ML16341E494

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Insp Repts 50-275/87-38 & 50-323/87-38 on 871004-1114. Violation & Deviation Noted.Major Areas Inspected:Plant Operations,Maint & Surveillance Activities & Followup of Onsite Events,Open Items & LERs
ML16341E494
Person / Time
Site: Diablo Canyon  Pacific Gas & Electric icon.png
Issue date: 12/24/1987
From: Johnston K, Mendonca M, Narbut P, Padovan L
NRC OFFICE OF INSPECTION & ENFORCEMENT (IE REGION V)
To:
Shared Package
ML16341E492 List:
References
50-275-87-38, 50-323-87-38, NUDOCS 8801130038
Download: ML16341E494 (76)


See also: IR 05000275/1987038

Text

U.

S.

NUCLEAR REGULATORY COMMISSION

. REGION V

Report Nos:

50-275/87-38

and 50-323/87-38

Docket Nos:

50-275

and 50-323

License

Nos:

DPR-80 and

DPR-82

Licensee:

Pacific Gas

and Electric Company

77 Beale Street,

Room 1451

San Francisco,

California 94106

Facility Name:

Diablo Canyon Units 1 and

2

Inspection at:

Diablo Canyon Site,

San Luis Obispo County, California

Inspection

Conducted:

October

4 through

November 14,

1987

Inspectors:

L.

M. Padovan,

Resident

Inspector

K.

E. Johnston,

Resident Inspector

P.

P.

Narbut, Senior Resident

Inspector

Date Signed

r+ vga'7

Date Signed

y wgz y/~p

Date Signed

Approved by:

P?-/z. r/P 7

M.

M. Mendonca,

Chief, Reactor Projects

Section

1 Date Signed

Summary:

Ins ection from October

4 throu

h November

14

1987

Re ort Nos.

50-275/87-38

and 50-323/87-38)

Areas

Ins ected:

The inspection

included routine inspections

of plant

operations,

maintenance

and surveillance activities, follow-up of on-site

events,

open items,

and licensee

event reports

(LERs),

as well as selected

independent

inspection activities'nspection

Procedures

25019,

30702,

30703,

50095,

61720,

61726,

62702,

62703,

71707,

71710,

90712,

92701,

92702,

92703,93702,

and 94703 were applied during this inspection.

Results of Ins ection:

One violation was identified regarding insufficient

acceptance criteria

Paragraph

2.b.).

One deviation

was identified regarding

the radiation monitoring system

(Paragraph 9.a.).

DETAILS

1.

Persons

Contacted

  • J.

D. Townsend,

Acting Plant Manager

  • J.

A. Sexton, Assistant Plant Manager,

Plant Superintendent

J.

M. Gisclon, Acting Assistant Plant Manager for Support Services

C.

L. Eldridge, guality Control Manager

  • K. C.

Doss, On-site Safety Review Group

R.

G. Todaro, Security Supervisor

D.

B. Miklush, Maintenance

Manager

D.

A. Taggert, Director guality Support

M. J.

Angus,

Work Planning Manager

T. J. Martin, Training Manager

W.

G. Crockett,

Instrumentation

and Control Maintenance

Manager

J.

V. Boots,

Chemistry

and Radiation Protection

Manager

L. F.

Womack, Operations

Manager

"T.

L. Grebel,

Regulatory Compliance Supervisor

S.

R. Fridley, Senior Operations

Supervisor

R.

S. Weinberg,

News Service Representative

D.

A. Malone, Senior

I8C Supervisor

"W.

B. McLane, Acting.Assistant Plant Manager/Technical

Services

The inspectors

interviewed several

other licensee

employees

including

shift foremen

(SFM), reactor

and auxiliary operators,

maintenance

personnel,

plant technicians

and engineers,

quality assurance

personnel

and general

construction/startup

personnel.

Denotes

those attending the exit interview on December

7, 1987.

2.

0 erational

Safet

Verification

General

During the inspection period, the inspectors

observed

and 'examined

activities to verify the operational

safety of the licensee's

facility.

The observations

and examinations

of those activities

were conducted

on

a daily, weekly or monthly basis.

On a daily basis,

the inspectors

observed control

room activities to

verify compliance with selected limiting conditions for operations

(LCOs) as prescribed

in the facility Technical Specifications

(TS).

Logs, instrumentation,

recorder

traces,

and other operational

records

were examined to obtain information on plant conditions,

and

trends

were reviewed for compliance with regulatory requirements.

Shift turnovers

were observed

on

a sample

basis to verify that all

pertinent information of plant status

was relayed.

During each

week, the inspectors

toured the accessible

areas

of the facility to

observe

the following:

(a)

General plant and equipment conditions.

(b)

Fire hazards

and fire fighting equipment.

(c)

Radiation protection controls.

(d)

Conduct of selected activities for compliance with the

licensee's

administrative controls

and approved

procedures.

(e)

Interiors of electrical

and control panels.

(f)

Implementation of selected

portions of the licensee's.physical

security plan.

(g)

Plant housekeeping

and cleanliness.

(h)

Essential

safety feature

equipment alignment

and conditions.

(i)

Storage of pressurized

gas bottles.

The inspectors

talked with operators

in the control

room, and'ther

plant personnel.

The discussions

centered

on pertin'ent topics of

general

plant conditions,

procedures,

security, training,

and other

aspects

of the involved work activities.

blhile touring the Unit 1 "pipe racks," the inspector

observed that

a

rope

had been

passed

over a vital electrical conduit to the operator

on a main steam isolation valve.

Apparently, the vital conduit had

been

used

as

a fixed point from which the rope was

used to raise

scaffolding material

from the ground to the pipe rack elevation.

This situation

was discussed

with General

Construction

(GC)

management,

and accordingly,

GC personnel

conducted tailboard

sessions

with all civil craft and discussed

approved rigging

techniques.

An analysis

performed

by Engineering verified no

conduit damage

occurred.

Reactor Coolant

S stem

RCS

Leaka

e Detection

S stem

Licensee

TS 3.4.6. 1 "Reactor

Coolant System

Leakage Detection

Systems" lists three

leakage detection

systems that shall

be

operable:

1)

The containment

atmosphere

particulate radioactivity monitoring

system.

This system

employs radiation monitor (RM) 11.

2)

The containment structure

sump

and the reactor cavity sump

level

and flow monitoring system.

3)

Either the containment

fan cooler collection monitoring system

or the containment

atmosphere

gaseous

radioactivity monitoring

system.

RM-12 monitors containment

atmosphere

gaseous

radioactivity.

RM-ll and

RM-12 employ the

same

sample

sump.

The licensee

normally

relies

on RM-11,

RM-12 and the containment

sump to fulfillthe

requirements

of TS 3.4.6. 1.

During a routine control

room

PS

inspection,

the inspector

noted that both RM-ll and

RM-12 were out

of service for sample

pump maintenance

and the operators

were

monitoring containment

fan cooler unit (CFCU) condensation.

Condensation

from each

CFCU collects in individual standpipes.

Each

standpipe

has

a drain valve,

a hi level alarm,

a hi-hi level alarm,

and

a volume of 7 liters.

The inspector

observed

than when the hi-hi level alarm is reached,

the operators

opened

the drain valve and logged the time.

As the

condensation

drained,

the alarms cleared,

and operators

then close

the drain valve.

The inspector

asked the shift foreman if there

existed

any quantitative criteria for evaluating drain valve cycling

frequency.

The shift foreman could not identify a quantitative

criteria,

however

he noted that qualitatively, if a significant

decrease

in the drain valve cycling frequency occurred,

actions

would be taken to identify possible

leakage.

As an example,

at one

point prior to the inspection,

the drain valve cycling frequency

was

at six minutes.

The licensee identified and repaired

a secondary

side leak in containment

and the cycling frequency

was reduced to

sixteen minutes.

The inspector

reviewed the licensee's

FSAR Section 5.2.7.4 which

states:

"The sensitivity and response

time of RCPB (Reactor Coolant

Pressure

Boundary)

leakage detection

systems

vary for different

methods of detection.

However, the diverse

systems

available

have the capability to detect continuous

leakage

rates

as

low

as

1 gpm within 1 hour1.157407e-5 days <br />2.777778e-4 hours <br />1.653439e-6 weeks <br />3.805e-7 months <br /> for unidentifiIed leaks

and

10

gpm for

identified leaks,

as required

by Regulatory Guide 1.45."

FSAR Table 5.2-16 indicated that the

CFCU leakage detection

system

can identify RCS leaks of 1 gpm in 1 hour1.157407e-5 days <br />2.777778e-4 hours <br />1.653439e-6 weeks <br />3.805e-7 months <br />.

Regulatory Guide 1.45

states

that leakage detection

systems

should

be adequate

to detect

a

leakage rate,

or its equivalent,

of 1 gpm in less

than

1 hours1.157407e-5 days <br />2.777778e-4 hours <br />1.653439e-6 weeks <br />3.805e-7 months <br />

(Section C.5)

and procedures

for converting various indications to a

common leakage equivalent

should

be available to the operators

(Section C.7).

The inspector

discussed

this issue with the operations

manager.

The

licensee

has

a procedure for the periodic evaluation of RCS leakage

(STP R-10).

STP R-10 provide instructions

and acceptance

criteria

for the surveillance

requirements

related to TS 3.4.6.2 "Operational

Leakage."

Although STP R-10 provides

acceptance

criteria for RM-11,

RM-12, and containment

sump monitoring, it does

not for the

CFCU

monitoring system since it is not specified in the surveillance

requirements

related

to

TS 3.4.6.2.

STP R-10 does provide

some

instruction for the

use of the

CFCU monitoring system,

but none that

would lead to the identification of a 1 gpm leak in 1 hour1.157407e-5 days <br />2.777778e-4 hours <br />1.653439e-6 weeks <br />3.805e-7 months <br />.

The

surveillance

procedure related to TS 3.4.6. 1 is for the calibration

of the

CFCU monitoring system

and does

not include operational

instructions

and acceptance

criteria.

Following discussions

with

the inspector,

the licensee

committed to include appropriate

instructions

and acceptance

criteria in the

RCS leakage detection

program.

The lack of appropriate

instructions

and acceptance

criteria for the

operation of the

CFCU collection monitoring system is an apparent

violation of the requirements

of 10 CFR Part 50, Appendix B,

Criterion V, which states,

in part, that activities affecting

quality shall

be prescribed

by documented

instructions

which shall

include appropriate quantitative or qualitative acceptance

criteria

(Open Item 50-323/87-38-01).

Residual

Meat Removal

Pum

Test

Gau

es

On October

28, 1987,

on a routine walkdown of the Unit 2 residual

heat

removal

(RHR) system,

the inspector

discovered

what appeared

to

be temporary instrumentation installed

on the suction

and discharge

instrumentation

lines of RHR pumps 2-1 and 2-2.

Two of the

instruments, differential pressure

(DP) gauges,

had tags identifying

installation for startup testing

on April ll, 1985 for RHR 2-1,

and

April 1,

1985 for

RHR pump 2-2.

These

two gauges,

numbers

709.5. 1

and 709.5.2 respectively,

were installed between

taps off the

suction pressure

gauge

(PI 631 and PI 632) instrument lines and the

discharge

pressure

transmitter

(PT 635 and

PT 647) instrument lines.

The

RHR pump 2-1

DP gauge

was installed to the instrument lines by

pressure

hoses

and

was supported

by plastic tie wrap to the

structure.

Two temporary suction pressure

gauges

on

RHR pump 2-2 were installed

and supported

in the

same

manner.

