ML17059B715
| ML17059B715 | |
| Person / Time | |
|---|---|
| Site: | Nine Mile Point |
| Issue date: | 09/15/1997 |
| From: | NRC OFFICE OF INSPECTION & ENFORCEMENT (IE REGION I) |
| To: | |
| Shared Package | |
| ML17059B713 | List: |
| References | |
| 50-220-97-06, 50-220-97-6, 50-410-97-06, 50-410-97-6, NUDOCS 9709220165 | |
| Download: ML17059B715 (86) | |
See also: IR 05000220/1997006
Text
U.S. NUCLEAR REGULATORY COMMISSION
REGION I
Docket/Report Nos.:
50-220/97-06
50-410/97-06
License Nos.:
NPF-69
Licensee:
Niagara Mohawk Power Corporation
P. O. Box 63
Lycoming, NY 13093
Facility:
Nine Mile Point, Units
1 and 2
Location:
Scriba, New York
Dates:
June 29- August 9, 1997
Inspectors:
B. S. Norris, Senior Resident Inspector
T. A. Beltz, Resident Inspector
J. C. Jang, Senior Radiation Specialist
W. A. Maier, Senior Emergency Preparedness
Specialist
R. A. Skokowski, Resident Inspector
Approved by:
Lawrence T. Doerflein, Chief
Reactor Projects Branch
1
Division of Reactor Projects
'7709220ih5 9709i5
ADQCK 05000220
6
TABLE OF CONTENTS
page
TABLE OF CONTENTS
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EXECUTIVE SUMMARY
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SUMMARY OF ACTIVITIES
Niagara Mohawk Power Corporation (NMPC) Activities ................
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Nuclear Regulatory Commission (NRC) Staff Activities
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OPERATIONS
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Conduct of Operations..........,
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01.1
General Comments
01.2
Inadvertent Initiation of the NMP1 Containment Spray System
02
Operational Status of Facilities and Equipment
02.1
NMP2 Shutdown and Unusual Event due to High Drywell Floor
Drain Leak Rate.........
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Operator Training and Qualification
05.1
Review of INPO Re-Accreditation Report
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Miscellaneous Operations Issues..........
08.1
(Closed) LER 50-410/97-03:
Technical Specification Violation
Caused
by Procedural Non-Compliance
Due to Personnel
Error
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08.2
(Closed) LER 50-410/97-05:
High Pressure
Core Spray System
Inoperable Due to Failed Unit Cooler ..................
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II. MAINTENANCE,... ~ ~.....................
M1
Conduct of Maintenance
M1.1
General Comments
M1.2
Calibration of NMP2 LPRM Neutron Monitoring System
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M1.3
NMP1 Reactor Protection System Calibration .......
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M1.4 Corrective Maintenance
Backlog ..................
M2
Maintenance
and Material Condition of Facilities and Equipment
M2.1
Repair of NMP2 Drywell Equipment Drain Tank Leak Rate
Monltol
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III.ENGINEERING...............................................
E1
Conduct of Engineering
E1.1
General Comments
E1.2
Engineering Backlog.......... ~...................
E8
Miscellaneous
Engineering Issues
E8.1
(Closed) IFI 50-410/96-06-02:
Clarification of Wording in the
NMP2 UFSAR Regarding
Full Core Offloads ........ ~....
E8.2
(Closed) IFI 50-410/96-06-04:
Review of Corrective Actions
~Associated with LER 50-410/96-03-01
E8.3
(Closed)'VIO 50-410/EA-96-116-1012:
Discrimination of an
Employee for Raising Safety Concerns.................
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Table of Contents (cont'd)
E8.4
(Closed) LER 50-410/97-02-02:
Potential Inoperability of
Emergency Diesel Generator Service Water Cooling Water
Outlet Valves During a Control Room Fire
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IV. PLANT
R1
R2
R3
R6
R7
P2
P3
P4
P5
P7
P8
S1
S8
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SUPPORT
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Radiological Protection and Chemistry (RP5C) Controls
R1.1
General Comments
R1.2
Implementation of the Radioactive Liquid and Gaseous
Efflu
Control Programs ~........................
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Status of RPRC Facilities and Equipment ..
R2.1
Compliance with Posting Requirements
R2.2
Calibration of Effluent/Process
Radiation Monitoring System
R2.3
Surveillance Tests for Air Cleaning Systems
and Plant Air
Balance
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RP&C Procedures
and Documentation ....................
R3.1
Review of Radioactive Effluents Procedures
and Reports ..
RPRC Organization and Administration
R6.1
Staffing Levels
Quality Assurance
R7.1
QA Audits of Effluent Activities
Status of Emergency Preparedness
(EP) Facilities, Equipment and
Resources ..'
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Emergency Response
Facilities ~...................
.EP Procedures
and Documentation
P3.1
Emergency Plan and Associated Procedures....
Staff Knowledge and Performance
in EP
P4.1
Staff Performance
in the Simulator
Staff Training and Qualification in EP . ~...................
P5.1
EP Qualification Tracking
P5.2
Drill and Exercise Performance
P5.3
General
EP Training
Quality Assurance
in EP Activities
P7.1
Deviation/Event Reports ........................
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External Audits
Miscellaneous
EP Issues
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P8.1
(Closed) IFI 50-220/96-07-19
and 50-410/96-07-19:
Weaknesses
in the Emergency Preparedness
Program....
Conduct of Security and Safeguards Activities..............
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'General Comments
Miscellaneous Security and Safeguards
Issues ..............
S8.1
(Closed) URI 50-410/97-04-11:
NMP2 Refuel Floor Access
Gate Found Unlocked ..
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Table of Contents (cont'd)
V. MANAGEMENTMEETINGS
X1
Exit Meeting Summary.........,.....
ATTACHMENT 1
- PARTIALLIST OF PERSONS CONTACTED
- INSPECTION PROCEDURES USED
- ITEMS OPENED, CLOSED, AND UPDATED
- LIST OF ACRONYMS USED
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EXECUTIVE SUMMARY
Nine Mile Point Units 1 and 2
50-220/97-06
8c 50-410/97-06
June 29 - August 9, 1997
This integrated
NRC inspection report includes reviews of licensee activities in the
functional areas of operations,
engineering,
maintenance,
and plant support.
The report
covers a six week period of inspections
and reviews by the resident staff, and regional
specialists in the areas of emergency preparedness
and radiological effluent monitoring.
PLANT OPERATIONS
During the inspection period, four procedural non-compliances
occurred as a result of
personnel
errors. (VIO) The most significant event was the inadvertent spray-down of the
NMP1 containment due to an operator opening the wrong valve during a surveillance.
In
addition, during the review of a Licensee Event Report, it was noted that the failure to
.. properly implement.a.procedure
resulted in NMP2 changing operational conditions without
meeting the requirements of the Technical Specification.
Several personnel performance
errors have been identified at both units during the past year; suggesting
continued NMPC
management. attention is warranted in this area.
The response
of the NMP2 control room crew and supervision to an increasing drywell
floor drain leak rate was good.
The work by maintenance
and engineering to identify and
repair the leaking flex-hose were also good.
RP support during the forced outage was
considered outstanding.
MAINTENANCE
The inspectors observed instrument and calibration (IRC) technicians perform surveillances
tests on safety related systems at both units.
In each case, the work was performed
carefully, with good communications between the IRC technicians
and with the control
room operators.
Since August 1996, NMP1 has made little progress
in lowering the total non-outage
corrective maintenance
(CM) backlog; in contrast, NMP2 has made slow, but steady,
progress
in lowering the backlog.
Both units reduced the percentage
of long-standing
safety-related
CM backlog items, and no long-standing safety-related
CM backlog items
were safety significant.
The inspectors considered the repairs of the NMP2 drywell equipment drain tank leak rate
monitor to be acceptable.
Procedures
and work orders were used at the job and all test
equipment was properly calibrated.
Executive Summary (cont'd)
ENGINEERING
Both units have experienced
an increase
in the overall engineering
backlog during the past
year.
However, NMPC management
was able to eliminate all long-standing
non-outage
PLANT SUPPORT
The NMPC program for posting of related regulatory documents was adequate
and in
compliance with the requirements of 10 CFR 19.11.
The licensee maintained and implemented very good programs for routine radioactive liquid
and gaseous
effluent releases.
They actively pursued program enhancements
in the
effluent program to maintain offsite exposure
as-low-as-is-reasonably
achievable.
The implementation of the emergency preparedness
program is inconsistent.
Some strong
areas were noted in the operational readiness
of the emergency response
facilities and
training content.
The evaluation to support the move of the Emergency Operations facility
was well documented.
However, some programmatic controls were weak: the
qualification tracking system failed to detect that the qualification of nine members of the
emergency response
organization had lapsed, and a required annual offsite augmentation
drill had not been performed in several years.
(VIO) The licensee's
annual audit of the
.emergency
preparedness
program was performance-based
but failed to identify the above
problems.
REPORT DETAILS
Nine Mile Point Units 1 and 2
50-220/97-06 & 50-410/97-06
June 29 - August 9, 1997
SUMMARYOF ACTIVITIES
Niagara Mohawk Power Corporation (NMPC) Activities
Nine Mile Point Unit 1 (NMP1) started the inspection period at full power.
On July 11,
the unit was shutdown due to an increasing drywell floor drain leak rate.
The source
of the leak was subsequently
determined to be a packing leak on a valve in the post-
accident sampling system.
The valve was repaired, and the unit was returned to service
on July 13; full power was achieved on July 16.
NMP1 maintained essentially full power
. for,. the remainder,.of.,the
inspection period.
NMP2
Nine Mile Point Unit 2;(NMP2) started the inspection period at 95% of full power, limited
due to the moisture separator reheaters
being isolated.
On August 4, control room
operators manually scrammed the reactor from 60% power.due to a high drywell floor
drain leak rate.
The. source of the leak was subsequently
determined to be a leaking
flexible drain hose on the "B" recirculation flow control valve.
(See Section 02.1 of this
inspection report.)
The inspection period ended with NMP2 in startup.
Mana ement Chan
es
During the inspection period, several changes were made to the Nine Mile Point senior
management
team:
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Mr. Martin McCormick, previously Vice President - Nuclear Engineering,
assumed
a new
position as Vice President - Special Projects, with a primary focus on developing the
New York Nuclear Operating Company (NYNOC).
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Mr. John Conway, previously Plant Manager - NMP2, became the new Vice President-
Nuclear Engineering.
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Mr. Kim Dahlberg, previously General Manager - Projects, is the interim Plant Manager-
NMP2, until a permanent selection is made.
Afterwards, Mr. Dahlberg will assume new
duties as the Vice President - Nuclear Operations.
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Mr. Norman Rademacher,
previously Plant Manager - NMP1, assumed
new duties
related to regulatory affairs and performance issues.
~'r. Richard Abbott, currently Vice President and General Manager - Nuclear, is the
interim Plant Manager - NMP1, until a permanent selection is made.
