ML17229A407
| ML17229A407 | |
| Person / Time | |
|---|---|
| Site: | Saint Lucie |
| Issue date: | 07/14/1997 |
| From: | NRC OFFICE OF INSPECTION & ENFORCEMENT (IE REGION II) |
| To: | |
| Shared Package | |
| ML17229A405 | List: |
| References | |
| 50-335-97-05, 50-335-97-5, 50-389-97-05, 50-389-97-5, NUDOCS 9707220384 | |
| Download: ML17229A407 (64) | |
See also: IR 05000335/1997005
Text
U.S.
NUCLEAR REGULATORY COMMISSION
REGION II
Docket Nos: 50-335,
50-389
License
Nos:
Report
Nos: 50-335/97-05,
50-389/97-05
Licensee:
Power
& Light Co.
Facility:
St. Lucie Nuclear Plant, Units
1
& 2
Location:
6351 South
Ocean Drive
Jensen
Beach,
FL
34957
Dates:
May 11 - June
14,
1997
4
Inspectors:
M. Miller, Senior Resident
Inspector
J.
Munday, Resident
Inspector
D. Lanyi, Resident
Inspector
M. Thomas,
Regional
Inspector
(paragraphs
08.1,
and
E8.1)
K. O'Donohue,
Resident
Inspector,
Vogtle (paragraphs
M1.4, and Ml.5)
P.
VanDoorn, Senior Resident
Inspector,
Watts Barr
(paragraphs
01.1, 02.4,
and Ml.l)
Approved by:
K. Landis, Chief. Reactor
Projects
Branch
3
Division of Reactor
Projects
<<.~
vvovaaoaae
sv'ov'xe
ADQCK OS000335
8
EXECUTIVE SUHMARY
St. Lucie Nuclear Plant, Units
1
8
2
NRC Inspection Report 50-335/97-05.
50-389/97-05
This integrated
inspection included aspects
of licensee operations,
engineer-
ing, maintenance,
and plant support.
The, report covers
a 5-week period of
resident inspection:
in addition, it includes inspections
performed by a
region-based
engineering
inspector
and two objectivity inspections
performed
by Resident
Inspectors
from other sites.
~oenati ons
~
The inspector witnessed
an Assistant Nuclear Plant Super visor stop all
Unit 2 operations activities when the pace of activities and span of
control
was judged to be inadequate.
The inspector considered this
briefing to be
a proactive step toward safely reaching
Hode 4 conditions
(paragraph 01.2).
~
The licensee
performed appropriate actions
and controls to enter
a
reduced inventory condition.
Crew sensitivity to the evolution was good
(par agraph 02.1).
Unit 2 containment closeout inspections
were detailed in their scope.
Only minor deficiencies
were noted
(paragraph
02.2).
On June 2-3,
a walkdown of both trains of the Unit 2 HPSI system
was
performed.
Some minor deficiencies
not affecting operability were noted
and referred to the licensee
(paragraph 2.3).
Discrepancies
between operators'nowledge
of appropriate Auxiliary
Pump oil levels. indicated
poor field practices to assure that
the correct oil levels were maintained
(paragraph
02.4).
,
Engineered
safeguards
testing
was completed satisfactorily and satisfied
'Technical Specification requirements.
In performing the test at the end
of the outage,
the licensee
was able to establish
an excellent level of
confidence in equipment
readiness
prior to the upcoming fuel cycle.
The
performance of testing
one train at
a time was considered
a significant
safety enhancement
to the test methodology
(paragraph 02.5).
The licensee's
implementation of the Foreign Haterial Exclusion program
at the entrance to the Unit 2 containment
as the unit approached
post-
outage startup
was insufficient to satisfy procedural
requi rements.
A
violation for failing to follow the governing procedure.was
identified
,
(paragraph
03.1) .
A number of. control .room instrument
problems were identified to be
a
.
weakness
in operator attention to the main control panels.
The
acceptance
of broken instrumentation
on the main control panels
by the
operato'rs.
particular ly f'ollowing a refueling- outage,
indicated
a
willingness to accept
inadequate
equipment
performance
(paragraph
04. 1).
~
Company. Nuclear Review Board activities remained
focused towards nuclear
safety.
The board effectively carried out thei r charter,
and members
displayed
a very good questioning attitude
(paragraph
08.5).
Maintenance
Personnel
were found to perform well and carefully followed procedures
in four monitored maintenance activities.
However.
one example of poor
planning
and poor procedural
guidance
was noted for post maintenance
testing of the
1C AFW trip and throttle valve.
(paragraph Ml.l)
The overall preparation
and conduct of modifications to SDC valve disks
was good.
The PC/H package
was prepared appropriately
and conduct of
the work was good.
(paragraph
M1.2)
Digital Data Processing
Unit constants
were found to have been
changed
per
a Work Order involving many particularly complicated steps involving
complex operations without an appropriate
level of detail provided in
the governing
Work Order.
This represented
a failure to comply with the
licensee's
procedure for the preparation of Work Orders
and was cited as
a violation (paragraph
M1.3).
Observations of work being performed
on the
Pump
was, in general,
performed adequately.
Procedural
per formance
was
acceptable
and calibrated
equipment
was
up to date.
All activities were
performed in a professional
and competent
manner.
In particular,
technicians
exhibited good working practices
by using additional
references
for setpoint verification and walking down procedures prior
to performance
(paragraph
H1.5).
Observations of work being conducted
on the 28 Hain Steam Isolation
Valve indicated satisfactory
maintenance
practices
(paragraph
H4.1).
The inspector
concluded that although the governing procedure
required
several
revisions during its'erformance,
Gas Vent
System flowpath testing
was performed satisfactorily.
The requi red
Technical Specification
was satisfied
(paragraph
H4.2)..
En ineerin
The inspector
reviewed several specific Engineering evaluations of
physical plant problems during the outage.
In all cases,
the reviews
were well prepared.
The staff adhered to all applicable codes.
and the
decision processes
were well documented.
(paragraph
E2. 1)
The licensee
has taken appropriate actions to determine the significance
and effect of the non-qualified Crosby relief valves
on the units
(paragraph
E2.2).
A discrepancy
was identified in the Unit 2 Digital Data Processing
System calorimetric program during power ascension
testing.
Although
the original modification package failed to proper ly identify cpmponents
0
requiring revision, the post-modification
VIIV adequately
encompassed
the
system
such that the error
was properly identiAed (paragraph
E2.3).
~
Digital Data Processing
System inaccuracies
leading to steady state
power levels in excess of licensed
1'imits were the result of a fai lure
on the part of the licensee to properly employ software controls in
1994.
The inspectors
found that the licensee's
root cause effort was.
in general.
comprehensive
and that the licensee
had properly assessed
the safety significance ef the event;
however,
two weaknesses
involving
failures to establish
root causes
were identified (paragraph
E8.2).
Plant
Su
ort
~
The training to allow the
SNPOs to up relieve as Are brigade team
leader
was adequate to meet all regulatory requirements.
The brigade
leader training was comparable to that which the
NWEs receive..
(paragraph
F5.1)
Summar
of Plant Status
Re ort Details
Unit 1 entered the period at full power and remained there'ntil
June
12 when
power was reduced to approximately,95
percent
due to a dropped control element
assembly.
The assembly
was recovered
and the unit returned to full power that
afternoon.
Unit 2 completed the refueling outage during this report period.
A reactor
startup
was
commenced
at 3:00 a.m.,
on May 24,
and went critical at 6:35 a.m.
later that morning.
Following low power physics testing,
power was increased
and
Mode
1 was entered
at 10:42 a.m.,
on May 25.
The main generator
was
synchronized to the grid at 7:34 p.m. later that day.
Full power was achieved
on May 29.
The unit remained at essentially full power the remainder of the
period with one exception.
On May 6, the unit reduced
power to approximately
90 percent
due to turbine control problems.
The unit returned to full power
the next day.
I. 0 erations
01
Conduct of Operations
01. 1
General
Comments
71707
Using inspection procedure
71707, the inspector
observed
Operations
activities.
This included Control
Room activities. three shift
turnoyers,
two special briefings, non-licensed
operator activities
associated
with testing of the Auxiliary'eedwater
System
(AFW), and
Operator logging.
The inspector also observed
a morning status
meeting,
a Plan of the
Day meeting,
and
a Weekly Plant Indicators
management
meeting.
In addition. plant tours of safety related equipment were
conducted.
In general.
the conduct of operations
was professional
and
safety-conscious;
specific events
and noteworthy observations
are
detailed in the sections
below.
Operators'ontrol
Room conduct
was generally good with good attention
to control boards
and good communications
noted.
Turnovers
and
briefings were thorough.-
Management
meetings
were generally thorough,
however, the inspector noted that the Weekly Plant Indicators contained
examples of errors, out-of-date information,
and misunderstood
information.
Two examples of poor logging were noted.
One was
an entry
at 8:20 a.m.
on June 3,
1997 which failed to identify which AFW flow
loop was being calibrated.
An entry at 2:05 p.m.
on June 3,
1997 failed
to identify that alarms that had been received
had immediately cleared.
One example
of. poor field performance
was noted
as described in Section
02.4.
01.2
Control
Room Observations
Dur in
Star tu
71707
On one occasion just prior to entering
Mode 4 conditions
on Unit 2. the
inspector noted that the ANPS stopped all Operations-related
work to
discuss
the on-going activities and refocus attention
as necessary.
An
extremely large amount of work was taking place simultaneously.
The
stated in the brief that although
no mistakes
had yet occurred,
the pace
that had been established left Operations
vulnerable.
The thrust of the
meeting was to better
coordinate the work to avoid making mistakes.
The
NPS discussed
the work to be completed,
the number of. operators
available.
and the priorities of the work to be completed.
Resources
were reallocated
as necessary
following that meeting.
The inspector
considered this briefing:to be
a proactive step toward safely reaching
Node 4 conditions
and indicated
an excellent safety ethic on the part of
the ANPS.
02
Operational
Status of Facilities
and Equipment
02.1
Unit 2 Nidloo
0 er ations
71707
a.
Inspection
Scope
On Hay 12, the inspectors
performed
a pre-midloop inspection of'nit 2
in accordance
with Region II Office Instruction 2216.
b.
Observations
and Findings
On Nay 12, the licensee
enter ed
a reduced
RCS inventory condition to
remove
SG nozzle
dams
and to replace
an
RCP seal.
Prior to reducing the
reactor
vessel
inventory to midloop conditions, the inspectors verified
the following:
Two independent
level instruments
were available with indication
in the main control
byroom.
The calibration of the vessel
level
instrumentation
was verified to have been current.
Tygon tubing
was installed
as the second level instrument.
The inspector
walked the run of tubing and verified it was not kinked or looped
and .was properly vented.
A remote
camera
and monitor were
installed to allow viewing of the tube from the control
room.
The manw'ay on top of the pressurizer
was verified to have been
open providing a vent
path.'wo
were verified to be available
on both
SPDS channels.
Instructions were'ssued'o
ensure that containment closure could
be accomplished if necessary.
Crews were tested to ensure that
the containment
could be closed within 30 minutes.
The inspector
reviewed the penetrations
that were to remain open at the time of
drain down and .verified that closure capability existed.
