ML14181A572

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Insp Rept 50-261/94-16 on Stated Date.Violations Noted. Major Areas Inspected:Operational Safety Verification, Surveillance Observation,Maint Observation & Followup on Previously Identified Items
ML14181A572
Person / Time
Site: Robinson Duke Energy icon.png
Issue date: 07/08/1994
From: Christensen H, Ogle C, William Orders
NRC OFFICE OF INSPECTION & ENFORCEMENT (IE REGION II)
To:
Shared Package
ML14181A569 List:
References
50-261-94-16, NUDOCS 9407290387
Download: ML14181A572 (22)


See also: IR 05000261/1994016

Text

pA REGu

UNITED STATES

o 0NUCLEAR

REGULATORY COMMISSION

REGION II

101 MARIETTA STREET, N.W., SUITE 2900

ATLANTA, GEORGIA 30323-0199

Report No.:

50-261/94-16

Licensee:

Carolina Power and Light Company

P. 0. Box 1551

Raleigh, NC 27602

Docket No.:

50-261

License No.: DPR-23

Facility Name: H. B. Robinson Unit 2

Inspection Conducted: May 22 - June 24, 1994

Lead Inspector: 9

4

7

O

.

rders Senior Resident Inspech r

4ate

Signed

Other Inspector:,--j2

.

. R. Ol, Resident Inspector

Date Signed

Approved by: j I 5C

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H. D.Christensen, Chief

Date Signed

Reactor Projects Section 1A

Division of Reactor Projects

SUMMARY

Scope:

This routine, announced inspection was conducted in the areas of operational

safety verification, surveillance observation, maintenance observation, and

followup on previously identified items.

Results:

A violation was identified involving an inoperable CV water level indication,

paragraph 3.b; an Unresolved Item was identified involving an inoperable post

accident containment vent path, paragraph 3.c; an apparent violation was

identified involving inadequate corrective actions to the findings of a

contracted surveillance program review, paragraph 6.a; a second apparent

violation was identified involving inadequate testing of the control room

ventilation system, paragraph 6.b; and a third apparent violation was

identified involving inadequate corrective actions associated with an MSIV

design deficiency, paragraph 6.c.

9407290387 940711

PDR

ADOCK 05000261

0

PDR

REPORT DETAILS

1.

Persons Contacted

R. Barnett, Manager, Projects Management

S. Billings, Technical Aide, Regulatory Compliance

A. Carley, Manager, Site Communications

B. Clark, Manager, Maintenance

  • T. Cleary, Manager, Mechanical Maintenance
  • D. Crook, Senior Specialist, Regulatory Compliance
  • W. Dorman, Manager, Corrective Action Program

J. Eaddy, Manager, Environmental and Radiation Support

  • D. Gudger, Specialist Regulatory Affairs

S. Farmer, Manager, Engineering Programs, Technical Support

B. Harward, Manager, Engineering Site Support, Nuclear Engineering

Department

  • M. Herrell, Acting Plant Manager

C. Hinnant, Vice President, Robinson Nuclear Project

  • J. Kozyra, Project Specialists, Licensing/Regulatory Programs
  • R. Krich, Manager, Regulatory Affairs

A. McCauley, Manager, Electrical Systems, Technical Support

  • G. Miller, Manager, Robinson Engineering Support Section
  • R. Moore, Acting Operations Manager
  • P. Musser, Manager, Engineering/Nuclear Assessment Department
  • D. Nelson, Acting Manager, Projects Management

M. Pearson, Plant General Manager

M. Scott, Manager, Reactor Systems, Technical Support

E. Shoemaker, Manager, Mechanical Systems, Technical Support

  • R. Wehage, Robinson Engineering Support Section

D. Winters, Shift Supervisor, Operations

  • L. Woods, Manager, Technical Support

Other licensee employees contacted included technicians, operators,

engineers, mechanics, security force members, and office personnel.

Acronyms and initialisms used throughout this report are listed in the

last paragraph.

2. Plant Status

The unit began the report period operating at 100 percent power, and

performed at power for the entire report period with no major

operational difficulties.

3. Operational Safety Verification (71707)

a.

General

The inspectors evaluated licensee activities to confirm that the

facility was being operated safely and in conformance with

regulatory requirements. These activities were confirmed by

direct observation, facility tours, interviews and discussions

with licensee personnel and management, verification of safety

system status, and review of facility records.

2

The inspectors reviewed shift logs, Operation's records, data

sheets, instrument traces, and records of equipment malfunctions

to verify equipment operability and compliance with TS. The

inspectors verified the staff was knowledgeable of plant

conditions, responded properly to alarms, adhered to procedures

and applicable administrative controls, cognizant of in-progress

surveillance and maintenance activities, and aware of inoperable

equipment status through work observations and discussions with

Operations staff members. The inspectors performed channel

verifications and reviewed component status and safety-related

parameters to verify conformance with TS.

Shift changes were

routinely observed, verifying that system status continuity was

maintained and that proper control room staffing existed. Access

to the control room was controlled and operations personnel

carried out their assigned duties in an effective manner. Control

room demeanor and communications were appropriate.

Plant tours were conducted to verify equipment operability, assess

the general condition of plant equipment, and to verify that

radiological controls, fire protection controls, physical

protection controls, and equipment tagging procedures were

properly implemented.

b.

Deenergized CV Water Level Instrument

At approximately 7:30 a.m. on May 26, 1994, during a review of CR

post-accident indicators, the inspectors observed that CV water

level as recorded on Channel 4 of stripchart recorder AR-100C, CV

Conditions Recorder, was indicating approximately -99 inches. The

inspectors questioned the shift supervisor on this reading since

the instrument typically indicates a small positive value for CV

water level.

