ML17277B593

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Application for Amend to License NPF-21,consisting of Change to License Condition 16 Incorporating Requirements of Reg Guide 1.97,Rev 2 for Flux Monitoring Following First Refueling Outage.Fee Paid
ML17277B593
Person / Time
Site: Columbia Energy Northwest icon.png
Issue date: 01/11/1985
From: Sorensen G
WASHINGTON PUBLIC POWER SUPPLY SYSTEM
To: Schwencer A
Office of Nuclear Reactor Regulation
References
RTR-REGGD-01.097, RTR-REGGD-1.097 GO2-85-014, GO2-85-14, TAC-57169, NUDOCS 8501240197
Download: ML17277B593 (6)


Text

REGULATORY INFORMATION DISTRIBUTION TEM (RIDS)

ACCESSION NBR:8501240197 DOC ~ DATE>> 85/01/11 NOTARIZED: NO DOCKET" 0 FACIL:50 397 BYNAME WPPSS Nuclear Pl oject~ Uni t 2'~ Washington Public- Power 05000397 AUTH AUTHOR AFFILIATION SORENSENiG>>CD Washington Public Power Supply System RECIP ~ NAME RECIPIENT AFFILIATION SCHWENCERgA ~ Licensing Branch 2

SUBJECT:

Application for amend to License NPF-21iconsisting of ch'ange to License Condition 16 incorporating requirements of Reg Guide 1,97iRev 2 for flux monitoring following. first>

refueling outage'ee paid, DISTRIBUTION CODE: A003D COPIES'ECEIVED:LTR ENCL o SIZE'>> -'

TITLE:- OR/Licensing Submittal: Suppl 1 to NUREG-0737(Gener ic Ltr~ 82"33)

NOTES! 05000397 OL: 12/20/83 REC IP IENT COPIES RECIPIENT COPIES ID CODE/NAME- LTTR ENCL ID CODE/NAME LTTR ENCL" NRR LB2 BC INTERNAL>> ADM/LFMB 1 IE/DEPER/EPB NRR" PAULSONgW 1 NRR/DHFS/HFEB NRR/DHFS/PSRB 1. NRR/DL/ORAB NRR/DL'/ORB5 5 NRR/DS I/CPB NRR/DSI/I CSB 1 NRR/DS I/METB RR AB 1, NRR/DSI/RSB RE FILE 1 RGN5.

SS/EPRPB 1 EXTERNAL: LPDR NRC PDR NSIC TOTAL NUMBER OF COPIES REQUIRED: LTTR 35 ENCL~

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Washington Public Power Supply System P.O. Box 968 3000 George Washington Way Richland, Washington 99352 (509) 372-5000

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'"'ocket No. 50-397 Director of Nuclear Reactor Regulation Attention: Mr. A. Schwencer, Chief Licensing Branch No. 2 Division of Licensing U.S. Nuclear Regulatory Commission Washington, D.C. 20555

Dear Mr. Schwencer:

Subject:

NUCLEAR PLANT NO. 2 OPERATING LICENSE NPF-21, REQUEST FOR AMENDMENT TO LICENSE CONDITION 16, ATTACHMENT 2, ITEM 3(b)

Reference:

Letter, G02-83-693, G. C. Sorensen (SS) to A.

Schwencer (NRC), "Source Range Monitor Qualifi-cation Re: Regulatory Guide 1.97", dated August 3, 1983 abilityy The subject license condition requires the Supply System to implement (installation or upgrade) requirements of Regulatory Guide 1.97, Rev.

2 for flux monitoring prior to March 31, 1985. As indicated in the reference letter, due to the Source Range Monitor (SRM) vendor's in-

.to completely environmentally qualify this equipment on a generic basis, the Supply System advised the NRC of our intention to replace the existing SRM's prior to startup following the first re-fueling outage. The purpose of this letter is to request an amendment incorporating such a change.

Accordingly, in accordance with 10 CFR Parts 50.90 and 2. 101, the Supply System hereby requests the subject license condition be amended as follows:

(b) "The Licensee shall implement'(installation or upgrade) requirements of Regulatory Guide 1.97, Rev. 2 for flux monitoring prior to startup following the first refueling outage."

This change is being requested in order to allow the Supply System to complete.our evaluation of the available alternatives, and to subse-quently install the equipment that will provide the greatest assurance of continued safe operation of our plant on the most cost effective basis.

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A. Schwencer Page Two REQUEST fOR AMENDMENT TO LICENSE CONDITION 16, ATTACHMENT 2, ITEM 3(b)

The Supply System has reviewed the requested amendment per 10 CFR 50.59 and 50.92 and has determined that no unreviewed safety question or no significant hazard will result. Further, the proposed change will not:

1) Involve a significant increase in the probability or consequences of an accident previously evaluated; or
2) Create the possibility of a new or different kind of accident from an accident previously evaluated; or
3) Involve a significant reduction in a margin of safety.

The significant hazards evaluation took into consideration the fact that under normal operating conditions the environmental qualification of the SRM's is not in question. The plant has a full range of flux monitoring capability with four (4) redundant channels. In the unlikely event of an accident condition prior to replacement, there are additional systems in place that would provide the Operations staff with sufficient data to assess reactor conditions (e.g., control rod position monitors, reactor vessel level and pressure monitors, etc.).

The Supply System has evaluated this request in accordance with the criteria in 10 GFR 170.21, and has included a warrant for one hundred fifty dollars

($ 150.00} as initial payment for this application for amendment under Facility Category A (Power, Reactors).

In accordance with 10 CFR 50.91, the State of Washington has been provided a copy of this letter.

Should you have any questions in this matter, please contact Mr. P. L.

Powell, Manager, WNP,-2'Licensing. As you are aware, prompt attention to this amendment is necessary; continued operation of WNP-2 requires approval of this amendment no later than March 31, 1985.

Very truly yours, G. C. Sorensen, Manager Regulatory Programs HLA/tmh cc: R Auluck - NRC WS Chin - BPA

-"EFSEC ewis JB Martin - NRC RV AD Toth - NRC Site

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