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2
Nuclear Regulatory Commission (NRC) Staff Activities
Ins ection Activities
The NRC conducted
inspection activities during normal, backshift, and deep backshift
hours.
In addition to the inspection activities completed by the resident inspectors,
regional specialists conducted
inspections
and reviews in the areas of effluent controls and
The results of the specialist inspections
are contained
in the
applicable sections of this report.
U dated Final Safet
Anal sis Re ort Reviews
A discovery of a licensee operating their facility in a manner contrary to the Updated Final
Safety Analysis Report (UFSAR) description highlighted the need for additional verification
that licensees were complying with UFSAR commitments.
While performing the
inspections discussed
in this report, the inspectors reviewed the applicable portions of the
UFSAR related to the areas inspected.
The inspectors verified that the UFSAR wording
was consistent with the. observed plant practices, procedures
and/or parameters.
I. OPERATIONS
01
Conduct of. Operations (71707, 90712, 92700)
'1.1
General Comments
Using NRC Inspection Procedure 71707, the resident inspectors conducted frequent
reviews of ongoing plant operations.
Specialist inspectors-in this area used other
procedures
during their reviews of operations activities; these inspection procedures
are listed,,as applicable, for the respective sections of the inspection report.
In
general, the conduct of operations was professional
and safety-conscious;
specific
events and noteworthy observations
are detailed in the sections below.
01.2
Inadvertent Initiation of the NMP1 Containme t S ra
S stem
a.
Ins ection Sco 'e
The inspectors reviewed the inadvertent initiation of the NMP1 containment spray
system.
The. inspectors discussed
the event with an onshift licensed reactor
operator and the Assistant Shift Supervisor (ASSS), and reviewed the associated
Deviation/Event Report (DER). The inspectors
also reviewed the associated
surveillance test procedure
and selected recorder traces, and attended
management
meetings relating to the event.
Topical headings such as 01, M8, etc., are used in accordance withthe NRC standardized reactor inspection report outline.
Individual reports are not expected to address
all outline topics.
The NRC inspection manual procedure or temporary
instruction that was used as inspection guidance is listed for each applicable report section.
b.
Observations
and Findin s
On July 1, 1997, containment spray quarterly surveillance testing was in progress
at NMP1. Containment spray pump ¹121 was taking a suction from the torus and
discharging back to the torus through flow control valve (FCV)80-118.
A licensed
control room operator was conducting the surveillance test and had established
the
proper flow path, in accordance
with the procedure.
The next step in the procedure
required the operator to establish
a system flow rate by throttling FCV 80-118.
The
operator inadvertently opened containment spray blocking valve 80-40.
Valve 80-
40 established
a direct flow path to the containment through the containment spray
The operator immediately identified the error and shut valve 80-40.
The
licensee estimated the valve was partially open for approximately thirty seconds.
Later, while standing at the control panel, the operator discussed
the event with the
inspectors.
The operator had a copy of surveillance test Procedure
N1-ST-Q6B,
"Containment Spray System Loop 121 Quarterly Operability Test," Revision 04.
The operator stated that he had the procedure
in one hand and had just throttled
FCV 80-118 with the other.
The operator removed his hand from the control
switch for FCV 80-118 to point to the flow gage and verify flow rate.
While
attempting to readjust the flow rate using FCV 80-118, the operator failed to
reverify that his hand was on the proper valve.
The control switch for valve 80-40,
physically located directly below the control switch for FCV 80-118 on the control
panel, was inadvertently operated.
Following the event, process computer data indicated that containment
temperatures
and pressures
changed very little due to the spray initiation. The
drywell floor drain (DWFD) sump rate-of-change
momentarily exceeded'Technical
Specification (TS) limits; however, the immediate isolation of the containment spray
restored the rate of change to within TS requirements.
The licensee estimated
between 150-200 gallons of water was discharged to the drywell. The inspectors
reviewed the DWFD recorder traces to independently verify the quantity of water
injected, and concurred with the licensee estimations.
NMP1 engineering staff performed an operability determination,
and determined that
the containment spray system, the containment,
and all equipment within
containment, remained operable.
The engineering operability determination was
reviewed, and subsequently
concurred upon, by the Station Operations Review
Committee (SORC).
The inspe'ctors considered the operability determination to be
detailed and to have received
a thorough review by NMP1 management.
In
addition, during a subsequent
plant shutdown and drywell entry, maintenance
and
engineering personnel examined the equipment in the drywall and confirmed that
there was no damage.
NMPC's apparent root cause of the event was that the consequences
of inadvertent
compone'nt operation during this surveillance test had not been considered;
As
such, less than adequate
self-checking was performed.
Licensee procedures
required independent
or peer verification when the failure to properly perform a step
could result in equipment damage,
personnel injury, or a reactor trip. During the
performance of the surveillance test, direct observation of valve manipulations was
not specifically required.
As a result of this event, NMP1 is evaluating the need for
generic procedural enhancements
to ensure that evolutions having the potential to
impact reactor plant safety are adequately
supervised.
Also, the NMP1 Operations
Manager directed that all control ro'om switch manipulations would now require a
peer verification. The inspectors considered the less than thorough appreciation for
the consequences
of improper control panel manipulations to be a weakness.
In addition to the above, the following personnel performance
errors occurred during
this observation period:
On July 23, NMP1 operators opened the wrong circuit breaker while isolating
motor generator set ¹167 prior to maintenance.
The label for the circuit breaker
opened did not agree with the markup (tagout) sheet and tag.
This resulted in
an unplanned
de-energization
of various equipment, including the control room
process computer.
On July 22,,during preventive maintenance
on the deluge sprinkler system,
a fire
brigade member operated
an incorrect valve, resulting in an unplanned
pressurization
of the water deluge sprinkler system in the NMP2 turbine building
condenser
area.
No equipment was damaged.
On July 18, a NMP1,radiological waste operator, clearing a markup following
maintenance,
positioned three valves different from the position on the
restoration sheet without permission from the Station Shift Supervisor (SSS).
This unexpected
system configuration later resulted in overflowing a tank in the
radiological waste building.
On all four occasions,
personnel failed to comply with or adequately implement
written procedures.
These procedural non-compliances
are violations of NMP1 TS, Section 6.8.1, and NMP2 TS, Section 6.8.1, regarding procedural adherence.
(VIO 50-220/97-06-01
and 50-410/97-06-01)
The inspectors noted that the above errors were a result of either inattention-to-
detail, a,lack of a questioning attitude, or a less-than-adequate
focus on potential
plant impact resulting from improper actions.
Many of the events resulted from
personnel lacking conservative judgement and decision making.
Although none of
the above issues had any immediate safety consequence,
the inspectors consider
this indicative of a continuing problems in personnel performance at Nine Mile Point.
Conclusions
During the observation period, four procedural non-compliances
occurred as a result
of personnel
errors. (VIO) The most significant event was the inadvertent spray-
down of the NMP1 containment due to'an op'erator opening the wrong valve during
a surveillance test,
These four, errors are just the latest examples of poor personnel
performance at both units during the past year, indicating the need for continued
NMPC management
attention in this area.
o.
02.1
5
Operational Status of Facilities and Equipment
NMP2 Shutdown and Unusual Event due to Hi h Dr well Floor Drain Leak Rate
Ins ection Sco
e
The NMP2 reactor was manually scrammed,
and an Unusual Event declared,
due to
increasing drywell floor drain (DWFD) leak rate.
The inspectors were in the control
room and observed the operating crew during the initial phases of the event.
Subsequently,
the inspectors monitored the licensee's activities associated
with the
identification and repair of the leak.
b.
Observations
and Findin s
On August 4, 1997, with NMP2 at 95% power, the control room received alarms
indicating increasing drywell (DW) radiation levels and pressure;
during the review,
the operators identified a rising DWFD leak rate.
NMP2 TS, Section 3.4.3.2, limits
unidentified leakage to 5.0 gallons per minute (gpm); otherwise, the unit must be
shutdown.
The TS define unidentified leakage as that which is not identified.
Examples of identified leakage. would be pump seal or valve packing leaks collected
into a sump, or leakage into the containment atmosphere
from a source which is
specifically known'nd is not part of the pressure
boundary.
In accordance
with NMPC procedures,
the initial response
by the SSS was to
reduce power to 60%.
Subsequently,
the SSS, in consultation with the Operations
Manager and Plant Manager, directed the reactor to be manually scrammed from
60%. The SSS declared an Unusual Event, in accordance
with the NMP2
Emergency Plan, when DW leakage exceeded
10 gpm.
The inspectors were in the
NMP2 control room during the. initial phases of the event, and considered the
response
by the control room crew and supervision to'be good.
The emergency
declaration was proper and timely. When DWFD leakage was reduced to less than
4.0 gpm, the SSS terminated the event, in accordance
with the Emergency Plan.
Notifications to the appropriate federal, state, and local officials were completed
within the required timeframe.
NMPC performed a comprehensive
review of the
plant response to the manual scram, per Procedure
N2-REP-6, "Post-Scram
Review," Revision 01.
When the plant was in a coLD sHUTDowN condition (i.e., reactor coolant temperature
less than 200'F), personnel entered the DW and found that the maintenance
drain
flexible-hose (flex-hose) on the "B" recirculation flow control valve (2RCS" HYV17B)
was leaking.
The inspectors entered the DW and observed the failed flex-hose.
NMPC decided to remove the flex-hose and cap the open pipe ends, rather that
replace it or attempt to repair it. The questions from the NMP2 engineering
and
maintenance staff revealed
a good. understanding
of the potential complications and
the need for contingencies if the repair did not proceed
as expected.
The inspectors
monitored the licensee's
plarlning meetings,.reviewed
tlie below documentation
associated
with the modification, and considered them acceptable:
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Engineering
Design Document Change DDC Number N2-97-063,
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Licensing Document Change Request LDCR Number 2-97-UFS-105,
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Safety Evaluation SE Number 97-82,
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Applicability Review AR,25509, and
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Maintenance Work Order WO 97-12122-06
In addition to the removal of the failed flex-hose, immediate corrective actions
included:
(1) an inspection of all remaining accessible flex-hoses in the DW, and (2)
an evaluation of equipment in the area of the water spray for detrimental affects.
Actions to prevent recurrence
included plans to remove as many of the flex-hoses
as possible during the next refueling outage.
The root cause evaluation for the
failed flex-hose will not be available until a destructive analysis, by an outside
contractor, is completed.
An inspector follow item (IFI) is opened to review the root
cause analysis and any supplementary
corrective actions.
(IFI 50410/97-06-02)
The inspectors noted that the NMP2 SORC members generally conducted
a
'thorough review of the DERs associated
with this event.
Several of the DERs
addressed
specific problems identified during the NMPC inspections of other flex-
hoses in the drywell~
Each discrepancy was satisfactorily addressed
before the
plant was restarted.
