ML15239A021

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Interim SALP Repts 50-269/89-01,50-270/89-01 & 50-287/89-01 for Aug 1987 - Jan 1989.Major Areas Inspected:Plant Operations,Radiological Controls,Emergency Preparedness, Security & Engineering/Technical Support
ML15239A021
Person / Time
Site: Oconee  Duke Energy icon.png
Issue date: 04/11/1989
From:
NRC OFFICE OF INSPECTION & ENFORCEMENT (IE REGION II)
To:
Shared Package
ML15239A020 List:
References
50-269-89-01, 50-269-89-1, 50-270-89-01, 50-270-89-1, 50-287-89-01, 50-287-89-1, NUDOCS 8904240237
Download: ML15239A021 (33)


See also: IR 05000269/1989001

Text

ENCLOSURE

INTERIM SALP BOARD REPORT

U. S. NUCLEAR REGULATORY COMMISSION

REGION II

SYSTEMATIC ASSESSMENT OF LICENSEE PERFORMANCE

INSPECTION REPORT NUMBER

50-269, 270, 287/89-01

DUKE POWER COMPANY

OCONEE UNITS 1, 2, AND 3

AUGUST 1, 1987 - JANUARY 31, 1989

8904240237 8 90411

PDR

ADOCK 05000269

Q

PDC

TABLE OF CONTENTS

Page

I.

INTRODUCTION.1

A.

Licensee Activities

1......1

B.

Direct Inspection and Review Activities .................... 3

II. SUMMARY OF RESULTS

4

Overview

4.......4

III.

CRITERIA

6

IV. PERFORMANCE ANALYSIS

7

A.

Plant Operations ......................................... 7

B.

Radiological Controls .................................... 10

C.

Maintenance/Surveillance ................................. 13

0.

Emergency Preparedness ................................... 18

E. Security-& Safeguards .................................... 20

F.

Engineering/Technical Support ............................. 22

G.

Safety Assessment/Quality Verification ..................... 24

V.

SUPPORTING DATA AND SUMMARIES .................................

27

A.

Escalated Enforcement Action

....

27

B.

Management Meetings ...................................... 28

C.

Confirmation of Action Letters ............................ 29

0.

Review of Licensee Event Reports .......................... 29

E.

Licensing Activities ..................................... 29

F.

Enforcement Activity ..................................... 30

G.

Reactor Trips ............................................ 30

H.

Effluent Release Summary ................................. 31

I.

INTRODUCTION

The Systematic Assessment of Licensee Performance (SALP)

program is an

integrated NRC staff effort to collect available observations and data on

a periodic basis and to evaluate licensee performance on the basis of this

information. The program is supplemental to normal regulatory processes

used to ensure compliance with NRC rules and regulations. It is intended

to be sufficiently diagnostic to provide a rational basis for allocation

of NRC resources and to provide meaningful feedback to the licensee's

management regarding the NRC's assessment of their facility's performance

in each functional area.

An

NRC SALP Board,

composed of the staff members listed below, met on

March 20, 1989, to review the observations and data on performance, and to

assess licensee

performance in accordance with Chapter NRC-0516,

"Systematic

Assessment

of Licensee

Performance."

The

guidance

and

evaluation criteria are summarized in Section III of this report.

The

Board's findings and recommendations were forwarded to the NRC Regional

Administrator for approval and issuance.

This report is the NRC's assessment of the licensee's safety performance

at Oconee Units 1, 2, and 3 for the period August 1, 1987 through

January 31, 1989.

The SALP Board for Oconee- was composed of:

C. W. Hehl,

Deputy Director, Division of Reactor Projects (DRP),

Region II (RH) (Chairman)

A. F. Gibson, Director, Division of Reactor Safety, (DRS), RH

J. P. Stohr, Director, Division of Raditation Safety and Safeguards

(DRSS), RH

A. R. Herdt, Chief, Reactor Projects Branch 3, ORP, RII

D. B. Matthews, Director, Project Directorate 11-3, Office of Nuclear

Reactor Regulation (NRR)

P. H. Skinner, Senior Resident Inspector, Oconee, ORP,

RH

D. Hood, Project Manager, Project Directorate 11-3, NRR

Attendees at SALP Board Meeting:

M. B. Shymlock, Chief, Project Section 3A,

DRP,

RII

B. R. Bonser, Project Engineer, Project Section 3A, DRP, RH

L. D. Wert, Resident Inspector, Oconee, DRP, RH

S. Ninh, Reactor Engineer, Technical Support Staff, DRP, RH

A.

Licensee Activities

During this SALP period, Unit 1 was on line for a total of 460 days

with a unit capacity factor of 82.28%, Unit 2 was on line for 476

days with a capacity factor of 81.5%, and Unit 3 was on line for 486

days with a capacity factor of 85.4%.

These capacity factors are

much better than the plant lifetime factors of approximately 68%. The

forced outage rates were 0.34%, 2.62% and 4.28% for Units 1, 2 and 3

2

respectively.

This is much lower than

the lifetime average of

approximately 12%.

The operating history during this assessment

period is described below.

Unit 1

Unit 1 began this SALP period at 85% power, limited by high lake

water (condenser circulating water) inlit temperature.

The Unit

reduced power to 80% on August 18,

1987 due to the temperature

reading of 79.5 dagrees F.

On September 2, 1987 the Unit was taken

off-line for the end of cycle 10 refueling outage.

The Unit returned

to service on November 6, 1987 but was taken off-line to conduct

turbine generator balancing.

The Unit returned to 100% power on

November 15,

1987

and

remained

basically at full power until

February 17,

1988,

when the Unit reduced power to 61% due to a

feedwater pump problem. The feed pump problem was corrected and the

Unit returned to full power on February 24 until July 1 when power

was reduced to approximately 25% to add oil to the "182" reactor

coolant pump (RCP).

The reactor was returned to full power on

July 2, 1988 and then tripped on July 5 due to a false indication of

lost feedwater flow. The Unit was restarted on July 6, 1988 and

returned to full power on July 8, 1988.

On August 30,

1988 the Unit

was again removed from service to add oil to "182" RCP and returned

to service the following day. Full power conditions were attained on

September 1, 1988 and remained at this point until the reactor

tripped on January 2, 1989,

due to an -operator error.

During the

recovery from this trip on January 3,

1989 with the unit at

approximately 25%, a fire occurred in the ITA (6900v)

switchgear that

caused extensive damage forcing the operators to manually trip the

reactor and place the plant in a natural circulation condition for a

short period of time.

At this time the licensee decided to commence

the end of cycle (EOC)

11 outage which was previously scheduled for

January 27, 1989.

Unit 2

Unit 2 began this reporting period operating at approximately 85%

power, limited by high water level due to fouling in the "B" steam

generator.

The Unit reduced power on August 6 to 71% due to a low

oil level in a reactor coolant pump.

On August 12,

1987 power was

further reduced, oil added to the pump and power level returned to

approximately 85% on the following day.

The unit remained at 85%

power except for changes due primarily to minor equipment problems,

until February 3, 1988 when the Unit was shut down for the EOC-9

-refueling outage. The outage was completed in early April and the

Unit returned to 100% power on April 15,

1988.

Since the steam

generators were chemically cleaned during the outage,

power was no

longer limited due to steam generator water levels.

