & Inspected Other TIP tubing.W/980715 Ltr ML17284A6731998-07-0101 July 1998 LER 98-009-00:on 980606,nuclear Steam Supply Shutoff Sys Group 3 & 4 Isolations During Testing Was Noted.Caused by Procedural Deficiency.Counseled Individuals Involved in preparation.W/980701 Ltr ML17284A6651998-06-24024 June 1998 LER 98-007-00:on 980530,inadvertent Full Scram & Division 1 ECCS Injection Was Noted.Caused by Failure to Meet Mgt Work Practice Expectation When Encountering Deficient Procedure. Incident Review Board Convened to Review event.W/980624 Ltr ML17284A6641998-06-24024 June 1998 LER 98-008-00:on 980531,inadvertent Full Scram During RPV Leak Testing in Mode 4 Was Noted.Caused by Change in Mgt Techniques.Revised Procedures to Take Into Account Addl Water Head in Pressure Sensing lines.W/980624 Ltr ML17284A6631998-06-19019 June 1998 LER 98-006-00:on 980520,discovered Discrepancies in Low Voltage Bus Calculations During Review of App R Calculations for High Impedance Fault Analysis.Caused Indeterminate. Implemented Procedural Changes Involving Operator Action ML17284A6551998-06-0404 June 1998 LER 98-005-00:on 980506,potential for Failure of RHR Sys Valve to Close on Isolation Signal Was Noted.Caused by Design Deficiency.Caution Tag Was Placed on RHR-V-40 Control Switch to Inform Plant Operators of limitation.W/980604 Ltr ML17284A6421998-06-0101 June 1998 LER 98-004-00:on 980502,determined That Primary Containment Penetration Overcurrent Protection Does Not Meet Reg Guide 1.63 Requirements.Caused by Inadequate Design Changes. Installed Addl Fuse in RHR-MO-9 circuit.W/980601 Ltr ML17292B3281998-04-0909 April 1998 LER 98-002-00:on 980311,reactor Scram & Plant Transient Occurred,Due to Failed Closed Main Steam Isolation Valve. Caused by Loss of Pneumatic Actuating Supply Pressure. Problem Evaluation Request Written for Failure of MS-V-22D ML17292B3291998-04-0909 April 1998 LER 98-003-00:on 980311,WNP-2 Experienced SCRAM Signal as Result of Low Rpv.Caused by Less than post-SCRAM Operational Strategy for Resetting SCRAM Signal in Conditions.Changes in post-SCRAM Operational Strategy implemented.W/980409 Ltr ML17292B2661998-03-0404 March 1998 LER 98-001-00:on 980203,automatic Start of HPCS EDG Was Noted.Caused by Operator Error.Operations Crew Stabilized Plant at Approximately 75% Reactor Power & Investigation of Event Was initiated.W/980304 Ltr ML17292B1111997-11-10010 November 1997 LER 97-011-00:on 971010,HPCS Battery Charger Failed.Caused by Failure of a Phase Firing Control Circuit Board Due to Aging During 7 Yrs of Use.Hpcs Sys Was Immediately Declared inoperable.W/971110 Ltr ML17292B1151997-11-0707 November 1997 LER 97-010-00:on 970906,discovered That TS SR 3.4.5.1 for Identified Portion of RCS Total Leakage Would Not Be Able to Perform within Time Limits of SR 3.0.2.Caused by Inadequate Methods.Method of Meeting SR 3.4.5.1 Established ML17292B0641997-09-24024 September 1997 LER 97-004-01:on 970327,plant Operators Manually Scrammed Reactor as Required by TS Due to Indication of Entry Into Region a of power-to-flow Map.Caused by Inadequate Attention to Detail.Established Event Evaluation teams.W/970924 Ltr ML17292B0241997-08-18018 August 1997 LER 97-009-00:on 970717,discovered Error in Recently Performed Inservice Testing procedure,OSP-TIP/IST-R701. Caused by Procedure Inadequacy.Plant Procedure OSP/TIP/IST-R701 Will Be changed.W/970818 Ltr ML17292B0291997-08-15015 August 1997 LER 97-008-00:on 970716,wire Seal Used to Lock Containment Instrument Air Pressure Control valve,CIA-PCV-2B,found Not Intact.Cause of Misadjustment of CIA-PCV-2B Unknown.Event Will Be Communicated to Plant employees.W/970815 Ltr ML17292B0201997-08-15015 August 1997 LER 97-S01-00:on 970718,failure to Take Compensatory Measure for Inoperative Microwave Security Zone Occurred. Caused by Personnel Error.Training Will Be Conducted W/ Appropriate Members of Security force.W/970815 Ltr ML17292A9481997-07-23023 July 1997 LER 97-007-00:on 970611,voluntary Rept of Automatic Start of DG-1 & DG-2 Was Experienced.Caused by Undervoltage Condition on Electrical Busses SM-7 & SM-8.Circulating Water Pump CW-P-1C Control Switch Placed in pull-to-lock.W/970723 Ltr ML17292A9201997-06-26026 June 1997 LER 97-006-00:on 970527,non-performance of Surveillance Requirement 3.6.1.3.2 for Blind Fanges,Was Noted.Caused Because Misunderstanding of Intent of Specs.Added Five Structural Assemblies for SP.W/970626 Ltr ML17292A8331997-04-28028 April 1997 LER 97-004-00:on 970327,plant Operators Manually Scrammed Reactor as Required by TS Due to Entry Into Region a of power-to-flow Map Following Planned Trip of Single Mfp. Event Evaluation teams,established.W/970428 Ltr ML17292A8311997-04-28028 April 1997 LER 97-005-00:on 970327,valid Reactor Scram Signal Received Due to Low Water Level Condition During Preparations for SRV Testing.Caused by Risks & Consequences of Decisions Not Completely Identified.Restored Water level.W/970428 Ltr ML17292A8251997-04-21021 April 1997 LER 97-003-00:on 970320,notification of Noncompliance W/Ts as TS SRs for Response Time Testing Were Not Being Met for Specified Instrumentation in Rps,Pcis & Eccs.Requested Enforcement Discretion for One Time exemption.W/970421 Ltr ML17292A7431997-03-20020 March 1997 LER 97-002-00:on 970218,determined That Rod Block Monitor (RBM) Calibr Values Were Not Set IAW Tech Specs.Caused by Calibr Procedures Inadequacies.Revised & re-performed RBM Channel Calibr procedures.W/970330 Ltr ML17292A7401997-03-13013 March 1997 LER 97-001-00:on 970211,reactor Water Cleanup Sys Blowdown Flow Isolation Setpoint Was Slightly Above TS Allowable Valve Occurred Due to Calculation Error.Lds Fss LD-FS-15 LD-FS-16 Were Declared inoperable.W/970313 Ltr ML17292A6641997-01-22022 January 1997 LER 96-009-00:on 961220,miscalculation of Instantaneous Overcurrent Relay Settings Resulted in Inoperability of safety-related Equipment.Caused by Utilization of Inappropriate Design.Testing Was completed.W/970122 Ltr ML17292A6461997-01-0606 January 1997 LER 96-008-00:on 961205,failure to Comply with TS Action Requirement for Emergency Core Cooling Sys Actuation Instrumentation Occurred Due to Unidentified Inoperability Condition.Pmr initiated.W/970106 Ltr ML17292A6371996-12-19019 December 1996 LER 96-007-00:on 961122,electrical Breakers Were Not Seismically Qualified in Test/Disconnect