ML12318A341

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IR 05000285-12-005 and Notice of Violation, 08/19/2012 – 09/30/2012, Fort Calhoun Station, Integrated Resident, Inservice Inspection, and Confirmatory Action Letter Report
ML12318A341
Person / Time
Site: Fort Calhoun Omaha Public Power District icon.png
Issue date: 11/13/2012
From: Hay M
Division Reactor Projects III
To: Cortopassi L
Omaha Public Power District
Hay M
References
EA-12-174 IR-12-005
Download: ML12318A341 (56)


See also: IR 05000285/2012005

Text

November 13, 2012

EA-12-174

Louis P. Cortopassi, Site Vice President

Omaha Public Power District

Fort Calhoun Station FC-2-4

P.O. Box 550

Fort Calhoun, NE 68023-0550

Subject: FORT CALHOUN - NRC INTEGRATED INSPECTION REPORT NUMBER

05000285/2012005, AND NOTICE OF VIOLATION

Dear Mr. Cortopassi:

On September 30, 2012, the U.S. Nuclear Regulatory Commission (NRC) completed an

inspection at your Fort Calhoun Station. The enclosed inspection report documents the

inspection results which were discussed on October 18, 2012, with Mike Prospero, Plant

Manager, and other members of your staff, and on November 7, 2012, with you, and other

members of your staff.

The inspection(s) examined activities conducted under your license as they relate to safety and

compliance with the Commission=s rules and regulations and with the conditions of your license.

The inspectors reviewed selected procedures and records, observed activities, and interviewed

personnel.

Based on the results of this inspection a Severity Level IV violation of NRC requirements was

identified involving the failure to update the Updated Safety Analyis Report. This violation was

evaluated in accordance with the NRC Enforcement Policy. The violation is being cited in the

enclosed Notice of Violation (Notice) and the circumstances surrounding it are described in

detail in the subject inspection report. The violation is being treated as a cited violation,

consistent with Section 2.3.2(a)(3) of the NRC Enforcement Policy. Specifically, this violation

was repetitive as a result of ineffective corrective actions and was identified by the NRC.

You are required to respond to this letter and should follow the instructions specified in the

enclosed Notice when preparing your response. If you have additional information that you

believe the NRC should consider, you may provide it in your response to the Notice. The NRC

review of your response to the Notice will also determine whether further enforcement action is

necessary to ensure compliance with regulatory requirements.

One NRC identified finding of very low safety significance (Green) was identified during this

inspection. This finding was determined to involve a violation of NRC requirements. The NRC is

treating this violation as a noncited violation consistent with Section 2.3.2 of the Enforcement

Policy.

UNITED STATES

NUCLEAR REGULATORY COMMISSION

REGION IV

1600 EAST LAMAR BLVD

ARLINGTON, TEXAS 76011-4511

L. Cortopassi

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If you contest these violations, you should provide a response within 30 days of the date of this

inspection report, with the basis for your denial, to the Nuclear Regulatory Commission, ATTN:

Document Control Desk, Washington DC 20555-0001; with copies to the Regional

Administrator, Region IV; the Director, Office of Enforcement, United States Nuclear Regulatory

Commission, Washington, DC 20555-0001; and the NRC Resident Inspector at Fort Calhoun

Station.

If you disagree with a cross-cutting aspect assignment in this report, you should provide a

response within 30 days of the date of this inspection report, with the basis for your

disagreement, to the Regional Administrator, Region IV and the NRC Resident Inspector at Fort

Calhoun Station.

In accordance with 10 CFR 2.390 of the NRC's "Rules of Practice," a copy of this letter, its

enclosure, and your response (if any) will be available electronically for public inspection in the

NRC Public Document Room or from the Publicly Available Records (PARS) component of

NRC's Agencywide Document Access and Management System (ADAMS). ADAMS is

accessible from the NRC Web site at http://www.nrc.gov/reading-rm/adams.html (the Public

Electronic Reading Room).

Sincerely,

/RA/

Mr. Michael Hay

Chief, Project Branch F

Division of Reactor Projects

Docket: 50-285

License: DPR-40

Enclosures:

1. Notice of Violation

2. NRC Inspection Report 05000285/2012005

w/Attachment: Supplemental Information

cc w/ encl: Electronic Distribution

L. Cortopassi

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DISTRIBUTION:

Electronic distribution by RIV:

Regional Administrator (Elmo.Collins@nrc.gov)

Deputy Regional Administrator (Art.Howell@nrc.gov)

DRP Director (Kriss.Kennedy@nrc.gov)

ACTING DRP Deputy Director (Barry.Westreich@nrc.gov)

ACTING DRS Director (Tom.Blount@nrc.gov)

ACTING DRS Deputy Director (Jeff.Clark@nrc.gov)

MC0350 Panel Chair (Anton.Vegel@nrc.gov)

MC0350 Panel Co-Chair (Louise.Lund@nrc.gov)

MC0350 Panel Member (Michael.Balazik@nrc.gov)

MC0350 Panel Member (Michael.Markley@nrc.gov)

Senior Resident Inspector (John.Kirkland@nrc.gov)

Resident Inspector (Jacob.Wingebach@nrc.gov)

Branch Chief, DRP/F (Michael.Hay@nrc.gov)

Senior Project Engineer, DRP/F (Rick.Deese@nrc.gov)

Project Engineer, DRP/F (Chris.Smith@nrc.gov)

Public Affairs Officer (Victor.Dricks@nrc.gov)

Public Affairs Officer (Lara.Uselding@nrc.gov)

Acting Branch Chief, DRS/TSB (Ryan.Alexander@nrc.gov)

Project Manager (Lynnea.Wilkins@nrc.gov)

RITS Coordinator (Marisa.Herrera@nrc.gov)

Regional Counsel (Karla.Fuller@nrc.gov)

Technical Support Assistant (Loretta.Williams@nrc.gov)

Congressional Affairs Officer (Jenny.Weil@nrc.gov)

OEMail Resource

ROPreports

RIV/ETA: OEDO (Cayetano.Santos@nrc.gov)

DRS/TSB STA (Dale.Powers@nrc.gov)

R:_REACTORS\\_FCS\\2012\\FCS 2012-005 RP JCK.DOCX

SUNSI Rev Compl.

Yes No

ADAMS

Yes No

Reviewer Initials

MCH

Publicly Avail.

Yes No

Sensitive

Yes No

Sens. Type Initials

MCH

SRI:DRP/F

SPE:DRP/F

SPE:DRP/F

C:DRS/PSB2

C:ORA/ACES BC:DRP/.F

JCKirkland

JFWingebach

RWDeese

JDrake

HGepford

MCHay

/RA via E/

/RA via E/

/RA/

/RA/

/CYoung for/

/RA/

11/13/12

11/13/12

11/8/12

11/13/12

11/13/12

11/13/12

ML 12318A341

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Enclosure 1

NOTICE OF VIOLATION

Omaha Public Power District

Docket No.:

05000285

Fort Calhoun Station

License No.: DPR-40

EA-12-174

During an NRC inspection conducted from June 18 to August 3, 2012, a violation of NRC

requirements was identified. In accordance with the NRC Enforcement Policy, the violation is

listed below:

Title 10 CFR 50.71(e) requires, in part, that each person licensed to operate a nuclear

power reactor under the provisions of 50.21 or 50.22, shall update periodically the final

safety analysis report (FSAR) originally submitted as part of the application for the

license, to assure that the information included in the report contains the latest

information developed. The submittal shall include the effects of all changes made in the

facility or procedures as described in the FSAR; and all safety analyses and evaluations

performed by the applicant or licensee either in support of approved license

amendments or in support of conclusions that changes did not require a license

amendment in accordance with § 50.59(c)(2). The updated information shall be

appropriately located within the update to the FSAR.

Contrary to the above, from December 2006 to June 2012, the licensee failed to assure

that the information included in the Updated Safety Analysis Report contains the latest

information developed, including the effects of all changes made in the facility or

procedures as described in the Report. Specifically, since December 2006, the licensee

stored a significant source of radioactivity in the Original Steam Generator Storage

Facility but failed to describe the volume of waste, the principal sources of radioactivity,

the total quantity of radioactivity, and the estimated dose rate at the site boundary per

curie of radioactivity in the Updated Safety Analysis Report.

This is a Severity Level IV violation (Section 6.1.d).

Pursuant to the provisions of 10 CFR 2.201, Omaha Public Power District is hereby required to

submit a written statement or explanation to the U.S. Nuclear Regulatory Commission,

ATTN: Document Control Desk, Washington, DC 20555-0001 with a copy to the Regional

Administrator, Region IV, and a copy to the NRC Resident Inspector - Fort Calhoun Station,

within 30 days of the date of the letter transmitting this Notice of Violation (Notice). This reply

should be clearly marked as a "Reply to a Notice of Violation; EA-12-0174" and should include

for each violation: (1) the reason for the violation or, if contested, the basis for disputing the

violation or severity level, (2) the corrective steps that have been taken and the results

achieved, (3) the corrective steps that will be taken, and (4) the date when full compliance will

be achieved. Your response may reference or include previous docketed correspondence if the

correspondence adequately addresses the required response. If an adequate reply is not

received within the time specified in this Notice, an order or a Demand for Information may be

issued as to why the license should not be modified, suspended, or revoked, or why such other

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action as may be proper should not be taken. Where good cause is shown, consideration will

be given to extending the response time.