However, during the SORC review of DER 2-97-2300, "Failed
Flex-Hose Resulting in Plant Scram," it was not noted during the engineering
disposition, nor'by any of the SORC members during the review, that the accident
analysis was inaccurate in that it assumed
there would be only one leak path from
the failed flex-hose.
After the DER was approved, the inspectors questioned the
unique design configuration of the flex-hose on 2RCS"HYV17B; specifically, a
.- catastrophic failure of this hose would equate to two leakage paths.
The NMP2
Plant Manager agreed that the accident analysis only accounted for half of the
'possible leakage.
Although'the overall consequences
did not change, the inspectors
considered this an example of a weak questioning attitude by the licensee's
engineering organization.
In addition, the inspectors discussed
the potential catastrophic failure of the flex-
hose as it related to the NMP2 Individual Plant Examination/Probability
Risk Analysis
(IPE/PRA).
For a small-break loss of coolant accident (SBLOCA), the IPE/PRA only
models pipe breaks greater than
1 inch; thus, a break of most 3/4 inch pipes would
be considered
a plant transient.
However, a complete failure of this 3/4 inch flex-
hose results in two leak paths and would be classified as a SBLOCA, since the total
break size is larger than
1 inch.
Nonetheless,
based on the relatively small number
of flex-hoses in this configuration, NMPC concluded that the overall probability of a
SBLOCA remained relatively unchanged.
The inspectors considered
NMPC's
conclusion to be acceptable.
The radiation protection (RP) support during the investigation and repairs of the flex-
- hose were outstanding,
Good ALARA[as-low-as-is-reasonably-achievable]
practices, such as pre-job briefs, protective clothing, and the use of remote cameras
in the DW, resulted in maintaining the total dose received at a minimum. The
maintenance
activities to repair the leak, including the RP and engineering support,
were well planned and executed.
Overall, the inspectors considered the efforts of
the NMP2 staff in response to the failed flex-hose to be above average.
c.
Conclusion
The response
of the NMP2 control room crew and supervision to an increasing DW
leakage was good.
The work by maintenance
and engineering to identify and repair
the leaking flex-hose were also good.
RP support during the forced outage was
considered outstanding.
05
Operator Training and Qualification
05.1
Review of INPO Re-Accreditation
Re ort
The Institute of Nuclear Power Operations
(INPO) conducted
a review of Nine Mile
.training programs from April 28 - May 2, 1997.
The INPO evaluation was based on
an NMPC self-assessment
and an on-site review.
The purpose of the review was to
determine the effectiveness of the below. training programs for re-accreditation
in
.accordance
with the standards
established
by. the INPO National Academy. for ..
Nuclear Training:
~
Non-Licensed Operators
~
Reactor Operators
~
Senior Reactor Operators
~
Station Shift Supervisors
~
~
Continuing Training for Licensed Personnel
The inspectors reviewed the INPO Re-Accreditation Evaluation Report, issued on
July 21, 1997, and identified no issues that the NRC was not already aware of. No
additional followup by the NRC is warranted.
08
MIscellaneous Operations Issues (90712, 92700)
08.1
Closed
.LER 50-410 97-03: Technical S ecification Violation Caused
b
Procedural
Non-Com liance Due to Personnel
Error
On June 8, 1997, approximately one hour after NMP2 changed
operational
conditions from Mode 2 (sTARTUF) to Mode
1 (RUN), a DW communication circuit
(2LAR-PNLUO3-12) was found to be energized.
This circuit was not provided with
backup containment penetration overcurrent protection and therefore, in accordance
with NMP2 TS 3.8.4.1, was required to be de-energized
following final DW
inspectio~.
Upon discovery; NMP2 licensed operators entered the appropriate TS Limiting
Condition of Operation (LCO), pnd de-energized
the circuit. The licensee determined
the root cause of the event to be personnel
error.
Particularly, the operator failed to
open the circuit breaker and observe the proper system response
(i.e., no self-
0
checking) during the performance of the Primary Containment AC Circuit Check.
Subsequently,
the operator was temporarily removed from watch standing duties;
remediation included counseling
on the use of self-checking techniques,
and the
performance of Job Performance
Measures
emphasizing self-checking.
Notwithstanding, the licensee violated TS 3.0.4, which states that entry into an
operational condition shall not be made unless the conditions for the LCO are met
without reliance on provisions contained
in the Action Statements.
This non-
repetitive, licensee-identified violation is being treated as a Non-Cited Violation,
consistent with Section VII.B.1 of the NRC Enforcement Policy.
(NCV 50-41 0/97-06-03)
The inspectors reviewed the Licensee Event Report (LER) and found it to be timely
and to accurately describe the event.
Also, the inspectors considered
the
immediate corrective actions and actions taken to prevent recurrence
appropriate.
This LER.is closed.
08.2
Closed
LER 50-41097-05:
Hi h Pressure
Core S ra
S stem lno arable Due to
Failed Unit Cooler
-The event described
in.this LER was discussed
in NRC IR 50-410/97-04, Section,
02.2.
The description and analysis of the event, as contained in the LER, is
consistent with the inspectors'nderstanding
of the event.
The corrective actions
in the LER state that a detailed failure analysis of the terminal board will be
performed, estimated to be completed by January 1998.
This LER is closed.
II. MAINTENANCE
'1
Conduct of Maintenance (61726, 62707)
M1.1
General Comments
Using NRC Inspection Procedures
61726 and 62707, the resident inspectors
periodically observed plant maintenance
activities and the performance of various
surveillance tests.
Specialist inspectors
in this area used other procedures
during
their reviews of maintenance
and surveillance activities; these inspection procedures
are listed, as applicable, for the respective sections of the inspection report.
In
general, maintenance
and surveillance activities were conducted
professionally, with
the work orders (WOs) and necessary
procedures
in use at the work site, and with
the appropriate focus on safety.
Specific activities and noteworthy observations
are
detailed in the inspection report.
The inspectors reviewed procedures
and observed
all or portions of the following maintenance/surveillance
activities:
Surveillance activities are included under "Maintenance."
For example, a section involving surveillance observations might
be included as a separate sub-topic under M1, "Conduct of Maintenance."
~
N1-ISP-036-003
~
N2-ESP-BYS-W675
~
N2-ESP-ICS-0@002
~
N2-RESP-04
~
WO 96-1 5884-00
~
WO 97-10019-00
~
WO 97-10944-00
~
WO 97-11224-00
High-Low Reactor Water Level Instrument Trip Channel
Test/Calibration
125 Volt DC Weekly Battery Surveillance
RCIC [Reactor Core Injection Cooling] Pump and Valve
Operability and System Integrity Test and ASME
[American Society of Mechanical Engineers] XI
Functional Test
LPRM [Local Power Range Monitor] Calibration
Replacement of the Division II Emergency
Dies'el
Generator
Fuel Transfer Pump Mechanical Seal
Drywell Equipment Drain Chart Recorder Behaving
Erratic
Erratic Indication on Drywell Equipment Drain Pump
Flows Causes
Erroneous
Leakage Rate
B Drywell Floor Drain Flow Rate Indication on Recorder
is Erratic
M1.2
Calibration of NMP2 LPRM Neutron Monitorin
S stem
a.
Ins ection Sco
e
The inspectors observed
a portion of the calibration of the local power range
monitors (LPRMs) by NMP2 instrument and controls (I&C) technicians.
In addition,
the inspectors reviewed the completed calibration documentation.
b.
Observations
and Findin s
With NMP2 operating at 95% of rated power, I&Ctechnicians performed
a
calibration of NMP2 LPRMs, using reactor engineering surveillance test, procedure
N2-RESP-4, "LPRM Calibration," Revision 02. The activities within the LPRM
cabinets were performed carefully and the technicians used good three-way
communications between themselves
and with the control room operators.
The
Supervisor, Reactor Engineering, reviewed the completed surveillance test the next
day'and confirmed that no unsatisfactory results were obtained.
The inspectors reviewed the precautions,
limitations, and potential plant impact
statements,
and verified that all necessary
actions had been taken.
Also, the
inspectors verified that the digital multimeter being used by the l&C technicians was
in calibration.
The inspectors performed an independent
review of the completed
surveillance test procedure
and identified no unsatisfactory results.
C.
Conclusion
The inspectors determined that the calibration of the NMP2 LPRMs was performed
carefully by the l&C technicians, with good communications
used consistently.
The
supervisory review identified, no unacceptable
results and was completed in a timely
manner.
M1.3
ar
10
NMP1 Reactor Protection
S stem Calibration
Ins ection Sco
e
The inspectors monitored NMP1 IRC technicians calibrate the instrument trip units
for the reactor water level high/low trip inputs to the reactor protection system
(RPS)
~
b.
Observations
and Findin s
Using instrument surveillance test procedure N1-ISP-0360003,
"Hi-Lo Reactor
Water Level Instrument Trip Channel Test/Calibration," Revision 02, NMP1 IRC
technicians verified the operability of the high and low level trip inputs to the RPS.
The performance of this surveillance test procedure required several personnel at
various locations: the lead technician was stationed
in the control room, another
was at the remote shutdown panel, and a third was at the analog trip system (ATS)
cabinets.'n
addition, since performance of the procedure generated
a half-scram, it
was classified as a "Category 1" activity, requiring a first-line supervisor from the
respective department to.be present during the entire activity.
The procedure was completed without incident.
The supervisory oversight was
performed without being intrusive.
Three-part communications were observed to be
consistently used by all personnel
involved in the'evolution, the IRC technicians, the
supervisor,
and the control room operators.
The technicians were knowledgeable of
the procedure
and the physical operation of the system.
Overall, the inspectors
considered the performance of the technicians during the surveillance test to be
thorough and professionally conducted.
C.
Conclusion
Performance of half-scram testing of the reactor protection system was completed
without incident.
Good three-part communications were consistently used by the
IRC technicians.
M1.4 Corrective Maintenance
Backlo
aO
Ins ection Sco
e
The inspectors reviewed the corrective maintenance
(CM) backlog for both units,
and discussed the backlog with the respective Maintenance
Managers and Outage
Managers.
b.
Observations
and Findin s
The inspectors reviewed the CM backlog trend data for the last year.The NMP1
hon-outage
CM backlog has remained relatively constant, approximately 400, from
August 1996 to July 1997.
The NMP1 Maintenance
and Outage Managers stated
11
that they considered the current CM backlog to be unsatisfactory,
and that they
developed
a plan to aggressively reduce it.
The NMP2 non-outage
CM backlog had been reduced from 412 in August 1996 to
242 in May 1997.
Overall, the inspectors considered that NMP2 has made
consistent progress
in lowering the backlog since August 1996.
The inspectors reviewed the CM backlog with respect to safety-related
items. At
both units, the inspectors identified no long-standing
(i.e. greater than three
months) items which could potentially impact safe plant operation.
In the past year,
the safety-related
CM backlog had remained relatively constant at NMP1, and had
been declining at NMP2. However, the percent contribution of long-standing safety-
related items to the overall CM backlog had been reduced slightly at both units
since August 1996.
