ML16341E256

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Insp Repts 50-275/87-13 & 50-323/87-12 on 870315-0425. Violations Noted:Failure to Take Corrective Action for Identified Deficiency & Violation of Procedure for Control Room Activities
ML16341E256
Person / Time
Site: Diablo Canyon  Pacific Gas & Electric icon.png
Issue date: 05/12/1987
From: Johnston K, Mendonca M, Narbut P, Padovan L
NRC OFFICE OF INSPECTION & ENFORCEMENT (IE REGION V)
To:
Shared Package
ML16341E254 List:
References
50-275-87-13, 50-323-87-12, IEIN-86-096, IEIN-86-96, IEIN-87-001, IEIN-87-1, NUDOCS 8706080092
Download: ML16341E256 (32)


See also: IR 05000275/1987013

Text

U. S.

NUCLEAR REGULATORY COMMISSION

REGION

V

Report Nos:

50-275/87-13

and 50-323/87-12

Docket Nos:

50-275

and 50-323

License

Nos:

DPR-80

and

DPR-82

Licensee:

Pacific Gas

and Electric Company

77 Beale Street,

Room 1451

San Francisco,

California 94106

Facility Name:

Diablo Canyon Units

1 and

2

Inspection at:

Diablo Canyon Site,

San Luis Obispo County, California

Inspection

Conducted:

March

15 through April 25,

1987

p

Approved by:

L. M.

Pa ovan,

Res~dent

Inspector

K. E. Jo nston,

Resident

In

ector

P.

P.

Nar ut, Senior Resident

In pector

M. M. Mendonca,

C ief, Reactor

Prospects

Section

1

Date Signed

~+re/8'7

g

d

4

ev

<iS

C~

vp'ate

Signed

W/<a r'8 7

Summary:

Ins ection from March

15 throu

h

A ril 25,

1987

Re ort Nos.

50-275 87-13

and

50-323

8 -1

Areas Ins ected:

The inspection

included routine inspections of plant

operations,

fo

ow-up of on-site events,

maintenance

and surveillance

activities,

and licensee

event reports

(LERs), as well as selected

independent

inspection activities.

Inspection

Procedures

30703,

57050,

61726,

62703,

71707,

71710,

73051,

90712,

92700,

92701,

and 93702 were applied during this

inspection.

Results of Ins ection:

Three violations were identified.

The first is for

fai ure to ta

e prompt corrective action for an identified deficiency.

The

second

is for a violation of facility Technical Specification 3.3.1.

This is

a violation of procedure for control

room activities.

8706080092

870512

PDR

ADOCK 05000275

8

PDR"

DETAILS

1.

Persons

Contacted

J.

D. Shiffer, Vice President

Nuclear Power Generation

"R.

C. Thornberry, Plant Manager

J.

A. Sexton, Assistant Plant Manager,

Plant Superintendent

"J.

M. Gisclon, Assistant Plant Manager for Technical

Services

J.

D. Townsend,

Assistant Plant Manager for Support Services

  • R.

G. Todaro, Security Supervisor

  • D. B.

Miklush, Maintenance

Manager

J.

E. Molden, Operations Training Supervisor

W.

G. Crockett,

Instrumentation

and Control Maintenance

Manager

M. J.

Angus,

Work Planning Manager

L.

F.

Womack, Operations

Manager

  • T. L. Grebel,

Regulatory Compliance Supervisor

S.

R. Fridley, Senior Operations

Supervisor

R.

S. Weinberg,

News Service Representative

"M.

W. Stephens,

I&C Administration General

Foreman

D.

A. Malone, Senior

I&C Supervisor

B.

L. Peterson,

Instrument Maintenance

General

Foreman

D.

L. Bauer,

Senior

Power Production Engineer, Electrical Maintenance

M.

M. Mendonca,

Chief, Reactor Projects

Section 1, from US

NRC Region

V

was also in attendance

at the resident's exit meeting.

The inspectors

interviewed several

other licensee

employees

including

shift foreman

(SFM), reactor

and auxiliary operators,

maintenance

personnel,

plant technicians

and engineers,

quality assurance

personnel

and general

construction/startup

personnel.

"Denotes

those attending the exit interview.

2.

0 erational

Safet

Verification

General

During the inspection period, the inspectors

observed

and examined

activities to verify the operational

safety of the licensee's

facility.

The observations

and examinations of those activities

were conducted

on

a daily, weekly or monthly basis.

On a daily basis,

the inspectors

observed control

room activities to

verify compliance with selected

LCOs as prescribed

in the facility

Technical Specifications.

Logs, instrumentation,

recorder traces,

and other operational

records

were examined to obtain information on

plant conditions,

and trends

were reviewed. for compliance with

regulatory requirements.

Shift turnovers

were observed

on a sample

basis to verify that all pertinent information of plant status

was

relayed.

During each week, the inspectors

toured the accessible

areas

of the facility to observe

the following:

(a)

General

plant and equipment conditions.

(b)

Fire hazards

and fire fighting equipment.

(c)

Radiation protection controls.

(d)

Conduct of selected activities for compliance with the

licensee's

administrative controls

and approved procedures.

(e)

Interiors of electrical

and control panels.

(f)

Implementation of selected

portions of the licensee's

physical

security plan.

(g)

Plant housekeeping

and cleanliness.

(h)

Essential

safety feature

equipment alignment

and conditions.

(i)

Storage of pressurized

gas bottles.

The inspectors

talked with operators

in the control

room,

and other

plant personnel.