The

RHR pump 2-2

DP gauge

was

installed directly to and supported

by a 1/4 inch

discharge

instrument line and attached

to the suction instrument line by a

pressure

hose.

The inspector discussed

these findings with the

RHR system engineer

and the engineering

manager.

The gauges

were removed

and the

RHR

pump inservice testing procedure,

STP P-38, for which the gauges

are

primarily used,

was revised

on November

12,

1987, to include

direction that test

gauges

are to be installed

and

removed for the

test.

However, in review of this item the inspector

addressed

a

number of questions

to the licensee:

1)

Was there

a design

change

package

or any form of procedural

control for the installation of DP gauges

709.5. 1 and 709.5.2

to the

RHR system

instrument lines?

2)

Was there

a design

change

package

or any form of procedural

control for the installation of DPI-635X and

DPR-647X for Unit

1 other than Nuclear Plant Problem Report

(NPPR)

DCI-79-TN-P0106?

The gauges

appear to be permanently

installed,

however the inspector could only identify a NPPR,

which is not a design

document, that refers to the installation

of these

gauges.

In addition, the Unit 1 design drawing are in

conflict since the

OVIDs indicate installation ~hereas

the

P8IDs

do not.

0

3)

The as

found installation of 709.5. 1 and 709.5.2 raises

a

seismic qualification question.

Could the gauges

have

caused

.

the instrument lines to fail during a seismic event,

and if so

what would have

been the consequences?

4)

What is the appropriate calibration frequency for these

gauges

and are they out of calibration if the due date

has expired?

A

review of the calibration records of gauges

709.5. 1 and 709.5.2

shows that their last calibration was performed in October

1985.

The calibration records

indicate the gauges

needed to be

calibrated

by April 1986,

a six month frequency.

The

calibration stickers also indicated that the last calibration

was performed in October 1985, but indicated

a due date of

October 1988,

a three year frequency.

The inspector did not

find any documentation for this discrepancy.

5)

Are there test

gauges

installed

on other plant safety related

systems

which have not had the appropriate

design

review?

Finally, on November 18, the inspector

noted that two temporary

gauges

were installed

on

RHR pump 2-2.

The inspector brought this

to the attention of the shift foreman

who had the gauges

removed.

The gauges

appear to have

been left following the November

13

performance of STP P-3B.

The revision of the procedure in use

had

a

step to remove temporary test gauges.

This step

was marked "N/A"

for not applicable with a note in the shift foreman's

log that the

Instrumentation

and Control department

had been

requested

to remove

the gauges.

This issue

and the five previous questions

are currently unresolved

(Open Item 50-323/87-38-02).

3.

Onsite

Event Follow-u

a 0

Performance of Maintenance Activities on the Wron

Com onent

On October 8, 1987,

an electrician performed portions of a

preventive maintenance

procedure

on the wrong Unit 1 containment

spray

(CS) system valve.

The electrician

had begun work on valve

CS-1-9001B,

the train

B

CS discharge isolation valve instead of

CS-1-9001A,

the train A discharge isolation valve.

The electrical

breaker for the motor operator

on CS-1-9001A

had been cleared at

5:22 a.m.

and the valve was declared

inoperable.

During the motor

operator termination inspection portion of the maintenance

procedure,

the electrician discovered

a loose termination in the

Limitorque operator

torque switch which could not be tightened.

When

the electrician

informed his foreman,

the foreman realized the

electrician

was

on the wrong valve and reported it to the control

room at ll:30 a.m..

The shift foreman declared

CS train

B

inoperable.

Since the train A valve was inoperable

because

power to

the actuator

was

removed,

the valve actuator

breaker

was racked

back

in.

Train

B was declared

operable at ll:55 a.m..

At 12:05 p.m.,

the licensee

reported to the

NRC operatiqns

center,

in accordance

with 10 CFR 50.72, that both

CS trains were inoperable

between ll:30

a.m.

and ll:55 a.m..

Prior to repairing the loose termination

on CS-1-9001B,

the licensee

performed

an operability check and discovered

the valve to be

operable.

In addition the licensee

determined,

through procedure

review and discussions

with the electrician,

the electrician

had not

done anything to the valve that would have rendered it inoperable.

As a result,

the licensee

determined that they had conservatively

declared

CS train

B inoperable

and at 3:34 p.m. called the

NRC

operations

center to rescind

the l2:05 p.m. report.

The electrician stated that

he mentally transposed

valve numbers

prior to working on the CS-1-9001B.

.He had previously consolidated

electrical prints associated

with his work at the electrical

shop,

filled out maintenance

data sheets,

obtained

a clearance,

and

had

hung

a maintenance

reg tag on the correct breaker.

All of these

items referenced

the correct valve identification.

The electrician

indicated that in this case

he failed to double check his

maintenance

work package

against the valve located in the field.

Valve identification was verified by the inspector to be

satisfactory.

However,

CS-1-9001A

and

B are identical valves

located next to each other.

As an immediate corrective action, the operations,

I&C, and

maintenance

departments

issued instructions to their staffs

on the

subject of "wrong unit-itis."

Examples of previous experiences

were

highlighted,

and existing features

(such

as labeling, color coding,

component identification numbers,

work order designations,

and other

work practices)

were reviewed.

In determining root cause of this event,

and in response

to

NRC

Information Notice 87-25 "Potentially Significant Problems

Resulting

form Human Error Involving Wrong Unit, Wrong Train, or Wrong

Component Events," the licensee

appropriately enlarged

the scope of

their review to encompass

previous other wrong unit/wrong component

experiences.

A generic evaluation of these

types of events

experienced

at Diablo Canyon during 1986 and 1987 was undertaken

by

OSRG members.

Eleven events

were evaluated utilizing Human

Performance

Evaluation System

(HPES) techniques.

HPES Report 87-033

was issued

on November 18,

1987.

Six general

causal

categories

were

identified which encompassed

the primary, secondary,

and tertiary

causes

for the subject events.

The primary causal

factor for 9 of

the ll events

was

a lack of an independent/self

verification prior

to the incorrect equipment

being affected.

The recommended

corrective actions

included "1) the inclusion in

work documentation nf a verification requirement to ensure

the

correct unit, and component

are affected;

2) to establish

a plant

policy for a mental self verification to be performed for equipment

not realistically verifiable via the preceding

recommendation;

and

3) periodic training and management

reinforcement of the two

previous

recommendations."

In a discussion

of this subject with the plant manager,

the

'nspector

was informed of additional actions

taken or under

consideration.

These

included:

o

Discussions with other nuclear utilities to determine

how the

generic problem was being addressed

at their facility.

o

Evaluation of color coding of procedures/clearances/work

packages.

o

Investigating the effect of painting floors and railing

different colors in the two units.

Having the worker develop check off sheets for each job

assignment.

The individual at the work station must then

indicate

on the sheets

that

he is at the correct location,

including independent verification and routine changing of the

check off sheets.

0

Use of a contract

human factors specialist.

o

Lower threshold of onsite reporting

and to disseminate

near

miss information rather than reportable

information only.

Follow-up of generic corrective actions

on this subject will be

performed

by the

NRC staff.

(Open Item 50-275/87-38-01).

b.

Unit 1 Containment Ventilation Isolation

CVI

At 9:14 a.m.

on October 22,

1987, with Unit 1 at 100 percent

power,

an automatic initiation of the CVI system occurred.

The sample line

isolation valves for containment air radiation monitors

(RMs) Rll

and

R12 closed

as designed.

All other

CVI system valves that

received isolation signals

were already closed

when the event

occurred.

As required by 10 CFR 50.72 (b) (2) (ii), a 4-hour

non-emergency

event report was

made at 9:45 that morning.

This event occurred

when

an Instrumentation

and Controls (I8C)

technician replaced

a blown fuse while troubleshooting

inoperable

control

room air particulate radiation monitor RM21.

After

replacing

a fuse,

the technician

energized

RM21.

Due to a seized

paper drive motor

o'n

RM21, the fuse blew, resulting in a voltage

spike

and

a CVI.

Operators verified that other containment

parameters

(temperature,

pressure,

sump levels,

area radiation) were

normal,

then reset the

CVI signal, reset the alarm, placed

RMll and

RM12 back in service,

and verified that

a high radiation condition

did not exist.

The licensee's

investigation revealed

the CVI initiation resulted

from noise susceptibility problems of the CVI initiation circuitry.

The source of electrical

noise

was the voltage spike produced

by the

fuse blowing on

RM21.

As corrective action,

the paper drive motor

on

RM21 was replaced.

A design

change

was initiated to add time

delay circuitry 'to radiation monitors RMll, RM12,

RM14A,

RM14B,

'1

0

RM28A, and

RM28B, which have

been

known to cause

CVIs from an

electrical

noise signal.

Once installed, this circuitry should

prevent these radiation monitors from initiating a CVI on a short

burst of electrical

noise,

but will allow them to function on a

valid signal.

Ino erable Unit 1 Rod Position Deviation Monitor

Technical Specification

(TS) surveillance

requirement 4.1.3.1.1

required that full length rod group positions

be verified to be

within group

demand limit at least

once every four hours

when the

rod position deviation monitor

(RPDM) was inoperable.

At 1: 12 a.m.

on October 20, 1987, with Unit 1 at 40 percent

power, the-time

interval requirement specified

by TS 4. 1.3. 1. 1 was exceeded,

including the

25 percent

allowed extension of TS 4.0.2.

The

RPDM

remained

inoperable for 9 hours1.041667e-4 days <br />0.0025 hours <br />1.488095e-5 weeks <br />3.4245e-6 months <br />

and 40 minutes,

during which time no

verification of rod positions

was logged.

An explanation of the

development of this situation is provided below.

At 8: 12 p.m.

on October 19, 1987, while reducing unit power in order

to clean the condenser,

the plant process

computer

(P-250) failed

and the assistant

control operator

(ACO) "rebooted" the P-250.

After rebooting the P-250,

the

ACO updated

the rod bank positions

for the

RPDM program.

During this update,

he incorrectly transposed

control

rod bank

D position with shutdown

bank

D position.

At approximately 8: 17 p.m.

the control

room received

the "P-250

RX

ALM AXIAL FLUX /

ROD

POS" annunciator

alarm due to the transposed

rod bank positions.

The control operator

(CO) verified the digital

rod position indications

(DRPI) agreed with demand

step counters

and

continued the power reduction.

The P-250 alarm typewriter displayed

a

"ROD BANK SE(UENCE" alarm and the annunciator printer indicated

a

"P-250

COMPUTER

ROD

POS

DEVIATION ALARM."

The

ACO checked

the alarm

typewriter printout but did not notice the transposed

rod bank

positions.

At approximately 8:30 p.m.

on October 19,

1987, the

"P"250

RX ALM AXIAL FLUX /

ROD

POS" alarm window cleared.

When the

alarm cleared,

the operators

concluded that the P-250

RPDM was

operable.

At 5:06 a.m.

on October

20,

1987,

a routine test of the

RPDM determined that the

RPDM was inoperable

and that the rod bank

positions

had been erroneously

updated.

The operators correctly

updated

the rod bank positions

and successfully

re-tested

rod

position deviation

and rod bank sequence

alarms.

The incorrect rod bank positions resulted in the rod sequence

alarm

received in the control

room at 8: 17 p.m.

on October 19,

1987.

Once

the P-250 rod supervision

program initiated this alarm, it then

suspended

the

RPDM calculation

(as designed).

The licensee

determined

the root cause of this event

was personal

error in'hat after rebooting the P-250,

the

ACO incorrectly updated

the rod bank positions for the

RPDM program when

he transposed

control rod bank

D position with shutdown

bank

D position.