If you contest this enforcement action, you should also provide a copy of your response with the

basis for your denial, to the Director, Office of Enforcement, United States Nuclear Regulatory

Commission, Washington, DC 20555-0001.

Because your response will be made available electronically for public inspection in the NRC

Public Document Room or from the NRCs document system (ADAMS), accessible from the

NRC Web site at http://www.nrc.gov/reading-rm/adams.html, to the extent possible, it should not

include any personal privacy, proprietary, or safeguards information so that it can be made

available to the public without redaction. If personal privacy or proprietary information is

necessary to provide an acceptable response, then please provide a bracketed copy of your

response that identifies the information that should be protected and a redacted copy of your

response that deletes such information. If you request withholding of such material, you must

specifically identify the portions of your response that you seek to have withheld and provide in

detail the bases for your claim of withholding (e.g., explain why the disclosure of information will

create an unwarranted invasion of personal privacy or provide the information required by

10 CFR 2.390(b) to support a request for withholding confidential commercial or financial

information). If safeguards information is necessary to provide an acceptable response, please

provide the level of protection described in 10 CFR 73.21.

In accordance with 10 CFR 19.11, you may be required to post this Notice within two working

days of receipt.

Dated this 13th day of November 2012

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Enclosure 2

U.S. NUCLEAR REGULATORY COMMISSION

REGION IV

Docket:

05000285

License:

DPR-40

Report:

05000285/2012005

Licensee:

Omaha Public Power District

Facility:

Fort Calhoun Station

Location:

9610 Power Lane

Blair, NE 68008

Dates:

August 19 through September 30, 2012

Inspectors:

J. Kirkland, Senior Resident Inspector

J. Wingebach, Resident Inspector

A. Klett, Reactor Operations Engineer

A. Rosebrook, Senior Project Engineer

R. Deese, Senior Project Engineer

F. Ramirez, Resident Inspector

K. Clayton, Senior Operations Engineer

W. Smith, Project Engineer

A. Fairbanks, Reactor Inspector

Approved By:

Michael Hay, Chief, Project Branch F

Division of Reactor Projects

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SUMMARY OF FINDINGS

IR 05000285/2012005; 08/19/2012 - 09/30/2012; Fort Calhoun Station, Integrated Resident,

Inservice Inspection, and Confirmatory Action Letter Report

The report covered a 6-week period of inspection by resident inspectors and announced baseline

inspections by region-based inspectors. One Green noncited violation and one Severity Level IV

cited violation were identified. The significance of most findings is indicated by their color

(Green, White, Yellow, or Red) using Inspection Manual Chapter 0609, Significance

Determination Process. The cross-cutting aspect is determined using Inspection Manual

Chapter 0310, Components Within the Cross Cutting Areas. Findings for which the significance

determination process does not apply may be Green or be assigned a severity level after NRC

management review. The NRC's program for overseeing the safe operation of commercial

nuclear power reactors is described in NUREG-1649, Reactor Oversight Process, Revision 4,

dated December 2006.

A.

NRC-Identified Findings and Self-Revealing Findings

Cornerstone: Initiating Events

Green. The NRC identified a noncited violation (NCV) of 10 CFR Part 50, Appendix B,

Criterion XVI, Corrective Actions, for the failure to take timely corrective actions with

respect to nonconforming conditions in several circuit breakers. These conditions were

determined to have been the cause of the 1B4A bus bar failure that initiated a fire on

June 7, 2011. These conditions were not corrected in a timely manner and the licensee

continued to operate with a degraded breaker for nine months after the breaker tripped

unexpectedly during the June 7, 2011, fire event. The licensee entered this issue into

their corrective action program as CRs 2012-01884 and 2011-5414.

The violation was determined to be more than minor because it affected the Initiating

Events Cornerstone attribute of protection against external events (i.e., fire). The issue

adversely affected the associated cornerstone objective of limiting the likelihood of those

events that upset plant stability and challenge critical safety functions during shutdown as

well as power operations because the condition that contributed to the fire event was left

uncorrected. The finding screened to Green in accordance with IMC 0609, Appendix G

because RCS makeup capability was not degraded. The inspectors determined that the

issue had a cross-cutting aspect in the area of Problem Identification and Resolution,

Corrective Action Program (P.1(d)). (4OA4.1.c.(3).2).

Cornerstone: Miscellaneous

SLIV. The inspectors identified a cited violation of 10 CFR 50.71(e), Maintenance of

Records, Making of Reports, for the failure to update the Updated Safety Analysis

Report with a detailed description of the Original Steam Generator Storage Facility.

Specifically, since December 2006, the licensee stored a significant source of

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radioactivity in the Original Steam Generator Storage Facility, but failed to describe the

volume of waste, the principal sources of radioactivity, the total quantity of radioactivity,

and the estimated dose rate at the site boundary per curie of radioactivity in the

Updated Safety Analysis Report. The licensee has entered this violation into their

corrective action program as Condition Report 2012-05725.

This issue was evaluated using traditional enforcement because it has the potential to

impact the NRCs ability to perform its regulatory function. This issue is being

characterized as a Severity Level IV violation in accordance with Section 6.1.d.3 of the

NRC Enforcement Policy. Cross-cutting aspects are not assigned to traditional

enforcement violations (Section 2RS08).

B.

Licensee-Identified Violations

None

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REPORT DETAILS

Summary of Plant Status

The station remained in Mode 5 with the fuel in the reactor vessel for the entire inspection period.

1.

REACTOR SAFETY

Cornerstones: Initiating Events, Mitigating Systems, and Barrier Integrity

1R08 Inservice Inspection Activities (71111.08)

a. Inspection Scope

During August through November, 2012, the inspectors completed a focused inspection

of the steam generators in response to the San Onofre Nuclear Generating Station

(SONGS) primary to secondary steam generator leakage. The inspection focused on

similarities of steam generator design, and verified that the types of degradation affecting

SONGS steam generators does not impact the steam generators at the Fort Calhoun

Station. The inspection focused on:

Retainer and freespan indications.

Adequacy of Mitsubishis thermal-hydraulic model.

Refueling outage eddy current testing results.

10 CFR 50.59 review

The inspectors reviewed the updated safety analysis report (USAR), steam generator

design documents, eddy current testing (ECT) procedures and data results, corrective

actions, and performed a walkdown of the steam generators. The inspectors also

attended a presentation provided to the licensee by Mitsubishi Heavy Industries (MHI).

Specifically, the inspectors reviewed:

10 CFR 50.59 evaluation of the replacement steam generators.

Eddy current examination reports for the 2008 refueling outage.

Secondary inspection results for the 2008 refueling outage.

MHI presentation that included discussions on retainer bar random vibrations, and

in-plane flow elastic instabilities of tube-to-tube wear.

Fort Calhoun steam generator long term inspection strategy plan.

Westinghouse second review of eddy current testing data.

Independent review of raw ECT data on EddyNet format

Industry experience has shown that most deficiencies in steam generator design are

typically identified during eddy current inspections following the first operating cycle. The

steam generators at Fort Calhoun Station were replaced in 2006, and inspected during

the refueling outage in 2008. NRC experts performed an independent review of select

ECT raw data, with an emphasis on low frequencies absolute data channels indicative of

tube-to-tube wear, with no issues identified. As a result of the information presented to

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the NRC, including a Westinghouse second review of ECT data, the NRCs independent

review of the same data, and positive industry experience of steam generator designs not

experiencing issues after a successful first cycle inspection, the inspectors determined

that reasonable assurance exists that the degradation mechanism experienced in

SONGS steam generators does not exist at this time for the Fort Calhoun Station.

The inspectors will review the following documentation as it becomes available:

Revised degradation and operational assessment.

Certain aspects documented as open items in the SONGS Augmented Inspection Team

report (ML12188A748) have the potential to require further inspections at Fort Calhoun

Station.

b. Findings

No findings were identified.

1R15 Operability Evaluations and Functionality Assessments (71111.15)

a. Inspection Scope

The inspectors reviewed the following assessments:

August 31, 2012, Operability of the reactor cavity walls prior to moving fuel from

the reactor vessel to the spent fuel pool

The inspectors selected these operability and functionality assessments based on the risk

significance of the associated components and systems. The inspectors evaluated the

technical adequacy of the evaluations to ensure technical specification operability was

properly justified and to verify the subject component or system remained available such

that no unrecognized increase in risk occurred. The inspectors compared the operability

and design criteria in the appropriate sections of the technical specifications and USAR to

the licensees evaluations to determine whether the components or systems were

operable. Where compensatory measures were required to maintain operability, the

inspectors determined whether the measures in place would function as intended and

were properly controlled. Additionally, the inspectors reviewed a sampling of corrective

action documents to verify that the licensee was identifying and correcting any

deficiencies associated with operability evaluations. Specific documents reviewed during

this inspection are listed in the attachment.

