ML16154A801

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Insp Repts 50-269/95-09,50-270/95-09 & 50-287/95-09 on 950430-0527.Deviations Noted.Major Areas Inspected:Plant Operations,Surveillance Testing,Maint Activities,Onsite Engineering & Technical Assistance & Plant Support
ML16154A801
Person / Time
Site: Oconee  
Issue date: 06/21/1995
From: Crlenjak R, Harmon P
NRC OFFICE OF INSPECTION & ENFORCEMENT (IE REGION II)
To:
Shared Package
ML16154A799 List:
References
50-269-95-09, 50-269-95-9, 50-270-95-09, 50-270-95-9, 50-287-95-09, 50-287-95-9, NUDOCS 9507120082
Download: ML16154A801 (22)


See also: IR 05000269/1995009

Text

REGU

lUNITED

STATES

NUCLEAR REGULATORY COMMISSION

REGION II

J 0101

MARIETTA STREET, N.W., SUITE 2900

ATLANTA, GEORGIA 30323-0199

Report Nos.: 50-269/95-09, 50-270/95-09 and 50-287/95-09

Licensee:

Duke Power Company

422 South Church Street

Charlotte, NC

28242-0001

Docket Nos.:

50-269, 50-270 and 50-287

License Nos.:

DPR-38, DPR-47 and DPR-55

Facility Name: Oconee Units 1, 2 and 3

Inspection Conducted: April 30 - May 27, 1995

Inspectors:

_

_

_

_

_

_

__

_

_

'4>z /

P. E. Harmon, Senior Re;Ydent Inspector

Date Signed

W. K. Poertner, Resident Inspector

L. A. Keller, Resident Inspector

P. G. Hum hrey, Resident Inspector

C. W. p

Reactor Inspector

Approved by:

// f

/

R. .

rlenj a(,' Cief

Dte igned

Reactor Projects Branch

SUMMARY

Scope:

This routine, resident inspection was conducted in the areas of

plant operations, surveillance testing, maintenance activities,

onsite engineering and technical assistance, plant support,

inspection of open items, and review of licensee event reports.

Inspections were performed during normal and backshift hours and

on weekends.

Results:

An Inspector Followup Item was identified in Plant Operations

regarding the inability to consistently activate the Standby

Shutdown Facility (SSF) within the time criteria, paragraph 2.f.

The licensee's efforts in cleaning the Unit 2 Main Condenser was

considered a strength, paragraph 2.d.

Within the area of Engineering, two deviations were identified.

The first deviation involved the failure to identify the solenoid

valves which operate the Main Steam Stop Valves as safety-related,

paragraph 6.b. The second deviation involved the failure to

perform a fatigue analysis for portions of reactor coolant system

auxiliary piping, paragraph 6.f.

ENCLOSURE 2

9507120082 950621

PDR

ADOCK 05000269

G

PDR

REPORT DETAILS

1.

Persons Contacted

Licensee Employees

  • B. Peele, Station Manager
  • E. Burchfield, Regulatory Compliance Manager
  • D. Coyle, Systems Engineering Manager

J. Davis, Engineering Manager

T. Coutu, Operations Support Manager

  • W. Foster, Safety Assurance Manager
  • J. Hampton, Vice President, Oconee Site

D. Hubbard, Maintenance Superintendent

C. Little, Electrical Systems/Equipment Manager

J. Smith, Regulatory Compliance

  • G. Rothenberger, Operations Superintendent

R. Sweigart, Work Control Superintendent

Other licensee employees contacted included technicians, operators,

mechanics, security force members, and staff engineers.

  • Attended exit interview.

2. Plant Operations (71707)

a.

General

The inspectors reviewed plant operations throughout the reporting

period to verify conformance with regulatory requirements,

Technical Specifications (TS), and administrative controls.

Control room logs, shift turnover records, temporary modification

log, and equipment removal and restoration records were reviewed

routinely. Discussions were conducted with plant operations,

maintenance, chemistry, health physics, instrument & electrical

(I&E), and engineering personnel..

Activities within the control rooms were monitored on an almost

daily basis.

Inspections were conducted on day and night shifts,

during weekdays and on weekends. Inspectors attended some shift

changes to evaluate shift turnover performance. Actions observed

were conducted as required by the licensee's Administrative

Procedures. The complement of licensed personnel on each shift

inspected met or exceeded the requirements of TS. Operators were

responsive to plant annunciator alarms and were cognizant of plant

conditions.

Plant tours were taken throughout the reporting period on a

routine basis. During the plant tours, ongoing activities,

housekeeping, security, equipment status, and radiation control

practices were observed.

2

b.

Plant Status

Unit 1 commenced the reporting period in cold shutdown for a

control rod drive mechanism refurbishment outage. The unit was

placed back in service on May 9, 1995, and continued to operate at

full power for the remainder of the reporting period.

Unit 2 operated near full power until May 4, 1995, when the unit

was shut down for extraction steam bellows replacement inside the

main condenser. The work was completed and the unit returned to

power on May 23, 1995.

Unit 3 operated at full power throughout the inspection period.

On May 24, 1995, the unit experienced a dropped control rod which

required a power reduction to approximately 50 percent. The unit

returned to full power the next day.

c.

Unit 1 Outage

Unit 1 shutdown on April 27, 1995, to perform control rod drop

time testing (Inspection Report 269,270,287/95-06).

As a result

of the testing, the licensee identified 5 control rods with drop

times greater than the Technical Specification (TS) limit of 1.66

seconds and commenced a cooldown to cold shutdown for a control

rod drive mechanism (CRDM) refurbishment outage. During the

outage the reactor vessel level was maintained between 80 inches

and 100 inches on the reactor vessel level indicator (LT-5).

The

licensee refurbished 9 CRDMs during the outage. These included

the 5 CRDMs that exceeded the TS limit of 1.66 seconds and 4 CRDMs

that exceeded 1.5 seconds. The refurbishment consisted of

replacing the CRDM thermal barriers with modified thermal

barriers. The slow rod drop times were the result of stuck ball

check valves. Modified thermal barriers have larger clearances in

the ball check area. The sticking ball check valves are a

previously identified problem which gets progressively worse.