Following a licensee investigation, the inspectors

were informed that this reading was in error, as a result of Level

Indicator, LI-802, Channel II CV Water Level being turned off.

The inspectors were also advised that LI-802 had been re-energized

and the stripchart indicator returned to normal.

The inspectors

independently verified CV water level indication returned to

normal on a subsequent CR tour.

The inspectors reviewed the ACR generated in response to this

event, written RO and SCO statements regarding the operation of

LI-802, and the stripchart printout for AR-100C. Based on this

review, the inspectors concluded that LI-802 became inadvertently

deenergized following the performance of instrument checks

coincident with shift turnover. As a result of this

deenergization, the number of CV Level (Wide Range) instruments

which were operable fell below the 2 minimum channels operable

required by TS Table 3.5.-5, Instrumentation To Follow The Course

Of An Accident. (This TS table does permit operation with one

channel of CV Level (Wide Range) inoperable for 30 days prior to

submitting a special report to the NRC.)

This condition existed

for approximately an hour until questioned by the inspectors.

The

3

inspectors concluded that this entry into the 30-day LCO permitted

by TS Table 3.5.-5 was unrecognized by the shift as a result of

their not knowing the status of LI-802.

Technical Specification 6.5.1.1 Procedures, Tests, and Experiments

requires in part that written procedures be established,

implemented, and maintained, covering the activities recommended

in Appendix A of Regulatory Guide 1.33, Revision 2, 1978,

including procedures for safe operation of the facility.

Operations Management Manual Procedure, OMM-038, Operations

Organizational Responsibilities is provided to define and

delineate the duties and responsibilities of Unit 2 Operations

personnel.

OMM-038 requires that the Shift Supervisor, Senior

Control Operator, and Control Operators be aware of the status of

plant equipment.

On May 26, 1994, control room operators failed to detect that

Level Instrument, LI-802, Channel II, Containment Vessel Water

Level, a Technical Specification required instrument was

deenergized for approximately an hour. This condition went

unrecognized until a related display of CV water level was

questioned by the inspectors. This is identified as a violation,

VIO: 94-16-01, Inoperable CV Water Level Indication.

c.

Inoperable Post Accident Containment Vent Path

On May 31, 1994, during a routine tour of the BIT room, the

inspectors observed that the inlet and outlet dampers for the B

PACV filter were shut with clearance tags attached. The

inspectors questioned the shift supervisor on the operability of

the system given that the dampers blocked flow through the B train

PACV flowpath. Specifically, the inspectors were concerned that

access to these dampers would be restricted following a LOCA due

to prohibitive radiation levels from adjacent piping in the BIT

room which would contain post-recirculation sump fluid.

Later that day, the clearance tags were removed, the dampers were

returned to the open position, and the PACV flowpath was returned

to service.

On June 8, 1994, the inspectors were advised that potential

radiation exposures would not have precluded restoring the system

when required following a LOCA. Based on times obtained to

restore the dampers during trial runs and calculated radiation

levels 30 days after a LOCA, the licensee stated that the train

could be returned to service with an exposure of about 150 mRem.

Investigation pertaining to the cause of this event continues at

the end of this report period.

4

This item will be tracked as an Unresolved Item pending the

conclusion of that investigation, URI: 94-16-02, Inoperable Post

Accident Containment Vent Path.

4.

Maintenance Observation (62703)

a.

General

The inspectors observed safety-related maintenance activities on

systems and components to ascertain that these activities were

conducted in accordance with TS, approved procedures, and

appropriate industry codes and standards. The inspectors

determined that these activities did not violate LCOs and that

required redundant components were operable. The inspectors

verified that required administrative, material, testing,

radiological, and fire prevention controls were adhered to. In

particular, the inspectors observed/reviewed the following

maintenance activities detailed below:

WR/JO 94-AIBC1

Replace EDG A.Control Side Exhaust Manifolds

WR/JO 94-AIBDI

Replace EDG A Opposite Control Side Exhaust

Manifolds

WR/JO 94-AGTR1

Remove Shipping Covers From A EDG

No violations or deviations were identified.

5.

Surveillance Observation (61726)

The inspectors observed certain safety-related surveillance activities

on systems and components to ascertain that these activities were

conducted in accordance with license requirements. For the surveillance

test procedures listed below, testing was accomplished by qualified

personnel in accordance with an approved test procedure, test

instrumentation was properly calibrated, and the tests conformed to TS

requirements. Upon test completion, the inspectors verified the

recorded test data was complete, accurate, test discrepancies were

properly documented and rectified, and the systems were properly

returned to service. Specifically, the inspectors witnessed/reviewed

portions of the following test activities:

OST-409

Emergency Diesels (Rapid Speed Start) (B EDG

Only)

No violations or deviations were identified.

5

6.

Licensee Action on Previous Findings (92701, 90702)

a.

Enercon Study

Introduction

URI 94-04-02 documents inspectors' concerns associated with 18

potential surveillance test deficiencies identified by Enercon

Services, Inc., in a TS surveillance program review completed

June 30, 1992. The inspectors' concerns centered on two issues.

First, the failure of the licensee to take corrective action

immediately after the deficiencies were identified, and second,

the possibility that TS required surveillance were not performed

properly as a result of inadequate surveillance procedures. The

following discussion will review the historical background

associated with the Enercon Study, provide an overview of the 18

issues identified by Enercon, and briefly review the disposition

of these items by the licensee.