These activities constitute completion of one operability evaluations inspection sample as

defined in Inspection Procedure 71111.15-05.

b. Findings

No findings were identified.

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1R22 Surveillance Testing (71111.22)

a. Inspection Scope

The inspectors reviewed the USAR, procedure requirements, and technical specifications

to ensure that the surveillance activities listed below demonstrated that the systems,

structures, and/or components tested were capable of performing their intended safety

functions. The inspectors either witnessed or reviewed test data to verify that the

significant surveillance test attributes were adequate to address the following:

Preconditioning

Evaluation of testing impact on the plant

Acceptance criteria

Test equipment

Procedures

Jumper/lifted lead controls

Test data

Testing frequency and method demonstrated technical specification operability

Test equipment removal

Restoration of plant systems

Fulfillment of ASME Code requirements

Updating of performance indicator data

Engineering evaluations, root causes, and bases for returning tested systems,

structures, and components not meeting the test acceptance criteria were correct

Reference setting data

Annunciators and alarms setpoints

The inspectors also verified that licensee personnel identified and implemented any

needed corrective actions associated with the surveillance testing.

August 28, 2012, OP-ST-FH-0005, Refueling System Spent Fuel Handling

Machine Refueling Interlocks Test

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September 1, 2012, OP-ST-FH-0002, Refueling System Fuel Transfer System

Interlocks Test

September 4, 2012, OP-ST-FH-0001, Refueling System Fuel Handling Machine

(FH-1) Interlocks Test

Specific documents reviewed during this inspection are listed in the attachment.

These activities constitute completion of three surveillance testing inspection samples as

defined in Inspection Procedure 71111.22-05.

b. Findings

No findings were identified.

2RS08 Radioactive Solid Waste Processing, and Radioactive Material Handling, Storage,

and Transportation (71124.08)

a.

Inspection Scope

This area was inspected to verify the effectiveness of the licensees programs for

updates to the Updated Safety Analyiss Report related to the processing, handling, and

storage of radioactive material.

b.

Findings

(1) Failure to Update the Updated Safety Analysis Report-Solid Wastes

Introduction. The inspectors identified a Severity Level IV violation of 10 CFR 50.71(e),

Maintenance of Records, Making of Reports, for failure to update the Updated Safety

Analysis Report with information about the Original Steam Generator Storage Facility that

was constructed in 2006 for long-term storage of large decommissioned components .

Description. In 2006, the licensee built the Original Steam Generator Storage Facility for

long-term solid radioactive waste storage of the two original steam generators, the

pressurizer, the reactor vessel head, and four concrete reactor vessel head missile shield

blocks. From the licensees estimation, the Original Steam Generator Storage Facility

contained 404 curies. However, this significant source of radioactivity was not described

in the licensees Updated Safety Analysis Report. On November 10, 2010, the NRC

identified a Severity Level IV noncited violation for the failure to update the Updated

Safety Analysis Report per 10 CFR 50.71(e) because the licensee had not described the

Original Steam Generator Storage Facility in the Updated Safety Analysis Report (NCV 05000285/2010004-03).

During the June 2012 radiation protection inspection, the inspectors toured the

Original Steam Generator Storage Facility and reviewed the licensees implementation of

corrective actions associated with the previous violation. The licensees corrective actions

for the 2010 noncited violation were initially addressed in Condition Report 2010-03636

and included an apparent cause analysis. The licensees apparent cause for the violation

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stated that the Engineering Change Package was developed to an unknowable or

changing [NRC] requirement. The condition report further stated that this violation

showed a common misapplication of the regulations related to storage which may have

been in place for several years. The condition report also stated that engineering will be

contacted to perform a 10 CFR 50.59 screening and update the USAR by January 2011.

However, the inspectors determined that the licensee did not implement corrective

actions based on the noncited violation as addressed in Condition Report 2010-03636.

In 2011, the licensee did not update the Updated Safety Analysis Report to describe the

Original Steam Generator Storage Facility.

Prior to the June 2012 inspection, the licensee performed a self-assessment as part of

Condition Report 2012-03704 to verify that Chapter 11 of the Updated Safety Analysis

Report had been updated, including a description of the Original Steam Generator

Storage Facility. Based on the self-assessment results, the licensee submitted a

revision to the Updated Safety Analysis Report Chapter 11.2.4.1, Radioactive Waste

Storage to the NRC in June 2012. The inspectors review determined that the

information added in the June 2012 revision of the Updated Safety Analysis Report was

inadequate. The licensees update in Chapter 11.2.4.1, of the Updated Safety Analysis

Report merely stated that radwaste waiting disposal is stored in the Original Steam

Generator Storage Facility located on the west side of the plant site, north of the main

access road. The inspectors concluded that the Original Steam Generator Storage

Facility was being used to store a significant source of radioactivity that was not

adequately described in Chapter 11 of the licensees Updated Safety Analysis Report.

Some of the information missing about the Original Steam Generator Storage Facility

included the volume of waste, the principal sources of radioactivity, the total quantity of

stored radioactivity, and the estimated dose rate at the site boundary per curie of stored

waste.

As of June 22, 2012, the inspectors concluded that the corrective actions implemented

in Condition Report 2010-03636 for the 2010 violation and the self-assessment under

Condition Report 2012-03704 were inadequate to comply with 10 CFR 50.71(e), in that,

Chapter 11 of the Updated Final Safety Analysis Report did not adequately describe the

Original Steam Generator Storage Facility. This issue was entered into the licensees

corrective action program as Condition Report 2012-05725.

Analysis. Failure to update the Updated Safety Analysis Report as required by

10 CFR 50.71(e) with a detailed description of the Original Steam Generator Storage

Facility was a performance deficiency. This issue was evaluated using traditional

enforcement because it had the potential to impact the NRCs ability to perform its

regulatory function. The issue was characterized as a Severity Level IV violation in

accordance with Section 6.1.d.3 of the NRC Enforcement Policy, in that, the erroneous

[incomplete] information in the Final Safety Analysis Report Update was not used to

make an unacceptable change to the facility or procedures. Cross-cutting aspects are

not assigned to traditional enforcement violations.

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Enforcement. 10 CFR 50.71(e), Maintenance of Records, Making of Reports, states, in

part, that each person licensed to operate a nuclear power reactor shall update

periodically the Updated Safety Analysis Report originally submitted as part of the

application for the license, to assure that the information included in the report contains

the latest information developed. Contrary to the above, from December 2006 to June

2012, the licensee failed to assure that the information included in the Updated Safety

Analysis Report contains the latest information developed to include the effects of all

changes made in the facility. Specifically, since December 2006, the licensee stored a

significant source of radioactivity in the Original Steam Generator Storage Facility, but

failed to describe the volume of waste, the principal sources of radioactivity, the total

quantity of radioactivity, and the estimated dose rate at the site boundary per curie of

radioactivity in the Updated Safety Analysis Report. This violation is being treated as a

cited violation, consistent with Section 2.3.2(a)(3) of the NRC Enforcement Policy:

NOV 05000285/2012005-01, Failure to Update the Updated Safety Analysis Report-

Solid Waste.

4.

OTHER ACTIVITIES

Cornerstones: Initiating Events, Mitigating Systems, Barrier Integrity, Emergency

Preparedness, Public Radiation Safety, Occupational Radiation Safety, and

Physical Protection

4OA2 Problem Identification and Resolution (71152)

.1

Routine Review of Identification and Resolution of Problems

a.

Inspection Scope

As part of the various baseline inspection procedures discussed in previous sections of

this report, the inspectors routinely reviewed issues during baseline inspection activities

and plant status reviews to verify that they were being entered into the licensees

corrective action program at an appropriate threshold, that adequate attention was being

given to timely corrective actions, and that adverse trends were identified and addressed.

The inspectors reviewed attributes that included the complete and accurate identification

of the problem; the timely correction, commensurate with the safety significance; the

evaluation and disposition of performance issues, generic implications, common causes,

contributing factors, root causes, extent of condition reviews, and previous occurrences

reviews; and the classification, prioritization, focus, and timeliness of corrective actions.

Minor issues entered into the licensees corrective action program because of the

inspectors observations are included in the attached list of documents reviewed.

These routine reviews for the identification and resolution of problems did not constitute

any additional inspection samples. Instead, by procedure, they were considered an

integral part of the inspections performed during the quarter and documented in Section 1

of this report.

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b.

Findings

No findings were identified.

.2

Daily Corrective Action Program Reviews

a.