Accordingly, the licensee has implemented a program to refurbish

CRDMs with drop times greater than 1.4 seconds during refueling

outages.

The licensee determined that the total rod worth and rod worth

versus time were within the Final Safety Analysis Report (FSAR)

assumptions assuming the slow rod drop times. The licensee plans

to submit a Licensee Event Report in accordance with 1OCFR50.73.

The CRDM refurbishment activity was completed on May 8, 1995, and

Unit 1 was returned to service on May 9, 1995. The inspectors

followed the outage activities and monitored plant conditions on a

routine basis. All activities observed were satisfactory.

Ill3

d.

Unit 2 Outage

Ruptured extraction steam piping bellows inside the main condenser

resulted in the shutdown of Unit 2 for approximately 19 days for

repairs. The problem was originally thought to be a ruptured "E"

bleed expansion bellows in the "A" water box. However, after the

unit was shut down and an inspection performed on all three of the

water boxes, the damage was found to be more extensive. As a

result, the expansion bellows were replaced on all of the

extraction lines (24) inside the condenser (A, B, and C Water

Boxes) and 2 bellows were replaced outside the condenser. After

the bellows replacement, a high pressure washdown and cleanup of

the condenser was performed and the Auxiliary Feedwater piping

that takes suction from the bottom of the condenser hotwell was

flushed. This was followed by a walkdown and closeout of the

condenser on May 19, 1995.

The licensee expanded their Foreign Material Exclusion (FME)

program to include the condenser and associated equipment. A

detailed procedure, Unit 2 Condenser Hotwell Cleaning Plan, was

prepared which included a step-by-step activity and documentation

for the completion and cleanup. It further included a final

inspection and approval of the completed effort by the following

organizations: Maintenance, Quality Assurance, Operations,

Chemistry, and a signoff by the project leader. The inspectors

performed an inspection of the condenser on May 18 and 19, 1995,

and determined the equipment to have been thoroughly cleaned. The

inspectors concluded that the licensee's inclusion of the Unit 2

Main Condenser in their FME program, and their thorough cleaning

efforts, was a strength.

e.

Unit 3 Dropped Control Rod

On May 24, 1995, Unit 3 experienced a dropped control rod from

full power. During the performance of the monthly control rod

movement performance test (PT/3/A/600/15), rod 2 group 1 was being

exercised to investigate a pre-existing problem with this rod's

100 percent withdrawn limit light. After the rod was placed on

its auxiliary power supply, the operators were attempting to pull

it to its 100 percent position when the rod dropped into the core.

The Integrated Control System (ICS) was in manual for this

evolution. If the ICS had been in automatic when the rod dropped,

there would have been an automatic runback to 55 percent power at

5 percent per minute. Since ICS was in manual, the automatic

runback could not take place. The operators entered AP/3/A/600/15

(Dropped Control Rods) and Reactor Power was manually reduced to

less than 60 percent per the procedure. The licensee attempted to

discover the cause of the dropped rod, but was not successful.

The rod was subsequently pulled back to within its group average

and then the complete group was withdrawn to 100 percent. The

licensee then completed the control rod movement performance test

and slowly returned to full power. The inspectors responded to

4

the control room following the dropped rod and observed the

recovery efforts. All activities observed were satisfactory.

f.

Standby Shutdown Facility (SSF) Activation Time

During the inspection period the inspectors observed drills

conducted by the licensee designed to verify that operators could

man and activate the SSF facility within the time assumed in

associated analysis.

The SSF is designed as a standby system for use under extreme

emergency conditions. The SSF is provided as an alternate means

to achieve and maintain hot shutdown conditions for up to 72 hours8.333333e-4 days <br />0.02 hours <br />1.190476e-4 weeks <br />2.7396e-5 months <br />

on all three units, following postulated fire, sabotage, or

flooding events.

Loss of all other station power is assumed for

each event. The licensee has taken credit for the SSF to meet the

requirements of 10 CFR 50, Appendix R, and the Station Blackout

Rule (1OCFR50.63).

The SSF is designed in part to: (1) maintain

a minimum water level above the reactor core, with an intact

Reactor Coolant System (RCS); (2) maintain reactor coolant pump

seal cooling; and (3) assure natural circulation and core cooling

by maintaining sufficient secondary side cooling water. RCS

inventory and seal cooling is provided by the SSF Reactor Coolant

Makeup (RCMU) pumps (one per unit).

Core cooling is provided by

the SSF Auxiliary Service Water (ASW) pump which supplies lake

water to the steam generators of the affected unit(s).

Power for

these pumps is provided by the SSF diesel generator. The Oconee

Probability Risk Assessment (PRA) results indicate that the

probability of an SSF event is about 3.0 E-04 per year.

The SSF is normally unmanned and requires manual activation by

operations personnel.

SSF activation includes starting the diesel

generator, SSF ASW pump, RCMU pump(s), and manipulating various

breakers and valves to establish flow paths. The SSF must be

activated within a certain time in order to prevent Reactor

Coolant Pump (RCP) seal damage/failure, or voiding in the RCS such

that natural circulation is lost. RCP seal failure creates a Loss

Of Coolant Accident (LOCA), an accident the SSF is not designed to

mitigate. Therefore, as part of the SSF Emergency Operating

Procedure (AP/O/A/1700/25), SSF makeup flow to the RCP seals and

ASW flow to the steam generators are required to be established

within 10 minutes.

On July 27, 1994, the licensee performed a drill that was written

with the intent of showing how plant personnel and equipment were

prepared to cope with mitigation of an Appendix "R" type event.

The drill scenario included a requirement to activate the SSF.

The SSF activation time for this drill was approximately 28

minutes. During this drill, it took approximately 8 minutes for

the personnel to acknowledge the need to activate the SSF and 20

additional minutes before the SSF was in service.

5

Subsequent to this drill, the inspectors noted that previous

activation times were non-conservative due to the failure to

include the time required for valve stroking (valves were not

actually stroked during the drills, rather the valves were assumed

to go instantly open or closed).