~
Both HPSI
pumps were available for inventory addition.
Also. both
trains of Shutdown Cooling
(SDC) were in operation.
Two Intake
Cooling Water
(ICW) pumps were operable
as required by Appendix A
of Operating
Procedure
NOP 2-0410022,
Revision 24,
"Shutdown
02.2
02.3
Cooling."
The 2A ICW pump was running and the 28
ICW pump breaker
was racked in and the
pump ready to be started if required.
~
Operations
did not plan to release
any electrical
busses
or
alternate
power sources for work while the unit was in reduced
inventory.
~
When the
RCS level reduction
was initiated. the licensee
invoked
additional operational
controls to ensure .there would be no level
perturbations.
Maintenance
was not allowed to perform any work
that could affect
RCS level or
SDC.
Conclusions
The licensee
performed appropriate actions
and controls to enter
a
reduced inventory condition.
Crew sensitivity to the evolution was
good.
Containment
Closeout
71707
On May 19, the, inspectors
accompanied
Quality Control
(QC) inspectors
on
an initial cleanliness
closeout of the Unit 2 containment building.
The
purpose of the inspection
was to ensur e that no foreign material
remained within containment.
The inspectors
divided into two groups.
The first group started their
inspection
on the lowest level of containment.
The other group started
their inspection at the containment
dome.
Overall the quality of the
containment
cleanup activities was adequate.
The inspectors
found many
minor deficiencies throughout containment.
For example, plastic bags
were found fallen next to the main steam piping.
A wrench was found
near the
foundation.
Multiple examples of plastic and
miscellaneous
trash were discovered
throughout containment.
The
inspectors
were thorough in their observations.
The containment inspections
were detailed in their scope.
Only minor
deficiencies
were noted.
Unit 2 Hi h Pressure
Safet
In 'ection
S stem Walkdowns
71707
On June 2-3,
a walkdown of both trains of the Unit 2 HPSI system
was
performed.
The inspection consisted of a'and
over hand walkdown of the
primary flow path of piping within the reactor auxiliary building as
well as
a walkdown of the main control
room panels.
The inspector
utilized the system operating procedure
as well as
P8ID 2998-8-078.
Sheet
130A.
The inspector also verified that the HPSI supply valves
from the
RWT were open.
There were some minor deficiencies not-
affecting operability noted
and referred to the licensee.
The overall condition of the system equipment
was good.
The inspector
noted that proper equipment oil levels were being maintained,
area
housekeeping
was acceptable
and no system leakage
was observed.,
In
02.4
02.5
addition,
as
a part of this inspection effort, the inspector
reviewed
portions of the Unit 2 Updated Final Safety Analysis Report
(UFSAR)
related to the HPSI system.
No discrepancies
associated
with the
were noted.
Low Oil Level in AFW Turbine
71707
During a plant tour. the inspector noted that bearing oil level for the
AFW pump
1C turbine was approximately
1 1/4-inches
below a mark on the
gauge glass casing.
This
mark was difficult to see
and the inspector
noted that the corresponding
gauge glass
for. the
2C AFW pump had two
marks which had been
enhanced with pencil to make these
more visible.
The vendor information stated
"Note filling marks
on the gauge glasses.
The oil level should not be allowed to drop below this level."
The inspector
questioned
two non-licensed
operators
regarding the proper
oil level
on
AFW pump
1C.
One was not sure
and the other stated that
about half way on the gauge glass
was acceptable.
The mark was at about
the two thirds height on the gauge glass.
The oil height was required
to assure
a slinger ring extends into the oil bath to provide oil to the
bearings
upon an initial pump start.
An oil pump was provided to supply
oil to the bearings
subsequent
to the initial start, therefore, this is
a long term bearing wear issue rather
than
a
pump operability issue.
Nevertheless,
this was considered
an example of poor field practices to
assure
desired oil level was maintained in the
AFW pump.
Periodic Test of the
En ineered Safet
Features
61726
Inspection
Scope
On Hay 18. the licensee
performed Engineered
Safety Features
(ESF)
testing in accordance with Procedure
OP 2-0400050,
Revision 23,
"Periodic Test of the Engineered
Safety Features."
The inspector
witnessed the pre-job brief and portions of'he performance of this
test.
Observations
and Findings
l
\\
The inspector attended
the pre-job.brief for this. surveillance
and noted
that it was attended
by all the test participants
and several
members of
licensee
management.
Following the brief, the plant was aligned to
support the test
and the participants
were individually briefed on the
specific tasks
each
was to perform;
The inspector witnessed the
performance of Sections
8.4 (A Train Loss of Offsite Power with
Integrated
Safeguards
(SIAS, CIAS, and
CSAS) Actuation Test with the
2AB
Buses Aligned to the A Side Electrical). 8.5
(2A.EDG 453
kW Load
Rejection
and SIAS/LOOP Swing Bus Testing with,.2AB Buses Aligned to A
Side Electrical);,and portions of 8.6 (Manual
A Train SIAS/CIAS/CSAS
Pushbutton 'Actuation Verification).
No abnormalities
were noted during
performance of these sections.
All systems
and components
responded
as
expected.
The inspector noted good communication
and coordination
among
the test participants.
03
03.1
This was
a reperformance of the failed April 15 surveillance.
Two
outstanding
issues
remain to be resolved.
During the April 15
surveillance,
the 2A1 Safety Injection Tank (SIT) Isolation valve failed
to open
on
a Safety Injection signal.
Engineering
has
been unable to
determine the cause of the failure.
The valve is only requi red to be
able to open if shut while in Mode 4.
The licensee
has revised its
operating
procedures
to open the
2A1 SIT isolation valve prior to
entering
Mode 5 while shutting
down and prior to exiting Mode 5 during
startup.
Engineering is:conducting further investigations to determine
the cause of the failure.
Another failure during the April 15 test involved the
2A Low Pressure
Safety Injection (LPSI)
Pump.
The pump started
as expected.
but then
tripped nine seconds later on thermal overload.
No mechanical
or
electrical
cause
was found.
The licensee
sent the motor to the vendor
for an evaluation,
but no cause
could be substantially
determined.
The inspector
found that the conduct of this surveillance at the end of
the outage (rather than at the beginning
as
had previously been the
practice)
met
TS surveillance
requirements.
The inspector further found
that the timing of the test
(immediately prior to post-outage
startup)
rovided an excellent opportunity to assess
the operational
readiness
of
ey safety systems
and components.
Additionally, the inspector
found
the licensee's
practice of performing this test one train at
a time
(rather than simultaneously
as
had been past practice)
enhanced
the
safety posture of the unit while the test
was being conducted.
As
performance of the test required creating losses of offsite power, the
single train methodology employed by the licensee
ensured that one train
of shutdown cooling was always operating.
Conclusions
This complicated surveillance
was completed satisfactorily and satisfied
Technical Specification requirements.
In performing the test at the end
of the outage.
the licensee
was able to establish
an excellent level of
confidence in equipment
readiness
prior to the upcoming fuel cycle.
The
performance of testing
one train at
a time was considered
a significant
safety enhancement
to the test methodology.
Operations
Procedures
and Documentation
Forei
n Material Exclusion
Control of the Unit 2 Containment
Bui ldin
71707
a.
Inspection
Scope
The inspector
reviewed the
FHE controls associated
with control of
material
being used inside the Unit 2 containment building during the
refueling outage after the containment closeout
was complete.
This
inspection consisted of a review of'he
FHE log. discussions
with FHE
monitors,
and Quality Instruction QI 13-PR/PSL-2,
Revision 29,
"Housekeeping
and Cleanliness
Control Methods."
Observations
and Findings
At the end of the Unit 2 refueling outage,
the containment bui'lding was
controlled
as
an
FME area.
On Nay 23,
1997. the inspector
reviewed the
- FME log book associated
with the containment building.
Inside the book
were instructions which stated that "With the exception of maintenance
personnel
working on the Reactor Drain Tank/Containment
Sump Project all
other personnel
shall complete the
FME log.
Health Physics personnel
(later changed to Security) shall
man the
FHE log desk
and ensure that
the log is completed for personnel
entering
and exiting the
RCB.
Maintenance
personnel
working on the Reactor Drain Tank/Containment
Project are not required to comply with the
FME log requi rements
since
a
FME walk down of the work area will be performed at the completion of
the project."
Also in the log book, were log sheets
indicating the
material that was taken into and out of containment.
On May 29, after the containment
was closed out and the
FME area
released,
the inspector
reviewed these
log sheets
and noted several
items that had not been
logged
as having been
removed from the
containment.
These items included;
paper,
safety belt, paperwork,
pen.
tape, bolts. radio with ear muffs," rubber suit, flashing light.
clearance
tags,
miscellaneous
hand tools, pipe wrench. five flashlights.
crescent
wrench,
one bottle of snoop.
and
a gauge.
In addition,
nineteen individuals signing in on the log failed to sign out upon
exiting.
The inspector
discussed
the instructions listed in the
FNE log with
various licensee
management
stating that these instructions did not
agree with the site procedure
for control of FHE.
The licensee stated
that it was not their intention to maintain the containment
as
an
FHE
area
as defined in the.QI.
Their philosophy was that after the sump
work was complete the entire area would be inspected
and any remaining
items would then
be removed.
Therefore it was not necessary
to log all
items entering into this particular
area.
However, they did require
that personnel
not working on the sump job complete the
FNE log.
The
inspector noted that the entrance to the containment
was identified as
an
FNE area,
that an
FHE log was established
to control material
entering
and exiting the area,
and that an
FHE monitor was established.
Procedure
QI 13-PR/PSL-2,
Section 5.5. stated,
in part, that foi Quality
Group
B systems
and components, "if an
FNE Control. Area is required.
the
control area
and controls-shall
be established.prio'r
to opening the
system or component.
FME controls in accordance
with this procedure
'hall
be established,
as -needed,'o
maintain the cleanliness
requirements.-
Appendix
B provides guidance
on the methods of
controlling foreign. material."
Section 7.6, "Definitions,." states that
Quality Group
B applies to the containment vessel.
Appendix 8 of this
QI states
in part that
"FHE control areas.
as defined by QI 13-PR/PSL-2,
are used in those situations
where it is not feasible/practical
to
install
an
FHE control device to prevent loss of foreign material into a
system/component.
Tools/materials
which are taken into FME control
7
areas
are logged for accountability."
In addition, Section 5.15,
"General
Housekeeping,"
step 11.A, states that,
"Material accountability
shall
be applied when misplaced tools equipment,
and other materials
could be detrimental to the plant item involved.
When material
accountability is applied. tools and other materials shall
be logged
into and out of the area."
The inspector
reviewed the site procedures f'r guidance
on when
a
FHE
monitor was required and:what training was required prior to assuming
that position.
QI 13-PR/PSL-2 stated that
FHE monitors
may be used at
the discretion of the Plant Management,
to control the area
around the
reactor cavity when the reactor vessel
head
was
removed
and in the fuel
handling building when work was taking place around the spent fuel pool.
With regard to training, Appendix A. step
1, states that the reactor
cavity monitor should receive orientation
as to the refueling process,
and this QI.
The QI made
no mention
concerning
FME monitors for other areas
or
any associated
training.
