ML16314B839
| ML16314B839 | |
| Person / Time | |
|---|---|
| Site: | Wolf Creek |
| Issue date: | 11/08/2016 |
| From: | Nick Taylor NRC/RGN-IV/DRP/RPB-B |
| To: | Heflin A Wolf Creek |
| Nick Taylor | |
| References | |
| IR 2016003 | |
| Download: ML16314B839 (48) | |
See also: IR 05000482/2016003
Text
UNITED STATES
NUCLEAR REGULATORY COMMISSION
REGION IV
1600 E. LAMAR BLVD.
ARLINGTON, TX 76011-4511
November 8, 2016
Adam C. Heflin, President and
Chief Executive Officer
Wolf Creek Nuclear Operating
Corporation
P.O. Box 411
Burlington, KS 66839
SUBJECT:
WOLF CREEK GENERATING STATION - NRC INTEGRATED INSPECTION
REPORT 05000482/2016003
Dear Mr. Heflin:
On September 30, 2016, the U.S. Nuclear Regulatory Commission (NRC) completed an
inspection at your Wolf Creek Generating Station. On October 19, 2016, the NRC inspectors
discussed the results of this inspection with Jaime McCoy, Vice President, Engineering, and
other members of your staff. Inspectors documented the results of this inspection in the
enclosed inspection report.
NRC inspectors documented one finding of very low safety significance (Green) in this report.
This finding involved a violation of NRC requirements. The NRC is treating this violation as a
non-cited violation (NCV) consistent with Section 2.3.2.a of the NRC Enforcement Policy.
If you contest the violation or significance of the NCV, you should provide a response within
30 days of the date of this inspection report, with the basis for your denial, to the U.S. Nuclear
Regulatory Commission, ATTN: Document Control Desk, Washington, DC 20555-0001; with
copies to the Regional Administrator, Region IV; the Director, Office of Enforcement,
U.S. Nuclear Regulatory Commission, Washington, DC 20555-0001; and the NRC resident
inspector at the Wolf Creek Generating Station.
If you disagree with a cross-cutting aspect assignment in this report, you should provide a
response within 30 days of the date of this inspection report, with the basis for your
disagreement, to the Regional Administrator, Region IV; and the NRC resident inspector at the
Wolf Creek Generating Station.
In accordance with Title 10 of the Code of Federal Regulations (10 CFR) 2.390, Public
Inspections, Exemptions, Requests for Withholding, a copy of this letter, its enclosure, and your
response (if any) will be available electronically for public inspection in the NRCs Public
Document Room or from the Publicly Available Records (PARS) component of the NRC's
A. Heflin
- 2 -
Agencywide Documents Access and Management System (ADAMS). ADAMS is accessible
from the NRC Web site at http://www.nrc.gov/reading-rm/adams.html (the Public Electronic
Reading Room).
Sincerely,
/RA/
Nicholas H. Taylor, Branch Chief
Project Branch B
Division of Reactor Projects
Docket No.: 50-482
License No.: NPF-42
Enclosure: Inspection Report 05000482/2016003
w/ Attachment: Supplemental Information
cc w/ encl: Electronic Distribution
SUNSI Review
By: NTaylor
Yes No
Non-Sensitive
Sensitive
Publicly Available
Non-Publicly Available
Keyword:
OFFICE
SRI/DRP/B
RI/DRP/B
C:DRS/PSB2
C:DRS/EB1
C:DRS/EB2
TL/DRS/IPAT
NAME
DDodson
FThomas
HGepford
TFarnholtz
GWerner
THipschman
SIGNATURE
/RA/
/RA/
/RA/
/RA/
/RA/
/RA/
DATE
11/7/2016
11/07/2016
11/1/16
11/2/16
11/2/16
11/3/16
OFFICE
C:DRS/OB
C:DRP/B
NAME
VGaddy
NTaylor
SIGNATURE
/RA/KDC
for
/RA/
DATE
11/01/16
11/8/16
Letter to Adam C. Heflin from Nicholas H. Taylor dated November 8, 2016
SUBJECT: WOLF CREEK GENERATING STATION - NRC INTEGRATED INSPECTION
REPORT 05000482/2016003
DISTRIBUTION:
Regional Administrator (Kriss.Kennedy@nrc.gov)
Deputy Regional Administrator (Scott.Morris@nrc.gov)
DRP Director (Troy.Pruett@nrc.gov)
DRP Deputy Director (Ryan.Lantz@nrc.gov)
DRS Director (Anton.Vegel@nrc.gov)
DRS Deputy Director (Jeff.Clark@nrc.gov)
Senior Resident Inspector (Douglas.Dodson@nrc.gov)
Resident Inspector (Fabian.Thomas@nrc.gov)
Administrative Assistant (Susan.Galemore@nrc.gov)
Branch Chief, DRP/B (Nick.Taylor@nrc.gov)
Senior Project Engineer, DRP/B (David.Proulx@nrc.gov)
Project Engineer, DRP/B (Steven.Janicki@nrc.gov)
Project Engineer, DRP/B (Jim.Melfi@nrc.gov)
Public Affairs Officer (Victor.Dricks@nrc.gov)
Project Manager (Balwant.Singal@nrc.gov)
Team Leader, DRS/IPAT (Thomas.Hipschman@nrc.gov)
Project Engineer, DRS/IPAT (Eduardo.Uribe@nrc.gov)
RITS Coordinator (Marisa.Herrera@nrc.gov)
ACES (R4Enforcement.Resource@nrc.gov)
Regional Counsel (Karla.Fuller@nrc.gov)
Congressional Affairs Officer (Jenny.Weil@nrc.gov)
RIV Congressional Affairs Officer (Angel.Moreno@nrc.gov)
RIV/ETA: OEDO (Jeremy.Bowen@nrc.gov)
RIV RSLO (Bill.Maier@nrc.gov)
ROPreports.Resource@nrc.gov
ROPassessment.Resource@nrc.gov
Enclosure
U.S. NUCLEAR REGULATORY COMMISSION
REGION IV
Docket:
05000482
License:
Report:
Licensee:
Wolf Creek Nuclear Operating Corporation
Facility:
Wolf Creek Generating Station
Location:
1550 Oxen Lane NE
Burlington, KS 66839
Dates:
July 1 through September 30, 2016
Inspectors: D. Dodson, Senior Resident Inspector
F. Thomas, Resident Inspector
M. Bloodgood, Operations Engineer
G. Guerra, CHP, Emergency Preparedness Inspector
C. Steely, Operations Engineer
Approved
By:
Nicholas H. Taylor
Chief, Project Branch B
Division of Reactor Projects
- 2 -
SUMMARY
IR 05000482/2016003; 07/01/2016 - 09/30/2016; Wolf Creek Generating Station; Maintenance
Effectiveness
The inspection activities described in this report were performed between July 1 and September
30, 2016, by the resident inspectors at Wolf Creek Generating Station and inspectors from the
NRCs Region IV office. One finding of very low safety significance (Green) is documented in
this report. This finding involved a violation of NRC requirements. The significance of
inspection findings is indicated by their color (Green, White, Yellow, or Red), which is
determined using Inspection Manual Chapter 0609, Significance Determination Process. Their
cross-cutting aspects are determined using Inspection Manual Chapter 0310, Aspects within
the Cross-Cutting Areas. Violations of NRC requirements are dispositioned in accordance with
the NRC Enforcement Policy. The NRCs program for overseeing the safe operation of
commercial nuclear power reactors is described in NUREG-1649, Reactor Oversight Process.
Cornerstone: Mitigating Systems
Green. The inspectors identified a Green non-cited violation of Technical Specification 5.4.1.a, for the licensees failure to adequately adjust testing and preventive maintenance
activities in accordance with Procedure AP 16B-003, Planning and Scheduling Preventive
Maintenance, Revision 5. Specifically, the licensee did not adjust a preventive
maintenance task for a General Electric HEA 86 lockout relay and test the relay in
accordance with vendor recommendations and industry operating experience, which
resulted in the NB0215 186/M lockout relay associated with the B essential service water
pump motor breaker failing as-found testing on August 2, 2016. The inspectors identified a
Green non-cited violation of Technical Specification 5.4.1.a, for the licensees failure to
adequately adjust testing and preventive maintenance activities in accordance with
Procedure AP 16B-003, Planning and Scheduling Preventive Maintenance, Revision 5.
Specifically, the licensee did not adjust a preventive maintenance task for a General Electric
HEA 86 lockout relay and test the relay in accordance with vendor recommendations and
operating experience, which resulted in the NB0215 186/M lockout relay associated with the
B essential service water pump motor breaker failing as-found testing on August 2, 2016.
The licensees corrective actions included replacing the armature assembly associated with
the relay and retesting the relay satisfactorily. Additional corrective actions to address the
preventive maintenance activities are expected as a result of Condition Reports 108440 and
108548.
This finding is more than minor because it is associated with the equipment performance
attribute of the Mitigating Systems cornerstone and affected the cornerstone objective to
ensure the availability, reliability, and capability of systems that respond to initiating events
to prevent undesirable consequences. Specifically, with the NB0215 186/M lockout relay
failed on or before August 2, 2016, the safety-related 4160 volt NB02 bus was susceptible to
locking out as a result of an overcurrent condition. In accordance with NRC Inspection
Manual Chapter 0609, Appendix A, Exhibit 2, Mitigating Systems Screening Questions, the
inspectors determined this finding is not a deficiency affecting the design or qualification of a
mitigating structure, system, or component that maintained its operability or functionality; the
finding does not represent a loss of system and/or function; the finding does not represent
an actual loss of function of at least a single train for greater than its Technical Specification-
allowed outage time; and the finding does not represent an actual loss of function of one or
more non-Technical Specification trains of equipment designated as high safety-significant.