Due to the lack of

documentation, it was impossible to determine if factoring in the

valve stroke times into the previous tests would have resulted in

test failures. The licensee agreed that valve stroke times should

be included in any future drill/test used to verify the SSF could

be placed into operation within 10 minutes. The licensee

concluded that valve stroke times would add 56 seconds to the Unit

1 activation time, 75 seconds to Unit 2, and 58 seconds to Unit 3

(NRC Inspection Report 50-269,270,287/94-38).

On December 7, 1994, the inspectors observed a special drill which

was conducted to verify that the SSF could be placed in service

within 10 minutes with valve stroke times included. The results

of the drill were as follows:

Unit 1-9:46, Unit 2-10:48, Unit 3

10:00 (times in minutes:seconds).

A conference call was held between the licensee, Region II, and

NRR to discuss the drill failures. During the call the licensee

maintained that the recent drill failures indicated the need for

additional operator training and procedural enhancements, but did

not indicate that the SSF was inoperable. The licensee

subsequently conducted additional operator training and revised

the SSF activation procedure. The licensee then performed another

3 unit drill scenario on December 20, 1994, similar to the one

conducted on December 7, 1994. The results of the drill were as

follows:

Unit 1-6:17, Unit 2-6:05, Unit 3-6:18.

The licensee indicated that they would continue to perform

periodic drills in order to test all shift personnel. Based on

the December 20, 1994, drill, the inspectors concluded that the

licensee's training and procedures had improved sufficiently to

provide reasonable assurance that the SSF could be manned within

10 minutes.

On May 24, 1995, the inspectors observed the first drill conducted

since the December 20, 1994, drill.

This was a single unit drill

utilizing operating shift personnel.

The drill was unsuccessful

in that the activation times were in excess of 10 minutes (10

minutes 18 seconds for RCMU, 11 minutes 4 seconds for ASW).

The

primary problem noted in this drill was the amount of time

required by the breaker operator to complete the required breaker

manipulations and notify the SSF control room operator. The

licensee initiated Problem Investigation Process (PIP) report

95-0596 to disposition the drill failure. As of the end of the

inspection period this evaluation was not complete. On May 25,

1995, a follow-up drill was performed successfully. The

inspectors continue to be concerned with the licensee's inability

to consistently meet the SSF activation time requirements.

II

6

The inspectors concluded that it is physically possible to

man the SSF within 10 minutes, but there is very little margin

for error. The inspectors will continue to follow the licensee's

efforts to ensure that training for SSF activation is adequate.

This matter is identified as Inspector Followup Item (IFI)

50-269,270,287/95-09-01: SSF Activation Time.

Within the areas reviewed, an IFI was identified regarding the

licensee's inability to consistently meet the SSF activation time

criteria, paragraph 2.f. The licensee's efforts in cleaning the Unit 2

Main Condenser was considered a strength, paragraph 2.d. All other

activities observed were satisfactory.

3.

Maintenance and Surveillance Testing (62703 and 61726)

a.

Maintenance activities were observed and/or reviewed during the

reporting period to verify that work was performed by qualified

personnel and that approved procedures adequately described work

that was not within the skill of the craft. Activities,

procedures and work orders (WO) were examined to verify that

proper authorization and clearance to begin work was given,

cleanliness was maintained, contamination exposure was controlled,

equipment was properly returned to service, and limiting

conditions for operation were met.

Maintenance activities observed or reviewed in whole or in part

are as follows:

(1) Perform Lubrication PM U2 TDEFWP (Annual), WO 95015174

The inspectors observed lubrication of the Unit 2 Turbine

Driven Emergency Feedwater Pump (TDEFWP) on May 17, 1995.

The activity was performed per maintenance procedure,

MP/0/A/1840/040, Pumps - Miscellaneous Components

Lubrication. Documentation was complete and work was

performed according to the procedure. The work was in

accordance with acceptable standards.

(2) Inspect/Clean 2FDW-FE-2B 'B' Venturi Flowmeter, WO 95034150,

Task 01

The inspector observed maintenance activities during the

removal and cleaning of the Unit 2, 'B' feedwater venturi.

The effort was in response to a high pressure differential

observed across the 2B Feedwater Control Valve during plant

operation. The problem was suspected to be a buildup of

magnetite in the feedwater nozzles in the steam generators.

Craftsmen were utilizing procedures, and documentation was

current for the work in progress. Torquing Procedure,

MP/0/A/1800/003, was included in the work package for re-

7

assembly of the equipment. The activity was performed to

acceptable standards.

(3) Power Range NI Calibration, WO 95033961

The inspectors observed Unit 2 nuclear instrumentation

calibration on May 23, 1995, during power ascension. The

activity was per IP/0/0301/003T, Reactor Protective System

Power Range Calibration At Power Instrument Procedure.

The

equipment was removed and returned to service in accordance

with instrument procedure IP/0/A/0305/015, Nuclear

Instrumentation RPS 'Removal From And Return To Service For

Channels A,B,C, and D. The effort was performed according

Ito the procedures and to acceptable standards.

(4) Motor Driven Emergency Feedwater (MDEFW) Pump Instrument

Calibration, WO 95031394

The inspectors observed portions of the calibration of the

low pressure service water flow instrument associated with

the 2A MDEFW Pump. The work activity was accomplished in

accordance with approved procedures. No deficiencies were

noted.

(5) Installation of Portable Reactor Building Chilled Water

System from the "B" Reactor Building Cooling Unit (RBCU) Low

Pressure Service Water (LPSW) Header, WO 95003828, Task 04

The installation of this portable chilled water system

allows for accelerated cooldown of the containment building

during unit shutdown, in order to allow work to begin inside

the containment building as soon as possible.

The work was

accomplished in accordance with MP/0/A/3007/050:

Installation, Operation, And Removal - Temporary Cooling Of

Reactor Building. The inspector reviewed the licensee's

10CFR50.59 evaluation associated with this task and

concluded that it was adequate. The inspector verified that

the installation of the temporary piping did not compromise

penetration room integrity. The licensee stated that the

chilled water would not be valved in until after the reactor

was subcritical.

The inspector concluded that the work was

done in accordance with approved procedures and did not

adversely affect plant safety.

b.