Background

LER 90-005, identified a failure to test RPS logic in accordance

with TS requirements. Based on similar previous occurrences

dating back to 1984, this deficiency was captured by VIO 90-11-01

as Failure To Take Adequate Corrective Action To Preclude

Repetition Of Inadequate Procedures Involving TS Required Tests.

In their September 21, 1990, supplemental response to the

violation, the licensee outlined their three-phase program to

prevent recurrences of additional inadequate surveillance testing

or TS non-compliance. Phase 3 of this program included an in

depth procedural verification of TS Table 4.1-1, Minimum

Frequencies For Checks, Calibrations, And Tests Of Instruments.

Enercon Services, Inc. was the contractor assigned to perform this

review. The project procedure for Enercon's review required that

significant inadequacies in surveillance test procedures be

documented on STP Review Deficiency Forms.

(Alternate procedures

were implemented for inadequacies characterized as immediate

safety concerns and for deficiencies of an administrative nature.)

Eighteen such STP review deficiency forms were provided in the

June 30, 1992, project final report.

In late December 1993 or early January 1994, the inspectors became

aware of and reviewed the Enercon report while researching an

unrelated deficiency in-containment spray system actuation

testing. On January 6, 1994, the inspectors questioned plant

management on the implication of the following statement contained

in the conclusions section of the final Enercon report:

"An important finding that came out of the Table 4.1-1

review was that many deficiencies that had been previously

attributed to Table 4.1-1, and in particular, Item 27, Logic

Channel Testing, were more appropriately associated with

6

other TS, such as Table 4.8-1 or SR 4.6.1.2 and other system

surveillance, because of the structure of the RNP TS. The

test circuitry that was found to be most often not

adequately tested, deals with ESFAS actuation circuitry.

Therefore, while there is high confidence that deficiencies

associated with required testing for Table 4.1-1 have been

identified and can be corrected, the overall acceptability

of the surveillance testing program is unknown until these

other TS surveillance, which have known problems, have had a

comprehensive review. Without an evaluation of the

procedures associated with these system-type surveillance,

additional failures to adequately comply with the TS SR

[surveillance requirements] are likely."

Following this questioning, the licensee instituted a detailed

review of the 18 Enercon deficiencies. Of the eighteen items, two

were considered reportable by the licensee and were the subject of

LER 94-001 dated March 7, 1994. The technical aspects of the LER

related to these two items are discussed below.

An April 15, 1994, supplement to the LER reviewed the failure of

the plant organization to promptly disposition the 1992 Enercon

report. The LER concluded that this failure was "...the result of

the lack of management oversight for the overall project."

The

supplemental LER notes that no plans or schedules were established

to track resolution of the 18 items nor was a methodology in place

to resolve differing views of the technical adequacy of the 18

items.

On June 29, 1994, during the exit interview for this inspection

report, the inspectors were advised by the licensee that the

Enercon report issues had also been raised independently by the

plant staff as a part of the restart readiness review. The

inspectors did not independently verify this statement. However,

based on the intensive review of backlog issues conducted by the

licensee coincident with startup on the early 1994 timeframe, the

inspectors concluded that this assertion was plausible.

Enercon Study Results

The following eighteen items were identified as surveillance test

procedure review deficiencies by the Enercon study:

1.

HBR does not utilize a master surveillance scheduling

system.

2.

The power supplies of the protection instrument

channels are not tested.

3.

Indicators on which channel checks are performed are

not listed.

7

4.

The test procedures used to satisfy TS channel

calibration requirements in general do not ensure

adequate overlap from sensor to actuating device.

5.

Incorporation of span and zero shift compensation due

to high static pressure could not be verified.

6.

Disagreement exists between MMM-006, Calibration

Program and the vendor technical manual on the

accuracy for Rosemount transmitters used to measure

reactor coolant flow.

7.

Channel calibrations do not include provisions to

check alarms.

8.

An overall program that contains or addresses

instrument setpoint calculations could not be found.

9.

The procedure used to calibrate the overpressure

protection system does not include the actuation of

the PORV solenoids.

10.

Inadequate functional testing and calibration of CV

wide range pressure instruments.

11.

Inadequate functional testing and calibration of CV

wide range level instruments.

12.

There is no functional testing performed on a monthly

basis on the 4kV undervoltage circuits as required by

TS.

13.

A difference exists between various documents

regarding the correct time delay for the 4kV

undervoltage time delay.

14.

Channel checks or channel functional tests were not

being performed on AFW flow indicators as required by

TS.

15.

Portions of TS required surveillance of the boric acid

makeup flow channel and RVLIS are performed using

vendor technical manuals instead of station

procedures.

16.

The logic associated with the IR block, low setpoint

power range block and P-10 is not tested until 75

percent power is reached.

[A situation could result

during a shutdown following an aborted startup in

which reliance was required on protection circuitry

that had not been tested.]

8

17.

Continuity checks on Engineered Safeguard equipment

specified in TS Bases 4.5 are not being performed.

18.

The recorder for power range detectors, the radiation

monitor recorder, and incore thermocouple recorder are

not being calibrated. [R.G. 1.97 concern]

IR 94-04 documents a previous inspection by a Region II based

specialist of the licensee's review and corrective actions

associated with these items. That inspection report, dated

March 22, 1994, concluded that the licensee had addressed these

issues in a satisfactory manner for restart.

Following that inspection effort, the licensee conducted a

reportability evaluation of the eighteen Enercon items. That

evaluation documented the licensee's technical interpretation of

the 18 items; outlined corrective action taken where deemed

necessary; and evaluated the reportability of the items. The

disposition of the items ranged from dismissing the concern due to

a lack of technical merit to revising plant procedures in order to

correct the identified deficiency.