- 3 -
The finding has a cross-cutting aspect in the area of problem identification and resolution,
operating experience, because the organization did not systematically and effectively
evaluate relevant internal and external operating experience in a timely manner. This issue
is indicative of current performance because the station did not take corrective actions to
address the stations failure to adequately consider operating experience, the station did not
recognize the need to revise the testing and maintenance strategy following the August 2,
2016, failure, and the same failure would be expected to occur [P.5]. (Section 1R12)
- 4 -
PLANT STATUS
Wolf Creek Generating Station began the inspection period operating at full power. On July 5,
2016, operators reduced power to approximately 68 percent after load swings were observed on
the main generator and the La Cygne transmission line was disconnected from Wolf Creek. On
July 6, 2016, operators increased power to approximately 85 percent and completed main
turbine valve cycle testing. Plant power was restored to approximately full power later on July 6,
2016. On September 2, 2016, reactor coolant system unidentified leakage was calculated to be
greater than 1 gallon per minute, Technical Specification 3.4.13 was entered, and a plant
shutdown was completed, after which the licensee remained shut down to begin refueling
outage 21.
REPORT DETAILS
1.
REACTOR SAFETY
Cornerstones: Initiating Events, Mitigating Systems, and Barrier Integrity
1R04 Equipment Alignment (71111.04)
Partial Walk-Down
a.
Inspection Scope
The inspectors performed partial system walk-downs of the following risk-significant
systems:
July 13, 2016, centrifugal charging pump A
August 2, 2016, emergency diesel generator A
The inspectors reviewed the licensees procedures and system design information to
determine the correct lineup for the systems. They visually verified that critical portions
of the systems and/or trains were correctly aligned for the existing plant configuration.
These activities constituted two partial system walk-down samples as defined in
Inspection Procedure 71111.04.
b.
Findings
No findings were identified.
1R05 Fire Protection (71111.05)
Quarterly Inspection
a.
Inspection Scope
The inspectors evaluated the licensees fire protection program for operational status
and material condition. The inspectors focused their inspection on six plant areas
important to safety:
- 5 -
July 19, 2016, fire areas A-2 and A-4, safety injection pump rooms A and B,
elevation 1,974 feet
August 1, 2016, fire area ESWC, essential service water vertical loop chase,
elevation 1,974 feet through 2087 feet
August 15, 2016, fire areas C-13, C-14, and C-35, control building and
communications corridor - trains A and B safety related electrical equipment air
conditioning units, elevation 2,016 feet
September 27, 2016, fire area RB-6, reactor building - general area, elevation
2,068 feet
September 27, 2016, fire area RB-10, reactor building - general area, elevation
2,047 feet
September 28, 2016, fire area C-16, control building and communications
corridor - trains A and B safety related battery and switchboard rooms, elevation
2,016 feet
For each area, the inspectors evaluated the fire plan against defined hazards and
defense-in-depth features in the licensees fire protection program. The inspectors
evaluated control of transient combustibles and ignition sources, fire detection and
suppression systems, manual firefighting equipment and capability, passive fire
protection features, and compensatory measures for degraded conditions.
These activities constituted six quarterly inspection samples, as defined in Inspection
Procedure 71111.05.
b.
Findings
No findings were identified.
1R06 Flood Protection Measures (71111.06)
a.
Inspection Scope
On July 20, 2016, the inspectors completed an inspection of the stations ability to
mitigate flooding due to internal causes. After reviewing the licensees flooding analysis,
the inspectors chose two plant areas containing risk-significant structures, systems, and
components (SSCs) that were susceptible to flooding:
Auxiliary feedwater pipe chase room 1206
Auxiliary feedwater pipe chase room 1207
The inspectors reviewed plant design features and licensee procedures related to
internal flooding. The inspectors walked down the selected areas to inspect the design
features, including the material condition of seals, drains, and flood barriers. The
inspectors evaluated whether operator actions credited for flood mitigation could be
successfully accomplished.
- 6 -
These activities constituted completion of one flood protection measures sample, as
defined in Inspection Procedure 71111.06.
b.
Findings
No findings were identified.
1R07 Heat Sink Performance (71111.07)
a.
Inspection Scope
On September 14, 2016, the inspectors completed an inspection of the readiness and
availability of risk-significant heat exchangers. The inspectors observed the licensees
inspection of the ultimate heat sink and the material condition of the ultimate heat sink.
Additionally, the inspectors walked down the ultimate heat sink to observe its
performance and material condition and verified that the ultimate heat sink was receiving
the required maintenance.
These activities constituted completion of one heat sink performance annual review
sample, as defined in Inspection Procedure 71111.07.
b.
Findings
No findings were identified.
1R11 Licensed Operator Requalification Program and Licensed Operator Performance
(71111.11)
.1
Review of Licensed Operator Requalification
a.
Inspection Scope
On July 7, 2016, and September 8, 2016, the inspectors observed a portion of an annual
requalification test for licensed operators and simulator training for an operating crew,
respectively. The inspectors assessed the performance of the operators and the
evaluators critique of their performance. The inspectors also assessed the modeling
and performance of the simulator during the requalification activities and simulator
training activities.
These activities constituted completion of two quarterly licensed operator requalification
program samples, as defined in Inspection Procedure 71111.11.
b.
Findings
No findings were identified.
- 7 -
.2
Review of Licensed Operator Performance
a.
Inspection Scope
The inspectors observed the performance of on-shift licensed operators in the plants
main control room. At the time of the observations, the plant was in a period of
heightened activity and risk due to control rod parking and chemical and volume control
system inservice check valve testing. The inspectors observed the operators
performance of the following activities:
July 5, 2016, performance of STS AC-001, Main Turbine Valve Cycle Test, and
reactor power ascension from 68 percent power
August 18, 2016, control rod parking and chemical and volume control system
inservice check valve testing
In addition, the inspectors assessed the operators adherence to plant procedures,
including the conduct of operations procedure and other operations department policies.
These activities constituted completion of one quarterly licensed operator performance
sample, as defined in Inspection Procedure 71111.11.
b.
Findings
No findings were identified.
.3
Biennial Review
a.
Inspection Scope
The licensed operator requalification program involves two training cycles that are
conducted over a 2-year period. In the first cycle, the annual cycle, the operators are
administered an operating test consisting of job performance measures and simulator
scenarios. In the second part of the training cycle, the biennial cycle, operators are
administered an operating test and a comprehensive written examination.
To assess the performance effectiveness of the licensed operator requalification
program, the inspectors reviewed both the written examination and operating test quality
and observed licensee administration of an annual requalification test while onsite. The
operating tests observed included five job performance measures and two scenarios that
were used in the current biennial requalification cycle. These observations allowed the
inspectors to assess the licensee's effectiveness in conducting the operating test to
ensure operator mastery of the training program content and to determine if feedback of
performance analyses into the requalification training program was being accomplished.
On July 26, 2016, the licensee informed the inspectors of the completed cycle results for
Wolf Creek Generating Station for both the written examinations and the operating tests:
9 of 9 crews passed the simulator portion of the operating test
53 of 53 licensed operators passed the simulator portion of the operating test
- 8 -
53 of 53 licensed operators passed the job performance measure portion of the
operating test
51 of 53 licensed operators passed the written examination
Two individuals failed the written examination. One individual was remediated, retested,
and passed their retake examinations. One individual was not remediated and the
individuals license was terminated by the licensee.
The inspectors observed examination security measures in place during administration
of the exams (including controls and content overlap) and reviewed any remedial training
and re-examinations, if necessary. The inspectors also reviewed medical records of
six licensed operators for conformance to license conditions and the licensees system
for tracking qualifications and records of license reactivation for four operators.
The inspectors reviewed simulator performance for fidelity with the actual plant and the
overall simulator program of maintenance, testing, and discrepancy correction.
The inspectors completed one inspection sample of the biennial licensed operator
requalification program.
b.
Findings
No findings were identified.
1R12 Maintenance Effectiveness (71111.12)
a.
Inspection Scope
The inspectors reviewed three instances of degraded performance or condition of safety-
related SSCs:
August 2, 2016, NB0215 186/M lockout relay failed to trip during as-found testing
August 8, 2016, train B 480 VAC electrical power distribution subsystem,
excessive voltage
September 19, 2016, trains A and B safety injection system, unplanned outages
The inspectors reviewed the extent of condition of possible common cause SSC failures
and evaluated the adequacy of the licensees corrective actions. The inspectors
reviewed the licensees work practices to evaluate whether these may have played a
role in the degradation of the SSCs. The inspectors assessed the licensees
characterization of the degradation in accordance with 10 CFR 50.65 (the Maintenance
Rule), and verified that the licensee was appropriately tracking degraded performance
and conditions in accordance with the Maintenance Rule.
These activities constituted completion of three maintenance effectiveness samples, as
defined in Inspection Procedure 71111.12.
- 9 -
b.
Findings
Introduction. The inspectors identified a Green non-cited violation of Technical
Specification 5.4.1.a, for the licensees failure to adequately adjust testing and
preventive maintenance activities in accordance with Procedure AP 16B-003, Planning
and Scheduling Preventive Maintenance, Revision 5. Specifically, the licensee did not
adjust a preventive maintenance task for a General Electric HEA 86 lockout relay and
test the relay in accordance with vendor recommendations and operating experience,
which resulted in the NB0215 186/M lockout relay associated with the B essential
service water pump motor breaker failing as-found testing on August 2, 2016.
Description. During performance of Procedure STN NB-215, DPEF01B Feeder Breaker
Trip Circuit Verification, Revision 1A on August 2, 2016, while the B essential service
water pump and breaker were out of service for maintenance, the 186/M lockout relay
failed to trip during as-found testing. The lockout relay provides protection to the B
essential service water pump motor and 4160 volt safety-related bus NB02 in the event
of an overcurrent condition. If the lockout relay fails to actuate and trip the B essential
service water pump motor breaker, it could result in damage to the B essential service
water pump motor or cause the NB02 bus to lockout due to an overcurrent condition on
the bus, which would be recognized by the NB02 bus protection circuitry.
