ML16341E828

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SALP Repts 50-275/88-18 & 50-323/88-17 for Aug 1987 - Jul 1988.Improvements Required in Area of Successful Implementation of Mgt Policy & Objectives
ML16341E828
Person / Time
Site: Diablo Canyon  Pacific Gas & Electric icon.png
Issue date: 09/29/1988
From:
NRC OFFICE OF INSPECTION & ENFORCEMENT (IE REGION V)
To:
Shared Package
ML16341E827 List:
References
50-275-88-18, 50-323-88-17, NUDOCS 8810170245
Download: ML16341E828 (92)


See also: IR 05000275/1988018

Text

U.

S.

NUCLEAR REGULATORY COMMISSION

REGION V

SALP

BOARD REPORT

SYSTEMATIC ASSESSMENT

OF

LICENSEE

PERPORMANCE

FOR

PACIFIC GAS

AND ELECTRIC COMPANY

DIABLO CANYON NUCLEAR POWER

PLANT

REPORT

NOS. 50-275/88-18

AND 50-323/88-17

EVALUATION PERIOD:

08/01/87 - 07/31/88

SALP

BOARD ASSESSMENT

CONDUCTED

SEPTEMBER 8,

1988

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TABLE OF

CONTENTS

Pacae

I.

Introduction

A.

Licensee Activities

B.

Direct Inspection

and Review Activities

II.

Summary of Results

A.

Overview

B.

Results of Board Assessment

C.

Changes

in SALP Ratings

from Previous

SALP

III. Criteria

IV.

Performance

Analysis

A.

Pl ant Operati ons

B.

Radiological Controls

C.

Maintenance/Surveillance

D.

Emergency

Preparedness

E.

Security

F.

Engineering/Technical

Support

G.

Safety Assessment/quality

Verification

H.

Fire Protection

5

8

11

15

16

19

22

26

V.

Supporting

Data and Summaries

A.

Enforcement Activity

B.

Confirmation of Action Letters

28

28

TABLES

Table

1

Table

2

Table

3

Table

4

Table

5

Table

6

Table

7

Table

8

Inspection Activities and Enforcement

Summary, Unit 1

Inspection Activities and Enforcement

Summary, Unit 2

Enforcement

Items, Unit 1

Enforcement

Items, Unit 2

Synopsis of Licensee

Event Reports,

Unit 1

Synopsis of Licensee

Event Reports,

Unit 2

Licensee

Event Reports,

Unit 1

Licensee

Event Reports,

Unit 2

'b

DETAILS

I.

INTRODUCTION

The Systematic

Assessment

of Licensee

Performance

(SALP) program is an

integrated

NRC staff effort to collect available observations

and data

on

a periodic basis

and evaluate

the licensee's

performance

based

on this

information.

The program is supplemental

to normal regulatory processes

used to ensure

compliance with NRC rules

and regulations.

It is intended

to be sufficiently diagnostic to provide

a rational basis for allocating

NRC resources

and to provide meaningful

feedback to the licensee's

management

regarding the NRC's assessment

of their facility's performance

in each functional area.

An NRC SALP Board,

composed of the members listed below,

met in the

Region

V office on September

8, 1988, to review the observations

and data

on performance

in accordance

with NRC Chapter

0516,

dated

June

6, 1988,

"Systematic

Assessment

of Licensee

Performance."

The Board's findings

and recommendations

were forwarded to the

NRC Regional Administrator for

approval

and issuance.

This report is the NRC's assessment

of the licensee's

safety performance

at the Diablo Canyon Nuclear Power Plant,

Units 1 and,2, for the period

August 1,

1987 through July 31,

1988.

The

SALP Board for Diablo Canyon

was

composed of:

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J.

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E. Chaffee,

Deputy Director, Division of Reactor Safety and Projects,

Region

V (Board Chairman)

W. Knighton, Director, Project Directorate

V,

NRR

Rood,

NRR Project Manager

P.

Zimmerman, Chief, Reactor Projects

Branch

J.

Pate,

Chief, Reactor Safety Branch

L. Montgomery, Chief, Nuclear Materials Safety

and Safeguards

Branch

M. Mendonca,

Chief, Reactor

Projects

Section

1

P.

Yuhas, Chief,

Emergency

Preparedness

and Radiological Protection

Branch

D. Schuster,

Chief, Safeguards

Section

F. Fish, Chief,

Emergency

Preparedness

Section

P. Narbut, Senior Resident

Inspector

B. Pereira,

Project Inspector

S. North, Senior Radiation Specialist

W. Schaefer,

Physical Security Specialist

P. O'rien, Project Inspector

Ramsey,

Reactor Inspector,

Engineering Section

"Denotes voting member in functional area of cognizance.

""Denotes voting member in all functional areas.

A.

Licensee Activities

Unit 1 started

the

SALP period at lOOX power and operated thru March

6,

1988 and then

commenced

the second refueling outage.

The second

refueling outage

was completed

on July 13,

1988, with a return to

power operations

which continued thru the end of this

SALP period.

The refueling outage

included refueling the core,

eddy current

testing of steam generators,

testing of 213 snubbers,

an integrated

leak rate test of containment

and significant unplanned work, such

as,

repair of leaking

CROM canopy welds,

replacement

of cracked

RCP

lube oil assemblies

and reversal

of 48 inch containment

purge

isolation valves.

Unit 1 experienced

four automatic reactor trips

during the

SALP period.

Unit 2 commenced

the

SALP period at 100X power and operated

continuously throughout the

SALP period.

Unit 2 experienced

one

automatic

and two manual reactor trips during the

SALP period.

B.

Direct Ins ection and Review Activities

Approximately 5416 on-site inspection

hours"were

spent in performing

a total of 59 inspections

by resident,

region-based,

headquarters,

and contract personnel.

Inspection activity for each unit in a

functional area are

summarized

in Tables

1 and 2, for Units

1 and 2,

respectively.

Three

NRC resident

inspectors

were on-site through

mid-May 1988, with two inspectors

onsite for the remainder of the

SALP period.

II.

Summar

of Results

A.

Overview

The

SALP Board found that the single most prevalent

commonality

noted in the various functional areas

assessed

was that the licensee

was defining and taking actions to improve performance

but that

progress

was being

made slowly.

This situation

was almost to the

point where the slowness

of the actions

became

a dominant negative

perception

as

opposed to a positive perception of the actions

themselves.

Notwithstanding the above

comments,

licensee

improvements

were

observed

during this

SALP period, including progress

made in the

areas of concern discussed

in the 1987

SALP.

Specifically, the

licensee

has

improved programs for root cause evaluation,

procedural

compliance,

and formality of communications.

A number of key issues

were developed

during this assessment

period.

Specifically, the

NRC found that minimal design basis

information

was available for use related to plant operations

and maintenance

~ activities.

Findings in this area

demonstrate

that communication

deficiencies

between corporate

engineering

and the site

have

resulted in an incomplete understanding

of the design basis

by the

site engineering staff.

To address this concern,

the licensee

has

undertaken

the development of a configuration management

program

including design basis definition and

a site system engineering

program.

The licensee

expects this program to be of the scope

necessary

to address

these

concerns,

however the program appears

to

have

been

slow in developing.

Another area for improvement identified during this assessment

has

been the

need for fully successful

implementation of

managements'olicy

and objectives.

Although corporate

management

established

a

presence

and set the tone in response

to significant events,

management

has not established

effective feedback or performance

monitoring methods to ensure that initiatives and expectations

are

implemented

as expected.

As a result,

management

has not been

completely aware that

some initiatives had not been carried out to

the extent expected.

Notable examples of this lack of feedback

and

monitoring were in the areas

of maintenance

backlog and in the

follow through of upper management's

guidance for event

investigation actions.

Contributing to these

problems

was the fact that the quality

organizations

appeared

to be insufficiently involved in the initial

review of events

and plant problems,

and were not providing

independent verification that management's

policies were being

successfully effected.

In some specific post event cases,

the

NRC

found it necessary

to supply the impetus for the licensee's

review

and verification of planned actions which had not been fully carried

through.

The functional areas

descriptions

provide additional specific

recommendations

for management

consideration.

B.

Results of Board Assessment

Overall, the

SALP Board concluded that PG8E's

management

has

continued to be involved and concerned with nuclear safety,

and that

licensee

resources

were ample

and reasonably effective in assuring

operational

safety.

The results of the Board's

assessment

of the

licensee's

performance

in each functional area,

including the

previous

assessments,

are

as follows:

A.

B.

C.

D.

E.

F.

H.

Functional

Area

Plant Operations

Radiological Controls

Maintenance/Surveillance

Emergency

Preparedness

Secur ity

Engineering/Technical

Support

Safety Assessment/

guality Verification

Fire Protection

Rating

Last

Period'

2

1

2

1

2

Rating

Thi,s

Period

2

1

2

1

2

2

Trend~

Improving

Improving

The trend indicates

the

SALP Board's appraisal

of the licensee's

direction of performance

in a functional area

near the close of the

assessment

period such that continuation of this trend

may result in

a change in performance level.

Determination of the performance

trend is made selectively

and is reserved for those

instances

when

it is necessary

to focus

NRC and licensee attention

on an area with

a declining performance trend, or to acknowledge

an improving trend

in licensee

performance.

It is not necessarily

a comparison of

performance

during the current period with that in the previous

period.

C.

Chan

es in SALP Ratin

s from the Previous

SALP

The

NRC had administratively changed,

to some degree,

the groupings

of activities included in SALP functional areas

during this

SALP

period.

Engirieering/Technical

was not a functional area last

SALP

period and therefore

was not rated.

Maintenance

and Surveillance

were separate

functional areas last

SALP period.

However,

both

areas

received

a rating of 2 during the last 'assessment.

Safety

Assessment/guality

Verification is

a

new functional area this

period.

It is similar to,

and more comprehensive

than,

the guality

Programs

and Administrative Controls Affecting Safety functional

area that also received

a 2 rating last

SALP.

Other functional

areas

rated last

SALP period are discussed,

as appropriate,

in the

functional area analyses

for this

SALP period,

such

as training

support

and facilities are discussed

in the Engineering

and

Technical

Support functional area.

Finally, the area of fire

protection

was included in this

SALP because

of the licensee's

extensive efforts in this area which resulted in an improved

performance rating and trend.

Recognizing these facts, there

has

been essentially

no numerical rating changes

in the various

SALP

categories

from the last

SALP evaluation.

III. CRITERIA

Licensee

performance is assessed

in selected

functional areas,

depending

on whether the facility is in a construction

or operational

phase.

Functional

areas

normally represent

areas significant to nuclear safety

and the environment.