This reportability evaluation concluded that Item 9 (inadequate

calibration of overpressure protection system) and Item 12 (lack

of monthly functional testing of the 4kV undervoltage devices)

were reportable. On March 7, 1994, these items were reported in

LER 94-001.

This report was made pursuant to 10 CFR 50.73 (a)(2)

(i)(B) as a condition prohibited by TS, since surveillance

requirements were not fully complied with and the associated TS

actions were not taken within the allowed time interval.

The

inspectors reviewed the LER and technical documentation associated

with these issues.

Item 9 of the Enercon study dealt with the failure to adequately

test the PORV actuation circuitry during monthly testing. The

concern centered on shortcomings in the licensee's surveillance

procedure which prevented testing the entire loop. The Enercon

report identified that the circuitry from bi-stables PC-502 and

PC-503 through auxiliary panel relays and permissive switches to

the associated solenoids was not tested. LER 94-001 acknowledged

this concern and outlined the corrective actions taken to resolve

this issue. These included a verification of the circuit

continuity and a modification to the surveillance test. The

inspectors noted from a review of Maintenance Surveillance Test,

MST-007, Reactor Coolant Low-Temperature Overpressure Protection

System Test (Monthly) that the procedure had been revised to

incorporate a measurement of voltage immediately upstream of the

test switch once bistables PC-502 or PC-503 had been actuated. In

their reportability evaluation for this item, the licensee also

took credit for the performance of Operations Surveillance Test,

OST-703, ISI Primary Side Valve Test Cold Shutdown Greater Than 48

Hours, as testing the circuit from test switch to the PORV

9

solenoids. These two items were evaluated by the licensee as

providing the supplemental testing required to verify the entire

PORV actuation circuitry thereby resolving the Enercon concern.

On June 28, 1994, the inspectors questioned the licensee's

resolution of this issue. Specifically, the inspectors were

concerned that no post-MST-007 verification of the test switch

continuity was conducted. The inspectors noted that with the

energize to actuate design of the PORV circuitry, an undetected

interruption in the PORV's actuation circuit at the test switch

following testing could render the valves inoperable. Similar

concerns had been identified by the licensee previously for the

energize to actuate containment spray system logic. The inspectors

will monitor the licensee's resolution of this issue.

Item 12 of the Enercon study dealt with the failure of the

licensee to conduct a functional test of the 4kV undervoltage

device on a monthly basis. These devices provide an anticipatory

trip signal when an undervoltage condition is sensed on the RCP

busses. These trips are the subject of line item 8 in TS Table

4.1-1. This failure was attributed by Enercon to a

misinterpretation by the licensee of a note contained on the

remarks section of TS Table 4.1-1, Minimum Frequencies For Checks,

Calibrations, and Tests Of Instrument Channels. This note, in the

4kV undervoltage section of the table, specifies "Reactor

Protection circuits only."

As documented in the Enercon report,

this had been previously interpreted to imply that only the logic

portion of the circuit was to be tested at the frequencies

specified in the TS table. LER 94-001 documents the licensee's

subsequent reevaluation of this note. Following this revised

interpretation, Special Procedure, SP-1294, Testing of 4kV

Undervoltage Trip Only For The Input To The Reactor Protection

Circuitry, was developed and successfully performed on January 30,

1994. The inspectors reviewed SP-1294 and have no further

questions on Item 12 of the Enercon report.

On June 14, 1994, the licensee recognized that potentially non

conservative values existed for the actual high steam flow ESF

setpoints.

Item 5 of TS Table 3.5-1, Engineered Safety Feature

System Initiation Instrument Setting Limits, requires that these

setpoints be less than or equal to 40 percent of full steam flow

below 20 percent power and less than or equal to 110 percent of

full steam flow at 100 percent power. It was recognized by the

licensee during the turbine first stage pressure channel accuracy

and scaling calculation, calculation RNP-I/Inst-1045, that the

actual setpoint exceeded the TS limit of 110 percent rated flow by

1.5 percent at 100 percent power. This incorrect setpoint

occurred as a result of changes made to the high steam flow

bistable setpoints based on measured steam flows in lieu of the

analytical limits used in the Updated FSAR. This change was

justified in Engineering Evaluation 87-201 in order to reduce the

occurrence of previously experienced steam flow instrument channel

activations observed during cold weather. The inspectors were

10

advised that the turbine first stage pressure accuracy calculation

during which this error was uncovered was part of the instrument

setpoint calculation effort.

Item 8 of the Enercon study identified as a deficiency, the lack

of an overall program that contained or addressed the instrument

setpoint calculations. The study recommended that a program be

developed to address instrument setpoint calculations. The

inspectors noted that while a Plant Improvement Request for a

setpoint methodology study was approved in 1989, work in earnest

on the program did not begin until January 1994. This occurred

following the detailed review of the Enercon report in January

1994 and on the heels of several other high visibility instrument

calibration issues at the HBR facility in 1993. The inspectors

also noted that this setpoint effort was initiated approximately

18 months after the June 1992 Enercon recommendations for such a

study.

Conclusions

The inspectors concluded that the licensee failed to take adequate

corrective action in a timely fashion to potential TS deficiencies

identified by Enercon in June of 1992. The failure of the

licensee to move forward on these issues after they were initially

identified, resulted in a delay of almost 18 months in resolving

deficiencies in the implementation of two TS required

surveillances.

Furthermore, the delay in implementing the

Enercon recommended setpoint study (a need identified internally

by CP&L in 1989) postponed recognition and resolution of

improperly set ESF high steam flow bistable setpoints.