The discussions

centered

on pertinent topics of

general

plant conditions,

procedures,

security, training,

and other

aspects

of the involved work activities.

While touring a Unit 2 containment penetration

area,

the inspector

observed

an acetylene

pressurized

gas (welding) bottle attached

to

an approximately

2 inch component cooling water

supply line for

support.

The welding, authorized

by Construction Entry Permit

15107,

was for replacement

of Post-LOCA Panel

80.

The inspector

discussed

the supporting of the gas bottle with the attendant

Bechtel welder.

The welder indicated

he

had not received

instruction about attaching pressurized

gas bottles to safety

related piping.

This situation

was brought to the attention of the

General

Construction Project Superintendent,

and

he was reminded

that similar problems

were encountered

during the Unit 1 refueling,

and that corrective actions

should

have

been previously instituted.

The Superintendent

indicated the topic would be discussed

with

Bechtel

supervision.

The inspector also noticed general

area lighting in the Unit 2

auxiliary building

had deteriorated.

For example,

some lighting

fixtures were not functioning around centrifugal charging

pumps 2-1

and 2-2, entry area to the residual

heat

removal

(R8R) heat

exchanger

2-2 and boron injection tank (BIT) room,

component cooling

water

pump

(CCW) 2-3, turbine driven auxiliary feedwater

pump, fuel,

handling building 100 foot elevation corridor by the

RWST,

and the

interspace

room (containing FI-85 and 88 for CCW to the

RHR heat

exchanger)

from the auxiliary building to the 100 foot containment

penetration

area.

These

items were brought to management's

attention for correction.

Units

1 and

2 Fuel Handlin

Bui ldin

Ventilation

S stem Walkdown

En ineered

Sa et

Features

S stem

Wa

downs

The inspector

performed

a walkdown of physically accessible

portions

of the

Fuel Handling Building Ventilation Systems of Units I and 2.

No equipment conditions or items that might degrade

system

performance

were identified.

Labelin

of Unit 2 Control

Room Annunciator Window

On Saturday, April 18,

1987,

unused control

room annunciator

window

PK 12-3 began flashing.

Operations

personnel

apparently attached

a

slip of paper to the window of the irrelevant annunciator.

However,'n

an act of levity, inappropriate

and unprofessional

wording was

written on the paper.

This wording was later transferred

to the

window through the use of a marking pen.

Specifically, the words

were

"EAT AT JOE'S."

Another shift subsequently

replaced

the

wording with a different, but similarly inapproriate

and

unprofessional

phrase utilizing a more formal lettering method.

The

words

on this occasion

were

"PATRONIZE BOB'S BEANERY."

At about

ll:30 a.m.

on April 19,

a

member of an Augmented Inspection

Team

(AIT) observed

the inappropriate

wording on the annunciator.

On

April 20,

1987 at approximately 8:00 a.m.,

a resident

inspector

and

the AIT member brought the fact of the annunciator

wording to the

attention of the plant superintendent

and other plant management.

However, just prior to the NRC's notification of plant management,

at 7:30 a.m.

on April 20th, the window lettering was identified by

the Operations

Manager

who immediatly directed that the lettering

be

removed.

Removal of the lettering was observed

by other plant

managers,

as well as representatives

of the

NRC.

The fact that several different shifts of plant operators

and their

supervisors

were aware of and condoned

the use of inappropriate

and

unprofessional

wording in the control

room, raises

a concern

regarding

the proper

exercise of professional

control

room

responsibi lities, and the proper job performance attitude,

by

operations

personnel.

The Operations

Manager

and Plant

Superintendent

met with the involved shift formen

(SFM) to discuss

their role in setting the leadership

tone for the entire facility.

The managers

emphasized

that actions of this nature

"never have

and

never will be acceptable

behavior."

Separately,

the Operations

Manager met with all

SFM and shift technical

advisors

(STAs) to

discuss

why the actions

taken

by the involved crews were not

acceptable.

No disagreements

were presented

by the

SFM and

STAs.

The managers

ascertained

that the actions

taken

by the operators

were an attempt to heighten

the fact that the flashing annunciator

was

a "nuisance

alarm" in need of repair.

Operators

did conclude

no

effect on plant safety or operations

would result prior to labeling

the window.

However, the

NRC is concerned

that this instance

represents

a failure of first line supervision,

or higher, to set

a

proper

and professional

tone in the conduct of control

room

operations

and that the enforcement

actions

contained

in this and

other reports

may have resulted

from such inattention to control

room responsibilities.

One

During'he next month, the Plant Nanager

and Plant Superintendent

plan to discuss

overall

management

expectations

with all operations

crews.

The use of inappropriate

wording on an annunciator is

a

potentially distracting activity in the control

room, contrary to

NPAP A-103, and is considered

a violation (Open Item

50-323/87-12-02).

violation and

no deviations

were identified.

3.

Onsite Event Follow-u

a ~

Unit 2 Safet

In ection

and Reactor Tri

The Unit 2 reactor

had

a safety injection, reactor trip and unit

trip on Narch 21,

1987 at 7:42 a.m..

The unit was at 97K power and

ramping to lOOX following a routine power reduction for turbine

governor valve testing.

Because of the safety injection, the

licensee

declared

as unusual

event.

Proper notifications were

made

in a timely manner.

The cause

was determined to be the unplanned

closure of main steam isolation valve (NSIV) 2-FCY-41.

The closure

of this valve caused

the steam flow in the other

3 steam

leads to

increase.

The high steam flow resulted in low steam generator

pressures.