During the test in accordance with Section 8.2, NB0215 186/M Lockout Relay Tests, of
STN NB-215, a direct current test voltage of 82.5 volts is momentarily applied. The relay
is expected to actuate at 80 volts or less, but it is considered within tolerance if it
actuates at less than or equal to 87.5 volts, and the licensee determined that it is
acceptable for the relay to actuate up to 95 volts. During the performance of STN NB-
215 on August 2, 2016, the test voltage was increased up to 125 volts, but the relay did
not trip. The licensee did not test the relay past this point and replaced the armature
assembly associated with the relay, calibrated it, and retested it prior to returning the
relay and system to service.
This test was last performed successfully using Procedure RNM C-1301, Miscellaneous
Relay and Meter Equipment, Revision 6, on August 10, 2009, and the NB0215 186/M
lockout relay passed. The current testing and preventive maintenance task is performed
every six years, and the August 2, 2016, test was conducted within the grace period for
the current preventive maintenance task frequency.
The inspectors reviewed applicable vendor documentation, GEH-2058, Auxiliary
Relays, Revision E, for type HEA61 relays. This vendor documentation states, During
any scheduled outage of the equipment and preferably at yearly intervals, the relay
should be tripped electrically to insure that it is in good operating condition, and that all
the circuits are complete so that the breakers can be tripped. The inspectors also
reviewed Wolf Creek corrective action document Performance Improvement Request
(PIR) 2003-2708, which evaluated OE16724 - General Electric Type HEA Lockout
Relay Test Interval. The PIR discussed contact made with General Electric, HEA relays
tend to be sluggish during the first operation when tested on a 3 to 5 year interval. The
problem applies to the whole family of HEA relays, and General Electric recommends
testing yearly. Wolf Creeks lockout relays were tested on a 6-year frequency.
The inspectors also reviewed industry operating experience from June 19, 2012, which
was evaluated by Wolf Creek Condition Report 54212. The industry operating
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experience made two recommendations that included determining the total population
of General Electric HEA 86 relays and the subset of General Electric HEA 86 relays that
are not normally actuated each cycle or within the [preventive maintenance] frequency.
Additionally, the event report recommended, Any that can be tested on line should be
tested as soon as practicable. The functional test should be an electrical trip that
actuates the relay coil. Replace any test failure with modified [General Electric] HEA 86
relays or suitable alternative. Corrective actions did not identify any necessary changes
to the testing or maintenance activities for the NB0215 186/M lockout relay.
The inspectors noted that Section 6.2, Establishing [Preventive Maintenance] Activities,
of Procedure AP 16B-003, Planning and Scheduling Preventive Maintenance,
Revisions 2 through 7, provided direction for implementing the preventive maintenance
program including consideration of vendor recommendations and operating experience.
The inspectors determined that the August 2003 and June 2012 operating experience
documents were not adequately evaluated, in that the licensees relay testing and
preventive maintenance activities were not adjusted after considering vendor
recommendations and industry experience. The failure to appropriately adjust testing
and maintenance activities for HEA relays resulted in the failure of the 186/M lockout
relay on August 2, 2016. Additionally, neither the licensees evaluation of Condition
Report 106164, which was written to address the equipment failure on August 2, 2016,
nor any other condition report identified the need to revise the testing and preventive
maintenance frequency.
The licensees corrective actions for the August 2, 2016, relay failure included replacing
the armature assembly associated with the relay, retesting the relay satisfactorily, and
returning the relay and system to service. The station entered the equipment condition
into the corrective action program as Condition Report 106164, and the licensee entered
Condition Reports 108440 and 108548 into the corrective action program to address the
inspectors concerns associated with the need to revise the testing and preventive
maintenance activity frequency for the subject relay.
Analysis. The inspectors determined that the failure to adequately adjust a testing and
preventive maintenance task for the NB0215 186/M General Electric HEA 86 lockout
relay in accordance with Procedure AP 16B-003, Planning and Scheduling Preventive
Maintenance, was a performance deficiency. This finding is more than minor because it
is associated with the equipment performance attribute of the Mitigating Systems
cornerstone and affected the cornerstone objective to ensure the availability, reliability,
and capability of systems that respond to initiating events to prevent undesirable
consequences. Specifically, with the NB0215 186/M lockout relay failed on or before
August 2, 2016, and the safety-related 4160 volt NB02 bus was susceptible to locking
out as a result of an overcurrent condition. The inspectors evaluated the finding using
Exhibit 2, Mitigating Systems Screening Questions, of Inspection Manual Chapter 0609, Appendix A, Significance Determination Process (SDP) for Findings At-Power,
issued June 19, 2012, and determined this finding is not a deficiency affecting the design
or qualification of a mitigating structure, system, or component that maintained its
operability or functionality; the finding does not represent a loss of system and/or
function; the finding does not represent an actual loss of function of at least a single train
for greater than its Technical Specification-allowed outage time; and the finding does not
represent an actual loss of function of one or more non-Technical Specification trains of
equipment designated as high safety-significant. Therefore, the inspectors determined
the finding was of very low safety significance (Green).
- 11 -
The inspectors determined that the finding has a cross-cutting aspect in the area of
problem identification and resolution, operating experience, because the organization did
not systematically and effectively evaluate relevant internal and external operating
experience in a timely manner. Specifically, PIR 2003-2708 and Condition Report 54212
documented vendor recommendations and industry operating experience regarding HEA
relay failures, and neither the vendor recommendations nor the industry operating
experience were effectively implemented and institutionalized through changes to station
processes, procedures, equipment, and training programs, and testing and preventive
maintenance activities were not adequately adjusted. This issue is indicative of current
performance because the station did not take corrective actions to address the stations
failure to adequately consider operating experience, the station did not recognize the
need to revise the testing and maintenance strategy following the August 2, 2016,
failure, and the same failure would be expected to occur [P.5].
Enforcement. Technical Specification 5.4.1.a, requires, in part, that procedures shall be
established, implemented, and maintained covering the applicable procedures
recommended in Appendix A of Regulatory Guide 1.33, Revision 2. Section 9.b of
Appendix A to Regulatory Guide 1.33, Revision 2, requires that preventive maintenance
schedules be developed to specify inspections of equipment and inspection or
replacement of parts that have a specific lifetime. The licensee established Procedure
AP 16B-003, Planning and Scheduling Preventive Maintenance, which provides
direction for implementing the preventive maintenance program to meet the Regulatory
Guide 1.33 requirement. Section 6.2 of Procedure AP 16B-003 requires, in part, that
preventive maintenance activities be developed by considering vendor
recommendations and operating experience. Contrary to the above, until October 16,
the licensee did not ensure that preventive maintenance activities were developed by
considering vendor recommendations and operating experience. Specifically, the
licensee did not ensure that adequate preventive maintenance activities were developed
for the NB0215 186/M lockout relay by considering vendor recommendations to trip the
relay electrically during any scheduled outage of the equipment and operating
experience documented in PIR 2003-2708 and Condition Report 54212. As a result, the
NB0215 186/M lockout relay failed on or before August 2, 2016, and the safety-related
4160 volt NB02 bus was susceptible to locking out as a result of an overcurrent
condition. The licensee entered this condition into its corrective action program as
Condition Reports 106164, 108440, and 108548. The licensee replaced the relay
armature assembly and retested the relay satisfactorily. Additional corrective actions to
address the preventive maintenance activities are expected as a result of Condition
Reports 108440 and 108548. This violation is being treated as a non-cited violation
consistent with Section 2.3.2 of the Enforcement Policy: NCV 05000482/2016003-01,
Failure to Adequately Adjust Testing and Preventive Maintenance for Safety-Related
Lockout Relays.
1R13 Maintenance Risk Assessments and Emergent Work Control (71111.13)
a.
Inspection Scope
The inspectors reviewed three risk assessments performed by the licensee prior to
changes in plant configuration and the risk management actions taken by the licensee in
response to elevated risk:
- 12 -
July 15, 2016, condensate storage tank valve housing lift near the condensate
storage tank and auxiliary building
July 19, 2016, planned A safety injection pump maintenance
August 10, 2016, planned maintenance on train B motor driven auxiliary
feedwater pump
The inspectors verified that these risk assessment were performed timely and in
accordance with the requirements of 10 CFR 50.65 (the Maintenance Rule) and plant
procedures. The inspectors reviewed the accuracy and completeness of the licensees
risk assessments and verified that the licensee implemented appropriate risk
management actions based on the result of the assessments.
The inspectors also observed portions of three emergent work activities that had the
potential to affect the functional capability of mitigating systems:
July 1, 2016, unplanned maintenance on the non-safety auxiliary feedwater
pump
July 6, 2016, weekly risk assessment and emergent reactor power changes in
response the La Cygne transmission line out of service
August 15, 2016, unplanned maintenance on the train B class 1E electrical air
conditioning unit
The inspectors verified that the licensee appropriately developed and followed a work
plan for these activities. The inspectors verified that the licensee took precautions to
minimize the impact of the work activities on unaffected SSCs.
These activities constituted completion of six maintenance risk assessments and
emergent work control inspection samples, as defined in Inspection Procedure 71111.13.
b.
Findings
No findings were identified.
1R15 Operability Determinations and Functionality Assessments (71111.15)
a.