10 CFR 50 Appendix B, Criterion XVI, Corrective Action, requires

in part that measures be established to assure that conditions

adverse to quality, such as failures, malfunctions, defective

material and equipment, are promptly identified and corrected.

On June 30, 1992, the licensee failed to promptly act upon 18

potential deficiencies identified by Enercon. Subsequent review

of these issues in January 1994 revealed deficiencies in the

implementation of two TS required surveillances. Furthermore, in

June 1994, during the conduct of a setpoint calculation study

recommended by the Enercon study, ESF high steam flow bistable

setpoints in excess of TS limits were discovered.

This is identified as an apparent violation, VIO 94-16-03, Failure

To Take Adequate Corrective Action To Potential Technical

Specification Deficiencies Identified By Enercon In June 1992.

b.

Control Room Ventilation Testing Deficiencies

Introduction

Unresolved Item 94-15-05, Control Room Ventilation System

Operability documented inspector concerns pertaining to the

licensee's testing methodology associated with determining the

ability of the control room ventilation system to maintain the

control room envelope at a positive pressure with respect to all

adjacent areas during an accident. At the end of that report

period, investigation pertaining to the testing methodology, the

past operability of the system, and the associated safety

significance were continuing.

The following delineates the

results of the analysis.

Background

During an inspection which ended on May 6, 1994, the results of

which are documented in Inspection Report 94-14, a Region II

inspector questioned the licensee's testing methodology associated

with confirming the ability of the control room ventilation system

to maintain the control room at a positive pressure with respect

to all adjacent areas during an accident. The inspector noted

that previous testing assessed the system's ability to maintain a

positive pressure relative to the outside atmosphere, but did not

verify the system's ability to maintain a positive pressure in the

control room envelope with respect to adjoining plant spaces,

which is a design basis function.

This departure from the test

methodology as described in the UFSAR, was identified to the

licensee as an apparent Deviation. The resident inspectors

questioned the system's ability to perform its intended safety

function, given the apparent inadequate scope of system testing.

The Plant Manager directed his staff to perform the testing

necessary to determine system operability.

On the afternoon of May 6, 1994, the control room ventilation

system was tested in the emergency pressurization mode to

determine if the system could produce and maintain a positive

pressure relative to adjacent areas.

The testing revealed that

the control room could only be pressurized to a pressure

approximately equal to an adjacent electrical equipment room, the

Hagan Room. By modifying the system's air flow balance, the

licensee was successful in creating a positive pressure between

the control room and the Hagan room, as well as all other adjacent

areas.

On the following day, an auxiliary building exhaust fan was turned

off to support ongoing auxiliary building ventilation flow balance

efforts. This resulted in another electrical equipment room

adjacent to the control room, the E/E2 room, going to a pressure

higher than that in the control room.

This pressure appeared to

be greater than the maximum pressure differential attainable by

12

the control room ventilation system when in the emergency

pressurization mode, based on the previous day's testing. It was

concluded that in the past, the E1/E2 room would have been at a

positive pressure with respect to the control room during certain

accident scenarios. The licensee restarted the auxiliary building

exhaust fan, and declared the control room ventilation system

inoperable until the issue could be resolved.

After assessing the system configuration, the licensee de

energized the auxiliary building supply fan which created a large

negative pressure in the auxiliary building. This resolved the

immediate concern relative to differential pressure between the

E1/E2 room and the control room. Subsequently, the licensee

restarted the auxiliary building supply fan after applicable

procedures were modified to de-energize the auxiliary building

supply fan during certain accident scenarios.

At the end of report period 94-15, the control room ventilation

system had been balanced to maintain the control room at a

positive pressure with respect to adjacent areas during accident

scenarios.

The licensee's evaluation concluded that this event was caused by

a failure to adequately understand and incorporate the licensing

basis for the system into the system's surveillance test program.

The licensee's proposed corrective actions include revision of the

appropriate plant procedures to ensure conservative testing.

Event Details

As previously stated, on May 7, 1994, Unit 2 was operating at 100

percent power. Auxiliary building ventilation system flow

balancing was in progress in an area containing emergency buses El

and E2 (i.e., E1/E2 Room).

This room is located in the auxiliary

building and is below the control room with a common floor/

ceiling. When the E1/E2 room exhaust fan, HVE-7 was secured for

the flow balancing activities, the air pressure increased in the

immediate area and several rooms adjacent to the control room,

including a room containing the reactor protection and control

analog instrumentation relay racks, the Hagan Room. Licensee

analysis determined that, under certain accident conditions, HVE-7

would stop operating and that the non safety-related supply fan,

HVS-1, could not be relied upon to stop. Therefore, under such

conditions, the air pressure in these rooms could become more

positive than the control room air pressure. This is contrary to

the licensing basis of the plant, which states that the control

room envelope is to be maintained under a positive differential

pressure with respect to adjacent areas during the emergency

pressurization mode of operation.

The licensee concluded that the E1/E2 room pressure had exceeded

the control room post accident pressure, and that an unanalyzed

13

condition existed. Accordingly on May 7, 1994, at 3:56 p.m. the

NRC was notified via the Emergency Notification System of this

condition pursuant to 10 CFR 50.72(b)(1)(ii). The immediate

corrective actions taken were to re-start HVE-7, which resulted in

a pressure reduction in the E1/E2 Room, until additional

administrative controls could be put in place.