Position.Circuit Breaker Mfg Did Not Consider Raced Out Breaker Position During Testing.Relocated Circuit breakers.W/961217 Ltr ML17292A4121996-08-0808 August 1996 LER 96-006-00:on 960709,average Power Range Monitor Rod Block Downscale Surveillance Not Performed Prior to Entry Into Mode 1.Caused by long-standing Misinterpretation of Requirements of Tss.Procedures revised.W/960808 Ltr ML17292A3801996-07-24024 July 1996 LER 96-004-00:on 960624,plant Was Manually Scrammed by Control Room Personnel Due to Reactor Water Level Transient Experienced During Testing of Digital Feedwater Sys.Caused by Programming Error.Sys Was corrected.W/960724 Ltr ML17292A3771996-07-24024 July 1996 LER 96-005-00:on 960624,determined Missed Surveillance Test Re Channel Check of Average Power Range Monitor.Caused by Inadequate Procedures.Revised Surveillance Procedure Re When APRM Checks Must Be performed.W/960724 Ltr ML17292A3641996-07-12012 July 1996 LER 96-003-00:on 960615,required Surveillance Test Not Performed When Required by TS 3.4.1.3.Caused by Inadequate Procedures.Implementing Surveillance Procedure & Reactor Plant Startup Procedures revised.W/960712 Ltr ML17292A3361996-06-20020 June 1996 LER 96-002-00:on 960504,critical Bus SM-8 Lost Power When Supply Breaker 3-8 Tripped.Caused by Personnel Error. Operators Counselled & Procedures revised.W/960620 Ltr ML17292A2861996-05-24024 May 1996 LER 96-001-00:on 960425,inadvertent ESF Actuations Occurred Due to Tripping of Temporary Power Supply to IN-3.Caused by Personnel Error.Operations Restored to IN-3 Loads & Reset ESF actuations.W/960524 Ltr ML17291B0891995-10-19019 October 1995 LER 95-011-00:on 950919,failed to Comply W/Ts SR for RCIC Sys Due to Analysis Deficiency That Resulted in Inadequate Surveillance Test Procedure.Surveillance Procedure Revised to Correct deficiency.W/951019 Ltr ML17291A9021995-07-0707 July 1995 LER 95-010-00:on 950609,HPCS DG Declared Inoperable Due to Discovery That TS Test Method Incomplete.Caused by Inadequate Testing Procedure.Test Procedure for HPCS DG Reviewed & Special Test Procedures written.W/950707 Ltr ML17291A9031995-07-0707 July 1995 LER 95-009-00:on 950607,inadvertent MSIV Closure Occurred During Surveillance Test Due to Poor Communication Between Test Team.Determined That MSIV Closure Not Valid Because Closure Not Triggered by Plant conditions.W/950707 Ltr ML17291A8501995-06-0808 June 1995 LER 95-006-01:on 950405,reactor Scram Occurred During Surveillance Testing Due to Protective Sys Relay Failure. Replaced Failed Relay Before Plant Startup ML17291A8101995-05-12012 May 1995 LER 95-008-00:on 940125,TS Wording Lead to Potential TS Violation.Caused by Lack of Clarity in Ts.Submitted Improved TS for Plant to Provide Addl clarity.W/950512 Ltr ML17291A7841995-05-0505 May 1995 LER 95-007-00:on 950222,emergency Diesel Start Occurred Due to Voltage Transient on BPA Grid.Confirmation Was Received at 17:51 H That Disturbance Had Originated in BPA Grid ML17291A7801995-05-0404 May 1995 LER 95-006-00:on 950405,main Turbine Trip Occurred During Performance of Surveillance Test Due to Protective Sys Relay Failed.Replaced Failed Relay Before Plant startup.W/950504 Ltr ML17291A7851995-05-0303 May 1995 LER 95-005-00:on 950222,inoperable IRM Had Been Relied Upon to Meet TS Requirements During Reactor Startup.Caused by Lack of Neutron Source to Test Instrumentation. Sys Knowledge Gained Will Be incorporated.W/950503 Ltr ML17291A7071995-03-25025 March 1995 LER 95-004-00:on 950226,malfunction in Main Turbine DEH Control Sys Caused All Four High Pressure Turbine Governor Valves to Rapidly Close.Caused by Blown Fuse.Suspected Faulty Circuit Card replaced.W/950325 Ltr ML17291A7011995-03-20020 March 1995 LER 95-002-00:on 950218,automatic Reactor Scram Occurred. Caused by Erroneous Positioning of Control During Performance of Scheduled Periodic Functional Test.Control repositioned.W/950320 Ltr 1999-07-20
[Table view] Category:RO)
MONTHYEARML17292B7421999-07-20020 July 1999 LER 99-001-00:on 990628,ESF Signal Closed All Eight MSIVs While Plant Was Shutdown.Caused by Failure of Relay RPS-RLY-K10D.Subject Relay Was Replaced & Tested on 990630. with 990720 Ltr ML17292B4451998-10-27027 October 1998 LER 98-012-01:on 980715,failure to Comply with Requirements of TS SR 3.8.4.7 Was Noted.Caused by Inadequate Work Practices.Training Session Was Held with Personnel.With 981027 Ltr ML17284A7561998-09-0303 September 1998 LER 98-013-00:on 980805,ESF Actuations Were Noted Due to Deenergization of Vital Electrical Bus SM-8.Caused by Inadequate Direction in Troubleshooting Plan.Will Conduct Training for Engineering Personnel.With 980903 Ltr ML17284A7571998-09-0202 September 1998 LER 98-014-00:on 980807,completion of TS 3.8.1.F Required Shutdown Due to Inoperability of EDG-2 Was Noted.Caused by Degraded Voltage Regulator for DG-2.Replaced Voltage Regulator & Associated Scrs.With 980902 Ltr ML17284A7551998-09-0202 September 1998 LER 98-015-00:on 980808,discovered Reactor Coolant Pressure Boundary Leak During Shutdown Conditions.Caused by Leakage from Socket Weld (Fwb 63) on Elbow Connection.Failed Piping Connection Was Replaced.With 980902 Ltr ML17284A7311998-08-17017 August 1998 LER 98-012-00:on 980716,determined That 24-month SR 3.8.4.7 Had Not Been Fulfilled within Specified Frequency.Caused by Inadequate Work Practices.License Requested & Received Enforcement Discretion Re Battery Svc test.W/980817 Ltr ML17284A7121998-07-23023 July 1998 LER 98-006-01:on 980520,discovered Discrepancies in Low Voltage Bus Calculations During Review of 10CFR50,App R Calculations for High Impedance Faults.Caused by Inadequate Work Practices.Implemented Procedural Changes ML17284A6951998-07-17017 July 1998 LER 98-011-00:on 980617,ECCS Pump Room Flooding Was Noted Due to FP Sys Pipe Break.Caused by Inadequate Design of FP Sys.Detailed Review of FP Sys Design Was Conducted. W/980717 Ltr ML17284A6961998-07-15015 July 1998 LER 98-010-00:on 980615,TS Required Shutdown Due to Inoperability of TIP Sys Isolation Valve Was Noted.Caused by Improper Installation of TIP Tubing.Reattached Affected Tubing & Inspected Other TIP tubing.W/980715 Ltr ML17284A6731998-07-0101 July 1998 LER 98-009-00:on 980606,nuclear Steam Supply Shutoff Sys Group 3 & 4 Isolations During Testing Was Noted.Caused by Procedural Deficiency.Counseled Individuals Involved in preparation.W/980701 