The coincidence of high steam flow and low steam

generator

pressure

caused

the safety injection signal.

The safety injection/trip recovery

was normal.

No offsite releases

occurred

as

a result of the event.

All equipment

operated

normally.

The cause

of the NSIV closure

was subsequently

determined to be

a

short in the NSIV position indication switch

(POS 821).

The

electrical control circuity is such that

a short across

the position

switch causes

an air solenoid valve

(SV 298) to open,

bleeding air

from the air operator of NSIV FCY-41, allowing the valve to begin to

drift shut.

Because

FCY-41 is

a reverse

mounted

power operated

check valve,

as

soon

as the disk dropped

a few degrees

into the flow

stream,

the force of the steam flow caused it to slam shut,

as

designed.

The cause of the short in

POS 821 was later determined to be water

intrusion into the switch," presumably

from heavy rains that morning.

The switch is designed

to be weathertight but examination

showed the

sealing

gasket material

had leaked over an extensive

period of time.

The licensee's

investigative actions

included:

o

The determination of the cause of the closure of FCV-41

discussed

above.

o

An engineering

walkdown examination of piping affected

by the

sudden

closure of FCY-41.

The results

were satisfactory.

The

walkdown identified three suspect

piping snubbers

which

subsequently

tested satisfactorily.

o

An x-ray examination of valve FCV-41, for any damage to the

seat or disk.

The results

were satisfactory.

The last two

examinations

were not required

by federal regulations

but were

good prudent technical

actions

taken

by the licensee.

o

The corresponding position switches of the other Unit 2

environmentally

exposed

MSIVs were checked electrically with

high voltage

(meggered)

to verify no water intrusion and

satisfactory operation.

Other corrective actions

taken prior to restart,

in addition to the

above,

included replacement of the defective switch and its mounting

and cabling harness

(proper engineering

approvals

were obtained).

Functional testing of the environmentally

exposed

MSIVs in Unit 2

was performed.

The Unit returned to power on March 26,

1987.

The

resident

inspector attended

the plant Technical

Review Group

(TRG)

meeting held on the event.

The group categorized

the event

as

isolated,

but recognized

the possibility that the other Unit 2

switches in dry environments

and the Unit 1 switches might be

subject to similar failure.

The

TRG therefore

decided to recommend

replacement

of all such switches in the next refueling outages

of

Units 1 and 2.

They also scheduled

meggering of the exposed

Unit 1

switches at the next unscheduled

outage.

The licensee

had examined industry failure data

bases for equipment

and found no evidence of repeated failure for these

switches.

The

licensee

therefore

determined that Part 21 reportability is not

required for this switch.

The licensee

performed

a review of past problem reports

on these

switches

and determined that in September

1986

a similar electrical

problem was noted

on FCV-41 (ground indication - valve would not

stay open) but the condition cleared

and would not repeat.

The

TRG

concluded that the condition at that time was possibly caused

by the

switch.

Unit 1 was also found to have

a problem with burned out

contacts

on

a similar switch which may have

been

caused

by a similar

condition.

The Unit 1 situation

was corrected

by a design

change

allowing the

use of spare

contacts

in the switch.

These indicators

might have led to the discovery of deteriorated

gaskets

in the

switch, but disassembly

of the switch was not performed

because

the

switch is not manufactured

in a way such that it can

be disassembled

for inspection (it is of riveted construction).

The inspector inquired as to whether the licensee

would conduct

a

study of other equipment which is environmentally qualified (Eg),

has sealing gaskets,

and

has

a similar situation where the gaskets

are not required to be replaced periodically.

The inspector

discussed

the fact that most

Eg equipment with gaskets

have the

gaskets

replaced periodically (generally

2 years).

The licensee

is

considering this action

(Open Item 50-323/87-12-01).

Unit 1 Reactor Tri

Due to 500

KV S stem Disturbance

On March 15,

1987 with Unit 1 in Mode 1,

a reactor trip occurred

when

an airplane crashed

into the Diablo Canyon-Gates

500

kV

transmission

line approximately

50 miles from the plant site.

When

the airplane collided with the 500

kV transmission line,

a three

phase to ground electrical fault occurred,

which caused

a large

500

kV system current

and Voltage transient.

The transient

created

a

low voltage condition on the plant auxiliary power system

and caused

a reactor trip due to reactor coolant

pump bus undervoltge relay

actuation.

The appropriate

emergency

procedures

were followed,

the

unit was stabilized in Mode 3,

and

a significant event

was declared.

All safety

systems

functioned properly.

At the time of the event,

the Unit 1 main generator

voltage

regulator

was in manual control, pending regulator adjustments

to

eliminate undesirable

system fluctuations observed

ear lier while in

automatic control.

The Unit 2 main generator

voltage regulator

was

in automatic control at the time of the event,

and was able to

adequately

compensate

for the voltage transient permitting continued

power operation of Unit 2.

The licensee

determined

the root cause of the reactor trip was the

inability of the unit to withstand the major 500

kV voltage

transient with the main generator

voltage regulator in manual

control.

With the regulator in manual control,

a low voltage

condition on the reactor coolant

pump bus could not be averted.

Subsequently,

adjustments

to the voltage regulator were completed

and the Unit 1 voltage regulator

was returned to automatic control.

RHR Crosstie

Valve Isolation

On March 17,

1987 at 0625

PST with Unit 2 at 100 percent

power,

RHR

crosstie

valve 8716B was closed

and

removed

from service for

installation of valve position indication.