Some functional areas

may not be assessed

because

of little or no licensee activities or lack of meaningful observations.

Special

areas

may be added to highlight significant observations.

The following evaluation criteria were used,

as applicable,

to assess

each functional area:

l.

Assurance of quality, including management

involvement and control.

2.

Approach to resolution of technical

issues

from a safety standpoint.

3.

Responsiveness

to

NRC initiatives.

4.

Enforcement history.

5.

Operational

events (including response

to, analysis of, reporting

of, and corrective actions for).

6.

Staffing (including management).

7.

Effectiveness

of training and qualifications program.

However, the

NRC is not limited to these criteria and others

may be used

where appropriate.

On the basis of the

NRC assessment,

each functional area evaluated is

rated according to three performance

categories.

The definitions of

these

performance

categories

are

as follows:

~Cate or

1:

Licensee

management

attention

and involvement are readily

evident

and place

emphasis

on superior performance of nuclear safety or

safeguards

activities, with the resulting performance substantially

exceeding

regulatory requirements.

Licensee

resources

are

ample

and

effectively used

so that

a high level of plant and personnel

performance

is being achieved.

Reduced

NRC attention

may be appropriate.

r

~Cate

or

2:

Licensee

management

attention to and involvement in the

performance of nuclear

safety or safeguards

activities are

good.

The

licensee

has attained

a level of performance

above that needed

to meet

regulatory requirements.

Licensee

resources

are adequate

and reasonably

allocated

so that good plant and personnel

performance

is being achieved.

NRC attention

may be maintained at normal levels.

~Cate or

3:

Licensee

management

attention to and involvement in the

performance of nuclear safety or safeguards

activities are not

sufficient.

The licensee's

performance

does

not significantly exceed

that needed to meet minimal regulatory requirements.

Licensee

resources

appear to be strained

or not effectively used.

NRC attention

should

be

increased

above

normal levels.

IVA

Performance

Anal ses

A.

Plant

0 erations

1.

~Anal sis

During the assessment

period; the licensee's

plant operations

activities were observed routinely by both the resident

and the

regional inspection staff.

Over 1600 hours0.0185 days <br />0.444 hours <br />0.00265 weeks <br />6.088e-4 months <br /> of inspection

effort were devoted to this functional area.

The licensee

was

noted to have

had several

accomplishments

in the operations

area during this

SALP period,

such

as

improvements

in the

formality of communications,

in attitudes

towards procedure

compliance,

and in timeliness of reporting, all of which were

concerns

from the previous

SALP.

Another improving trend in

the licensee's

performance

has

been

an improvement in the

formal review of operational

events

and the formalization of

the consequent

action plans.

However, events did continue to

occur due to a lack of procedural

compliance

and the failure to

stop activities in the face of uncertainty.

These

problems

and

others

appear to have

been exacerbated

by some middle

management's

(site

and corporate)

missed opportunities

on a

day-to-day basis to provide feedback

and to interact with plant

staff.

In the plant operations

area,

high-level corporate

management

has frequently been involved in site activities.

As an

example,

Vice President

Nuclear

made

a weekly trip to the site

to discuss plant performance.

In addition, in response

to

plant events

management

established

a presence

and set the tone

for collecting information, establishing

root cause

and taking

corrective actions,

as evidenced

in the July 17,

1988 natural

circulation cooldown event at Unit 2 due to ground faulting.

However,

management

has not been totally effective in

establishing

feedback or performance monitoring methods to

ensure that initiatives and expectations

are

implemented

as

expected.

Examples of this are the relatively high number of

illuminated control

room annunciators,

the failure of some

plant supervision to satisfy their requirements

for plant

surveillance tours

and interaction with plant staff as noted

during the April 26 management

meeting,

and the absence

of

gA/gC overview of post event action plan implementation.

The licensee's

approach to the technical resolution of plant

problems resulting from operational

events

has generally

improved over the inspection period.

As late

as about half way

through the period

some restart

reviews were not thorough in

that they lacked indepth root cause

analysis

and did not probe

ancillary problems

experienced

during events.

For example,

following the December

13 Unit 1 reactor trip due to a main

feedwater

pump trip, the licensee

did not thoroughly address

problems

noted during the event with the condenser

steam

dumps,

resulting in a subsequent

turbine trip at low power.

Towards

the end of the period,

the licensee

had improved the'estart

review process

by implementing detailed action plans which

address

both the root cause of the event

and ancillary problems

experienced.

The licensee

was in the process

of incorporating

these

changes

in the restart

procedure at the end of the

period.

However, the licensee

has

been

slow in establishing

formal root cause

reviews for less significant operational

events

which warrant 'changes

to plant procedures

or programs.

For example, guality Evaluations,

the lowest level of root

cause evaluations,

were not initiated for the March 10

pressurizer

pressure

transient at Unit 1 or the June

1

Auxiliary Feedwater spill at Unit 1.., Both of these

events

warranted

changes

to plant procedures.

The licensee's

responsiveness

to

NRC initiatives in the

operations

area

has

been generally adequate.

The licensee

has

made progress

in priority issues

addressed

in the previous

SALP

such

as procedural

compliance,

formality of communications

and

sensitivity to seismic

issues.

As an example,

in the area of

seismic sensitivity, the licensee identified in this period

a

number of operability concerns

when seismic

supports

were

identified to be missing

on equipment.

However,

as discussed

below, events

during the assessment

period indicate that

continued attention is warranted in the areas

of communications

and procedural

compliance.

Three enforcement

items were assigned to'this functional area

for two occurrences

dealing with attention to procedures.

First,.the overpressurization

of the Unit 1 Reactor Coolant

Drain Tank on March ll, resulted

from operations

personnel

going beyond the scope of their procedure.

Second,

the lack of

meaningful

acceptance

criteria for the containment

fan cooler

unit operation

was not noted by operators

in either unit.

Other operational

events during the period also resulted

from

plant personnel

proceeding

beyond the scope of their procedures

and authority,

such

as the January

31 turbine runback at Unit 2

which resulted

from an operator incorrectly using

a multimeter

he was not qualified to use.

The issue of plant personnel

proceeding in the face of uncertainty

was discussed

with

licensee

management

during the April 26 management

meeting,

and

war rants continued attention.

Examples of proceeding in the

face of uncertainty included the Unit 1 containment ventilation

isolation early in the

SALP period on February 17,

1988 (in

which the shift Foreman

concurred to the "functionality" of a

miswired flow transmitter)

and the September

1, 1988 Unit 1

reactor trip, soon after the

end of the

SALP period (in which a

shift foreman did not take action to open

an instrument root

valve which ultimately caused

the trip).

These .examples of

communication

breakdowns

indicate that management

attention to

revising the "culture" in operations

has not yet been fully

effective and that an overall operational attitude which

aggressively identifies, elevates

to management

attention,

and

resolves

problems is required in the operations

functional

area.

As shown by the synopsis of licensee

event reports

(LERs) in

Tables

5 and 6,

a large portion of the events

in the operations

area during the period fall into established

problem areas,

such

as procedural

inadequacy

or non-compliance.

In addition

to procedural

problems,

the most predominant

source of events

due to human error were in the category of'rong unit, wrong

train.

This category of events

was addressed

by the licensee's

Human Performance

Evaluation

System group resulting in changes

. to operating procedures

and t'raining to avoid this type of

error.

Another source of events in this area

were

a number of

containment

and fuel handling buil,ding ventilation mode changes

due to instrumentation sensitivity to electronic noise.

Although the licensee

has

a program to eliminate these types of

problems, its implementation

has

been

slow.

In general,

events

were reported in a timely fashion

and information and analysis

was complete.

The licensee's

qualified and licensed operational staffing,

on

shift and otherwise available,

continued to be ample

and well

qualified.

Overall, operations

personnel

appeared

to be

knowledgeable

of plant systems

and performance,

and responded

to significant and complicated

events effectively and

professionally.

For example,

operators

responded

quickly and

prudently to the impending failure of an isophase

bus motor

operated

disconnect

on November

7 at Unit 2,

as well as, to

ground indications

on vital buses at Unit 2 of July 17.

During the reporting period one replacement

examination

was

conducted in December

1987 by the

NRC.

A total of twelve

reactor operator candidates

and three senior operator

candidates

were administered written and operating tests

during

the replacement

examination.

All twelve reactor operator

candidates

and all three senior reactor operator

candidates

passed

these

examinations.

No generic weaknesses

were observed

during these

examinations.

The facility has

used the

NRC

Examiner Standards

for their own requalification examination

format and content.

They have also

been responsive

to

NRC

initiatives for developing

a facility question

bank for

facility and

NRC use.

2.

Performance

Ratin

Category

2, Improving trend.

3.

Board Recommendations

Licensee

management

should continue to develop sensitivity in

the maturing period of operations

towards the development of

proper attitudes with respect to thorough communications,

work

practices

related to procedural detail

and compliance,

and not

proceeding in the face uncertainty or freelancing.

In

addition,

management

should assure that there is an acceptable

degree of management

and supervisory

involvement in the

day-to-day operations

of the plant, including plant visibility,

and first hand assessments

of the implementation of initiatives

and expectations.

The licensee

should continue to improve its

root cause analysis of events

and lower the threshold of the

use of quality evaluations

to include less significant events.

Radiolo ical Controls

1.

~Anal sis

Five inspections

were performed in the radiological controls

area during this appraisal

period.

More than 312 hours0.00361 days <br />0.0867 hours <br />5.15873e-4 weeks <br />1.18716e-4 months <br /> were

expended

in the areas of occupational

radiation protection,

radioactive waste

management,

and radiochemical

confirmatory

measurements.

In addition, the resident inspectors

provided

continuing observations

in this area.

The licensee

demonstrated

excellent performance

in keeping

exposures

ALARA during the early part of the appraisal

period.

Specifically in 1987, which included

a Unit 2 refueling outage

and

a major portion of underwater fuel pool reracking for Unit

1,

DCPP only expended

335.6 person-rem for both Units.

The

1987 average for

PWR plants

was

372 person-rem

per Unit.

However, during the latter part of the appraisal

period, the

licensee

experienced

problems that challenged their ALARA goal

for 1988.

Specifically, the licensee

established

a goal of 600

person-rem for 1988, that included exposures

for a Unit 1 and

Unit 2 refueling outage

and underwater

spent fuel pool

reracking for both Units.

As of June

30, 1988,

about 442

person-rem

had been

expended with the fuel pool reracking

completed for Unit 1 and about two weeks remaining

on the Unit

1 refueling outage.