Additionally, when the

ACO was in the process

of checking for the

cause of the alarm, the alarm cleared

even though the P-250

RPDM was

J.

0

inoperable.

Since there did not appear to be

a problem with the

P-250,

the

ACO suspended

his search for the cause of the alarm.

After further review, the licensee still could not determine

the

cause of the annunciator

window clearing.

Accordingly on October

20, 1987, at about 12:57 p.m. the

RPDM was again declared

inoperable

pending further investigation

and P-250 test results.

The four hour

rod bank verifications required

by TSs were initiated at that time.

Root cause

determination of the window

clearing is considered

an

followup item.

(Open Item 50-275/87-38-02).

The Operations

Department

issued

an Operations

Summary Report

covering this event.

This summary

emphasized

the need to properly

update the rod position data following the P-250 reboot.

This

summary

was to be reviewed with all operations

personnel.

Unit 1 Fuel Handlin

Buildin Ventilation

S stem

On October 26, 1987, at 2:00 p.m., with Unit 1 at 100 percent

power,

the fuel handling building (FHB) ventilation system shifted into the

iodine removal

mode when

FHB area radiation monitor RE-59 lost

electrical

power.

Power was momentarily interrupted

when General

Construction

(GC) electricians lifted a lead to RE-59 when

installing a design

change

on monitors

RE-32 and RE-33.

This mode transfer constitutes

an actuation of an engineered

safety

feature

(ESF), which was reported to the

NRC at 2:55 p.m..

The

FHB

ventilation system

was shifted back to the normal

mode of operation

at 2:05 p.m..

The licensee's

investigation revealed that

GC electricians

were in

the process

of installing time delay relays in the circuitry to

radiation monitors

RE-32 and RE-33 in accordance

with design

change

notice

(DCN) DCl-EE-33354

RO.

The

DCN specified

AC power was to be

obtained

from an

AC terminal strip at the location where

RE-59

received its

AC power.

Discussions

were held with the responsible

IEC foreman to see if

there would be any adverse effects if the

AC power lead to RE-59 was

lifted.

After referring to electrical circui

diagrams

and the

RM

58/59 removal

from service

STP I-119Bl, the foreman determined

no

adverse effects would occur if the channel

was

removed from service.

In accordance

with the STP,

removal

from service

was accomplished

by

jumpering terminals in post accident monitoring panel

2 to prevent

the receipt of "LO" and "HI" radiation alarms in the control

room.

However,

when

a power lead to RE-59 was lifted, the

FHB ventilation

shifted to the iodine removal

mode.

Further investigation revealed

that the jumpers,

which were

installed

as called out in the procedure,

jumpered the

AC power to

the relays

and not the relay contacts,

as

assumed

by the

I8C

foreman.

Accordingly, when the

AC power was lost, the relay

de-energized,

causing the

ESF actuation.

Had the contacts

been

jumpered,

an

ESF actuation

would not have occurred

from lifting the

AC power lead.

10

The licensee

determined

the root cause to be personnel

error, in

that the plant I8C foreman reviewing the work instruction for the

design

change did not perform a sufficient enough review of the

circuit diagrams to determine

the effects of using

STP I-1119Bl for

installation of this design

change.

Licensee corrective actions

included:

o

the individual involved in this event

was counseled;

o

lessons

learned

from this event were to be reviewed with all

instrumentation

and controls

foremen through

a tailboard;" and

o

lessons

learned

from this event were to be incorporated into an

instrumentation

and controls technician quarterly training

seminar.

Ino erable

uadrant

Power Tilt Ratio

PTR

Alarm

TS surveillance

requirement 4.2.4.1 required calculation of gPTR

every

12 hours1.388889e-4 days <br />0.00333 hours <br />1.984127e-5 weeks <br />4.566e-6 months <br />

when the Unit 1 gPTR alarm was inoperable.

At 4:00

p.m.

on October

27,

1987, the

gPTR alarm became

inoperable

when one

of four nuclear instrumentation

system

(NIS) upper

and lower

detector

current comparators,

that provide input to the alarm,

was

disabled.

These detector

comparators

were disabled for 17.5 hours5.787037e-5 days <br />0.00139 hours <br />8.267196e-6 weeks <br />1.9025e-6 months <br />,

during which time the

gPTR was not calculated

once every 12 hours1.388889e-4 days <br />0.00333 hours <br />1.984127e-5 weeks <br />4.566e-6 months <br />

as

required, by the TS.

At 4:00 p.m.

on October 27, 1987, during calibration of NIS channels

N-41, N-42, N-43,

and N-44,

numerous

power range flux deviation

annunciator

alarms

were received.

It was determined that NIS

channel

N-44 was causing

the annunciator

alarms since it had not

been calibrated yet.

Because

of the alarms,

the shift foreman

ordered

the upper and lower comparators

for NIS channel

N-44

defeated.

The shift foreman did not realize that defeating

these

comparators

caused

the

gPTR alarm to become

inoperable

which

required the

gPTR to be calculated

every

12 hours1.388889e-4 days <br />0.00333 hours <br />1.984127e-5 weeks <br />4.566e-6 months <br />

as specified

by TS

4. 2. 4. l.

On October 28, 1987, the

I&C technician,

who defeated

the

comparators

on October 27, noted the comparators

were still

defeated.

He notified the shift foreman

who, then declared

the

gPTR

alarm inoperable.

At 9:29 a.m.

October 28, 1987,

NIS channel

N-44 comparators

were

reinstated

and Surveillance Test Procedure

(STP)

R-25 "Calculation

of quadrant

Power Tilt Ratio" was successfully

performed.

The licensee's

analysis

determined

the root causes

to be 1)

personnel

error in that the shift foreman

had the compar ators

defeated without realizing that this would make the

gPTR alarm

inoperable,

2) training deficiency in that there

was

a lack of

emphasis

on the specific function of the comparators

channel

defeat

11

switch's relation to TS 4.2.4.1,

and 3) labeling on the switch was

misleading

and did not specify gPTR.

The following corrective actions

were taken

by the licensee:

o

The comparators

channel

defeat switches for Units 1 and

2 and

the simulator were relabeled to indicate that operation of this

switch defeats

the

gPTR alarm.

o

The annunciator

alarm windows will be relabeled

from "PWR

RNG

FLUX DEVIATION" to a legend that indicates

a gPTR alarm.

o

The Operations

Department will write an Operations

Incident

Summary report which will be reviewed with all operations

personnel.

o

The Operations

Department will institute

a policy that requires

logging instrumentation into a log when

no applicable procedure

is available to record the defeat of the instrument.

Entr

Into Technical

S ecification

TS

3'.3 - More Than

One Shut-

down Bank Control

Rod Not Full

Withdrawn

On October

S,

1987, at 4:05 p.m. with Unit 1 at 100 percent

power,

a

slow plant shutdown

was initiated in accordance

with TS 3.0.3 when

four shutdown

bank control rods,

which had been inserted

one step,

were not able to be fully withdrawn within one hour as required

by

TS 3. 1.3.5 "Shutdown

Rod Insertion Limit."

An Unusual

Event was

declared

by the licensee.

At 5:30 p.m.

the shutdown

bank rods were

fully withdrawn,

TS 3.0.3

was exited,

and at 5:43 p.m. the Unusual

Event was terminated.

During the performance of monthly surveillance test

STP R-1A

"Exercising Full-Length Control Rods,"

a rod control urgent failure

alarm was received

when shutdown

bank

A group

2 control rods were

inserted

one step.

The indicator fuses for both shutdown,

and

control,

bank

A group

2 control rods failed, preventing withdrawal

of the rods.

I8C shift technicians

placed

shutdown

bank

A on

DC

hold power, replaced

the fuses,

and the urgent failure alarm was

reset locally.

As control rod

DC hold power was removed,

another

urgent failure alarm was received

when one of the fuses

(A65) blew a

second

time.

After further engineering

eval.uations,

the fuse was.

again replaced

and the urgent failure alarm was reset

from the

control

room.

Shutdown

bank

A was then fully withdrawn to 228

steps,

normal

rod control

was verified to be operable,

and

TS 3.0.3

was exited.

The event did not affect the ability of the rods to

drop into the core if required in response

to a reactor trip signal.

Root cause analysis of the fuse fai lures

was continuing at the time

this report was issued.

The inspector

observed that soldering

on

one

end of one of the power fuses

was of poor quality.

Since the

root cause

was under investigation,

I8C implemented monthly optical

pryometry (heat) inspection of control rod drive fuses until

corrective actions

have

been determined

and implemented.

Resolution

e

12

of this issue is considered

an open item (Open Item

50-275/87-38-03).

Failure of the Unit 2 Iso hase

Bus

C Phase

Motor 0 crated Disconnect

Re uirin

a Unit Tri

On November 7, 1987, at 1: 15 p.m.

a unit trip of Diablo Canyon Unit

2 was manually initiated due to the apparent failure of a motor

operated

disconnect

(MOD) in the main generator

25 kv isophase

Bus

"C".

At 1: 10 p.m.

a fire watch on rounds noticed green

and white light

emitting from the isophase

bus

room.

The fire watch notified the

control

room which dispatched

two operators.

The operators

confirmed the finding and deduced that arcing was occurring on one

of the buses.

They informed the control

room which initiated an

emergency

shutdown.

Following a brief discussion,

a manual unit

trip was initiated.

The unit trip was initiated by the operators

since, -in addition to initiating a turbine trip which initiates

a

reactor trip, it opens

the generator

output breakers

and transfers

electrical

loads to the startup transformers,

eliminating load on

the isophase

buses.

The licensee

made

a non-emergency

report in

accordance

with 10 CFR 50.72.

The licensee's initial inspection of the isophase

buses

determined

that the

MOD for Phase

C had caused

the arching.

The

MODs are

used

to isolate the generator

from the main transform to allow it to

supply plant loads

from 500kv offsite power during shutdown.

An MOD

is comprised of two sets of 62 stationary contact fingers arranged

in a cylinder,

one joined by flex link to the transformer side of

the bus, the other joined similarly to the generator

side of the

bus.

These sets of contacts

are separated.

Sliding over the

stationary contacts

is a cylinder of 62 copper shunt bars with

silver contact plates at both ends of each bar.

In the closed

position the contacts

of the stationary cylinders

make

up with the

contacts

on movable cylinder.

In the open position the movable

cylinder is retracted

over the transformer contacts.

The movable

cylinder is motor operated with control in the control

room.

The

licensee's initial inspection discovered

contacts

and shut bars

damaged

and discolored.

It was determined that the

MOD could not be

reused.

The licensee

did not have

an extra

MOD in plant stock.

In addition,

the vendor

no longer manufactures

that model

MOD.

A potential

replacement

was located at Cleveland Electric Company's

Perry Unit 2

on November 8.

An engineer

was sent to inspect the Perry

MOD to

ensure compatibility and to arrange for purchase

and transportation.

In response

to the event,

on November 10, the Vice President,

Nuclear

Power Generation,

invoked

AP C-18 "Event Investigation,"

.

which requires

the establishment

of an event investigation

team

(EIT).

The purpose of the team is to perform an in depth

investigation of significant events,

determine

probable

cause,

and

"achieve complete technical

understanding

of an event in a manner

13

that is timely, objective,

systematic,

thorough,

and technically

sound."

This was the first time AP C-18, issued July 1987,

was

invoked.

The EIT established

an action plan to determine

the root cause of

the failure.