Inspection Scope

In order to assist with the identification of repetitive equipment failures and specific

human performance issues for follow-up, the inspectors performed a daily screening of

items entered into the licensees corrective action program. The inspectors accomplished

this through review of the stations daily corrective action documents.

The inspectors performed these daily reviews as part of their daily plant status monitoring

activities and, as such, did not constitute any separate inspection samples.

b.

Findings

No findings were identified.

4OA3 Followup of Events and Notices of Enforcement Discretion (71153)

.1 (Open) Licensee Event Report 05000285/2011-010-00: Fire Causes a Circuit Breaker to

Open Outside Design Assumptions

On June 7, 2011, a bus fault in load center 1B4A initiated a switch gear fire that resulted

in the opening of a circuit breaker which supplies power to load center 1B3A, associated

with the opposite train. A fire in one fire area that resulted in a loss of power to a load

center associated with the opposite train is not in compliance with 10 CFR 50, Appendix

R. The analysis assumes that a fire in a fire area affecting one train of power will be

isolated such that power associated with the redundant train will be maintained.

A root cause analysis is being performed to determine the cause of the failure.

The affected bus was de-energized and the Halon system extinguished the fire. The

Halon system was recharged and restored to service. Inspections and testing of the

unaffected 480 V buses, the supply circuit breakers to the 480 V buses, and the 480 V

bus tie circuit breakers were performed. Appropriate 480 V supply circuit breakers and

bus tie circuit breakers passed their inspections and testing. The fire damaged switchgear

(1B4A), which contains two 480V supply circuit breakers, 1B4A and BT-1B4A (supply

circuit breaker to the associated island bus), is being replaced. Additional corrective

actions will be specified following the completion of the root cause analysis.

.2 (Open) Licensee Event Report 05000285/2012-014-00: Containment Beam 22 Loading

Conditions Outside of the Allowable Limits

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On July 11, 2012, while performing the Extent of Condition for an existing Condition

Report (CR) it was determined that Beam B-22, a structural member of the containment

internal structure at the 1013 foot elevation, loading conditions were outside the allowable

limits for both Working Stress and No Loss of Function load combinations as noted in the

USAR Section 5.11. This condition was identified on July 11, 2011, while the unit was

shutdown and reported to the U.S. Nuclear Regulatory Commission (NRC) Headquarters

Operations Center the same day at approximately 1603 CDT under Event Notification 48094.

A cause analysis is being evaluated and will be published in a supplement to this LER.

.3 (Open) Licensee Event Report 05000285/2012-015-00: Electrical Equipment Impacted by

High Energy Line Break Outside of Containment

While reviewing a draft of the Master List Reconstitution for Electrical Equipment

Qualification (EA-FC-08-011), Fort Calhoun Station (FCS) Engineering Department

identified that some of the listed components may not be qualified for the environments

where they are located. This was discovered during a comprehensive re-evaluation of

potential high energy line breaks and radiological impacts outside containment initiated in

response to issues identified by the station staff. This condition was identified on

September 16, 2011, while the unit was shutdown.

A cause analysis is in progress. The results of the analysis will be published in a

supplement to this LER.

.4 (Open) Licensee Event Report 05000285/2012-016-00: Unanalyzed Charging System

Socket Welds to the Reactor Coolant System

On July 17, 2012, Fort Calhoun Station (FCS) identified a deficiency as part of the

analyses being performed in support of resolution to the question as to whether some

Class I pipe was potentially not qualified as Class 1. Condition Report (CR) 2012-07724

documented that preliminary results from an Thermal Fatigue Analysis on the chemical

and volume control system (CVCS) concluded that; 1) The 2 inch socket welded fittings

on Reactor Coolant System (RCS) branch line piping cannot be qualified, and 2) The 2

inch charging lines are considered to be in an unanalyzed condition exceeding thermal

cycle fatigue and seriously degraded.

A cause analysis was completed and determined that the CVCS Class 1 piping was

constructed using socket welded fittings.

CVCS was declared inoperable. The normal charging headers to the RCS are classified

as inoperable until further evaluations or required repairs are performed. CVCS has been

isolated to prevent any further thermal transients to the suspect welds. In addition, the

affected waste disposal piping line which was scoped under the extent of condition is

being addressed under CR 2012-12184. Contingency actions have already been taken to

secure the letdown line so no thermal stress may be introduced to those socket welds.

The affected welds will be replaced prior to plant heatup.

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4OA4 IMC 0350 Inspection Activities (92702)

Inspectors began the IMC 0350 inspection activities, which include follow-up on the restart

checklist contained in Confirmatory Action Letter (CAL) 4-12-002 issued June 11, 2012. The

purpose of the beginning phase of this inspection is to assess the licensees performance and

progress in addressing its implementation and effectiveness of FCSs Integrated Performance

Improvement Plan (IPIP), significant performance issues, weaknesses in programs and

processes, and flood restoration activities. This phase of inspection determines whether the

depth and breadth of performance concerns are understood.

Inspectors used the criteria described in baseline and supplemental inspection procedures,

various programmatic NRC inspection procedures, and IMC 0350 to assess the licensees

performance and progress in implementing its performance improvement initiatives. Inspectors

performed on-site and in-office activities, which are described in more detail in the following

sections of this report. This report covers inspection activities from July 16 through

August 18, 2012. Specific documents reviewed during this inspection are listed in the

attachment.

The following inspection scope, assessments, observations, and findings are documented by

CAL restart checklist item number.

.1 Causes of Significant Performance Deficiencies and Assessment of Organizational

Effectiveness

Section 1 of the restart checklist contains those items necessary to develop a comprehensive

understanding of the root causes of safety-significant performance deficiencies identified at

Fort Calhoun Station. In addition, Section 1 includes the independent safety culture

assessment with the associated root causes and findings. The integration of the

assessments under Item 1.f identifies the fundamental aspects of organizational performance

in the areas of organizational structure and engagement, values, standards, culture, and

human behaviors that have resulted in the protracted performance decline and are critical for

sustained performance improvement. Section 1 reviews also include an assessment against

appropriate NRC Inspection Procedure 95003 key attributes. These assessments are

documented in section 4OA4.5.

.a Flooding Issue - Yellow Finding

Item 1.a is included in the restart checklist for the failure of Fort Calhoun Station to

maintain procedures and equipment that protects the plant from the effects of a design

basis flood. These deficiencies resulted in a Yellow (substantial safety significance)

finding.

(1) Inspection Scope

Item 1.a is included in the restart checklist because the licensee failed to maintain

procedures and equipment that protects the plant from the effects of a design basis

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flood. These deficiencies resulted in a finding having Yellow (i.e., substantial) safety

significance. During the inspection period covered by this report, the NRC inspectors

assessed, and will continue to assess during upcoming inspection periods, the

licensees root cause, extent of cause, and extent of condition evaluations related to

the Yellow finding. In addition, the inspectors continued to verify that corrective

actions are adequate to address the root and contributing causes.

The onsite activities included specific walk-downs of licensee procedure to mitigate

flooding such as PE-RR-AE-1001, Flood Barrier and Sandbag Staging and

Installation, PE-RR-AE-1002, Installation of Portable Steam Generator Pumps,

Abnormal Operating Procedure (AOP)-1, Acts of Nature Section I, Flood, and

OI-CW-1, Circulating Water System Normal Operation, Attachment 18, Sand

IntrusionMitigation. In addition, the inspectors completed a more detailed walk-down

of the intake structure and pre-staged flooding equipment; interviews with personnel

involved in the flooding emergency preparedness and recovery efforts; and

observation of recovery effort meetings. The in-office activities consisted of reviews

of documents associated with the recovery efforts, procedures associated with

flooding mitigation strategies, system lesson plans, and condition reports.

(2) Assessment

The inspectors review focused mainly on the adequacy of procedures that are

associated with mitigation strategies for a design basis flood. As a result of the

various procedure walk-downs, the inspectors had observations associated with

procedure sustainability and quality. For example, PE-RR-AE-1001, Attachment 23,

Fuel Transfer Hose to Emergency Diesel Generator (EDG) Day Tanks, does not

prescribe a specific plan to route the EDG fuel transfer hose. This procedure

attachment is used to provide the EDG day tanks with fuel in the event elevated river

levels were expected to last longer than 7 days. The inspectors identified that the

procedure did not contain detailed information regarding how the hose would be

routed from the tanker at the entrance of the plant to the EDG day tanks to ensure it

will not be damaged by other plant traffic. This observation was provided to the

licensee and was placed in the Corrective Action Program.

During the walk-down of the flooding procedures listed in the scope of this report

section, the inspectors also noted that, even though the main pieces of equipment

and tools listed in the procedures were pre-staged, some of the smaller tools were

not. The inspectors noted that if the licensee had a more meticulous pre-staging of

equipment including small tools and consumables, the number of trips to the tool

room would be minimized and flood preparations would be more efficient. The

licensee entered this observation into the corrective action process.