Operations

personnel

later recognized this action placed the plant into a configuration

described

in IE Information Notice (IN) 87-01

"RHR Valve

Misalignment Causes

Degradation of ECCS in PWRs."

Closing valve

8716B was not consistent with the plant's

RHR system safety analysis

assumption that

RHR injection into all four Reactor Coolant System

(RCS) cold legs would be available,

assuming

a single active failure

of one of the

RHR pumps.

With the crosstie

valve closed,

and if

only one

RHR pump was operable,

injection flow would be provided to

only two of the

RCS cold legs.

However, during the time that valve

8716B was closed,

both

RHR pumps were operable

and together

were

capable of injecting into all four

RCS cold legs.

Upon

identification of the concern,

RHR crosstie

valve 8716B was opened

and

RHR system configuration was returned to normal.

As corrective action, additional

guidance

was provided to Operations

personnel

regarding the repositioning or removal

from service of

Emergency

Core Cooling System

(ECCS) valves that are

system related

rather than train related.

Plant Engineering

has

reviewed all

applicable test procedures

relative to this guidance.

Also,

Westinghouse

was contacted to perform

a site specific analysis

regarding the acceptability of injection into only two

RCS cold

legs.

The inspector

forwarded information to Region

V

about

a

potential generic safety question

concerning

the

need for Technical

Specifications for the

RHR crosstie

valves.

Information possessed

by the licensee,

describing the impact of

closing

a crosstie

valve on

RHR system operability,

was not made

available to plant operators

and personnel

involved in equipment

clearance activities in a timely manner.

On October 30,

1986 the

Onsite Safety

Review Group

(OSRG) issued Action Request

A0042404,

which identified the consequences

of isolating an

RHR crosstie

valve,

and specifically indicated operations

personnel

should

be

made

aware of those

consequences.

Shortly thereafter,

OSRG

representatives

discussed

this situation with licensee

management.

Actions taken

by PG8E included 1) submitting proposed

inservice

testing program changes

to

NRC to change

the frequency of crosstie

valve stroke testing from quarterly to only during cold shutdown,

and 2) obtaining Westinghouse

evaluation of IN 87-01.

However, the

licensee failed to take timely corrective action for operations

personnel

and clearance

coordinators

to prevent the situation from

developing

on Unit 2.

In a related matter,

the Training Department

had obtained

information from the Institute of Nuclear

Power Operations

(INPO)

"Network" and

NRC Daily Plant Reports

about the

D.

C.

Cook plant

safety injection system

(SIS) crosstie

valve isolation which

occurred

on September

12,

1986.

An instructor lesson

guide

was

prepared

by the Training Department,

and by February

1987

requalification training was provided to all five operating

crews

regarding isolating the SIS crosstie

valves.

However, the

applicability of the SI crosstie

valve information to the

RHR system

was not stressed

enough to prevent the condition from occurring at

Diablo Canyon.

As corrective action, the licensee's

Training

Department

agreed to devise

ways to identify critical training

information and

make it stand out during training classes.

The failure to take timely corrective action,

described

in this

section of this report, is an apparent violation of the requirements

of 10 CFR 50, Appendix

B (Item 50-275/87-13-01).

Unit 2 Loss of RHR

Pum

Durin

Col d Shutdown

On April 10,

1987 while Unit 2 was in cold shutdown with the hot

legs at mid-loop in preparation for the installation of the steam

generator

nozzle

dams,

both

RHR pumps were shut off for 86 minutes.

The

RHR pumps were shut off at 2125 hours0.0246 days <br />0.59 hours <br />0.00351 weeks <br />8.085625e-4 months <br />

due to cavitation.

The

cavitation occurred

due to a loss of hot leg water inventory which

initiated vortexing in the

RHR suction line.

The loss of inventory

resulted

from an increase

in

RHR letdown to makeup

volume control

tank (VCT) level which was being inadvertently drained.

An

engineer,

in preparation for a containment penetration

leak rate

test,

was draining the reactor coolant

pump seal

return line.

Two

leaking boundary valves

on this line provided the drain path from

the

VCT to the Reactor Coolant Drain Tank (RCDT).

The operators

terminated

the event when they opened

a gravity feed

path from the refueling water storage

tank

(RWST) to the

RCS after

receiving word that the steam generator

manways,

which had been

scheduled for removal,

were still in place.

The operators

were then

able to restart

an

RHR pump to re-establish

flow through the core.

The

RHR pump discharge

temperature

registered

220 degrees

F,

indicating that boiling had occurred.

In the process

of flooding

the

RCS,,

one steam generator

manway (which had been untorqued,

but

not removed)

leaked approximately

30 gallons.

In addition,

steam

was emitted when

a tygon hose running from the reactor vessel

head

vent to the top of the pressurizer

ruptured

due to high temperatures

and slight pressurization.

An NRC Augmented Inspection

Team (AIT) was dispatched

to the site

and began investigation April 14,

1987.

An analysis of this event

and an evaluation of the licensee's

preparedness

and response will

be contained in the AIT's Inspection

Report (50-323/87-18).

Unit 1

RCP Bus

E Underfre uenc

Rela

Between

1123 hours0.013 days <br />0.312 hours <br />0.00186 weeks <br />4.273015e-4 months <br />

on April 19,

and

0206 hours0.00238 days <br />0.0572 hours <br />3.406085e-4 weeks <br />7.8383e-5 months <br />

on April 20,

1987,

one Unit 1 reactor coolant

pump

(RCP) underfrequency

(U/F) trip

channel,

which had been discovered

inoperable at 0930 hours0.0108 days <br />0.258 hours <br />0.00154 weeks <br />3.53865e-4 months <br />

on April

19,

was inadvertently left in a bypassed

condition.