10 CFR 50, Appendix B, Criterion
V requires that activities affecting
quality shall
be prescribed
by documented
procedures
of a type
appropriate to the circumstances
and shall
be accomplished
in accordance
with these
procedure.
Procedure
QI 13-PR/PSL-2 is the procedure that
implements this requirement
with regard to foreign material control.
Failure to adequately control the material entering
and exiting the Unit
2 containment is
a violation of this procedure
and is identified as
50-389/97-05-01.
"Failure to Control Foreign Material Entering and
Exiting the Unit 2 Containment.."
Conclusions
The inspector concluded that the licensee's
implementation of the
program at the entrance to the Unit 2 containment
as the unit approached
.post-outage
startup
was insufficient to satisfy procedural
requirements.
A violation for failing to follow the governing procedure
was
identified.
04.1
Operator
Knowledge 'and Performance
Monitorin of Control
Room Instrumentation
71707
Inspection
Scope
The inspector walked down the Unit 2 control. room instrumentation to
verify proper operation
and to verify operator
awareness
of those
instruments
not functioning properly.
't
Observations.
and Findings
'I
On Hay 24, the inspector walked down the control panels in the main
control
room paying particular attention to instrumentation that
appeared to be indicating erroneous
values or operating incorrectly.
During the outage
many of these
instruments
had been out of service for
maintenance.
At this time the plant was in the process of being aligned
for startup.
The inspector
noted three flow recorders
not indicating
roper values
and three recorders that were not inking as indicated
elow:
~
FR 3323
- HPSI Loop 2A2 8 2A1 flow indicating 90 gpm with the
system out of service.
~
FR 3306 - Shutdown Cooling 2A Loop flow indicating 500
gpm with
the system out of service.
~
FR 3301 - Shutdown Cooling 2B Loop flow indicating 1000
gpm with
the system out of ser vice.
The recorder
was also not inking.
~
PR-07-4B/5B - Containment
and
Sump pressure
had one of two pens
not inking.
~
LR 12-11B - Condensate
Storage
Tank level was not inking
The inspector
questioned
the operators
because
none of these
instruments
had work requests
(WRs) written to have them repaired.
The inspector
requested
that the chart paper
be unrolled to determine
how long these
conditions existed.
It was noted that in all cases
the conditions
had
existed for at least two days without any action having been taken by
Operations.
WRs were written for the instruments with erroneous
indications.
The operator
on shift adjusted the recorders
not inking
until they inked properly.
On June 3, the inspector
again walked down
the control panels
and noted two additional recorders
not inking as
indicated below:
~
LR-12-11B - Condensate
Storage
Tank level again not inking
~
PR-08-1/2 - 2A and
2B SG Outlet/Turbine Inlet pressure
had only
one of three
pens inking.
Again. the inspector
noted that .these, problems .had been. occurri.ng for at
least two days without action being taken.
This was brought to the
attention of the control
room staff and licensee
management.
1
The inspector
reviewed Procedure
OP-2-.0010125,
Revision 10,
"Schedule
Of
Periodic Tests,
Checks
and Calibrations,"
and noted that step
21
required that control
room chart recorders
be checked
each midnight
shift for, proper timing ..and to verify the chart paper
was not low.
In
addition, the step required that the recorders
be stamped.
Although the
procedure
does not explicitly state that the recorders
are-to
be
verified to be operating properly, a'discussion
with several
operators
indicated that was the intent.-
After this was brought to the attention of management,
the instruments
were promptly repaired.
08
08.1
Conclusions
The inspector
considered
the large number of instrument
problems
identified to be
a weakness
in operator attention to the main control
panels.
The 'acceptance
of broken instrumentation
on the main control
panels
by the operators,
particularly following a refueling outage,
indicates
a willingness to accept
inadequate
equipment
performance.
Hiscellaneous
OperationsIssues
Closed
VIO 50-335 389/96-01-01
"Tem orar
Chan
es to Procedures
Im ro erl
Chan
ed Intent of Procedures"
92901
Inspection
Scope
This violation (VIO) involved a failure of the licensee's
Facility
Review Group
(FRG) and the Plant General
Hanager
(PGH) to review and
approve temporary changes
(TCs) to procedures,
which involved a change
of intent, prior to implementation.
This inspection effort focused
on
the licensee's
corrective actions specified in the response to this VIO
and review of other related documentation.
Observations
and Findings
The inspector
reviewed the corrective actions specified in the
licensee's
response to this VIO for compliance with the Technical
Specifications
(TS) and applicable licensee
procedures.
The inspector
reviewed the
FRG meeting minutes for the TCs listed in the subject
and verified that the TCs had been
reviewed by the
FRG and approved
by
the
PGH.
The inspector also reviewed Administrative Pro'cedure
(ADH)
ADH-11.03, Revision 0,
"Temporary Changes to Procedures."
This
procedure
had been previously issued
as Administrative Procedure
0010148.
Procedure
ADH-11.03 had been revised to provide additional
guidelines
regarding what TCs to procedures
could be considered
as
changing the intent of a procedure.,
In addition, the procedure
had been
revised to include expanded
change of intent guidelines
and prior
approval
requirements
for TCs. .If a..TC was determined..to
involve a
change of intent.,to
a procedure the,.change
was..then
required to,be
processed
as
a normal procedure
change
request rather than
a TC.
The inspector
reviewed
some
TCs which had been
implemented in 1997 in
order to verify that the TCs had been -implemented in accordance
with
Procedure
ADH-11.03..
During review of these
TCs, the inspector
did not
identify any examples
where the
TC involved a change of intent to the
applicable procedure.
During further review of these
TCs. the inspector
made the following observations
which indicated that additional
clarifications to Procedure
ADH-11.03 may be warranted.
~
During review of TC 1-97-044, the inspector noted that the author
of the
TC performed the 50.59 screening
as the qualified reviewer
and also signed
as the first member of the plant management staff
to indicate one of the two approvals
required for the TC.,
4
10
Procedure
ADM-11.03 stated that the
TC author
was responsible for
obtaining the review and signature
approval of the
TC from two
members of the plant management staff prior to implementation.
Although Procedure
ADM-11.03 does not specifically prohibit the
author from performing the 50.59 screening
and also being one of
the two approvers of a TC, the inspector questioned
whether this
TC met the intent of Procedure
ADM-11.03 with regard to
incorporating adequate
independence
in the review process relative
to this TC.
The inspector also questioned
the licensee's
definition for
a
"member of plant management staff" with regard to employees
who
could approve
TCs.
Procedure
ADM-11.03 defined
a member of plant
management staff as
a permanent
Florida Power and Light Company
(FPL) employee
who was functioning at the Plant St. Lucie (PSL)
site in a supervisory capacity.
Examples given in Procedure
ADM-
11.03 for
FPL employees
meeting this definition were
foreman/reactor
control operator
(RCO) and above for bargaining
unit employees,
and senior plant technician
and above for non-
bargaining unit employees.
The inspector
noted that
some of these
examples
given in Procedure
ADM-11.03 were not consistent with the
licensee's
organizational
chart with regard to employees
functioning in a supervisory capacity.
For
example,
the author of
TC 1-97-044
was
a system engineer.
As stated
above, this system
engineer
also signed
as the first member of plant management staff
to indicate one of the
TC approvals.
However, this system
engineer
was not listed in a designated
supervisory position on
the licensee's
organizational
chart.
The inspector also questioned
whether
adequate training had been
provided to all the employees
(included under the licensee's
examples
as
members of plant management staff) with regard to the
review and approval of TCs.
The inspector noted that there were
training requirements
specified for the qualified reviewer and the
- second
member of the plant management staff'ho could approve
a
was required to hold a Senior Reactor, Operator 's
(SRO) license
on
the unit-affected.
There were no specific training requirements
for the first member of the plant management staff who could
approve
a.TC.
During review of TC 1-97-053, the inspector
noted that the
TC was
approved
by only one member from the plant management staff
instead of two members,
as required by, Procedure
ADM 11.03 and the
TS for both units.
During further'review
and discussion of this
TC with licensee
personnel,
the inspector
noted that the licensee
had identified this issue prior to this inspection
and
had issued
- condition report
(CR) 97-1060:,
The inspector further noted during
review of-a licensee .Quality Assurance
(QA)- Audit Report
(QSL-DOC-
97-04), that
QA had identified two TCs that contained 'only the
signature of the nuclear plait supervisor
(NPS) indicating plant
'anagement
staff approval.
V
C'
~
During review of TC 1-97-054, the inspector noted that an
individual other than the
TC author
completed Part A of the
Temporary
Change Checklist (Appendix
B of Procedure
ADM-11.03).
Step
6. 1. 1.B of Procedure
ADM-11.03 and Part
A of the Temporary
Change Checklist both stated that Part A was to be completed
by
the
TC Author.
The inspector noted that these steps
were
inconsistent with Step 3.4.2 which stated that the
TC Author or
person
assigned
the responsibility for the TC complete Part A of
the Temporary
Change Checklist.
~
The inspector noted several
examples
where the TC request
form
indicated that
a procedure
on the other unit was affected by the
TC.
There did not appear to be
a clear tracking mechanism to
ensure that the procedure
on the other was changed.
The inspector
discussed this item with licensee
personnel
who indicated that the
document proofreading guidelines provided another
opportunity to
remind personnel
to address
the affected procedures
on the other
unit.
The inspector discussed
these observations
with licensee
management
who
indicated that Procedure
ADM-11.03 would be reviewed to determine if any
additional
changes
or clarifications were needed.
The inspector stated
that licensee
actions to address
the above observations
regarding the
process will be tracked
as Inspector Followup Item (IFI) 50-335.389/97-
05-02,
"Licensee
Review and Clarification of Procedure
(ADM-11.03) for
Performing Temporary Changes to Procedures."
Violation 50-335,389/96-
01-01 will be closed.
c.
Conclusions
The inspector concluded that the licensee
had taken adequate
cor rective
actions to address
VIO 50-335,389/96-01-01.
This VIO will be closed.
The inspector
concluded
from the review of some
TCs which had been
implemented in 1997 that additional clarifications to Procedure
ADM-
11.03, with regard to implementation of the
TC process,
may be
warranted.
A new inspector
followup item was identified to review the
licensee's
actions to address
the inspector's
observations
with regard
to the clarification of Procedure
ADM-11.03.
08.2
Closed
LER 50-335/95-003
"Automatic Reactor
Tri
Durin
Turbine.
.
Overs
eed Surveillance Testin
Due to Personnel
Error"
92901
On July 8.
1995, a'eactor trip occurred
due to high pressurizer
pressure
when
a valving error
occurred during main turbine overspeed
testing.
The procedure
being used,
OP 2-0030150.
"Secondary Plant
Operating
Checks
and Tests,"
required that the Overspeed
Protection
Control
(OPC) solenoid valve be isolated from the test header by-closing
a manual
valve.
The non-licensed
operator
removed the, locking device
from,-the valve, but got-distracted,
and failed to close it:
Subsequently,
the governor
and intercept valves closed which ultimately
resulted in the reactor trip.
08.3
12
Corrective actions for this event included counselling the involved
individual, revising the procedure to include additional verification
for critical steps.
reviewing the event with other operators
during
formal training,
and reviewing other load threatening surveillances to
ensure
adequate
precautions to prevent personnel
error are present.