The inspectors observed surveillance activities to ensure they

were conducted with approved procedures and in accordance with

site directives. The inspectors reviewed surveillance

performance, as well as system alignments and restorations. The

inspectors assessed the licensee's disposition of any

discrepancies which were identified during the surveillance.

  • II8

Surveillance activities observed or reviewed in whole or in part

are as follows:

(1) Control Rod Drive Trip Time Testing, PT/O/A/0300/01

The inspector observed Unit 2 Control Rod Drive Mechanism

(CRDM) trip time testing on May 22, 1995. The test was

conducted per the procedure and all rod drop times were

within acceptable limits. TS requires that CRDMs fall into

the reactor core at a time not to exceed 1.66 seconds with

the reactor at full flow conditions.

Twelve CRDMs were modified during the reporting period while

Unit 2 was in an outage. Nine additional CRDMs were

modified during the last refueling outage, which brings the

total of Unit 2 modified CRDMs to 21.

The modification was

necessary to eliminate excessive drop times and consisted of

replacing of the thermal barrier with one which has larger

clearances at the ball check. The larger clearances prevent

ball valve sticking, thus allowing the rods to fall into the

reactor core at a faster speed. All activities observed

were satisfactory.

(2) Low Pressure Injection Pump Test - Decay Heat,

PT/2/A/0203/06B

On April 10, 1995, the inspector observed testing and

reviewed the completed documentation of PT/2/A/0203/06B, Low

Pressure Injection Pump Test - Decay Heat .

The test was

performed on the 2B LPI pump while the reactor was at cold

shutdown as required by the procedure. The test was to

demonstrate operability of the pump, identify problem areas

as early as possible, stroke test the discharge check

valves, and perform a partial stroke of the A and B reactor

vessel LPI header check valves. Test results were

determined to be acceptable and the testing activity was

adequate.

(3) Control Rod Drive Trip Time Testing, PT/0/A/0300/01

The inspector observed portions of the Unit 1 CRDM testing

performed on May 9, 1995, following an outage to replace 9

CRDMs due to slow drop times. The drop times of the 9 CRDMs

that had been replaced during the outage improved

significantly, with the slowest rod drop time at 1.384

seconds. The slowest rod in the core dropped in 1.420

seconds. During performance of the test, Rod 10 Group 5 did

not record a drop time. Investigation by the licensee

determined that the position indication switch was

defective. The licensee replaced the switch and

successfully retested the rod.

9

(4) Keowee Hydro Emergency Start Test, PT/0/A/0620/16

The inspector observed the subject test on May 24, 1995.

This annual test is required by TS 4.6.2. The purposes of

this test were: (1) demonstrate operability of each Keowee

Hydro Unit's (KHU) emergency start circuitry from each

control room; (2) demonstrate each KHU will reach rated

speed and voltage within 23 seconds of emergency start

initiation; and (3) demonstrate each KHU can supply greater

than 25 MW to the system grid. The inspector reviewed the

test procedure, attended the pre-test briefing, and observed

the test from the Keowee Control Room. The inspector

concluded that all test acceptance criteria were met and

that procedural compliance was adequate.

Within the areas reviewed, licensee activities were satisfactory.

4.

Onsite Engineering (37551)

During the inspection period, the inspectors assessed the effectiveness

of the onsite design and engineering processes by reviewing engineering

evaluations, operability determinations, modification packages and other

areas involving the Engineering Department.

a.

Unit 2 Feedwater Control Pressures

During the Unit 2 outage for condenser repairs, an investigation

of a problem with high pressure differential across the 2B

Feedwater Control Valve was performed. Main feedwater spray

nozzle N in the 2A steam generator header ring was evaluated and

the results indicated a magnetite buildup of approximately 0.070

inches in the inside diameter of the holes measured. Each steam

generator has a total of 32 Feedwater spray nozzles with 82 holes

each that were originally drilled to a diameter of 0.188 inches.

The licensee decided to restart the unit and change the feedwater

chemistry in an effort to eliminate the magnetite buildup. The

changes included: (1) raising the ammonia concentration from 400

600 ppb to 1500 ppb; (2) adding dimethylamine on a continuous

basis at <1 ppm; and (3) adding a mixture of dimethylamine and

trimethylamine on a continuous basis at <1 ppm. The effects of

the chemical addition will be evaluated by monitoring feedwater

system pressures.

Within the areas reviewed, licensee activities were satisfactory.

5.

Plant Support (71750 and 40500)

The inspectors assessed selected activities of licensee programs to

ensure conformance with facility policies and regulatory requirements.

During the inspection period, the areas of Radiological Controls,

Physical security and Fire protection were reviewed.

10

a.

Unit 3 Fire Drill

The inspectors observed a fire drill on May 16, 1995. The drill

was for a simulated fire within Unit 3 at the stator coolant pump

in the basement level of the Turbine Building. A total number of

14 fire brigade members responded to the fire. The simulated fire

involved the 600 volt pump motor and a maximum of 0.5 gallons of

lube oil.

After the drill was completed, the licensee evaluated the activity

with the team members. The critique considered the area selected

as a command post, personnel accountability, communications with

the main control room, type of extinguisher utilized, and the

approach taken by the team. The inspector concluded that the

drill constituted effective training, and that the licensee's

self-assessment of the drill was adequate.

b.

Equipment Located Adjacent to Unit 3 Main Transformer

The inspectors questioned the licensee's decision to park a

semi-trailer (box type) adjacent to the Unit 3 main transformers.

The trailer contained equipment necessary for transformer

re-blocking and oil purification. The spare transformer was

scheduled to be reworked and put in service when Unit 3 is taken

off-line June 6, 1995, for its refueling outage, in order to make

another transformer available for re-blocking and oil

purification. Although the transformers were not safety-related,

the inspectors were concerned that the trailer could collide with

the transformer as a result of high winds, maneuvering, or other

type of accident, and cause a loss of generator output and

subsequent unit trip.

The inspectors learned that associated risks had been evaluated by

the licensee prior to locating the trailer in that area and that

the activity was allowed per Oconee Nuclear Site Directive 1.3.7,

Conduct Of Operations In The Switchyard. The entire trailer

moving process was coordinated with the Operations staff and was

under the control of the Switchyard Coordinator. The process was

well planned and controlled.