The facility

Technical Specifications

require that

an inoperable

channel

be

placed in a tripped condition within 6'ours.

On April 19, at approximately

0930 hours0.0108 days <br />0.258 hours <br />0.00154 weeks <br />3.53865e-4 months <br />,

I&C shift control

technicians

(SCTs) performing

STP I-9A, "Trip Actuating Device

Operational

Test,

12

KV Undervoltage,

Underfrequency,"

discovered

that U/F relay 81VER3 would not trip when frequency

was lowered

below its minimum setpoint of 53.9

Hz.

U/F relay 81VER3 is one of

three relays which provides

an input to the reactor protection

system

(RPS)

two out of three underfrequency

reactor trip.

As

required

by Surveillance

Test Procedure

(STP) I-9A, an

SCT attempted

to notify the Shift Foreman

(SFM) that

81VER3 was inoperable.

However, miscommunications

between the

SCT and

SFN resulted in the

Unit 1 SFN interpreting that the

SCT was having problems with the

relay and was going to notify his foreman to have the problem

resolved.

At that time the

RPS bistable related to relay 81VER3 was

tripped since the relay test transfer switch was in the "Test"

position and the Technical Specification

Equipment Operability

Status

Sheet

(AP C-6S4), in possession

of the

SFM, correctly listed

the relay as tripped.

Following the discussions

with operations,

the mids shift

Instrumentation

and Control (I8C) technicians

conducted

a turnover

with the day shift.

The off going shift informed the on coming

shift that the

SFN had been notified of the failure of U/F relay

81VER3 and requested

the oncoming shift verify the inoperability of

relay 81VER3.

At approximately

1030 hours0.0119 days <br />0.286 hours <br />0.0017 weeks <br />3.91915e-4 months <br /> the day shift SCTs went

to the control

room to have

a turnover briefing with the

SFM.

However, the operability of 81VER3 was not discussed.

The

SCTs then

proceeded

to 12

KV Bus

E and verified all the test equipment

was

setup

as the mids shift had left it.

They then tested relay 81VER3

and confirmed that it was inoperable.

0

One of the

SCTs proceeded

to the control

room and requested

permission to continue with undervoltage

relay testing,

the next

step in STP I-9A.

To continue with the undervoltage

relay portion

of STP I-9A, the procedure

requires that the

RCP underfrequency

relay test switch is returned to the

"NORMAL" position.

Since the

test switch had been turned to "NORMAL" when the

SCT approached

the

control operator

(CO), the

CO, observing that the underfrequency

status light was not lit, and assuming that since it was not lit and

the

SCT was requesting

permission to proceed,

the problems

on relay

81VER3 had been taken care of and the relay was available for

service.

Based

on this, the

CO dated

and timed the Equipment

Declared Operable 'portion of the Technical Specification

Equipment

Operability sheet for 81VER3.

This was

done at 1123 hours0.013 days <br />0.312 hours <br />0.00186 weeks <br />4.273015e-4 months <br />.

At this

time,

U/F relay 81VER3 was not tripped and represented

a channel

bypass

to the logic of the

RPS, i.e.

a channel

which,would not trip

on

a genuine

U/F condition.

Therefore,

a

2 out of 2 logic was

required for an U/F trip on Bus

E.

Once granted permission,

the

SCTs continued with the undervoltage

relay testing.

However,

upon completion of the relay testing,

the

SCTs did not perform the "return to service" portion of the

STP.

This was

done since relay

81VER3 was inoperable

and required repair

by electrical

maintenance.

Although it provided

a tracking system

for the inoperable relay, it was not timely enough to have the

bistable tripped, within the requirements

of the technical

specifications.

At approximately

0200 hours0.00231 days <br />0.0556 hours <br />3.306878e-4 weeks <br />7.61e-5 months <br />

on April 20, 1987, the mids shift SCTs

who had originally discovered

the inoperability of relay 81VER3

entered

the control

room and noticed that the status light for relay

81VER3 was not lit.

Upon further review they discovered that the

returned to service portion of STP I-9A had not been performed

and

there

was

no indication in I8C's logs that relay 81VER3 had been

repaired.

When asked,

the

SFM informed the

SCTs that

as far as

he

knew, relay 81VER3 was operable

and in service

and requested

the

SCTs test the relay to determine its operability.

At 0206 hours0.00238 days <br />0.0572 hours <br />3.406085e-4 weeks <br />7.8383e-5 months <br />,

the

RCP U/F relay test switch was placed in "TEST", essentially

tripping the channel.

At 0220 hours0.00255 days <br />0.0611 hours <br />3.637566e-4 weeks <br />8.371e-5 months <br />,

the

SCTs determined that relay

81VER3 was still inoperable.

Therefore,

relay 81VER3 was in a

non-tripped condition between

1123 hours0.013 days <br />0.312 hours <br />0.00186 weeks <br />4.273015e-4 months <br />

and 0206 hours0.00238 days <br />0.0572 hours <br />3.406085e-4 weeks <br />7.8383e-5 months <br />,

a total of

15 hours1.736111e-4 days <br />0.00417 hours <br />2.480159e-5 weeks <br />5.7075e-6 months <br />

and 43 minutes,

following a surveillance

where it had been

determined

inoperable.

Technical Specification 3.3. 1, Table 3.3-1,

Item 16, specifies that

the minimum number of operable

channels for the reactor trip on

RCP

underfrequency

is two per bus, with the provisions of Action

Statement

6 applicable.