On April 17,

1988 the Unit experienced a turbine-generator runback to 44% due to a

stator coolant flow instrumentation problem. The Unit power was then

decreased to approximately 25% to repair the instrumentation and

3

returned

to

100% power

on April 20.

The Unit remained at

approximately 100% power, with the exception of short periods when

the Unit was used to load follow on the grid, until June 6 when it

was shut down due to steam generator tube leaks. It was returned to

service on July 16 and following resolution of several secondary

system problems returned to 100% power on July 29.

On August 26 the

Unit tripped from 100% power due to a faulty high moisture separator

drain tank level signal.

This was repaired and the Unit returned to

100% power on August 27 and remained at that power level for the

duration of this SALP period.

Unit 3

Unit 3 commenced this reporting period operating at full power until

January 3, 1988 when power was reduced due to a steam generator tube

leak.

The leak stabilized on January 10,

1988 and the unit was

returned to full power.

On April 2 power was reduced to 88% to

conserve the core for the summer load period, but was shut down on

April 17 due to steam generator tube leakage.

The Unit was returned

to power on May 11,

1988 and remained at power until the Unit was

shut down to begin the EOC 10 refueling outage on August 10,

1988.

The outage was completed on September 23, 1988 but several turbine

problems delayed the return to full power.

The unit was returned to

service and full power conditions on September 26,

1988 until

November 14,

1988 when the reactor tripped twice.

The cause of the

first trip could not be determined,- however, the unit was restarted.

At about 40%, the second trip occurred but this time the cause was

determined to be a faulty relay in the steam generator level

circuitry and was corrected.

The Unit was restarted and returned to

full power op November 16,

1988.

On January 11,

1989 the Unit was

shut down due to fouling of the reactor building cooling units

(RBCU).

The

RBCUs were cleaned, and retested. Unit 3 returned to

service and has remained at full power for the remainder of this SALP

period.

B.

Direct Inspection and Review Activities

During the assessment period, routine inspections were performed at

Oconee by the NRC staff.

Special inspections were conducted as

follows:

-

February 22 -

26, 1988, a special inspection in the areas of

Environmental Qualification (EQ)

of electrical equipment.

It

included a review of Duke

Power Company's implementation of

requirements of 10 CFR 50.49 for Oconee and an inspection of EQ

electrical equipment.

-

April

25 -

May 5,

1988,

a special inspection to review the

adequacy of Emergency Operation Procedures.

4

-

May 9 -

13 and May

19 -

27,

1988,

a quality verification

functional inspection (QVFI)

was conducted in the areas of

operations and surveillance testing, maintenance,

and design

control.

-

July 11 -

29,

1988, a special trial Maintenance Team Inspection

(MTI) of the methodology prescribed by NRC temporary instruction

TI 2515/97, Maintenance Inspecticn to evaluate the implementa

tion of the licensee's maintenance program.

-

January 4 -

14, 1989, an Augmented Inspection Team investigated

the reactor trip on January 2 and the fire on January 3, 1989.

II. SUMMARY OF RESULTS

Overview

Oconee was operated in an overall safe manner during this assessment

period. Strengths were observed in the areas of Plant Operations,

Radiological Controls

and Emergency

Preparedness.

A decline in

performance was identified in the areas of Security and Maintenance

and Surveillance.

Additional managerial attention is needed to

return these areas to their previous performance status.

Operations performance continued to be a strength.

The number of

a-utomatic trips were reduced well below the industry average and

below the goals established by the licensee.

Corporate interest and

oversight of plant activities was very apparent. Fire protection was

adequate. Good progress has been made in plant cleanliness which

resulted in a reduction of contaminated areas.

Management

was

frequently observed in various areas of the plant providing oversight

of activities and guidance to personnel in those areas. The operator

training and experience were excellent.

The

Radiological Controls area is considered a strength.

The

reduction of contaminated areas noted above and the continuing effort

to further reduce these areas was noteworthy.

The reduction of

person-rem by use of mockup training and use of remote devices and

other training activities is

also noteworthy.

A weakness was

identified in the extended period of inoperability of several

Radiation Indicating Alarms.

The

licensee

has

strong maintenance and surveillance programs.

However, over this assessment period, numerous performance problems

in maintenance were identified. These performance

problems were

characterized by inattention to detail,

miscommunication,

and

procedure/personnel

errors

resulting

in violations

of

NRC

requirements.

Over the period Oconee

station has had good

availabililty and few operational problems directly attributable to

maintenance.

5

Surveillance

activities have also experienced a decrease in

effectiveness. Surveillances were completed on time with only minor

problems identified. However, notable problems were identified in

the in-service testing of valves.

The chemistry program in

conjunction with the chemical cleaning of Unit 1 and 2 steam

generators and the continued attention being provided to meet the

guidelines recommended by the Steam Generators Owners Group

has

minimized degradation of the steam generator tubes.

Emergency Preparedness activities have been maintained as a strength.

The licensees many drills conducted in this area have been beneficial

as demonstrated by the utilities actions during several actual

conditions that occurred during this assessment period.

However, a

weakness was noted that involved an incorrect classification of an

emergency declaration during the conduct of the annual drill.

The Security area,

which histori-cally has been a strong area,

experienced a significant number of minor problems during this

assessment period.

Although no single problem was overly signi

ficant, the number of problems identified showed a distinct decrease

in the effectiveness of the security effort.

Of special note is the

continuing problem with the closed circuit television assessment

capability attributed to poor design and installation.

Management

reacted positively to weaknesses

identified in the

Engineering/Technical Support area during the previous assessment

period.

This effort was

noted

in the

assignment of design

engineering personal to the site and the restructuring of corporate

engineering groups to a site specific function rather

than

a

discipline function as was used in the past.

Management activities

have resulted in the self-identification of several significant

problems notable among these was the HPI system mode requirements

previously not addressed correctly by the operations staff. Although

progress has been made in this area weaknesses still exist such as

those associated with communications

and simulator hardware and

software. Additional management attention may be needed to achieve

the desired results in this area.

With respect to the Safety Assessment/Quality Verification area

several aspects of plant performance were assessed.

The licensee

continues to perform self initiated technical audits and use other

sources to improve safety performance.

QA,

QC

and management

continue to provide good oversite of all activities.

The quality of

Licensee Event Reports have improved. Weaknesses were noted in the

area of complete follow through of activities. This was exemplified

by the lack of thoroughness associated with the HPI "piggyback" mode

of operation issue and several

issues concerning

10

CFR 50.59

evaluations.

6

Rating Last

Rating This

Functional Area

Period

Period

Plant Operations

1/2

-

1

(operations & fire protection)

Radiological Controls

2

1

Maintenance/Surveillance

1/1

2

Emergency Preparedness

1

1

Security

1

2

Engineering/Technical Support

2

2

(engineering, training & outages)

Safety Assessment/

2/2

2

Quality Verification

(quality programs & licensing)

III. CRITERIA

Licensee performance is assessed in selected functional areas, depending

on whether the facility is in a construction or operational

phase.

Functional areas normally represent areas significant to nuclear safety

and the environment. Some functional areas may not be assessed because of.

little or no licensee activities or lack of meaningful observations.

Special areas may be added to highlight significant observations.

The following evaluation criteria were used, as applicable, to assess each

functional area:

1. Assurance of quality, including management involvement and control;

2. Approach

to the resolution of technical issues from a safety

standpoint;

3.

Responsiveness to NRC initiatives;

4.