C.
Conclusions
M2
M2.1
Since August 1996, NMP1 had made little progress
in lowering the total non-outage
CM backlog items and NMP2 had made slow, but consistent,
progress
in lowering
the total backlog of non-outage
CM items.
Both units had reduced the percentage
of long-standing safety-related
CM backlog items, and no long-standing safety-
related CM backlog items having safety consequence
were identified.
Maintenance and Material Condition of Facilities and Equipment (62707)
Re air of NMP2 Dr well E ui ment Drain Tank Leak Rate Monitor
lns ection Sco
e
The NMP2 drywell equipment drain tank (DWEDT) leak rate monitor exhibited erratic
indication on the pump flow rate chart recorder.
The instrument was declared
inoperable and a 30-day LCO was entered.
The inspectors evaluated the use of an
alternate means of determining leak rate.
In addition, selected portions of the repair
activities were monitored, and discussions
were held with the maintenance
supervisor.
b.
Observations
and Findin s
On June '23, 1997, the chart recorder for monitoring the NMP2 DWEDT leak rate
(2DER-FR123) exhibited erratic indication of flow rate.
The SSS declared the
instrument inoperable, entered
a 30-day shutdown
LCO in accordance
with TS 3.4.3.1.b, and initiated DER 2-97-1872.
Using WO 97-10019-00, IRC conducted
troubleshooting
of the recorder; however, no further erratic behavior was noted
initially and the technicians were unable to identify the cause for the erratic
behavior.
Subsequently,
on June 27, the recordei was returned to service.
On July 12, the chart recorder again indicated erratic pump flows and was declared
A second
DER (¹2-97-2049) was written, noting that this appeared to
12
be a repeat failure.
NMPC considered the that the recorder itself could potentially
be the problem; corrective actions in WO 2-97-10944 included replacing the chart
paper drive motor, the servo-amplifier card, and several corroded wires.
The
recorder was returned to service on July 18; on July 19, the indications were still
erratic and the recorder was declared inoperable.
A new WO (2-97-11224) was
generated,
consisting of signal tracing with an oscilloscope,
measurement
of power
supply voltages, verification that no additional corrosion existed, and tightening of
all terminal connections.
In addition, the differential pressure transmitter instrument
lines were flushed, refilled, and vented to remove any entrapped
air.
A final
calibration was performed after completion of maintenance.
No further problems
have been noted.
NMPC determined the root cause to be multiple degraded
components
and air in the
transmitter sensing
lines.
The immediate corrective actions appeared
adequate.
Actions to prevent recurrence
included a review, by NMPC, of IRC procedures to
ensure the maximum reliability of control room recorders.
The inspectors discussed
the failed instrument with several shift operators
and
noted that all crews-were able to use an alternate method.to determine drywell
equipment leak rate, as required by TS 3.4.3.1.
The inspectors observed portions
of the repair activities and noted that maintenance
work orders and calibration
procedures
were in use at the job site, and that all test equipment was in
calibration.
The inspectors identified no discrepancies
during the review of the
associated
DERs, WOs, 5 calibration records.
c.
Conclusion
The inspectors considered the repairs of the NMP2 DWEDT leak rate monitor to be
adequate.
Procedures
and work orders were used at the job and all test equipment
.was properly calibrated.
III. ENGINEERING
E1
Conduct. of Engineering (37551)
E1.1
General Comments
Using NRC Inspection Procedure 37551, the resident inspectors frequently reviewed
design and system engineering activities and the support by the engineering
organizations to plant activities.
Specialist inspectors
in this area used other
procedures
during their reviews of engineering activities; these inspection
.procedures
are listed, as applicable, for the respective sections of the inspection
.
report.
0
13
E1.2
En ineerin
Backlo
a.
Ins ection Sco
e
The inspectors
assessed
the backlog of engineering work for both units.
Specifically, the inspectors reviewed DER trend data and the temporary modification
backlog.
The inspectors discussed
the issues with engineering staff for both units.
b.
Observations
and Findin s
The inspectors reviewed the engineering
DER backlog trend data for the last year,
noting a steady increase
in backlog items during the past few months at both units.
For NMP1, the engineering
DER backlog had risen from 207 in June 1996 to 298 in
June 1997,
The NMP2 engineering
DER backlog had risen from 274 in June 1996
to 364 in June 1997.
The inspectors discussed,
with both engineering staffs, the proposed
actions to
reduce the backlog.
Both units have established
a multi-disciplined DER team to
. assist in backlog reduction.and to improve the quality of DER dispositions.
As part
of this effort, NMP2 increased
resources
by 13 temporary engineers,
and NMP1
was evaluating similarly supplementing
the engineering staff.
Further refinement of
backlog prioritizatioh and reevaluation of refueling modifications was another
management
action item to reduce the backlog.
The inspectors noted that licensee
management
had been addressing
the engineering backlog, but that the current
trend indicated these actions were ineffective during the last year.
The inspectors additionally reviewed the status of temporary modifications at both
units.
The inspectors noted that only one non-outage
greater than one year old existed, and that was at NMP1
~ The long-standing
temporary modification for NMP1 was the Thermex modular waste treatment
system, which became
a permanent modification subsequent
to the inspection '
period.
The inspectors considered that NMPC's goal to eliminate long-standing
non-
outage temporary modifications was appropriate
and appeared to be effective.
C.
Conclusions
The engineering
DER backlog for both units has risen over the last year.
NMPC's
efforts have had minimal impact in reducing the overall engineering
DER backlog
during the past year.
Management's
goal to eliminate long-standing
non-outage
temporary modifications was appropriate
and appeared to be effective.
14
E8
Miscellaneous Engineering Issues (90712, 92700, 93903)
E8.1
Closed
IFI 50-410 96-06-02:
Clarification of Wordin
in the NMP2 UFSAR
Re ardin
Full Core Offloads
a.
Ins ection Sco
e
During a 1996 NRC inspection, it was identified that the NMP2 UFSAR did not
accurately reflect the practice of performing a complete reactor core offload for a
normal refueling outage.
At that time, NMPC committed to clarify the wording in
the NMP2 UFSAR, and an inspector follow item (IFI) was opened to track the
completion of the revision.
The inspectors reviewed the licensee's documentation
which approved the change.
b.
Observations
and Findin s
The inspectors reviewed the following NMPC documents
related to the changes to
Section 9.1.3 of the NMP2 UFSAR:
~
Safety Evaluation Number SE-96-074, Revision 0, "Spent Fuel Pool Cooling,
Residual Heat Removal, Alternate Decay Heat Removal, and Secondary
Containment"
'
Applicability Review Number AR-12996, Revision 0
~
Licensing Document Change Request Number LDCR- 2-96-UFS-084, Revision 0
!
SORC Minutes for Meeting 96-79-02, which approved the change
The changes
clarified the fact that a full core offload was the normal practice, and
that the transfer of fuel to the spent fuel pool could begin as early as 96 hours0.00111 days <br />0.0267 hours <br />1.587302e-4 weeks <br />3.6528e-5 months <br /> after
reactor shutdown.
The inspectors noted that the approved changes were
incorporated into the UFSAR in May 1997.
c.
Conclusion
The inspectors considered the safety evaluation and associated
documents to be
complete and to accurately reflect the practice currently used by NMP2 for normal
reactor refueling evolutions.
No unreviewed safety questions were identified during
the review.
E8.2
Closed
IFI 50-410 96-06-04:
Review of Corrective Actions Associated with
LER 50-410 96-03-01
a.
Ins ection Sco
e
During a 1996 NRC inspection, it.was noted by the inspectors that the corrective
actions detailed in an LER appeared to appropriately address the identified root
causes..ln the associated
NRC inspection report, an IFI was opened to track the
completion of the corrective actions.
~,
15
b.
Observations
and Findin s
The inspectors reviewed the corrective actions described
in LER 50-410/96-03-01,
associated with the full core offload and operation of the spent fuel pool cooling
system outside of design basis.
The corrective actions, and review to verify
completion, included:
~
The training program for personnel qualified to perform safety evaluations
and
applicability reviews was revised to include a discussion of the need to perform
a thorough review of the system design basis when writing and/or revising
procedures.
The inspectors verified that the training lesson plan (QAR-SE-Q/R/S-030,
Revision 1, "QARSE [Qualified Applicability Reviewer/Safety Evaluator]
Qualification, QARSE Requalification, or QARSE SORC/SRAB [Station Operation
Review Committee/Safety Review and Audit Board]) was appropriately revised
to incorporate
a description of the event and the associated
LER.
~
~ -The UFSAR and associated
refueling procedures
were revised to address spent
fuel pool cooling operations.
N2-FHP-13.1
Complete Core Offload, Revision 04
N2-FHP-13.2 Complete Core Reload, Revision 05
N2-FHP-13.3 Core Shuffle, Revision 00
The UFSAR revision was discussed
in Section E8.1 of this report.
The fuel
handling procedures
(listed below) were reviewed and appeared to contain the
necessary
changes
in response to the deficiencies noted in the inspection report
and the LER related to spent fuel pool cooling requirements
and a partial core
offload with fuel shuffle.
~
Divisional bus outage procedures,
operating procedures,
and refueling
administrative procedures were revised to include spent fuel pool cooling system
design basis requirements.
Spent Fuel Pool Cooling and Cleanup System, Revision 08
Shutdown Operations Protection Instruction, Revision 02
Shutdown Safety, Revision 02
The inspectors reviewed the below operating and administrative procedures/
instructions and determined that the changes
appeared to adequately
address
the system design basis requirements of the UFSAR and Technical
Specifications.
N2-OP-38
N2-ODI-5.60
NIP-OUT-01
On September 29, 1996, NMPC informed the NRC that the divisional bus outage
work was not scheduled for the September
1996 refueling outage; as such, the
procedures would.not be revised until prior to the next scheduled
bus outage
16
during the next refueling (Spring 1998).
The inspectors verified that the
associated
procedures
(N2-PM@12 and N2-PM@13) had been deactivated.
~
A lessons learned transmittal was issued describing the event and the need to
perform an in-depth review and evaluation of design basis when writing and/or
revising procedures.
The inspectors reviewed the Lessons
Learned Transmittal, dated July 16, 1996,
and verified that applicable personnel
in affected departments
were trained.
~
A review was conducted of selected portions of the UFSAR to validate that
necessary
programs and procedures
were in place which comply with the
NMPC reviewed the UFSAR for the following systems:
control rod drive, reactor
core isolation cooling, reactor building closed loop cooling, and non-safety
portions of main steam.
Numerous
DERs were written to resolve identified
discrepancies.
The inspectors reviewed a sample of the DERs and considered
-. the identification and resolutions to be:adequate.
Based on the above reviews, this item is closed.
c.
Conclusion
The corrective actions related to NMP2 practices contrary to the UFSAR for full core
offload during refueling, and the operation of the spent fuel pool cooling system
were thorough and acceptable.