Action Statement

6 specifies that with the

number of operable

channels

one less

than the total

number of

channels,

power operation

may proceed provided the inoperable

channel

is placed in the tripped condition within 6 hours6.944444e-5 days <br />0.00167 hours <br />9.920635e-6 weeks <br />2.283e-6 months <br />

and the

minimum channels

operable

requirement is met.

Since relay 81VER3

was discovered

inoperable at 0930 hours0.0108 days <br />0.258 hours <br />0.00154 weeks <br />3.53865e-4 months <br />, it was required to be

tripped at 1530 hours0.0177 days <br />0.425 hours <br />0.00253 weeks <br />5.82165e-4 months <br />.

Therefore,

the licensee

operated

in a

10

condition not provided for in their Technical Specifications for 10

hours

and

36 minutes.

STP I-9A requires that for a channel

out of tolerance

due to an

apparent

module fai lure, the

I8C supervisor

and

SFM are to be

notified immediately that the channel

is inoperable.

In addition,

STP I-9A restates

the requirements

of Technical Specification 3.3. 1,

specifically that an inoperable

channel

is placed in a tripped

condition within 6 hours6.944444e-5 days <br />0.00167 hours <br />9.920635e-6 weeks <br />2.283e-6 months <br />.

Had either conditions of this procedure

been successfully

executed,

the licensee

would not have violated

their Technical

Specifications'he

provision in STP I-9A that requires

the notification of the

SFM

was attempted

by the

SCTs.

However, apparent

miscommunications

and

the resulting assumptions

led operations

and

I8C to reach

separate

conclusions with regards

to the operability of relay 81VER3.

This

example of miscommunication

appears

to be related to other examples

of informal or secondhand

communications

adversely affecting quality

of work or operations

(Inspection

Report Nos.

50-275/87-04

and

50-323/87-04,

50-275/86-29

and 50-323/86-27,

and 50-275/87-10

and

50-323/87-09).

In this example,

the verbal

communication path,

as

opposed to a formal signed transfer,

existed

when the

CO and

SFM

were permitted to declare

the equipment operable

through verbal

communications with the

SCTs.

The licensee

should consider this

apparent

avenue

where

a miscommunication

can result in the return to

service of inoperable

equipment.

The "Precautions"

section of STP I-9A reiterates

the requirements

of

Technical Specification 3.3. 1, specifically that an inoperable

U/F

channel

is to be placed in a tripped condition within 6 hours6.944444e-5 days <br />0.00167 hours <br />9.920635e-6 weeks <br />2.283e-6 months <br />.

A

tripped channel

is indicated

by a status light in the control

room.

Steps

2. h. i and 2. h. 2 of STP I-9A require the

SCTs to initial that

the

RCP U/F test switch was placed in "NORMAL" and the

RCP

Bus

E U/F

status light is out.

Although the body of the procedure

does not

provide steps

to be taken for an inoperable

channel, it should

have

been apparent

to the

SCTs

upon completion of these

steps that they

were leaving relay 81VER3 in a bypassed

condition and were setting

up for a Technical Specification violation as described

in the

precautions

section of STP I-9A.

The licensee

should address

the

familiarity of personnel

with the precautions

section

and other

sections of surveillance test procedures

which precede

the procedure

section,

The inspector

noted that the licensee

promptly initiated an

investigation into this event.

This investigation included

statements

from both shifts of SCTs involved on April 20 and both

operations shifts involved on April 22,

1987.

A Technical

Review

Group was convened

on April 23.

Proposed corrective actions include

(1) an incident report which will detail the miscommunication to be

read by all operations shifts

and discussed

with all I8C shifts and

(2) a revision to STP I-9A which will separate it into ten

procedures,

one for each relay,

and provide guidance

in the body of

the procedure

regarding actions to be taken

when

an inoperable

channel

is discovered.

However,

these actions

do not completely

mitigate the significance of this event in that this is an example

of a reoccurring problem of communications

compounded

by I8C

maintenance

personnel

not fully understanding

the. precautions listed

in their procedure.

Therefore, this is an apparent violation (Open

Item 50-275/87-13-02).

4.

Maintenance

The inspectors

observed portions of, and reviewed records

on, selected

maintenance activities to assure

compliance with approved procedures,

technical specifications,

and appropriate

industry codes

and standards.

Furthermore,

the inspectors verified maintenance activities were

performed

by qualified personnel,

in accordance

with fire protection

and

housekeeping

controls,

and replacement

parts

were appropriately

cer tified.

a.

Diesel Generator

Coolin

Water Shutdown Switch

The inspector

observed portions of calibration of temperature

switch

95 which activates

the jacket water temperature

relay on Unit 2

diesel-generator

2-2.

With the diesel in local control,

and the

mode control switch (on the diesel

generator

local panel) in the

test

mode,

the diesel

engine,

generator field, and generator air

circuit breaker

are tripped through shutdown relay SDR-22 if the

high jacket water temperature

relay picks

up.

Work was performed in

'ccordance

with Work Order R-0018690.

The as found switch setpoint

was

195 degrees

F, which did not fall within the acceptance

band of

205 degrees

F plus or minus

4 degrees

F.

Accordingly, the switch

setpoint

was adjusted to 204.8 degrees

F.

However, completion of

the work was not possible,

as electrical

power to the diesel

generator

local control panel

was not available.

Without electrical

power at the panel,

temperature

switch activation of the shutdown

relay could not be observed.

b.