The
inspector
reviewed the current revision of the aforementioned
procedure,
Revision 85,
and noted that the appropriate
revisions
had been
made.
Additionally, other portions of the procedure
were also reviewed
and
were also noted to have been revised to add additional verifications to
critical steps.
This
LER is closed.
Closed
LER 50-335/95-009
"Missed Technical
S ecification Scheduled
Surveillance
Oue to Personnel
Error"
92901
This surveillance
was missed
on October
20,
1995,
when the licensed
operator initialed the Technical Specification tracking sheet prior to
performing the required surveillance.
The surveillance
was
a
verification of Control Element Assembly
(CEA) position indication by
comparing the reed switch position indication and pulse counting
position indication.
A form,
known as the
CEA log. listed each
CEA and
provided two blanks to record the position from the two aforementioned
methods.
Upon completion of the
CEA log, the operator
then was to
initial the check sheet signifying the surveillance
was completed.
On
this date,
the check sheet
was initialed but the
CEA log sheet
was not
completed.
Corrective actions included performing the surveillance,
counselling the
involved individual. issuing
a
memo to operators reiterating plant
policy regarding
documentation of work activities,
and referencing the
CEA log sheet in the surveillance
check sheet.
Since this event
occurred,
the surveillance
check sheet
procedure
has
changed.
The check
sheet is currently
a section of Procedure
OP 2-0010125.
Revision 9,
"Schedule of Periodic Tests,
Checks,
and Calibrations."
The inspector
reviewed this procedure
and verified that the
CEA log was referenced in
this procedure.
'This
LER is closed.
Closed
LER 50-389/97-001
"Containment Isolation Actuation Due to
Increased
Radiation Levels Ourin
Removal of U
er
Guide Structure"
.
~92901
The details of this event were previously discussed
in Inspection Report
97-04.
The inspector
has since reviewed the
LER and verified the
corrective actions were appropriate.
Com an
Nuclear
Review Board
CNRB
71707
The inspector
attended
a portion of CNRB meeting
No. 443 held at St.
Lucie on.May 20.
-The inspector verified that the meeting
was conducted
in accordance with Technical Specification 6.5.2.
Generally, the
CNRB
meets monthly, rotating the location of the meeting
among the three
sites (e.g.,
Turkey Point. St. Lucie
and Juno Beach).
Representatives
from all three locations are present at each meeting.
'3
The inspector noted that the St. Lucie Plant Manager's
report was very
informative and it sparked
a good exchange of questions
and
a healthy
discussion.
The inspector also noted that the
CNRB addressed
self-
assessment
issues
and held
a discussion of early warning indicators in
order to identify degrading
performance.
The inspector
concluded that
the
CNRB remained
focused towards nuclear
safety, effectively carried,
out their charter,
and that members displayed
a very good questioning
attitude.
II. Maintenance
Hl
Conduct of Maintenance
Ml.1
General
Comments
61726 62707
a.
Inspection
Scope
Using inspection procedures
61726 and 62707, the inspector
obser ved
portions of the f'ollowing activities:
~
Work Order
(WO) 97005642-01,
Calibration of AFW Flow Loop FT-09-
2Al:
Procedure
2-1400064F,
Revision 38, "Installed Plant
Instrument Calibration (Flow)."
Note:
Personnel
identified a
leak in the equalization valve and. therefore.
were unable to
complete the calibration.
~
18 Month Preventive
Maintenance
Inspection of Valve
HV-09-11 (1C AFW Pump to 1A Steam Generator);
Procedure
940072.
Revision 14, "Preventive Maintenance of Environmentally Qualified
Limitorque Motor Operated
Valve Actuators."
~
WO 3200, Torque Switch Preventive
Maintenance for Valve HV-09-11;
Procedure
80.01, .Revision 0, "Limitorque Model SHB-000 Torque
Switch Preventive Maintenance."
~
18 Month Preventive
Maintenance
Inspection of
Valve HV-08-3 (1C AFW Trip and Throttle Valve): 'rocedure
0940069,
Revision
18, "Preventive Maintenance of Non-
Environmentally Qualified Limitorque Motor Operated
Valve
Actuators."
The inspector also observed portions of post maintenance testing of
valves associated
with the
1C AFW pump.
b.
Observations
and Findings
Personnel
were knowledgeable
and performed in accordance
with procedural
requirements.
Good material
support
and management
oversight
was noted.
A thorough inspection of wiring on Valve MV-08-3 identified wiring
damage which was carefully repaired.
Also, wiring was rebundled to ease
installation of the limit switch cover.
One example of poor work
planning was noted.
Valve MV-08-3 was initially stroke time tempted
Hl.2
a.
'4
resulting in also running the
1C AFW pump.
Subsequently,
maintenance
personnel
informed Operations that the valve operation
had to be
verified at all remote locations in accordance with a general
step in
the procedure.
Operations
was not aware of the requirement
and an
additional
unnecessary
pump run resulted.
Also, no specific procedural
steps
were provided for the testing.
Operators
had to energize the
remote shutdown panel
using
a Deviation Log.
Licensee Administrative
Procedure
0010120.
Revision 91,
"Conduct of Operations."
does allow
routine tasks to be performed without specific procedures.
however. this
testing could have been conducted better if'ore specific guidance
had
been provided.
In addition, preplanning activities such
as the pre-
evolution briefing failed to identify the testing requirement.
The
licensee
indicated that
a post briefing had identified similar
weaknesses'onclusions
Personnel*performed
well and carefully followed procedures.
However,
one example of poor planning
and poor procedural
guidance
was noted for
post maintenance testing of the
1C AFW trip and throttle valve.
Pressure
Lockin
Hodifications to Unit 2 Shutdown Coolin
Isolation
Valves
62707
37551
Inspection
Scope
The inspector
reviewed the plant modification package.
PC/H 96138.
"Drilling of Valve Disk for V3651,
V3652,
and V3480," and observed
some
of the maintenance activity associated
with the modification.
Obser vations
and Findings
This Plant Change/Hodification
(PC/H) package provided for the
modification of Unit 2 SDC isolation valves
V3651,
V3652,
and V3480
located in containment
on the hot leg suction lines to the
2A and 28
LPSI pumps.
The licensee's
intent was to satisfy commitments associated
with Generic Letter 95-07,
"Pressure
Locking and Thermal Binding of
Safety-Related
Power-Operated
Gate Valves."
The modification consisted
of drilling a 3/16 inch hole in'the upstream
(reactor coolant) side of
the valve disk to vent the bonnet of high pressure fluid.
This would
revent the conditions that allow pressure
locking to occur.
The
icensee
previously performed this modification on another Unit 2 valve,
and this modification was endorsed
in NUREG-1275,
Volume 9,
"Operating
Experience
Feedback
Report
- Pressure
Locking and Thermal Binding of
Gate Valves."
The inspector
reviewed the
PC/H package
and noted that it was clearly
written, the 50.59 screening
was appropriately performed.
and all
reviews
and approvals
were timely.
The individuals performing the
approvals
and reviews were appropriate.
The package
clear ly'dentified
the. work instructions
and al.l post-modification testing required.
I
'5
The work was performed after all fuel had been
removed from the reactor
vessel.
Freeze
seals
were installed to isolate the hot leg piping to
allow draining.
The inspector observed portions of valve V3480
disassembly,
and valve V3652 reassembly.
Maintenance
personnel
were
knowledgeable
about the job, appropriate
reference material
was at the
job site,
QC oversight
was appropriate,
and all Measuring
and Test
Equipment
was properly checked out and calibrated.
Two problems occurred during reassembly of the first valve worked, valve
V3480.
When the crew initially was installing the valve yoke, they
determined that the stem was rotated
180 degrees
from the requi red
position.
Although the valve was symmetrically similar, it was not
exact.
Inattention to detail
by the maintenance
crew allowed them to
install the stem backwards.
The valve was disassembled
again.
verified that the gasket,
valve seat,
and valve body were not damaged.
The valve was subsequently
reassembled.
The second
problem occurred during the retorquing of the bonnet.
After
satisfactorily completing the final torque sequence.
the licensee
performed the required post-work calibration check of'he wrench.
The
calibration check
was unsatisfactory.
Condition Report 97-0918
was
issued to document the deficiency and the bonnet
was later retorqued
satisfactorily.
The inspector
judged the overall quality of the maintenance
work to be
good.
The maintenance
workers were familiar with the work procedures.
Reference material
was in the work area.
Radiological control practices
were noted to be good.
Quality Control verifications were performed
as
required,
and problems were raised to the appropriate levels of
management.
Conclusions
The inspector
judged the overall preparation
and conduct of the
modification to the
SDC valve disks to be good.
The
PC/M package
was
prepared appropriately
and conduct of the work was good.
Installation of Unit 1'DDPS Constants
62703
92902
Inspection
Scope
The inspector
reviewed
WO 97004867 which documented the revision of
(FW) flow constants
in DDPS,
This activity occurred in
February.
1997.
In addition, the inspector
reviewed ADM-0010432,
Revision 11, "Control of Plant Work Orders" to determine if the
WO was
in compliance with the controlling administrative procedure.
Observations
and Findings
The. purpose of WO 97004867,
as stated in the package,
was to allow
testing of the
DDPS to verify calorimetric equation for FW flow, and
', 16
verify inputs
as necessary.
The work instructions contained the
following steps:
"1)
At System Supervisor discretion obtain clearance
or permission to
lift/land leads
8 manipulate local valves
and document the
Independent Verification sheets of ADH-0010432 (Fig. g4).
2)
Hook up test equipment
as determined
necessary
by supervisor to
allow measurement
of FW flow inputs
and verify calorimetric
equation for FW flow.
Perform tests
as determined
by supervisor.
3)
Hake adjustments if necessary
at discretion of, supervisor.
4)
Remove all test equipment
when work complete.
5)
If required troubleshoot/repair
associated
loop components
as
directed
by supervisor
using manufacture
tech manuals
as
references,
as necessary.
6)
Document all work performed
and parts replaced
on the journeymans
work report."
The
WO basically relied on the super visor to determine the actions
necessary
to complete the objective of the
WO.
ADH-0010432, Revision,
ll, "Control of Plant Work Orders" step 7.1. 1 stated,
in part, that
plant work activities which can affect the performance of guality
Related
systems,
components.
structures,
and equipment shall
be
appropriately planned
and performed in accordance
with written
procedures,
documented
instructions
and approved
drawings to ensure the
equipment
meets its design function.
In addition, step 7.3.2.D states,
in part, that "if a work task is particularly complicated,
involved many
steps to complete,
involves complex operations
which must be completed
in. a specific order, or has other, demanding
requirements (i.e.,
beyond
the skill of the craft). then sufficient details to accomplish the task
must be provided in NPWO."
The planner
may use any of the following:
~
Plant procedures
(specific sections
or the entire procedure)
~
Maintenance Guidelines
.
~
Reuse Specifications
~
Specific step-by-step
work instructions
~
Technical
Manual step-by-step
work instructions
I
0
Conclusions
17
M1.4
M1.5
The inspector concluded that completion of this
WO involved many
particu1ar ly complicated
steps involving complex operations with a
Ouality Related
component without providing one of the approved
methods
as delineated
in ADM-0010432.