During this inspection period, the inspectors assessed the flood preparations

associated with the emergency response facilities such as the Technical Support

Center (TSC), the Operations Support Center (OSC), and the Emergency Operations

Facility (EOF). The inspectors reviewed the licensees plan to provide for an alternate

emergency response facility in case the original locations were expected to flood.

- 14 -

The licensee was able to demonstrate that an adequate plan existed for alternate

TSC, OSC, and EOF facilities in case of a flood. In addition, the inspectors noted that

there are no thresholds to transfer the TCS and OSC to alternate locations. The

inspectors also noted a general lack of rigor and details in the procedures to respond

to prepare and respond to a flood. Specifically, the inspectors noted the licensee did

not have detailed plan on managing the distribution of resources and personnel, and

the strategy during the preparation time for an imminent flood. As a result of the

inspectors observations, the licensee is currently constructing a resource-loaded

schedule that delineates the different tasks and times requested for all the

preparations needed prior to a flood. The inspectors will review the plan and continue

to have further discussions with licensee operations and emergnency preparedness

personnel. Further in-depth Emergency Preparedness (EP) inspections will be

performed by EP inspectors and will be documented in the future as part of Restart

Checklist Item 5.f.

The inspectors reviewed the basis for the number of hours that the licensee bases

their entire flooding planning on. The inspectors wanted to ensure that the technical

foundation for that window of preparation time was adequate and that the licensee

would still be able to stage equipment, stack sand bags, and assemble flood barriers

in enough time before the plant grounds start to flood.

(3) Findings

No findings of significance were identified.

.b Reactor Protection System contact Failure - White Finding

Item 1.b is included in the restart checklist for the failure of Fort Calhoun Station to

correct a degraded contactor, which subsequently failed, in the reactor protection system.

These deficiencies resulted in a White (low to moderate safety significance) finding.

(1) Inspection Scope

The NRC inspected and will continue to inspect the root cause, extent of cause, and

extent of condition related to the contactor failure and the associated process failures.

The on-site activities included interviews and discussions with staff performing

evaluations of significant performance issues, programs, and processes; and

observation of conduct of recovery effort meetings.

(2) Assessment

The team completed the review of revision 2 of the Root Cause Analysis for the

contactor failure, RCA 2011-0451, during previous inspection weeks. However, no

progress was made in this area during the six weeks of this reporting period because

the licensee started a new root cause analysis (revision 3) the week of

September 24, 2012. Revision 3 of this root cause analysis will supersede the

previous two versions because of errors, omissions, and poor clarity. The licensee

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continues to try to pull this date up for completion of the root cause itself to

November 9, 2012, and does not currently have a schedule for completion of all

corrective actions. The NRC will close out this issue for restart after the inspections

verify that the station has 1) completed revision 3 of this root cause analysis,

2) completed the corrective actions from the root cause analysis, and 3) completed all

actions necessary to prevent re-occurrence.

(3) Findings

No Findings of significance were identified.

.c Electrical Bus Modification and Maintenance - Red Finding

Item 1.c is included in the restart checklist because the licensee failed to adequately

design, modify, and maintain the electrical power distribution system, which caused a fire

in the safety-related 480 volt (V) electrical switchgear. These deficiencies resulted in a

finding having Red (i.e., high) safety significance.

(1) Inspection Scope

During the inspection period, the NRC assessed (and will continue to assess during

upcoming inspection periods) the licensees root cause, extent of cause, and extent of

condition evaluations related to the fire and associated equipment and process

failures.

The on-site activities included a walk-down of the remains of the breaker that was on

fire and a tour of the switchgear rooms, interviews and discussions with licensee staff,

and observation of recovery effort meetings. The in-office activities, which were

conducted at the inspectors normal duty stations, consisted of reviews of documents

associated with the recovery efforts, conditions reports, root cause analyses, scoping

procedures, calculations, and drawings.

The team also reviewed modification EC 33464, Replace AK-50 480 V Main and

Bus-Tie Breakers With Molded Case Type or Equivalent, Revision 0, which replaced

12 General Electric AK-50 low voltage power circuit breakers with Nuclear Logistics

Incorporated/Square-D Masterpact circuit breakers / cradle assemblies, and digital

trip devices in November 2009. The modification replaced six feeder circuit breakers

and six bus-tie breakers.

The team interviewed the system engineers responsible for the 480 VAC distribution

system and electrical maintenance technicians that maintained the system. The team

interviewed operations personnel and discussed procedures and training for the

modification. The team reviewed the modification to determine if the requirements of

10 CFR 50.59, Changes, Tests and Experiments, were met, including understanding

the possible failure modes, and to assess the post-modification testing completeness

for cradle and breaker positioning, electrical resistance, and other critical parameters.

- 16 -

(2) Assessment

As previously discussed in NRC IR 050-00285/2012004, when evaluating whether a

risk significant finding may be closed, NRC IP 95002 directs inspectors to :

1) To provide assurance that the root and contributing causes of individual and

collective (multiple greater than green inputs) risk-significant performance

issues are understood.

2) To independently assess and provide assurance that the extent of condition

and the extent of cause of individual and collective (multiple greater than

green inputs) risk-significant performance issues are identified.

3) To independently determine if safety culture components caused or

significantly contributed to the individual and collective (multiple greater than

green inputs) risk-significant performance issues.

4) To provide assurance that a licensees corrective actions for risk-significant

performance issues are sufficient to address the root and contributing causes

and prevent recurrence.

In order to achieve these objectives the inspectors independently reviewed the

licensees evaluations of the event and determined that the following conditions

contributed to 1) the initiation of the fire event or 2) the unexpected system response

to the initiating event. In the inspectors assessment are SCAQs based upon the

OPPD QA manuals definition since each of these conditions would have precluded

plant response to the event from ending up outside plant design basis and resulting in

a high safety significance (RED) finding.

OPPD committed to meeting the criteria in IEEE 384-1981, IEEE Standard Criteria

for Independence of Class 1E Equipment and Circuits. This standard describes

independence requirements for Class 1E equipment, including those required for safe

shutdown. Section 5.10.1 of IEEE 384-1981 states that an electrically generated fire

in one Class 1E division shall not cause a loss of function in its redundant Class 1E

division. OPPD also committed to the design criteria in IEEE 308-1974, IEEE

Standard Criteria for Class 1E Power Systems for Nuclear Power Generating

Stations. Criterion 5.2.2(3), Independence, states that distribution circuits to

redundant equipment shall be physically and electrically independent of each other.

Criterion 4.6, Equipment Protection, states that Class 1E power equipment shall be

physically separated from its redundant counterpart or mechanically protected as

required to prevent the occurrence of common failure modes due to design basis

events. The IEEE standard defines design basis events to include postulated

phenomena such as fires. Fort Calhoun USAR also specifies that any subsequent

fault induced by a single failure shall be considered to be part of that single failure and

not treated as a separate failure.

1) The postulated cause of the fire was a high impedance connection between

the breaker cradle assembly and the 480 VAC bus stabs which caused

localized overheating and the bus bar failure, which initiated the event. This

- 17 -

condition was the focus of CR 2011-5414. The licensees corrective actions

developed included replacing the damaged switchgear components,

correcting and/or verifying the alignment of the remaining breaker and cradle

assemblies, correcting the silver plating on all the breaker stabs, and revising

design procedures. The inspectors reviewed the corrective actions completed

and planned and concluded they were adequate to preclude repetition of this

SCAQ. However, NLI and Square D (the vendors for the breaker) completed

an independent RCA for the event on 8/22/12. As of the end of the inspection

period the NRC had not completed its review of this independent RCA.

2) During the fire, a phase-to-phase arc fault occurred for 42 seconds, which

generated a fault current value of 16,000 amperes (A), until operators

manually de-energized Transformer T1B-4A by opening Breaker 1A4-10. In

accordance with 480 VAC, 4160 VAC and Fire protection system design

criteria and IEEE Standards, a fault should be isolated by the breaker closest

to the fault. This would have isolated and arrested the fault and prevented it

from impacting other electrical buses. However, Breaker 1A4-10s breaker trip

setpoint was such that a phase-to-phase fault on the line side of Breaker 1B4A

would not be cleared. This allowed the fire to continue, produce combustion

products, and develop the subsequent ground fault between the BT-1B4A

breaker and the island bus. Although the licensee generated CR 2012-01630

on March 1, 2012, which acknowledged this condition, the licensee had yet to

complete an analyze the adequacy of the breaker trip set points as of the

conclusion of this inspection period. Therefore, the 4160 VAC bus is still not

protected against an arc fault event on the 480 VAC bus upstream of the 480

VAC feeder breaker and this vulnerability is still present.