Unit 2 Emer enc

Diesel Air Com ressor

The inspector

observed portions of preventative

maintenance

performed

on the Unit 2 emergency

diesel

generator

(D/G) 2-2 air

compressor

2-2.

The maintenance

included changing the air

compressor

belts

and filters.

The inspector

observed that the belts

were replaced with an appropriate

replacement

and installed within

acceptable

tightness

tolerances.

The inspector

noted that one step,

with one sign-off, in the work order included the installation of

three different sets of parts.

The maintenance

personnel

involved

at the time of the inspection

had been

issued only two sets of

parts.

The package

had been worked on by previous

crews

and

following crews were to complete the job.

The inspector

noted that

with one sign-off for three parts there

was the potential for

confusion.

The inspector

discussed

this issue with the maintenance

manager

who

found the level of control of parts for the air compressors

adequate

for the quality of work performed

based

on the following:

12

o

The Plant Information Management

System

(PIMS) computer

tracking of parts

issued to the field is referenced

by work

order

number and is therefore

a verification of what parts

are

installed,

and

o

The air compressors

are not class

lE equipment

and the filters

are not quality related.

The inspector also discussed

this concern with work planning

personnel

who noted that the appropriate

method for maintenance

personnel

to document the implementation of two parts out of three

would be to add

a note in the comments section of the package.

The

inspector

reviewed the completed work package

and noted that this

was done.

Based

on the above,

the inspector

found the level of

control of parts for this maintenance activity was adequate.

Unit 2 Emer enc

Diesel

Generator

2-2 Undervolta

e Auxiliar

Rela

s

The inspector

observed portions of Maintenance

Procedure

E-55,

"Routine Preventive

Maintenance of +SG'uxiliary Relays,"

performed

on the

4KV breaker undervoltage auxiliary relays

27XHHB2,

27YHHB2, and

27ZHHB2 associated

with emergency

diesel

generator

2-2.

The maintenance

procedure

requires that the relay is cleaned

thoroughly and then checked for appropriate

pickup and dropout

voltages.

The inspector

observed that the maintenance

was performed

with an appropriate

clearance

and that calibrated

instruments

were

used to record pickup and dropout voltages.

No violations or deviations

were identified.

5.

Survei 1 1 ance

By direct observation

and record review of selected

surveillance testing,

the inspectors

assured

compliance with TS requirements

and plant

procedures.

The inspectors verified that test equipment

was calibrated,

and acceptance

criteria were met or appropriately dispositioned.

a.

Diesel

En ine Generator

1-3 Manual Start

The inspector

observed portions of STP M-9A-3, "Diesel

Engine

Generator

1-3 Routine Surveillance Test."

The test

was performed in

preparation of returning

D/G 1-3 to service following a maintenance

outage.

As required

by procedure,

the diesel

was started

manually

from the Unit 2 control

room.

Prior to the inspector's

observation

of the test,

the operators

attempted to parallel the diesel

generator

to its bus,

but the breaker failed to close.

It was

determined that the contactor coupling had not fully made

up due to

the breaker

not having been

racked in completely.

Since these

are

the types of problems the surveillance is designed to uncover prior

to placing the diesel

generators

back in service,

the corrective

action taken

was to correctly rack in the breaker.

Once the breaker

was closed

and the diesel

was slowly loaded to 2.6

MW the inspector

observed

an auxiliary operator collect field data.

The inspector

0

'3

verified testing

was accomplished

in accordance

with an approved

test procedure

and that test data

was accurate

and complete.

b.

Waste

Gas

S stem

Ox

en Anal zer

The inspector

observed portions of functional testing of the Unit 2

waste

gas

oxygen monitoring system in accordance

with STP I-79A

"Functional Test of Waste

Gas

System

Oxygen Analyzer 75."

Special

Radiation

Work Permit 86-020 was approved

and in effect for the

test.

Alarm and protective function setpoints

were found to be

within acceptance

criteria,

and the data sheet

was completed

as

required

by the procedure.

Required administrative approvals to

perform the test

had been obtained.

c.

Unit 1

SSPS

Slave

Rela

0 eration

The inspector

observed portions of STP H-16J, "Operation of Slave

Relay

K612 Train A 8 B."

Slave Relay K612B, when actuated,

closes

steam generator

blowdown and sample lines for containment isolation

Phase

A.

Relay

K612A has

no function and is not tested.

Technical Specification 4.3.2. 1 Table 4.3-2 requires that Solid State

Protection

System

(SSPS)

slave relays related to containment

isolation are tested

on a nominal quarterly frequency.

The

licensee,

however,

performs slave relay testing for containment

isolation within 72 hours8.333333e-4 days <br />0.02 hours <br />1.190476e-4 weeks <br />2.7396e-5 months <br /> of'he Actuation Logic Testing

(STP

I-16A2) which is required in Table 4.3-2 to be performed

on

a

monthly frequency or at least every

62 days

on

a staggered test

basis.

The inspector

observed

communications

between operations

personnel

performing the test.

Appropriate test data

was taken,

and

systems

were returned to service

as required

by the procedure.

No violations or deviations

were identified.

6.

NRC IE Information Notice 86-96

Closed

IE Information Notice (IE-IN) 86-96,

"Heat Exchanger

Fouling Can Cause

Inadequate

Operability of Service Water Systems,"

discusses

the potential

for fouling in heat exchangers

in raw water systems

and its affects

on

a

facility's ability to reject heat to the ultimate heat sink.