Enforcement history;

5. Operational and construction events (including response to, analyses

of, reporting of, and corrective actions for);

6.

Staffing (including management); and

7.

Effectiveness of training and qualification program

However, the NRC is not limited to this criteria and others may have been

used where appropriate.

7

On the basis of the NRC assessment,

each functional area evaluated is

rated according to three performance categories.

The definitions of these

performance categories are as follows:

1. Category 1. Licensee management attention

and

involvement

are

readily evident and place emphasis on superior performance of nuclear

safety or safeguards activities, with the resulting performance

substantially exceeding regulatory requirements.

Licensee resources

are ample and effectively used so that a high level of plant and

personnel performance is being achieved.

Reduced NRC attention may

be appropriate.

2.

Category 2. Licensee management attention and involvement in the

performance of nuclear safety or safeguards activities are good. The

licensee has attained a level of performance above that needed to

meet regulatory requirements.

Licensee resources are adequate and

reasonably allocated so that good plant and personnel performance is

being achieved. NRC attention may be maintained at normal levels.

3.

Category 3. Licensee management attention to and involvement in the

performance of nuclear safety or safeguards activities are not

sufficient. The licensee's performance does not significantly exceed

that needed to meet minimal

regulatory requirements.

Licensee

resources appear to be strained or not effectively used.

NRC

attention should be increased above normal levels.

The SALP Board may also include an appraisal of the performance trend of a

functional area. This performance trend will only be used when both a

definite trend of performance within the evaluation period is discernable

and the Board believes that continuation of the trend may result in a

change of performance level.

The trend, if used, is defined as:

Improving: Licensee performance was determined to be improving near the

close of the assessment period.

Declining: Licensee performance was determined to be declining near the

close of the assessment period and the licensee had not taken meaningful

steps to address this pattern.

IV. PERFORMANCE ANALYSIS

A.

Plant Operations

1. Analysis

During

this

assessment pertod

routine

inspections

and

evaluations of plant operations were performed by the resident

and regional inspection staffs. A total of five automatic trips

occurred during this rating period, two on unit 1, one on unit 2

and two on unit 3. One manual trip was also experienced. Seven

automatic trips occurred during the last rating period.

8

The quality of operations has been maintained at a high level of

performance.

The number of automatic reactor trips has been

reduced below the industry average of 2.1 automatic trips a year

and the goal established- by the licensee of no more than two

trips per unit per year.

Upper level management continues to be extensively involved in

all aspects of plant operation.

The licensee has taken action

to provide senior reactor operator training to most of the

superintendents

and many

senior supervisory personnel.

In

addition some of the superintendents have rotated positions in

order to provide a greater understanding of how each discipline

functions to support the overall effort of safe and efficient

operation.

Management

has

been observed frequently in the

control room and touring the plant areas. Outage management has

shown major improvement.

Outage time

has been reduced to

approximately 45 days without any significant reduction in the

quantity and quality of work being accomplished.

The Shift

Engineers, who are licensed senior operators, are very involved

in coordination of outage work during backshift and weekends.

The low turnover rate (less than 3%) maintained by the licensee

has been instrumental in maintaining a continued high experience

level and a high level of competence in the operations staff.

Due in part to this low turnover rate, the amount of overtime

required of the operators has not been excessive. In addition to

the experience in the operations group, senior personnel with

operating experience have been placed in various other groups.

Control

room demeanor and attentiveness has been good. There

have been several instances where operator attention and quick

action have prevented a reactor trip due to malfunctioning

components.

To promote professionalism,

the operators,

in

conjunction-with -the- operators* at Catawba and McGuire,

have

developed a set of operator principles. These are posted in the

control rooms and other operations areas and identify their

commitment to excellence. Operations staffing level continues to

exceed TS requirements for shift crew composition.

A high level

of attention to details beyond their normal duties on the part

of several non-licensed equipment operators (NEO) identified and

assisted in resolving several problems.

Examples of this were

the identification of a problem with the Emergency

Power

Switching Logic (EPSL)

and also identification of a containment

isolation valve being mispositioned.

Only two instances have

been identified where operators have failed to follow their

procedures. These primarily occurred during the early part of

this assessment period and were attributed to the incorrect use

of identifying steps as "not applicable" by the supervisor or an

isolated personnel error. Improvement in this area has occurred

during this period due to managements attention to this problem

and the continued emphasis

by management

to follow their

procedures.

9

Communications Ltween operations

and

other

groups

is

acceptable, but there have been several

instances where

inadequate communications have caused a problem.

Examples of

this

communication

problem

between operations

and

the

performance group involved a loss of all power on Unit 3 for

approximately 15 minutes while in decay heat removal during the

last refueling outage.

Another communication problem between

operations and the instrumentation and electrical group resulted

in a runback on Unit 3 as a result of a pulled fuse while

troubleshooting the rod drive system. Communications

between

operations and the General Office Engineering staff resulted in

a significant safety concern as discussed in more detail in

section G. Improvements have been noted in this area in recent

months, but continued management attention should be provided in

this area.

An Augmented Inspection Team (AIT)

reviewed two incidents that

occurred on January 2 and 3, 1989 on Oconee Unit 1. The AIT was

established to review the events associated with a reactor trip

from 100% power that occurred on January 2 and an explosion and

fire in the 6900 volt switchgear that resulted in a manual reactor trip from a low power level and subsequent operation in

a natural circulation condition on January 3.

The conclusion

reached by the AIT was that during the first incident, the

operators took appropriate actions to maintain the plant in a

safe condition. The AIT determined that during the second event

the firefighting techniques and results were adequate,

and that

the reactor trip that had occurred the previous day did not

contribute to the fire and trip on the following day.

In

addition the team concluded that management was highly involved

in both the actions taken during the evolutions and the repairs

following the stabilization of the unit.

The team identified

weaknesses in the training of operators and supervisors in areas

associated with .use

of pressurizer auxiliary spray,

the

requirements

for operation in the Thermal

Shock Operating

Region, and natural circulation with low decay heat conditions.

As a result of these findings, the licensee has taken action to

conduct additional training and provide additional guidance in

these areas.

An Emergency Operating Procedure (EOP) inspection found that the

Oconee Emergency Procedures (EP)

and Abnormal

Procedures (AP')

adequately cover the broad

range of emergencies and other

significant events required by Regulatory Guide 1.33, Section 6.

The team found technical discrepancies in the licensee's

procedures for cooldown using the HPI system, boron dilution,

loss of condenser circulating water intake canal/dam failure and

reactor coolant

pump

operation.

Also inconsistencies in

operator interpretation of important terms indicated a need for

further operator training in EOP terminology use.

The licensee

is correcting these inconsistencies.

10

The plants housekeeping arcd material condition continued to be

acceptable and continued to improve. Although progress has been

made in housekeeping, specific areas are frequently identified

where debris has accumulated especially following outages.

Management is making an effort to correct this problem.

With respect to fire protection, the licensee's fire protection

procedural program

and implementation

of fire

prevention

administrative controls were found to meet NRC requirements and

guidelines. Fire systems required for protection of safety

related plant areas were

being maintained operable.

The

staffing of the Safety/Fire Protection Department onsite and in

the corporate Design Engineering group was adequate. The onsite

group was staffed with two fire protection specialists who have

primary responsibility for the implementation of the Fire

Protection Program.