The Unit 1 outage

was extended in excess

of 45 days

due to unexpected

and unplanned

tasks that evolved

during the outage.

The licensee

also experienced

exposure

levels that were 10-20K higher than expected for the Unit 1

outage.

Although the Radiation Protection

Department

had done

an excellent job in ALARA planning,

they observed

excessive

time and dose

expended

in radiation areas

due to inefficient

preparation

and planning by various work groups,

which were

brought to management's

attention

and acted

upon

on

a case

by

case

basis.

During an

NRC outage

inspection,

similar

observations

were also brought to management's

attention.

The

poor ALARA practices

observed

represented

a need for

improvement in management

oversight from all

DCPP Departments.

The licensee attributed most of the inefficiencies to the large

force of contract workers

who lacked nuclear plant experience.

To prevent similar problems during the upcoming Unit 2

refueling outage,

DCPP's

management

has decided to establish

an

inplant central control work center that will be manned

24

hours per day and

7 days per week by key decision making plant

staff (foreman

and above).

These individuals will have the

responsibility to observe

work in progress

and target the

identification and response

to inefficient work practices.

In

addition, onsite

and corporate

higher level management

plan to

spend

more time inplant during the Unit 2 outage.

During an

NRC maintenance

team inspection,

which occurred late in the

SALP evaluation period,

a clear

understanding

of the concept,

individual and organizational

responsibilities

of ALARA by

maintenance

and I8C foreman

and craftsmen/technicians

was

identified.

The inspection

included

an examination of the work

order generation

process

as it applied to ALARA.

The process

was

such that reviews were performed using historical

and

current data with appropriate

levels of supervisory

and

management

review.

Post

ALARA reviews were performed which

were factored into the historical data base.

With the Unit 2

refueling outage

remaining for 1988,

DCPP still expects

to meet

or be below the

PWR average.

The licensee

continued to

experience.

good fuel performance for both Units.

During this appraisal

period, the licensee

continued to

demonstrate

managements'nvolvement

in ensuring quality.

The

licensee

met the challenge of an extended

Unit 1 refueling

outage

and underwater fuel pool reracking for both Units with

no significant radiological

problems.

In one example,

10

immediately after

an event

on December

9=, 1987, involving a hot

particle incident during the Unit 1 underwater fuel pool

reracking task,

DCPP's

management

took immediate steps

to

determine

the root cause

and implement corrective actions to

prevent recurrence.

Another example of program quality was

noted in the licensee's

conservative

approach to ensure that

all safety precautions

were taken

and minimal exposure

expended

when

a Unit 1 incore detector

was stuck out of the five path

position.

Corporate

support

and involvement with onsite

activities appeared

to be excellent throughout the appraisal

period.

The licensee's

program for radiochemical

measurements

was excellent.

Radiochemical

procedures

and measurement

quality control practices

were well-considered

and consistently

implemented.

Accuracy of radiological

measurements

was good

when compared

by the

NRC Mobile Laboratory.

The licensee

continued to resolve technical

issues with

appropriate

conservatism,

technical

expertise

and supporting

documentation.

The issues

addressed

included clarification of

the reporting requirements. for process

monitor alarms,

deficiencies

in the radioactive

laundry cleaning facility's

ventilation

system,

and exposure

evaluations

due to hot

particle contaminations.

The licensee

has

been responsive

to

NRC initiatives with

conservatism

routinely exhibited.

One example concerning

an

inspector's

observations

of poor operating conditions involving

the licensee's

clean waste sorting operations

was immediately

acted

on by licensee

management.

This operation

was

immediately halted

and did not resume until work practices

were

brought

up to industry standards'he

last

SALP Board

Recommendation

addressed

the reduction of liquid radioactive

effluents.

Annual discharge

beginning in 1986 totaled

approximately

11 and

5 curies respectively with approximately

1

curie in the first half of 1988.

Two Severity Level IV violations and

one associated

deviation

were identified during this appraisal

period.

The violations

involved the failure to maintain access

controls to very high

radiation areas

in accordance

with Technical Specifications

requirements

and adherence

to radiological

access

control

procedure.

The deviation,

assessed

in the engineering

and

technical

support

area involved radiation monitor data that

were not being recorded in the control

room rack as described

in the licensee's

FSAR.

The violations were not representative

of a programmatic

breakdown,

however they did indicate

a need

to improve management

oversight

and attention to detail.

Four

LERs were submitted in this functional area during this

appraisal

period.

Two of the

LERs were for failure to maintain

access

controls to very high radiation areas

in accordance

with

Technical Specification requirements.

One of these

LERs

involved two separate

incidents.

The

NRC inspection of these

events identified one violation described

above.

In addition,

11

although the licensee

had informed the Region

V Office of the

incidents,

the licensee

did not have

a clear

command of the

reporting requirements

based

on their interpretation of 10 CFR Part 50.73

and

NUREG. 1022,

Supplement

1.

To their credit the

licensee

aggressively

pursued

understanding

and reported these

events after consultation with the NRC's

AEOD/TPAB Branch.

The

other two LERs involved the failure to perform a plant vent air

sample flow estimate

and high radiation levels from a hot

particle that caused

the Unit 1 Fuel Handling Building

Ventilation System to shift to the iodine removal'ode.

With

respect to these

two LERs, corrective actions

were timely and

effectively implemented.

Staff positions

are identified and authorities

and

responsibilities

are well defined.

Expertise

was available in

both the plant and corporate staffs

and the

use of outside

consultants

continued to be minimal.

Experience

levels for

management

and technician staff's continue to meet and/or

exceed

commitments

made

by the licensee.

Corporate

management

oversight

and technical

support

was observed

during

inspections,

especially during refueling outages

and other

major onsite tasks.

2.

Performance

Ratin

Category

1.

3.

Board Recommendations

Licensee

management

of all departments

should continue to focus

their attention

on ensuring that all personnel,

with emphasis

on an inexperienced

contractor

or

new employees,

are

knowledgeable

of and practice

ALARA concepts

and improve work

efficiencies in radiation areas.

Mid-level management

should

increase

oversight to improve the level of attention to detail

and to ensure that procedural

requirements

are adhered

to by

all levels of their staffs'.

C.

Maintenance/Surveillance

1.

~Anal ala

This functional area

was observed routinely during the

assessment

period by both the -resident

and regional inspection

staff.

Approximately 1269 hours0.0147 days <br />0.353 hours <br />0.0021 weeks <br />4.828545e-4 months <br /> of inspection effort were

devoted to this functional area.

In addition,

a team

inspection in October

1987 focused

on plant chemistry and

another

team inspection in July 1988.focused

on maintenance

activities.

The licensee

has

shown improvement in the area of

formality of communications

between operations

and

maintenance/surveillance

personnel,

which was raised

as

a

concern in the last

SALP.

Another identified strength

was

improved mechanical

and electrical

maintenance

procedures.

Also, the licensee

consolidated

the maintenance

organizations

12

(electrical

and mechanical

maintenance,

I&C, procurement,

and

work planning)

under

one Maintenance

Manager which holds the

potential for improved coordination of maintenance activities.

Problems

from the previous

SALP, which the licensee

has not

dealt with in an effective manner,

were (1) the tracking and

control of maintenance

backlog, particularly in the

I&C area,

and (2) the continuing relatively large

number of personnel

'errors reported.

Other weaknesses

identified during this

SALP

period included

I&C procedures,

engineering

involvement,

and

occasionally

slow implementation of industry and site specific

experience

lessons

learned.

Management

was usually involved in site activities and there

was consistent

evidence of prior planning

and assignment

of

priorities.

For example,

the licensee's

programs for

procurement

and storage of materials

were examined

and found to

be well executed

and supported

by management.

However,

as

noted in the cover letter to the May 5,

1988 inspection report,

in some

cases

specific management

expectations

were repeatedly

not implemented

such

as those dealing with foreign material

exclusion.

Additionally, the maintenance

backlog problems

and

the excessive

number of illuminated control

room annunciators

as discussed

in the April 26 manag'ement

meeting

and identified

during the maintenance

team inspection is indicative that

management

has not been completely effective in controlling and

supporting maintenance activities.

A significant improvement,

which was indicative of management

involvement,

was

made in the area of mechanical

and electrical

maintenance

procedures

that were revised during this period.

These

procedures

included

good detail

and quantitative data,

and provided specific instructions

and guidance to the craft.

In contrast,

some

segments

of I&C procedures

were found to be

marginal.

Examples of weakness

included the instrumentation

loop tests

and calibration procedures

for measuring

and test

equipment,

which appeared

to provide inadequate

guidance.

Additionally, at the end of the

SALP period it was determined

that important procedure

changes,

some necessary

to avoid plant

trips,

had been

requested

by ICC technicians

but had not been

implemented over a long period of time.

The licensee,

towards

the

end of the assessment

period had applied additional

resources

to revise

I&C procedures.

"Further, in the evaluation of management

involvement,

the

maintenance

inspection

team in July 1988 found that (1)

licensee

management

had not proper ly assessed

the safety

significance of current. maintenance-related

problems,

(2)

programs for measuring

and improving maintenance

performance

were weak, (3) performance

standards f'r maintenance

personnel

were not well defined,

and (4) the quality program

organizations

had missed opportunities to improve the

maintenance

program.

II

13

In the area of resolution of technical

issues for the

maintenance

and surveillance

area,

the licensee

generally

established

a clear understanding

of issues.

The licensee

properly acted

upon

a number of potentially generic

issues

discovered

as

a result of maintenance

and surveillance

activities.

For example,

the 48 inch containment

purge valves

were determined to have

a preferential direction for leak tight

operability during testing.

The licensee

took a conservative

and technically sound approach of reversing the valve through

a

design

change.

However, the licensee

was slow and in some

cases

not thorough in incorporating industry experience

into

maintenance activities

as identified by the maintenance

team

inspection for the plant air systems.

In addition, in some

cases

the licensee

was slow in learning from their own

experience

as with the December

17 turbine trip due to steam

dump problems despite

a history of similar problems which

dictated the

need to perform thorough electrical

and mechanical

grooming of the valves prior to startups.

The licensee's

efforts to learn from their own'and industries

experience

deserves

continued attention.

Also, during the

SALP period, plant engineering

had

occasionally

shown

a lack of understanding

and critical

assessment,

of technical

issues

in the maintenance

and

surveillance

areas.

As an example,

engineering did not propose

any corrective maintenance

action

on the component cooling

water surge tank isolation valve when its stroke time increased

dramatically.

Although, the stroke time remained within the

"Action" limit, the increased

stroke time indicated

impending

problems.

Following the issuance

of a notice of violation in

this area,

the valve exceeded

the "Action" limit and was

declared

inoperable.