Ltr ML17284A6651998-06-24024 June 1998 LER 98-007-00:on 980530,inadvertent Full Scram & Division 1 ECCS Injection Was Noted.Caused by Failure to Meet Mgt Work Practice Expectation When Encountering Deficient Procedure. Incident Review Board Convened to Review event.W/980624 Ltr ML17284A6641998-06-24024 June 1998 LER 98-008-00:on 980531,inadvertent Full Scram During RPV Leak Testing in Mode 4 Was Noted.Caused by Change in Mgt Techniques.Revised Procedures to Take Into Account Addl Water Head in Pressure Sensing lines.W/980624 Ltr ML17284A6631998-06-19019 June 1998 LER 98-006-00:on 980520,discovered Discrepancies in Low Voltage Bus Calculations During Review of App R Calculations for High Impedance Fault Analysis.Caused Indeterminate. Implemented Procedural Changes Involving Operator Action ML17284A6551998-06-0404 June 1998 LER 98-005-00:on 980506,potential for Failure of RHR Sys Valve to Close on Isolation Signal Was Noted.Caused by Design Deficiency.Caution Tag Was Placed on RHR-V-40 Control Switch to Inform Plant Operators of limitation.W/980604 Ltr ML17284A6421998-06-0101 June 1998 LER 98-004-00:on 980502,determined That Primary Containment Penetration Overcurrent Protection Does Not Meet Reg Guide 1.63 Requirements.Caused by Inadequate Design Changes. Installed Addl Fuse in RHR-MO-9 circuit.W/980601 Ltr ML17292B3281998-04-0909 April 1998 LER 98-002-00:on 980311,reactor Scram & Plant Transient Occurred,Due to Failed Closed Main Steam Isolation Valve. Caused by Loss of Pneumatic Actuating Supply Pressure. Problem Evaluation Request Written for Failure of MS-V-22D ML17292B3291998-04-0909 April 1998 LER 98-003-00:on 980311,WNP-2 Experienced SCRAM Signal as Result of Low Rpv.Caused by Less than post-SCRAM Operational Strategy for Resetting SCRAM Signal in Conditions.Changes in post-SCRAM Operational Strategy implemented.W/980409 Ltr ML17292B2661998-03-0404 March 1998 LER 98-001-00:on 980203,automatic Start of HPCS EDG Was Noted.Caused by Operator Error.Operations Crew Stabilized Plant at Approximately 75% Reactor Power & Investigation of Event Was initiated.W/980304 Ltr ML17292B1111997-11-10010 November 1997 LER 97-011-00:on 971010,HPCS Battery Charger Failed.Caused by Failure of a Phase Firing Control Circuit Board Due to Aging During 7 Yrs of Use.Hpcs Sys Was Immediately Declared inoperable.W/971110 Ltr ML17292B1151997-11-0707 November 1997 LER 97-010-00:on 970906,discovered That TS SR 3.4.5.1 for Identified Portion of RCS Total Leakage Would Not Be Able to Perform within Time Limits of SR 3.0.2.Caused by Inadequate Methods.Method of Meeting SR 3.4.5.1 Established ML17292B0641997-09-24024 September 1997 LER 97-004-01:on 970327,plant Operators Manually Scrammed Reactor as Required by TS Due to Indication of Entry Into Region a of power-to-flow Map.Caused by Inadequate Attention to Detail.Established Event Evaluation teams.W/970924 Ltr ML17292B0241997-08-18018 August 1997 LER 97-009-00:on 970717,discovered Error in Recently Performed Inservice Testing procedure,OSP-TIP/IST-R701. Caused by Procedure Inadequacy.Plant Procedure OSP/TIP/IST-R701 Will Be changed.W/970818 Ltr ML17292B0291997-08-15015 August 1997 LER 97-008-00:on 970716,wire Seal Used to Lock Containment Instrument Air Pressure Control valve,CIA-PCV-2B,found Not Intact.Cause of Misadjustment of CIA-PCV-2B Unknown.Event Will Be Communicated to Plant employees.W/970815 Ltr ML17292B0201997-08-15015 August 1997 LER 97-S01-00:on 970718,failure to Take Compensatory Measure for Inoperative Microwave Security Zone Occurred. Caused by Personnel Error.Training Will Be Conducted W/ Appropriate Members of Security force.W/970815 Ltr ML17292A9481997-07-23023 July 1997 LER 97-007-00:on 970611,voluntary Rept of Automatic Start of DG-1 & DG-2 Was Experienced.Caused by Undervoltage Condition on Electrical Busses SM-7 & SM-8.Circulating Water Pump CW-P-1C Control Switch Placed in pull-to-lock.W/970723 Ltr ML17292A9201997-06-26026 June 1997 LER 97-006-00:on 970527,non-performance of Surveillance Requirement 3.6.1.3.2 for Blind Fanges,Was Noted.Caused Because Misunderstanding of Intent of Specs.Added Five Structural Assemblies for SP.W/970626 Ltr ML17292A8331997-04-28028 April 1997 LER 97-004-00:on 970327,plant Operators Manually Scrammed Reactor as Required by TS Due to Entry Into Region a of power-to-flow Map Following Planned Trip of Single Mfp. Event Evaluation teams,established.W/970428 Ltr ML17292A8311997-04-28028 April 1997 LER 97-005-00:on 970327,valid Reactor Scram Signal Received Due to Low Water Level Condition During Preparations for SRV Testing.Caused by Risks & Consequences of Decisions Not Completely Identified.Restored Water level.W/970428 Ltr ML17292A8251997-04-21021 April 1997 LER 97-003-00:on 970320,notification of Noncompliance W/Ts as TS SRs for Response Time Testing Were Not Being Met for Specified Instrumentation in Rps,Pcis & Eccs.Requested Enforcement Discretion for One Time exemption.W/970421 Ltr ML17292A7431997-03-20020 March 1997 LER 97-002-00:on 970218,determined That Rod Block Monitor (RBM) Calibr Values Were Not Set IAW Tech Specs.Caused by Calibr Procedures Inadequacies.Revised & re-performed RBM Channel Calibr procedures.W/970330 Ltr ML17292A7401997-03-13013 March 1997 LER 97-001-00:on 970211,reactor Water Cleanup Sys Blowdown Flow Isolation Setpoint Was Slightly Above TS Allowable Valve Occurred Due to Calculation Error.Lds Fss LD-FS-15 LD-FS-16 Were Declared inoperable.W/970313 Ltr ML17292A6641997-01-22022 January 1997 LER 96-009-00:on 961220,miscalculation of Instantaneous Overcurrent Relay Settings Resulted in Inoperability of safety-related Equipment.Caused by Utilization of Inappropriate Design.Testing Was completed.W/970122 Ltr ML17292A6461997-01-0606 January 1997 LER 96-008-00:on 961205,failure to Comply with TS Action Requirement for Emergency Core Cooling Sys Actuation Instrumentation Occurred Due to Unidentified Inoperability Condition.Pmr initiated.W/970106 Ltr ML17292A6371996-12-19019 December 1996 LER 96-007-00:on 961122,electrical Breakers Were Not Seismically Qualified in Test/Disconnect Position.Circuit Breaker Mfg Did Not Consider Raced Out Breaker Position During Testing.Relocated Circuit breakers.W/961217 Ltr ML17292A4121996-08-0808 August 1996 LER 96-006-00:on 960709,average Power Range Monitor Rod Block Downscale Surveillance Not Performed Prior