No violations or deviations were identified.

6.

Inspection of Open Items (92901, 92902 and 92903)

The following open items were reviewed using licensee reports,

inspection record review, and discussions with licensee personnel, as

appropriate:

11

a.

(Closed) Deviation 50-269,270,287/93-31-01:

Potential Single

Failure Could Blowdown Both Steam Generators

This deviation involved a postulated break in the line downstream

of the motor operated valves from the steam supply to the

Auxiliary Steam header (MS-24 and MS-33). As the licensee

maintained both MS-24 and MS-33 open for the unit supplying

auxiliary steam, the postulated break would potentially result in

the simultaneous blowdown of a unit's steam generators. This was

contrary to statements contained in Section 10.3.2 of the FSAR

that indicated the arrangement of the isolation valves on

Auxiliary Steam lines (i.e., MS-24 and 33) prevents blowdown of

both steam generators from a single leak in the system. The focus

of Deviation 93-31-01 was the blowdown of both steam generators

through the auxiliary steam header, although the issue was also

relevant to a break downstream of MS-82 and MS-84 (TDEFWP steam

header isolation valves).

In a letter dated February 24, 1994, the licensee agreed that the

deviation existed, but maintained that the vulnerability in

question did not constitute an Unreviewed Safety Question (USQ)

because it was bounded by the FSAR Chapter 15 steam line break.

The only corrective action proposed in this response was to change

the wording in the FSAR to indicate that certain pipe breaks could

blow down both steam generators. Due to continued NRC concerns,

the licensee agreed to provide the NRC their engineering analysis

that provided the basis for concluding that there was no USQ, and

that no corrective action was necessary (other than amending the

FSAR).

The office of NRR subsequently reviewed the licensee's

analysis and determined that the postulated event involved an USQ

per 10 CFR 50.59, in that it presented the possibility for an

accident of a different type than any evaluated in the safety

analysis report.

On January 6, 1995, the licensee was provided with the results of

NRR's review. On January 9, 1995, a conference call was held

between Region II, NRR and the licensee. During the call the

licensee stated that they would conservatively consider the

vulnerability to be an USQ, pending further review. The

licensee's immediate corrective actions were to close one of the

two steam supply valves to the common steam headers (Auxiliary

Steam and Turbine Driven Emergency Feedwater supply) on all 3

units. This effectively eliminated the vulnerability in question.

In a letter dated February 8, 1995, the licensee submitted a

revised response to the deviation. In this response the licensee

indicated that this potential scenario had been identified to the

NRC in a High Energy Line Break (HELB) submittal dated April 25,

1972. The HELB submittal was reviewed and found acceptable by the

NRC, as documented in the Oconee plant licensing safety

evaluation. Based on this additional information, the NRC

concluded that this potential failure scenario did not constitute

an USQ.

12

The revised deviation response also indicated that the licensee

would perform an engineering analysis, using probabilistic risk

analysis (PRA), to determine the safest configuration of valves

MS-24, MS-33, MS-82, and MS-84 during normal operation. On April

20, 1995, the licensee determined that future steam lineups would

maintain either MS-24 or MS-33 closed, and both MS-82 and MS-84

open. The inspector reviewed the FSAR changes relative to this

issue and concluded that they effectively resolved the deviation.

b.

(Closed) Unresolved Item 50-269,270,287/93-30-02:

Main Steam Stop

Valve (MSSV) Requirements

On November 3, 1993, the Unit 1 Main Steam Stop Valves (MSSVs)

inadvertently closed due to an electrical fault.

When the fault

cleared, 2 of the 4 MSSVs did not reopen per design.

This

resulted in a severe secondary transient, which included

depressurizing the "B" Once Through Steam Generator (OTSG) to the

point where all the feedwater in the steam generator flashed to

steam, and a resultant dryout of the steam generator. The plant

was manually tripped due to low steam generator water level.

The

licensee's post trip investigation revealed that the failure of

the MSSVs to reopen was due to stuck test solenoid valves (channel

B), caused by Electro-Hydraulic Control (EHC) system fluid residue

formation internal to the solenoids. The licensee also discovered

that they were not meeting the solenoid vendor's recommendations

for cycling the solenoid valves (both channels A and B), and that

the lack of cycling resulted in the EHC fluid residue formation

which ultimately led to the test solenoid failures. The resident

staff questioned why these test solenoid valves were not safety

related since they were the backup, or channel B, actuation

devices for closing the MSSVs. The licensee subsequently stated

that the test solenoids were not required to be safety-related.

However, the master trip solenoid valves and disk dump valves

(channel "A") were definitely required to be safety-related but

had never been identified or treated as such.

The NRC subsequently determined that both the Channel "A" and "B"

solenoid valves should have been classified as safety-related.

This determination was based on the current licensing basis for

Oconee. The original licensing basis for Oconee only identified

the reactor coolant system, reactor vessel internals, reactor

building, engineered safeguards systems, and emergency electric

power sources as essential systems and components. The MSSV

solenoids would not have been classified as safety-related under

this criteria. However, evolutionary requirements, specifically

the licensee's commitments to Generic Letter 83-28, Section 2.2,

would result in these solenoid valves being classified as safety

related. Section 2.2 of the licensee's generic letter response

indicates that portions of the Main Steam System from the steam

generator to, and including, the first normally closed or

automatic isolation valve, are safety-related. Failure to

classify the MSSV solenoid valves (Channels A and B) as safety-

13

related is identified as Deviation 50-269,270,287/95-09-02:

Generic Letter 83-28 Commitment Relating to MSSV Solenoids.

c.

(Closed) Violation 50-287/93-24-01: Inadequate Post Modification

Test Program

This violation identified that an adequate post modification test

program had not been established following a modification of the

Unit 3 Load Shed Channel 1 circuitry resulting in the channel

being inoperable from March 1987 to August 1993.

The licensee corrected the specific wiring discrepancy identified.

Enhancements had been implemented to the modification and testing

program prior to this violation being issued. These enhancements

included the development of a Modification Test Plan and issuance

of Test Acceptance Criteria by design engineering. The licensee

also implemented a configuration control inspection to ensure that

the as-built configuration matched the drawings. This

configuration control inspection identified the subject wiring

discrepancy. Accordingly, this item is considered closed.

d.