The action plan was based

on the precepts

that switch

failure could only be caused

by increased

ambient temperatures

due

to inadequate

cooling', degraded

switch contact,

increased

load on

the switch,

and contact misalignment.

The action plan included

a

review of the bus cooling system

and temperature

data,

an inspection

of the adjacent

MODS, interviews of plant personnel

and the switch

representative,

and reviews of historical data, electrical

maintenance

records

and vendor drawings.

The licensee identified that the

MOD failure resulted

from a number

of contributory factors.

Specifically, the licensee

determined that

high abient temperatures

occurring five weeks prior to the failure

combined with degraded

switch contact resulted in increased

switch

resistance.

The increased

resistance

increased

heat which in

addition to increasing resistance

also

may have degraded

switch

contact.

This situation escalated

until the MOD's condition

produced arcing which was identified by operators.

The high abient temperatures

five weeks prior to the event were

caused

by a local heat wave.

The degraded

contacts

was attributed

to the hardening of lubrication grease,

possible contact

misalignment,

and

an accumulation of dust

on the contacts.

As corrective action,

the licensee

plans to develop

a comprehensive

preventive maintenance

procedure for the

MODs.

In addition,

the

licensee will develop

a surveillance

program which will address

isophase

bus cooling and the alignment of the isophase

bus contacts.

The licensee will also evaluate

the switch design to determine if

larger silver insert contacts will improve switch alignment.

In

addition, the licensee will evaluate

the desirability of different

MOD altogether.

Section

4.

c. discusses

maintenance activities related to

installation of the replacement

MOD.

In addition to the work

performed

on the Phase

"C" MOD, the licensee

inspected,

cleaned

and

lubricated, with guidance

from the manufacturer,

the

Phase

"A" and

"B" MODs.

The licensee

also visually inspected

the Unit 1 MOOS.

The

MODs were declared

operable

on November

13 and the licensee

started

up November

13 and 14.

The inspector will follow-up the

licensee's

corrective actions

in the normal course of future

inspections.

Seismic Plates

Missin

from Containment

H dro en Monitor Panels

On October 20, 1987,

an Instrumentation

and Control (I8C) technician

discovered

seismic support plates missing from all four containment

hydrogen monitors (two for each unit).

A search of the surrounding

area turned

up only one plate.

This was reported to operations

which declared

the hydrogen monitors inoperable.

In accordance

with

TS 3.6.4. 1 "Hydrogen Analyzers/Monitors"

a 72 hour8.333333e-4 days <br />0.02 hours <br />1.190476e-4 weeks <br />2.7396e-5 months <br /> action statement.

was entered.

The licensee's offsite engineering

analyzed

the effects of the

support plates

on the operability of the containment

hydrogen

monitors.

The plates

were required to support isolation modules for

the following:

a)

Indication and recording

on Containment

Hydrogen concentration

on the post accident monitoring panel in control

room.

b)

c)

d)

Signal input to the emergency

response facility data

system for

containment

hydrogen concentration.

Cell failure alarm.

High and low hydrogen concentration

alarms.

The licensee

determined that

a seismic event would not cause

the

loss of the ability to analyze

containment

hydrogen concentration

and that indication would be available at the

100 foot auxiliary

building panel

and the remote Post

LOCA sampling

room.

Based

on

this evaluation the licensee

determined that the hydrogen monitors

had never

been inoperable.

The licensee's

Instrumentation

and Controls (I8C) department

performed

an unsuccessful

search

to identify when the plates

had

been

removed.

At the end of this report period, the

I8C department

had

an open quality evaluation to determine action to prevent

recurrence.

This will be followed by the inspector during routine

inspection.

In addition,

an open non-confofmance

report related to

seismic bracing for control

room recorders

dealt with the

same

issue

of not restoring equipment to its design configuration following

maintenance

or surveillance, will be followed as

a related

item.

Unit 2 Fuel Handlin

Buildin Ventilation

S stem

S urious Shift to

Iodine Removal

Mode

On October

12, 1987, at 1:47 a.m., with Unit 2 at 97K power,

the

fuel handling building ventilation system

(FHBVS) shifted into the

iodine removal

mode.

This mode change constituted

an actuation of

an engineered

safety feature.

The operators,

were able to shift the

FHBVS to the normal

mode at 2:20 a.m.

In its normal

mode,

the

FHBVS exhausts

through exhaust

fan E-4 which

does not have charcoal filters.

In the iodine removal

mode,

the

FHBVS exhausts

through charcoal filters on the suction of exhaust

fans

E-5 and E-6.

The system is designed

to switch to iodine

removal

mode

on either

a failure of E-4 or high radiation in the

fuel handling building.

The licensee

experienced

similar shift to the. iodine removal

mode

on

July 7, 1987,

and November 18,

1987.

The licensee

has not

identified the cause

for spurious sh'ifts to iodine removal

mode.

15

There

have

been

no printouts

on the annunciator typewriter

indicating fan failure or a radiation monitor signal.

The licensee.

has investigated digital circuitry logic diagrams

and logic states

to determine possible

causes.

The licensee

has installed

a

multi-point data recorder to gather data if this event recurs.

This

was

a corrective action planned

as

a result of the October

12 event

and was staged for installation but not installed for the November

18 event.

These

events

and

a number of other

FHBVS and auxiliary building

ventilation system problems

are being followed up by the inspector.

One violation and

no deviations

were identified.

4.

Maintenance

The, inspectors

observed portions of, and reviewed records

on, selected

maintenance activities to assure

compliance with approved procedures,

technical specifications,

and appropriate

industry codes

and standards.

Furthermore,

the inspectors verified maintenance activities were

performed

by qUalified personnel,

in accordance

with fire protection

and

housekeeping

controls,

and replacement

parts

were appropriately

certified.

a.

Unit 2 Auxiliar Buildin Ventilation

S stem Exhaust

Fan E-2

Periodic Maintenance

Ins ection

The inspector observed

the performance of a periodic maintenance

inspection of the auxiliary building ventilation system exhaust

fan

ABVS-2-E-2.

The inspection included the cleaning,

meggering,

and

general

inspection of the fan motor,

a belt tightness

check,

and

an

inspection

and greasing of the fan inlet vanes.

The inspection

was

being conducted

in accordance

with a work order.

The inspector

noted that the belt tightness

check was being

performed with a tensioner

supplied

by the belt manufacturer.

The

mechanic

was performing the test in accordance

with instructions

supplied

by the vendor.

The instructions cited tolerances

for the

belts.

The maintenance

work order did not specify the

use of the

tensioner.

It instructed the mechanic to "slap" the belts

and note

whether they were "springy."

In following up this maintenance activity, the inspector attended

the Technical

Review Group

(TRG) dispositioning of a nonconformance

report

(NCR) regarding the fan belts

on ABVS-2-E-1 coming off the

belt sheaves.

The root cause

was established

to include

inconsistent

maintenance activity regarding belt installation, belt

tightening and belt and

sheave

inspection.

The

TRG determined that

corrective action should include

a maintenance

procedure to deal

specifically with belt installation.

The inspector

found the

corrective actions to be acceptable

to address

ventilation fan belt

problems including the inconsistencies

witnessed

during the

maintenance

of ABVS-2-E-2.

16

Unit 2 Motor 0 crated Disconnect

Re lacement

On November 7, 1987, Unit 2 was shut

down due to arcing of the

isophase

bus

C motor operated

disconnect

(MOD) (See Section

3. g.).

The

MOD had degraded

beyond recovery

and the licensee,

without a

replacement

part was forced to investigate other alternatives.

The

licensee

found a suitable

replacement part of Cleveland Electric

Company's

Perry plant.

However,

the replacement

was not identical

and required modifications to the plant prior to installation.

The inspector

reviewed the design

change

(DCN) associated

with the

MOD replacement.

The Perry

MOD was designed to be installed to a

16" square

bus whereas

the Diablo Canyon isophase

buses

are 21"

square at the

MOD.

To install the

MOD at Diablo, the flex links to

the bus

had to be placed together rather than 3" apart.

This

required the drilling of 64 holes in each

bus (transformer

and

generator

sides).

The licensee

evaluated

reduced contact area

between the flex links, due to the unused bolt holes.

The licensee

and the determined that contact area would be reduced

by

approximately 5.5X and found this acceptable

since the bus capacity

rating is approximately

15X above the actual

bus current.

The

inspector

independently calculated that contact surface

area would

be reduced

by approximately 6.0X.

The inspector reviewed the work order for the

MOD installation

and

found it referenced

the

DCN.

In addition the work order addressed

actions

necessary

to comply with TS 3.8. l.l.

The action statement

related to TS 3.8. 1. 1 allows offsite power supplied

from 1 of 2

sources

to be unavailable for 72 hours8.333333e-4 days <br />0.02 hours <br />1.190476e-4 weeks <br />2.7396e-5 months <br />.

The inspector discussed

the work with the electrician performing the

job and noted that the replacement

was being performed in accordance

with the work order and

DCN.

On November 4, 1987,

a leak from the bonnet of Unit 1 boric acid

evaporator recirculation valve FCV-739 occurred, resulting in about

125 gallons of borated water spillage onto the auxiliary building

floor and into the auxiliary building sump.

The leak was isolated,

and

a contamination

survey (number 13049) indicated

no contamination

was created

by the leaking component.

Action Request

(AR) A0089605

and Work Order

(WO) C0024356 were issued to remove the valve's air

actuator

and replace

the ruptured valve diaphragm.

WO C0024359

was

also issued to investigate

the cause of the diaphragm rupture at the

time the valve was disassembled.

The inspector

observed

the

disassembly,

which was performed

by qualified individuals in

accordance

with the work order.

Maintenance

personnel

concluded

the

diaphragm rupture

was caused

by over-stroking the stem and old age

of the diaphragm.

Additionally, a hole was found in the bonnet of

the valve, which was the source of the leakage.

The hole in the

carbon steel

bonnet

was caused

by boric acid corrosion.

Both the

diaphragm

and bonnet were replaced.

17

As another

diaphragm valve (CVCS-1-547 "emergency borate flow to the

volume control tank outlet isolation valve" ) had recently also

leaked,

the inspector questioned

whether the elastomer

diahpragm

material

was qualified for post accident conditions.

In discussion with onsite project engineering staff members,

the

inspector

concluded

documentation

was available to demonstrate

the

diaphragm material

was qualified for 40 years considering

normal

plus loss of coolant accident

(LOCA) radiation exposure.

However,

this time interval

was based

upon

a normal

diaphragm temperature

of

120 to 150 degrees

F.

Since

many diaphragm valves are

used in heat

traced

systems (at 165 degrees

F) or otherwise hot systems,

the

expected life of the diaphragms

decreases

dramatically.

In

particular, ITT-Grinnell Maintenance

and Instruction Manual

OC-663263-117-1

on page

33 specified

a diaphragm replacement

program

of:

o

inspect diaphragms

every six months, if accessible

(using

V

notched vent plug)

o

replace

diaphragms

every five years - more frequently if

extreme (temperature)

service

o

for inaccessible

valves,

replace

the diaphragms

every plant

maintenance

shutdown or at least every two years.

The manual also specified

a maximum six year shelf life for valve

diaphragms.

The inspector's

evaluation of the licensee's

preventative

maintenance

(PM) program to systematically

replace

diaphragms

exposed

to elevated

temperatures

concluded that for about

29 percent

(187) of these valves,

the diaphragms

had not been replaced

every

five years,

as specified in the

PM program.

AR A0029492,

issued

on

July 15, 1986,

documented that the diaphragm

inspections/replacements

were not done

due to difficulties in

clearing the valves

and

due to ALARA considerations.