to Entry Into Mode 1.Caused by long-standing Misinterpretation of Requirements of Tss.Procedures revised.W/960808 Ltr ML17292A3801996-07-24024 July 1996 LER 96-004-00:on 960624,plant Was Manually Scrammed by Control Room Personnel Due to Reactor Water Level Transient Experienced During Testing of Digital Feedwater Sys.Caused by Programming Error.Sys Was corrected.W/960724 Ltr ML17292A3771996-07-24024 July 1996 LER 96-005-00:on 960624,determined Missed Surveillance Test Re Channel Check of Average Power Range Monitor.Caused by Inadequate Procedures.Revised Surveillance Procedure Re When APRM Checks Must Be performed.W/960724 Ltr ML17292A3641996-07-12012 July 1996 LER 96-003-00:on 960615,required Surveillance Test Not Performed When Required by TS 3.4.1.3.Caused by Inadequate Procedures.Implementing Surveillance Procedure & Reactor Plant Startup Procedures revised.W/960712 Ltr ML17292A3361996-06-20020 June 1996 LER 96-002-00:on 960504,critical Bus SM-8 Lost Power When Supply Breaker 3-8 Tripped.Caused by Personnel Error. Operators Counselled & Procedures revised.W/960620 Ltr ML17292A2861996-05-24024 May 1996 LER 96-001-00:on 960425,inadvertent ESF Actuations Occurred Due to Tripping of Temporary Power Supply to IN-3.Caused by Personnel Error.Operations Restored to IN-3 Loads & Reset ESF actuations.W/960524 Ltr ML17291B0891995-10-19019 October 1995 LER 95-011-00:on 950919,failed to Comply W/Ts SR for RCIC Sys Due to Analysis Deficiency That Resulted in Inadequate Surveillance Test Procedure.Surveillance Procedure Revised to Correct deficiency.W/951019 Ltr ML17291A9021995-07-0707 July 1995 LER 95-010-00:on 950609,HPCS DG Declared Inoperable Due to Discovery That TS Test Method Incomplete.Caused by Inadequate Testing Procedure.Test Procedure for HPCS DG Reviewed & Special Test Procedures written.W/950707 Ltr ML17291A9031995-07-0707 July 1995 LER 95-009-00:on 950607,inadvertent MSIV Closure Occurred During Surveillance Test Due to Poor Communication Between Test Team.Determined That MSIV Closure Not Valid Because Closure Not Triggered by Plant conditions.W/950707 Ltr ML17291A8501995-06-0808 June 1995 LER 95-006-01:on 950405,reactor Scram Occurred During Surveillance Testing Due to Protective Sys Relay Failure. Replaced Failed Relay Before Plant Startup ML17291A8101995-05-12012 May 1995 LER 95-008-00:on 940125,TS Wording Lead to Potential TS Violation.Caused by Lack of Clarity in Ts.Submitted Improved TS for Plant to Provide Addl clarity.W/950512 Ltr ML17291A7841995-05-0505 May 1995 LER 95-007-00:on 950222,emergency Diesel Start Occurred Due to Voltage Transient on BPA Grid.Confirmation Was Received at 17:51 H That Disturbance Had Originated in BPA Grid ML17291A7801995-05-0404 May 1995 LER 95-006-00:on 950405,main Turbine Trip Occurred During Performance of Surveillance Test Due to Protective Sys Relay Failed.Replaced Failed Relay Before Plant startup.W/950504 Ltr ML17291A7851995-05-0303 May 1995 LER 95-005-00:on 950222,inoperable IRM Had Been Relied Upon to Meet TS Requirements During Reactor Startup.Caused by Lack of Neutron Source to Test Instrumentation. Sys Knowledge Gained Will Be incorporated.W/950503 Ltr ML17291A7071995-03-25025 March 1995 LER 95-004-00:on 950226,malfunction in Main Turbine DEH Control Sys Caused All Four High Pressure Turbine Governor Valves to Rapidly Close.Caused by Blown Fuse.Suspected Faulty Circuit Card replaced.W/950325 Ltr ML17291A7011995-03-20020 March 1995 LER 95-002-00:on 950218,automatic Reactor Scram Occurred. Caused by Erroneous Positioning of Control During Performance of Scheduled Periodic Functional Test.Control repositioned.W/950320 Ltr 1999-07-20
[Table view] Category:TEXT-SAFETY REPORT
MONTHYEARML17284A9001999-10-31031 October 1999 Rev 0 to COLR 99-15, WNP-2 Cycle 15,COLR GO2-99-177, LER 99-S01-00:on 990903,failure to Take Compensatory Measure within Required Time Upon Failure of Isolation Zone Microwave Unit,Was Noted.Caused by Personnel Error.Provided Refresher Training on Compensatory Measures.With1999-10-0101 October 1999 LER 99-S01-00:on 990903,failure to Take Compensatory Measure within Required Time Upon Failure of Isolation Zone Microwave Unit,Was Noted.Caused by Personnel Error.Provided Refresher Training on Compensatory Measures.With ML17284A8941999-09-30030 September 1999 Monthly Operating Rept for Sept 1999 for WNP-2.With 991012 Ltr ML17284A8801999-08-31031 August 1999 Monthly Operating Rept for Aug 1999 for WNP-2.With 990910 Ltr ML17284A8691999-07-31031 July 1999 Monthly Operating Rept for July 1999 for WNP-2.With 990813 Ltr ML17292B7421999-07-20020 July 1999 LER 99-001-00:on 990628,ESF Signal Closed All Eight MSIVs While Plant Was Shutdown.Caused by Failure of Relay RPS-RLY-K10D.Subject Relay Was Replaced & Tested on 990630. with 990720 Ltr ML17292B7271999-06-30030 June 1999 Monthly Operating Rept for June 1999 for WNP-2.With 990707 Ltr ML17292B6961999-05-31031 May 1999 Monthly Operating Repts for May 1999 for WNP-2.With 990608 Ltr ML17292B6641999-04-30030 April 1999 Monthly Operating Rept for Apr 1999 for WNP-2.With 990507 Ltr ML17292B6391999-03-31031 March 1999 Monthly Operating Rept for Mar 1999 for WNP-2.With 990413 Ltr ML17292B5871999-02-28028 February 1999 Monthly Operating Rept for Feb 1999 for WNP-2.With 990311 Ltr ML17292B5571999-01-31031 January 1999 Monthly Operating Rept for Jan 1999 for WNP-2.With 990210 Ltr ML17292B5621999-01-31031 January 1999 Rev 1 to COLR 98-14, WNP-2 Cycle 14 Colr. ML17292B5341999-01-15015 January 1999 Part 21 Rept Re Incorrect Modeling of BWR Lower Plenum Vol in Bison.Defect Applies Only to Reload Fuel Assemblies Currently in Operation at WNP-2.BISON Code Model for WNP-2 Has Been Revised to Correct Error ML17292B5331999-01-15015 January 1999 Part 21 Rept Re XL-S96 CPR Correlation for SVEA-96 Fuel. Defect Applies Only to WNP-2,during Cycles 12,13 & 14 Operation.Evaluations of Defect Performed by ABB-CE ML17292B4791998-12-31031 December 1998 Washington Public Power Supply Sys 1998 Annual Rept. with 981215 Ltr ML17292B5351998-12-31031 December 1998 Monthly Operating Rept for Dec 1998 for WNP-2.With 990112 Ltr ML17292B5741998-12-31031 December 1998 WNP-2 1998 Annual Operating Rept. with 990225 Ltr ML17284A8231998-11-30030 November 1998 Monthly Operating Rept for Nov 1998 for WNP-2.With 981207 Ltr ML17284A8081998-10-31031 October 1998 Monthly Operating Rept for Oct 