E8.3
Closed
VIO 50-410 EA-96-116-1012:
Discrimination of an Em lo ee for Raisin
Safet
Concerns
On July 24, 1996, the NRC issued
a Severity Level II Notice of Violation (Notice)
and imposed a Civil Penalty of $80,000 against NMPC for discrimination against a
former employee for raising safety concerns at the. Nine Mile facility. The Notice
was based on the Recommended
Decision and OI'der of a U.S. Department of Labor
Administrative Law Judge.
The NRC noted in the letter which transmitted
the'otice
that NMPC denied that any discrimination occurred against the individual, but
that corrective actions were taken to ensure
an environment free for raising safety
concerns.
These. actions included:
~
reemphasizing to management
the rights and responsibilities of employees to
raise safety issues;
~
reinforcing, at all levels of management,
the value of reporting issues to improve
performance;
and
~
reemphasizing
the availability of the Quality First Program.
h
Based. on frequent observation by the resident inspectors, it appears that NMPC has
promoted an open environment for raising safety concerns.
In addition, the
17
inspectors have not seen any attitudes or actions by management
to indicate that
they are privately or internally dismissing this violation, thereby creating a "chilling
effect" at the Nine Mile Point site.
This item is closed.
Closed
LER 50-410 97-02-02:
Potential Ino erabilit
of Emer enc
Diesel
Generator Service Water Coolin
Water Outlet Valves Durin
a Control Room Fire
The technical issues related to this were described
in NRC IR 50-410/97-04.
The
LER was timely and satisfactorily described the issues.
The inspectors reviewed the
root cause
and corrective actions provided in the LER and considered them to be
appropriate.
This LER is closed.
IV. PLANT SUPPORT
Using NRC Inspection Procedure 71750, the resident inspectors routinely monitored
the performance of activities related to the areas of radiological controls, chemistry,
security, and fire protection.
Minor deficiencies were
discussed with the. appropriate management,
significant observations
are. detailed.
below.
Specialist inspectors in the same areas used other procedures
during their
reviews of plant support activities; these inspection procedures
are listed, as
applicable, for the respective sections of the inspection report.
R1
Radiological Protection and Chemistry (RP&C) Controls (71750, 84750)
R1.1
General Comments
During entry into and exit from radiologically controlled areas (RCAs), the inspectors
verified that proper warning signs were posted, personnel entering were wearing.
proper dosimetry, personnel
and materials leaving were properly monitored for
radioactive contamination,
and monitoring instruments were functional and in
calibration.
During periodic plant tours, the inspectors verified that radiation work
permits (RWPs) and survey maps were current and accurately reflected plant
conditions.
They observed activities in the RCAs and verified that personnel were
complying with the requirements of applicable RWPs, and that workers were aware
of the radiological conditions in the area.
R1.2
Im lementation of the Radioactive
Li uid and Gaseous
Effluent Control Pro rams
a.
Ins ection Sco
e
The inspectors toured the plant, including the control rooms, and reviewed liquid
and gaseous
effluent release permits, airborne tritium quantification techniques,
and
unplanned
and unmonitored release pathways.
b.
Observations
and Findin s
18
The inspectors toured the control rooms and selected radioactive liquid and gas
processing facilities and equipment.
Included in this review were the effluent
radiation monitor systems
(RMS) and air cleaning systems at both units.
All
equipment was operable at the time of the tour. The inspectors noted that the
licensee maintained and monitored air balances for the reactor, turbine, and
radioactive waste (radwaste) buildings at both units to assure conformance to
UFSAR specifications.
The inspectors toured the NMP2'RMS calibration laboratory.
This laboratory was equipped with two operable calibration chambers
(closed and
open air calibrators). The open air calibrator was an excellent methodology to avoid
back-scattering
radiation during process/area
RMS detector calibration.
During the review of selected radioactive liquid and gaseous
effluent discharge
permits, the inspectors determined that the discharge permits were complete and
met the criteria of the TS-required Offsite Dose Calculation Manual (ODCM) for
sampling and analyses at the frequencies
and lower limits of detection established
in the ODCM. The inspectors noted that.there had been no radioactive liquid
~ releases from NMP1 -for several. years while pursuing. effluent ALARAand plant
>
'ater
conservation.
The inspectors
also noted that there were no unplanned/unmonitored
radioactive
liquid or gas releases
since the previous inspection conducted
in September
1995.
The inspectors noted that the licensee had reviewed the effluent control programs
relative to the NRC Inspection and Enforcement
(IE)Bulletin 80-10, "Contamination
of Nonradioactive System and Resulting Potential for Unmonitored, Uncontrolled
Release of Radioactivity to Environment."
Recently, the licensee re-reviewed the
safety evaluation reports for the turbine building (a potential -unmonitored release
pathway) to determine if better monitoring devices could be used to demonstrate
compliance with IE Bulletin 80-10 using more restrictive criteria. The inspectors
noted that the previous safety evaluation concluded that there was no unmonitored
release through the turbine building.
The inspectors requested the licensee demonstrate
its capabilities in monitoring and
quantifying airborne tritium. The NMP2 staff calculated the total amount of water
loss from the spent fuel pool (SFP).
The licensee assumed that water loss was due
to evaporation from the SFP released to the environment via the plant main stack.
The licensee calculated the airborne tritium released
results.
Calculated airborne tritium released through the plant main stack during
February 1997 was 6,190 micro-Curie per day (pCI/day).
Measured airborne tritium
release for this same period was 5,390 yCI/day, which was an excellent
comparison.
The inspectors noted that the airborne tritium measurement
error was
about 50%, as reported in the licensee's
semiannual report.
The inspectors stated,
through this comparison, that the licensee demonstrated
its capability to, measure
airborne tritium releases accurately.
The NMP1 staff had some difficulty in calculating the airborne tritium released from
the SFP to the main stack since condenser
gases were also directed to the main
, ~
8'. 'I ~
L
19
stack.
Consequently,
the licensee found it difficultto determine the tritium
contribution from the SFP.
The licensee stated that the tritium fractions (SFP and
steam evacuation) will be determined using airborne tritium measurement
results
during plant operations
and during a refueling outage, since there is no airborne
tritium releases
due to condenser
gases during a refueling outage.
C.
Conclusion
Based on the above reviews and observations,
the inspectors determined that the
licensee maintained and implemented effective radioactive liquid and gaseous
effluent control programs.
The licensee was vigorously pursuing the enhancement
of the effluent control programs at both units through: (1) the elimination of all
radioactive liquid releases from NMP1; (2) re-reviewing the safety evaluation to
comply better with IE Bulletin 80-10 requirements;
and (3) the establishment of a
RMS calibration laboratory in NMP2.
R2"
Status of RP&C Facilities and Equipment (71750, 84750)
.R2.1 .,Com liance with Postin
Re uirements of 10 CFR Part 19 71750
aO
Ins ection Sco
e
The inspectors evaluated
licensee compliance with the NRC requirements of Title 10
of the Code of Federal Regulations (10 CFR) Part 19, "Notices, Instructions and
Reports to Workers:
Inspections
and Investigations," relative to posting of
regulatory documents.
The inspectors reviewed the NMPC implementing procedure,
reviewed the location and content of postings both onsite and offsite, and,
discussed
the issue with NMPC licensing staff.
b.
Observations
and Findin s
The inspectors reviewed NMPC Nuclear Division Directive NDD-RPR, "Regulatory
Posting Requirements,"
Revision 03, which established
requirements for the posting
of regulatory documents,
including NRC Form 3 and enforcement correspondence.
The inspectors determined that NDD-RPR adequately
implemented the requirements
of 10 CFR 19.11.
The procedure
also described posting locations and which
documents were to be posted.
The inspectors determined that the posting areas
specified in NDD-RPR were maintained and were in sufficient locations to allow
ready access
by plant personnel.
All documents
required to be posted were
available for review. The inspectors considered that the NMPC program was
adequate
and in compliance with the posting requirements of 10 CFR Part 19.11.
The. inspectors discussed with the licensing staff the periodicity and documentation
-of posting verification. by the licensee. -Licensing staff stated that posting
.
verification was conducted
on a periodic basis, but was not formally documented.
The inspectors noted that many of the posted documents'related
to enforcement
correspondence
were old issues and no longer required posting; however,
0
20
maintaining the posting beyond that required was conservative
and did not
contradict either licensee procedures
or NRC regulations.
c.
Conclusions
The NMPC program to meet posting of regulatory documents was adequate
and
was in compliance with the requirements of 10 CFR 19.11.
R2.2
Calibration of Effluent Process
Radiation Monitorin
S stems
a.
Ins ection Sco
e
The inspectors reviewed the RMS availability, selected
IRC calibration procedures,
and the most recent calibration results for the following effluent/process
RMS, as
designated for each unit.
~
Liquid Radwaste Effluent Radiation Monitor
~ -Service Water Effluent Radiation Monitor
~
Main Steam Line Radiation Monitors
~
Stack Gaseous
Effluent Monitors (Low and High Ranges)
~
Offgas Radiation'Monitors
~
Emergency Condenser Vent Monitors
NMP2
~
Liquid Radwaste Effluent Radiation Monitor
~
Service Water Effluent Radiation Monitor
~
Cooling Tower Blowdown Line Radiation Monitor
~
Cooling Tower Blowdown Flow Rate
~
Radwaste/Reactor
Building Vent Monitors (Low and High Range)
~
Main Stack Gaseous
Effluent Monitors (Low and High Range)
b.
Observations
and Findin s
The IRC, chemistry, and radiation protection departments
had the responsibility to
perform electronic and radiological calibrations for the above radiation monitors.
All
calibration results reviewed were within the licensee's acceptance
criteria, with the
exception of the liquid radwaste effluent radiation monitor.
The last annual and
quarterly calibrations of this monitor were on September
6, 1994, and
August 29, 1995, respectively.
The licensee did not release any radioactive liquid
since the last calibration.
Calibration, and the operability of this monitor, is required
-by TS only prior to radioactive liquid release to the environment.
The licensee's,
intention was that the radioactive liquid effluent radiation monitor would be
calibrated and made operable prior to any anticipated radioactive liquid release.
21
During the review of the above RMS calibration documentation,
the inspectors
independently
calculated and compared several calibration results, including linearity
tests and conversion factors.
The inspectors determined that the licensee's results
were comparable to the independent
calculations.
The inspectors noted that ownership of RMS varied.
For example, the stack RMS
availability was tracked and trended by the chemistry staff, while the radiation
protection department
had responsibility for the radioactive liquid effluent RMS.
NMP2
The radiation protection department
had the responsibility to perform electronic and
radiological calibration for all NMP2 RMSs.
The inspectors noted that one individual
was responsible for the program, and effectively tracked the availability for all
effluent, process,
and area RMSs.
Calibration results were within the licensee's
acceptance
criteria. The responsible
individual demonstrated
the RMS status to the
inspectors at the monitoring panel in the control room during the plant tour.