However,

no

licensee

action was taken to effectively resolve the identified

concerns.

In discussions

with licensee

maintenance

management,

the licensee

agreed to evaluate corrective actions to assure

periodic

preventative

maintenance

of valve diaphragms.

Additionally, the

inspector identified concerns

regarding the licensee's

procedures

for valve stroke adjustment.

With the

numerous

types of diaphragm

valves

and operators

used at Oiablo Canyon,

the stroke adjustment

procedures

were not specific

enough to provide necessary

vendor

recommended

adjustment

information for each diaphragm/valve

combination in use at the plant.

In summary,

several

issues

remain outstanding

regarding this

subject.

They include

18

o

corrective actions to assure periodic diaphragm

replacement

(including valve clearance

problems)

o

diaphragm shelf life

o

diaphragm valve stroke adjustment

(manual

and operated

valves)

o

status

(open or closed) of vent plugs

on valve bodies in the

plant,

and need for vent lines to drains.

These

items are considered

unresolved

(Item 50-275/87-38-04).

No violations or deviations

were identified.

5.

Surveillance

By direct observation

and record review of selected

surveillance testing,

the inspectors

assured

compliance with TS requirements

and plant

procedures.

The inspectors verified that test equipment

was calibrated,

and acceptance

criteria were met or appropriately dispositioned.

a.

Functional Test of Area Radiation Monitor RM-10

b.

The inspector

observed

I8C surveillance testing of auxiliary

building control board area radiation monitor RM-10.

Thi s quarterly

testing

was conducted in accordance

with Work Order number

R0029327

and SfP I-107A.

The test verified the channel

responded

to its

check source,

high voltage

was within operating limits, local

and

remote alarm conditions were annunciated,

and the recorder

and

computer

outputs

were generated.

Appropriate authorizations

to

perform the test

had been obtained prior to beginning the test.

Data sheets

were verified to be correctly filled out and data

obtained

met acceptance

criteria.

Through discussions

with the

technician,

the inspector

concluded the technician

was qualified to

perform the test.

Solid State Protection

S stem

SSPS

Slave Rela

Testin

The inspector witnessed control operators

perform portions of

Surveillance Test Procedure

(STP) M-16P3 and M-16P4, continuity

testing of slave relays.

The inspector

noted that the two operators

performed the testing in accordance

with the, procedure,

reviewing

the procedure prior to performing it and establishing

communication

between

the

SSPS

room and the control

room during its performance.

No findings were identified.

No violations or deviations

were identified.

6.

En ineerin

Safet

Feature Verification

Auxiliar

Buildin

and Control

Room Ventilation

S stems

The inspector performed

a walkdown of the physically accessible

portions of the Units 1 and

2 auxiliary building ventilation system

f

19

(ABVS) and control

room ventilation system

(CRVS).

The inspector

looked at damper positions,

control

room and local indication,

breaker position,

and general

equipment condition.

The inspector

identified empty radiation waste

drums resting against

ABVS damper

26-A.

This was brought to the licensee's

attention

as

a possible

seismic interaction problem (see section 9.d.).

No violations or deviations

were identified.

TI 2500/19 - Low Tem er ature

Over ressure

Protection

LTOP)

Unresolved Safety

Ussue

(USI) A-26:

Reactor Vessel

Pressure

Transient

Protection for Pressurized

Water Reactors

was concerned with the

installation of an effective mitigation system for low temperature

overpressure

transient conditions.

The inspector verified that

LTOP

systems

were installed

on Units 1 and 2,

as described

below.

The

LTOP system at Diablo Canyon

uses

two pressurizer

power operated

relief valves

(PORVs)

as relief devices to protect the reactor coolant

system

(RCS) from brittle fracture at low temperatures.

The

LTOP system

inserts

a low-temperature

pressure

setpoint of 450 psig into the control

circuits of PORVs

PCV-455C and

PCV-456.

The normal setpoint of'he

PORVs

is 2335 psig.

The

LTOP system continuously

compares

actual

loop pressure

to the fixed pressure

setpoint of 450 psig.

When armed,

the

LTOP system

will open

PCV-455C

and

PCV-456 at 450 psig as

sensed

by

RCS loop,

wide-range

pressure

transmitters

PT-403 and PT-405, respectively.

Two conditions must be met to arm the

LTOP system:

The

LTOP circuits

must be enabled

by means of toggle switches,

and

RCS cold leg temperature

must be at or below 330 degrees

F.

Pressure

comparison,

arming of the

LTOP circuits,

and

PORV actuation

are all accomplished

in two separate,

mutually redundant

and independent

LTOP trains,

one each for PCV-455C and

PCV-456

'he

LTOP system is disabled during normal (at-power) plant operation.

During plant cooldown,

the system is enabled

in accordance

with Operating

Procedure

(OP) L-5 "Plant Cooldown from tIinimum Load to Cold Shutdown."

A separate

toggle switch is provided to enable

each train.

The enable

toggle switches

are located next to the control switches for PCV-455C

and

PCV-456 in the control

room.

When the switch is in the "cut in"

position,

a fixed setpoint of 450 psig is inserted into the automatic

control circuit for opening the>associated

PORV.. However,

the

PORV will

not open unless

cold leg, wide-range

temperature

is equal to or less

than

330 degrees

F.

When

LTOP is armed,

the normal

PORV setpoint of 2335 spig

remains operative but any pressure

excursions

should

be terminated

by the

PORVs at the

LTOP setpoint.

When the switch is in the "cut out"

position, the 450 psig setpoint is removed from the control circuit for

the associated

PORV.

A "PORV Low Setpoint Cut Out" annunciator installed in control

room

annunciator

window PK05-10 indicates that

RCS temperature

has

decreased

to 330 degrees

F or less while one or both

LTOP enable

switches

remain in

cut out position.

This annunciator will actuate

on either of the

following conditions:

20

o

RCS loop 3, cold leg, wide range temperature

(TE-433B) less than or

equal to 300 degrees

F,

and the

PCV 455C low setpoint protection cut

out switch not in the cut in position.

o

RCS loop 2, cold leg, wide range temperature

(TE-423B) less

than or

equal to 330 degrees

F, and the

PCY-456 low setpoint protection cut

out switch not in the cut out position.

Additionally, annunciator

window PK05-20 "Pzr Relief/Safety Vlvs Open"

indicates,

via

PORV position switches,

when

PORVs

PCY-455C

and

PCV"456

open.

The design of the licensee's

LTOP system

was reviewed by the NRC's Office

of Nuclear Reactor Regulation

as indicated in Diablo Canyon Supplemental

Safety Evaluation Report

(SSER)

Number 27.

Item 14 of that

SSER

specified that the

LTOP systems

"provided for Diablo Canyon, Units 1 and

2, meet the requirements

of RSB 5-2 and are acceptable...."

NRC Branch

Technical Position

RSB 5-2 considered

items

such

as the following:

o

10 CFR 50 Appendix

G limits for the

RCS while operating at low

temperatures

o

single active component failures

o

use of IEEE Standard

279 in the design

o

need for annunciation

o

testability

o

system "guality Group Classification" in accordance

with NRC

Regulatory Guide 1.26

o

seismic design classification

o

electrical

power source

The inspector

reviewed Unit 2 electrical

schematic

number 441306

and

verified the

LTOP system

was designed with redundant electrical

channels.

From a review of the design

change

package

used to instal,l the

LTOP

system,

the licensee re-verified the system

was installed

as

an

instrument Class lA (seismic)

system.

LTOP operating

procedures

(OPs)

and administrative controls were reviewed

by the inspector.

Technical Specification

(TS)

LCOs 3.4. 1.3 "Reactor

Coolant System - Hot Shutdown"

and 3.4. 1.4. 1 "Reactor Coolant System-

Cold Shutdown - Loops Filled" specified:

"A reactor coolant

pump shall not be started with one or more of the

Reactor Coolant System cold leg temperatures

less

than or equal to

323 degrees

F unless:

(1) the pressurizer

water level is less than

50K, or (2) secondary

water temperature

of each

steam generator

is

less than

50 degrees

F above

each of the Reactor Coolant System cold

leg temperatures."

c

21

OP L-1 "Plant Heatup

from Cold Shutdown to Hot Standby"

incorporated this

TS statement

in the Precautions

and Limitations section of the procedure.

However, the inspector

noted the

TS statement

was not included in OP L-5

"Plant Cooldown from Minimum Load to Cold Shutdown.'"

This situation

was

discussed

with operations

management

and action request

A0090871

was

issued

by the licensee to include the statement

in L-5 to enhance

the

procedure.

OP L-5 did include specific steps to (1) disable both SI

pumps,

(2) disable all but one centrifugal charging

pump,

and (3) cut in

LTOP when Tavg was less

than

350 degrees

F and

T cold was greater

than

323 degrees

F.

Step ll.d of OP L-5 also specified that with a solid

RCS

condition, all pressurizer

heaters

were to be turned off and

a caution

tag be attached

to the heater controls in the control

room.

OP L-6

"Refueling" indicated the

RCS low pressure

protection

system

was to be

cut in as

a initial plant condition for that mode of plant operation.

Another statement,

existing in OPs L-5, L-l, and A-6: I "Reactor Coolant

Pump's - Place in Service,"

was

as follows:

"With the

RCS in the solid condition, if all

RCPs are shutdown for

more than

5 minutes

and the seal injection water temperature

is less

than the coolant temperature,

do not start

an

RCP until the primary

system

has

been cooled to the temperature

of the seal injection

water, or a steam bubble is drawn in the PZR."

The purpose of this statement

in the

OPs

was to caution against

low

temperature

overpressurization

of the

RCS.

Operator training on the

LTOP system

was reviewed

by the inspector,

also.

Training of licensed operators

was conducted

by the licensee utilizing

Instructor

Lesson

Guides

LA-1 "Reactor Coolant System

and Auxiliaries"

and LA-4a "Pressurizer

and Pressure/Level

Control."

Lesson

number

LA-1

discussed

LTOP features

such

as annunciation,

setpoints,

source of

pressure

signal, enabling circuits, pressure

transient conditions,

and

vessel brittle fracture

and neutron embrittlement.

This training was

provided'uring the first week of training classes.

Ouring the sixth

week,

LA-4a presented

the specifics of the

LTOP design

and operation

once

again.

Several

simulator scenarios

were also observed to contain

shutdown operations with the

LTOP feature cut-in.

In particular,

lesson

LS-4-3B "Cold Shutdown/Loss of Cooling" involved shutdown operations with

a failure of PT-403,

causing

an inadvertent initiation of a

PORV.

Training attendance

records

were also

sampled

by the inspector.

Surveillance

records pertaining to

LTOP components

were also reviewed.

STPs I-68A and I-69A required functional testing of the

PORV overpressure

protection channels

(excluding

PORV operation) within 31 days prior to

entering

a plant condition in which

PORVs are required to be operable.

This testing verified proper operation of temperature

and pressure

inputs

to the overpressurization

actuation logic.

STPs

I-68B and I-69B required

calibration of PORV overpressure

protection channels

403 and 405 at least

once per 18 months.

STPs

I-68C and I-69C were also performed to measure

the reaction time timing of the

PORV actuation circuitry.

No violations or deviations

were identified.

22

8.

Radiolo ical Protection

~

~

The inspectors periodically observed radiological protection practices

to

determine whether the licensee's

program was being implemented in

conformance with facility policies

and procedures

and in compliance with

regulatory requirements.