1998 for WNP-2.With 981110 Ltr ML17292B4451998-10-27027 October 1998 LER 98-012-01:on 980715,failure to Comply with Requirements of TS SR 3.8.4.7 Was Noted.Caused by Inadequate Work Practices.Training Session Was Held with Personnel.With 981027 Ltr ML17284A7831998-09-30030 September 1998 Monthly Operating Rept for Sept 1998 for WNP-2.With 981007 Ltr ML17284A7491998-09-10010 September 1998 WNP-2 Inservice Insp Summary Rept for Refueling Outage RF13 Spring,1998. ML17284A7561998-09-0303 September 1998 LER 98-013-00:on 980805,ESF Actuations Were Noted Due to Deenergization of Vital Electrical Bus SM-8.Caused by Inadequate Direction in Troubleshooting Plan.Will Conduct Training for Engineering Personnel.With 980903 Ltr ML17284A7571998-09-0202 September 1998 LER 98-014-00:on 980807,completion of TS 3.8.1.F Required Shutdown Due to Inoperability of EDG-2 Was Noted.Caused by Degraded Voltage Regulator for DG-2.Replaced Voltage Regulator & Associated Scrs.With 980902 Ltr ML17284A7551998-09-0202 September 1998 LER 98-015-00:on 980808,discovered Reactor Coolant Pressure Boundary Leak During Shutdown Conditions.Caused by Leakage from Socket Weld (Fwb 63) on Elbow Connection.Failed Piping Connection Was Replaced.With 980902 Ltr ML17284A7681998-08-31031 August 1998 Monthly Operating Rept for Aug 1998 for WNP-2.With 980915 Ltr ML17284A7311998-08-17017 August 1998 LER 98-012-00:on 980716,determined That 24-month SR 3.8.4.7 Had Not Been Fulfilled within Specified Frequency.Caused by Inadequate Work Practices.License Requested & Received Enforcement Discretion Re Battery Svc test.W/980817 Ltr ML17284A7261998-07-31031 July 1998 Monthly Operating Rept for July 1998 for WNP-2.W/980810 Ltr ML17284A7121998-07-23023 July 1998 LER 98-006-01:on 980520,discovered Discrepancies in Low Voltage Bus Calculations During Review of 10CFR50,App R Calculations for High Impedance Faults.Caused by Inadequate Work Practices.Implemented Procedural Changes ML17284A6951998-07-17017 July 1998 LER 98-011-00:on 980617,ECCS Pump Room Flooding Was Noted Due to FP Sys Pipe Break.Caused by Inadequate Design of FP Sys.Detailed Review of FP Sys Design Was Conducted. W/980717 Ltr ML17284A6961998-07-15015 July 1998 LER 98-010-00:on 980615,TS Required Shutdown Due to Inoperability of TIP Sys Isolation Valve Was Noted.Caused by Improper Installation of TIP Tubing.Reattached Affected Tubing & Inspected Other TIP tubing.W/980715 Ltr ML17284A6731998-07-0101 July 1998 LER 98-009-00:on 980606,nuclear Steam Supply Shutoff Sys Group 3 & 4 Isolations During Testing Was Noted.Caused by Procedural Deficiency.Counseled Individuals Involved in preparation.W/980701 Ltr ML17284A6751998-06-30030 June 1998 Ro:On 980617,flooding of RB Northeast Stairwell with Consequential Flooding of Two ECCS Pump Rooms.Caused by Inadequate Fire Protection Sys Design.Pumped Out Water from Affected Areas to Point Below Berm Areas of Pump Rooms ML17284A6641998-06-24024 June 1998 LER 98-008-00:on 980531,inadvertent Full Scram During RPV Leak Testing in Mode 4 Was Noted.Caused by Change in Mgt Techniques.Revised Procedures to Take Into Account Addl Water Head in Pressure Sensing lines.W/980624 Ltr ML17284A6651998-06-24024 June 1998 LER 98-007-00:on 980530,inadvertent Full Scram & Division 1 ECCS Injection Was Noted.Caused by Failure to Meet Mgt Work Practice Expectation When Encountering Deficient Procedure. Incident Review Board Convened to Review event.W/980624 Ltr ML17284A6631998-06-19019 June 1998 LER 98-006-00:on 980520,discovered Discrepancies in Low Voltage Bus Calculations During Review of App R Calculations for High Impedance Fault Analysis.Caused Indeterminate. Implemented Procedural Changes Involving Operator Action ML17284A6551998-06-0404 June 1998 LER 98-005-00:on 980506,potential for Failure of RHR Sys Valve to Close on Isolation Signal Was Noted.Caused by Design Deficiency.Caution Tag Was Placed on RHR-V-40 Control Switch to Inform Plant Operators of limitation.W/980604 Ltr ML17284A6421998-06-0101 June 1998 LER 98-004-00:on 980502,determined That Primary Containment Penetration Overcurrent Protection Does Not Meet Reg Guide 1.63 Requirements.Caused by Inadequate Design Changes. Installed Addl Fuse in RHR-MO-9 circuit.W/980601 Ltr ML17284A6491998-05-31031 May 1998 Rev 0 to COLR 98-14, WNP-2,Cycle 14 Colr. ML17292B4031998-05-31031 May 1998 Monthly Operating Rept for May 1998 for WNP-2.W/980608 Ltr ML17292B3921998-04-30030 April 1998 Monthly Operating Rept for Apr 1998 for WNP-2.W/980513 Ltr ML17292B3291998-04-0909 April 1998 LER 98-003-00:on 980311,WNP-2 Experienced SCRAM Signal as Result of Low Rpv.Caused by Less than post-SCRAM Operational Strategy for Resetting SCRAM Signal in Conditions.Changes in post-SCRAM Operational Strategy implemented.W/980409 Ltr ML17292B3281998-04-0909 April 1998 LER 98-002-00:on 980311,reactor Scram & Plant Transient Occurred,Due to Failed Closed Main Steam Isolation Valve. Caused by Loss of Pneumatic Actuating Supply Pressure. Problem Evaluation Request Written for Failure of MS-V-22D ML17292B3371998-03-31031 March 1998 Monthly Operating Rept for Mar 1998 for WNP-2.W/980409 Ltr ML17292B2641998-03-0404 March 1998 Performance Self Assessment,WNP-2. ML17292B2661998-03-0404 March 1998 LER 98-001-00:on 980203,automatic Start of HPCS EDG Was Noted.Caused by Operator Error.Operations Crew Stabilized Plant at Approximately 75% Reactor Power & Investigation of Event Was initiated.W/980304 Ltr ML17292B2911998-02-28028 February 1998 Monthly Operating Rept for Feb 1998 for WNP-2.W/980313 Ltr ML17284A7971998-02-17017 February 1998 Rev 28 to Operational QA Program Description, WPPSS-QA-004.With Proposed Rev 29 ML17292B3591998-02-12012 February 1998 WNP-2 Cycle 14 Reload Design Rept. 1999-09-30
[Table view] |
Text
ULA INFORMATION DIST TIO YSTEM (RIDS>
ACCESSION NBR:8708250086 DOC. DATE: 87/08/21 NOTARIZED: NO DOCKET FACIL: 50-397 WPPSS Nuclear Pro Ject> Unit 2i Washington Public Poee 05000397 AUTH. NAME AUTHOR AFFILIATION 'k WASHINGTON. B. L. Washington Public Power Supply System POWERSI C. M. Washington Public PoUjer Supply System RECIP. NAME REC1P IENT AFFILIATION
SUBJECT:
LER 87-024-00: on 870722I limitorque motor-operated open-direction torque switch bypass pumper discovered missing.
Caused bg personnel error. *11 missing Jumpers installed memo re top tier drawings issued to -personnel. W/870821 -ltr.