3) The bus separation scheme design was inadequate to meet the systems

design criteria , IEEE standards, and the 1971 NRC Standard Review Plan

(SRP). (Note: however, the inspectors recognize that OPPD was licensed to

operate FCS prior to the SRP). OPPDs bus separation scheme design

allowed combustion products from the Bus 1B4A fire to be communicated to

and affect the island bus because of the physical configuration of the bus duct

work and because there is only one bus tie breaker on each end of the island

buses. This configuration and the fire event resulted in the development of an

electrical short to ground between Breaker BT-1B4A and Island Bus 1B3A-4A,

which was powered from the opposite safety bus (Bus 1B3A). Thus both

independent trains of vital AC power were adversely affected by a fault on a

single bus. FCSs corrective actions restored the original configuration of the

480V switchgear. The inspectors were not aware of any formal evaluation

which reviewed this design vulnerability and/or operability evaluation as of the

end of the inspection period. This design vulnerability is still present.

4) The DC bus separation scheme design for the DC buses was questioned by

the inspectors. During the fire event on June 7, 2011, grounds developed on

both DC buses. OPPD evaluated the inspectors concern and were able to

demonstrate that there was no adverse impact on the DC buses. While the

- 18 -

condition did result in degradation of the DC busses,t he DC buses are an

ungrounded system by design; therefore, a single ground would not impact

system operation. This condition was determined not to be a SCAQ, because

it is consistent with plant and system design basis and did not contribute to the

unexpected plant response during the event. This concern was adequately

evaluated by OPPD and can be considered closed.

5) The breaker coordination scheme design did not respond as expected during

the fire event. Breaker 1B3A tripped when a fault developed on Island Bus

1B3A-4A, which resulted in both Bus 1B3A and Island Bus 1B3A-4A being lost

during the event. In accordance with system design requirements, Breaker

BT-1B3A should have isolated the fault. Because of the fire and breaker

coordination failure, six of nine vital 480 V buses were either manually or

automatically de-energized during the event, and minimum ECCS system

capacity was not maintained. This condition was the focus of CR 2011-6621.

Corrective actions developed were reviewed by the inspectors and determined

to be adequate to preclude repetition of this SCAQ. This SCAQ and the

associated finding 2012-004-04 can be closed

The inspectors determined the above conditions were SCAQ based upon the

following. Condition #1 is a SCAQ because it resulted in the initiation of an electrical

fault on a single 480 VAC bus and the resulting fire which caused significant

equipment damage and resulted in an EAL declaration. Condition #2 is a SCAQ

because it 1) allows a fault on a single 480 VAC bus to adversely impact the

associated 4160 VAC bus and the remaining 480 VAC on this train, 2) prevents the

fault from being deenergized thus allowing the fire to burn for an additional 42

seconds causing significant equipment damage, and 3) develops charged particles

and soot which allow the design vulnerability discussed in condition 3 to be exploited.

Condition #3 is a SCAQ because this design vulnerability is the mechanism which

allows a single fault to impact both trains of safety related equipment (ECCS,

480VAC, and SSE) and thus is not with the design basis and is an unanalyzed

condition. As a result, during the event, the fault impacted the 1B3A-1B4A island bus

which is powered from the opposite train from the fault. Condition #5 is a SCAQ

because it resulted in a loss of breaker coordination which is relied upon per the Fire

Protection Safe Shutdown Design to protect both trains of SSE during a postulated

fire event, thus this was beyond the system design basis and was an unanalyzed

condition. As a result during the event, a second bus on the opposite train from the

fault was lost and all high pressure make up water sources (HPSI and Charging) were

lost and could not be restored via remote manual operator action.

During this inspection period the inspectors focused on SCAQs 2, and 3. In 1991,

FCS completed a breaker coordination study of the 4160 VAC and 480 VAC

distribution systems. The inspectors identified that the breaker coordination survey

correctly identified that the breaker trip setpoints does not provide full protection

against a 4160VAC/480VAC transformer fault or a 480V Load Center Bus Fault. The

study evaluated that this was acceptable due to the possibility of a fault is extremely

- 19 -

small and the fact that the USAR Section 8.3.1 does not state that all breakers are

coordinated.

The inspectors challenged this conclusion on the basis that the major concern is fault

protection and clearance. The June 7, 2011 fire demonstrated that not showing

protection against a 480 VAC load center fault would prevent the fault from being

cleared, allow a 480 VAC fault to adversely impact the associated 4160 VAC bus.

This lack of protection turned a fire on a single 480VAC bus into an unisolable fault on

the 4160 VAC bus, which is the worst case design basis single failure for ECCS since

the entire 4160 VAC bus and thus each of the associated 480VAC on the train are

also lost. In addition, since the fire is allowed to continue to burn, the known bus

separation design vulnerability is allowed to be exploited as soot and charged particle

are allowed to collect on the associated bus tie breaker (physically located in the

same switchgear cabinet) and develop a fault on the opposite train. This takes plant

response outside of the design basis. Thus, the inspectors questioned the validity of

the studys conclusion. This concern was still under review by the inspectors at the

end of the inspection period.

(3) Findings

.1 Untimely Corrective Actions for 480 VAC Breaker Issues

Introduction: The inspectors identified a Green noncited violation (NCV) of

10 CFR 50, Appendix B, Criterion XVI, Corrective Actions. Specifically, FCS failed

to take timely corrective actions to address non conforming conditions identified in

several breakers during their review of the June 7, 2011, 1B4A Bus fire and abnormal

system response event. Specifically, several breakers were observed to have

significant breaker cradle assembly to bus stab misalignment and high impedance

connections were identified. These conditions were determined to have been the

cause of the 1B4A bus bar failure that initiated the fire; however, this condition was

not corrected for several months. Additionally, FCS continued to operate with a

degraded 1B3A breaker for nine additional months after the breaker tripped

unexpectedly during the event. The breaker remained in service until February 2012.

Description: Following the June 7, 2011, 1B4A breaker fire and abnormal 480 VAC

system response event, FCS wrote several CRs and conducted Root Cause Analysis

(RCA) CR 2011-05414 related to the why the fire occurred. A separate CR

(2011-6621) was written to document and review the unexpected tripping of the 1B3A

breaker during the fire event. FCS initially failed to properly evaluate the significance

of the event as an event significant to nuclear safety, in accordance with FCS

corrective action program procedure . FCS only evaluated the event with respect to

the plant conditions at the time of the fire (i.e., the plant was shutdown for a refueling

outage). In September 2011, during the NRCs Special Inspection of the fire event,

FCS revised its risk assessment and determined that if the fire had occurred at power,

it would have been an event significant to nuclear safety because of the loss of all

high pressure injection sources (HPSI and charging pumps), that adversely impacted

both trains of safe shutdown equipment (SSE).

- 20 -

In July 2011, boroscope inspections of the undamaged 480 VAC breakers were

conducted as an Extent of Condition (EOC) review. These inspections revealed that

four other breakers had significant breaker cradle finger to bus stab misalignment and

appeared to be contacting the stabs beyond the silver plating on the stabs and

created a high impedance connection. This was the same failure mechanism that

CR 2011-5414 concluded was the most likely cause of the 1B4A bus failure and fire.

However, once this condition adverse to quality was identified to exist, the condition

was not corrected until November 2011. During this work, one of the breakers,

Breaker 1B3C was found to have discolorations on the fingers of the cradle assembly,

and this was believed to be heat related. This indicated that at least one other

breaker was potentially progressing down the same failure mechanism as 1B4A.

As discussed in IR 05000285/2011014, the initiating event likelihood of a fire was

calculated to increase to 7.0 x 10-2/year from a baseline likelihood of 2.5 x 10-5 / year

due to this misalignment condition. This significant increase in the likelihood of

another fire occurring due to the same cause as the June 7th, 2011, fire, would make

the misalignment identified in July 2011 a Significant Condition Adverse to Quality

(SCAQ). SCAQs and CAQs must be identified and corrected commensurate with the

safety significance of the issue. Because this issue was determined to have Red (i.e.,

high) safety significantce by the NRC and to be significant to nuclear safety in

accordance with FCSs own risk re-assessment in September 2011, the NRC

determined that waiting to address the issue until November 2011 was not determined

to be a timely corrective action.

In addition, during the 1B4A breaker fire, the 1B3A breaker tripped unexpectedly to

clear a fault induced at the BT-1B4A Bus Tie breaker. This fault should have been

cleared by the BT-1B3A breaker, but the 1B3A breaker tripped first, contrary to the

FCS Breaker Coordination design Scheme. CR 2011-6621 was written to document

the abnormal 480 VAC system response, but it was classified originally as a C level

CR, and no formal evaluation was assigned. It was determined via CR 2011-5514

that 1B3A tripped before BT-1B3A because the breaker coordination curves were set

close to each other in a manner that allowed 1B3A to trip first (i.e., it won the relay

race). The 1B3A breaker was returned to service on June 22, 2011. In September

2011, this CR was brought back to the stations corrective action review board

(CARB) meeting and reassigned as a level A CR, and a root cause evaluation was

assigned. This was due to the fire event risk being re-evaluated. This root cause

rejected the relay race explanation and identified several potential failure

mechanisms that could have caused the breaker to trip outside the coordination

scheme. Troubleshooting was commenced by testing the breakers locally and by

testing the BT-1B3A and 1B3A breakers at the NLI facility in October 2011. These

tests did not identify any problems, and the breakers were returned to FCS and

returned to service.