In addition, engineering

has failed twice

in the last year to perform administrative functions necessary

to update recurring task schedules

resulting in missed

surveillances

in the Inservice Test (IST) area.

Similarly,

weaknesses

identified in the maintenance

team inspection

were

primarily attributable to inadequate

engineering

involvement

and lapses of management

oversight.

The licensee

received ten notices of violation in this area.

The violations highlighted weaknesses

described

in this

functional area.

The violations included three instances

where

plant configuration did not meet design or design drawings,

two

~ . instances

of procedural

non-compliance,

and two for failure to

maintain cleanliness

controls around the reactor coolant system

during the refueling outage.

The licensee

reported twenty-nine events with causes

attributable to this area.

Of these,

eighteen

were attributed

to personnel

error or procedural

deficiency, of which one led

to a reactor trip.

The reactor trip was

due to an attempt to

perform maintenance

on

a shared 'leg of the three, reactor

coolant flow transmitters

of one loop.

Due to an overly

permissive

I8C surveillance

procedure

and what appeared

to .be

a

14

lapse of management

attention to this critical plant activity,

a technician

was allowed to go beyond the scope of the written

methods

based

on a verbal

concurrence

from supervision.

The

other eleven events

resulted

from design,

manufacturing or

installation errors

or component failures.

Generally,

the

licensee

performed

a thorough assessment

of the causes

of these

problems

and identified reasonable

corrective actions.

The licensee

s response

to

NRC initiatives,

such

as the problem

associated

with counterfeit material,

was found to be

comprehensive

and timely.

The licensee's

efforts in the areas

of Inservice Inspection (ISI) and the containment

integrated

leak rate test (ILRT) were examined

and found to be properly

implemented

and technically "state-of-the-art".

In regards to

the conduct of the

ILRT on Unit 1, licensee

engineering

personnel

demonstrated

a proper inquisitiveness

and

consequently identified a potentially generic problem regarding

a preferred seating direction for large butterfly valves

as

was

discussed

above.

However, there were

a number of instances

discovered

by the licensee

during this period where plant

maintenance activities in the past

have adversely affected

equipment seismic qualification.

This points to a need for

more detailed

design basis

documentation

and implementation in

procedures

and training which was also reinforced by the

maintenance

team inspection.

A special

chemistry

team inspection

was conducted

during the

SALP evaluation

pet iod.

A total of 218 hours0.00252 days <br />0.0606 hours <br />3.604497e-4 weeks <br />8.2949e-5 months <br /> of inspection

effort was expended

in this area excluding the confirmatory

measurement

of radioactive

species

inspection which was

conducted concurrently.

,The confirmatory measurement

program

is addressed

in the Radiological

Control portion of the report.

It appeared

that plant and corporate

management

provided

appropriate

levels of support

and supervision to chemistry

related activities.

The licensee's facilities were found to be

"state-of-the-art" for both primary and secondary

analyses.

In

the area of systems affecting plant chemistry,

the team found

the licensee

to be aware of the advantages

of improved chemical

control

and active in pursuing

improved control.

The

licensee's

efforts in erosion/corrosion

control were found to

be above industry standards.

With respect to the Post Accident

Sampling System

(PASS), it was found that the systems

met the

intent of NUREG-0737, that technician training and retraining

programs

were acceptable

and that appropriate administrative

control measures

had been

implemented.

'n July 1988, the maintenance

area

was reorganized

by the

licensee,

as previously mentioned, to include mechanical,

electrical,

I&C, work planning,

and procurement.

This area

was

generally well staffed

and

had

key positions identified and

responsibilities

defined.

In the mechanical

and electrical

area,

expertise

was available within the staff and staffing

appeared

to be ample to control backlog.

In the

IKC area,

15

staffing appeared

strained with overtime necessary

to control

backlog

and the

use of consultants

to revise procedures.

Training of maintenance

personnel

continued to be

a strength.

It appeared

from the

SALP Board analysis that the training

program

and personnel

knowledge

has prevented

a greater

number

of plant events related to I&C activities.

However, in

mechanical

maintenance

one enforcement

item dealt with

refueling outage contract personnel

inadequately

prepared to

change

a gasket in the safety injection system.

The lack of

training contributed to the failure to follow procedural

requirements.

2.

Performance

Ratin

Category

2

3.

Board Recommendations

In the maintenance/surveillance

area,

licensee

management

should take steps to:

1) integrate,

in a timely and thorough

manner, configuration control measures

including design basis

information; 2) assess

and incorporate

lessons

learned

from

plant experience

and industry experience;

3) increase attention

in the

I&C area particularly with regard to adequacy of

staffing,

and procedure quality; 4) encourage

integration of

engineering into the program

and problem resolution processes;

5) enhance

programs for measuring

and improving maintenance

performance

and 6) instill the attitude that activities are to

be stopped

whenever there is any uncertainty.

Emer enc

Pre aredness

1.

~Anal sis

Inspections

performed during this

SALP period included

one

routine inspection

and the observation of the annual

emergency

preparedness

exercise.

Approximately 151 hours0.00175 days <br />0.0419 hours <br />2.496693e-4 weeks <br />5.74555e-5 months <br /> of direct

inspection

was devoted to the assessment

of emergency

preparedness

at Diablo Canyon Nuclear

Power Plant.

Licensee

performance

during this assessment

period demonstrated

management

was actively involved in achieving quality. Decision

making regarding

changes

to the emergency

preparedness

program

appeared

to be at a level that assures

adequate

management

review.

Management

review of items affecting emergency

preparedness

have

been thorough

and technically sound.

Corporate

management

was actively involved in matters affecting

site emergency

preparedness

and supports

the site's efforts

regarding

emergency

preparedness.

This was most recently

exemplified by the Vice President,

Nuclear

Power Generation

serving

as

an observer of the Emergency Operations Facility

activities during the August 1988 emergency

preparedness

I

16

exercise.

Records

and documents

related to emergency

preparedness

are well maintained

and available.

The licensee's

approach to the resolution of technical

issues

from a safety standpoint

has always

been conservative

and

technically sound.

An examination of some of the licensee's

declared

emergency

events

demonstrated

conservative

classifications

and actions.

The licensee

has evaluated

technical

issues affecting safety thoroughly and resolutions of

the issues

regarding

emergency

preparedness

have

been

conservative

and timely.

One recent

example in this area

was

improvements to the licensee's

classification procedure

EP-G-1.

EP-G-1 was significantly revised to be conservative

and to

remove

some of the "grey areas"

or judgement calls that

may

lead to a non-conservative

classification of an emergency

event.

Other

improvements

included

an increased

emphasis

on

event reportabi lity and classification

noted in the simulator

training and the introduction of more specialized

courses for

managers

and decision

makers in emergency

response.

Licensee

management

has

been very responsive

to concerns

identified by the

NRC.

Timely and thorough corrective actions

have

been initiated when concerns

were brought to their

attention.

There were

no violations identified during this assessment

period,

and

no licensee

event reports.

The staffing and training in the functional area of emergency

preparedness

continues to exceed

the industry norm.

This is

evidenced

by the improvements to emergency training mentioned

above

and the capabilities of the emergency

response

organization

demonstrated

during the annual

exercise.

Emergency

response

training records

were current

and well maintained.

Performance

Ratin

Category l.

3.

Board Recommendations

The licensee

should continue'o maintain management

attention

to ensure

a continued high level of emergency

preparedness

at

Diablo Canyon.

E.

~Securi t

~Aaa1 sis

During this assessment

period of August 1,

1987 through July

31,

1988,

Region

V conducted

two physical security inspections

at the Diablo Canyon Nuclear Power Plant.

A total of

approximately

260 hours0.00301 days <br />0.0722 hours <br />4.298942e-4 weeks <br />9.893e-5 months <br /> of direct inspection effort were

conducted

by regional

inspectors.

In addition, the resident

17

inspectors

provided continuing observations

in this area.

There were

no material control

and accounting inspections

conducted during this assessment

period.

With regard to management's

involvement in assuring quality,

corporate

and plant management

continued to review the

operation of the overall security program.

They have generally

implemented

remedial

measures

to correct deficiencies

identified in the course of both internal

and

NRC security

inspections.

In May 1988, the licensee

moved to a temporary

access facility and began to upgrade their permanent security

access

control building.

This remodeling is scheduled

to be

completed

by April 1989.

Additionally, during this assessment

period,

the licensee

replaced their security card readers

with

more reliable units.

Since August 1986,

each security inspection report has

identified deficiencies with installed closed circuit

television

(CCTV) cameras.

Some deficiencies

were minor,

however,

some deficiencies

rendered

many cameras

ineffective.

During this assessment

period, plant management

indicated that

actions

would be accelerated

to resolve continuing maintenance

and

image clarity problems with the

CCTV cameras.

The previous

SALP report

recommended

that Security,

Maintenance

and Operations

Departments

improve their internal coordination

to resolve

concerns

regarding plant work crews

removing

portions of vital area barriers without considering the

secur ity impact of their actions.

During this

SALP period,

improved coordinations

have resolved this previous

concern.

Additionally, security

management

demonstrated

a coordinated

effort with other plant staff in preventing safety/security

problems at Diablo Canyon.

The previous

SALP report

recommended that the licensee

resolve

the safety/security

issue involving radio communication

frequencies

for security

and operations

personnel.

During this

assessment

period,

the security

management

began modifying

their radio communication

equipment to avoid possible

interference with the radio communication

equipment assigned

to

the Units

1 and

2 operations staff.

These modifications are

approximately

70K complete.

During the assessment

period, four information notices related

to security were issued.

These related to criminal prosecution

by the

US Department of Justice resulting in the conviction of

two individuals for falsification of security training records;

the discovery of falsified pre-employment

screening

records;

potential

problems resulting from security weaknesses

identified during safeguards

Regulatory Effectiveness

Reviews;

and weaknesses

in the

use

and protection of Safeguards

Information.

The lice'nsee's

actions,

as reviewed to date,

were

found to be appropriate,

however,

the last three information

18

notices

were issued after the most recent of the two security

inspections.

In response

to the August 1986,

NRC policy statement

on Fitness

for Duty of nuclear

power plant personnel,

corporate

and plant

management

continued to support their established

Fitness for

Duty Program.

As designed,

this program requires that all

applicants

seeking on-site

employment

must satisfactorily

complete

a pre-employment

drug and alcohol urinalysis test.

Current on-site

employees

were grandfathered

into the program

and were not required to pass

a urinalysis test.

The current

Fitness

for Duty Program

does

not follow the industrial

standards

published

by Edison Electric Institute (EEI) i.e.,

the requirement for random or regular periodic chemical testing

is not included.