10 CFR 50 Appendix
B Criterion V.
requi res, in part, that activities affecting quality shall
be prescribed
by documented instructions,
procedures,
or drawings. of a type
appropriate to the ci rcumstances
and shall
be accomplished
in accordance
with these instructions,
processes.
or drawings.
ADM-0010432, is the
licensee
procedure that implements this requirement
with regard to
maintenance
planning.
Failure to provide adequate
work instructions for
the performance of WO 97004867 is
a violation of this procedure
and was
identified as
VIO 50-335/97-05-03,
"Failure to Provide Adequate
Work
Instructions
For a Work Order."
62707
Inspection
Scope
. The inspector
observed portions of perf'ormance of Operating
Procedure
OP-2-0010125A,
Revision ll, "Surveillance Data Sheet
24 Valve Testing
Procedures."
Observations
and Findings
On May 20, the inspector
observed the valve stroking of Unit 2 vacuum
relief valves
FCV-25-7 and FCV-25-8.
The procedure
steps
required
coordination
between operations
and instrumentation
and control
personnel
and included independent verification.
The personnel
performing the procedure
were knowledgeable
and familiar with the
required steps.
It was noted that although the terminals to be jumpered
for each valve were distinctly identified. the operator further verified
the listed terminals using the control wiring. diagram number 529.
Conclusions
The inspector concluded that referencing the control wiring diagram was
a good practice.
The independent verification steps
were performed
correctly and Data Sheet
24 performance
was acceptable.
1
Auxiliar
Ter r
Turbine Post Maintenance Activities
62707
Inspection
Scope
The inspector
observed
several
post maintenance activities on 2C
Auxiliary Feedwater Turbine.
The placement
and removal of clearance
number
2-97-05 was observed
as well as performance of the following
procedures:
~
.
2-0700028.
Revision 7, "Auxiliary Feedwater Turbine Mechanical
And
Electrical Trip Tests"
0
18
~
2-M-0109, Revision 7,
"2C Auxiliary Feedwater Terry Turbine
Disassembly,
Inspection,
and Reassembly"
~
2-0700050,
Revision 4, "Auxiliary Feedpump Periodic Tests"
~
2-IMP-0901, Revision 3,
"2C Auxiliary Feedwater.
Pump Governor Oil
Change Instruction"
The
WOs reviewed f'r completeness
and applicability included:
~
Pump Overspeed
Task"
~
"Turbine Drive for Auxiliary Feedwater
Pump 2C"
~
WO post-maintenance
test for 97002292,
"Repack Valve V9103"
b.
Observations
And Findings
On May 21,
1997, the inspector observed
several
post-maintenance
activities on the
Pump.
The electrical trip test
was performed while the
pump was uncoupled
from the turbine and
completed without complications.
As part of the test.
the mechanical
~
trip set point is raised to a value greater
than the electrical trip
setpoint to ensure the
pump trips on the electrical
and not the
mechanical trip. It was noted that the Instrumentation
and Control
(18C) technicians
used additional
references
along with the test
procedure to verify the mechanical trip setpoint
was correct when the
tripset point was returned to normal status.
After the electrical trip test,
maintenance
personnel
coupled the
pump
to the turbine by replacing the spool piece per
2-M-0109.
To allow the
spool piece replacement.
operations
personnel
placed clearance
2-97-05.
The clearance
was placed,
the independent verification was performed.
and
a third managerial
verification was completed prior to the spool
piece replacement.
The pump spool piece
was verified to be correctly
positioned using the match marks
and the alignment
was completed without
incident.
When removing clearance
2-97-05. the trip and throttle valve
control switch was to be returned to the locked open position.
However,
the valve was not latched correctly;.therefore,
when the control switch
was placed in the open position the valve indication was intermediate
rather than open.
A nuclear plant operator relatched-the
valve and the
remainder of the clearance
was
removed without incident.
After being coupled,
2C feedwater
pump was rolled in preparation for the
governor oil replacement activity.
The inspector noted that the pre-job
brief was very detailed.
While waiting for the
pump to be rolled. the
inspector
observed
an. IKC technician; walking through the governor oil
replacement
procedure prior to performance to ensure familiarity with
the procedure.
While. the
pump was,being rolled, the post maintenance
test for valve V9103 was completed
by the nuclear plant operator.
4
Conclusions
'9
4
M4
M4. 1
The inspector
concluded that, in general,
the activities were performed
adequately.
The procedure
performance
was acceptable
and the calibrated
equipment
was
up to date.
All activities were performed in a
professional
and competent
manner.
In particular, the
18C technicians
exhibited good working practices
by using additional
references
for
setpoint verification and walking down procedures
prior to performance.
Maintenance Staff Knowledge and Performance
Unit 2 Main Steam Isolation Valve Maintenance
62707
Inspection
Scope
The inspector witnessed portions of the maintenance activities
associated
with the Unit 2 MSIV, HCV-08-1B.
The work was being
performed in accordance with WO 95035292.
Observations
and Findings
Throughout the refueling outage the inspectors
witnessed portions of the
maintenance activities associated
with the rebuild of the 08-1B MSIV.
On May 15. the inspector witnessed the valve bonnet bolts being torqued.
The
WO required several
passes
of increasing torque until
a final value
of 3300 ft-lbs was obtained.
Maintenance
was using
a hydraulic torque
wrench to tighten the nuts which was attached
by hoses to an oil sump.
The torque value applied to the nuts
was increased
as the operating oil
pressure
being supplied to the wrench was increased.
A gauge
was
mounted
on the oil sump to indicate the operating oil pressure.
The
inspector
reviewed the
WO and noted that, although the bonnet nuts were
still being tightened,
the final torquing step
was already signed
by
personnel
from both the licensee
and the valve contractor.
The
inspector questioned the
QC individual working for the contr.actor and
was told that after the nuts were torqued to the final value of 3300 ft-
lbs, the wrench being used
was checked for calibration.
During
calibration. the contractor
QC individual noted that the operating oil
ressure,
indicated
on the gauge,
was not equal to the torque value
eing applied by the wrench. i.e.,
an indication of 100 psi operating
oil pressure
did not equal
100 ft-lbs of torque supplied
by the wrench.
However. this had been his understanding
up to that point, which
resulted in the bonnet nuts being undertorqued.
Upon discovery..the
bonnet nuts were torqued to the proper value and verified by both
contractor
and licensee
QC inspectors.
The inspector obtained the names.
through tool usage logs, of other
individuals who had used this type of tool to determine if this
misconception
was generic in nature.
Three people were interviewed and
all had
a complete understanding of the difference between operating oil
pressure
and applied torque.
In addition. the problem was discussed
with the
QC supervisor
and the
QA manager.
The licensee
questioned all
personnel
who had used these tools and confirmed that no
'0
misunderstanding
existed with regard to this problem.
In addition, the
inspector verified that the "Restricted
use" sticker was affixed to the
tool being used
on the job site and that it had the proper conversions
between operating oil pressure
and applied torque.
Conclusions
The inspector concluded that although there
was confusion about
how to
determine proper torque values with the hydraulic wrench. the nuts were
not overtorqued,
the problem was identified by the maintenance
process
as intended,
and the proper torque was later applied to the bonnet nuts.
Licensee
and inspector review determined that this was
an isolated
problem associated
with this job only.
Post Maintenance Testin
of the Reactor Coolant
Gas Vent
S stem
RCGVS
~62707
Inspection
Scope
The inspector
witnessed portions of the performance of Procedure
2-OSP-
01.02,
Revision 2,
"Reactor
Coolant
Gas Pent
System Flow Path
Verification." and reviewed the entire procedure
upon completion.
Observations
and Findings
On May 15. the inspector witnessed portions of the performance of
Operations Surveillance
Procedure
2-0SP-01.02,
Revision 2, "Reactor
Coolant
Gas Vent System Flow Path Verification."
This procedure
verifies that the
RCGVS is free of obstructions
by flushing water
through the pipin'g.
This. system
was to be flushed in three sections.
The inspector verified that the flowpath and overlap of'ach section
was
adequate to ensure the entire system
had been flushed.
The
instrumentation
used
was adequate for the various attributes
needing
verification.
In addition, the inspector
noted that personnel
safety
was maintained during the evolution.
The procedure
required several
revisions during the process
but each time work was stopped until the
revisions were completed.
Conclusions
The inspector
concluded that although it required several
revisions
during its performance,
the procedure
was proper ly performed.
The
requi red Technical Specification
was satisfied.
E2
E2.1
'1
III. En ineerin
Engineering Support of Facilities and Equipment
En ineerin
Su
ort of Facilities and
E ui ment
37551
Inspection
Scope
The inspector
reviewed three separate
Engineering
issues that occurred
during the Unit 2 outage.
First. several
Hotor Operated
Valve (HOV)
torque switches
could not be properly set.
Second.
an In Service
Inspection (ISI) program inspection identified unacceptable
indications
in Safety Injection (SI) piping.
Third, Ultrasonic Testing
(UT) of Hain
Steam
(HS) piping indicated that the wall thickness of the pipe would
not be greater than the minimum wall thickness at the end of the next
cycle.
The inspector
reviewed the evaluations,
and calculations.
Observations
and Findings
Dur'ing the Unit 2 outage,
the licensee identified that the torque
switches for the Pressure
Operated Relief Valve (PORV) block valves
and
the
HS Isolation Bypass
Valves were not functioning properly.
Condition
Reports were written on both problems.
Condition Report 97-1034
documented
the
PORY problem and
CR 97-1021
documented the
HS isolation
discrepancy.
The
PORV block valves are three inch gate valves with SB-00 actuators.
Electrical Haintenance
was unable to set torque switches
to meet the
Engineering specified torque values.
They were able to set the open
torque switch such that valve thrust at the torque switch trip was
greater than the minimum required valve thrust.
However. the corrected
maximum allowable total thrust and the corrected
maximum thrust at the
torque switch trip was exceeded
for the opening stroke.
Engineering determined that the
PORV block valves were acceptable for
use
as left.
The Engineering specified torque values
were too
conservative.
The inspector
reviewed the disposition
and determined
that the assumptions
and calculations
were appropriate.
The
HS bypass
valves are three inch globe valves with SB-00 actuators.
The
1B valve did not produce sufficient thrust to open the valve under
the design basis pressure differential.'Replacing the valve yoke did
not improve the valve's performance.
The lA valve worked properly until
heated,
at which point, the unit also could not produce sufficient
thrust.
The Engineering evaluation for the
HS bypass
valves did not
accept the valves
as left.
These valves are required to shut
on a
containment isolation signal.
However, the licensee
could not show that
these
valves could perform their function under all circumstances.
The
valves were deenergized
shut before restarting the unit pending further
disposition.
'2
Routine ISI of the 2Al SI Tank piping detected the presence of surface
discontinuities in the austenitic stainless
steel
pipe.
The flaw size
was in excess of that allowed in the class
2, six inch, schedule
160
piping.
American Society of Mechanical
Engineers
Boiler and Pressure
Vessel
Code
(ASHE) Section
XI required that unacceptable
flaws be
removed
or reduced to an acceptable
size.
The flaws. were chased
through the final area resulting in a wall thickness
reduction of 0.2
inches.
Engineering determined that the depth,
wandering,
and branching
of the flaw were indicative of Chloride Stress
Corrosion Cracking.