In February 2012, both breakers BT-1B3A and 1B3A were removed and sent to NLIs

factory test facility. During this round of testing, the symptoms observed on

June 7, 2011, were repeated. With 1B3A and BT-1B3A in series with a fault source,

- 21 -

the 1B3A breaker tripped instantaneously before the BT-1B3A breaker could trip.

Further inspection revealed that the WAGO jumpers disabling the Zone Selective

Interlock (ZSI) function were not installed in the correct location; therefore, the ZSI

feature was not disabled as originally intended. The jumpers were restored to their

proper positions, and proper breaker coordination was observed. Licensee

inspections were conducted on the remaining breakers at FCS in a timely manner,

and no further issues were identified.

However, the fact that the 1B3A breaker was in service in a known degraded

condition from June 22, 2011, until February 27, 2012, is another example of

corrective actions not being timely, and exposing the plant to unnecessary risk.

Analysis: The failure to take timely corrective actions for known SCAQs or CAQs was

within FCSs ability to foresee and prevent and is therefore a performance deficiency.

The performance deficiency was evaluated using NRC Inspection Manual Chapter 0612, Appendix B, Issue Screening, and the issue was determined to be more than

minor because it affected the Initiating Events Cornerstone attribute of protection

against external events (i.e., fire) because the condition that contributed to the fire

event was left uncorrected. The issue adversely affected the associated cornerstone

objective of limiting the likelihood of those events that upset plant stability and

challenge critical safety functions during shutdown as well as power operations. This

issue also affected the Mitigating System Cornerstone.

The inspectors evaluated the finding using NRC Inspection Manual Chapter 0609,

Attachment 4, Initial Characterization of Findings. IMC 0609, Attachment 4 directs

the user to use of IMC 0609, Appendix G, Shutdown Operations SDP, since FCS

was in cold shutdown during the entire exposure period. Using IMC 0609 Appendix

G, Attachment 1, Phase 1 Operational Checklists for Both PWRs and BWRs,

Checklist 4, PWR Refueling Operation: RCS level > 23' or PWR Shutdown Operation

with Time to Boil > 2 hours2.314815e-5 days <br />5.555556e-4 hours <br />3.306878e-6 weeks <br />7.61e-7 months <br /> And Inventory in the Pressurizer, the issue screens to

having Green (i.e., very low) safety significance because RCS makeup capability was

not degraded since one or more low pressure makeup water sources would remain

available. The inspectors determined that the issue had a cross-cutting aspect in the

area of Human Performance, Decision Making, in that the licensee failed to use

conservative assumptions and adopt a requirement to demonstrate that the proposed

action is safe in order to proceed rather than a requirement to demonstrate that it is

unsafe in order to disapprove the action (H.1.b).

Enforcement: 10 CFR 50, Appendix B, Criterion XVI, Corrective Actions, states that

measures shall be established to assure that conditions adverse to quality, such as

failures, malfunctions, deficiencies, deviations, defective material and equipment, and

non-conformances are promptly identified and corrected. In the case of significant

conditions adverse to quality, the measures shall assure that the cause of the

condition is determined and corrective action taken to preclude repetition.

Contrary to the above, from July 2011 until November 2011, a SCAQ related to the

misalignment of the 480 VAC breakers, which was identified as the cause of the 1B3A

- 22 -

fire, was identified to exist in other equipment, but corrective actions to preclude

repetition were not taken in a timely manner. Additionally from June 22, 2011, until

February 27, 2012, a known degraded breaker was allowed to remain in service for

approximately 8 additional months until the cause was identified. This was also not

timely. FCS corrected the nonconforming conditions in the breakers and has revised

its corrective action program. However, because this violation was of very low safety

significance, and FCS has entered this issue into their its corrective action program as

CRs 2012-01884 and 2011-5414, the NRC is treating this as an NCV in accordance

with Section 2.3.2 of the NRC Enforcement Policy;05000285/2012005-02, Untimely

Corrective Actions for 480 VAC Breaker Issues.

.e Third-Party Safety Culture Assessment

Item 1.e is included in the restart checklist because the NRC recognizes the importance

of nuclear plant licensees establishing and maintaining a strong safety culture, a work

environment where management and employees are dedicated to putting safety first. In

addition, nuclear power plants should have a work environment where employees are

encouraged to raise safety concerns, and where concerns are promptly reviewed, given

the proper priority based on their potential safety significance, and appropriately resolved

with timely feedback to the originator of the concerns and to other employees.

(1) Inspection Scope

The NRC attended safety conscious work environment (SCWE) training that FCS

provided to its supervisors on September 13, 2012. The site vice president

introduced the training class with a discussion of why the training was being

conducted. The training material included the topics of employee protection,

regulations, the definition of SCWE and its relationship to safety culture, the attributes

of SCWE, discrimination, and the safety culture survey results performed at FCS in

May 2012. The instructor emphasized the importance of encouraging people to enter

issues into the FCS corrective action program (CAP).

(2) Assessment

Inspectors thought that the training content was adequate and that the opportunity at

the end of the training for supervisors to discuss the safety culture survey results was

beneficial. During the training, the instructor discussed the differences between the

concepts of perception of retaliation versus proof of retaliation. A question of

perception versus proof of retaliation also came up during the meeting on

July 19, 2012, in which fundamental performance deficiencies were discussed. NRC

inspectors commented to FCS staff during a weekly debrief that insights from the

sites employee concerns program manager, union, and human resources department

could have been incorporated into the training to help clarify what types of behavior

FCS employees are perceiving as retaliation.

- 23 -

(3) Findings

No findings or violations of NRC requirements were identified; however, the NRC will

continue its assessment of this CAL item. This restart checklist item remains open.

.2 Flood Restoration and Adequacy of Structures, Systems, and Components

Section 2 of the Restart Checklist contains those items necessary to ensure that important

structures, systems and components affected by the flood are in adequate condition to

support safe restart and continued safe plant operation. Section 2 reviews will also include

an assessment of how the licensee addresses the NRC Inspection Procedure 95003 key

attributes as described in Section 6.

.a Flood Recovery Plan Actions Associated With Facility and System Restoration

Item 2.a is the NRCs independent evaluation of Fort Calhoun Stations Flood Recovery

Plan. An overall flood recovery plan is important to ensure the station takes a

comprehensive approach to restoring the facility structures, systems, and components to

pre-flood conditions.

On August 30, 2011, Fort Calhoun Station issued Revision 1 to the Fort Calhoun Station

Post-Flooding Recovery Action Plan, (FRAP) that provided for extensive reviews of plant

systems, structures, and components to assess the impact of the floodwaters. On

September 2, 2011, the NRC issued Confirmatory Action Letter (CAL) 4-11-003, listing

235 items described in the Fort Calhoun Station Post-Flooding Recovery Action Plan that

the licensee committed to complete. These 235 items were broken down into three

sections: items to complete prior to exceeding 210 degrees Fahrenheit in the reactor

coolant system, items to complete prior to reactor criticality; and items to complete

following restart of the plant. On June 11, 2012, the NRC issued CAL 4-12-002. This

CAL incorporates all the actions required by CAL 4-11-003.

The areas to be inspected are identified in the CAL. Inspection items are considered

complete when the licensee has submitted a closure package that has been satisfactorily

reviewed by the inspectors

(1) CAL Action Item 1.2.1.4

i.

Inspection Scope

The purpose of Action Item 1.2.1.4 was to return B.5.b materials to their proper

location. This item was required to be completed prior to exceeding 210 degrees

Fahrenheit in the Reactor Coolant System.

During the 2011 flood some B.5.b materials were displaced from their normal

location in the FCS warehouse to other locations on site.

- 24 -

After flood waters receded, the B.5.b materials were relocated from their

temporary location in the training center truck bay to their permanent location.

The licensee inventoried the equipment per Attachment 11 of OCAG-1,

Operational Contingency Action Guideline.

The inspectors performed an independent inventory of all B.5.b materials listed in

attachments 8, 9, 10, and 11 to ensure all equipment was accounted for.

This activity constitutes completion of Action Item 1.2.1.4 as described in

Confirmatory Action Letter 4-12-002.

ii. Findings

No findings were identified.

(2) CAL Action Item 2.1.1.3

i.

Inspection Scope

The purpose of Action Item 2.1.1.3 was to flush fire protection piping connected to

the fire protection header ring which flowed river water during flood mitigation

actions. This item was required to be completed prior to exceeding 210 degrees

Fahrenheit in the Reactor Coolant System.