During subsequent flow balancing activities, the resident

inspectors raised questions concerning the amount of outside air

makeup going into the control room. The licensee determined that

during a system alignment to support auxiliary building

ventilation flow balancing (i.e., HVS-1 and HVE-7 secured), a

negative pressure in the room which contains the control room

ventilation system equipment had been developed, and due to

outside air makeup fan housing in-leakage, the outside air makeup

to the control room had indeed increased to approximately 420

cubic feet per minute (CFM), which is beyond Technical

Specification (TS) section 4.15 limit of 400 CFM. The exact

amount of air increase could not be positively determined.

However, to compensate for this concern, the outside air makeup

was adjusted and reduced to 340 CFM.

Analysis Of Event

This event was caused by the licensee's failure to adequately

understand and incorporate the system's licensing basis into the

system surveillance test program. Further, the control room

ventilation system design was incomplete, in that it did not

consider all auxiliary building ventilation system lineups and the

effects of these line-ups on the control room ventilation system.

The existing control room ventilation system was installed via a

modification during 1991.

The post-modification system test

demonstrated that the system design requirements were met in that

the system could reproduce and maintain a positive pressure in the

control room with respect to all adjacent areas. However,

periodic Operations Surveillance Test Procedure, OST-750, intended

to satisfy the requirements of Technical Specification (TS) 4.15,

does not ensure a positive pressure is maintained with respect to

areas adjacent to the control room other than the outside, as

committed to in the Updated Final Safety Analysis Report (UFSAR).

Therefore, the ability of the system to perform its intended

function during the emergency pressurization mode of operation has

not been demonstrated since post-modification acceptance testing

in 1991.

The licensee's evaluation of the event indicated that the minimal

testing required by TS had been performed, but the control room

ventilation system testing committed to in the UFSAR had not been

incorporated into the surveillance testing program. Specifically,

the UFSAR states that the control room envelope is to be

maintained under a positive differential pressure with respect to

14

adjacent areas during the emergency pressurization mode of

operation. The UFSAR further states, that periodic testing is

required to demonstrate that the control room can be pressurized

to a minimum of 1/8 inch of water gage with respect to the

outdoors and during normal operation, the system will be

periodically tested to demonstrate that a positive pressure can be

maintained in the control room. The licensee's testing

methodology does not test the control room envelope with respect

to adjacent areas, nor does it contain an acceptance criteria of

1/8 inch of water gage pressure with respect to the outdoors.

The licensee's analysis also indicated that under certain accident

conditions, with specific equipment failure assumptions, the

control room could have been at a pressure less positive than

adjacent area pressures. This scenario could have potentially

resulted in a release of contaminated materials into the control

room envelope. However, calculations have been performed

demonstrating that plant operators would have up to one hour to

secure HVS-1 without radiation dose limits per the General

Criterion 19 of Appendix A to 10 CFR 50 being exceeded.

Accordingly, the licensee concluded that operating in this

condition had minimal effect on plant safety.

Corrective Actions

On May 8, 1994, exhaust fan HVE-7 and the supply fan HVS-1 were

secured, and the areas considered adjacent to the control room,

were verified to be at a pressure condition less than that of the

control room when the control room ventilation system was operated

in the emergency pressurization mode. Plant operating procedures

and emergency operating procedures were revised to place operating

restrictions on HVS-1.

In addition, the licensee plans to revise

Procedure EST-023 to reflect the testing requirements as specified

in the TS and the UFSAR.

Conclusions

Technical Specification 3.15.1 requires that during all modes of

plant operation, except cold shutdown, the Control Room Air

Conditioning System shall be operable with two trains of active

safety-related components and the shared safety-related passive

components.

10 CFR 50 Appendix B Criterion XI requires that a test program be

established to demonstrate that structures, systems, and

components will perform satisfactorily in service. Implicit in

this criterion is the requirement that the testing demonstrate the

ability of safety related components to perform their intended

safety function under design basis conditions.

Sections 6.4 and 9.4.2 of the Updated Final Safety Analysis Report

defines the intended safety function of the Control Room Air

15

Conditioning System to be, in part, the ability to maintain the

control room under a positive pressure with respect to adjacent

areas and the outdoors when the system is operated in the

emergency pressurization mode.

The test program established by the licensee to demonstrate that

the control room air ventilation system would perform it's

intended safety function was inadequate in that it did not ensure

that the system could produce and maintain a positive pressure in

the control room with respect to areas adjacent to the control

room and the outdoors.

On May 7, 1994, with the plant operating at 100 percent power,

licensee testing to confirm the operability of the control room

ventilation system revealed that pressure in a room adjacent to

the control room exceeded the control room pressure that would

exist during the emergency pressurization mode of operation. This

indicates that the system may have been incapable of performing

it's intended safety function since the system was installed in

1991.

This is an apparent violation, 94-16-04, Inadequate Control Room

Ventilation Testing Program.

c.

Inadequate Corrective Action To MSIV Design Deficiency

Unresolved Item 94-04-01, documented the resident inspectors'

concerns pertaining to inadequacies associated with MSIV testing

and design. The inspectors' primary concerns focused on the

licensee's failure to identify and correct a design deficiency in

the MSIV air accumulator volume, which resulted in the failure of

the valves to meet the TS required five second closure time and

the licensee's failure to comprehensively evaluate and act upon

available operating experience information including an

Information Notice (IN) incorporating H. B. Robinson as an

example, concerning the air accumulator design deficiency. The

issue was left open pending the completion of a licensee team

evaluation of the issue.

Event Summary

On January 29, 1994, the unit was in hot shutdown conditions.

During main steam isolation valve (MSIV) operability testing, all

three MSIVs were declared inoperable when they failed to meet the

Technical Specification (TS) required closure time.