Inspection Scope
The inspectors reviewed four operability determinations that the licensee performed for
degraded or nonconforming SSCs:
July 1, 2016, operability determination of auxiliary feedwater system equipment
while the condensate storage tank valve house was removed
August 2, 2016, operability determination of B essential service water traveling
screen foot sprocket and collar set screw degradation
- 13 -
August 10, 2016, operability determination of shutdown and control bank rod
insertion limits in the cycle 21 safety analysis
August 15, 2016, operability determination of Class 1E electrical equipment air
conditioning unit SGK05B out of service as a result of a clogged condensation
drain line
The inspectors reviewed the timeliness and technical adequacy of the licensees
evaluations. Where the licensee determined the degraded SSC to be operable, the
inspectors verified that the licensees compensatory measures were appropriate to
provide reasonable assurance of operability. The inspectors verified that the licensee
had considered the effect of other degraded conditions on the operability of the
degraded SSC.
The inspectors reviewed operator actions taken or planned to compensate for degraded
or nonconforming conditions. The inspectors verified that the licensee effectively
managed these operator workarounds to prevent adverse effects on the function of
mitigating systems and to minimize their impact on the operators ability to implement
abnormal and emergency operating procedures.
These activities constituted completion of five operability and functionality review
samples, which included one operator work-around sample, as defined in Inspection
Procedure 71111.15.
b.
Findings
No findings were identified.
1R18 Plant Modifications (71111.18)
a.
Inspection Scope
The inspectors reviewed two permanent plant modifications that affected risk-significant
SSCs:
August 30, 2016, station black out diesel generator permanent electrical feed to
non-safety auxiliary feedwater pump
August 30 and 31, 2016, revision of SYS GK-122, Manual CRVIS Line-Up,
impacting the control room air conditioning unit 4A control room discharge
isolation damper
The inspectors reviewed the design and implementation of the modifications. The
inspectors verified that work activities involved in implementing the modifications did not
adversely impact operator actions that may be required in response to an emergency or
other unplanned event. The inspectors verified that post-modification testing was
adequate to establish the operability or functionality of the SSCs as modified.
These activities constituted completion of two samples of permanent modifications, as
defined in Inspection Procedure 71111.18.
- 14 -
b.
Findings
No findings were identified.
1R19 Post-Maintenance Testing (71111.19)
a.
Inspection Scope
The inspectors reviewed seven post-maintenance testing activities that affected risk-
significant SSCs:
July 13, 2016, B centrifugal charging pump
July 25, 2016, A pressure relief isolation valve breaker
August 3, 2016, B emergency diesel generator and fuel oil transfer pump
August 10, 2016, B auxiliary feedwater pump
August 31, 2016, train B auxiliary building and control room pressure testing
September 21, 2016, post-accident monitoring nuclear instrumentation testing
September 22, 2016, intermediate range nuclear instrument cable testing
The inspectors reviewed licensing- and design-basis documents for the SSCs and the
maintenance and post-maintenance test procedures. The inspectors observed the
performance of the post-maintenance tests to verify that the licensee performed the tests
in accordance with approved procedures, satisfied the established acceptance criteria,
and restored the operability of the affected SSCs.
These activities constituted completion of seven post-maintenance testing inspection
samples, as defined in Inspection Procedure 71111.19.
b.
Findings
No findings were identified.
1R20 Refueling and Other Outage Activities (71111.20)
a.
Inspection Scope
On September 2, 2016, reactor coolant system unidentified leakage was calculated to be
greater than 1 gallon per minute, Technical Specification 3.4.13 was entered, and a plant
shutdown was completed, after which the licensee remained shut down to begin
refueling outage 21. During the stations refueling outage that was in progress at the
end of the inspection period, the inspectors evaluated the licensees outage activities.
The inspectors verified that the licensee considered risk in developing and implementing
the outage plan, appropriately managed personnel fatigue, and developed mitigation
strategies for losses of key safety functions. This verification included the following:
Review of the licensees outage plan prior to the outage
- 15 -
Monitoring of shut-down and cool-down activities
Verification that the licensee maintained defense-in-depth during outage activities
Observation and review of reduced-inventory and mid-loop activities
Observation and review of fuel handling activities
These activities constituted partial completion of one refueling outage sample, as
defined in Inspection Procedure 71111.20.
b.
Findings
No findings were identified.
1R22 Surveillance Testing (71111.22)
a.
Inspection Scope
The inspectors observed four risk-significant surveillance tests and reviewed test results
to verify that these tests adequately demonstrated that the SSCs were capable of
performing their safety functions:
In-service tests:
September 6, 2016, STS MT-008, Spring Loaded Safety Valve Settings,
Revision 25
Reactor coolant system leak detection tests:
September 1 and 2, 2016, STS BB-006, Water Inventory Balance Using the
NPIS Computer, Revision 14
Other surveillance tests:
July 28, 2016, STS IC-211A, Actuation Logic Test Train A Solid State Protection
System, Revision 36A
August 31, 2016, STN AP-102, NSAFP Full Flow Test, Revision 7
The inspectors verified that these tests met technical specification requirements, that the
licensee performed the tests in accordance with their procedures, and that the results of
the test satisfied appropriate acceptance criteria. The inspectors verified that the
licensee restored the operability of the affected SSCs following testing.
These activities constituted completion of four surveillance testing inspection samples,
as defined in Inspection Procedure 71111.22.
- 16 -
b.
Findings
No findings were identified.
Cornerstone: Emergency Preparedness
1EP2 Alert and Notification System Evaluation (71114.02)
a.
Inspection Scope
The inspector verified the adequacy of the licensees methods for testing the primary
and backup alert and notification system. The inspector also reviewed the licensees
program for identifying emergency planning zone locations requiring tone alert radios
and for distributing the radios, and reviewed audits of distribution records. The inspector
interviewed licensee personnel responsible for the maintenance of the primary and
backup alert and notification system and reviewed a sample of corrective action system
reports written for alert and notification system problems. The inspector compared the
licensees alert and notification system testing program with criteria in NUREG-0654,
Criteria for Preparation and Evaluation of Radiological Emergency Response Plans and
Preparedness in Support of Nuclear Power Plants, Revision 1; FEMA Report REP-10,
Guide for the Evaluation of Alert and Notification Systems for Nuclear Power Plants,
and the licensees current FEMA-approved alert and notification system design report,
dated May 7, 2008.
These activities constituted completion of one alert and notification system evaluation
sample as defined in Inspection Procedure 71114.02.
b.
Findings
No findings were identified.
1EP3 Emergency Response Organization Staffing and Augmentation System (71114.03)
a.
Inspection Scope
The inspector verified the licensees emergency response organization on-shift and
augmentation staffing levels were in accordance with the licensees emergency plan
commitments. The inspector reviewed documentation and discussed with licensee staff
the operability of primary and backup systems for augmenting the on-shift emergency
response staff to verify the adequacy of the licensees methods for staffing emergency
response facilities, including the licensees ability to staff pre-planned alternate facilities.
The inspector also reviewed records of emergency response organization augmentation
tests and events to determine whether the licensee had maintained a capability to staff
emergency response facilities within emergency plan timeliness commitments.
These activities constituted completion of one emergency response organization staffing
and augmentation testing sample as defined in Inspection Procedure 71114.03.
b.
Findings
No findings were identified.
- 17 -
1EP5 Maintenance of Emergency Preparedness (71114.05)
a.
Inspection Scope
The inspector reviewed the following for the period November 2014 to July 2016:
After-action evaluation reports for licensee drills and exercises;
Independent audits and surveillances of the licensees emergency preparedness
program;
Self-assessments of the emergency preparedness program conducted by the
licensee;
Licensee evaluations of changes made to the emergency plan and emergency
plan implementing procedures;
Drill and exercise performance issues entered into the licensees corrective
action program;
Emergency preparedness program issues entered into the licensees corrective
action program;
Maintenance records for equipment supporting the emergency preparedness
program; and
Emergency response organization and emergency planner training records.
The inspector reviewed summaries of corrective action program reports written by the
licensee between November 2014 and July 2016 associated with emergency
preparedness and selected 23 to review against program requirements, to determine the
licensees ability to identify, evaluate, and correct problems in accordance with planning
standard 10 CFR 50.47(b)(14) and 10 CFR Part 50, Appendix E, IV.F. The inspector
verified that the licensee accurately and appropriately identified and corrected
emergency preparedness weaknesses during critiques and assessments.
The inspector reviewed one licensee evaluation of the impact of changes to the
emergency plan and implementing procedures to determine the licensees ability to
identify reductions in the effectiveness of the emergency plan in accordance with the
requirements of 10 CFR 50.54(q)(3) and 50.54(q)(4). The inspector verified that the
evaluation of proposed changes to the licensee emergency plan appropriately identified
the impact of the changes prior to being implemented.
The inspector reviewed records pertaining to the maintenance of equipment and facilities
used to implement the emergency plan against program requirements to determine the
licensees ability to maintain equipment in accordance with the requirements of 10 CFR
50.47(b)(8) and 10 CFR Part 50, Appendix E, IV.E. The inspector verified that
equipment and facilities were maintained in accordance with the commitments of the
licensees emergency plan.
- 18 -
These activities constituted completion of one sample of the maintenance of the
licensees emergency preparedness program as defined in Inspection
Procedure 71114.05.
b.
Findings
No findings were identified.
1EP6 Drill Evaluation (71114.06)
Training Evolution Observation
a.
Inspection Scope
On July 7 and August 11, 2016, the inspectors observed simulator-based licensed
operator requalification training that included implementation of the licensees
emergency plan. The inspectors verified that the licensees emergency classifications,
off-site notifications, and protective action recommendations were appropriate and
timely. The inspectors verified that any emergency preparedness weaknesses were
appropriately identified by the evaluators and entered into the corrective action program
for resolution.
These activities constituted completion of two training observation samples, as defined
in Inspection Procedure 71114.06.
b.
Findings
No findings were identified.
4.