The enforcement history for the period of August 1,

1987

through July 31,

1988 included two Severity Level IV violations

related to the licensee's

failure to properly escort

a visitor

inside the protected

area,

and their failure to provide

an

adequate

clear zone for surveillance

around

a portion of the

protected

area perimeter.

During this

SALP period, Diablo Canyon reported

eleven

-safeguards

events.

Seven

(64K) of these

events

were caused

by

personnel

error.

Nine of these

events

occurred after

a change

in the requirements

of 10 CFR 73.71(c),

and thus were reported

in the Licensee

Event Report

(LER) format.

These

eleven events

related to:

failed security compensatory

measures(4);

degraded

barriers(3);

drug-related

events(2);

and miscellaneous

events(2).

During the past four years,

the perimeter security alarms at

the Intake Structure

have

been inoperative

and the licensee

has'ontinued

to provide long term compensatory

measures

at this

area.

The licensee

needs to finalize their changes

to the

design of both the security barriers,

and the associated

perimeter security alarm system at the Intake Structure.

Three

of the four safeguards

events

concerning the failed

compensatory

measures

involved security officers being found

inattentive at their security posts at the Intake Structure.

These security officers had been posted at the perimeter

of

this separated

protected

area to compensate

for the inoperative

perimeter alarms.

With respect

to staffing,

key positions

were identified and

responsibilities

were generally well defined.

The security

training staff appears

capable of performing its assigned

missions.

2.

Performance

Ratin

Category

2.

19

3.

Board Recommendations

Licensee

management

is encouraged

to finalize their

modifications to the protected

area barrier and the perimeter

alarms at the Intake Structure.

Additionally, the licensee

is

encouraged

to minimize the deficiencies

and to improve the

image clarity of their

CCTV cameras.

Further,

the licensee

is encouraged

to reexamine their current

Fitness for Duty Program with respect to the

EEI guidance

pertaining to chemical testing of body fluids;

En ineerin

and Technical

Su

ort

1.

~Anal sis

During the assessment

period, the licensee's

engineering

and

technical

support activities were observed routinely by both

the resident

and the regional

inspection staff.

Approximately

208 hours0.00241 days <br />0.0578 hours <br />3.439153e-4 weeks <br />7.9144e-5 months <br /> of inspection effort were devoted to this functional

area in addition to extensive

management

review.

The

engineering

department

has initiated a number of programs

to

deal with identified weaknesses

such

as the configuration

management

process

and the system engineering

program.

However, these

programs

have progressed

slowly and

as

a result,

design

and plant configuration information is not readily

available to the site for implementation.

In addition,

engineering analysis of operations

and maintenance activities

has

been limited by a slow implementation of the system

engineering

program.

In the engineering functional area,

there

was evidence of prior

planning and assignments

of priorities.

The licensee's

efforts

in the seismic re-evaluation

program demonstrated

a high level

of management

involvement and control of the quality and

timeliness of this engineering effort in that the license

condition was met on schedule.

In other instances,

implementation of engineering

improvement

items

was sometimes

slow and incomplete.

The issue of greatest

concern in the

engineering

and technical

support area

has

been the

implementation of the design basis into plant operations

and

maintenance.

In addition to'ndustry-wide findings ot

inadequate

design

and configuration management,

at Diablo

Canyon

a number of events

and findings pointed to a need for

emphasis

by the licensee in this area.

Events in this area

included

a number of instances

where components

had.seismic

bracing inadvertently

removed,

including a main steam line

'estraint

disassembled

at power,

and the auxiliary saltwater

system performance limits were challenged

by, what appeared

to

be,

an improperly thought out change to an operating procedure

setpoint.

The licensee

recognized

the

need for enhancing configuration

management

and initiated a task force to evaluate

what

20

improvements

were

needed

and

how to implement them.

The

licensee

has considered

such aspects

as what should

and'houldn't

be contained

in a design basis

document

and what

organization is to be responsible

for it.

At the

end of the

period few recommendations

had been

implemented.

Although the

licensee's

planned efforts appear

to be comprehensive,

the

implementation

schedule

was not defined at the end of -the

SALP

evaluation period.

At the start of the assessment

period, the licensee

recognized

the

need for independent

engineering oversite of the operation

and maintenance

of plant systems

and established

the system

engineering

program.

The maintenance

team inspection,

conducted at the

end of the period identified that the system

engineering

program

had not been fully developed.

The issues

raised

by the team included inadequate

training and

requirements

for system engineers

in addition to a poorly

defined job scope.

As an example,

the team found that the

system engineer

responsible

for air systems

did not have

a

thorough understanding

of the plant air system.

Further,

the

maintenance

team was unable to obtain from the licensee

a clear

definition of safety significance of certain air system

check

valves although the questions

were posed early in the

inspection.

In their approach

to the resolution of technical

issues

and in

response

to

NRC initiatives, the licensee

often performed

thorough detailed technical

reviews,

such

as the analyses

of

pressurizer

surge line movement

and main steam line noise.

Also, the licensee's

analyses

and proposed

Technical

Specification

changes

to reduce

the potential for reactor trips

was considered

a conservative,

well-thought-out effort.

However, in other cases

inspectors

found that both corporate

and plant engineering

did not take the initiative on potential

safety problems, with the result that

NRC inspectors

supplied

the impetus.

An example of this was the discussion

on the

design of the auxiliary salt water system which began in April

1988,

was only, recently responded

to by the licensee,

and

has

not yet been resolved.

In addition, engineering

was slow and

'not completely accurate

in establishing definitive

acceptance'riteria

for equating

RCS leakage to the containment

fan cooler

condensate

system collection rate, after the subject

was raised

as

an

NRC concern.

As discussed

in the maintenance

and

surveillance

area,

engineering

performance

in the surveillance

testing area

was noted to have weaknesses

regarding engineering

judgement

and follow through (the failure to identify valve

RCV-16 for maintenance after testing

showed erratic stroke

.

times)

and engineering administrative actions (failures to

update test schedules

led to missed surveillances)

and failure

to have

an administrative procedure for changing

IST acceptance

parameters.

One strength

and

key improvement over the

assessment

period has

been the increased direct involvement in

plant operations

and operational

events

by the Onsite Project

Engineering

Group

(OPEG).

This group

was instrumental

in

21

identifying a missing main steam line pipe restraint

as

an

operability concern

and in another

instance identifying a poor

maintenance

practice of not blocking pipe support spring cans

when draining water filled lines.

An additional

concern regarding the timeliness of important

engineering actions

was identified soon after the

end of the

SALP period.

On September

1, 1988 Unit 2 experienced

a reactor

trip due to planned testing of the seismic trips.

The reactor

trip would not have occurred if appropriate

design

change

actions, identified after

a precedent trip on March 5, 1988,

had been

implemented.

Also, on September

1, 1988, Unit 1

experienced

a reactor trip during an attempted

startup

due to a

turbine antimotoring device being inadvertently valved out.

The closure of the valve had been

noted

and documented

on

August 6,

1988 by an engineer

and

made

known to the shift

foreman.

The lack of action in the ensuing

weeks directly

caused

the unnecessary

reactor trip.

In the area of engineer ing, five enforcement

items were issued.

One violation concerned

erroneous

dimensions

used in a

calculation regarding available reactor

head vent area.

This

particular notice of violation highlighted

a lack of

understanding

of a fundamental

practice

such

as

independent

verification of design inputs

by an engineering

group.

A

violation for a lack of cleanliness

controls

assessed

in the

maintenance

area

on the

same job highlighted

a lack of

understanding

of fundamental

cleanliness

controls

by the

involved field engineering

group as well as the maintenance

personnel,

who were ultimately responsible.

In addition two devi.ations applicable to both units were

assessed

in the engineering

area.

The deviations

were

departures

from FSAR committments to have control

room

recorders for radiation monitors

and to have redundant

power

supplies for certain

steam generator

level instrumentation.

These deviations

demonstrated

a lack of follow through in the

area of committments.

The licensee's

engineering organizations

included

a plant

engineering

group reporting to the plant manager,

the Nuclear

.

Engineering

and Construction

Group located in San Francisco

with a group onsite,

and the Nuclear Operations

Support group

also in San Francisco.

The licensee's

engineering

groups

were

generally.. well staffed with considerable

resources.

However,

there

appeared

to be

a need to f'ully implement the licensee

committment to a system engineer

program at the plant to assure

appropriate

maintenance

of the plant de'sign basis in the

operation of the units.

The facility's training programs for both licensed

and

non-licensed

personnel

have

been accredited

by INPO.

The

facility simulator has generally performed well and properly

models almost all scenarios

used to date

by the

NRC.

In

22

addition, the facility continued,

as discussed

in previous

SALP's, to have outstanding

technical training facilities.

These facilities appear to have the capability to simulate

and

provide training for a substantial

number of potential

evolutions encountered

by plant personnel.

In summary,

the

technical

support provided by the plants training staff was

found to be well executed

and included adequate staff and

outstanding training facilities.

2.

Performance

Ratin

Category

2

The

SALP Board deliberated

at length

as to whether

a declining

trend in engineering

and technical

support

was clearly evident.

The Board ultimately decided that

no trend

was apparent.

3.

Board Recommendations

The licensee

is encouraged

to increase

emphasis

on documenting

the design basis

and ensuring its implementation in plant

activities.

The licensee

should ensure that basic design

criteria are

known and available to appropriate plant

personnel.

In addition the licensee

is encouraged

to fully implement the.

system engineering

program,

and ensure that adequate

configuration control is maintained.

The licensee

should

provide increased

attention to improve the communications

and

interaction

between plant and engineering

groups.

These

efforts should assure

that

a proper culture

and sense

of

responsibility is instilled in the plant and engineering

groups

to assure that problems

are dealt with and resolved in a timely

manner,.

Finally, the licensee

management

should assure that the

fundamentals

of nuclear plant operation, e.g.,

independent

verification and cleanliness

controls,

are understood

by

engineering

personnel.

Safet

Assessment/ ualit

Verification

~Anal sis

This functional area

was observed routinely during the

assessment

period by both the resident

and regional inspection

staffs

and includes

assessments

made

by NRR

HQ staff in the

area of reviews of responses

to generic letters

and other

regulatory initiatives.

Approximately 1620 hours0.0188 days <br />0.45 hours <br />0.00268 weeks <br />6.1641e-4 months <br /> of inspection

effort were devoted to this function'al area.

The performance

of Quality Assurance,

Quality Support,

onsite Quality Control,

the Onsite Safety

Review Group,

and the Plant Staff Review

Committee were included in this assessment

as well as the

licensee

organizations

involved in the review of regulatory

and

23

industry initiatives.