The licensee subsequently determined that previous MSIV testing

had not demonstrated MSIV operability. This condition was caused

by the licensee's failure to correct an MSIV design deficiency. A

modification was implemented on February 7, 1994 to correct this

design deficiency, and all three valves were subsequently declared

operable.

16

Event Details

On January 29, 1994, the unit was in hot shutdown conditions at

normal operating temperature and pressure. During post

maintenance testing following removal, testing, and re

installation of the "A" Main Steam Isolation Valve control

solenoid, the MSIV failed to close within five seconds with non

safety-related instrument air supplied to the valve actuator.

Technical Specification (TS) 3.4.1.e states that the reactor shall

not be heated above 350 degrees F unless the MSIVs are operable

and capable of closing in five seconds or less. TS 4.7.1 states

that the MSIVs are tested at each refueling interval to verify

closure time of five seconds or less, and that the valves are

tested at no flow and at no load conditions. On January 30, 1994,

at 10:23 p.m., the "C" MSIV was tested to verify its capability to

close within five seconds after receiving a close signal at no

flow and at no load conditions. This MSIV also failed to meet the

stroke time requirements. As a result of the "A" and "C" MSIVs

failing to meet stroke time requirements, the "B" MSIV was tes

and it also exceeded the five second requirement. It should bv

noted, that this testing was performed with non-safety related

instrument air supplied to the valves.

Because the stroke times the three valves were in excess of five

seconds, the valves were declared inoperable in accordance with TS 3.4.1.e, and each valve was secured in its closed position in

accordance with the action statement of TS 3.6.3 for an inoperable

containment isolation valve. Subsequent testing determined that

with instrument air isolated to the MSIV actuators (i.e., only the

safety-related MSIV air accumulators providing the actuating

motive force), all three valves required in excess of five seconds

to close.

On April 25, 1994, following a review of the completed root cause

investigation of the MSIV failures, the licensee determined that

the previous practice of testing the MSIVs with instrument air

valved in, did not demonstrate valve operability. Review of

historical test data identified that MSIV testing was performed in

this configuration (i.e., with instrument air valved in) from 1984

to 1994. As a result, the capability of the MSIVs to perform

their design function had not been demonstrated since 1984.

Background Information

During November 1984, the NRC conducted an inspection of MSIV

testing. This inspection resulted in a Notice of Violation (NOV)

84-44-02 which stated that, contrary to American Society of

Mechanical Engineers (ASME) Code requirements invoked by TS 4.0.1.a, the MSIVs, as "fail-safe" valves were not being tested by

"observing the operation of the valves upon loss of actuator

power."

NRC Inspection Report 84-44 interpreted the requirement

as meaning that the MSIVs should be tested without use of

17

instrument air as the source of actuator power since instrument

air is a non-safety grade system.

On January 8, 1985, the MSIVs were tested under Special Procedure

SP-647, "Main Steam Isolation Valve Operability Test," with steam

line pressure at approximately 980 psig, no pressure differential

across the valve, and with instrument air isolated. The safety

related MSIV air accumulators provided the only motive force to

close the valves during the test. Although the valves closed, the

test did not confirm that closure times were within five seconds

since the valve stroke times were not measured. Conclusions from

the testing were that all three MSIVs closed, but drifted open

within ten minutes because accumulator pressure alone could not

keep the valves closed with no differential pressure across the

valve. To compensate for this concern, a temporary nitrogen

source was added to the valve actuators to provide the additional

motive force to keep the valves closed in the event of a loss of

instrument air.

The licensee's response to NOV 84-44-02 on March 8, 1985, stated

that the Procedure OST-702, "ISI Secondary Side Valve Test," was

intended to meet the ASME Section XI Code requirements. The

response further stated that the test was performed at cold

shutdown conditions, and that Procedure OST-501, "Main Steam

Isolation Valve (Refueling)," satisfied the operability

requirements of TS 4.7 (i.e., MSIV closure within five seconds) at

hot, no load conditions. At that time, no changes to Procedure

OST-501 were considered necessary. This response summarized the

results of the January 8, 1985, test and stated that a bottled

nitrogen backup to the MSIV actuators had been provided on an

interim basis to ensure adequate pressure is available to close

the valves within the safety analysis assumption for steam

generator tube rupture. The temporary nitrogen backup was removed

during 1986 by modification M-882. This modification also

installed a redundant solenoid in the closing side of the actuator

vent path, preventing the motive closing air from being vented off

of the actuator. However, post modification testing did not

ensure the valves would close within five seconds.

Analysis of Event

This condition was caused by the licensee's failure to correct a

design deficiency resulting in the failure of the valves to meet

the TS required five second closure time. Further, testing the

MSIVs with instrument air supplied to the actuators masked the

fact that the accumulators were not sufficiently sized to close

the valves within five seconds under hot, no load conditions.

Previous licensee analyses and reviews of changes to MSIV testing

procedures did not address the inconsistency between the Updated

Final Safety Analysis Report (UFSAR) statement that the instrument

air system is not required to function during accident conditions,

18

and the previous reliance on instrument air to meet TS required

closure time.

Contributing factors for this condition were inadequate post

modification test procedures for modification M-882 to demonstrate

MSIV operability, and the failure to evaluate and act upon

available operating experience information including an

Information Notice (IN)

concerning the air accumulator design

deficiency.