The entire Safety/Fire Protection staff

actively

monitored

plant

activities

to

assess

proper

implementation of the program.

In addition, a Fire Protection

Engineer was also assigned to the site from the corporate Design

Engineering office.

The overall quality of the staff was a

program strength.

Two violations were identified in this area:

a. A- Severity Level

IV violation for failure to follow

procedures which resulted in a loss of low temperature

overpressure protection for a total of 8 minutes.

(88-28,

Unit 3 only)

b. A Severity Level IV violation for an inadequate procedure

for testing the Emergency Power Switching Logic causing a

complete loss of all AC power to Unit 3. (88-28,

Unit 3

only )

2.

Performance Rating

Category: 1

Previous Rating: Operations:

1

Fire Protection: 2

3.

Recommendations

None

B.

Radiological Controls -.

1. Analysis

Inspections were conducted in the areas of radiation protection,

radiological effluents,

and confirmatory measurements during

this assessment period.

11

The

licensee's health physics (HP)

radwaste

and chemistry

staffing levels compared favorably to other facilities of

similar size.

Eighty-seven percent of licensee health physics

technicians were ANSI/ANS 3.1 qualified, with the remainder to

be qualified during the current

SALP period.

Contract HP

technicians

have usually been

hired

to support

refueling

outages. However, a refueling outage originally scheduled for

January 28,

1989, started three weeks earlier without contract

technicians.

The

licensee

provided

radiation protection

efficiently in the

interim period

by

reassigning

office

personnel to the field. The experience of contract technicians

was a program strength since a high percentage of contract HP

technicians had previous outage experience at Oconee.

The

licensee HP staff also had a low turnover rate.

A finding that retraining for contract HP technicians had not

been formalized was corrected by changing the HP manual to

require retraining for those who had not worked on site in the

last twelve months.

The site specific HP training course

contained elements required for course accreditation.

Management

support for the radiation protection program was

demonstrated by the installation and operation of Constant Air

Monitors, a state-of-the-art whole body counter,

an automated

laundry monitor for screening of protective clothing, and a new

radioactive waste sorting and compacting facility.

The licensee continued to have

an aggressive contamination

control

program.

Dedicated decontamination crews maintained

approximately ninety-three percent of

the

radiologically

controlled area (RCA) as non-contaminated.

The licensee's approach to resolving HP technical issues was

adequate. Problems associated -with the plant breathing

a-ir

systems were identified during an inspection and corrective

action included calibration of system pressure gauges,

operator

intervention

upon carbon monoxide monitor failure, as-built

drawings for the location of air manifolds and pressure gauges,

and provision for direct communication between the control room

and HP personnel concerning the breathing air system.

Weaknesses were identified in the licensee program to control

personnel exposure to radiation. Violations were identified for

workers

entering containment without reporting to

the HP

technician as instructed and for workers entering and exiting

high radiation areas without knowledge of area dose rates and

without adequate monitoring of self-reading pocket dosimeters.

In addition, high radiation area hot spots,

greater than 100

millirem per hour at 18 inches, were not labeled after shielding

had

been

installed.

Licensee

management

understood

12

the issue and committed to take the approprie-e and necessary

corrective actions.

The licensee established a goal of 1,000 person-rem for 1988 for

all three units. During 1988,

the licensee's collective dose

was 879 person-rem or 293 person-rem per unit as measured by

TLD.

The low station collective exposure was attributed to

efficient ALARA planning during outages and use of robotics in

maintenance of steam generators.

The dose received in 1988 is

the lowest dose since 1975 for the licensee which is usually at

or below the national average for PWRs.

Liquid and gaseous effluents for calendar year 1987,

and the

first half of 1988,

were within regulatory limits.

Offsite

doses did not exceed 10 CFR

50,

Appendix I ALARA criteria.

Liquid and gaseous effluents for 1985 through the first half of

1988 are summarized in this report (see

Section V.1).

The

licensee reported a total of three abnormal liquid releases and

no gaseous releases during July 1987 to June 1988.

Licensee management attention to and

involvement

in the

calibration and operation of process and effluent monitors was

not sufficient in that the Low Pressure Service Water radiation

monitors (RIA-35)

have been inoperable since 1985.

Corrective

actions to upgrade the entire RIA monitoring system are under

development but-will not be implemented for approximately three

years.

A confirmatory measurements inspection showed agreement between

licensee and

NRC measurements with the

exception of two

radionuclides in three counting geometries.

The licensee was

responsive to NRC initiatives as demonstrated by an agreement to

analyze additional spiked samples.

The results of these

analyses are currently- pending.

A violation was identified

during this inspection for failure to provide

an approved

procedure for the sampling of the Unit 1 condenser offgas.

Two violations were identified.

a.

Severity Level IV violation for failure to identify

radiation hot spot locations after shielding had been

installed and to instruct personnel in the precautions or

procedures to minimize exposure to radiation (89-02).

13

b. Severity Level

IV violation for failure to proviJe an

approved procedure for the sampling of the Unit 1 condenser

offgas (88-31).

2.

Performance Rating

Category: 1

Previous Rating: 1

3. Recommendations

None

C.

Maintenance/Surveillance

1. Analysis

Evaluation of this functional area was based on the results of

routine inspections performed

by

the resident inspectors,

routine inspections by regional

inspectors, and

special

inspections in the area of Environmental Qualification (EQ)

of

Electrical

Equipment,

a'

Quality

Verification

Functional

Inspection (QVFI), and a Maintenance Team Inspection (MTI).

Overall

the licensee has

adopted

strong maintenance

and

surveillance programs.

However,

over this assessment period,

numerous performance problems were identified. These performance

problems were characterized

by

inattention

to

detail,

miscommunication,

and procedure/personnel errors resulting in

violations of NRC requirements.

Over the period Oconee station has had good availability and

few operational problems directly attributable to maintenance.

The licensee's management

was very supportive of a strong

maintenance progra.- This, was exemplified by the presence of

the station manager and superintendent during daily outage

meetings and other meetings that become necessary during periods

of routine operations when meetings are not normally conducted.

Management also was observed frequently in the various plant

areas watching activities and reviewing the conditions in the

areas.

Management

has established goals to increase their

preventive maintenance/corrective maintenance ratio to 70% and

reduce their outsta-nding work requests that are over three

months old to less than 450. During the latter portion of this

assessment period the plant had nearly achieved their goal,

in

that the preventive/corrective ratio was about 65% and the work

requests greater than three months old numbered about 200

for the site.

14

The QVFI which included the areas of maintenance and surveil

lance testing identified a number of minor violations, and found

work practices and procedural controls to be acceptable. Also

the inspection concluded that based on the low component failure

rate and few repetitive failures the licensee's corrective and

preventive maintenance programs appeared to be effective.

However, one instance was identified by the resident inspectors

where safety-related components

had been

omitted from the

preventive maintenance program. This was a failure to provide

proper maintenance for the Reactor Building Cooling Unit (RBCU)

drop out plates. When the drop out plates were tested in their

as-found condition, the plates would not function as designed.

At the end of this SALP period, this issue was still under NRC

review for escalated enforcement.

Enforcement in this functional area has increased since the

previous assessment period.

Thirteen violations in the

maintenance and surveillance area were identified this period

compared with one violation in the maintenance area and one

violation in the surveillance areas during the previous SALP

period. Most of the violations during this period have had only

minor safety significance.