(Closed) Violation 50-270/93-21-01: Inadequate Modification

Procedure

This violation identified that the Torque Switch Bypass

Modification procedure for the PORV Block Valve 2RC-4 was

inadequate in that the procedure inadvertently deleted the valve

open indication in the Standby Shutdown Facility.

The inspector determined that the licensee corrected the wiring

discrepancy and counseled the individuals involved in the original

wiring modification. The licensee also circulated the Notice of

Violation response to other individuals responsible for developing

modification packages. This item is closed.

e.

(Closed) Unresolved Item 50-269,270,287/93-30-03: Emergency

Condenser Cooling Water System Requirements

This item questioned the adequacy of isolating the Continuous

Vacuum Priming system from the Condenser Circulating Water system

intake piping. Subsequent to this item being opened, the NRC

conducted a service water inspection and the licensee deleted the

TS requirement that the Emergency Condenser Circulating Water

system be operable with respect to decay heat removal.

Accordingly, this item is considered closed.

f.

(Closed) Unresolved Item 50-269,270,287/94-08-03:

Fatigue

Analysis for RCS Auxiliary Piping

During a visit to Oconee on March 1994, members of the NRC staff

identified an apparent nonconformance with a licensing basis

requirement. Specifically, the Oconee FSAR states that the RCS

II

14

pressure boundary piping including the attachment piping to the

first isolation valve, is required to be designed to USAS B31.7,

Class I standards. However, the staff identified that the

attached piping was designed to USAS B31.7, Class II standards.

As such, the RCS attached piping did not have fatigue analysis as

required by B31.7 I. Unresolved Item 50-269,270,287/94-08-03 was

written to track this issue.

In a letter dated October 3, 1994, the licensee provided the NRC

with the conclusion that a nonconformance did not exist, and the

rationale for that conclusion. In response, NRC concluded in a

letter to the licensee dated April 27, 1995, that the

nonconformance does in fact exist, and that an evaluation should

be performed by the licensee to demonstrate compliance with the

FSAR criteria. FSAR section 3.2.2.1 contains a definition of the

Class I system under the Nuclear Power Piping Code, USAS B31.7.

The definition also contains the statement that the class includes

connection piping up to and including the first isolation valve.

The letter further requested a schedule for either performing the

analysis or additional justification for not performing the

analysis within 60 days of the date of the NRC letter.

This unresolved issue has been determined to be a Deviation from

requirements contained in the FSAR, and will be tracked as

Deviation 50-269,270,287/95-09-03:

Fatigue Analysis for RCS

Auxiliary Piping.

g.

(Closed) Inspector Followup Item 50-269,270,287/93-13-05:

Failure

of Keowee Voltage Regulator

In 1993, several intermittent failures of the Keowee voltage

regulators to switch to Automatic during routine starts occurred.

The root cause could not be identified, but appeared to be due to

an unreliable voltage regulator cam switch. Three failures

occurred on Unit 2 between September 1992 and November 1992.

Failures also occurred three times on Unit 1 between December 1992

and May 1993. The Keowee units were evaluated and considered

Conditionally Operable by Problem Identification Process (PIP)

report 0-093-0385. As a compensatory measure and a condition of

the Operability Determination accompanying the PIP, the Keowee

operator was required to manually verify the position of the cam

switches after the unit was shut down.

After the Conditional Operability was imposed, no further failures

occurred until April 20, 1995, when Unit 1 failed again. At that

time, troubleshooting found that a bad module in the synchronizer

was the root cause of the failures. The module was delivering a

continuous raise pulse instead of an intermittent raise pulse to

the Keowee voltage regulator when attempting to match machine

voltage to grid voltage. This caused the machine voltage to be

driven out of the preset position before the regulator could be

switched to Automatic. The synchronizer for Unit 1 had been

15

replaced with the one from Unit 2 in December 1992. The single

bad module was responsible for the failures on both Keowee units.

These failures would have affected the Keowee unit's ability to

generate to the grid, but not their safety functions. The

Conditional Operability and compensatory measures were closed by

the licensee after the module was replaced and tested. This item

is closed.

h.

(Closed) Escalated Action 91-167:

Failure to Follow

Procedures/Inadequate Procedures

This Notice of Violation and Imposition of Civil Penalties, was

the result of violations identified during inspections which

reviewed the degradation of decay heat removal that occurred on

September 7, 1991, and the over-pressurization of the Low Pressure

Injection (LPI) System piping which occurred on September 19-20,

1991.

This escalated action combined the three apparent

violations identified in NRC Inspection Report 50-269,270,287/91

32.

The inspector reviewed the licensee's commitments as provided

in the response to the above Escalated Action. These commitments

were: (1) provide guidance for changing operating trains while in

decay heat removal and adjusting low pressure service water flows;

(2) increase surveillance frequency of critical parameters during

shutdown operations; (3) reduce the cold shutdown temperature

alarm setpoint to provide for earlier indication of inadequate

decay heat removal; (4) increase control room personnel control

over remote testing of valves in a system that had not been

removed from service; (5) provide supplemental training to

licensed operators on the operating procedures used for shutdown,

startup, and cold shutdown; (6) improve management of control room

workload; (7) identify a single individual as having

responsibility for monitoring critical core parameters;

(8) increase Unit Supervisor oversite of control room activities

that may impact operator performance; (9)

delineate proper chain

of command and communications channels; (10) communicate

management expectations of supervisor and operator

responsibilities; and (11) conduct of pre-job briefings before

performing evolutions that significantly affect plant

configuration.

Based on a review of current plant procedures and other

documentation available at the time of inspection, the inspector

found the licensee had met these commitments. This item is

closed.

Two deviations from commitments were identified. The first deviation

involved the safety-related classification of the solenoid valves used

to actuate the Main Steam Stop Valves (paragraph 6.b). The second

deviation involved the failure to perform a fatigue analysis for certain

portions of RCS auxiliary piping (paragraph 6.f).

16

7.