The inspectors verified that health physics

supervisors

and professionals

conducted

frequent plant tours to observe

activities in progress

and were generally

aware of significant plant

activities, particularly those related to radiological conditions and/or

challenges.

ALARA consideration

was found to be an integral part of each

RWP (Radiation

Work Permit).

No violations or deviations

were identified.

9.

~0ee

Items

as

Unit 2

S ent Fuel

Pool Area Radiation Monitor

0 en Item

50-323/87-34-01

Closed

In inspection report 50-323/87-34, it was noted

by the inspector

that from April 1985 to October

1987

no apparent capability existed

for recording the atmospheric radioactivity in the spent fuel and

new fuel storage

areas of Unit 2.

FSAR table 11.4-1, "Radiation

Monitors and Readouts"

shows that both the spent fuel pool area

monitor (RE-58) and the

new fuel storage

area monitor (RE-59) are

recorded

by RR-58 and

RR-59 respectively,

at the radiation

monitoring rack-A.

For Unit 1 and Unit 2, this feature

has

never been

implemented.

When RE-58 and RE-59 were installed

on both units, the wrong

interface

between

the monitor and existing recorder

was installed.

The design

change to install

a new interface

was delayed

when plans

were

made to install

a

new recorder

design.

At the time of this

report,

a

new recorder

had not been installed.

The absence

of a

recording device

was

more notable for Unit 2 until October 1987,

since the inputs to the P-250 plant computer from RE-58 and RE-59

were processed

by the wrong computer routine until that time.

Failure to have

a recording device installed for RE-58 and

RE-59 for

both Units is an apparent

deviation from the commitments of FSAR

Table 11.4-1 (Item 50-323/87-38-03).

Section ll of this report discusses

problems. identified with the

containment

temperature

monitors for Unit 2.

There appear to be

a

number of long standing

problems with other radiation monitoring

systems.

While the licensee is addressing

the large backlog of

items in a methodical

fashion,

they do not appear to be in a

position of addressing

new problems with the monitoring systems

as

they occur unless

required

by technical specifications.

In the

cases

of RE 58 and

59 and the containment

temperature

monitors, the

problems

have existed since startup.

b.

Grade

8 Bolts (0 en Item 50-275/87-04-05

Closed

0

23

In November 1986, in response

to concerns of counterfeit bolts, the

Vender Program Branch of the then Division of Inspection

and

Enforcement

requested

the licensee

to supply a sample of SAE J429

Grade

8 bolts for chemical

analysis

and tensile testing.

In a

letter dated February 13,

1987, the Vender Program Branch informed

the 'licensee that one of the licensee

supplied bolts

had failed the

tensile test

by approximately

10K.

In response,

the licensee

placed all Grade

8 bolts from the affected

vendor .on hold.

The licensee

also identified that

no Grade

8 bolts

had been

issued for safety-related

use.

The licensee

tested

32

bolts from 15 heat

codes

and found only 2 did not pass

the wedge

tensile

load test.

Based

on the test results,

the licensee lifted

the hold on all bolts for safety related applications

except for the

two heat

codes which failed the wedge tensile

load test.

Subsequently,

on September

16,

1987,

the Office of Nuclear Reactor

Regulation

(NRR) informed the licensee that the original testing

had

been performed incorrectly.

Based

on the licensee's

actions

and the

findings of NRR, this item is closed

(Open Item 50-275/87-04-05,

closed).

Boron In ection Tank

BIT

Relief Valve

0 en Item 59-323/87-34-02

~0en

By letter dated

November 6, 1987, the licensee

provided information

to the

NRC regarding

leakage

from the Unit 2 BIT relief valve.

The

letter specifically addressed:

o

Clarification of the

FSAR update description of the BIT thermal

relief valve installation.

o

Potential

valve leakage

rates

and doses

from radioactivity

associated

with postulated

post-LOCA conditions.

o

The licensee's

leak reduction program,

including pending

revisions to STP M-86 "Leak Reduction of Systems

Outside

Containment Likely to Contain Radioactive Materials Following

an Accident (NUREG-0578, TMI-9)."

The letter responds

to the questions

posed in Inspection

Report

50-323/87-34

(unresolved

item 50-323/87-34-02).

The licensee's

response will be addressed

by the Office of Nuclear Reactor

Regulation.

The commitments

made in the letter wi 11

be followed up

in the course of routine inspection.

The inspectors

discussed

with

the licensee

two concerns

regarding this issue.

Specifically:

1)

Has the licensee initiated a corrective action/root

cause

evaluation of why FSAR leakage limits for post

LOCA

recirculation were not incorporated into STP M-86, and,

2)

what consideration

is being given to leakage

evaluation

between

refueling outages?

24

This item remains

unresolved.

d.

Licensee Action Re ardin

Seismic

Hazard Sensitivit

50-275/87-26-02

Closed

This open item dealt with the recurring examples of transient

items

which were found by the inspectors

to represent

a hazard to

important safety equipment if an earthquake

occurred.

Such items

included heavy I8C mobile test carts next to safety related control

cabinets

and not in active use.

During the current reporting period the inspectors identified

additional

examples

on seismic

hazards

which indicated that the

licensee's

actions to sensitize plant staff to seismic

hazards

had

not been sufficient to preclude recurrence.

Specifically,

on October 23,

1987,

the inspectors

noted

55 gallon

waste

drum stacked

two high and leaning against controls for safety

related ventilation damper

E-22B.

Additionally, a nitrogen bottle

was observed tied to structure in the Unit 2 containment penetration

area at elevation

115 feet.

Additionally, on October 13,

1987, the

inspector

noted

10 to 12 pieces of turbine cowling parts,

estimated

to weigh several

hundred

pounds

each,

temporarily stored

on

electrical conduit for and on the ventilation duct for the Unit 2

control

room pressurization

system.

The licensee's

housekeeping

procedure

(NPAP-C-10) requires that

ancillary items

be stored

so that they will not impact and

damage

safety related

equipment.

The licensee is currently evaluating the

impact of the observed

items

on the related

equipment.

The failure

to comply with the procedural

requirement to protect safety related

equipment will be followed as

an unresolved

item pending the

licensee's

evaluation.

(Item 50-323/87-38-04).

No violations or deviations

were identified.

10.

Ph sical Securit

Security activities were observed for conformance with regulatory

requirements,

implementation of the site security plan,

and

administrative

procedures

including vehicle

and personnel

access

screening,

personnel

badging, site security force, manning,

compensator'y

measures,

and protected

and vital area integrity.

Exterior lighting was

checked during backshift inspections.

No violations or deviations

were identified.

11.

Licensee

Event

Re ort Follow-u

a.

Status of LERs

Based

on an in-office review, the following LERs were closed out by

the resident

inspector:

0

J

25

Unit 2:

87-15,

87-15

Rev

1

87-05

Rev 1

b

r

The

LERs were reviewed for event description,

root cause,

corrective

actions taken,

generic applicability and timeliness of reporting.

Red Tele

hone

vs

LER Trackin

The licensee

has evaluated

the following 10 CFR 50.72 events for

reportability under 50.73

and has determined that 50.73 report is

not required.

The resident inspectors

have

examined the licensee's

rationale

and determined that regulatory requirements

have

been

met.

50.72 Report

Date/Unit

Event

Reference

NCR

etc.

10/8/87/Unit 1

REN 10245

NCR 8 DCI-87-EM-112

Maintenance activity on wrong

component

and entry into TS 3.0.3

due to inoperable

redundant trains.

One train

later determined to have not

been inoperable.

No violations or deviations

were identified.

~

~

12.

Containment

Local

Leak Rate Testin

The inspector

reviewed the licensee's

containment

)ocal leak rate testing

program through direct observation,

record review,

and procedure

review

for compliance with 10 CFR 50 Appendix J "Primary Reactor

Containment

Leakage Testing for Water-Cooled

Power Reactors,"

and the licensee's

Technical Specifications.

The inspector

reviewed the licensee's

programs for Type

B leak rate

testing,

which includes the testing of electrical penetrations

and

containment air lock doors,

and for Type

C leak rate testing which

includes

the testing of containment isolation valves.

The inspector

found that all applicable penetrations

were addressed

by approved

Type

B

and Type

C test procedures.

The procedures

for

were found to be in

accordance

with the requirements

of 10 CFR 50 Appendix J.

The procedures

require testing to be performed at or above the containment

design

pressure

of 47 psig with leakage

rates

determined

using the maximum

pathway leakage.

The procedures

also provided clear acceptance criteria

and appropriate

action consistent with the Technical Specifications.

The inspector witnessed

the performance of two Type

C tests

and

determined that the engineer performing the tests

complied with the

procedures

using test equipment with calibration.

The inspector

reviewed the licensee's

procedure for the combined

Type

B

and Type

C leakage evaluation.

The procedure

requires

an evaluation

be

26

performed

on a nominal

24 month frequency

and to be updated

whenever

an

individual test is performed.

The inspector reviewed the licensee's

total leakage calculation

and tracking and found them to be acceptable.

No violations or deviations

were identified.

13.

Inde endent

Ins ection

a.

Review of Annual

Re ort of Chan

es

Tests

and

Ex eriments

The licensee

submitted

PG8E letter

NO: DCL-87-270 to the

NRC on

November 9, 1987.

The letter is the required annual

report of

changes,

tests

and experiments

conducted

under the licensee's

cognizance

in accordance

with the requirements

of 10 CFR 50.59.

The

licensee's

report was reviewed by the inspector.

No violations were

identified.

b.

Technical

Review Grou

Effectiveness

The inspector

reviewed the effectiveness

of the licensee's

technical

review group (TRG) over the past year.

The purpose of the

TRG is to

evaluate

nonconformances

for cause

and establish

the corrective

actions required to prevent recurrence.

The procedural

requirements

for the

TRG are contained

in licensee administrative

procedure

(AP)

C-12 "Identification and Resolution of Problems

and

Nonconformances."

In general,

the inspectors

have noted

improvement in the conduct of

TRG.

The areas of improvement

has

been in:

o

The identification of root cause.

o

The identification of effective corrective actions.

These

improvements

can

be attributed in part to a

TRG chairman

training program.

The program teaches

techniques

which can

be

'employed to determine root cause

and corrective actions.

Some areas

of weakness

have

been:

o

A tendency of addressing

too narrow a scope.

o

Not having appropriate

persons

attend, specifically those with

first hand

knowledge of nonconformance.

o

Participants without first hand knowledge making decisions

based

on assumptions.

The inspectors will continue to monitor the effectiveness

of the

TRG

during routine inspection

and event follow-up.

No violations or deviations

were identified.

14.

Follow-u

of Re ional

Re uests

0

27

Containment

Tem erature Honitorin

The licensee for Arkansas

Nuclear Unit 1 reported to the

NRC that

average

containment

environment temperatures

at the time of the

report exceed

those

used

as

bases for environmental qualification

and post-accident

analysis.

Therefore,

the inspector

performed

an

examination to determine

the adequacy of Diablo Canyon's

containment

temperature

monitoring system,

including the following questions:

o

What containment

temperatures

are the bases for environmental

qualification (Eg) and loss of coolant accidents

(LOCA)?

o

Do the licensee's

TSs include temperature

limits for the

primary containment

and, if so, what are they?

o

How are the temperatures

measured

and recorded?

o

Has the licensee

had difficulty keeping containment

temperatures

within limits?

The licensee

assumed

120 degrees

.F as

an average

containment

temperature for both the initial conditions for the peak containment

pressure

analysis following a

LOCA and-environmental

qualification.

The plant TS 3.6. 1.5 establishes

an average

containment temperature

f 120 degree

F as

a limiting condition for operation.