One of the violations was a failure to -follow procedures

associated with a freeze seal which thawed allowing a spill of

approximately

30,000

gallons

of

slightly

radioactively

contaminated water,

a small amount of which resulted in an

uncontrolled release to the chemical

treatment

pond

and

subsequently off-site (Violation a).

A second violation involved a failure to perform an adequate

verification to assure work was being performed on the correct

component prior to performing maintenance.

This resulted in the

removal of packing from an instrument valve on an operating unit

rather than the shutdown unit. This error resulted in a leak of

approximately

40

gpm

in the auxiliary building.

Although

operations personnel did a good job in isolating the leak and

maintaining the unit in a safe condition, several persons were

contaminated and a spill of approximately 1,000 gallons of

contaminated water occurred (Violation b).

Inattention to detail was a major contributing factor in the

violations identified during the EQ inspection.

This resulted

in the failure to fully document essential information in the

licensee's EQ files and subsequently in a failure to include the

information concerning these specific EQ requirements in the

development of some surveillance and maintenance procedures

(Violation c, k and 1).

15

A Maintenance Team Inspection (MTI) was conducted in July 1988.

A weakness was identified in communication/coordination between

the plant maintenance department and the

Duke Transmission

Division.

This

was

exemplified in a violation

involving

verification and calibrations

in the Instrumentation

and

Electrical (I&E) maintenance area (Violation h).

During the MTI other weaknesses were identified that related to

10CFR50.59 reviews. One example involved the licensee's failure

to perform an adequate 50.59 review for the inoperability of the

ground detector prior to startup of Unit 2.

This issue is

discussed further in the Safety Assessment/Quality Verification

section of this SALP report.

The quality of maintenance and surveillance planning at Oconee

has been good. This area has been enhanced due to the efforts

of the integrated scheduling group and the use of dedicated

engineers permanently assigned to this group.

Through the

efforts of management and this group, the outage periods have

been *reduced without a reduction in the quantity or quality of

work being accomplished.

One major activity that was undertaken

was an effort to assure all work is completed on a component or

system when it

is

taken out. of service (through

closer

coordination of the various onsite groups) to preclude redundant

testing.

Materials

control,

which

includes procurement,

receiving

activity, and material storage, was good during this assessment

period. Violation (m) related to access control of material

storage areas

and does not impact the quality of material

handling and storage.

Because it

is a three-unit station and must plan for a minimum

of two major .refueling

outages per year,

the- station has

established a fairly large, stable work force in the area of

maintenance. The Oconee site is also the home base for the

Southern division of Duke Power Company's

Construction and

Maintenance Division (CMD),

which is an additional resource for

trained and qualified maintenance personnel.

-The chemistry program is being implemented in a satisfactory

manner to meet Technical Specification limits and the guidelines

recommended by the Steam Generators Owners Group.

The licensee

is continuing, through the effectiveness

16

of

plant components and chemistry control,

to minimize

degradation of the steam generator tubes.

Surveillance and

preventive maintenance programs

have been expanded for the

Once-Through-Steam-Generators

and the Decay Heat Removal Heat

Exchangers in order to identify potential problem areas.

The

licensee has made improvements in analytical methods with the

installation of online ion chromatography analyses systems.

Surveillances continue to be performed with only occasional

problems.

Surveillances have been performed as required by

Technical Specifications. There have been very few instances of

missed surveillances during this period.

The QVFI identified that licensee technicians performing a valve

stroke timing surveillance test did not recognize that the

stroke-time performance did not meet its acceptance criteria. A

review of previous testing also identified that the preceding

test had not met the acceptance criteria (Violation d).

Another inadequacy with the licensee's surveillance program was

stroke time testing was not being performed as specified by ASME

Section XI requirements.

Section XI of the ASME Boiler and

Pressure Vessel Code requires timing to begin at the signal

initiation and conclude at the actual closure as opposed to the

"light to light" criteria being utilized by the licensee

(Violation e).

The method in-use by the licensee was based on

the timing method that had been approved by the NRC for the IST

program established at the Catawba Nuclear Station.

Examples of licensee response to surveillance failures in MOVATS

testing were identified to be poor in that there was an apparent

attitude by

some personnel

that acceptance criteria for

Inservice Test Program

(IST) program valves was guidance and

not a requirement.

Additional examples were identified where

corrective actions for failed surveillances were delayed,

minimal,

or not performed.

Other items observed were a failure

to verify that all specified acceptance criteria in MOVATS

testing was performed (i.e. to verify ease of movement of an

actuated valve) and several valves which meet the requirements

for IST program valves were not entered into the IST program

(violation f).

The thirteen violations listed below represent a significant

increase over the previous SALP period.

There was one violation

in the maintenance area and one violation in the surveillance

.

area during the previous SALP period.

'Most of the violations

during this period have had only minor safety significance.

a. Severity Level IV violation for failure to follow procedure

on freeze seal of a line to the BWST resulting in a 30,000

17

gallon

spill of slightly contaminated

borated water

(87-51).

b.

Severity Level IV violation for inadequate procedures to

assure the correct component was identified prior to

performing work which resulted in a spill of contaminated

water due to the work being performed on the incorrect

valve and also with a main steam valve that was incorrectly

removed from a supply line to the auxiliary feedwater pump

turbine (88-08).

c.

Severity Level IV violation for inadequately documenting

the performance characteristics for the Victoreen High

Range Radiation Monitor System (88-03)(EQ).

d.

Severity Level IV violation for failure to keep accurate

records for PT/2/A/0150/22A, operational valve functional

test on May 11,

1988,

and nuclear equipment operator fire

watch logs on May 19, 1988 (88-13).

e.

Severity Level IV violation for failure to routinely

measure valve stroke times from actuation signal. initiation

to the end of the actuation cycle (88-13).

f. Severity Level IV violation for failing to include valves

LPSW-773 and HP-98 in the valve inservice testing program

(88-13).

g.

Severity

Level IV violati6n

for failure to follow

procedures relative to correctly filling out work requests

and for inadequate cleanliness levels in the reactor

protection and engineered safeguards cabinets (88-13).

h.

Severity .Level

IV violation for procedural problems related

to

verification

and

calibration

of

control

room

instrumentation

and battery undervoltage alarm relays,

circuit breaker maintenance,

4160 volt switchgear,

and

ground detection circuit alarm set points (88-17).

i.

Severity Level

IV violation for failure

to

follow

procedures resulting in overpressurization of a safety

related pipe section. (88-32, Unit 3 only)

j.

Severity Level V violation for failure to follow, in its

entirety, the procedure for component verification while

performing RPS Channel-"B" calibration and functional tests

(87-44).

k.

Severity Level V violation for the reactor building level

transmitter junction box not being maintained completely

18

filled with oil and,

therefore,

not in the as tested

configuration (88-03)(EQ).

1. Severity Level V for deficient EQ maintenance procedures in

that requirements in the Equipment Qualification Reference

Index

were

not properly addressed in the maintenance

procedures (88-03)(EQ).

m. Severity Level V violation for failure to maintain access

control to storage areas. (87-32, Unit 3 only)

2.

Performance Rating

Category: 2

Previous Rating:

Surveillance 1

Maintenance 1

3.

Recommendations

Increased management attention is warranted in this area due to

the reduced attention to detail and increase in personnel and

procedural errors.