Review of Licensee Event Reports (92700)

The below listed Licensee Event Reports (LER) were reviewed to determine

if the information provided met NRC requirements. The determination

included:

adequacy of description, compliance with Technical

Specification and regulatory requirements, corrective actions taken,

existence of potential generic problems, reporting requirements

satisfied, and the relative safety significance of each event. The

following LERs were reviewed:

a.

(Closed) LER 270/93-03:

Design Deficiency Results in Technical

Inoperability of the Reactor Coolant Makeup (RCMU) System

The inoperability was due to the RCMU system letdown line orifices

being too small to pass adequate flow during certain Standby

Shutdown Facility (SSF) accident scenarios. With full letdown

flow there would be an increase in Reactor Coolant System (RCS)

volume. Assuming no operator action, no RCS leakage, and little

or no designed leakage through the Reactor Coolant Pump (RCP)

seals, the potential existed to overfill the pressurizer in an SSF

event. Licensee analysis indicated that it would take

approximately nine hours for this scenario to occur. This

vulnerability existed since initial SSF operation and was the

result of a design oversight. The licensee initially compensated

for the vulnerability by adding steps to the SSF Emergency

operating procedure. These changes included the use of the

reactor vessel head vent valves to control pressurizer level

during an SSF event. The TS LCO was exited after these procedure

changes were made. Subsequently, the licensee has eliminated the

vulnerability on Units 1 & 2 by replacing their RCMU letdown

orifices with the appropriately sized orifices. The Unit 3 RCMU

letdown orifice is scheduled to be replaced during the upcoming

refueling outage (3EOC15). The inspector considered the

determination that the RCMU systems were technically past

inoperable to be conservative. Despite the lack of specific

procedural guidance, the inspector concluded that over a 9 hour1.041667e-4 days <br />0.0025 hours <br />1.488095e-5 weeks <br />3.4245e-6 months <br />

time frame mitigating actions would have been accomplished to

prevent the pressurizer from becoming water solid (i.e.,

increasing the cooldown of the RCS in order to shrink the water

volume).

The inspector concluded that the licensee's corrective

actions were acceptable.

b.

(Closed) LER 269-93-05, Inoperable Control Rods Due To Defective

Procedure Results In Technical Specification Violation

Three control rods, 2 in Unit 1 and 1 in Unit 2, initially failed

to meet the TS required drop time during their refueling outages

in January 1993 and March 1992, but were successfully tested prior

to restart.

On April 29, 1993, Unit 2 began a refueling outage which included

rod drop time testing while at hot shutdown. One control rod

17

dropped at approximately 1.9 seconds. The TS limit is less than

or equal to 1.66 seconds. This rod had been identified during the

previous refueling outage as being slow and was repeatedly dropped

until the drop time came within TS limits. As a result of the

Unit 2 rod's performance, the Unit 1 test data was reevaluated and

two rods were declared inoperable on May 4, 1993, while Unit 1 was

at 100% power. Discretionary Enforcement was obtained to continue

operation of Unit 1 until the end of the cycle, ending April 1994.

The slow control rod on Unit 2 was replaced prior to startup.

The Root Cause of this event was determined to be a procedural

deficiency, with a contributing cause of equipment

failure/malfunction. The procedural deficiency was found to be a

change made to the Control Rod Drop Time Test Procedure

(IP/0/A/0330/003A).

Prior to that change, a rod that dropped

slower than 1.40 seconds (but within the TS requirements) was

required to be evaluated by Reactor Engineering. That evaluation

requirement was deleted, such that a rod that dropped at 1.65

seconds was deemed acceptable with no evaluation. The testing of

the slow Unit 2 rod confirmed that a rod which had dropped slower

than 1.40 seconds should be expected to become slower during the

operating cycle. Conversely, rods that dropped with times less

than 1.40 seconds would not exhibit any appreciable slowing during

the cycle. An Engineering evaluation taking this phenomena into

account should have concluded that the two slow (but within the TS

limits) rods on Unit 1 would eventually have exceeded the 1.66

second drop times at some point in the operating cycle. However,

since the criteria to perform evaluations of rods slower than 1.40

seconds had been deleted, an evaluation was not performed.

The corrective actions included removal and repair of the slow

CRDM mechanisms during the next refueling outage, and the revision

of IP/0/A/0330/033A. The inspector determined that the corrective

actions had been completed for this event.

c.

(Open) LER 269/93-06, Design Deficiency Results In A Condition

Outside The Design Basis Of Containment For A Main Steam Line

Break

On June 2, 1993, the licensee determined that the main steam line

break analysis in the FSAR had not taken into account either the

heat added to the event by RCS structural metal, or the continued

feedwater addition.

In February 1980, Inspection & Enforcement (IE) Bulletin (BU)

80-04 required review of the steam line break accident to

determine if the potential for containment overpressure existed as

a result of runout flow from the Emergency Feedwater system or

from other energy sources such as continuation of Main Feedwater

or Condensate flow. The licensee's response dated May 7, 1980,

concluded that containment overpressure would not result from the

described scenario.

18

In 1993, the licensee performed a reanalysis of the scenario and

concluded that containment pressures could reach values in excess

of 2.5 times the containment design pressure. The licensee had

not considered several energy addition sources in their original

BU 80-04 submittal. Those sources included continued addition of

feedwater to the faulted steam generator and heat added by the

passive metal structure of the Reactor Coolant System. The

licensee submitted a Supplemental Response to BU 80-04, dated

August 19, 1993, which detailed the results of the reanalysis.

The Supplemental Response committed to implement modifications to

all three Oconee units to provide automatic isolation of Main

Feedwater during a main steam line break. The implementation of

the modifications is currently scheduled to begin with the

refueling outage for Unit 3, beginning June 1995. Units 1 and 2

are scheduled for modification in October 1995, and March 1996,

respectively.

LER 269/93-06 does not address the role of continued feedwater

supply to the faulted steam generator, but instead describes the

deficiency in the original calculation as a failure to consider

the heat added by the RCS metal structure. Sensitivity studies

indicate that the continued feedwater addition is the major source

of the additional energy considered in the new calculation. The

inspector determined that LER 269/93-06 does not adequately

describe the reasons for the original calculational error or the

corrective actions planned to isolate feedwater. The licensee has

agreed to supplement LER 269/93-06 to clarify the role of

continued feedwater.