",-'uring the review of the'above
RMS calibration documentation,
the inspectors
also
independently
calculated and compared several calibration results, iricluding linearity
tests and conversion factors.
The inspectors determined that the licensee's results
were comparable to the independent
calculations.
c.
Conclusions
Based on the above reviews, the inspectors determined that the licensee maintained
and implemented good calibration and assessment/trending
programs for effluent,
processand
area radiation monitoring systems.
R2.3
Surveillance Tests for Air Cleanin
S stems and Plant Air Balance
80
Ins ection Sco
e
The inspectors reviewed the licensee's most recent surveillance test results for the
below systems,
and the status of the air balance for the following buildings:
~
Reactor Building Emergency Ventilation System
~
Control Room AirTreatment System
NMP2
~
~
Control Room Outdoor Air Special Filter Train System
22
Air Balance for both Units
~
Turbine Buildings
~
Reactor Buildings
~
Radwaste
Buildings
~
Control Rooms
b.
Observations
and Findin s
All surveillance results (visual inspection, in-place HEPA [high efficiency particulate
air] and charcoal leak tests, air capacity tests, pressure drop tests, and laboratory
tests for the iodine collection efficiencies) were within TS acceptance
criteria. Air
balance for the turbine, reactor, and radwaste buildings and the control room were
maintained as described
in the UFSAR.
Recently, the NRC Office of Nuclear Reactor Regulation (NRR) identified a potential
conflict regarding the charcoal testing methodology for the iodine collection
efficiency performed by the licensee/contractor
laboratory.
The licensee's TS
specify Regulatory Guide (RG) 1.52, Revision 2, March 1978, Position C.6.a, as the
requirement for the laboratory testing of the charcoal; and RG 1.52 references
American National Standards
Institute (ANSI) N509-1976, "Nuclear Power Plant Air-
Cleaning Units and Components."
ANSI N509-1976 specifies that testing is to be
performed in accordance
with paragraph 4.5.3 of RDT M-161T, "Gas Phase
Adsorbents for Trapping Radioactive Iodine and Iodine Components."
The essential
testing criteria are:
(1) 70% or 95% relative humidity (RH); (2) 5-hour pre-
equilibration time, with air at 25
C and plant specific RH; (3) 2-hour challenge,
with gas at 80
C and plant-specific RH; and (4) 2-hour elution time, with air at
25
C and plant-specific RH. The latest acceptable
methodology for the laboratory
testing of the charcoal is ASTM [American Society for Testing and Materials]
D 3803-1989, which requires licensee's to maintain 30
C during all testing phases.
The inspectors confirmed that the licensee also used ASTM D 3803 methodology.
C.
Conclusions
Based on the above reviews, the inspectors determined that the licensee maintained
the plant air cleaning systems in accordance with established
design specification
and TS requirements.
R3
RP5C Procedures
and Documentation (84750)
R3.1
Review of Radioactive Effluents Procedures
and Re orts
ao
Ins ection Sco
e
The inspectors reviewed selected chemistry procedures to determine whether the
licensee could implement the radioactive liquid and gaseous
effluent control
programs effectively. The inspectors
also reviewed the 1995 and 1996 Semiannual
Effluent Reports for both units; and contents of the ODCM.
23
b.
Observations
and Findin s
The inspectors noted that effluent control procedures
were detailed and easy to
follow, and that ODCM requirements were incorporated into the appropriate
procedures.
The licensee had good procedures
to satisfy the ODCM requirements
for routine and emergency operations.
The inspectors reviewed the 1995 and 1996 Semiannual
Radioactive Effluent
Release
Reports for both units.
These reports provided data indicating total released
radioactivity for liquid and gaseous
effluents.
The reports also summarized the
assessment
of the projected maximum individual and population doses resulting
from routine radioactive airborne and liquid effluents.
Projected'doses
to the public
were well below the TS limits. The inspectors determined that there were no
anomalous
measurements,
omissions or adverse trends in the reports.
The NMP1 and NMP2 ODCMs provided descriptions of the sampling and analysis
programs, which were established for quantifying radioactive liquid and gaseous
effluent concentrations,
and for calculating projected doses to the public. All
necessary
parameters,
such as effluent radiation monitor setpoint calculation
methodologies,
site-specific dilution factors, and dose factors, were listed in the
~
ODCM. The licensee adopted other parameters from RG 1.109 as appropriate.
c.
Conclusions
Based on the above reviews; the inspectors determined that the NMPC effluent
control procedures
were sufficiently detailed to facilitate performance of all
necessary
steps for routine and emergency operations, the licensee effectively
implemented the ODCM requirements for reporting effluent releases
and projected
- doses to the public, and the licensee's
ODCM contained sufficient information to
acceptably implement and maintain the radioactive liquid and gaseous
effluent
control programs.
R6
RPRC Organization and Administration (84750)
The inspectors reviewed the organization and administration of the radioactive liquid
and gaseous
effluent control programs and discussed with the licensee changes
made since the last inspection; conducted
in September
1995.
There were no
changes
since the last inspection of the programs.
Staffing levels appeared to be
appropriate for the conduct of routine and emergency operations.
24
R7
Quality Assurance
(QA) in RPRC Activities (84750)
R7.1
QA Audits of Effluent Activities
aO
Ins ection Sco
e
The inspectors reviewed the 1995 and 1996 QA audits and chemistry measurement
laboratory QA/QC [quality control] data to validate the quantification methodology
for the total releases.
b.
Observations
and Findin s
The inspectors reviewed QA Audit Report Numbers95-019 and 96-022,
The
inspectors noted that the audit teams included technical personnel.
The 1995 and
1996 audit teams identified no findings of safety significance.
The inspectors noted
that the. scope and technical depth of the audits were sufficient to assess
the
quality of the radioactive liquid and gaseous
effluent control programs.
The licensee maintained
a good.QA policy and verified program performance
throughout the chemistry department,
including the analytical measurement
laboratory. The inspectors reviewed the QC data for intra/inter-laboratory
comparisons.
When discrepancies
were found, effective resolutions were
determined
and implemented.
C.
Conclusions
Based on the above reviews, the inspectors determined that the licensee's
audits'were sufficient to effectively assess
the radioactive'liquid and gaseous
effluent control programs.
The licensee implemented
a very good QA/QC program
to validate measurement
results for effluent samples.
P2
Status of Emergency Preparedness
(EP) Facilities, Equipment and Resources
(82701)
P2.1
Emer enc
Res
onse Facilities
aO
Ins ection Sco
e
The inspectors toured the offsite Emergency Operations Facility (EOF), the offsite
Joint News Center (JNC), and the onsite Operations Support Center (OSC).
The
inspectors conducted
an audit of the instrumentation,
supplies, and equipment
contained
in the EOF and OSC, and reviewed completed quarterly inventories for the
.past four calendar quarters for completeness,
accuracy,
and compliance.
b.
Observatiohs
and Findin s
The licensee had recently (December 1996) relocated to a new EOF, sharing the
.facility used arid maintained by the New York Power Authority (NYPA) for the
25
James A. Fitzpatrick nuclear plant.
The NRC had previously accepted this facility
for use by the Fitzpatrick plant.
As part of the agreement for the use of this facility,
NMPC built and maintained
a new JNC facility for use by the two licensees.
The inspectors
noted that NMPC had provided for separate
resources for their use in
the central decision-making
area of the EOF and had provided for co-locating with
NYPA in the support areas of the EOF for those events that would result in an
emergency at both sites.
As part of the relocation, NMPC committed to perform a
drill with NYPA that would demonstrate
the dual activation of the facility by both
sites.
The NMPC portions of the EOF were kept in an acceptable
state of readiness.
Required procedures
were in place, including adequate
numbers of emergency
classification matrices.
Telephone lists for important emergency response
organization personnel
and locations were readily available.
A spot check of
telephone circuit operability showed no inoperable circuits.
The inspectors noted that there were more items at the EOF and OSC than were
specified on the NMPC inventory sheets.
Licensee
EP staff explained that the
overages
resulted from the closure of the alternate
EOF, which was no longer
required, and the transfer of those instruments to the remaining facilities. The
inspectors reviewed'a sample of inventory and equipment surveillance tests and
verified that they had been performed in the last four calendar quarters.
The review
of DERs showed recurring problems in late submittals of completed inventories to
the EP staff for their review (see section P7.1).
The inspectors'our of the JNC showed adequate
telephone capacity for use by
both the licensee's staff and the news media.
A spot check of telephones
showed
no inoperable circuits.
C.
Conclusions
The inspectors concluded that the maintenance
of the emergency response
facilities
and equipment was being well implemented and that the facilities were operationally
ready.
P3
EP Procedures
and Documentation (82701)
P3.1
Emer enc
Plan and Associated Procedures
The inspectors reviewed the change made to the Nine Mile Point Nuclear Station
Site Emergency Plan that provided for the EOF relocation and the safety evaluation
performed for this change.
The inspectors also reviewed recent changes the
licensee made to the emergency plan implementing procedures
and emergency plan
maintenance
procedures.
The inspectors performed this review in the NRC regional
office. The safety evaluation written for the move of the EOF was well-thought out
and systematically done.
The author drew references from recognized
NRC
.sources,
including the plant's safety evaluation report.
The safety evaluation
26
included a review of the change's effect on the emergency
plan, including licensing
commitments.
The inspectors concluded that the changes
made to the below
procedures
did not decrease
the overall effectiveness of the Nine Mile Point Nuclear
Station site emergency
plan and, after limited review of the changes,
no NRC
approval is required in accordance
with 10 CFR 50.54(q).
Implementation of these
changes
is subject to future inspection effort to confirm that the changes
have not
decreased
the effectiveness of the emergency plan.
~
EPIP-EPP-08
~
EPIP-EPP-1 2
~
EPIP-EPP-13
~
EPIP-EPP-21
~
EPIP-EPP-28
~
EPIP-EPP-30
~ 'PMP-EPP-02
Off-Site Dose Assessment
and Protective Action
Recommendation,
Revision 7
Re-Entry Procedure,
Revision 3
Emergency Response
Facilities Activation and Operation,
Revision 7
Radiation Emergencies,
Revision 3
Fire Fighting, Revision 3
Prompt Notification System Problem Response,
Revision 2
Emergency Equipment Inventories and Checklists, Revision 10
P4
Staff Knowledge and Performance in EP (82701)
P4.1
Staff Performance
in the Simulator
a.
Ins ection Sco
e
The inspectors observed the EP activities of two shift crews, one from each unit, on
the respective plant-specific simulators.
They observed
each crew, which included
licensed reactor operators
and senior reactor operators, communicators,
and dose
. assessment
personnel,
in the performance of one scenario'.-The activities observed
.
included assessment
of plant conditions, classification of emergency events,
notification of offsite authorities, offsite dose assessment,
and the formulation and
transmittal of protective action recommendations.
b.
Observations
and Findin s
The crews were knowledgeable
in the performance of their duties.
Operators were
.able to assess
plant conditions quickly and accurately.