The previous

SALP assessment

had

identified a need for the licensee

to improve the timeliness

and quality of root cause

analyses

and to: improve management

focus

on the identification and correction of problem areas

including those identified through industry'xperience.

During

this

SALP period the licensee

has

moved forward in these

areas

with improvements

in areas

such

as the performance of technical

audits

by Quality Assurance,

improved formality and tracking of

action plans for reactor trips and other events,

and specific

root cause training for involved managers

and supervision.

Further improvements

are clearly indicated to be required

as

identified in the body of this analysis

in the areas of

lowering the licensee's

threshold for root cause

analysis

and

in the area of effective management

followup and assessment

of

event action plans.

Licensee

management

has

been involved in site activities in the

quality verification area

and

has taken corrective actions to

improve these

programs

as

needed.

For example,

the licensee

has

a number of levels of root cause/corrective

action

evaluations

procedures

and to some extent all levels

have

seen

some

improvement.

A significant improvement

was the

establishment

of a formalized licensee

Event Investigation

Team

(EIT), a team lead by a member of corporate

management

to

evaluate

some of the more significant or technically

complicated events.

This concept,

a fallout of the April 1987

RHR event investigation includes

a detailed action plan.

The

first EIT initiated by the licensee

reviewed the failure of the

motor operated

disconnect

on November 11,

1987.

The review was

found by the inspectors

to be indepth

and thorough.

An apparent

weakness

in the EIT process

was identified

fol.lowing a more recent event.

Specifically, it appeared

that

neither

the

QA nor

QC departments

were actively involved in an

independent verification of the scope

and completeness

of

action taken in accordance

with the action plan.

For example

subsequent

to the July 17,

1988 reactor trip, the resident

inspector

sampling of actions identified areas

of oversight in

scope or ommissions

in actions; specifically a lack of

inspection for failed-welds

on fuse holder cabinets

and

a

failure to fully perform high voltage testing of affected

circuit breakers.

QA and

QC also appear to have

a lack of

significent involvement and input in the initial analysis of

operational

events

and in decisions for restart.

Their

involvement appears

to be concentrated

in after the fact

Technical

Review Group

(TRG) meetings

on'on-Conformance

Reports

(NCR) related to the event.

An innovative approach

in the quality verification program

has

been the development

by QA of audits

based

on the safety system

functional inspections

performed

by the

NRC.

These audits

concentrate

on one activity or system

from design to

implementation

and operation.

Although these

inspections

24

started with limited findings, the audits

and findings have

increased

in depth

and scope during the

SALP period.

The

SALP Board analyzed

the 26 completed licensing actions for

this assessment

period.

The Board concluded that the licensee

should strive to continue to improve the quality of licensing

submittals.

The major objective should

be to improve the

safety basis for requested

license

amendments.

As a minimum,

the submittal

should discuss

the basis for the original

requirement,

and why the proposed

change

continues to meet the

applicable safety criteria and maintains

an adequate

margin of

safety.

Also, greater

emphasis

should

be placed

on the prompt

resolution of long-standing safety issues.

In the licensee's

approach to the resolution of technical

issues

from a safety standpoint,

an understanding

of issues

is

generally apparent.

Early'n the

SALP period there

was

a lack

of a structured

formalized indepth review of root cause

and

ancillary problems for reactor trips or other events.

These

problems

were most evident following the December

13,

1987

reactor trip and the subsequent

turbine trip due to poor steam

dump performance.

Later in the

SALP period the licensee

had

improved the scope of the restart

reviews

and intends to issue

a revised restart

procedure

to reflect those

improvements.

The licensee's

response

to major regulatory initiatives such

as

Bulletins and Gener ic Letters

has

been generally comprehensive

and timely.

However the licensee's

attention to and followup

of committments to inspection findings has occasionally

been

found to be slow and/or

incomplete

as

was the case with

findings in the

IST area with engineering,

with the engineering

corrective actions associated

with a lack of acceptance

criteria for containment

fan cooler collection rates

and with

the resolution of design criteria for the

ASW system with

engineering.

These technical

areas

were discussed

in

engineering

but are highlighted here. as well from the

~

standpoint that licensee

management

did not consistently

ensure

thorough

and timely closeout of regulatory safety initiatives

identified by inspection findings.

Also, on occasion

the

quality organizations

have

been ineffective in dealing with a

problem in a timely way.

An example

was the ineffective action

taken during the Unit 1 outage in resolving the cleanliness

condition for reactor vessel

head work previously discussed.

The onsite

and offsite safety committees

were assessed

on a

routine basis

by the resident

inspectors

through attendance

at

selected

meetings

and review of the committees

minutes,

."

findings and recommendations.

No significant issues

were

developed

from this limited review.

gA and

gC involvement was

encouraging

in this area,

but continued

development of these

organizations

as active participants is warranted.

A major issue in the previous

assessment

period,

NCR review,

has

improved over this assessment

period.

TRG chairmen

have

25

received training in root cause identification and

as

a result

NCR reviews appear to be more indepth.

In addition, the format

of the

NCR has

improved including a more thorough description

and analysis of the events.

Although assessments

are generally

good, there

have

been

inadequate

root cause

analyses

and

untimely corrective actions

as discussed,

for example,

in the

cover letter of the February 17,

1988 inspection report.

In addition, at times the inspectors

found that the lowest

level of root cause evaluation,

the guality Evaluation,

was not

being implemented for less significant eventsthat

warranted

a

change to procedure

or program.

Two examples of such events

were described

in the operations

functional area regarding

a

pressurizer

pressure

transient

and an auxiliary feedwater

spill.

This is another indication of the lack of adequate

gC

oversite of plant operations.

This issue related to high

thresholds for initiating root cause

assessment

of plant

problems

was also

an issue

discussed

in the cover letter to the

maintenance

team inspection.

In general,

the licensee's

LERs adequately

described

the major

aspects

of each event,

including component

or system failures

that contributed to the event

and the significant corrective

actions

taken or planned to prevent recurrence.

The reports

were reasonably

complete,

generally well written and easy to

understand.

The root causes

were identified as appropriate.

Previous similar occur rences

were properly referenced

in the

LERs as applicable.

One aspect of LERs identified for

potential

improvement

was related to water

hammer events.

The

first event

was related to repairing

RHR check valves at Unit 1

on June

25,

1988,

and the second

event

was related to the Unit

2 natural circulation cooldown event

on July 17,

1988.

The

descriptions of the water

hammer aspects

of the events

were

minimal given the serious potential of such events.

There were four violations attributed to this area.

None of

the violations were considered repetitive nor indicated

a

programatic

breakdown.

The quality verification organizations

appeared

to be

adequately

staffed

and evaluated

a substantial

percentage

of

site activities,

such

as maintenance

and procurement.

Some

significant problems identified by the gA/gC organizations

. included

N&TE instruments

fou'nd out of calibration and not

receiving timely review,

and the adequacy of the sealing of a

temporary containment penetration, used during the outage for

pass

through of a temporary

system.

Performance

Ratin

Category

2

26

Board Recommendations

The licensee

should continue to focus

management

attention

towards the thorough evaluation of plant problems

and the

development

and implementation of well thought-out corrective

action/investigation

plans with overall

management

responsibility defined.

This should include the involvement of

quality verification organizations

in the review of events

and

the independent verification of actions.

Also, licensee

management

should assure that the quality organizations

are

effectively used for routine conditions,

such

as the onsite

and

offsite review committees.

The licensee

should strive to continue to improve the quality

of licensing submittals.

The major objective should

be to

improve the safety basis for requested

license

amendments.

Finally, the approach for handling regulatory safety

initiatives identified by inspection findings should

be

assessed

programmatically,

to ensure that thorough

and timely

consideration

is provided.

H.

Fire Protection

~Anal ala

During this assessment

period,

40 hours4.62963e-4 days <br />0.0111 hours <br />6.613757e-5 weeks <br />1.522e-5 months <br /> were expended

by one

NRC inspector conducting

an inspection in the fire protection

area.

In addition, the resident

inspectors

provided continuing

observation

in this area.

Improvements

were

made in this area.

In the last Salp assessment,

the

NRC expressed

concern that the

licensee's

capability to detect fires in the earliest possible

stage,

make timely responses

and accomplish

manual fire

suppression

was questionably

adequate

due to the geographical

responsibilities

delegated

to the site fire brigade.

The licensee

demonstrated

management's

involvement in assuring

quality in the fire protection area

by initiating a program for

improvements

in this area

and allocating required

funds for the

program goals which extend

beyond the scope of concerns

expressed

by the

NRC.

The program goals

have objectives that

address

the optimum performance of fire protection features

rather than satisfying regulatory requirements

as

a minimum.

The licensee's

response

to

NRC initiatives included upgrading

the fire alarm system in safety related

areas

to a system with

improved technology

and reliability to provide the earliest

possible detection of fires; developing

a Plant Information

Management

System

(PIMS) for fire barrier and fire protection

feature configuration management;

clarification of agreements

with offsite fire departments

so that the minimum five-man fire

brigade will be available on-site at all times to respond to

fires in safety related areas;

and implementing

a wildland fire

fuel management

program.

27

The licensee

demonstrated

timely and effective resolution to

technical

issues

from a safety standpoint

by responding

to the

NRC concern for the geographical

responsibilities

delegated

to

site fire brigade.

The licensee's

resolution to this concern

included limiting the site fire brigade geographical

responsibilities

to safety related

areas

and non-safety related

areas within the immediate vicinity of safety related

areas.

Responsibility for firefighting in remote areas within and

outside of the site area

boundary

was delegated

to a separate

maintenance fire brigade

and offsite fire departments.

There

was

no enforcement history and

no LER's submitted during

this assessment

period.

In response

to operational

events,

the licensee

implemented

a

wildland fuel management

program to reduce

the potential

impact

of external wildland fires on plant operations

such

as those

that occurred during a 1982 wildland fire.

The program is

comprehensive

and is based

on examination of alternate

methods

for wildland fuel reduction/modification that are consistent

with other land uses objectives for short and long terms.

In

addition to potential disruption of safety related operations,

the licensee

determined that wildland fires pose significant

risk to the uninterrupted

power output of the plant.

Therefore,

the wildland fuel management

program objectives

implemented

by the licensee

extend

beyond the scope of

regulatory requirements

with the incorporation of practical

measures

for wildland fire prevention

by the reduction of fuel

volumes.

These

measures

include controlled burning to create

"fuel mosiacs",

mechanical

removal of vegetation,

chemically

fire retarding vegetation

and annual

evaluation of fuel growth

and age classes.