DISTRIBUTION CODE: IESSD COPIES RECEIVED: LTR I ENCL TITLE: 50. 73 Licensee Event Report (LER)i Incident Rpti g etc.SIZE: P NOTES:
RECIPIENT COPIES RECIPIENT COPIES ID CODE/NAME LTTR ENCL ID CODE/NAME LTTR ENCL PD5 L* 1 1 PD5 PD 1 1 SAMWORTH> R 1 INTERNAL: ACRS MICHELSON 1 1 ACRS MOELLER 2 2 AEOD/DOA 1 1 AEOD/DSP/NAS 1 1 AEOD/DSP/RO*B 2 2 AEOD/DSP/TPAB 1 DEDRO 1 NRR/DEBT/ADB 1 0 NRR/DEST/CEB 1 1 NRR/DEBT/ELB 1 1 NRR/DEST/ICSB } 1 NRR/DEBT/MEB 1 1 NRR/DEST/MTB NRR/DEBT/PSB 1 1 NRR/DEST/RSB 1 1 NRR/DEBT/SGB 1 1 NRR/DLPG/HFB 1 1 NRR/DLPG/GAB 1 1 NRR/DOEA/E*B 1 1 NRR/DREP/RAB 1 1
-- REP/RPB 2 2 NRR/PMAS/ ILRB 1 1 REG FIL 02 1 1 RES DEPY GI 1 1 ORDI J 1 1 RES/DE/EIB 1 1 RGN5 FILE 01 1 EXTERNAL: EQ5G QROH M 5 5 H ST LOBBY WARD 1 1 LPDR 1 1 NRC PDR } 1 NSIC HARRIS' 1 1 NSIC MAYSI G 1 1 TOTAL NUMBER OF COPIES REQUIRED: LTTR 43 ENCL 42
NRC Form 358 (843)
~ 0 V.S. NUCLEAR REGULATOAY COMMISSION APPROVED OMB NO. 31600)0e EXPIRES: 8/31/88 LICENSEE EVENT REPORT {LER)
FACILITY NAME (I) DOCKET NUMBER (2I 'PAGE 3 Washin ton Nuclear Plant - Unit 2 o 5 o o o 3 9 OF 07
""'(" M1ss1ng 1mitorque o or pera or pen- 1rec 1on orque 1
Switch Bypass Jumpers Caused hy Personnel Error EVENT DATE I5) LEA NUMBER (6) REPORT DATE {7) OTHER FACILITIES INVOLVE'D (8)
MONTH DAY YEAR YEAR sEQUENTIAL SeeI RS~~ MONTH OAY YEAR FACILITYNAMES DOCKET NUMBER(S)
NUMBER AF: NUM88 R 0 5 0 0 0 0 7 2 2 8 7 8 7 0 2 4 0 00 821 87 0 5 0 0 0 OPERATING THIS REPORT IS SUBMITTED.PURSUANT T 0 THE REQUIREMENTS OF 10 CFR (): /Check One or more ol the follovf/nP/ (11 MODE (8) 20A02(8) 73.7118) 20A05(c) 50.73(e) (2)(lv)
POWER 20A05(el(i)(l) 50.38(cl(l) 50.73(e)(2)(v) 73.71(cl LEYEL 0 0 20A05(s)(l)(8) 50M4)(2) 50,734) (2)(vill (2)(vill)(BI OTHER /Specify /n Ahrtrect tN/ow end /n Text, f/RC Form
('a+8 20A05(s)(I)(IBI 50.734) l2)(ll 50.73(sl (2)(vill)(A) 3SBA/
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NAME TELEPHONE NUMBER W h'iance En ineer COMPLETE ONE LINE FOR EACH COMPONENT FAILURE DESCRIBED IN THIS REPORT (13)
AREA CODE 50 93 77- 20 0
)N CAUSE SYSTEM COMPONENT MANUFAC.
TVRER REPORTABLE TO NPADS g ' CAUSE SYSTEM COMPONENT MANUFAC.
TUREA EPOATABLE TO NPAOS
.. +g L(WN SUPPLEMENTAL REPORT EXPECTED (le)
EXPECTED MONTH mM DAY YEAR SUBMISSION DATE (15)
YES fir yer, complete EXPECTED SUBS//$ $ /Oh/ DATE/ NO ABBTRAcT /Limit to fe00 rpecer, I e., epproxlmerely fifmen t/nore specs rypevrrltNn linn/ (15)
On July 22, 1987, while the plant was in Cold Shutdown, Plant engineers and electricians discovered a Limitorque motor operator open-direction torque switch bypass .jumper missing. This bypass jumper was required to be installed by a Plant Co(I)1itment in response to IE Circular No. 81-13 "Torque Switch Electrical Bypass Circuit for Safeguard Service Valve Motors.H The missing jumper was discovered by Plant personnel investigating the cause of a motor failure on a Main Steam Isolation Valve Leakage Control System Valve Motor Operator (MSLC-V-lA and MSLC-M0-1A).
A review of Plant documentation led to the field inspection of all MSLC inboard valves. All 12 Inboard MSLC Valves were found with the open-direction torque switch bypass jumpers missing.
Plant Management delayed restart of the Plant and organized a Task Force to further investigate the scope of the problem. The Task Force reviewed all Safeguard Service Valve Motors and identified 66 valves to be field inspected. Only two other valves were found with,jumpers missing. They were Residual Heat Removal Valve RHR-V-GA, a shutdown cooling crosstie isolation valve, and Plant Service Mater Valve SM-V-90, an isolation valve to a Diesel Generator Building Corridor Heating and Ventilation System.
8708250086 870820>97 PDR ADOCK 0500PDR 8
NAC Form 385
~ nnl
~ 0 NRC Form 3EEA U.S. NUCLEAR REGULATORY COMMISSION (943 I LICENSEE EVENT REPORT ILER) TEXT CONTINUATION APPROVEO OMB NO, 3150W104 EXPIRES: 8/31/88 FACILITY NAME Ill DOCKET NUMBER 12l LER NUMBER IEI PACE 13)
YEAR 'gK SEOVENTIAL REVISION NVMEER NVMEER Washington Nuclear Plant - Unit 2 0 5 0 0 0 3 87 02 40 0 2 oF0 7 TEXT ///mare E/>>ae /I Iea>>ler/, Iree I//aa'a>>//E/IC Farrrr 3BEI'a/1131 Abstract (continued)
The first Task Force recommended that the Safeguard Service Valve Motor list for WNP-2 be reviewed for completeness. A second Task Force-reviewed this list and determined that six additional valves should be added to the list. Three of these valves should have been included on the original list. They are Main Steam Valve MS-V-146, the main steam supply to auxilaries and Standby Gas Treatment Valves SGT-V-3Al and 382, inlet valves to SGT. secondary fans. The other three valves FPC-V-149 (demineralized effluent to suppression pool water) and AS-V-68A and 8 (auxilary steamline reactor building isolation valves) were installed after Plant startup and the list was not updated.
The cause of the missing jumpers was attributed to either: 1) personnel error on the part of Plant personnel who removed installed jumpers while using non top-tier plant drawings (no documentation could be found that authorized or documented removal of the jumpers), or 2) The jumpers were never installed because of conflicting installation directions from the Plant Architect/
Engineer.
The majorcorrective actions are: 1) all missing jumpers were installed prior to Plant restart, 2) the Plant Manager issued a memorandum to all Plant personnel remi ndi ng them of their responsibility to use top tier drawings, 3) the Safeguard Service Valve Motor list will be formalized and included in the Plant Design data base, 4) the Maintenance Department will undertake an effort to improve documentation. of work performed, and 5) a Engineering effort to upgrade Plant Electrical Wiring Diagrams to top tier status will be expedited.
There are no unacceptable adverse consequences associated with this event because: 1) the missing jumpers do not effect valve operability and 2) each valve/system was backed by redundant systems.
Plant Conditions a) , Power Level - 0'4 b) Plant Mode - 4 (Cold Shutdown)
Event Description On July 22, 1987, while the Plant was in Cold Shutdown, Plant engineers a'nd electricians discovered a Limitorque motor operator open-direction torque switch bypass jumper missing. This bypass jumper was required to be installed by a Plant Commitment in response to IE Circular No. 81-13 "Torque Switch Electrical Bypass Circuit for Safeguard Service Valve Motors". The missing jumper was discovered by Plant personnel investigating the cause of a motor failure on a Main Steam Isolation Valve Leakage Control System Valve Motor Operator (MSLC-V-lA and MSLC-M0-1A).
NIIC SOIINI SEER RU.S GPO'.1088&824 538/455 18 43l
~ O NRC FOIRI 348A U.S. NUCLEAR REGULATORY COMMISSION (94/31 LICENSEE EVENT REPORT ILERI TEXT CONTINUATION APPROVED OMS NO, 3150M(04 EXPIRES; 8/31/88 FACILITYNAME ('ll DOCKET NUMBER (21 LER NUMBER (8) PAGE (31 YEAR SEGVENTIAL ~i'm: REVISION N% NVMOER NVMIER Washin ton Nuclear Plan - Ij i o s o o o q OF TEXT /// mo/4 4Pooo /I IoqooRE IISS mREUosN/ Hl/C %%dmI 3884'4/ (IT(
Plant Engineers, in an effort to determine the cause of the missing bypass jumper, initiated a review of construction documentation and maintenance records for MSLC-V-1A and the other inboard MSLC isolation and bleed valves.