0. Emergency Preparedness

1. Analysis

The regional inspection conducted during this assessment period

by both resident and regional inspectors included a routine

emergency preparedness

inspection and two annual

emergency

response exercises.

Four Emergency Plan revisions were also

submitted by the licensee for NRC review.

Overall,

during this SALP period,

the licensee, with one

exception noted below, continued to demonstrate the capability

to

fully

implement

the

critical

aspects

of

emergency

preparedness during simulated or actual emergency events.

The licensee's response to simulated emergencies during the

annual emergency

preparedness exercises demonstrated their

capability to effectively implement the Emergency

Plan.

A

partial participation exercise was performed on November 11,

1987. A full scale exercise was performed April 14,

1988.

An

exercise

weakness

involving

an

incorrect .

emergency

classification was identified during .the latter exercise.

Specifically, a Site Area Emergency should have been promptly

declared based on

the simulated loss of reactor shutdown

capability concurrent with a LOCA greater than

50 gpm.

In

response to this finding, the licensee promptly revised the

Emergency Plan and respective implementing procedure to more

clearly define Site Area Emergency,

Emergency Action Levels

(EAL)

regarding loss of shutdown function.

Additionally, the

19

respective revised Emergency Plan implementing procedure was

rendered more user friendly.

Corrective action also included

training

of all operations personnel regarding

EALs

and

emergency classification.

The license also effectively demonstrated their capability to

correctly use EALs and promptly identify and classify an actual

Alert resulting from the loss of functicns needed to maintain

Unit 3 in cold shutdown.

Additionally, four Notification of

Unusual Event (NOUE)

were promptly classified including a fire

and a steam generator tube leak.

The annual exercises demonstrated the licensee's proficiency in

promptly

implementing

protective

action

recommendations

consistent with the licensee's Emergency Plan and respective

emergency procedures, and EPA Protective Action Guidelines. The

exercises also disclosed the licensee's prompt and effective

implementation of dose assessment and projections attending

simulated

offsite

releases

of

radioactive

materials.

Comprehensive critiques were conducted following each exercise.

Licensee-identified findings were recorded

and corrective

actions required were implemented.

The routine emergency preparedness inspection found that the

licensee maintained the capability for prompt notification and

effective -communications with-offsite support agencies and

emergency

response facilities.

Instrumentation

and supplies

were

appropriate

and

emergency

preparedness

training

was

complete and effective.

The site emergency organization continued to demonstrate a

strong commitment to training by development of drill scenarios

and consistent use of Oconee plant specific Probabilistic Risk

Assessment

(PRA)

.data to render

such drills realistic and

challenging. The experience developed as a result of frequent

unannounced drills and practice exercises has significantly

enhanced the capability of emergency response personnel during

evaluated exercises and actual emergencies.

No emergency preparedness violations were identified during this

assessment period.

2.

Performance Rating

Category:

1

Previous Rating:

1

3.

Board Comments

Failure to promptly and correctly classify a simulated event during

an emergency exercise is normally considered by the NRC to show a

significant weakness in a licensee's emergency preparedness program.

20

Such a wea.kness would not be expected in a SALP Category 1 program.

It was noted however, that the licensee implemented a prompt and very

effective response to the exercise weakness.

Subsequently, the

licensee effectively demonstrated this capability during this

assessment period, during an actual Alert and four NOUEs.

The Board

therefore concluded that the performance in this area was SALP 1.

E.

Security and Safeguards

1. Analysis

The Physical Security functional area evaluates and assesses the

adequacy of the security force to provide protection for the

stations vital systems and equipment. To determine the adequacy

of the protection provided, specific attention was given to the

identification

and

resolution

of

technical

issues,

responsiveness

to

NRC

initiatives, enforcement

history,

staffing, effectiveness of training, and qualification.

The

scope of this assessment includes all

licensee activities

associated with access control, physical barriers, detection and

assessment,

armed

response,

alarm stations, power supply,

communications,

and compensatory measures for degraded security

systems and equipment. This evaluation is based on routine and

special inspections conducted by the NRC in this area and

related functional areas.

Authority and responsibilities associated with the security

organization

were

clearly delineated and appeared

to be

effective. The site contract force is adequately staffed and

appropriately trained and equipped.

The facility guard Training

and Qualification Plan is implemented on a continuing basis at

all levels of the security organization using the onsite

training staff.

The licensee has provided the security force with adequate

procedures. Security plan changes are submitted on a timely

basis and licensee records are complete, adequately maintained

and available. Licensee events reports are prompt and complete.

The

licensee's independent security program audit covered

various aspects of the site security program and the program

auditors were

thorough

and well acquainted with licensee

commitments.

The regional staff identified a problem with the closed circuit

television (CCTV)

assessment capability at the beginning of this

rating period. This poor CCTV assessment was partially due to

low priority maintenance but more significantly due to poor

design and installation. This problem was not resolved at the

end of the rating period, demonstrating a slow response to

regulatory concerns and a lack of urgency in addressing this

21

issue.

The li-ansee has been relying on long term compensatory

measures to provide this assessment capability.

One Material Control and Accountability inspection was conducted

during the SALP period.

This inspection was performed to

determine whether the licensee had limited his possession and

use of special nuclear material

(SNM)

to authorized locations

and uses, and had implemented an adequate and effective prografm

to account for and control all SNM in possession under license.

The inspection determined that the licensee had developed and

was maintaining an adequate safeguards program for the control

and use of both fuel and non-fuel SNM.

External reporting was

found to be accurate and timely.

While the licensee has experienced an increase in the number of

security related violations, they are not indicative of a major

security program breakdown.

Six of the violations cited during

this reporting period were

licensee identified.

Analysis

indicates that the majority of the violations are attributable

to errors by individual members of the security force relative

to adherence to procedural requirements and documentation rather

than hardware

and equipment associated problems.

The one

violation identified by regional inspection concerned a degraded

vital barrier that had not been previously identified by the

licensee. These violations indicate a need for additional

attention-to detail, and increased regulatory sensitivity on the

part of the security force.

The violations identified were as follows:

a. Severity Level

IV for allowing an employee into the

protected area without a picture badge. (87-45)

b. Severity Level IV for allowing a visitor into the protected

areas without a hands-on search.

(87-46)

c.

Severity Level IV for failure to control

Safeguards

Information.

(87-50)

d.

Severity Level IV for transmitting Safeguards Information

over unprotected telecommunication circuits.

(87-50)

e.

Severity Level

IV for degradation of the Central Alarm

Station barrier bullet resistivity.

(88-10)

f. Severity Level V for allowing the training certification

of a member of the security force to expire.

(87-46)

g.

Severity Level V for allowing an escorted visitor into the

protected

area

with

incorrect access authorization

documentation. (88-10)

22

2. Performance Rating

Category: 2

Previous Rating:

1

3. Recommendations

The Board recognized the continued high level of management and

oversight and support provided the contract security force in

the areas of training, staffing and procedural guidance.

However, the lack of responsiveness in resolving a long standing

issue relating to the assessment capability of the closed

circuit television system and the increase in the number of

violations, attributable to personnel error, detract from an

otherwise favorable evaluation of the security program.

The

Board recommends management emphasis in these areas.

F. Engineering/Technical Support

1. Analysis

The Engineering Technical Support functional area addresses the

adequacy of technical and engineering support for all plant

activities.