All classifications were
correct.
Notifications were made in a timely fashion.
The crews were able to stay
current with a rapidly degrading plant condition, in which escalations of emergency
classes were occurring within minutes of each other.
Dose assessment
personnel
were familiar with the operation of the automated
dose assessment
model and were
able to make correct protective action recommendations
based on the projected
offsite doses.
c.
Conclusions
The inspectors concluded that, the members of the emergency response
organization
responsible for on-shift plant conditions assessment,
classification, notification, and
0
0
27
offsite radiological consequence
assessment
were adequately trained in the
performance of their duties.
p5
Staff Training and Qualification in EP (82701)
P5.1
EP Qualification Trackin
ao
Ins ection Sco
e
The inspectors reviewed EP training records, training procedures,
and the portions
of the emergency
plan dealing with training. They also interviewed EP and training
staff with EP training responsibilities and reviewed a recent qualification status
report-for the entire emergency response
organization.
Finally, they interviewed
two individuals to determine their knowledge of their responsibilities for EP
qualification tracking.
b.
Observations
and Findin s
A training specialist in the licensee's training department was responsible for
administering the EP training program.
The specialist maintained
a close liaison with
the EP staff, although functionally separate from it. The training specialist reviewed
qualification status of emergency response
organization
(ERO) members each
calendar quarter, and scheduled the training to ensure that qualifications were kept
current.
The continuing training for ERO members to maintain their qualifications was given
annually and the-training (including specialized training for certain ERO members)
was required to be completed within the prior 15 months:to prevent lapse of
qualification.
The data base printouts used for review of this requirement did not
sort to give a list of individuals coming due for.retraining.
Rather, they provided an
"X" in the heading for continuing training or specialized training for each member of
the ERO who had the training within the required time. The printout did not give
any indication of impending lapse of qualifications.
It omitted the "X" only after an
individual's qualification had lapsed.
ERO members qualified within the last year
also did not have the "X" in the heading for continuing training or specialized
training, since they had been qualified based on their initial training.
The inspectors reviewed the printout for the ERO qualifications and questioned the
fact that some individuals assigned
dose assessment
duties at the EOF did not
appear to have completed the specialized training.
The training specialist, after
reviewing the records of the individual ERO members, discovered that nine members
of the dose assessment
staff at the EOF had lapsed in their qualifications.
Most of
these
ERO members had lapsed in early June, 1997; however, they continued to be
listed on the ERO roster.
Three of these individuals were initial responders;
i.e.,
ERO members who are the designated
responder for their position during a rotating
duty period.
28
The licensee staff took immediate corrective action to address this oversight,
including informing the ERO members whose qualification had lapsed, and
designating qualified individuals to respond.
The license documented
the problem
on a DER, and they scheduled
remedial training for the members whose
qualifications had lapsed.
Notwithstanding, the failure to maintain the training
requirements of the approved Site Emergency
Plan is a violation of NRC
requirements.
(VIO 50-220/97-06-04 and 50-410/97-06-04)
The licensee has also delegated
some responsibilities for the administration of the
EP training and qualification program to the individual ERO members.
This
delegation was proceduralized
in NIP-EPP-01, "Emergency Response
Organization
Expectations
and Responsibilities."
One of these responsibilities was for the
Team
1 initial responders
to maintain secondary
responder
personnel
in sufficient
quantity to support the requirements of the Site Emergency Plan.
Another
responsibility was for the individual ERO members to maintain their training and
qualifications current.
These individuals did not have a method for readily
determining the status of their own, or their subordinates,
qualifications in order to
satisfy these requirements.
The inspectors interviewed two Team
'1 initial responders
with responsibility for
~
maintenance
of subordinate
ERO members.
Neither of these individuals knew how
to verify the qualification status of the secondary
responders
for which they were
responsible.
Both believed that the Community Alert Network (CAN) printout listing
the telephone
numbers of the secondary
responders
listed only fully qualified ERO
members.
The Director, Emergency Preparedness,
(EPD) told the inspectors that
this was not the case, that the CAN printout only listed the names of members who
had been designated for ERO response.
Conclusions
The inspectors concluded that the licensee's method for tracking EP qualifications
was inadequate for meeting the procedure requirements.
Licensee training staff
could not readily identify personnel who needed periodic training until the
qualification had lapsed.
Based on the limited number of personnel interviewed, the
inspectors concluded that the expectations
and requirements of ERO personnel were
not clearly understood.
The inspectors identified the failure to maintain the training
requirements
listed in the approved Site Emergency
Plan as a violation of NRC
requirements.
(VIO)
Drill and Exercise Performance
Ins ection Sco
e
The inspectors reviewed the approved Site Emergency Plan requirements for the
conduct of drills and exercises
and the EP Maintenance
Procedures
covering
the'equired
drill and exercise scheduling
and performance objectives.
They also
reviewed a recent matrix of drills and objectives to determine how effectively the
licensee was complying with the requirements of the plan and procedures.
b.
Observations
and Findin s
29
The licensee conducts
EP drills and exercises
in accordance with the requirements
of two procedures.
EP Maintenance
Procedure
EPMP-EPP-01,
"Maintenance of
lists periodic requirements for drills and exercises,
and
EPMP-EPP-04,
"Emergency Exercise/Drill Procedure," contains
a required
performance-based
matrix for the conduct of drills and exercises.
Both procedures
specify frequencies at which the various objectives are to be demonstrated.
The licensee's drill matrix lists the drills and exercises for the past six years and the
objectives from the two EPMP procedures that were demonstrated
in each drill. The
inspectors'eview of this matrix showed that the objectives were satisfied with one
exception.
Procedure
EPMP-EPP-01
required the conduct of an annual
augmentation
drill, by activation of the notification system, with actual personnel
response
from offsite to the emergency facilities.
- The inspectors. determined that the licensee had been taking credit for satisfying
this objective through the periodic notification drills they performed during off-hours.
. These notification drills, however, did not require actual transit by the ERO members
to their assigned
emergency response facility. The inspectors learned, through
discussion with the EPD, that a call-out of the ERO with actual report to the
facilities from offsite'had not been performed since November 1994.
The inspectors discussed this fact with the EPD and learned that licensee
management
did not expect an actual report of the ERO from offsite to the ERFs,
and that the procedure
did not correctly reflect the actual expectation.
The EPD.
stated that NMPC recognized the value of such augmentation
drills, but that they
were infrequently performed, and that there was no intention to procedurally
formalize such a practice beyond the requirement to conduct an off-hours exercise
every six years.
The EPD reported that the annual augmentation
drill requirement in EPMP-EPP-01
had been contained
in that procedure since 1991.
The licensee had failed to
recognize the existence of this requirement, despite its explicit wording, and was
taking credit for its completion with the performance of the periodic call-out drills in
which ERO members respond via telephone with an estimate of their reporting time.
The practice of estimating the reporting time, however, had only recently been
implemented as a result of an NRC observation during the last EP program
inspection.
(NRC.lR 96-04 Section P2)
. The licensee had performed a comparison check of the Site Emergency Plan, the EP
.implementing procedures,
EP.maintenance
procedures,
and established
practices
within the past year.
The purpose of this comparison was to identify and resolve
conflicts between the various documents
and practices.
This effort failed to reveal
the discrepancy between the augmentation
drill requirement in EPMP-EPP-01
and
.'he accepted practice of performing call-out notifications without actual report to
the ERF.
The failure to conduct the annual callout drill is a violation of the
30
Emergency
Plan and EP Maintenance
Procedures.
(VIO 50-220/97-06-05 and 50-
410/97-06-05)
C.
Conclusions
Emergency drills/exercises have satisfied the requirements of the EP maintenance
procedures
with the exception of the annual callout drill. (VIO) This is significant in
that a comparison was recently performed to identify conflicts, but NMPC failed to
recognize the existing requirement.
P5.3
General
EP Trainin
ao
Ins ection Sco
e
The inspectors reviewed EP training records, training procedures,
lesson plans, job
performance measures,
and the portions of the emergency plan dealing with
training. As part of this review, they reviewed the presentation
and training
feedback forms from the licensee's recently completed pilot program of computer-
based EP-continuing training.- They also interviewed EP.and training staff with EP
training responsibilities.
The inspectors attended
a training lesson that was given to
- some ERO members at the newly established
EOF and reviewed the lesson plan and
attendance
record's for the training given to ERO responders
prior to the relocation
to the new EOF.
Finally, the inspectors interviewed four individuals to determine
their impressions of the EP continuing training recently received.
b.
Observations
and Findin s
The training specialist instructs for,some lessons, monitors. the instruction given by
subject matter experts for other training, and maintains the overall EP training
program.
This same individual also oversees the maintenance
of the general
employee and radiation protection training programs.
The training that the inspectors observed was held on-station at the EOF and was
administered by the Team
1 initial responder
responsible for the clerical staff. The
EP Training Specialist also administered some of the lesson.
The training was
highly-task oriented, with the instructor leading the trainees around to the various
work stations where they would be performing duties.
The attendees
asked
questions freely, and the instructor readily answered those questions.
The
attendees
were provided a task to perform, and quizzed at the end of the training.
The licensee instituted a pilot training program during the last unit outage in which
initial responders
in the ERO were given an opportunity to take their EP continuing
training by use of a computer-based
training presentation.
They were to take a quiz
and return it to the Training Department.
Also, they were given feedback forms to
communicate their impressions back to the Training Department.'he
inspectors
noted that the computer-based
training was generally'ell received by the
attendees.
Two ERO members interviewed felt that it was'a positive experience.
Comments received on the feedback forms were mostly favorable.
0
31
The content of the computer-based
lesson presentation for the Technical Support
Center (TSC) initial responder continuing training was consistent with the content of
the formal lesson plan for that course.
The training included lessons
learned from
past Nine Mile Point drills as well as lessons
learned from the industry that were
presented
in NRC inspection reports.
There were skill-oriented presentations
on
proper three-way communications
and effective listening,
The EP training given in preparation for the relocation of the EOF was completed for
nearly all the responders
shortly before the move to that facility. Lesson plans
focused on the tasks to be performed and equipment to be used by the responders.
C.
Conclusions
The inspectors concluded that the general content of the EP training program was
well maintained and the program well implemented.
The training given to the EOF
responders
was adequate
and conducted
before the move.
The computer-based
training pilot training program was effectively implemented and met all training
objectives.
P7
Quality Assurance in EP Activities (82701)
P7.1
Deviation Event'Re
orts
aO
Ins ection Sco
e
The inspectors reviewed the outstanding
DERs dealing with EP that were assigned
to other groups for resolution, as well as the DER backlog for the EP group and the
'rend-analysis
performed.by'the'EP staff on DERs assigned to them.
The inspector
- also reviewed the outstanding entries in the Emergency Preparedness
Task Tracking
System (EPTTS).
b.
Observations
and Findin s
The licensee
EP staff frequently relied on the use of DERs to document and track EP
issues.