Pending implementation of the modification to provide feedwater

isolation and resolution of LER adequacy, this LER will remain

open.

d.

(Open) LER 270/93-02:

Loss of Air Testing For Accumulator Valves

Not Performed Per SOER 88-1

Air operated valves with backup accumulators, High Pressure

Injection valves HP-5 and HP-21, were evaluated as to their

ability to maintain containment isolation during a loss of

instrument air. Acceptance criteria for testing these valves was

a pressure loss of <5 pounds per square inch (psi) over a 15

minute time period for the air accumulator leakage. The test

method and acceptance criteria was questioned by the system

engineer as to the ability of these valves to maintain containment

integrity over a long period of time with a loss of the control

air system.

Oconee engineering evaluated several scenarios with respect to the

effect of the accumulator leakage and determined that the system

pressure would tend to keep the HP-5 valves closed and would tend

to open the HP-21 valves. However, HP-21 was determined to be

operable on Unit 1 because of a relief valve in the system that

19

would prevent system pressure building high enough to open the

valve. Units 2 and 3 would stay closed for a minimum of 3 hours3.472222e-5 days <br />8.333333e-4 hours <br />4.960317e-6 weeks <br />1.1415e-6 months <br />

with the control air accumulator pressure and after that time the

system pressure would tend to open these valves. Units 2 and 3

HP-21 valves were determined to be conditionally operable due to a

change to the Unit 2 and 3 Abnormal Operating Procedure which

requires that these valves be manually closed within 3 hours3.472222e-5 days <br />8.333333e-4 hours <br />4.960317e-6 weeks <br />1.1415e-6 months <br />

following a Small Break Loss Of Coolant Accident and a single

failure of the redundant isolation valve.

Replacement of Units 1, 2, and 3 High Pressure Injection valves,

HP-5 and HP-21, is scheduled to be completed by June 1, 1996.

Therefore, this LER will remain open until the replacement is

completed.

e.

(Closed) LER 270/93-05: Operator Isolated Potential Transformers

On The Wrong Unit Resulting In A Reactor Trip

This LER involved a Unit 2 reactor trip that occurred on August

25, 1993. The unit tripped from 100% power when an operator

mistakenly pulled the generator metering relay and regulating

equipment drawers to the disconnect position on Unit 2 instead of

pulling those on Unit 1.

The immediate corrective actions included controlling the unit

after the trip and closing the Unit 2 potential transformer

drawers. In addition, a telephone in the immediate area of the

equipment was repaired to improve communications between the

control room and operators taking equipment out of service in that

area. Unit designations were attached to the surge

capacitor/potential transformer cubicles for all 3 units. The

inspector verified these corrective actions had been completed.

The licensee completed additional actions which included

enhancement of Operations Procedure OP/0/A/1107/05, Backcharging

Unit Main And Auxiliary Transformers, in an attempt to lessen the

possibility of operator error and added labeling to the equipment

that matched nomenclature in the procedure. The inspector

observed this activity and determined it to be complete.

A second part of the commitment was to reinforce the use of the

Stop-Think-Act-Review (STAR) process with emphasis on ensuring the

correct unit is verified.

The remainder of the licensee's commitment was to install unit

specific locks on the unit potential drawers. This effort has

been completed on Units 1 & 2, but not on Unit 3. However, work

has been scheduled to be completed on Unit 3 during the upcoming

refueling outage.

)

20

8.

Exit Interview

The inspection scope and findings were summarized on May 31, 1995, with

those persons indicated in paragraph I above. The inspectors described

the areas inspected and discussed in detail the inspection findings

addressed in the summary and listed below. No dissenting comments were

received from the licensee. The licensee did not identify as

proprietary any of the material provided to or reviewed by the

inspectors during this inspection.

Item Number

Status

Description/Reference Paragraph

Inspector Followup Item

Open

SSF Activation lime

269,270,287/95-09-01

(paragraph 2.f)

Deviation

Closed

Potential Single Failure Could

269,270,287/93-31-01

Blowdown Both Steam

Generators (paragraph 6.a)

Unresolved Item

Closed

Main Steam Stop Valve

269,270,287/93-30-02

Requirements (paragraph 6.b)

Deviation

Open

Generic Letter 83-28

269,270,287/95-09-02

Commitment Relating to MSSV

Solenoids (paragraph 6.b)

Violation 287/93-24-01

Closed

Inadequate Post Modification

Test

Program (paragraph 6.c)

Violation 270/93-21-01

Closed

Inadequate Modification

Procedure (paragraph 6.d)

Unresolved Item

Closed

Emergency Condenser Cooling

269,270,287/93-30-03

Water System Requirements

(paragraph 6.e)

Unresolved Item

Closed

Fatigue Analysis for RCS

269,270,287/94-08-03

Auxiliary Piping (paragraph

6. f)

Deviation

Open

Fatigue Analysis for RCS

269,270,287/95-09-03

Auxiliary Piping (paragraph

6. f)

Inspector Followup Item

Closed

Failure of Keowee Voltage

269,270,287/93-13-05

Regulator (paragraph 6.g)

Escalated Action 91-167

Closed

Failure to Follow

Procedures/Inadequate

Procedures (paragraph 6.h)

I

21

LER 270/93-03

Closed

Design Deficiency Results in

Technical Inoperability of the

Reactor Coolant Makeup (RCMU)

System (paragraph 7.a)

LER 269-93-05

Closed

Inoperable Control Rods Due To

Defective Procedure Results In

Technical Specification

Violation (paragraph 7.b)

LER 269/93-06

Open

Design Deficiency Results In A

Condition Outside The Design

Basis Of Containment For A

Main Steam Line Break

(paragraph 7.c)

LER 270/93-02

Open

Loss of Air Testing For

Accumulator Valves Not

Performed Per SOER 88-1

(paragraph 7.d)

LER 270/93-05

Closed

Operator Isolated Potential

Transformers On The Wrong Unit

Resulting In A Reactor Trip

Paragraph 7.e)