To determine the adequacy of support provided,

specific attention was given to the identification and

resolution -of

technical

issues, responsiveness to NRC

initiatives, enforcement history, staffing, effectiveness of

training and qualification.

The scope of this assessment

includes all

licensee activities associated with plant

modifications,

technical support provided for operation,

maintenance,

testing and surveillance, operator training,

procurement,

and configuration control.

This evaluation is

based on routine and special inspections conducted by the NRC in

this area and related functional areas.

Engineering and technical support in this assessment period has

been generally good.

Design engineering

(DE)

activity has

resulted in a number of self-identified plant problems as well

as improvement initiatives.

The effective utilization of

engineering resources has been demonstrated by a number of

issues addressed by the licensee.

An exception to the generally

good performance was a recurrence of a communications weakness

which was identified in the previous SALP assessment period.

The commdtnication effort has improved during the latter part of

-this SALP period.

The plant engineering staff, outside the DE organization, is

assigned to various plant functional activities,

(i.e.,

operations, maintenance, and radiological controls), providing

more timely evaluation and resolution of plant problems.

In

particular, maintenance engineering support was strong with

23

regard to involvement in field work and accessibility by craft

personnel.

Maintenance engineering activity involving failure

analysis, preventive maintenance, and material qualification was

effective.

The quality of engineering

and technical support has been

compromised by the quality of the communication between the

plart and DE. The OE/plant communication was identified as a

weakness

in the previous

assessment period and

has

been

demonstrated as a weakness during this assessment period.

The

DE organization failed to provide the plant with adequate

information regarding HPI

system mode requirements and Safe

Shutdown Facility HVAC configuration requirements.

The former

issue resulted in a violation

(see

violation (a)-Safety

Assessment/Quality Verification).

Although the initial

HPI

design deficiency was licensee identified the resolution was

initially inadequate due to a DE/plant communications failure.

Management

has

taken action to resolve the communication

problem. This action was to reorganize DE on a site dedicated

basis, establish a small on-site DE contingent to facilitate the

DE/plant interface,

and assign system engineers to selected

safety significant systems.

These actions were

not fully

implemented prior to the occurrence of the communications

deficiencies discussed above.

The operator training and requalification training programs are

good although some simulator weakness were identified during

this assessment period.

The

supplementation of

simulator

training staff with experienced plant operators on a two year

rotation was a notable contributor to training program quality.

Generally the simulator is

updated to incorporate Unit 1

modifications,

however,

simulator hardware

and

software

nonconformances existed this assessment period which impacted

the value of simulator training.

An example of a hardware

nonconformance was

the control

instrumentation

for the

Pressurizer Power Operated Relief Valve which differed between

the control room and simulator.

A modification completed at the

end

of

the

assessment

period

corrected this

hardware

nonconformance.

The Loss of Instrument Air simulation which did

not accurately reflect the actual plant evolution was an example

of a software -nonconformance.

Although the overall training

program was generally good,

simulator nonconformances which

required performance compensations by the operators-in-training

impacted the value of the training.

Two

replacement examinations were

administered during the

assessment period. Eleven of eleven SRO candidates passed and

six of seven RO candidates passed. Material submitted for exam

24

development contained minor information deficiencies but was

generally adequate and legible.

The violation identified below is an outage related violation.

During refueling outages on all three units, containment

isolation was compromised by open one-inch emergency hatch

equalizing valves and small gaps (3 to 4 square inches) in hatch

seals.

These failures to maintain containment isolation were

the result of an inadequate temporary modification and

inadequate attention to detail regarding all aspects of

maintaining containment isolation during refueling outages.

This violation was identified by Duke Power staff and reported

to the NRC.

One violation was identified during this assessment period.

a. Severity Level IV for failure to maintain containment

conditions during refueling outages (87-49)

2. Performance Rating

Category: 2

Previous Rating:

Engineering Support 2

Training 2

3.-- Recommendations

The board noted an improved performance in this area over the

assessment period. While many positive attributes were observed

in this area relating to self-identified plant problems, there

was recurring weakness in the quality of communications between

design engineering and other plant organizations.

To achieve

further improvement, management attention is required in this

area.

G. Safety Assessment/Quality Verification

1. Analysis

This section includes an assessment of licensee activities

associated with the implementation of licensee safety policies;

licensee activities related to amendment, exemption and relief

requests; response to Generic Letters, Bulletins, and other NRC

initiatives.. This section also includes licensee activities

related to the resolution of safety issues and self assessment

activities.

The evaluation of licensee activities is based upon observations

of numerous licensing actions active or completed during the

assessment period. This included about 252 licensing activities

for the three Oconee units, of which 54 were licensing

amendments completed during this period.

25

Management involvement is evident at the corporate

and station

levels through planning

and

assignment of priorities for

activities associated with licensing.

Duke

is an active

participant and often assumes leadership roles for the industry

regarding generic issues. This industry involvement includes,

for example, the Association of Edison Illuminating Companies,

NUMARC,

various codes and standards committees,

owners group

committees,

trade groups much as the American Nuclear Society

and Health Physics Society and numerous others.

The extent of

Duke's involvement is commendable and much is accomplished that

could not be achieved on an individual plant basis.

However,

Duke has not provided timely resolution and implementation of

several significant, longstanding generic issues for Oconee such

as ATWS mitigation design approvals, Regulatory Guide 1.97 and

several TMI issues.

Duke is also an active participant in the B&W Owners Group

(BWOG)

safety and performance improvement program (SPIP)

which

has

recommended

numerous

modifications

to

enhance

plant

performance. Duke has made significant contributions to the

SPIP and has incorporated a large number of these recommenda

tions at Oconee.

However, a significant number

which should

enhance performance of systems such as the main feedwater system

and the integrated control system are still being evaluated

for implementation.

Duke's staff generally displays in-depth knowledge of the plant

and of technical and regulatory issues.

Duke tends to be well

prepared and to provide ample support during meetings, site

visits and conference calls.

Licensee Event Reports submitted by the licensee were generally

well written and provided a sufficient depth of information.

The reports describe the relevant aspects of the events,

including component or system failures that contributed to the

events and the significant corrective actions taken or planned

to prevent recurrence.

Previous similar occurrences were

appropriately acknowledged in the reports.

The licensee has demonstrated the capability to identify plant

problems and has dedicated resources to resolve these problems.

Mechanisms to identify plant

problems

include corporate

self-initiated technical audits (SITA),

audits required by

Technical Specification 6.1.3 information sharing with other

Duke plants, and a design calculation review program. The SITA

program and design calculation review program were developed

using the

NRC Safety System Functional

Inspection (SSFI)

philosophy as guidance.

Oconee developed a prioritized list of

systems which they will examine.

These mechanisms identified

problems related to the High Pressure Injection (HPI)

system,

start-up transformer circuit breakers, containment penetration

fire barriers, Reactor Building Cooling Unit (RBCU)

capacities,

26

electrical sliding link problems,

and emergency power system

overloading.

The resources

to evaluate and resolve these

problems,

particularly the

RBCU fouling problems,

have

been

considerable and reflect management commitment to operate and

maintain a safe plant. Engineering activity in response to an

NRC identified potential control panel configuration control

problem was timely and comprehensive once the operability

impact implications were recognized.

Additionally, the

Oconee

performance group and

design

engineering have been extensively involved in heat transfer

performance testing of the Reactor Building Cooling Units (RBCU)

for most of this assessment period.