TS 4.6. 1.5

requires that containment

temperature

be determined

by averaging

4

of 8 containment temperature

monitors every 24 hours2.777778e-4 days <br />0.00667 hours <br />3.968254e-5 weeks <br />9.132e-6 months <br />.

The TS action requires

temperature

be reduced

below 120 degrees

F in

8 hours9.259259e-5 days <br />0.00222 hours <br />1.322751e-5 weeks <br />3.044e-6 months <br />

or

shutdown.

Both units were originally designed with 30 containment

temperature

monitors.

Four monitors measure

vessel

shield wal 1 (at the

same

elevation) at four corners.

These monitors feed the P-250 computer

and annunciate

at 130 degrees

F.

The purpose of the four monitors

is to monitor concrete

temperature.

In addition,

two wide range

monitors were installed in each unit to meet the requirements

of

Regulatory Guide 1.97.

The final 24 monitor containment

temperature

in various areas

and input to the containment air temperature

measuring

system panel.

Eight of these

are

used to fulfillTS

4.6. 1.5 requirements.

The final sixteen monitors were installed to

monitor temperatures

during the containment .integrated

leak rate

test

(CILRT).

On Unit 1,

12 of the CILRT monitors can

be selected

individually or

as

an average for input to the control

room.

The control

room input

feeds

a chart recorder,

the safety parameter display system

(SPDS),

the P-250 computer,

and an annunciator.

The P-250 computer inputs

to an annunciator

which alarms at 120 degrees

F.

On Unit 2, the CILRT temperature

monitors

have

been

spared

in place

at the containment air temperature

monitor system

panel

in

accordance

with a design

change

since the contractor

used for the

CILRT does their own containment

temperature

monitoring.

The eight

28

TS 4.6. 1.5 monitors were designed

to input an average of the

selected

monitors to the control

room (the chart recorder,

annunciator,

SPDS,

and P-250).

However, the individual select

switches

do not remain depressed

after selection

and

a signal

does

not reach the control

room.

This condition has existed since Unit 2

startup.

As a result, the only direct containment

temperature

monitors in the control

room are the containment hi-range monitors.

At the time of the inspection,

the licensee

had identified the

select switch deficiencies

and

a design

change

was being initiated.

The inspector

reviewed the annunciator

response

manual

and found

some

inadequacies.

Firstly, the selected

containment air

temperature

monitor system monitors were not listed as possible

inputs to the

"CONTMT ENVIRONMENT P-250" annunciator.

Secondly,

the

list of "operator actions"

was incomplete.

In response

to the

inspector's

findings, the licensee initiated an action request to

revise the annunciator

response

procedure.

The revised procedure

will be reviewed during routine inspection.

The licensee

has

had

no problems

keeping the containment

below 120

degrees

F due to a large design margin in the component cooling

water

(CCW) system which cools the containment

fan cooler units.

The licensee

generally maintains

average

containment

temperature

around

95 degrees

F.

No violations or deviations

were identified.

~

~

~

~

~

15.

Alle ation Follow-u

a.

Alle ation No:

ATS RV-87-0034

Characterization

During the public comment portion of the Atomic Safety Licensing

'oard

hearing

on spent fuel racks held at Avila Beach

on June

15,

1987

an individual announced

to the board that

he had

a previously

undisclosed allegation that unqualified weld joints were used at

Diablo Canyon.

Subsequently,

discussions

with the individual and

the resident inspector revealed that the concern

was specifically

the joining tube steel

shapes

in a "tee" configuration

on pipe

supports.

The individual stated that the joint configuration wasn'

qualified to

AWS Dl. 1, the American Welding Society's Structural

Welding Code.

Im lied Si nificance to Plant Desi

n

Construction

or 0 eration

. The inspector

examined the previous history of allegations at Diablo

Canyon for the subject of the welding of tube steel

and examined

AWS

D1. 1-82, the Structural

Welding Code.

The results of that examination

show that the individuals concerns

had

been previously examined

and found acceptable

by the

NRC as

summarized

below.

29

AWS 01. 1-82 has

some special

requirements

for the weld joint

configuration which is formed when tube steel is used.

The joint

configuration is called

a flare-bevel

groove weld and refers to the

geometry obtained

when

a round bar is placed against

a flat plate.

AWS Dl-l limits the amount of effective weld throat that can

be

assumed

by the designer

using such

a configuration and requires

tests to verify the effective throat is achieved.

The licensee,

however, did not perform pipe support welding in

accordance

with AWS D. 1.1 but rather qualified welders

and welding

procedures

to the

ASME Boiler and Pressure

Vessel

Code.

This fact

was the subject of the Diablo Canyon Allegation Management

Program

(Allegation ¹110)

and was addressed

and found to be satisfactory in

the

NRC Safety Evaluation report,

NUREG 0675 Supplement

No.

22

(SSER

22).

It should

be noted parenthetically

here that the issue of proper

flare bevel welding was explored extensively at Diablo Canyon in

response

to allegations

and inspection findings.

Below is

a partial

list of allegations

and the safety evaluation reports that evaluated

the stated situations

as satisfactory:

o

Allegation 92

Flare bevel welds were undersize

and not

per code

(SSER 22)

o

All,egation 94

o

Allegation 103

o

Allegation 105

Pipe welding procedures

were

used for

structural

welding

(SSER 21)

Structural

shapes

are not specified

on Weld

Procedure

Specifications

(SSER 22)

Weld joint 'geometry not specified

on Weld

Procedure

Specifications

(SSER 22)

The safety evaluations

describe

the

NRC staff's evaluations

and

concluded that the flare bevel welds comply with AWS D. l. 1 and the

quality was good.

The

NRC staff performed

independent

inspections

and

had independent

inspections

performed for the

NRC by Lawrence

Livermore National Laboratory (LLNL) personnel

(under contract).

Further,

the

NRC staff had Pullman

Power provide an evaluation of

flare bevel

welded joints for tube steel.

The evaluation

showed

that all welds

made

on various sizes of tube steel

met or exceeded

AWS Dl. 1 effective throat requirement.

Additionally NRC Inspection

Report 50-275/84-11

and 50-323/84-11

states

that

LLNL performed independent

inspection of tube steel

radius of curvature

and

NRC reviewed the w'eld tests

performed by the

licensee

to show that the proper effective throat

had been achieved.

The

NRC inspectors

also

examined

samples

cut from various sizes of

tube steel.

The inspectors

stated that they had

a high degree of

confidence that the weld throat thickness

assumed

by the designer

had been effectively implemented.

30

The inspector therefore

concluded that the question of flare bevel

welds

as

used at Diablo Canyon for joining tube steel

members in

pipe supports

had been fully addressed

in previous allegations.

In regards

to the specific concern stated,

specifically tube steel

joined to tube steel

in a "tee" configuration,

the inspector

reviewed the applicable welding procedure

(weld procedure 7/8), the

specification for installation and inspection of pipe supports

(Pullman

Power Products Specification

ESD 223

AWS D. l. 1), the

allegations,

and

PG8E responses

to the allegations.

These

documents

show an evolution of improving specifications,

requirements,

and actions.to

demonstrate

that the pipe support

welding was adequate.

The "tee" configuration is addressed

in PGCE

letter DCL-84-40 of February 7, 1984 (to the NRC), Attachment 3, in

regard to the proper welding symbols to be used for the

configuration.

AWS Dl. 1 allows for partial penetration

welds without backing bars

and with root openings of various amounts.

The flare bevel weld

being questioned

is a partial penetration

weld being welded with a

root opening.

The licensee's

actions to perform production/qualification tests

for

the flare bevel configuration were not performed until after

a great

deal of welding had already

been performed but that subject

was

fully covered in the resolution of allegations previously discussed

and it was adequately

demonstrated

that the design engineers

assumption of good weld metal for 5/8 of the tube steel

thickness

was achieved.

Staff Position

The staff position is that the welding of tube steel

had not indeed

been qualified per

AWS Dl. 1 literal requirements

but that this

subject

had been thoroughly examined

and found acceptable

by the

NRC

in the examination of previous allegations.

Action Re uired

None.'lle

ation

No:

ATS RV-87-0033

Characterization

The alleger

stated that guality Assurance

(gA) had done

an audit on

measuring

and test equipment

and

had found that the equipment

was

seriously out of calibration and

had been for several

years.

The

alleger stat'ed

these conditions

had been reported to upper

management

who did nothing and that workers

had then

gone

anonymously to the gA manager

who then performed

an audit.

The

alleger stated that upper management

"got the man". who had given

~4'i

31

information to gA, they denied

him raises,

gave

him a pay cut and

took him off the overtime list.

Im lied Si nificance to Desi

n

Construction or 0 erations

Measuring

and testing equipment, if seriously out of calibration,

could lead to plant equipment operability verification tests

being

inaccurately performed

and verifications of performance

parameters

invalid.

If upper

management

had been unresponsive

to correcting equipment

seriously out of calibration,

then the licensee's

responsiveness'o

safety issues

would be in question.

If the person identifying the safety concern

was the object of

retribution for raising those concerns,

then the licensee's

actions

would have

a chilling effect on other personnel

who might have

safety concerns.

Assessment

of Safet

Si nificance

The inspector

examined

records of the audit, actions

taken

as result

of the audit,

and discussed

those actions with involved plant

personnel

including gA, gC,

and IIC.

The inspector

examined the audit report

(PG&E audit report 87134P)

dealing with the measuring

and test equipment

(M&TE) area.

The

audit was performed by PG&E gA personnel

from May 7 to June 3, 1987.

The audit report found the

M&TE programs for mechanical

maintenance

and electrical

maintenance

adequately

implemented.

For the

Instrumentation

and Controls department,

the audit revealed

several

findings.

The most significant finding was that

some permanently installed

M&TE (such

as pressure

gages)

had not been included in all the

M&TE

administrative

programs.

More specifically, industry standards

and

the licensee's

procedures

require that when measuring

and test

equipment is sent back for periodic recalibration,

and if the item

found to be out-of-calibration,

then

an evaluation

must be made of

all equipment

on which the

M&TE item was used,

to ensure

whatever

test was

done

and its results

were still acceptable.

The licensee's

procedures

did this for portable

M&TE.

The audit finding points out

that

some test procedures utilize installed plant equipment,

such

as

gages,

for reading of test acceptance

values

and,

as such, that

installed equipment is "M&TE" which, although it is periodically

recalibrated,

should also trigger an evaluation of test data if it

is found out-of-calibration.

The specific audit findings and licensee

actions

taken were:

o

Nonconformance

Report

NCR DCO-87-TI-N072 documented that

out-of-tolerance plant equipment

(used

as

M&TE) did not have

'/

~L'

A

32

adequate

actions taken to evaluate

the situations

where the

equipment

was

used for performance tests.

The licensee initiated a review to determine

the impact of

previously performed tests

done with plant installed

NOTTE.

Nonconformance

Report

NCR DCO-87-TI-N050 documented that

history searches

for out-of-tolerance test equipment were not

completed in a timely manner.

The licensee's

corrective action was to revise the

appropriate

procedures

to provide

a time limit for the

history searches

and to conduct training.

The licensee

also determined that

a contributory cause

was having more

stringent than necessary

tolerance

requirements.

Note:

The nonconformance

was written by plant staff.

Plant management

personnel

stated to the inspector that

the

NCR was defined

and in process

of issuance prior to

the audit and was not a result of the gA audit.