OTHER ACTIVITIES
Cornerstones: Initiating Events, Mitigating Systems, Barrier Integrity, Emergency
Preparedness, Public Radiation Safety, Occupational Radiation Safety, and
Security
4OA1 Performance Indicator Verification (71151)
.1
Mitigating Systems Performance Index: High Pressure Injection Systems (MS07)
a.
Inspection Scope
The inspectors reviewed the licensees mitigating system performance index data for the
period of July 1, 2015, through September 12, 2016, to verify the accuracy and
completeness of the reported data. The inspectors used definitions and guidance
contained in Nuclear Energy Institute Document 99-02, Regulatory Assessment
Performance Indicator Guideline, Revision 7, to determine the accuracy of the reported
data.
These activities constituted verification of the mitigating system performance index for
high pressure injection systems, as defined in Inspection procedure 71151.
- 19 -
b.
Findings
No findings were identified.
.2
Mitigating Systems Performance Index: Cooling Water Support Systems (MS10)
a.
Inspection Scope
The inspectors reviewed the licensees mitigating system performance index data for the
period of July 1, 2015, through September 12, 2016, to verify the accuracy and
completeness of the reported data. The inspectors used definitions and guidance
contained in Nuclear Energy Institute Document 99-02, Regulatory Assessment
Performance Indicator Guideline, Revision 7, to determine the accuracy of the reported
data.
These activities constituted verification of the mitigating system performance index for
cooling water support systems, as defined in Inspection Procedure 71151.
b.
Findings
No findings were identified.
.3
Drill/Exercise Performance (EP01)
a.
Inspection Scope
The inspector reviewed the licensees evaluated exercises and selected drill and training
evolutions that occurred between October 2015 and June 2016 to verify the accuracy of
the licensees data for classification, notification, and protective action recommendation
opportunities. The inspector reviewed a sample of the licensees completed
classifications, notifications, and protective action recommendations to verify their
timeliness and accuracy. The inspector used definitions and guidance contained in
Nuclear Energy Institute Document 99-02, Regulatory Assessment Performance
Indicator Guideline, Revision 7, to determine the accuracy of the data reported. The
specific documents reviewed are described in the attachment to this report.
These activities constituted verification of the drill/exercise performance indicator as
defined in Inspection Procedure 71151.
b.
Findings
No findings were identified.
.4
Emergency Response Organization Drill Participation (EP02)
a.
Inspection Scope
The inspector reviewed the licensees records for participation in drill and training
evolutions between October 2015 and June 2016 to verify the accuracy of the licensees
data for drill participation opportunities. The inspector verified that all members of the
licensees emergency response organization in the identified key positions had been
counted in the reported performance indicator data. The inspector reviewed the
- 20 -
licensees basis for reporting the percentage of emergency response organization
members who participated in a drill. The inspector reviewed drill attendance records and
verified a sample of those reported as participating. The inspector used definitions and
guidance contained in Nuclear Energy Institute Document 99-02, Regulatory
Assessment Performance Indicator Guideline, Revision 7, to determine the accuracy of
the data reported. The specific documents reviewed are described in the attachment to
this report.
These activities constituted verification of the emergency response organization drill
participation performance indicator as defined in Inspection Procedure 71151.
b.
Findings
No findings were identified.
.5
Alert and Notification System Reliability (EP03)
a.
Inspection Scope
The inspector reviewed the licensees records of alert and notification system tests
conducted between October 2015 and June 2016 to verify the accuracy of the licensees
data for siren system testing opportunities. The inspector reviewed procedural guidance
on assessing alert and notification system opportunities and the results of periodic alert
and notification system operability tests. The inspector used definitions and guidance
contained in Nuclear Energy Institute Document 99-02, Regulatory Assessment
Performance Indicator Guideline, Revision 7, to determine the accuracy of the data
reported. The specific documents reviewed are described in the attachment to this
report.
These activities constituted verification of the alert and notification system reliability
performance indicator as defined in Inspection Procedure 71151.
b.
Findings
No findings were identified.
4OA2 Problem Identification and Resolution (71152)
Routine Review
a. Inspection Scope
Throughout the inspection period, the inspectors performed daily reviews of items
entered into the licensees corrective action program and periodically attended the
licensees condition report screening meetings. The inspectors verified that licensee
personnel were identifying problems at an appropriate threshold and entering these
problems into the corrective action program for resolution. The inspectors verified that
the licensee developed and implemented corrective actions commensurate with the
significance of the problems identified. The inspectors also reviewed the licensees
problem identification and resolution activities during the performance of the other
inspection activities documented in this report.
- 21 -
b. Findings
No findings were identified.
4OA3 Follow-up of Events and Notices of Enforcement Discretion (71153)
Plant Events
a. Inspection Scope
For the plant events listed below, the inspectors reviewed and/or observed plant
parameters, reviewed personnel performance, and evaluated performance of mitigating
systems. The inspectors communicated the plant event to appropriate regional
personnel, and compared the event details with criteria contained in IMC 0309,
Reactive Inspection Decision Basis for Reactors, issued October 28, 2011, for
consideration of potential reactive inspection activities. As applicable, the inspectors
verified that Wolf Creek staff made appropriate emergency classification assessments
and properly reported the events in accordance with 10 CFR Parts 50.72 and 50.73.
The inspectors reviewed Wolf Creeks follow-up actions related to the events to assure
that Wolf Creek implemented appropriate corrective actions commensurate with their
safety significance.
Excessive unidentified reactor coolant system leakage resulting in
commencement of technical specification required shutdown on September 2,
2016 (event notice 52218)
Seismic monitor triggered on September 3, 2016, due to seismic event during
plant shutdown
These activities constituted completion of two event follow-up samples, as defined in
b. Findings
No findings were identified.
4OA5 Other Activities
World Association of Nuclear Operators (WANO)/Institute of Nuclear Power Operations
(INPO) Report Review
a. Inspection Scope
The inspectors reviewed the final report for the WANO/INPO assessment conducted in
September 2015. The inspectors evaluated this report to ensure that NRC perspectives
of Wolf Creek Nuclear Operating Corporation performance were consistent with any
issues identified during the assessments. The inspectors also reviewed this report to
determine whether any significant safety issues were identified that required further NRC
follow-up.
- 22 -
b. Findings
No findings were identified.
4OA6 Meetings, Including Exit
Exit Meeting Summary
The inspectors presented the inspection results to Mr. C. Reasoner, Site Vice President, and
other members of the licensee's staff of the results of the licensed operator requalification
program inspection on June 30, 2016. The final results of the inspection were telephonically
presented to Mr. R. Meyer, Licensed Supervising Instructor, Simulator and Exam Group, and
other members of your staff on August 8, 2016. The inspectors asked the licensee whether any
materials examined during the inspection should be considered proprietary. No proprietary
information was identified.
On August 4, 2016, the inspector presented the results of the onsite inspection of the
emergency preparedness program to Mr. A. Heflin, President and Chief Executive Officer, and
other members of the licensee staff. The licensee acknowledged the issues presented. The
licensee confirmed that any proprietary information reviewed by the inspector had been returned
or destroyed.
On October 19, 2016, the inspectors presented the inspection results to Mr. J. McCoy, Vice
President, Engineering, and other members of the licensee staff. The licensee acknowledged
the issues presented. The licensee confirmed that any proprietary information reviewed by the
inspectors had been returned or destroyed.
Attachment
SUPPLEMENTAL INFORMATION
KEY POINTS OF CONTACT
Licensee Personnel
R. Acree, Licensed Instructor
T. Baban, Manager, System Engineering
W. Brown, Superintendent, Security Operations
T. Broyles, Manager, Information Services
D. Campbell, Superintendent, Maintenance
J. Dagenette, Emergency Planning
M. Dale, Emergency Planning
T. Damashek, Simulator Fidelity Coordinator
T. East, Superintendent, Emergency Planning
J. Edwards, Manager, Operations
D. Erbe, Manager, Security
R. Fincher, Manager, Quality
R. Flannigan, Manager, Nuclear Engineering
J. Fritton, Oversight
B. Gagnon, Supervisor, Security
N. Good, Licensing Engineer
C. Gross, Manager, Chemistry
C. Hafenstine, Manager, Regulatory Affairs
A. Heflin, President and Chief Executive Officer
S. Henry, Manager, Integrated Plant Scheduling
R. Hobby, Licensing Engineer
J. Isch, Superintendent, Operations Work Controls
J. Knapp, Superintendent, Operations Training
B. Lee, Licensed Supervising Instructor, Operator Requalification
D. Mand, Manager, Design Engineering
J. McCoy, Vice President, Engineering
R. Meyer, Licensed Supervising Instructor, Simulator and Exam Group
W. Muilenburg, Supervisor, Licensing
L. Ratzlaff, Manager, Maintenance
C. Reasoner, Site Vice President
A. Servaes, Licensed Instructor
M. Skiles, Manager, Radiation Protection
T. Slenker, Supervisor, Operations Support
S. Smith, Plant Manager
M. Storts, Engineer
A. Stueve, Engineer
A. Stull, Vice President and Chief Administrative Officer
M. Tate, Superintendent, Security Operations
J. Yunk, Manager, Training
A-2
LIST OF ITEMS OPENED, CLOSED, AND DISCUSSED
Opened and Closed 05000482-2016003-01
Failure to Adequately Adjust Testing and Preventive
Maintenance for Safety-Related Lockout Relays
(Section 1R12)
LIST OF DOCUMENTS REVIEWED
Section 1R04: Equipment Alignment
Procedures
Number
Title
Revision
CKL BG-120
Chemical and Volume Control System Normal Valve Lineup 41
CKL BG-130
Chemical and Volume Control System Switch and Breaker
Lineup
31A
CKL JE-120
Emergency Fuel Oil System Lineup
19
CKL KJ-121
Diesel Generator NE01 and NE02 Valve Checklist
39
STS BG-100B
Centrifugal Charging System B Train Inservice Pump Test
51
SYS BG-201
Shifting Charging Pumps
66
SYS EG-120
Component Cooling Water System
39
Drawings
Number
Title
Revision
M-12BG03
Piping and Instrumentation Diagram Chemical & Volume
Control System
48
M-12JE01
Piping and Instrumentation Diagram Emergency Fuel Oil
System
19
M-12KJ01
Piping and Instrumentation Diagram Standby Diesel
Generator A Cooling Water System
13
M-12KJ02
Piping and Instrumentation Diagram Standby Diesel
Generator A Intake Exhaust. F.O. and Start . Air Sys.