No
internal pipe degradation
was noted.
IWC 2430 also required
an increased
scope of the
inspection to include an additional
number of components within the same
examination category,
approximately equal to the number of components
examined initially.
The licensee
examined four more areas
and
determined that three of the areas
were acceptable.
The fourth area
was
ground out and blended
as allowed by Section XI.
The inspector verified
that the dispositions
agreed with the
ASME code.
The corrective actions
were appropriate,
and the documentation
was adequate.
On May 5, routine
UT of the
HS piping revealed that an area
near the
2D
Moisture Separator
Reheater
(MSR) had
a wall thickness
below the
screening
thickness for that grade pipe.
The pipe supplied main steam
flow to the
HSR reheater
bundle.
This non-safety related
system pipe
was standard wall constructed of American Society for Testing
and
Materials
(ASTH) A106 GR
B material.
The wall thinning was general
in
nature,
indicating flow accelerated
corrosion.
Engineering
performed
a minimum required wall thickness calculation for
the pipe per
ASHE Boiler and Pressure
Vessel
Code Case
N-480.
The
calculation indicated that the actual piping thickness
was greater than
the minimum requi red then,
but would be less than minimum before the
next outage.
The inspector verified that the Code case
was properly
used
and implemented,
and determined that the conclusion
was sound.
Engineering
performed
a localized wall reduction calculation to further
refine the immediacy of the replacement of the piping.
They determined
that,
for the small area in question, waiting until the next outage to
replace the section of piping was acceptable.
The inspector
reviewed
the calculations
and assumptions
and concluded that they were in
accordance
with the applicable
ASME code.
PNAI 97-05-160
was generated
to track replacement of the pipe during the next short notice outage of
sufficient. duration -and conditions.-
c.
Conclusions
The inspector
reviewed several
specific cases of Engineering's
evaluations of physical plant problems during the outage.
In all cases,
the reviews were well prepared.
The staff adhered to all applicable
codes,
and the decision processes
were well documented.
E2.2
" 23
En ineer in
Su
ort of Crosb
Relief Valve Re lacement
37551
Inspection
Scope
In August 1995,
Crosby Valve and
Gage
Company informed the licensee that
they had identified blowdown concerns
on twenty-three. relief valves sold
to St. Lucie.
Crosby stated that these
valves
had either variations in
blowdown setpoints
and/or the setpoints
were not confirmed
by
operational testing.
The licensee initiated
a St. Lucie Action Report.
STAR 1-951024
on August 31,
1995 to evaluate the issue.
Of the twenty-
three valves identified, the licensee
determined that ten were currently
installed in Unit 1 and none were installed in Unit 2.
Recently.
a
Condition Report
was issued
(CR 97-0514)
asser ting that one of these
valves should
have been replaced last Unit 1 outage,
but was not.
The
inspector.reyi.ewed,,the
facts behind the original
STAR and examined the
adequacy of Engineering's
management
of the issue.
Observations
and Findings
The final disposition of the
STAR was completed
on October 6,
1995.
It
individually evaluated
and accepted for use the ten installed valves.
The assessment
concluded that the relief valves would function as
designed
and tested with the cur rent blowdown values.
Safe
oper ation of
the plant during all operating conditions would not be affected,
and
variations
and lack of blowdown data were not considered
a substantial
safety hazard.
The STAR also
recommended that the valves should be
replaced at the ear liest opportunity once replacements
were available.
The STAR was assigned to Planning to replace
and/or retest these valves.
In March 1996, the
STAR process
was replaced
by the Condition Report
process.
The STAR was administratively closed
on March 30,
1996 and
PMAI PM96-03-733 was issued with Engineering
as the responsible
organization.
No action had been taken by Planning
due to outage
preparations
and limited resources.
Engineering did not immediately
pursue the
PMAI due to lack of time before the outage"(less
than one
month), other priorities related to the outage.
lack of certified
replacement
valves,
and lack of funding.
After the last Unit 1 outage,
Engineering coordinated with Juno
Beach
and 'Planning to respond to the PMAI.
Ten work requests
were initiated
to replace the installed Unit 1 valves.
Additionally. the licensee
addressed
the use of Crosby spares
programmatically
'by issuing Procedure
GMP-14; -"Inspection.and
Maintenance-of .Crosby Relief-Val-ves."
- This
procedure
ensured that actual
blowdown tests satisfy the design
requirements of the system.
This way,
.a non-qualified Crosby valve
could not be installed in either unit.
Since last August, the 'licensee
has
been actively working on replacing
'he
valves.
The licensee
has budgeted
funds for offsite blowdown
testing.
Installation of the qualified valves
has
been scheduled
for
the. upcoming Unit 1 fall outage.
Conclusions
'4
E2.3
The licensee
has taken appropriate
actions to determine the significance
and effect of the non-qualified Crosby valves
on the plants.
Furthermore,
the licensee's
decision to retest the affected valves
and
to replace
any as required is reasonable.
However, the licensee
exhibited poor project prioritization as evidenced
by the eight months
that the
STAR resided with Planning without any action taken to closeout
the item.
Unit 2
DDPS Software Revision Error
92903
Inspection
Scope
The inspector
reviewed documents
associated
with erroneous
computer data
which affected the reactor calorimetric calculations.
These
documents
included
CR 97-1185.
several
WOs,
and
PC/M 96147.
In addition, the
inspector attended
the
FRG meeting which discussed
the event
and actions
taken to resolve the condition.
Observations
and Findings
During the Unit 2 refueling outage,
both feedwater
flow venturis were
removed.
cleaned,
and recalibrated.
The recalibration resulted in the
need to change the span of the flow transmitters
from 0-800 inches water
to 0-900 inches water.
This, in turn, resulted in a revision to the
span of each feedwater flow input to the Digital Data Processing
System
(DDPS) flow calculation.
The
DDPS software was modified in accordance
with PC/M 96147
and
WO 970115831A.
During the startup following the refueling outage,
the licensee
performed
manual calorimetrics at various
power levels to ensure that
,they compared favorably with the
DDPS,
as part of the post modification
testing of'he
DDPS.
This verification and validation
(V8V) was being
performed
as part of the corrective action from an event
on Unit 1 in
which the
DDPS was discovered to contain erroneous
data
and resulted in
incorrect power indication.
This requirement
was tracked by Plant
Managers Action Item (PMAI) 97-03-055 with a requi red completion of
"prior to Unit 2 startup."
On May 26, the manual calorimetric indicated
a reactor
power level of
50.6 percent while the
DDPS indicated 47.7 percent.
The reactor
engineer
recalibrated the
RPS instrumentation to the higher,
more
conservative,
value.. At 80 percent
power, another
manual calorimetric
was performed which indicated
5 percent
higher
than the
DDPS.
The licensee's
investigation revealed that the discrepancy
was the
result of an incorrect instrument
span
from the feedwater flow
instrumentation
which input to the, calorimetric performed by the
DDPS.
Although the licensee
had modified the span of the feedwater flow
inputs. they had failed to identify that the feedwater flow averaging
circuit also required
a revision based
on the new span.
This resulted
'5
in the calculation performed by this circuit to be based
on
a span of
800 inches of water vs 900 which resulted in the observed error.
Once
identified, the licensee
changed the span in the feedwater flow
averaging circuit within DDPS in accordance
with WO 9701271901,
and
reperformed the manual calorimetric'with satisfactory results.
The inspector discussed
with the licensee
why the corrective actions
taken in response to the Unit 1
DDPS event,
discussed
in paragraph
E8.2
of this report
and in LER 50-335/97-002,
did not prevent this event from
occurring.
The licensee stated that the feedwater
flow averaging
ci rcuit is actually computer
code that can only be changed
by a
modification to the source
code.
It was not'
constant that could be
changed
due to,plant conditions.
The licensee stated that. while all
other constants
loaded into DDPS were verified to be correct, the code
was not.
Therefore, it was not considered to be included as part of the
corrective action for the Unit 1 events
The inspector
reviewed
PC/0 96147
and discussed
the methodology the
licensee
used in determining which DDPS components
needed modification.
The licensee stated that because
there
was
a recognized
lack of
expertise
on this system within FPL, vendor expertise
was solicited to
determine what
DDPS modifications were necessary
as
a result of the
feedwater flow transmitter
span change.
Neither the vendor
nor the
licensee identified that the feedwater
averaging circuit required
a span
change.
However, the licensee
had developed
a
VLV plan which would
encompass
the modifications being performed such that the system
as
a
whole would be tested prior to'being completely returned to service.
Although the averaging circuit was not identified during the design
and
implementation stage,
the licensee did identify the error during the
return to service test.
As part of the corrective action of this event, the licensee
reviewed
the
DDPS software to identify other incidents where similar problems
existed.
Two additional similar averaging circuits were identified. the
feedwater temperature
averaging circuit and the steam generator
A and
8
pressure
averaging circuit but were determined
not to contain errors.
In addition, the following is
a list,of corrective actions the licensee
is taking in response to this event.
PHAI
97-03-057
DUE DATE
Complete
~ DESCRIPTION
Develop operating procedures
for DDPS which
will identify all the points
and their
locations.
26
PMAI
97-03-279
97-03-61
97-03-273
97-03-274
97-03-278
97-03-055
97-03-056
97-03-059
.,97-03-060
97-03-058
97-03-275
97-03-276
DUE DATE
Complete
Complete
Complete
9/30/97
8/30/97
Complete
9/30/97
3/31/98
3/31/98
11/30/97
3/31/98
12/29/97
DESCRIPTION
Identify the responsibilities of the various
disciplines that are involved in work relating
to computer systems.
(AP 4000060,
Revision 3,
"Maintenance
Departmental
Control of Computer
Software,"
has
been issued but on hold pending
training.)
Perform point check
on all Unit 2 DDPS inputs.
(Unit 1 was
reviously checked.)
Revise
AP 4000060
and Nuclear Engineering
QI
3.7,
"Computer Software Control," to provide
ade uate
ost-maintenance
testing.
Revise existing
PCM process to include
ade uate
ost maintenance testing.
Create master
and backup copies of software
f'r the Unit 2 generator
temperature
monitoring computer,
M&TE calibration
computer,
and the radiation monitoring
corn uter.
Develop generic
V&V requirements to challenge
all critical attributes within both Unit 1 and
Unit 2
DDPS for all software changes.
Develop generic
V&V requirements to challenge
all critical attributes within both Unit 1 and
Unit 1
DDPS for all software changes.
Revise Unit 1
DDPS software to reflect the
correct calibration curve for the feedwater
tern erature
RTDs.
Revise Unit 1
DDPS software to reflect the
correct calibration curve for the Reactor-
Coolant
Pum
Watt Transducers.
Ensure configuration control for all
critical'nit
1 and Unit 2 DDPS constants
by entering
them into TEDB or ensuring they are documented
in a controlled
roc'edure.
Develop the baseline
V&V plan for the-battery
test data collection system.
METE calibration
system.
and Units
1 and
2 time response
systems.
Evaluate the need for a
V&V plan and develop
if required for Units
1 and 2 generator
temperature
monitoring system
and Units
1 and
2 se uence of events
recorders.