Due to fouling problems

discovered at McGuire, Duke began looking at all heat exchangers

for reduced

heat removal

rates

due to fouling.

It was

discovered by performance testing and calculations that the

RBCU's were not capable of removing their design heat capacity

due to both air and water side fouling.

Although the problem

has not yet been fully resolved, this group (with support from

design engineering personnel) has dedicated significant effort

toward resolution of this issue.

Duke has displayed a

cooperative attitude with the NRC regarding its experiences in

this field which has been a benefit to the NRCs efforts to

develop generic conclusions and assess the need for future

regulatory-guidance.

The station manager initiated a program to conduct detailed

reviews of specific INPO Significant Operating Event reports

(SOERs).

This review consists of extensive discikssion and

analysis

sessions

involving most of the

senior onsite

management. Several changes contributing to safety enhancement

have been incorporated into procedures as a result of these

discussions.

Breakdowns in communication, however, have hindered the

resolution of problems once they have been identified.

One

significant example

of this, which resulted

in escalated

enforcement,

was the failure of Design Engineering to provide

the plant with adequate information regarding HPI system mode

requirements. This resulted in a lack of procedural guidance

associated with the high pressure injection "piggyback" mode of

operation (violation a).

Another example of a communication

breakdown as mentioned in the Engineering/Technical

Support

section was the Safe Shutdown Facility HVAC system circulating

water pump requirements.

27

The licensee provided timely, sound responses to NRC generic

letters, and bulletins.

This was evident in the licensees

resolution of issues in NRC Bulletins on main steam safety

valves,

masonary

wall

designs,

nonconforming

materials

and fastener testing.

Oconee initiated a program during this SALP assessment period to

upgrade 10 CFR 50.59 evaluations.

This resulted in improved

evaluations for permanent and temporary modifications, however,

documentation of some evaluations for valve replacements and

alarm/setpoint

changes

was

weak.

This

resulted

in

violation (b).

Another example of this problem is addressed in

the Maintenance/Surveillance section.

Two violations were identified during this assessment period.

a. A Severity Level III violation with a $50,000 civil

penalty for a lack of procedural guidance associated with

high pressure injection piggyback operation during a loss

of coolant accident. (88-25)

b.

Severity Level V violation for failure to provide the basis

for determination that changes did not affect an unreviewed

safety question for multiple alarm and set point changes

(88-13)

2.

Performance Rating

Category: 2

Previous Rating:

Quality Programs 1

Licensing Activities 2

3.

Recommendations

Management attention as provided during the latter portion of

this SALP period should continue in this area.

V.

SUPPORTING DATA

A.

Escalated Enforcement Actions

1. Civil Penalties

Severity Level III violation issued on December 13,

1988 for a

lack of procedural

guidance associated with high pressure

injection "piggyback" mode of operation during a loss of coolant

accident. ($50,000 CP)

28

2.

Orders

August 6, 1987 -

Elevated lake water temperature, Oconee 1

August 19, 1987 -

Elevated lake water temperature, Oconee 2

B.

Management Meetings

October 27, 1987

-

SALP meeting with licensee at Oconee

site

March 1, 1988

-

NRC/DPC meeting at NRC office in

Washington to discuss Integrated Safety

Assessment Program

January 15, 1988

-

Enforcement Conference at Region II

related to protection of safeguards

information in electronic transmission

January 28, 1988

-

Technical meeting with Duke Design

Engineering in Charlotte, NC to discuss

current issues and concerns

June 7, 1988

-

Meeting in Atlanta Region II offices

to discuss findings of

NRC

Quality

Assurance Team

July 1, 1988

Enforcement Conference at Region II

related to environmental qualification

of electrical equipment

September 8, 1988

-

Meeting at Oconee to discuss fouling

of Reactor Building Cooling Units

September 12, 1988

-

Enforcement Conference at Region II

related to high pressure injection

"piggyback" mode of operation

29

October 6, 1988

-

Enforcement Conference at Region II

related

to

potential

degraded

capabilities of the Reactor Building

Cooling Units (RBCU)

January 6, 1989

-

Enforcement Conference at Region II

related to the inadequate design of the

Lee Station transmission system

January 12, 1989

-

Meeting at Oconee site by with Duke

Licensing group,

NRC licensing Project

Managers, and NRC Region II personnel

C.

Confirmation of Action Letters (CAL)

January 5, 1989

-

CAL issued following switchgear fire

to maintain equipment related to the

fire in the "as found" condition

0.

Review of Licensee Event Reports (LERs)

During the evaluation period,

29 LERs for Units 1, 2, and 3 were

analyzed. The distribution of the events by cause, as determined by

the NRC staff, was as follows:

Cause

Total

Component

4

Design

7

Construction, fabrication

or installation

0

Personnel:

-

operating activity

3

- maintenance activity

2

- Test/calibration activity

6

- Other

4

Other

3

29

E.

Licensing Activities

During the evaluation period, review of 252 licensing actions and 54

licensing amendments was completed for the three Oconee units.

30

F.

Enforcement Activity

No. of Deviations and Violations in

Functional

Each Severity Level

Area

Dev.

V

IV

III

II

I

Plant Operations

2

Radiological Controls

2

Maintenance/Surveillance

4

9

Emergency Preparedness

Security

2

5

Engineering/Technical

1

Support

Safety Assessment/Quality

1

1

Verification

TOTAL

7

19

1

G.

Reactor Trips

.

A total of five automatic trips occurred during this rating period,

two on Unit 1, one on Unit 2 and two on Unit 3.

Seven automatic trips occurred during the previous rating period. One manual trip

was also experienced. The trips are described in more detail below.

1.

Unit 1

a. On July 5 an automatic trip occurred from 100% power due to

an error by an Instrument and Electrical (I&E)

technician

while troubleshooting a turbine header pressure instrument.

b. On January 2, 1989, a trip from 100% power occurred during

surveillance of the Reactor Protection System due to an I&E

technician error.

Channel D was tripped when Channel A was

also in a tripped condition.

c.

On January 3, 1989, a manual trip from less than 15% power

due to a fire in a 6900V Reactor Coolant Pump switchboard.

2.

Unit 2

a.

On August 26,

1988,

an automatic trip occurred from 100%

power due to a anticipatory reactor trip on turbine trip

caused by a faulty Moisture Separator Reheater high level

instrument.

31

3.

Unit 3

a.

On November 14,

1988,

the reactor tripped from 100% power

due to a main turbine trip.

The reason for the main

turbine trip could not be identified and the reactor

returned to power.

b.

On November

14 while recovering from the trip discussed

above, the reactor again tripped. Power was at 39% and the

reason for the trip was a main turbine trip due to faulty

relay in the steam generator high level circuitry.

The

reactor tripped

due

to

high reactor

coolant

system

pressure.

H.

Effluent Release Summary

(First

Half)

Activity Released (Curies)

1985

1986

1987

1988

1. Gaseous Effluents

Fission and Activation

2.35 E+4 2.43 E+4

1.05 E+4

1.85 E+4

Products

lodines and

6.14 E-3 5.41 E-2

1.58 E-2 9.74 E-2

Particulates

2. Liquid Effluents

Fission and Activation

4.16 EO

5.85 EO

2.90 EO

1.57 EO

Products

Tritium

1.24 E+3 1.34 E+3 9.49 E+2 4.28 E+2