22
M-12KJ03
Piping and Instrumentation Diagram Standby Diesel
Generator A Lube Oil System
17
M-13BG02
Piping Isometric CVCS-Max. Charging Flow A & B Train-
Auxiliary Bldg.
11
M-13BG09
Small Piping Isometric CVCS Seal Water Injection Auxiliary
Building
15
A-3
Drawings
Number
Title
Revision
M-12BG03
Piping and Instrumentation Diagram Chemical & Volume
Control System
48
M-13BG10
Small Piping Isometric RC PP Seal Water Return & Excess
Letdown Flow-Auxiliary Bldg.
2
Condition Reports
106338
Section 1R05: Fire Protection
Procedures
Number
Title
Revision
AP 10-102
Control of Combustible Materials
19
AP 10-106
Fire Preplans
17
Condition Reports
106124
106133
106335
Miscellaneous
Number
Title
Revision
E-1F9905
Fire Hazard Analysis
7
Section 1R06: Flood Protection Measures
Procedures
Number
Title
Revision
AP 10-104
Breach Authorization
35
Drawings
Number
Title
Revision
M-120103
Symbols and Legend for System Flow and Piping and
Instrumentation Diagrams
1
M-12FC02
Piping & Instrumentation Diagram Auxiliary Turbines
Auxiliary Feedwater Pump Turbine
23
M-12LE01
Piping and Instrumentation Diagram Turb. Bldg. and Aux.
Feedwater Pump Rooms Oily Waste System
8
A-4
Drawings
Number
Title
Revision
M-13FC06
Small Piping Isometric Auxiliary Feedwater Pump Turbine
Drains - Aux. Bldg.
8
M-13LE01
Piping Isometric Oily Waste Sump Discharge Tendon
Access & Aux. Building
3
M-17LF01
Plumbing and Drainage System Notes, Symbols and
Schedules
2
M-17LF02
Plumbing and Drainage System Details
2
M-OP1151
Drainage Systems (LE) Auxiliary Building El. 1974-0, El.
1989-0 & El. 2000-0 Area 5
6
Condition Reports
90879
100653
100654
100655
106165
Work Orders
08-303899-000
15-397860-000
16-416247-000
16-416247-001
16-416247-002
Miscellaneous
Number
Title
Revision
FL-01
Flooding of the Auxiliary Building
2
FL-04
Summary of Flood Levels in All Aux. Bldg Rooms Due to
Pipe Break or Crack
2
LE-M-002
Flood Level in Auxiliary Building Rooms 1206 & 1207 Due
to Pipe Break
1
Section 1R07: Heat Sink Performance
Procedures
Number
Title
Revision
STN MT-004
Ultimate Heat Sink Dam Surveillance Vertical Movement
And Sedimentation
5
Drawings
Number
Title
Revision
S-0080
Ultimate Heat Sink Plan & Sections
16
A-5
Work Orders
15-409222-000
15-409921-000
Miscellaneous
Number
Title
Revision
C-404
Periodic Surveillance of Safety Related Water Control
Structures and Reservoir
8
WR-WC-UH-1
Area Capacity - Ultimate Heat Sink
1
WR-WC-UH-1A
Elevation-Area-Capacity of UHS
0
Z065-C-001
Evaluation of Annual UHS Sediment Measurements
10
Section 1R11: Licensed Operator Requalification Program
Procedures
Number
Title
Revision
AI 28A-100
Condition Report Resolution
10A
AI 30B-015
Licensed Operator Requalification Examination Guidelines
10A
AI 30C-001
Continued Assurance of Simulator Fidelity
16A
AI 30C-004
Simulator Real Time Capacity Testing
5B
AI 30C-005
Simulator Steady State Testing
9A
AI 30C-007
Simulator Core Testing
3
AI 30C-008
Scenario Based Testing
2A
AI 30C-010
Post Event Testing
1
AI 30E-002
Evaluation
42
AI 30E-013
Written and Oral Examinations
24
AI 30E-015
Just-In-Time Training
11
AI 30E-023
Remediation
3
AI 30E-23-01
Remediation Plan
2
Procedure Use and Adherence
42
Procedure Users Guide for Abnormal Plant Conditions
33
AP 21-001
Conduct of Operations
77
AP 22-001
Conduct of Pre-Job and Post-Job Briefs
19
Licensed Operator Requalification Training Program
28
A-6
Procedures
Number
Title
Revision
EPP 06-006
Protective Action Recommendations
9
GEN 00-004
Power Operation
86
GEN 00-008
RCS Level Less Than Reactor Vessel Flange Operations
29
OFN MA-038
Rapid Plant Shutdown
28
STN SF-001
Control Rod Parking
18A
STS AC-001
Main Turbine Valve Cycle Test
52
STS BG-210
CVCS Inservice Check Valve Test
33
Condition Reports
70423
76993
76995
88178
94596
96734
99058
99576
100662
101655
102267
106525
106526
Miscellaneous
Number
Title
Revision/Date
Reactivity Maneuver Plan
July 6, 2016
Simulator Differences List
April 13, 2016
Simulator Steady State Testing
Transient Test 3 - Simultaneous Closure of All Main
Steam Isolation Valves
Transient Test 5 - Trip of a Single RCP
Transient Test 7 - Maximum Rate of Power Ramp
Week 0 - SRO and RO Written Examination
Week 0 - 5 JPMs, 2 Scenarios
Week 1 - 5 JPMs, 2 Scenarios
Week 4 - 5 JPMs, 2 Scenarios
Week 7 - 5 JPMs, 2 Scenarios
APF 06-002-01
Emergency Action Levels
17A
DTI 212
Maintaining Simulator Setup Current with the Plant
1
DTIF 212-01
Maintaining Simulator Setup Checklist and Index Sheets
April 11, 2016
LR5004009
Mid Loop Operations
6
A-7
Miscellaneous
Number
Title
Revision/Date
Scenario 16-11
2016 Biennial Requalification Exam
0
Scenario 16-12
2016 Biennial Requalification Exam
0
Section 1R12: Maintenance Effectiveness
Procedures
Number
Title
Revision
Planning and Scheduling Preventive Maintenance
7
MGE EOOP-05
Insulation Resistance Testing
23
MPE E009-01
Siemens Breaker Cubicle Maintenance, Testing and
Swapping
5
MPE E009Q-01
13.8 KV and 4.16 KV Switchgear Inspection and Testing
34A
STN NB-215
DPEF01B Feeder Breaker Trip Circuit Verification
1A
STS KJ-015B
Manual/Auto Fast Start, Sync & Loading of EDG NE02
42
STS NB-005
Breaker Alignment Verification
29
SYS NG-132
Energizing NG02, NG04 and NG06E
22
SYS NG-332
Deenergizing NG02, NG04 and NG06E
20
Drawings
Number
Title
Revision
E-K3EF01A
Schematic Diagram Essential Service Water Pump B
12
KD-7496
One Line Diagram
59
Condition Reports
29718
54212
54926
64870
64999
65676
66396
66398
77718
83510
85417
85309
88661
95773
97335
98587
98588
100088
100380
100384
100629
100716
102162
104411
104413
104869
106164
106180
106211
106273
106286
108440
108548
A-8
Work Orders
08-303899-000
Miscellaneous
Number
Title
Revision/Date
54926
Functional Failure Determination Checklist
August 16, 2012
64870
Functional Failure Determination Checklist
May 16, 2013
64999
Functional Failure Determination Checklist
April 4, 2013
65676
Functional Failure Determination Checklist
April 17, 2013
66396
Functional Failure Determination Checklist
April 28, 2013
74290
Functional Failure Determination Checklist
November 27,
2013
77718
Functional Failure Determination Checklist
January 25, 2014
83510
Functional Failure Determination Checklist
August 7, 2014
85309
Functional Failure Determination Checklist
July 23, 2014
85417
Functional Failure Determination Checklist
July 23, 2014
88661
Functional Failure Determination Checklist
November 12,
2014
90187
Functional Failure Determination Checklist
January 5, 2015
93127
Functional Failure Determination Checklist
April 1, 2015
93146
Functional Failure Determination Checklist
April 1, 2015
93357
Functional Failure Determination Checklist
April 1, 2015
97335
Functional Failure Determination Checklist
July 26, 2015
98434
Functional Failure Determination Checklist
August 25, 2015
106164
Functional Failure Determination Checklist
August 30, 2016
EM-01
Maintainence Rule Final Scope Evaluation
Printed
September 19,
2016
EM-02
Maintainence Rule Final Scope Evaluation
Printed
September 19,
2016
EM-03
Maintainence Rule Final Scope Evaluation
Printed
September 19,
2016
A-9
Miscellaneous
Number
Title
Revision/Date
EM-04
Maintainence Rule Final Scope Evaluation
Printed
September 19,
2016
EM-05
Maintainence Rule Final Scope Evaluation
Printed
September 19,
2016
EM-06
Maintainence Rule Final Scope Evaluation
Printed
September 19,
2016
EM-07
Maintainence Rule Final Scope Evaluation
Printed
September 19,
2016
EM-08
Maintainence Rule Final Scope Evaluation
Printed
September 19,
2016
EM-09
Maintainence Rule Final Scope Evaluation
Printed
September 19,
2016
GEH-2058
Auxiliary Relays
E
NB-01
Maintenance Rule Final Scope Evaluation
Printed September
27, 2016
NB-02
Maintenance Rule Final Scope Evaluation
Printed September
27, 2016
NB-03
Maintenance Rule Final Scope Evaluation
Printed
September 27,
2016
NB-04
Maintenance Rule Final Scope Evaluation
Printed
September 27,
2016
NB-05
Maintenance Rule Final Scope Evaluation
Printed
September 27,
2016
NG
System Health Report
April 1, 2016
through June 30,
2016
NG-01
Maintenance Rule Final Scope Evaluation
August 9, 2016
NG-02
Maintenance Rule Final Scope Evaluation
August 9, 2016
NG-03
Maintenance Rule Final Scope Evaluation
August 9, 2016
A-10
Miscellaneous
Number
Title
Revision/Date
NG-04
Maintenance Rule Final Scope Evaluation
August 9, 2016
PIR 2003-2708
Section 1R13: Maintenance Risk Assessment and Emergent Work Controls
Procedures
Number
Title
Revision
AI 14-011
Lifting and Rigging
7
AI 22C-013
Protected Equipment Program
17
AP 14-001
Control of Heavy Loads, Lifting, and Rigging
4
Control of Locked Component Status
70
On-Line Nuclear Safety and Generation Risk Assessment
22
Risk Management and Contingency Planning
11
Operability Determination and Functionality Assessment
32
GEN 00-004
Power Operation
86
STN AP-101
NSAFP Recirc Test
11
STN EM-001A
Train A Leakage Inspection Program of Safety Injection
System
2A
STN EM-201
Safety Injection System Valve Test
11A
STS EM-100A
Safety Injection Pump A Inservice Pump Test
39
STS EM-201A
Safety Injection System Train A Inservice Valve Test
7
SYS GK-200
Non-Functional Class 1E A/C Unit
35
Drawings
Number
Title
Revision
M-12BG03
Piping and Instrumentation Diagram Chemical & Volume
Control System
48
M-12EJ01
Piping and Instrumentation Diagram Residual Heat
Removal System
52
M-12EM01
Piping & Instrumentation Diagram High Pressure Coolant
Injection System
42
M-12EM02
Piping & Instrumentation Diagram High Pressure Coolant
Injection System
21
A-11
Drawings
Number
Title
Revision
M-12EM03
Piping & Instrumentation Diagram High Pressure Coolant
Injection System Test Line
2
M-13GK01
Small Piping Isometric Room Coolers And Compressors
Vents and Drains - Aux. Bldg.