27
PMAI
DUE DATE
97-03-277
7/1/98
97-06-288
8/31/97
97-06-289
3/31/98
97-06-290
3/1/98
c.
Conclusions
DESCRIPTION
Evaluate the need for a
V8V plan and develop
if required for air condition unit maintenance
tracking system,
Units
1 and
2 DDPS,
and Units
1 and
2 turbine control systems.
Modify Units
1 and
2 DDPS
VBV test plans to
provide testing for each of the believable
value
rocessor
averaging/scaling
functions.
Evaluate the need for computer systems
software training and software
VSV training.
Ensure software control program improvements
implemented in response to PMAI 97-03-054
address
the lessons
learned
from this event
and from the Turkey Point eagle
21 software
V8V event.
E8
Although the original modification package failed to identify .all the
components
requiring revision, the post-modification
V8V adequately
encompassed
the system such that the error
was properly identified.
Miscellaneous
Engineering Issues
E8.1
Closed
URI 50-335/94-08-03
" ualit
Level of PORV and
SRV Dischar
e
Pi in "
92903
a.
Inspection
Scope
This item involved a concern regarding the licensee's clarification of
the safety classification of the pressurizer
PORV and safety relief
valves
(SRV) discharge piping.
The inspection effort focused
on the
licensee's
corrective actions to address this unresolved
item and the
review of other
r elated documentation.
b.
Observations
and Findings-
r
The inspector
reviewed the licensee's
actions for compl,iance with
applicable sections of the
UFSAR, TS,
and licensee
procedures.
The
inspector noted that the Unit 1 pressurizer
PORV and
SRV discharge
piping was designated
as quality group
D (non-safety related)
and non-
seismic by the licensee.
During the review of various design documents,
applicable
UFSAR sections,
and
FPL correspondence
to the
NRC, the
inspector
determined that, although the pressur.izer
PORV and
discharge piping was designated
as non-seismic,
the licensee
had
seismically analyzed the discharge piping and supports.
'The inspector
noted that analyses
performed
by the licensee
included the Unit 1
American National Standards
Institute (ANSI) 831. 1 Class
1 Stress
'8
. Analysis for the Pressurizer
Relief Valve Piping, Seismic Analysis
Performed
on Discharge Piping,
and the Seismic Anchor and Restraint
Movement Analysis.
Conclusions
The inspector
concluded
from review of the
UFSAR and applicable design
documents that the Unit 1 pressurizer
PORV and
SRV discharge piping was
designated
as quality group
D (non-safety related)
and non-seismic
by
the licensee.
The inspector further concluded that,
although the
pressurizer
PORV and
SRV discharge piping was designated
as non-seismic,
the licensee
had seismically analyzed the discharge piping and
associated
supports.
This URI,is closed.
EBS 2
Closed
URI 50-335/97-03-07
"Issues Relatin
to Exceedin
Unit 1
Licensed
Stead
State
Power Levels"
92903
This URI involved maintenance
and engineering
issues relating to Unit 1
exceeding the steady state licensed
power level of 100 percent
as
'eported
in IR 97-03.
Specifically, four issues
were identified and
included the following:
1.
Whether the licensee's
software
VSV processes
were adequate
and in
agreement with the licensee's
OA Plan.
2.
Whether the licensee's
OA Plan requi rements
were violated
regarding control of software
and manuals.
3.
Whether corrective actions to previous events
should have
prevented this event
and whether
data available to the licensee
should
have resulted in earlier detection of the condition.
4.
The extent to which licensed steady state
power limits for Unit 1
were exceeded
during the current Unit 1 fuel cycle.
With regard to items
1 and 2;
In June,
1994,
feedwater flow scaling
constants
were revised in accordance
with plant procedures
and were
subsequently
installed into the
DDPS.
However, the new constants
were
not added to the Master/Backup
copy of the software..
10 CFR 50 Appendix
B Criterion
V requi res, in part, that activities affecting quality shall
be prescribed
by documented instructions,
procedures,
or drawings of a
type appropriate to the circumstances
and shall
be accomplished
in
accordance
with these instructions,
procedures,
or drawings:
., Procedure
QI 2-PR/PSL-3,
Revision 0, "Control- of Computer Software,"
was
the'ocument
which implemented this requirement with respect to the control
of revisions to computer
software.
Step 5.5 of that procedure required that
a form similar to Appendix A
Form 2 of that procedure
be used to document revisions to software.
This form required information such
as the impact the change would have
on the plant, the documentation that needed revision, the installation
instructions,
contingency instructions,
a validation test plan
29
independent verifications,
and implementation sign-offs.
In addition,
step 5. 10.2 stated,
in part, that "computer software access
shall
be
controlled in order to ensure that only approved versions [of software]
are in use.
and modifications are authorized with written approval."
Step 5. 10.5 stated that
"measures
shall
be taken to 'ensure
superseded
or
invalid computer software is not available for use."
.
Contrary to the above,
these
steps
were not followed to control
and
document the revision to':the
FW flow constants
in the
DDPS.
As
a
result. the master/backup
copy of the software
was not revised which
ultimately resulted in the wrong revision being reinstalled
and used in
the
DDPS.
The licensee identified this problem while performing repai rs
on
flow transmitter
and corrected it the next day.
The inspector
found that this was not a violation that could reasonably
have been prevented
by the licensee's
corrective action for a previous
violation that occurred within the past two years.
Actions were taken
within ten minutes to alleviate the concern raised
by the problem and it
was corrected
by modification within twenty hours of discovery.
Further, it was not apparent that the failure to use the appropriate
procedure to document
and control the software revision was willful.
Therefore, this licensee identified and corrected violation is being
treated
as
a Non-Cited Violation, consistent with Section VII.B.1 of the
This issue wi 11
be treated
as non-cited
violation NCV 50-335/97-05-04,
"Failure to Use the Proper Procedure to
Document
and Control
DDPS Software Revisions."
The licensee's
investigation concluded with the same root cause
which was documented in
LER 50-335/97-002.
With respect to item 3, the inspector
reviewed
LER 50-335/86-005-00,
which related to a failure to proper ly reinitialize the Unit 2 DDPS
computer such that old incore detector sensitivities
were loaded (these
sensitivity values are periodically updated
by DDPS to account for
burnup of the rhodium detectors
which comprise the incore strings).
While the subject
LER did relate to the control of software,
the issue
did not relate di'rectly to the current issue in a way. that would
constitute
a prior opportunity to identify the current issue.
With respect to the fourth item, the inspector
reviewed the licensee's
root. cause evaluation for the subject event to verify the maximum power.
level reached
during the event.
The licensee initially estimated
l3DPS
calorimetric power to be indicating approximately
.63 percent. lower than
actual
power.
This estimate
was based
on the, mathematical
results of
comparing the as-found feedwater flow scaling constant to the correct
value for the constant.
In the course of the root- cause investigation,
the licensee identified two additional, conservative.. errors involving
instrument calibration which offset the initial estimate of maximum
power error.
The first error involved the selection of calibration curves for
temperature
RTDs.
The
RTDs sensing
temperature
were
comprised of two manufacturer
types;
Rosemount
and
WEED.
The l,icensee
J
30
found that the temperature
sensing circuits employing Rosemount
were calibrated using the generic
WEED RTD curves
used for the
WEED
RTOs.
The net effect was that the Rosemount
RTOs were reporting
temperature
approximately 1.5 degrees
too low.
When incorporated into
the calorimetric calculation, this tended to overestimate
power by
approximately
. 14 percent.
While the effect on the calorimetric
calculation
was conservative,
the inspector
found. through interviews
with personnel,
that this effect was fortuitous.
The licensee
had
issued
a
PHAI to address:this
issue (to correct the curve), but the
inspector
found that the licensee
had taken
no action to determine
how
the erroneous calibration curve had been applied.
The inspector
considered this
a weakness
in the licensee's
root cause effort.
The second error involved the scaling of RCP watt transducers.
The
transducers
were designed to provide
a milliampere
(mA) output
proportional to power input by the pumps.
The error resulted in a
1
mA
output equating to 8600
kW, versus
9600
kW, as designed.
When these
errors were factored into the calorimetric calculation,
the error tended
to overestimate
reactor
power by approximately
.06 percent.
As in the
case of the feedwater
RTOs, the inspector
found that, while the licensee
intended to correct the settings
associated
with this discrepancy,
the
licensee
had initiated no efforts to determine
how the error came to be
in the first place or to ensure that the proper level of controls
existed for this setpoint.
Upon discussing the issue with the licensee,
a
CR was generated to determine the cause for the transducer
setting
inaccuracy.
When the two errors described
above were factored in against the
estimated
.63 percent
nonconservative
error already identified, the
effect was to offset that. error.
The net result was
a .43 percent
nonconservative
power error in the
DDPS calorimetric calculation.
Consequently.
Unit
1 operated at approximately 100.43 percent of rated
thermal
power for those periods during the current fuel cycle when
indicated reactor
power was
100 percent.
Regarding safety significance,
the inspector noted that the safety
analysis for Unit 1 assumed initial power conditions of 102 percent for
.all pressure
related
(ONBR limiting) events.
The inspector discussed
the degree of known uncertainty in power measurement
with the licensee.
The maximum uncertainty
was determined to 1. 16 percent.
When the known
calorimetric error
was added to the known uncertainty figure, the. worst
case
power error total
was 1.59 percent,
which was within the 2 per cent
nonconservative
error assumption
made in the accident analysis.
The
inspector
concluded that the unit was not outside of'ts accident
analysis
as
a result of the "subject condition.
'.
Conclusions
The inspectors
concluded that the
DDPS inaccuracies
leading to steady
state
power levels in excess of licensed limits were the result of a
failure on the part of the licensee to properly employ software controls
in 1994.
The inspectors
found that the licensee's
root cause effort
i'-"4
E8.3
E8.4
S8
S8.1
'1
was, in general,
comprehensive
and that the licensee
had properly
assessed
the safety significance of the event;
however,
two weaknesses
involving failures to establish
root causes
were identified.
Closed
URI 50-335/97-03-05
"Failure to Obtain
FRG Review for Interim
CR Dis osition"
92903
The inspector
discussed this issue with the licensee,
who stated that
the "disposition" referenced
in this
URI was,
instead,
an "operability
determination,"
covered
by
a different portion of procedure
AP-0006130,
Revision 7, "Condition Reports,"
from that requi ring
a
FRG review.
The
inspector
reviewed the subject
CR, the licensee's
TQAR, and
NRC Generic Letter 91-18 (which discusses,
through attachments,
degraded
and
nonconforming conditions) in this light and found the licensee's
position acceptable.
The subject determination
was not
a disposition of
the condition at the time it was prepared,
a disposition
was being
prepared at the time in an expedited
fa'shion,
and corrective actions
were implemented promptly.
As the subject determination
was not
a
disposition to the condition, it did not require
a
FRG review.
This
item is closed.
Closed
URI 50-335/97-03-06
"Post Maintenance Testin
Issues
Associated with DDPS Constant
Chan es"
92903
This issue
r elated to a fai lure on the part of the licensee to perform
a
nuclear
and delta-T calibration of the NI system
as post-maintenance
testing following the installation of correct
flow spans into
DDPS.
The licensee stated that the purpose of post-maintenance
testing
was to ensure that the component
which had received maintenance
was in
proper working order following the maintenance.