However,

it was further observed that the issue of untimely action

on history searches

was identified by plant gC in quality

evaluation written on June

27,

1986

(gE 003235).

o

Nonconformance

Report DCO-87-gA-N001 documented that

calibration accuracy ratios between calibration standards

and

H8TE had not, in all cases,

been

documented'.

The licensee's

action includes the forming of a task group

to provide corrective action.

'I

Audit Finding Report

AFR 87-110 described

the condition that

radiation protection

and environmental

monitoring equipment

which was being maintained

by ICC did not have

a list which

specified which equipment, if any, should

be under the quality

assurance

program.

The licensee's

action was

was to perform an initial

assessment

that indicated

no adverse

impact on plant

conditions.

Radiation protection equipment in use

had

been calibrated.

The Chemistry

and Radiation P'rotection

manager stated that action

had been initiated to define

which radiation protection equipment should

be designated

as

under

the quality assurance

program but that the

methods of calibration

need not be changed

since they had

not been found faulted by the audit.

The

NRC had

performed

a team inspection,

in October 1987, of the

chemistry

and radiochemistry laboratory standards.

The, inspection

found the calibration methodology to be

sound (Reference

Inspection

Report 50-275/87-24.

o

Audit Finding Report AFR-111 de'scribed

twelve items of

NOTTE

which had been

logged out for long periods of time and which

0

33

could not be located during the audit and did not have adequate

traceablity of use through the usage

logs.

Licensee corrective actions

include procedure

revisions to

strengthen

logout controls, training of personnel

and the

missing equipment

was resolved.

r

o

Audit Finding Report

AFR 87-112 reported that

no list 'or

procedure existed to identify which I8C equipment required

calibration stickers.

The licensee's

corrective action was to revise the

applicable

procedure to include

a list of I8C equipment

requiring calibration stickers.

o

Audit Finding Report AFR-87-113 reported several

related

concerns,

specifically:

that procedures

had not been

used for all calibrations

performed

by I8C.

Four cases

were observed

where

a shop work

follower or work order was used.

that the electronic calibration lab procedure

manual did not

contain copies of seven procedures

used

by I8C to calibrate

chemistry and radiation protection equipment.

that the procedure

used

had not been

documented

on the records

for 29 devices.

that six procedures

did not have documentation of review for

completeness

by I8C technicians.

Licensee actions

include correcting the calibration lab

procedure

book, eliminating work order based instructions

and using only approved procedures,

developing

a procedure

review checklist, correcting procedure errors,

and

including an entry (to indicate the procedure

used)

on

calibration data sheets.

o

Audit Finding Report

AFR 87-114 stated that the Master

Calibration Schedules

(MCS) was outdated

and incomplete.

Temporary procedure

changes

had not been

documented.

Four sets

of duplicate

equipment identification numbers

were noted.

Six

out-of-tolerance

notices did not have all information recorded.

Two pressure

gages

did not meet

a transfer standard

accuracy

requirement of 4: 1 and did not have

a documented

authorization

permitting this.

The licensee's

actions

included deleting the

MCS and

utilizing an electronic data

base

equipment list and

calibration schedule

(which had been in formative and

concurrent use), eliminating all duplicate identification

numbers,

resolving the missing information on

out-of-tolerance notifications,

and including the transfer

34

standard

accuracy

requirement in a procedure

development

checklist.

o

Audit Finding Report

AFR 87-115 reported that the

I8C

electronic calibration lab did not meet the requirements

for

cleanliness,

controlled access

or environmental

monitoring.

The licensee's

corrective action including temporary

utilization of the general

construction facilities

calibration laboratory and plans to upgrade

the plants

calibration facility.

Discussion

The

sum of audit findings and nonconformance

reports discovered

by

the licensee

and documented for corrective actions indicate that

indeed the control of measuring

and test equipment,

and installed

plant indication used for test data,

was not totally adequate.

It

is to the licensee's

credit that the the problems

were identified

through the licensee's

quality assurance

process.

It is somewhat

to the licensee's

detriment that the problems

were not more promptly

identified and corrected

by line management

responsible for the

activities.

The key to identifying the problems in the

t4hTE area

appeared

to be

the advent of a senior technician,

experienced

in calibration

laboratory procedures

and practices,

on the plant staff.

The

technician properly identified perceived

problems to his supervision

and management

in early 1987 but no comprehensive

actions

were

initiated at that time (based

on the lack of documented

problem

identification).

gA personnel

in conducting

an audit of t4hTE in the general

construction

area

became

aware of the perceived

problems in the

plant calibration facility and both contacted

the senior technician

and focused their audit efforts in the plant area.

The senior technician

was properly forthright with the auditors in

identifying perceived

weakness

and areas

requiring correction.

The inspector

discussed

the MTE situation with the senior

technician

subsequent

to the receipt of an anonymous allegation.

The senior technician indicated that

he

had discussed

his opinions

regarding the NTE area with his supervision

and management

and the

gA auditors.

He indicated that

he

had not been adversely treated

and was comfortable in bringing up the matters.

He indicated that

he personally did not like overtime

and that the lack of overtime

was his choice.

The inspector concluded that there

was

no evidence

that the senior technician

had been "gotten" by upper management.

The inspectors

review of licensee

corrective actions

was conducted

in November 1987.

The inspector

noted that much of the corrective

action was not complete

and was scheduled for completion in December

1987 and later in 1988.

35

The major corrective actions

are to utilize the better calibration

facility at General

Construction until such time as the funded I8C

.

shop

and calibration lab is constructed,

to revise procedures

extensively,

and to perform history searches

on installed plant

equipment which has

been

used to measure

plant performance

parameters.

In this regard,

the licensee first generated

a list of

all plant equipment

used to measure plant performance

parameters

in

safety related (technical specification)

uses.

This list identified

445 applicable

items.

Of these,

the licensee

began to evaluate

which items

had been

found out of calibration at the time of

recalibration.

The licensee

sampled

119 items

and found 79 were

found out of calibration, that is, not within the accuracy stated

for the instrument.

The licensee

then evaluated

a sample of 39 of

the 79 for effect on the plant parameter

measured

and found that

accounting for instrument inaccuracy the plant parameter

was

satisfactory for the safety analysis

required value.

The licensee

has put further analysis

on a hold based

on these results

and is

evaluating the sufficiency of the sample size.

Further,

the

licensee's

rationale for not doing further historical review is that

the'nstruments

being questioned

are in current calibration and the

tests

were reperformed during the Unit 1 and Unit 2 refueling

outages

and therefore further research

would not identify a plant

parameter currently out of specification,

only those that were, if

any.

However, the inspector observed that the licensee's

sample results

showed

79 of 119 items of installed plant measuring

equipment

was

out of calibration at the time of recalibration.

The

FSAR section

17.2 and

IEEE 498 both indicate the recalibration intervals

should

be adjusted

to provide assurance

that measurements

are taken with

instruments with adequate

accuracy.

Responsible

licensee

personnel

stated that consideration

of calibration interval adjustments

have

not been

made

and that the data

base for such considerations

is

being developed

through the recalibration program.

The inspector

was informed that responsibilitjes

and methodologies for evaluating

calibration frequencies for installed plant measuring

equipment

would be included in the procedure

revisions being written to

implement 'measuring

and test equipment requirements

on installed

plant measuring

equipment.

Staff Position

The staff position is that the allegation is partially substantiated

but was overstated

in its severity.

The licensee's

guality

Assurance

department

did perform an audit of SEE

and

had identified

findings requiring corrective action.

The findings demonstrate

that

the plants measuring

and test equipment

programs

lack controls in

some areas

(e.g.

lack of evaluative history searches

for installed

plant equipment

found out of calibration)

and poor execution of

existing administrative

requirements

in some areas

(e.g.

lack of

cleanliness

in the calibration facility, lack of procedures

for some

calibrations,

lack of timely evaluative history searches

for

portable ATE found out of calibration).

0

~,

36

The staff-found the licensee's

sampling of the effect of

out-of-tolerance

measuring

and test equipment

found druing

recalibration

on important plant performance

parameters

measured

with that equipment

has not identified instances

of

plant operation

with performance

parameters

outside of safety analysis limits.

The staff found that since the plant parameters

have

been recently

satisfactorily remeasured

during the Unit 1 and Unit 2 refueling

outages

with instruments still within their calibration period.

The staff found problems with the

M&TE program were identified by an

experienced

senior technician to his supervision

and managemnt

and

that no significant actions

were taken until the

gA audit was

performed.

The staff found that the senior technician

who identified M&TE

problems did not consider himself "gotten by management."

Action Re uired

No further action is considered

required for the resolution of the

allegation.

Follow-up of M&TE problems identified by the

gA audit

will be performed in the normal course of future inspections.

Follow-up of the apparent

lack of timely and aggressive

problem

identification and resolution

by plant staff, both before

and after

the gA, audit is a item concern which parallels

the concern raised

in inspection report 50-275/87-08 regarding the timely

identification and resolution of procurement

issues.

Follow-up of

this concern will be performed in a future insepection

and is

considered

an unresolved

item (Item 50-275/87-38-05).

Unit 1

S ent Fuel

Pool Rerackin

As a result of the September ll, 1987, Initial Decision of the NRC's

Atomic Safety

and Licensing Board,

on October 20,

1987, the

NRC issued

Ammendment

numbers

22 and 21 to the Facility Operating

License for Unit 1

and Unit 2, respectively.

These

amendments

authorized

PG&E to rerack the

spent fuel pools,

arid reinstated

the effectiveness

of Amendment

No.

8

(Unit 1 ) and Amendment

No.

6 (Unit 2) which were issued

on May 30,

1986.

The effectiveness

of these

amendments

was stayed

by the U.S.

Court of

Appeals for the Ninth Circuit until the completion of a prior NRC

hearing,

which has

now been completed

and

an Initial Decision issued.

The amendments

allowed the expansion of the spent fuel storage

capacity

of each spent fuel pool

(SFP)

from 270 spaces

to 1324 spaces.

The

amendment

also provided for storage

in the present

racks or the

new racks

(or both) until the installation of the

new racks

was complete.

Accordingly, during October 1987, the licensee

began preliminary

preparations

for wet reracking of the Unit 1 SFP.

Work Order C0023076

and design

change

package

(QCP) 35810 were issued to accomplish this

task.

Previously,

the existing low density racks were welded to

embedment plates

in the

SFP steel liner.

DCP 35810 specified accessible

attachment

welds

on the low density racks were to be cut by divers

0

pi

k

37

utilizing a hand held hydraulic cut off tool.

Remote operated

cut off

tools will be used to cut welds unaccessible

to the divers.

Remaining

weld material

on the pool floor would then

be ground where installation

of bearing plates for the feet of the

new high denisty racks are

required.

As of the ending date of the report period, preparations

for

grinding of the attachment

weld on the feet of existing low denisty rack

number

5 were in process.

Previous

NRC inspection of high density rack procurement

documents,

receipt inspection procedures,

storage

procedures,

welding

qualifications,

vendor supplied records,

and direct observation of

ongoing installation activities was documented

in NRC Inspection

Reports

50-275/86-04,

86-13, 86-18,

and 86-23.

No violations or deviaitons

were identified.

17.

Unresolved

Item

Unresolved

items are matters

about which more information is required to

determine whether they are acceptable

or may involve

violations or

deviations.

Three unresolved

items were identified during this

inspection

and are discussed

in paragraphs

2.c., 4.c., 9.d.

and 15.b..

18.

Exit

In addition to weekly exits,

on December

7, 1987,

an exit meeting

was

conducted with the licensee's

representatives

identified in paragraph l.

The inspectors

summarized

the scope

and findings of the inspection

as

described

in this report.