14
Condition Reports
66605
66841
105564
105614
105615
105625
106303
106322
106416
107185
Work Orders
13-366479-000
13-378954-000
14-390199-000
15-405362-000
15-405970-000
15-408584-000
15-409609-000
15-409615-000
15-409616-000
15-409617-000
15-409618-000
16-411165-000
16-416523-000
16-416523-001
13-366479-000
Miscellaneous
Number
Title
Revision/Date
Control Room Turnover Checklist
August 12, 2016
15-400938-053
Rigging and Hoisting Checklist
July 14, 2016 16-302
Control Room Risk Assessment Log/Work Schedule;
Risk Assessment Dates - July 7, 2016, through July 10,
2016
June 9, 2016 16-305
Control Room Risk Assessment Log/Work Schedule;
Risk Assessment Dates - July 25, 2016, through July 31,
2016
July 24, 2016 16-307
Control Room Risk Assessment Log/Work Schedule;
Risk Assessment Dates - August 8, 2016, through
August 14, 2016
August 9, 2016 16-308
Control Room Risk Assessment Log/Work Schedule;
Risk Assessment Dates - August 15, 2016, through
August 21, 2016
August 1, 2016 16-308
Daily Operational Focus Senior Leadership Review
Team People Solving Problems
August 16, 2016
M-622.1-00061
Instruction Manual For Package Air Conditioner Units
W42
WCNOC-4
Report on Control of Heavy Loads
18
A-12
Section 1R15: Operability Evaluations
Procedures
Number
Title
Revision
AI 22A-001
Operator Work Arounds/Operator Burdens/Control Room
Deficiencies
12
Reload Core Configurations
0
GEN 00-005
Minimum Load to Hot Standby
87
Drawings
Number
Title
Revision
M-020-0K037
General Arrangement Model 45A Traveling Water Screen,
8-0 Wide x 43-0 Centers
W08
M-020-0K057
FMC/Foot Section Assembly for 8-0 Wide Water Screen
W01
Condition Reports
79425
89251
105567
106183
106289
106296
106416
106417
106425
106438
107042
Miscellaneous
Number
Title
Revision/Date
Control Room WR/WO Log
September 10,
2016
014512
Safety-Related Power For Temp Fans Between SGK05A &
B Areas
3
015147
ESW Traveling Water Screen Sprocket Set
1
APF 21-001-02
Control Room Turnover Checklist, Days
September 9,
2016
APF 21-001-04
Auxiliary Building Ops Relief Checklist, Nights
September 10,
2016
APF 21-001-05
Turbine Building Ops Relief Checklist, Nights
September 10,
2016
APF 21-001-06
Site Operator Relief Checklist, Nights
September 10,
2016
APF 21-001-09
Fire Brigade Leader Relief Checklist, Nights
September 10,
2016
A-13
Miscellaneous
Number
Title
Revision/Date
CR 105567
Basic Engineering Disposition - Auxiliary Building Water
Intrusion Via Penetration P125W2312 or CST Sump Drain
June 30, 2016
E-1F9910
Post-Fire Safe Shutdown Area Analysis
14
EQSD-1
Equipment Qualification Design Basis Document
9
M-020-0K015
Instruction Manual for Traveling Water Screens
W21
OE-EF-16-002
FEF01B - ESW Traveling Water Screens
0
OE-EF-16-002
FEF01B - ESW Traveling Water Screens
1
OE NB-16-004
Operability Evaluation associated with CR 106417
0
Operability Evaluation - SF/Rod Control System
0
SCA-16-0008
ESW Traveling Screen Footshaft Collar Setscrew
0
Various
Operational Issues Database
September 10,
2016
Section 1R18: Plant Modifications
Procedures
Number
Title
Revision
STN AP-102
NSAFP Full Flow Test
7
SYS AP-122
Non-Safety Aux Feed Pump Operation
8
SYS AP-124
Non-Safety Aux Feed Pump Operation On Recirc
1
SYS GK-122
Manual CRVIS Line-Up
22
Drawings
Number
Title
Revision
KD-7496
One Line Diagram
60
M-12AP01
Piping & Instrumentation Diagram Condensate Storage And
Transfer System
14
M-12GK01
Piping & Instrumentation Diagram Control Building HVAC
13
Condition Reports
106373
106725
A-14
Miscellaneous
Number
Title
Revision/Date
14776
Field Change Notice-SBO Feed For Non-Safety Auxiliary
Feedwater Pump
3
16-1517
Document Revision Request
August 30, 2016
50.59 Evaluation
2016-0002
Dedicated Operator to Support Maintenance Activity on
GKD0081
August 30, 2016
Basic
Engineering
Disposition
Required Function of GKD0081
August 30, 2016
STN AP-102
NSAFP Full Flow Test
Performed
August 31, 2016
Section 1R19: Post-Maintenance Testing
Procedures
Number
Title
Revision
AI 16-007
Electrical Safety Manual
10
AP 12-003
15
Post Maintenance Testing Development
18A
Identification and Control of Materials, Parts, and
Components
16
STS AL-102
MDAFW Pump B Inservice Pump Test
45A
STS AL-201B
MDAFW Pump B Inservice Check Valve Test
16A
STS BG-100B
Centrifugal Charging System B Train Inservice Pump Test
51
STS IC-433
Channel Calibration Nuclear Instrumentation System Post
Accident Monitoring N61
17
STS JE-001B
Emergency Diesel Fuel Oil System Train B Test
12
STS KJ-015B
Manual/Auto Fast Start, Sync & Loading of EDG NE02
42
STS MT-024A
Functional Test of 480 and 120 Volt Molded Case Circuit
Breakers
14
STS PE-004
AUX Building And Control Room Pressure Test
16
STS PE-061
Control Room/Control Building Habitability Test
1
SYS GK-122
Manual CRVIS Line-Up
21
SYS GK-200
Non-Functional Class IE A/C Unit
35
A-15
Drawings
Number
Title
Revision
E-13GK13A
Schematic Diagram Class IE Electrical Equipment A/C Unit
7
M-622.1A-00002 SGK05A & SGK05B Air Conditioner Electrical Schematic
W13
M-622.1-00003
IE Electrical Equipment Air Handling Unit Layout
SGK05A(3-4-1) & SGK05B(3-4-1)
W16
M-12AL01
Piping & Instrumentation Diagram Auxiliary Feedwater
System
28
M-12GK01
Piping & Instrumentation Diagram Control Building H.V.A.C. 13
M-12GK02
Piping & Instrumentation Diagram Control Building H.V.A.C. 22
M-12GK03
Piping & Instrumentation Diagram Control Building H.V.A.C. 20
M-13GK01
Small Piping Isometric Room Coolers And Compressors
Vents And Drains - Aux. Bldg.
14
M-1H1521
Heating, Ventilating, & Air Cond. Auxiliary Building El.