This is an extensive effort that involve

10,000 acres of wildland vegetation

on various slopes

and

elevations within and outside the site boundary.

This effort

is expected to reduce the potential of wildland fire

occurrences

by 30 to 50 percent.

The licensee's

management

and technical staff, responsible for

implementing fire protection requirements,

appeared

to be

appropriately

knowledgeable

in fire protection

and nuclear

engineering,

and they appeared

to be maintaining

a balanced

approach

toward implementing

a program aimed at obtaining

prudent objectives.

To enhance

the effectiveness

of the licensee's

training and

qualifications program,

as part of a joint venture with offsite

fire departments

and California Polytechnical Institute, the

licensee is in the process

of upgrading existing fire brigade

training facilities to a certified internal structural

firefighting burn facility.

The

new facility is expected

to be

completed in the fall of 1989.

Finally, as

a measure

of the

licensee's

training effectiveness,

the licensee's fire watches

have detected

and reported fires and unusual

events

(such as,

28

the Motor Operated

Disconnect arcing) in their early stages

and

avoided

more serious

consequences.

2.

Performance

Ratin

Category 1, Improving Trend

3.

Board Recommendations

Licensee

management

should continue its efforts to be sensitive

to practical fire protection

and nuclear engineering

concerns

through the development

and implementation of program goals

that are not aimed at mere regulatory compliance but are

intended to achieve effective, reliable

and safe plant

operations.

Management is strongly encouraged

to continue

active involvement in the day-to-day fire protection aspects

of

plant operations

and provide leadership, visibility and first

hand assessments

of the implementation of initiatives and

expectations

in this area.

SUPPORTING

DATA AND SUMMARIES

A.

Enforcement Activit

A summary of inspection activities for Units 1 and

2 are provided in

Tables

1 and

2 respectively

along with a summary of enforcement

items from these

inspections.

A description of the enforcement

items for Units 1 and

2 are provided in Tables

3 and 4,

respectively.

During this

SALP period,

no escalated

enforcement

items were identified.

B.

Confirmation of Action Letters

None

29

TABLE 1

INSPECTION ACTIVITIES AND ENFORCEMENT

SUMMARY 8/1/87 - 7/31/88

DIABLO CANYON UNIT 1

Functional

Area

Ins ections

Conducted

Enforcement

Items

Inspection"

Percent

Severit

Level

Hours

of Effort I II III

IV

V

Dev

Plant Operations

994

30'1

2

2.

Radiological Controls

198

6. 04

1

3.

Maintenance/

Surveillance

654

19. 94

3

1

4.

Emergency

Preparedness

73

2. 23

5.

6.

Security

Engineering/

Technical

Support

171

160

5. 22

4. 88

7.

Safety Assessment/

equality Verification

1009

30. 77

3

1

8.

Fire Protection

20

.61

TOTAL

3279

100

15

2

2

Allocations of inspection

hours to each functional area are

approximations

based

upon

NRC Form 766 data.

Severity levels are in accordance

with NRC Enforcement Policy (10 CFR Part 2, Appendix C).

Data reflects Inspection

Reports

87-31 through 88-17.

30

TABLE 2

INSPECTION ACTIVITIES AND ENFORCEMENT SUMMARY 8/1/87 - 7/31/88

DIABLO CANYON UNIT 2

Functi onal

Ar ea

1.

Plant Operations

606

27. 71

Ins ections

Conducted

Enforcement

Items

Inspect)on

Percent

Severest

Leve

Hours

of Effort I II III

V

V

Dev

2.

Radiological Controls

114

3.

Maintenance/

Surveillance

615

4.

Emergency

Preparedness

78

5. 21

28. 12

3. 57

5.

Security

6.

Engineering/

Technical

Support

95

48

4. 34

2. 19

7.

Safety Assessment/

quality Verification

611

27.93

8.

Fire Protection

20

.93

TOTAL

2187

100

Allocations of inspection

hours to each functional area

are

approximations

based

upon

NRC Form 766 data.

8

1

2

~*

Severity levels are in accordance

with NRC Enforcement Policy (10 CFR Part 2, Appendix C).

Data reflects Inspection

Reports

87-31 through 88-16.

31

TABLE 3

DIABLO CANYON UNIT 1

ENFORCEMENT ITEMS

(08/01/87 - 07/31/88

Inspection

~Re ort Ro.

87-38

87-38

~Sub 'ect

Failure to include acceptance

criteria for the operation of the

'containment

fan cooler collection

monitoring system.

Deviation:

Radiation Monitors

RE-58 and RE-59, installed in April

1985,

were not recorded in the

control

room radiation monitoring

racks.

Severity

Functional

Level

Area

IV

Deviation

87-44

On January

7, 1988,

a visitor inside

the protected

area,

in the adminis-

tration building cafeteria,

became

separated

from, and was not under

the control of, his assigned

escort.

Condition existed for approximately

3 minutes.

IV

88-02

At time of the inspection,

several.

Reg.

Guide 1.97 instruments

were not

calibrated within the established

interval.

IV

88-02

88-03

Deviation:

At time of the inspection,

the wide range

steam generator

level

instrumentation

did not meet the

redundancy criteria in that all four

of the wide range

steam generator

instruments

were powered

from one

power supply.

On February 24, 1988,

a equality

Control Inspector

stamped

and

initialed his acceptance

of clean-

liness

on the inspection plan without

visually inspecting inside the body

of valve No.

8484B for cleanliness.

Deviation

IV

88-04

During the performance

of the routine

surveillance test of containment

spray

pump

No. 1-1 (STP P-48)

on February 10,

1988, the reference

f'low rate of 300 +

5

GPM was not established.

IV

32

TABLE 3 (continued)

Licensee failed to provide

a clear

zone for surveillance at the protected

area perimeter.

IV

On April 14, 1988,

a Zone

3 house-

keeping area,

established

for the

Unit 1 reactor vessel

head cable tray

area,

was found to contain loose tools

which were not entered

on the provided

log.

On March 11,

1988, draining of safety

Accumulators

1-2 and 1-4 was initiated

prior to venting the accumulators,

causing relief valve actuation

on the

RCDT inventory to the reactor cavity

sump.

IV

On March 11,

1988, Calculation

No.

880311-0

had been

signed

as prepared

verified, but was not identified as

preliminary even though design input-

data requiring verification was

used

and

had not been verified.

The

calculation's result was in error

due to dimensional

input data being

in error.

IV

Two licensee action requests

reported

that two very high radiation

area

doors were found to be shut but

not locked.

IV

Corrective actions

taken by licensee

did not preclude repetition of lack

of required cleanliness

controls.

IV

On April 27, 1988, while replacing

spiral

wound gaskets,

on a Unit 1

safety injection relief valve header

flange,

mechanics

used

an unauthorized

lubricant instead of the prescribed

Felpro N-5000 and not complete the

data

sheets

prescribed

by MP M-54.4.

IV

Since licensing of'nit 1 on November 2,

IV

1984,

a test program

has not been

'stablished

and implemented to assure

required surveillance testing of plant

check valves.

33

TABLE 3 (continued)

On July 21,

1988 the applicable test

procedures

did not pr ovide for testing the

10K atmospheric

dump valves actuating

systems

to demonstrate

operational

readiness

for loss of normal air supply

and nitrogen backup supply.

IV

As of July 21, 1988, revisions to the

FSAR

V

have not been submitted to the

NRC

reflecting changes

to the compressed air-

system.

Failure to properly implement

ASME code

IV

requirements

for inservice testing of

safety rel'ated auxiliary feedwater

pumps.

Failure to implement required

measures

to

IV

ensure

proper review of changes

to plant

procedures

for performance of inservice

testing.

A

34

TABLE 4

DIABLO CANYON UNIT 2

ENFORCEMENT ITEMS

(08/01/87 - 07/31/88

Inspection

~Re or t No.

87-38

87-38

87-39

~Sob 'ect

Failure to include acceptance

criteria for the operation of the

containment

fan cooler collection

monitoring system.

Deviation:

Radiation Monitors

RE-58 and RE-59, were not recorded

in the control

room radiation

monitoring racks.

On May 5,

1987 maintenance

personnel

torch heated to 1200 degrees'F

and

mechanically pulled S.S.

RHR piping

adjacent

to flow element

FE-641A

without prior approval

by the

appropriate

engineering

organizations.

Severity

Functional

Level

Area

IV

Deviation

IV

87-39

Work order C0011616 Activity 02 of

May 5, 1987,

was issued in lieu of an

approved

procedure

and directed

heating of a

RHR pipe to 1200 degrees

F.

The pipe was subsequently

heated

which

likely caused sensitization

of the

stainless

steel

pipe.

IV

87-43

In April 1985,

two differential pressure

IV

gauges

were installed across

the Unit 2

RHR pumps without implementing Adminis-

trative Procedure

Procedure C-lSl,

Revision 3, or any other form of

procedural

control.

As a result, the

gauges

remained in place until

November 1987 following identification

by the inspector.

87-43

On November 13, 1987, the Unit 2 Shift

Foreman did not complete

step 8. 13 to

Surveillance Test Procedure

P-3B

which states:

"Remove

gauges

tempo-

rarily installed for this test" prior

to signing that the procedure

had been

completed.

Gauges

were not removed

until November

18,

1987 following

identification by the inspector.

V

35

TABLE 4 (continued)

At time of the inspection,

several

Reg.

Guide 1.97 instruments

were not

calibrated within the established

interval.

IV

Deviation:

At time of the inspection,

the wide range

steam generator

level

instrumentation

did not meet the

criteria in that al.l four of the

wide range

steam generator

level

instruments

were powered

from one

power supply.

Deviation

Records

for Unit 2 indicated that

valve

RCV-16 stroke time increased

143% on November 29,

1986 and the

test frequency

was increased

to once

each

month.

The original

92 days

valve stroke time test frequency

was

resumed after May 4, 1987, without

the performance of valve corrective

action in the form of repair,

replacement

or detailed engineering

analysis.

IV

On February

19,

1988,

a licensee

employee entered

the radiological

controls area

by stepping over

a

posted

boundary at a point not

established

as

a normal personnel

access

control point.

In addition,

the individual did not have written

authorization to enter

the area.

IV

Failure to properly perform quality

evaluations

of plant deficiencies

as required

by plant procedures.

IV

c'

3)

36

TABLE 5

DIABLO CANYON UNIT 1

SYNOPSIS

OF

LICENSEE

EVENT REPORTSA"

5.

Emergency

Preparedness

Security

Functional

Area

1.