The threshold for use of this corrective action tool was low. The EP staff
wrote one DER to document the failure of some senior managers to attend required
EP continuing training. The EPD stated that he relies on the DER process to ensure
that the EP activities delegated to the line organizations
are completed properly.
.The inspectors noted six open DERs that the EP group was tracking related to the
inventory of ERF equipment.
The DERs dealt with improperly completed inventories
and with failures of the reporting groups to forward the completed inventories to the
EP staff.
In May 'l997, the EP staff changed the EPMP procedure goverriing the
conduct of the inventories to require forwarding the completed inventories.
The.
- inspectors could not establish the success of this action, since another DER was:
written during the week of the inspection.
The EP staff performed a trend analysis of DERs assigned to them for resolution in
accordance
with Instruction NTI-3.0, "Nuclear Learning Center Self Assessment
Instruction."
The inspectors determined that the EP staff had performed the trend
32
analysis correctly in accordance
with NTI-3.0. The inspectors concluded that, due
to the small number of DERs assigned to the EP staff, the results of the trend
analysis were inconclusive.
The EP staff tracks tasks internally via the EPTTS system.
The EPTTS backlog
contained some long-standing
items that were more than three years old. New due
dates had been assigned to items that had missed their original due dates.
When
questioned
by the inspectors about this practice, the EPD stated that the EPTTS
was an informal system, used by the EP staff, for tracking tasks that were not
captured
in any other administrative procedure/system.
The inspectors noted that
the EPTTS has no procedure or instruction governing its use.
C.
Conclusions
The inspectors concluded that the licensee made good use of the DER system to
maintain the quality control of EP activities; however, the DER system showed
'""- limited success
in ensuring adequate
oversight of EP activities assigned to other
groups, as demonstrated
by repeated
problems with facility inventory processing.
The inspectors concluded that the EPTTS was useful as a reminder file of EP tasks,
. but a poor indicator of the EP.staff's effectiveness
in documenting, trending, and
correcting problems.
P7.2
ao
External Audits
Ins ection Sco
e
The inspectors reviewed the annual QA audit reports for the'last three years, paying
particular attention to the 1997 audit, which was completed in May.
b.
Observations
and Findin s
The audits reviewed were performed by teams that included personnel from other
utilities who were knowledgeable
in EP. They were performance-based
to a limited
extent in that they included observation of a single drill performance.
The audits
looked at the interface between the licensee with the State and local governments
in EP matters.
Copies of the audit reports were made available to the State and
local governments.
The 1997 audit team reviewed drill records and procedure changes,
and had one
minor finding in the latter area.
Despite this fact, the audit team did not find that
the licensee had not followed a long-standing
drill requirement
(see Section P5.2).
Also, the 1997 audit team did not draw any conclusions about the EP staff's need
to write repeated
DERs dealing with improperly processed
facility inventories see
Section P7.1).
C.
Conclusions
The inspectors determined that the annual QA audits met the regulatory
requirements of 10 CFR 50.54(t), but were not effective in identifying some
problems in the licensee's
EP organization.
33
P8
Miscellaneous
EP Issues (92904)
P8.1
Closed
IFI 50-220 96-07-19 and 50-410 96-07-19:
Weaknesses
in the
Emer enc
Pre
aredness
Pro ram
This item was opened
in response to a finding during the 1996 Integrated
Performance Assessment
Program (IPAP) team inspection (NRC IR 50-220/96-201
and 50-410/96-210), in which the IPAP team concluded that sufficient weaknesses
existed in the EP program at Nine Mile Point to warrant increased
inspection effort.
The'inspectors
reviewed this item by evaluating whether actions employed by the
EP staff to identify, correct, and prevent recurrence of problems were adequate to
justify less inspection effort and close the item.
Based on the problems identified during this inspection period, including two
violations, the inspectors confirmed that weaknesses
program.
Additional NRC attention in this area willoccur during the follow-up to
'the violations.
This item is being administratively closed.
S1
Conduct of Security and Safeguards Activities
S1.1
General Comments
During routine tours, the inspectors verified that security posts were properly
staffed, protected area gates and vital area access points were locked or guarded,
and isolation zones were free of obstructions.
In general, access controls were in
accordance with the Nine Mile Point Security Plan.
S8
Miscellaneous Security and Safeguards
Issues
S8.1
Closed
URI 50-410 97-04-11:
NMP2 Refuel Floor Access Gate Found Unlocked
During a tour of the NMP2 reactor building, NRC inspectors found the access gate
to the NMP2 refuel floor improperly secured.
At that time, DER 2-97-1806 was
initiated to determine the significance, root cause,
and necessary
corrective actions
to prevent recurrence.
The inspectors reviewed the completed
DER, and discussed
the issue with the Security Manager and Nine Mile senior management.
The DER
disposition noted that the gate was neither a security barrier nor a radiological
boundary.
As such, there was no requirement for the gate to be locked.
However,
further review by NMPC determined that there were numerous gates and doors that
unnecessarily
required the use of a hard key or an electronic card reader.
Corrective
actions included a review of all locked doors/gates,
with the potential to remove the
unnecessary
access control.
The DER identified the cause as weak management
direction; in that, expectations
were not well understood with respect to ensuring
that gates/doors
were locked.
This URI is closed.
34
V. MANAGEMENTMEETINGS
X1
Exit Meeting Summary
At periodic intervals, and at the conclusion of the inspection period, meetings were
.held with senior station management
to discuss the scope and findings of this
inspection.
The exit meetings for specialist inspections were conducted
upon
completion of their onsite inspection:
~
July 18, 1997
~
Radioactive Effluents Monitoring
July 18, 1997
The final exit meeting occurred on August 21, 1997.
During this meeting, the
resident inspectors findings were presented.
NMPC did not dispute any of the
inspectors findings or conclusions.
Based on the NRC Region
I review of this
report, and discussions with NMPC representatives,
it was determined that this
report does not contain safeguards
or proprietary information.
ATTACHMENT1
PARTIALLIST OF PERSONS CONTACTED
Nia ara Mohawk Power Cor oration
R. Abbott
D. Barcomb
C. Beckham
D. Bosnic
J. Burton
H. Christensen
J. Conway
G. Correll
A. DeGracia
S. Doty
K. Dahlberg
G. Helker
..P. Mazzafero
L. Pisano
R. Randall
P. Smalley
R. Smith
C. Terry
R. Tessier
K: Ward
C. Ware
D. Wolniak
Plant Manager,
NMP1 (Acting)
Manager, NMP2 Radiation Protection
Manager, Quality Assurance
Manager, NMP2 Operations
Director, ISEG
Manager, Security
Vice President,
Nuclear Engineering
Manager, NMP1 Chemistry
Manager, NMP1 Work Control
Manager, NMP1 Maintenance
Plant Manager, NMP2 (Acting)
Manager, NMP2 Work Control
Manager, NMP1 Technical Support
Manager, NMP2 Maintenance
Manager,
NMP1 Engineering
Manager,
NMP1 Radiation Protection
Manager,
NMP1 Operations
Vice President,
Nuclear Safety Assessment
& Support
Manager, Training
Manager, NMP2 Technical Support
Manager, NMP2 Chemistry
Manager, Licensing
INSPECTION PROCEDURES USED
IP 37551:
IP 61726:
IP 62707:
IP 71707:
IP 71750:
IP 82701:
IP 84750:
IP 90712:
IP 92700:
IP 92901:
IP 92903:
IP 92904:
On-Site Engineering
Surveillance Observations
Maintenance Observation
Plant Operations
Plant Support
Operational Status of the Emergency Preparedness
Program
Radioactive Waste Treatment, and Effluent and Environmental
Monitoring
In-Office Review of Written Reports of Nonroutine Events at Power
Reactor Facilities
Onsite Followup of Written Reports of Nonroutine Events at Power
Reactor Facilities
Followup - Operations
Followup - Engineering
Followup - Plant Support
Attachment
1
ITEMS OPENED, CLOSED, AND UPDATED
OPENED
50-220
8L
50-410/97-06-01
50-410/97-06-02
50-410/97-06-03
Multiple examples of failure to follow procedures
IFI
Review root cause and additional corrective actions after
destructive testing of flex-hose
Personnel
error resulted in changing from STARTUP to
RUN without meeting all conditions of the TS
50-220
8L
50-410/97-06-04
50-220 5
50-41 0/97-06-05
CLOSED
50-410/96-06-02
IFI
Clarification of wording in the NMP2 UFSAR regarding full
core offloads
Review. of corrective actions associated
with LER 96-03-01
Weaknesses
in the emergency preparedness
program
IFI
IFI
50-410/96-06-04
- 50-220
8L
50-41 0/96-07-1 9
50-410/97-04-1
1
50-410/
EA-96-1 1 6-1 01 2
50-410/97-06-03
.
NMP2 refuel floor access gate found unlocked
Discrimination of an employee for raising safety concerns
Personnel
error resulted in changing from STARTUP
to RUN without meeting all conditions of the TS
Potential inoperability of EDG service water cooling water
outlet valves during a control room fire
TS violation caused
by procedural non-compliance
due to
personnel
error
HPCS system inoperable due to failed unit cooler
50-410/97-02-02
LER
50-410/97-03
LER
LER
50-410/97-05
UPDATED-
none
Annual retraining of some ERO members was
not completed
An annual
ERO augmentation
callout drill was not performed
since 1994
LIST OF ACRONYMS USED
ANSI
ASSS
CFR
As Low As Reasonably Achievable
American Society of Mechanical Engineers
American Society for Testing and Materials
American National Standard
Assistant Station Shift Supervisor
Analog Trip System
'ode
of Federal Regulations
Corrective Maintenance
A-2
Attachment
1
DER
DWEDT
DWFD
GL
gpm
IFI
IR
ltkC
LCO
LER
NRC
NYNOC
QARSE
RH
SORC
SRAB
TS
Deviation/Event Report
Drywell (containment)
Drywell Equipment Drain Tank
Drywell Floor Drain
Enforcement Action
Flow Control Valve
Generic Letter
gallons per minute
High Efficiency Particulate Air
High Pressure
Inspection and Enforcement
Inspector Follow Item
Inspection Report
Instrumentation
and Control
Joint News Center
Limiting Condition for Operation
Licensee Event Report
Local Power Range Monitor
Non-Cited Violation
~ Niagara Mohawk Power Corporation
Nuclear Regulatory Commission
New York Nuclear Operating Company
New York Power Authority
Offsite Dose Calculation Manual
Small Break Loss of Coolant Accident
Station Operations Review Committee
Senior Reactor Operator
Safety Review and Audit Board
Station Shift Supervisor
Technical Specification
Updated Final Safety Analysis Report
Violation
Operations Support Center
Quality Assurance
Qualified Applicability Reviewer/Safety Evaluator
Radiologically Controlled Area
Reactor Core Isolation Cooling
Regulatory Guide
Relative Humidity
Radiation Monitoring System
Radiation Work Permit
Work Order
A-3
7