204.7-6 Area 2
9
Condition Reports
106157
106725
106740
Work Orders
15-400229-001
15-406641-019
15-407224-000
16-417261-000
Miscellaneous
Number
Title
Revision/Date
16-0044
Wolf Creek Nuclear Operating Corporation - Essential
Required Reading
July 21, 2016
APF 21-001-02
Control Room Turnover Checklist
32
STS AL-102
MDAFW Pump B Inservice Pump Test
Performed
August 10, 2016
STS AL-210B
MDAFW Pump B Inservice Check Valve Test
Performed
August 10, 2016
A-16
Section 1R20: Refueling and Other Outage Activities
Procedures
Number
Title
Revision
Scaffold Construction and Use
24
Outage Risk Management
18A
GEN 00-008
RCS Level Less Than Reactor Vessel Flange Operations
30
GEN 00-009
Refueling
38
Condition Reports
107125
107138
Miscellaneous
Number
Title
Revision
APF 22B-001-04 Mode 4
8
APF 22B-001-05 Mode 5 Loops Filled
12
APF 22B-001-06 Mode 5, Loops Not Filled OR Mode 6 RCS Inventory
Between Reactor Vessel Flange (indicated Level of 100.1
In.) AND 23FT. Above Vessel Flange (Indicated Level of
376 In.)
10
APF 22B-001-07 Mode 5 or 6, RCS Lowered Inventory (Indicated Level At Or
Below 100.1 in. And Higher than 3 Ft. Below the Reactor
Vessel Flange) OR RCS Reduced Inventory - Below 3 Ft.
Below Vessel Flange (indicated Level of <64.1 In.)
9
APF 22B-001-08 Mode Mode 6 23ft. Above Vessel Flange (Indicated Level
376.0) and Core Alterations
9
APF 22B-001-09 No Mode - Defueled
9
APF 22B-001-10 Shutdown Safety Function Status & Assessment Summary
9
Section 1R22: Surveillance Testing
Procedures
Number
Title
Revision
ALR 117
0
Program Plan For Containment Leakage Measurement
15
RCS Unidentified Leak Rate Monitoring Program
5
A-17
Procedures
Number
Title
Revision
OFN BB-007
RCS Leakage High
18
STN AP-102
NSAFP Full Flow Test
7
STS BB-006
RCS Water Inventory Balance Using the NPIS Computer
14
STS CR-001
Shift Log for Modes 1, 2, & 3
97
STS IC-211A
Actuation Logic Test Train A Solid State Protection System
36A
STS MT-008
[Steam Generator] Spring Loaded Safety Valve Settings
25
SYS KU-121
Energizing NB01 From Station Blackout Diesel Generators
4
SYS KU-124
SBO Generator Local or Manual Operation
2
Drawings
Number
Title
Revision
M-12AB02
Piping & Instrumentation Diagram Main Stream System
16
M-12BB01
Piping & Instrumentation Diagram Reactor Coolant System
12
Condition Reports
95553
105668
106763
106804
106822
106859
106862
106867
Work Orders
15-406204-000
15-406207-000
15-406208-000
15-406209-000
15-406210-000
15-406211-000
15-406212-000
15-406213-000
16-411417-000
Miscellaneous
Number
Title
Revision/Date
52218
Event Notification Report: Technical Specification Required
Shutdown
September 2,
2016
M-022-00001
Station Blackout Diesel Generator Kohler Instruction
Manual
W02
A-18
Section 1EP2: Alert Notification System Testing
Miscellaneous
Number
Title
Revision/Date
2014 Tone Alert Radio Audit Report
December 4,
2014
2015 Tone Alert Radio Audit Report
December 2,
2015
ANS Report
WCNOC REP-10 Design Review Report
May 7, 2008
EPP 06-019
Alert and Notifications System Sirens
9
EPP 06-022
Tone Alert Radio Maintenance/Compensating Measures
5A
Section 1EP3: Emergency Response Organization Augmentation Testing
Procedures
Number
Title
Date
14-Q4
Quarterly Callout Test
December 14, 2014
15-Q1
Quarterly Callout Test
February 10, 2015
15-Q2
Quarterly Callout Test
June 17, 2015
15-Q3
Quarterly Callout Test
September 30, 2015
15-Q4
Quarterly Callout Test
December 13, 2015
16-Q1
Quarterly Callout Test
March 28, 2016
Drill
Unannounced Callout Drill Report
May 4, 2016
Section 1EP5: Correction of Emergency Preparedness Weaknesses and Deficiencies
Procedures
Number
Title
Revision/Date
AI 26A-003
Regulatory Evaluations (Other Than 10CFR50.59)
16
AP 06-002
Radiological Emergency Response Plan
18
AP 06-004
Equipment Important to Emergency Response
4
Emergency Planning Responsibilities
13
Emergency Response Duties and Responsibilities
15
Corrective Action Program
22a
EPP 06-009
Drill and Exercise Requirements
10
A-19
Procedures
Number
Title
Revision/Date
Annual Emergency Planning Review; includes:
Annual Evacuation Time Estimate Update Review
Annual On-Shift Staffing Analysis Review
December 8, 2014
Annual Emergency Planning Review; includes:
Annual Evacuation Time Estimate Update Review
Annual On-Shift Staffing Analysis Review
December 7, 2015
Condition Reports
85703
86306
88447
89360
89606
89831
90728
91773
94541
94739
95958
96306
97232
97396
97410
100702
101392
101484
101650
101858
101859
102885
105010
106171
106177
106178
106230
106223
Miscellaneous
Number
Title
Date
15-03-EP
Quality Assurance Audit Report (Emergency
Preparedness)
June 29, 2015
15-SA-01
Semi-Annual Health Physics Drill
February 15, 2015
15-SA-02
Semi-Annual Health Physics Drill
July 28, 2015
16-05-EP
Quality Assurance Audit Report (Emergency
Preparedness)
June 21, 2015
16-SA-01
Semi-Annual Health Physics Drill
February 17, 2016
16-SA-02
Semi-Annual Health Physics Drill
June 22, 2016
Drill
2015 Site Medical Drill
September 17, 2015
Drill
2016 Site Medical Drill
July 13, 2016
QA-2015-0151
Assessment: E-Plan Drill Performance Observations
December 11, 2015
QA-2016-0213
Assessment: E-Plan Drill Report Review
June 29,, 2016
QH-2014-0916
Quick Hit Review: NRC Performance Indicator
November 20, 2014
QH-2014-0919
Quick Hit Review: Emergency Planning New Rule
Implementation
November 4, 2014
QH-2015-1004
Quick Hit Review: Fukushima Response
Implementation Lessons Learned Workshop
March 16, 2015
A-20
Miscellaneous
Number
Title
Date
QH-2016-1252
Quick Hit Review: 2015 Industry HAB Evaluated
Exercises
March 16, 2016
QS-2014-0727
Assessment: Fourth Quarter Emergency Planning
Department Assessment
December 30, 2014
QS-2015-0102
Surveillance: TSC Readiness
April 13, 2015
QS-2015-0134
Surveillance: August 11 ERO Drill
August 31, 2015
QS-2015-0145
Surveillance: Security Event Response
November 4, 2015
QS-2015-1411
Surveillance: 08/11/2015 EPlan Drill
August 20, 2015
QS-2016-1565
Surveillance: Emergency Siren
January 12, 2016
Review
Letters of Agreement
December 15, 2015
Test
Monthly Communications Test
November 2014
through July 2016
Condition Reports
85703
86306
88447
89360
89606
89831
90728
91773
94541
94739
95958
96306
97232
97396
97410
100702
101392
101484
101650
101858
101859
102885
105010
106171
106177
106178
106230
106223
Section 1EP6: Drill Evaluation
Procedures
Number
Title
Revision
EPP 06-006
Protective Action Recommendations
9
Condition Reports
106425
Miscellaneous
Number
Title
Revision/Date
2016 E-Plan Schedule
June 6, 2016
77899
Scheduled Offering Roster - Simulator LR4414101
0
A-21
Miscellaneous
Number
Title
Revision/Date
Shift Engineer Simulator Performance Evaluation Summary
Sheet - SM Time for New Shift Manager Quals -
LR4414101
0A
E-Plan Simulator Performance Evaluation Summary Sheet
- SM Time for New Shift manager Quals - LR4414101
2
APF 06-002-01
Emergency Action Levels
17A
EPF 06-007-01
Wolf Creek Generating Station Emergency Notification -
August 11, 2016
12E
LR4407001
Cycle 17-1 Practice CPE
1
LR4414101
SM Time For New Shift Manager Quals
0
Regulatory Assessment Performance Indicator Guideline
7
Scenario 16-11
2016 Biennial Requalification Exam
0
Scenario 16-12
Biennial Requalification Exam
0
Section 4OA1: Performance Indicator Verification
Procedures
Number
Title
Revision
AI 26A-004
Emergency Planning Performance Indicators
8
Condition Reports
107112
Miscellaneous
Number
Title
Revision/Date
MSPI Derivation Report
July 2016
BG-07
MSPI Unavailability For Chemical & Volume Control
System BG-07, Train A Data
BG-07
MSPI Unavailability For Chemical & Volume Control
System BG-07, Train B Data
System Health Report
April 1, 2016
through June 30,
2016
EM-01
MSPI Unavailability For High Pressure Coolant Injection
System EM-01, Train A Data
A-22
Miscellaneous
Number
Title
Revision/Date
EM-01
MSPI Unavailability For High Pressure Coolant Injection
System EM-01, Train B Data
EG-01
MSPI Unavailability For Component Cooling Water
System EG-01, Train A Data
EG-01
MSPI Unavailability For Component Cooling Water
System EG-01, Train B Data
Regulatory Assessment Performance Indicator Guideline 7
Section 4OA3: Event Follow-Up
Procedures
Number
Title
Revision
ALR 00-098D
15A
ALR 00-098B
14
ALR 00-098E
Seismic Recorder On
15
APF 06-002-01
Emergency Action Levels
17A
OFN SG-003
Natural Events
30
Condition Reports
106904
Miscellaneous
Number
Title
Revision/Date
APF 20-002-01
Post-Trip/Event Review Data Package
September 2,
2016