Plant Operations

2.

Radiological

Controls

3.

Maintenance/Surveillance

SALP Cause

Code"

A

B

C

D

E

X

3

0

4

3

3

0

3

0

0

1

0

0

10

3

1

2

3

0

0

0

0

0

0

0

7

1

0

0

0

3

Total s

13

19

6.

7.

8.

Engineering/Technical

Support

Safety Assessment/

equality Verification

Fire Protection

1

0

0

0

0

0

0

0

0

0

0

0

0

0

0

0

0

0

24

4

5

6

6

3

48

Cause

Codes:

A - Personnel

Error

B - Design,

Manufacturing or Installation Error

.

C - External

Cause

D - Defective Procedures

E - Component Failure

X - Other

Synopsis

includes

LER Nos.

87-12 through 88-22

(LERs 88-4,

17,

18

presently not issued)

and

upon 'Safeguai d

LERs 87-S03 through 88-S11.

37

TABLE 6

DIABLO CANYON UNIT 2

SYNOPSIS

OF

LICENSEE

EVENT REPORTS**

Functional

Area

1.

Plant Operations

2.

Radiological

Controls

3.

Maintenance/Surveillance

4.

Emergency

Preparedness

5.

Security

6 ~

Engineering/Technical

Support

7.

Safety Assessment/

qua 1 ity Ver ificati on

8.

Fire Protection

SALP Cause

Code"

A

B

C

D-

E

X

1

1

2

0

-

1

0

0

0

0

0

0

0

3

3

0

3

1

0

0

0

0

0

0

0

0

0

0

0

0

0

0

0

0

0

0

0

0

0

0

0

0

0

0

0

0

0

0

0

Totals

10

Cause

Codes:

4

4

2

3

2

0

15

A - Personnel

Error

B - Design, Manufacturing or Installation Error

C - External

Cause

D - Defective Procedures

E - Component Failure

X - Other

  • "

Synopsis

includes

LER Nos.

87-18 through 88-07

t

l,

38

TABLE 7

DIABLO CANYON UNIT 1

LICENSEE

EVENT REPORTS

(08/01/87 - 07/31/88)

LER

Title

~Sal

Area

Cause

Code

87-12

Containment fan cooler Unit 1-3 Cooling Mater

flow rate out of Tech Spec limit due to

out-of-tolerance

flow instrument.

3/E

87-13

Containment Ventilation Isolation Initiation

due to personnel

error.

1/A

87-14

87-15

87-16

Inadvertent start of diesel

generator

1-3

due to personnel

error.

Failure to satisfy Tech Specs

6. 12, high

radiation area

due to personnel

error.

Entry into Tech Spec 3.0.3 four shutdown

bank control rods not fully withdrawn due

to fuse failure from poor solder joint

between the top end cap

and the metal

fuse

link of the fuse.

3/A

2/A

1/E

87-17

87-18

87-19

U

87-20

Cont. Ventilation Isolation Initiation due

to Voltage Spike during troubleshooting.

Fuel Handling Building ventilation system

shifted to iodine removal

mode

due to

personnel

error.

Failure to satisfy Tech.

Specs.

4. 1. 3. 1. 1 &

4. 1.3.2 for inoperable

rod position

deviation monitor due to personnel

error.

Failure to meet Tech.

Spec.

4.2.4: 1 for

inoperable

quadrant

power tilt ratio

alarm due to personnel

error.

3/B

3/A

1/A

1/A

87-21

87-22

Actuation of engineered

safety features

due to inadvertent

grounding of

electrical

component.

Reactor Coolant System Control

Room .

Temperature

Recorders

declared

inoperable

due to inadvertent failure

to reinstall seismic restraints.

3/A

3/A

39

TABLE 7 (continued)

Reactor Trip following Main Feed

Water

Pump Trip during surveillance

test

due to failed "Push to Test"

lamp socket.

Reactor trip when Source

Range

Channel

N-32 detector voltage failed high due

to a capacitor failure.

3/E

1/E

High Steam Generator

Water Level Main

Turbine Trip and Main Feedwater Isolation

during startup

due to lack of Guidance

for operators.

1/D

Mode 1 Entry while in Action Statement

TS 3.6.2.2.a

in Violation of T.S. 3.0.4

due to lack of Procedural

Guidance.

1/D

Radiation Monitor Alarm and Hot Particle

caused

Fuel Handling Ventilation System

Change

due to failure to perform survey.

2/D

Entry into T.S.

3..0.3

when both trains

of Auxiliary Building Ventilation were

inoperable

due to a procedural

deficiency.

3/A

Missed Surveillance

when the

ESF Time

Response

Test Frequency

was not followed

due to misinterpretation of T.S.

3/A

Failure to Perform Plant Vent Air Sampler

Flow Estimate

Required

by T. S.

3. 3. 3 ~ 10

due to personnel

error.

2/A

Reactor Coolant System

Low Flow Signal

Reactor Trip Due to inadequate

procedural

guidance.

Spurious Actuation of Containment Ventilation

Isolation

Due to Noise

on Radiation Monitoring

channels'ower

source.

3/D

1/C

Reactor Trip Breakers

Missing Seismic Clips.

(Voluntary) to .be issued.

Containment Ventilation Isolation due to

Electronic Noise and late issuance

of

10 CFR 50.72 Required

Report

Due to

Inadequate

Procedural

Guidance.

1/C

~1

40

TABLE 7 (continued)

88-06

Fuel Handling Building Ventilation

System

and Control

Room Ventilation

System

Mode Changes

due to Inverter

Failure.

1/E

88-07

Actuation of Engineered

Safety Features

caused

by Electrical

Component Grounding

due to personnel

error.

6/A

88"08

Violation of T.S.

6. 12 when two very high

radiation area

doors were left unlocked

due to personnel

error.

2/A

88-09

Mestinghouse

ARD Relays experience

degradation

due to granules

of coil

potting compound lodging between

the

Relay Armature and Coil Spool (voluntary).

3/B

88-10

88-11

Containment Ventilation Isolations

due

to Electronic Noise.

4

Fuel Handling Building Ventilation System

Shift to Iodine Removal

Mode when Radiation

Monitor 1-RM-58 exceeded

the High Alarm Set

Point due to Background Radiation

Fluctuations.

1/C

1/C

88-12

88-13

88-14

88-15

Violation of T.S.

4. 11.2 when

18C technicians

secured

the continuous particulate

and iodine

plant vent sample,

due to personnel

error.

Main steam line isolation due to inadequate

communications

between

I&C technicians

and

the control

room operators.

Contamination of the diesel

generator

day

tank fuel oil due to biofouling (voluntary).

Reactor Coolant

Pump Motor Upper Oil Reservoir

Assemblies

Degradation attributed to metal

fatigue (voluntary).

3/A

3/A

3/C

3/E

88-16

Missed Surveillance

due to lack of Procedural

guidance.

.3/0

88-17

88-18

ECCS check valves (to be issued)

(voluntary).

Safety valve setpoint drift (to be issued)

(voluntary).

~g

41

TABLE 7 (continued)

Mispositioned capstan

spring tangs

on

Pacific Scientific Company snubbers

(voluntary).

3/B

Reactor trip from overtemperature-delta

temperture protection logic due to

personnel

error.

3/A

Reactor trip from high-high steam generator

level protection logic due to inadeuate

operating procedure.

1/0

Missed surveillance

of plant ventilation

system flow rate monitor

FR-12 due to

personnel

error.

3/A

42

TABLE 7

LER

TITLE

DIABLO CANYON UNIT 1

SECURITY LICENSEE

EVENT REPORTS

(08/01/87 " 07/31/88)

SALP AREA

CAUSE

CODE

87-S03

87-S04

87-S05

87-SOG

88-S01

88-S03

88-S05

88-S06

88-S09

88-S10

88-S11

Failure of Security Compensatory

Measure

Inadequate Vital Area Barrier

Loss of Emergency (Security)

Power

Report of Capsule

(non drug)

Found Inside Protected

Area

Adverse

Media Interest - Plant Employee

Degraded

Protected

Area Barrier

Degraded Vital Area Barrier

Failure of Security Compensatory

Measure

Failure of Security Compensatory

Measure

Involvement of Reactor

Operator with Drugs

Failure of Security Compensatory

Measure

5/A

5/B

5/X

5/X

5/X

5/A

5/A

5/A

5/A

5/A

5/A

Og

43

TABLE 8

DIABLO CANYON UNIT 2

Licensee

Event Reports

(08/01/87 - 07/31/88)

LER

87-18

87-19

87-20

87-21

Title

T.S. Violation 3.0.3

due to Both Trains of Auxiliary

building ventilation unavailable to start

on

Automatic Start Signal.

Auto Start of Diesel Generator

2-2 due to a

broken wire during reinstallation of a 4KV breaker.

Redundant

Trains of Aux. Building

Ventilation inoperable.

Failure to meet T. S.

inoperable

Rod

Position Deviation Monitor Due to

Personnel

Error.

SALP Area

Cause

Code

3/D

3/B

1/B

1/A

87-22

87-23,

87-24

87-25

88-01

88-02

88-03

Fuel Handling Building Ventilation,

System shifted to Iodine Removal

Mode

due to unknown cause.

Accumulator Cracking

due to Intergranular

Stress

Corrosion (voluntary).

Manual Trip of Reactor

from 98K arcing at

contacts

on Isophase

Bus Motor-Operated

Disconnect Switch

Potential

loss of containment integrity

when FCV-661 failed

LLRT due to dust

on

valve seat while FCV-660 was potentially

inoperable

due to personnel

error.

=

Spurious Actuation of the Fuel Hahdling

Building Ventilation System Iodine Removal

Mode due to Electronic Noise

.Reactor trip due to an undetected failed

Relay during Seismic Trip Channel Calibration

CVI & FHB Ventilation Mode Change

due to a

Power Supply Transient

& Second

CVI & FHB

Ventilation Mode Change

& Control

Room

Ventilation System

Mode Change

due to

personnel

error.

1/C

3/B

3/D

3/B

1/C

3/E

3/A

~ <

~ 'l

~'ABLE

8 (continued)

88-04

88-05

CVI due to Power Supply Transient

and

failure of CVI Protection Train A valves to

close

due to Installation error and

procedural

deficiency.

CVI initiation due to Electronic Noise

Caused

by Mechanical

Wear on the Check

Source

Latch.

3/0

1/E

88-06

88-07

Missed Surveillance

due to Personnel

error.

Autostart of. diesel

generato~

2-1 due to

inadvertent

removal of vital bus potential

fuse block during preventive

maintenance

(personnel

error).

3/A

3/A

V

C