As required

in Administrative Procedure

(AP) C-14Sl, "Dissemination of Operating

Experience,"

the licensee

reviewed IE-IN 86-96 for applicability to the

Diablo Canyon Site.

Their review concluded that only one safety related

heat exchanger

was subject to the potential for fouling, specifically the

CCW heat exchanger.

The Auxiliary Saltwater

(ASW) system,

which takes

its supply from the Pacific Ocean

and is the plant's ultimate heat sink,

removes

heat from the

CCW system through the

CCW Heat exchanger.

The

following design features

and operational

and maintenance activities are

in place to minimize fouling of the

ASW system.

1)

Bar racks

and traveling screens

remove debris at the intake to the

ASW pumps.

2)

Periodic demusseling

and desliming minimizes fouling of the

ASW

system.

0

3)

CCW heat

exchanger

differential pressure

(delta

P) can

be monitored

in the control

room.

Excessive fouling will result in a high alarm

at a delta

P of 167 inches of water.

The heat exchanger

is

considered

operable with up to 170 inches of water delta

P.

If high

delta

P is verified, Annunciator Response

procedures

require that

the heat exchanger is isolated for cleaning.

4)

As part of the monthly surveillance testing program,

CCW heat

exchanger

performance is measured.

The

CCW system,

which is

a closed

loop system that cools all other safety

related water cooled heat exchangers,

gets its makeup

from the makeup

water system.

The makeup water system

has three

main sources

of water;

the seawater

evaporator,

Diablo Creek and associated

waterwells,

and the

seawater

reverse-osmosis

unit.

All sources

are processed

through

a

clarifier, filter beds

and demineralizers.

Based

on the above discussion,

the inspector

concludes

the licensee

has

adequately

addressed

this issue

and it is thereby closed.

No violations or deviations

were identified.

Licensee

Event

Re ort Follow-u

Based

on an in-office review, the following LERs were closed out by the

resident inspector:

Unit 1:

86-21, 87-02,

87-04

Unit 2:

87-01, 87-02

The

LERs were reviewed for event description,

root cause,

corrective

actions taken,

generic applicability and timeliness of reporting.

Unit 2

LER 87-01 "Reactor Trip on Low-Low Steam Generator

Water Level"

failed to identify miscommunication

between

the

SFM and

CO as

a

contributing factor to the trip.

As documented

in Section 3.b of NRC

Inspection

Report (IR) 50-323/87-09,

at the time of the event the

SFM was

involved in a shift turnover briefing.

The

SFM had previously

communicated

to the

CO that

he wanted the plant to be on line by a

certain time, but did not mean to suggest that the turbine

ramp

up should

begin.

However, the

CO interpreted

the communication

such that the

turbine

ramp

up was initiated, while other experienced

operators

were

also participating in the briefing.

Via cover letter to the IR dated

March 31,

1987, the licensee

was requested

to provide written response

to

the

NRC describing corrective actions to prevent reoccurrence

of

miscommunications

of this nature.

In the

LER the licensee

did not

identify miscommunication

between

the

SFM and

CO as

a contributing factor

to the trip.

Accordingly, Pacific Gas

and Electric should take the steps

necessary

to be assured

that this event,

and all future events,

are

adequately

assessed

and reported to the

NRC,

and corrective actions

are

taken for all contributing factors to the events.

The licensee

agreed to

revise the

LER.

0

15

No violations or deviations

were identified.

8.

Defeated Safet

Features

and Intentional Entr

Into T.S. 3.0.3

Recently, at another nuclear

power plant in the United States,

operators

defeated

a plant safety feature

by inserting

a

dummy signal into safety

circuitry and then intentionally entering T.S. 3.0.3 for operational,

convenience.

In response

to this occurrence,

the inspectors

evaluated

the licensee's

controls which prohibit actions of this nature at Diablo

Canyon.

Administrative Procedure

(AP) C-4S1 "Mechanical

Bypass,

Jumper

, and Lifted Circuit Log Accountability System" specifically directs that,

if installation of a "jumper" results in " a change in the function of a

system operation

as described

in the

FSAR" a safety evaluation

must be

performed in accordance

with plant procedures.

For the purposes

of the

procedure,

the term "jumper" refers to an electrical

jumper, lifted

electrical

lead,

mechanical

bypass

or modification,

and any other bypass

which renders

a safety feature

incapable of performing its intended

function (such

as insertion of a

dummy signal).

The safety evaluation

must then

be approved

by the Plant Staff Review Committee prior to

installation of the jumper.

The inspector

concludes

the licensee's

procedure

AP C-4S1 addresses

the identified concern.

Regarding intentional entry into T. S.

3. 0. 3. for operational

convenience,

Operations

Department

personnel

indicated to the inspector that plant

policy prohibits intentional entry into T.S. 3.0.3.

The inspector

ascertained

that the licensee

had

no written policy in this regard,

and

that this policy was not specifically addressed

in operator

training

classes.

Accordingly, the licensee

agreed to perform the following:

o

A shift foreman's

memo stating plant policy on this matter would be

issued

and reviewed

by all operating shift crews.

o

Revisions to APs to preclude intentionally entering T.S. 3.0.3 would

be pursued.

o

Training Lesson

Plan

LM-8 will be revised to inform all licensee

candidates

that T.S. 3.0.3 should not be intentionally entered.

This policy will also

be covered during requalification training of

licensed operators.

No violations or deviations

were identified.

9.

Exit

On April 29,

1987

an exit meeting

was conducted with the licensee's

representatives

identified in paragraph l.

The inspectors

summarized

the

scope

and findings of the inspection

as described

in this report.