The licensee
contended
that the appropriate
post-maintenance
test for DDPS feedwater flow span
changes
was
a manual calorimetric (which was, in fact, performed) which
would compare
DDPS on-line calorimetric output to the manual result.
The inspector
agreed that the manual calorimetric was the appropriate
post-maintenance
test for the subject work and that no violation
existed.
This item is closed..
IV. Plant
Su
ort
Hiscellaneous
Security and Safeguards
Issues
Closed
IFI 50-335 389/96-16-03
"Im lementation of Interim Plant
Actions to Detect
New Tam erin
"
92904
This item was identified to follow licensee's
interim actions to detect
new tampering following an event involving suspected
tampering of plant
equipment.
These interim actions
included daily plant inspections
by
system engineers,
managers,
and personnel
responsible for housekeeping
in certain locations, of specific areas
looking for evidence of
tampering.
In addition, Condition Reports
and Work Orders were reviewed
dai3y f'r conditions which could have resulted
from tampering.
Finally,
operational
checks of specific equipment
were performed to assure
proper
F5
F5.1
b.
'2
operation.
The inspectors
witnessed
many of these activities.
After a
discussion with NRC Regional
management,
the licensee discontinued
these
interim actions.
This IFI is closed.
Fire Protection Staff Training and Qualification
Fire Bri ade Leader
Chan
es
64704
Inspection
Scope
Due to the lack of licensed
board operators.
the licensee
decided to
down relieve the Nuclear Watch Engineers
(NWEs) to RCOs temporarily.
Before this action, the
NWEs were the fire brigade leaders.
The
licensee
determined that the Senior
Nuclear Plant Operators
(SNPOs),
whowere non-licensed
operators,
would perform the function of the Fire
Brigade Leader.
The inspector
reviewed the qualifications of the
SNPOs
and reviewed the additional training required to meet all requi rements.
Observations
and Findings
Both units'ire Protection
Plans
meet the requirements of 10 CFR 50
Appendix
R with allowed exemptions.
Appendix R,Section III.H requires.
in part
...
The brigade leader
shall
be competent to assess
the potential
safety consequences
of .a fire and advise control
room personnel.
Such competence
by the fire brigade leader
may be evidenced
by
possession
of an operator's
license or equivalent
knowledge of
plant safety related
systems.
Section III.I(8) requires that fire brigade leaders
also receive
training on direction and coordination of fire fighting activities.
Both units'FSARs describe the fire fighting program as meeting these
portions of Appendix R.
Turkey Point has
used senior non-licensed
operators
as the fire brigade
leader for some time:
The training programs at St. Lucie and at Turkey
Point were designed to take
a person with little nuclear
power
background,
and, through time, increase their knowledge
and skills to a
point that they would be able to apply for a license.
The
SNPO position
was designated
for the most senior
and knowledgeable
non-licensed
operators.
Administrative Procedure,
AP 0005740,
"Non-Licensed Operator
Initial Training and Qualification," specifically states
the subject
matter that the non-licensed
operators
are required to know.
Besides
systems
knowledge
and practical operations training. the
SNPOs are
required to exhibit knowledge of integrated plant operations.
During the weeks of Hay 26 and June 2, the licensee
conducted fire
brigade leader training for the SNPOs.
This was the same type of
training that the
NWEs routinely receive.
The inspector attended
portions of the training.
Class sizes
were small, generally five to
eight members.
The instructor s presented
the lesson
plans well,.
The
P
'3
inspector noted that many good questions
were asked
by the
SNPOs
and
that the participation levels were high.
The subject matter covered
was
appropriate.
The first topic covered
was
on procedures
and procedural
requirements.
All applicable procedures
were discussed,
particularly
the Emergency
Plan implementation.
The instructors
discussed
the
classification of fire related events,
and what type of help was to be
expected
from outside sources.
Next, the group discussed
leadership qualities
and
how to be
a leader.
It was evident to the inspector that there were
some
SNPOs
who held
reservations
about being the fire brigade leader,
but private
discussions
with the operators
at later times indicated that very few
doubted that they would be able to perform the function if necessary.
After this, the discussions
turned to the duties of the fire brigade
leader.
Again, the inspector
noted .that good conversations
were held.
Finally, the
SNPOs role played
some fire scenarios.
As the instructor
facilitated the discussions,
the team members
discussed
the best places
to set
up command posts,
how to distribute personnel.
hazardous
material
issues,
and other topics.
Overall the quality of training was judged to
be good.
The licensee
had plans to run drills with the
SNPOs acting
as
fire brigade leaders
when possible.
c.
Conclusions
The training to allow the
SNPOs to up relieve as fire brigade team
leader
was adequate to meet all. regulatory requirements.
The brigade
leader training was comparable to that which the
NWEs receive.
V. Hang ement Heetin
s and Other
Areas
Xl
Exit Meeting Summary
The inspectors
presented
the inspection results to members of licensee
management
at the conclusion of the inspection
on June 20,
1997.
An interim
exit meeting
was held on May 23.
1997, to discuss
the findings of Region based
inspection.
The licensee
acknowledged
the findings presented.
The inspectors
asked the licensee
whether
any materials
examined during the
inspection should
be considered proprietary.
No proprietary information was
identified.
-.
Licensee
'4
PARTIAL LIST OF
PERSONS
CONTACTED
M. Allen. Training Manager
C. Bible, Site Engineering
Manager
.
W. Bladow, Site Quality Manager
G. Boissy, Materials Manager
H. Buchanan,
Health Physics Supervisor
D. Fadden,
Services
Manager
R. Heroux.
Business
Manager
H. Johnson.
Operations
Manager
J.
Marchese,
Maintenance
Manager
C. Marple. Operations
Supervisor
J. Scarola,
St. Lucie Plant General
Manager
A. Stall, St. Lucie Plant Vice President
E. Weinkam, Licensing Manager
W. White, Security Supervisor
Other licensee
employees
contacted
included office, operations,
engineering,
maintenance,
chemistry/radiation,
and corporate personnel.
INSPECTION
PROCEDURES
USED
IP 37551:
IP 61726:
IP 62703:
IP 62707:
IP 64704:
IP 71707:
IP 92901:
IP 92902:
IP 92903:
IP 92904:
~0ened
Onsite Engineering
Surveillance
Observations
Maintenance
Observations
,
Maintenance
Observations
Fire Protection
Program
Plant Operations
Followup - Plant Operations
Followup - Maintenance
Followup - Engineering
Followup - Plant Support
ITEMS OPENED,
CLOSED,
AND DISCUSSED
50-389/97-05-01
"Failure to Control Foreign Material Entering
and Exiting the Unit 2 Containment."
(paragraph
3.1)
50-335,389/97-05-02
IFI
"Licensee
Review and Clarification of Procedure
(ADM-11.03) for Performing Temporary Changes to
Procedures."
(paragraph
08. 1)
50-335/97-05-03
"Failure to Provide Adequate
Work Instructions
For
a Work Order." (paragraph
M1.3)
50-335/97-05-04
Closed
50-335/94-08-03
r
50-335,389/96-01-01
50-335,389/96-16-03
50-335/97-03-07
50-335/97-03-05
50-335/97-03-06
Discussed
50-389/97-03-04
'5
"Failure to Use the Proper Procedure to Document
and Control
DDPS Software Revisions."
(paragraph
E8.2)
"Quality Level of PORV and
SRV Discharge
Piping." (paragraph
E8.1)
"Temporary Changes to Procedures
Improperly
Changed Intent of Procedures."
(paragraph
08. 1)
IFI
"Implementation of Interim Plant Actions to
Detect
New Tampering."
(paragraph
S8. 1)
"Issues Relating to Exceeding Unit 1 Licensed
Steady State
Power Levels." (paragraph
E8.2)
"Failure to Obtain
FRG Review for Interim CR
Disposition" (paragraph
E8.3)
"Post Maintenance Testing Issues
Associated with
DDPS Constant
Changes"
(paragraph
E8.4)
"Nonconforming Reactor
Coolant
Pump Penetration
Fault Protection"
(cover letter)
ADM
ANSI
ASME Code
ATTN
CFR
CIAS
CNRB
CR
DDPS
LIST OF ACRONYMS USED
Administrative Procedure
(system)
American National Standards
Institute
Administrative Procedure
American Society of Mechanical
Engineers Boiler and Pressure
Vessel
Code'merican Society for Testing
and Materials
Attention
Control Element Assembly
Code 'of Federal
Regulations
Containment Isolation Actuation Signal
Company Nuclear
Review Board
Condition Report
Containment
Spray Actuation System
Digital Data Processing
System
Departure
From Nucleate, Boiling Ratio
Demonstration
Power
Reactor
(A type of operating license)
Enforcement Action
Emergency
Core Cooling System
FHE
FR
FRG
GMP
gpm
I8C
ICW
IFI
kW
LER
LR
mA
M8TE
HOV
MS
NI
No.
NPF
NPWO
NRC
NWE
OP
PC/M
PGM
PMAI
PSL
.
QI
RCB
RCGVS
RCO
'6
Engineered
Safety Feature
The Florida
Power
8 Light Company
Flow Recorder
Facility Review Group
Final Safety Analysis Report
General
Maintenance
Procedure
Gallon(s)
Per Minute (flow rate)
Hydraulic Control Valve
High Pressure
Safety Injection (system)
Instrumentation
and Control
Intake Cooling Water
[NRC] Inspector Followup Item
InService Inspection
(program)
KiloWatt(s)
Licensee
Event Report
Low Pressure
Safety Injection (system)
Level Recorder
Milliampere
Measuring
8 Test Equipment
Motor Operated
Valve
C
Hain Steam Isolation Valve
Moisture Separator/Reheater
NonCited Violation (of NRC requirements)
Nuclear
Instrument
Number
Normal Operating
Pressure
Nuclear
Production Facility (a type of operating license)
Nuclear Plant Supervisor
Nuclear
Plant Work Order
Nuclear Regulatory
Commission
Nuclear Watch Engineer
Operating
Procedure
Protection Circuit
Plant Change/Hodification
NRC Public Document
Room
Plant General
Manager
Plant Management Action Item
Power Operated Relief Valve
Plant St. Lucie
Quality Assurance
Quality Control
Quality Instruction
Quality Surveillance Letter
Reactor Containment Building
Gas Vent System
Reactor Control Operator
Reactor
Coolant
Pump
r
V
4
RII
.
SMB
SNPO
St.
TEDB
TQAR
TS
'7
Region II - Atlanta, Georgia
(NRC)
Reactor Protection
System
Resistive Temperature
Detector
Refueling Water
Tank
Safety Train 8
Shut
Down Cooling
Safety Injection (system)
Safety Injection Actuation System
Safety Injection Tank
Type of valve actuator
Senior
Nuclear Plant [unlicensed]
Operator
Safety
Parameter
Display System
Senior Reactor [licensed] Operator
Saint
Temporary
Change
Total Equipment
Data
Base
Topical Quality Assurance
Report
Technical Specification(s)
Updated Final Safety Analysis Report
[NRC] Unresolved
Item
United States
Nuclear Regulatory Commission
Ultrasonic Test
Verification and Validation
Violation (of NRC requirements)
Work Order
Work Request
4r~ ~
(