The results of the review were: 1) Construction documentation conclusively showed the jumpers for the inboard isolation valve motor operators were installed (MSLC-MO-1A through 1D); 2) There was no information on bypass jumper removal in any of the Plant maintenance documentation, and; 3) The construction documentation for the inboard bleed valve motor operators (MSLC-MO-2A through 2D and MSLC-MO-3A through 3D) was inconclusive as to whether the jumpers were ever installed. A field inspection of all the inboard MSLC Valves found no open-direction torque switch bypass jumpers installed.
Maintenance Work Requests were prepared and the required bypass jumpers were installed. This. work was completed on July 22, 1987.
As a result of the above findings, Plant Management delayed the planned Plant restart and organized a Task Force to further investigate the scope of the problem.
IE Circular 81-13 requested Plants to install torque switch bypass circuits to prevent a possible faulted condition (torque switch failure or premature actuation) from inhibiting a valve in accomplishing its safety function. In response to IE Circular 81-13 the Plant Architect/Engineer (Burns 8 Roe, Inc.)
prepared a list of valves for WNP-2 which required torque switch bypass circuits. Burns and Roe, Inc., subsequently issued direction to incorporate these bypass circuits into the Plant design. This work was completed prior to Plant Startup pre-operational testing. The bypass circuit requirement was implemented by either; 1) the use of a limit switch in parallel with the to~que switch which prevented the torque switch from being activated until the valve was nearly fully opened or closed; or 2) by hardwiring a jumper around the torque switch.
The Task Force began by reviewing informational as-built sketches of motor operator valve (MOV) wiring made for an equipment qualification walkdown performed 'during the Spring of 1986. This review concluded that a problem may exist in implementation of the open-direction hardwired torque switch bypass circuits (jumpers). The Task Force recommended that MOVs with open-direction hardwired torque switch bypass circuits be field inspected.
The Burns 8 Roe, Inc., list of Safeguard Service Valve Motors included 179 valves of which 116 valves have open or open/close torque switch bypass circuits. Those MOVs which used limit switch bypass circuits were eliminated from the field inspection list because there were no previous plant problems associated with these circuits. Also, some MOVs with hardwired bypass circuits which were known, for various reasons, to have the jumpers installed were also eliminated from the field inspection list. Sixty-six (66)"MOVs were field inspected to verify the installation of the open-direction torque switch bypass jumper. Oply two of the 66 MOVs inspected were found with jumpers missing (RHR-MO-6A and SW-MO-90). It was determined that the jumper in SW-MO-90 was NRC FORM 3444 o U.S.OPO,'1988 0824 538/485 (9831
~ ~
NRC Ferro~A U.S. NUCLEAR REGULATORY COMMISSION
)943)
LICENSEE EVENT REPORT {LER) TEXT CONTINUATION APPROVEO OMB NO. 3)50&)04 EXPIRES: 8/31/88 FACILITY NAME Ill OOCKET NUMBER (2) LER NUMBER IS)
YEAR I@ SEOVENTIAL rP> REVISION NUM VRC< NVMBER
- ' 0 s OF Washin ton Nuclear Plan U TEXT ///more e/reee /e rfr/rkerL we //I/oR5/ HRC form 3///)AS I Ill) removed due to personnel error in reading a Plant drawing during the Spring of 1987 outage. No documentation was found which documented the removal of. the jumper in RHR-MO-6A. New jumpers were installed in both of these MOVs. The inspection results also confirmed the valve field inspection criteria as no problems with limit switch bypass circuits were found. This work was completed hy July 24, 1987.
During this investigation it was determined that the original Burns 8 Roe, Inc.
Safeguard Service Valve Motor List should be reviewed for completeness. This led to formation of a second Task Force comprised of Operations, Technical
- Staff and Engineering personnel. This review resulted in the addition of six new MOVs to the Safeguard Service Valve Motor list. Three of the six valves were installed after the original list was made (FPC-V-149 and AS-V-68A/)3), and the other three valves (MS-V-146 and SGT-V-3Al and 3I32) were omitted from the original list. A Plant Modification Request (PMR) was prepared processed, and approved to install jumpers in each of these valves, except for FPC-V-149. The required bypass circuit was included in the original FPC-V-149 Plant Modification package. This work was completed on July 25, 1987.
There are two causes for the missing jumpers; 1) In one case plant records show the bypass jumpers were installed; however, the Electrical Wiring Diagrams (nontop tier drawings) did not show the jumpers and the jumpers were subsequently removed to make valve wiring conform to these non top-tier drawings. Also, documentation of Plant work activities was insufficient to determine when the jumpers were removed. (Cause for MSLC-MO-lA,through 10, RHR-M0-6A, and SW-MO-90.); 2) In the second case it is believed the bypass jumpers were not installed during startup because of conflicting information in the Electrical Elementary Drawings, Connection Diagrams, and Electrical Wiring Diagrams included in the implementing Project Engineering Directives (PED).
Both cases are the result of personnel error in that Plant personnel did not follow Plant directives regardi ng top-tier drawing use and Architect/Engineer personnel prepared and issued incomplete design packages.
There are two reasons for the additions to the original Safeguard Service Valve Motor list: 1) The Plant Architect Engineer Burns 8 Roe, Inc., for reasons unknown, missed three valves that should have been included on the original list, and 2) the Supply System due to an oversight did not maintain the list after the Plant was licensed.
Immediate Corrective Action After the first missing jumpers were found, a Plant Task Force of Engineers and Maintenance personnel was formed to review all selected Safeguard Service Valve Motors to ensure that torque switch bypass jumpers were properly installed.
All missing jumpers were installed by July 25, 1987.
NRC FORM SESA e U.S GPO.)085 0528 538/l55
$ 83)
~ 0 NRC form 366A U.S, NUCLEAR REOULATORY COMMISSION I9 83 I LICENSEE EVENT REPORT (LER) TEXT CONTINUATION APPROVEO OMB NO. 3150&)06 EXPIRES: 8/3) /88 FACILITY NAME )1) DOCKET NUMBER ITI LER NUMBER IS) PACE )3)
SEOUKNTIAL VISION rr UM 6 rr lrQM 6 rl Washin ton Nuclear Plant - Unit 2 o s o o o 3 g 8 7 0 2 4 00 05 oF0 7 TEXT ///moro opooo /1 r//rior/, rroo ~HRC forrrr 3/E)AS/ l)T)
A second Task Force of Operations, Technical, and Engineering personnel reviewed the Safeguard Service Valve Motor List to ensure its completeness.
Six new valves were added to the Safeguards Service Valve Motor List and Engineering direction was issued to install, where necessary, torque switch bypass .jumpers.
The first Task Force also reviewed Plant top-tier drawings to ensure that the torque switch bypass jumpers were properly shown. Five top-tier plant Electrical Elementary Drawings were identified as needing revision. A Plant Modification request was processed and implemented to revise these drawings.
Further Corrective Action and Evaluation The Plant Manager issued on a memorandum July 28, 1987 reminding Plant personnel of thei r responsibility to use top-tier drawings when performing modifications, maintenance, testing, or troubleshooting plant hardware.'he design criteria for Safeguard Service Valve Motor selection will be formalized. After the design criteria is formalized, WNP-2 valves will be re-reviewed against this criteria and a formal valve safety function list as related to IE Circular 81-13 will be issued. This valve safety function list will be incorporated into the WNP-2 design data base..