In 1985, an analysis was received from another utility that their

MSIVs would fail to close if instrument air was not utilized as an

additional motive force. The utility implemented a modification

to increase the accumulator volume to ensure required closure

times of the MSIVs with instrument air isolated. NRC Information

Notice 85-84, "Inadequate Inservice Testing of Main Steam

Isolation Valves," referenced ASME Section XI, and stated that

reliance should not be placed on non-safety related systems (e.g.,

instrument air) to mitigate the consequences of an accident. It

should be noted that Robinson was one of the plants discussed in

the Notice. As a result, modification M-882 was implemented to

ensure an adequate pressure source was available for closure of

the MSIV's. During the development of this modification, the

plant staff assumed that the accumulators would have sufficient

volume to close the MSIVs if a solenoid valve was added to the

vent path to prevent venting of the accumulator air. However, as

stated above, the post-modification testing did not verify

acceptable closure times.

TS 3.4.1.e states that the reactor shall not be heated above 350

degrees F unless the main steam stop valves (i.e., MSIVs) are

operable and capable of closing in five seconds or less. TS 4.7.1

states that the MSIVs are tested at each refueling interval to

verify closure time of five seconds or less, and that the valves

are tested at no flow and at no load conditions. While not

specifically required, the licensee has interpreted that this

testing should be at maximum steam pressure, with instrument air

isolated. Since MSIV testing was not consistently performed under

these condition from 1984-1994, MSIV operability was not

demonstrated.

Preliminary licensee analysis indicated that under certain

postulated accident conditions failure of a MSIV to close within

five seconds could have resulted in a release of radioactive

material that exceeds 10 CFR Part 100 limits.

Corrective Actions

On February 7, 1994, additional MSIV Accumulator tanks were

installed to provide an increased volume of compressed air to

assist MSIV closure within the required five second time period.

  • 0

'9

Following completion of this modification and subsequent post

modification testing, all three valves were declared operable.

Procedure OST-501 is to be conducted with the plant in hot

shutdown condition with the main steam header warmed and

pressurized. The procedure establishes a no flow condition

downstream of the MSIVs and is to be performed with instrument air

isolated.

Procedure OST-702 was revised to allow hot testing of the MSIVs by

including sections to establish a no flow condition downstream of

the MSIVs and isolation of instrument air during the MSIV

operability portion of the test.

The licensee stated that the Design Basis Document for the Main

Steam System will be revised to include references to the

licensing basis for the system and supporting calculations and

studies that define the details of expected MSIV performance.

The licensee also stated that the UFSAR will be revised to ensure

that it correctly characterizes the accident mitigation

requirements for the MSIVs.

Conclusions

10 CFR 50 Appendix B Criterion XI requires that a test program be

established to demonstrate that structures, systems, and

components will perform satisfactorily in service. Implicit in

this criterion is the requirement that the testing demonstrate the

ability of safety related components to perform their intended

safety function under design basis conditions.

The licensee's testing program failed to demonstrate the

capability of the main steam isolation valves (MSIVs) to perform

their intended safety function of steam generator isolation within

five seconds. This failure included:

Failure to test the MSIVs while in hot shutdown condition

between June 1992 and January 1994.

Failure to test the MSIVs with instrument air (a non-safety

related system) isolated while in hot shutdown between

January 1985 and January 1994.

Failure to verify the integrity of the MSIV accumulators and

their associated piping between January 1985 and January

1994.

10 CFR 50 Appendix B, Criterion III, Design Control, requires in

part that design control measures be implemented to ensure that

systems/components are capable of performing their intended safety

function, such as by design reviews or suitable testing programs.

20

The licensee's design control measures, as they pertain to the

main steam isolation valves, were inadequate, in that in January

1994, with the reactor in hot shutdown condition, the licensee

determined that the valves were incapable of closing in the

required time and/or remaining closed if instrument air, a non

safety related system, was isolated from the valve actuators.

This constitutes an Apparent Violation 94-16-05, Inadequate

Corrective Action Concerning MSIV Accumulator Volume.

9.

Exit Interview (71701)

The inspection scope and findings were summarized on June 27, 1994, with

those persons indicated in paragraph 1. The inspectors described the

areas inspected and discussed in detail the inspection findings listed

below and in the summary. Dissenting comments were not received from

the licensee. The licensee did not identify as proprietary any of the

materials provided to or reviewed by the inspectors during this

inspection.

Item Number

Description/Reference Paragraph

VIO: 94-16-01

Inoperable CV Water Level Indication

URI: 94-16-02

Inoperable Post Accident Containment Vent Path

Apparent Violation:

Inadequate Corrective Action to Potential TS

94-16-03

Deficiencies Identified By Enercon

Apparent Violation:

Inadequate Control Room Ventilation Testing

94-16-04

Program

Apparent Violation:

Inadequate Corrective Action Concerning MSIV

94-16-05

Accumulator Volume

10.

List of Acronyms and Initialisms

AFW

Auxiliary Feedwater

BIT

Boron Injection Tank

CR

Control Room

CV

Containment Vessel

EDG

Emergency Diesel Generator

ESF

Engineered Safety Feature

ESFAS

Engineered Safety Feature Actuation System

FSAR

Final Safety Analysis Report

HBR

H. B. Robinson

IR

Intermediate Range

LER

Licensee Event Report

LCO

Limiting Condition of Operation

LI

Level Indicator

LOCA

Loss Of Coolant Accident

PACV

Post Accident Containment Vent

21

MMM

Maintenance Management Manual

OMM

Operations Management Manual

OST

Operations Surveillance Test

PORV

Power Operated Relief Valve

RCP

Reactor Coolant Pump

RNP

Robinson Nuclear Plant

RO

Reactor Operator

RPS

Reactor Protection System

SCO

Senior Control Operator

SR

Surveillance Requirement

STP

Surveillance Test Procedure

TS

Technical Specification

URI

Unresolved Item

VIO

Violation