Engineering efforts already in progress to upgrade Electrical Wiring Diagrams to top-tier status will be expedited. Electrical Elementary Drawings, Connection Diagrams and Electrical Wiring Diagrams (EWDS) for all Safeguard Service Valve Motors will be cross checked to ensure that each drawing accurately reflects the Plant design with respect to torque switch bypass circuits.
Drawings with known inconsistencies resulting from the field inspection will be revised to reflect as-built status.
The Plant'Maintenance Department will undertake an effort to improve the .
documentation of work activities performed.
Safety Significance There are no unacceptable adverse consequences associated with this event.
First, these valves were designed to perform without the torque switch bypass circuits installed. Periodically, operation of these valves is demonstrated by Plant Surveillance Testing or by operational use. The torque switch bypass circuits were installed only to provide added assurance that a faulted condition would not prevent the valve from performing its safety function. So the chance of one of these valves not performing its safety function because of a missing .torque switch bypass circuit is remote. Secondly, the discussions which follow show that each system 'with a valve found with a missing bypass jumper is adquately protected by redundant components or systems.
NRC FORM 366A o U.S GPO:1988&826 638/46S ISA)
NRC Form 3SSA V.S, NUCLEAR REGULATORY COMMISSION 1943 l LICENSEE EVENT REPORT ILER) TEXT CONTINUATION APPROYEO OMS NO. 3150&IGO EXPIRES: 8/31/88 FACILITYNAME 111 DOCKET NUMBER (2l LER NUMSER LSI PAGE 131 P re SEOVENT/AL ALYrerON NVMSER NVMSTA Washington Nuclear Plant - Unit 2 0 s 0 0 o 3 9 8 7 0 2 4 0 0 O6 oFO TEXT /// more 3/roce II /e//kre/L rree ~ /c/ 'orre/HRC Forrrr 3//SA3/11TI The NSLC system is used to control and direct main steam valve leakage through the SGT system under post accident conditions when the MSIVs are closed and core damage is present. Failure of a single NSLC valve would not jeopordize this function since the system is redundant and can draw off leakage either between or outboard of the redundant MSIVs. (I/ISLC-V-lA through 10, MSLC-V-2A through 20, and MSLC-V-3A through 30 are all part of the inboard-draws off leakage between the inboard and outboard MSIVs-system.)
Similarly, the failure of main steam supply to auxilaries valve (an NSLC outboard boundary valve) NS-V-146 to close would .not disable the NSLC system.
Again, because of MSLC redundancy, a failure of NS-V-146 would not jeopordize NSLC operation since the NSLC could be aligned the Inboard System which draws off leakage between the NSIVs.
The Residual Heat Removal System Valve RHR-V-6A is a crosstie isolation valve used to isolate the RHR Loop A Pump (RHR-P-lA) suction from the Shutdown Cooling Suction Line. The Safety function direction of RHR-V-6A is the open direction. In the event RHR-V-6A failed to open, only the RHR Loop A Shutdown Cooling mode of operation would be affected, and RHR Loop A Shutdown Cooling is backed by the redundant RHR Loop 8 Shutdown Cooling. Only one RHR Shutdown Cooling Loop is requi red to remove core decay heat following a'lant Shutdown.
Further, during non-accident conditions RHR-V-6A is accessible and could he opened manually, and, if neither RHR Shutdown Cooling Loop is available Alternative Shutdown Cooling which provides an alternate flow path would be available. Therefore, the failure of this valve would not cause unacceptable adverse consequences because of system redundancy, component accessibility, and/or alternate availability.
Auxilary Steam System Valves AS-V-68A and B'are Isolation valves for the Auxilary Steamline which is routed through the Reactor Building. These valves are designed to close to isolate a high energy break in the Auxilary steamline in the Reactor Building. Since these are redundant, 'in series, valves a double failure is highly unlikely the missing jumpers in AS-NO-68A and B is not a significant degradation of safety. A .break in these lines has no direct affect on reactor operation, since the Auxilary Steam is supplied from an oil fired steam boiler.
There are two independent Standby Gas Treatment (SGT) Divisions and only one Division is required to operate to meet plant safety requirements. In addition, each Division has a primary fan and a backup fan capable of meeting the Division requirements. SGT-V-3A1 and 3B2 are inlet valves to the backup fans of each SGT Division. These valve are required to open'only if the primary SGT fan in the, Division does not successfully start. The inlet valves for the primary fans had the proper torque switch bypass circuits installed.
Even in the event of a primary valve or fan failure only one of these valves would need to successfully open to meet safety requirements. Therefore there are no unacceptable adverse consequences because multiple failures would have
'to occur before the operability .of this system would be challenged.
NIIC FORM 3eeA e U.S GPO.1988 0.82A 838/ASS 19431
U.S. NUCLEAR REOULATORY COMMISSION NRC FormD08A (943 I LICENSEE EVENT REPORT (L'ERI TEXT CONTINUATION APPROVED OMS NO. 3(50-010e EXPIRES: 8/31/88 FACILITY NAME (11 DOCKET NUMSER (21 LER NUMSER (Sl PACE (31 SSOUENTIAL N~ei REVISION NUMOSR NVMSTR Washington Nuclear Plant TEXT /// more g>>ce ifroeoier/
oeo adWa'oval //RC Ferne 3(E(l'e/
Unit (I1l 2 o << o o 3 9 7 8 7 0 2 00 07 OF 0 7 No safety significance is associated with FPC-V-149 since the correct torque switch bypass=circuit was installed. The only problem associated with this valve is it was not included on the original Safeguard Service Valve Motor list.
The Service Water Valve SW-V-90 opens to allow cooling water to the the Diesel Generator (DG) Building Corridor Heating and Ventilation System. SW-V-90 is powered from Division 2 and if it fails to operate is backed by two exhaust fans powered from Division l. These fans will automatically actuate and mai ntain the DG Building corridor within design limits. Therefore, even in the unlikely event of the failure of this valve plant safety is not significantly reduced.
This event posed no threat to the health and safety of the public or Plant personnel.
Similar Events None EIIS Information Text Reference EIIS Reference System , Component Residual Heat Removal (RHR) System BO RHR-V-6A BO ISV RHR-MO-6A BO MO RHR-P-lA I30 P Essential Service Water (SW) System BI SW-V-.90 BI V 9<-MO-90 BI MO Main Steam Leakage Control (MSLC) System SB V SB'S-V-146 MSLC-V-1A-1D, 2A-20 and 3A-30 SB FCV MSLC-M0-1A-10, 2A-2D and 3A-3D SB MO Standby Gas Treatment (SGT) System BH SGT-V-3A1/3B2 BH Fuel Pool Cooling (FPC) System DA FPC-V-149 DA Auxiliary Steam (AS) System AS-V-68A/B ISV AS-MO-68A/B MO NRC fORM SOOA oU.S.OPO:1985 0.824 538/OSS (9431
WASHINGTON.PUBLIC POWER SUPPLY SYSVEM P.O. Box 968 ~ 3000 George Washington Way ~ Richland, Washington 99352 Docket No. 50-397 August 21, 1987 Document Control Desk U.S. Nuclear Regulatory Commission Washington, D.C. 20555 Subiect: NUCLEAR PLANT NO. 2 LICENSEE EVENT REPORT NO.87-024
Dear Sir:
Transmitted herewith is Licensee Event Report No.87-024 for the WNP-2 Plant.
This report is submitted in response to the report requirements of 10CFR50.73 and discusses the items of reportability, corrective action taken, and action taken to preclude recurrence.
Very truly yours, C.M. owers (M/D 927M}
WNP-2 Plant Manager CMP:ac
Enclosure:
L'icensee Event Report No.87-024 cc: Mr. John B. Martin, NRC - Region V Mr. R. T. Dodds, NRC Site (M/D 901A)
INPO Records Center - Atlanta, GA Ms. Dottie Sherman, ANI Mr. D. L. Williams, BPA (M/D 399)