In preparation for the Missouri River flooding in 2011, the licensee installed a

water filled protection device around the plant. This required large quantities of

water to be provided for extended periods of time. The licensee utilized the

electric driven fire pump, PF-1A to fill the individual sections of the protection

device with some of the exterior fire hose cabinets. This activity deposited river

water into the underground fire main piping around the plant.

The licensee performed OP-ST-FP-0011, Fire Protection System Hose Station

Operability Test to flush the underground fire main and to operate all exterior fire

hydrants. Each fire hydrant was flushed for approximately 2 hours2.314815e-5 days <br />5.555556e-4 hours <br />3.306878e-6 weeks <br />7.61e-7 months <br /> with clean,

fresh water.

The inspectors reviewed the USAR, procedure requirements, and technical

specifications to ensure that the surveillance activities demonstrated that the

systems, structures, and/or components tested were capable of performing their

intended safety functions. During performance of the surveillance test, Fire

Hydrant FP-3C was identified as degraded during flushing activities.

The licensee created a new action item in the flood recovery action plan, 2.1.3.8,

which was to replace FP-3C. The licensee replaced the fire hydrant, as well as its

associated isolation valve, FP-114.

The inspectors observed the installation of the fire hydrant and isolation valve, as

well as the postmaintenance testing to ensure the effect of testing on the plant

- 25 -

had been adequately addressed; testing was adequate for the maintenance

performed, and acceptance criteria were clear and demonstrated operational

readiness; and test instrumentation was appropriate.

This activity constitutes completion of Action Item 2.1.1.3 as described in

Confirmatory Action Letter 4-12-002, as well as flood recovery plan action item

2.1.3.8.

Findings

ii. No findings were identified.

(3) CAL Action Item 2.1.1.9

i.

Inspection Scope

The purpose of Action Item 2.1.1.9 was to complete full flow testing of fire pumps.

This item was required to be completed prior to exceeding 210 degrees

Fahrenheit in the Reactor Coolant System.

Due to the flooding conditions and the location of the water filled protection

device, access to the fire protection test header valves and general area required

for testing equipment was restricted. To complete full flow testing of the fire

pumps, a test rig was installed on a truck with fire hoses attached to the test

header. This test configuration required the areas west of the intake structure to

be clear. Due to the conditions from the flooding event the tests had to be

delayed until the flood waters had receded and the water filled protection device

was removed.

Surveillance Tests SE-ST-FP-0002 'Fire Protection System Motor Driven Fire

Pump Full Flow Test' and ST SE-STFP-0003 'Fire Protection System Diesel

Driven Fire Pump Full Flow Test' were completed as soon as the testing area and

equipment was accessible. Both the electric motor driven fire pump FP-1A and

the diesel driven fire pump FP-1 B passed their respective surveillance tests and

were returned to service and declared operable.

The inspectors reviewed the USAR, procedure requirements, and technical

specifications to ensure that the surveillance activities demonstrated that the

systems, structures, and/or components tested were capable of performing their

intended safety functions.

The inspectors witnessed and reviewed test data to verify that the significant

surveillance test attributes were adequate to address the following:

Preconditioning

Evaluation of testing impact on the plant

- 26 -

Acceptance criteria

Test equipment

Procedures

Jumper/lifted lead controls

Test data

Testing frequency and method demonstrated technical specification

operability

Test equipment removal

Restoration of plant systems

Fulfillment of ASME Code requirements

Updating of performance indicator data

Engineering evaluations, root causes, and bases for returning tested

systems, structures, and components not meeting the test acceptance

criteria were correct

Reference setting data

Annunciators and alarms setpoints

This activity constitutes completion of Action Item 1.2.1.4 as described in

Confirmatory Action Letter 4-12-002.

ii.

Findings

No findings were identified.

(4) CAL Action Item 2.2.1.32

i.

Inspection Scope

The purpose of Action Item 2.2.1.32 was to assess the effects of the flood on the

Communications System and identify actions to restore the system. This item

was required to be completed prior to exceeding 210 degrees Fahrenheit in the

Reactor Coolant System.

The inspectors independently reviewed the system to identify if there were any

temporary modifications in place, any outstanding preventive or corrective

maintenance required, and reviewed all open condition reports, as well as all

- 27 -

condition reports created since January 1, 2011. The inspectors also conducted a

complete system walkdown to identify any adverse conditions and to verify all

system components were functioning properly. The inspectors compared the

results of their independent assessment to those contained in the licensees

Flooding Recovery Startup System Health Assessment report.

The Plant Communications System uses a combination of dial telephones,

dedicated telephone lines, intra-plant intercom/paging facilities, Paging System

and a 800 MHz Radio Communication System for on-site information relaying and

alarm notification. It also provides off-site communications with other facilities and

support personnel. The Plant Communications System does not perform any

safety related functions.

The inspectors identified no adverse conditions associated with the Plant

Communications System.

This activity constitutes completion of Action Item 2.2.1.32 as described in

Confirmatory Action Letter 4-12-002.

ii. Findings

No findings were identified.

(5) CAL Action Item 2.3.1.1

i.

Inspection Scope

The purpose of Action Item 2.3.1.1 was to assess whether motors were to be

tested for possible use, refurbished or replaced. This item was required to be

completed prior to exceeding 210 degrees Fahrenheit in the Reactor Coolant

System.

The licensee determined that five normally dry pump motors were wetted for some

period of time: the three circulating water pump motors, CW-1A, CW-1B, and

CW-1C; and the Demineralized Water Storage Tank inlet and outlet pump motors,

DW-69 and DW-70.

The inspectors performed an independent assessment of which motors may have

been wetted. The assessment included individual inspector walkdowns during

and after the flood, and conversations with inspectors who had been present

during the site flooding in 2011. The inspectors also searched all opened

condition reports since the onset of flooding and concurred with the licensee that

the circulating water and demineralized water pumps were the only normally dry

pump motors that had been wetted by floodwaters.

The licensee also created action items 2.3.1.2 through 2.3.1.8 to track completion

of items associated with the circulating water pump motors, and action items

- 28 -

2.3.1.9 through 2.3.1.16 to track completion of items associated with the

demineralized water pump motors.

In addition to these five pumps, the switchgear room ventilation condensing units,

VA-89 and VA-90 were flooded when the water filled protection device around the

plant collapsed. These condensing units were repaired prior to the issuance of

the flood recovery plan.

This activity constitutes completion of Action Item 2.3.1.1 as described in

Confirmatory Action Letter 4-12-002.

ii. Findings

No findings were identified.

(6) CAL Action Items 2.3.1.2 and 2.3.1.1

i.

Inspection Scope

The purpose of Action Items 2.3.1.2 and 2.3.1.3 were to take oil sample from

bearing housings and evaluate if water had gotten in contact with the bearings in

the circulating water pump motors, CW-1A, CW-1B, and CQ-1C. These items

were required to be completed prior to exceeding 210 degrees Fahrenheit in the

Reactor Coolant System.

The licensee took cold oil samples from each of the circulating water pump

motors upper and lower bearing reservoirs on September 6 and 7, 2011. The

samples were then sent to a third party laboratory for analysis.

The inspectors observed the sampling of the oil and reviewed the analyses

results. Each of the 6 samples were first tested for water contamination via the

Crackel Test. The Crackle Test is a standard laboratory test to detect the

presence of water in lubricating oil. A drop of oil is placed on a hotplate that has

been heated to approximately 400 degrees Fahrenheit. The sample then bubbles,

spits, crackles or pops when moisture is present. The Crackel test showed

undetectable for water content for all samples except for the inboard bearing

reservoir for CW-1C motor.

The samples were then tested utilizing the Karl Fisher Titration method. This

method uses anode and titrant solutions to determine concentrations of water in

the oil. The Karl Fisher Titration results showed the inboard bearing reservoir for

CW-1C motor to contain approximately 110 parts per million (ppm) water, where

the other five bearing reservoirs contained between 20.0 and 21.5 ppm water.

This is indicative of flood water ingress into the inboard bearing reservoir for CW-

1C motor.

The refurbishment of CW-1C pump motor will be completed and evaluated under

Confirmatory Action Letter item 2.3.1.4,

- 29 -

This activity constitutes completion of Action Items 2.3.1.2 and 2.3.1.3 as

described in Confirmatory Action Letter 4-12-002.

ii. Findings

No findings were identified.

(7) CAL Action Items 2.3.1.5 and 2.3.1.6

i.

Inspection Scope

The purpose of Action Items 2.3.1.5 and 2.3.1.6 were to perform visual and

boroscope inspections of the circulating water pump motors and evaluate the

results. These items were required to be completed prior to exceeding 210

degrees Fahrenheit in the Reactor Coolant System.

The licensee performed a visual inspection of the circulating water pump motor

internals and termination boxes on September 8, 2011.

The inspectors performed an independent visual inspection of the pump motors,

and observed the licensee using the boroscope. The inspectors evaluated the

boroscope photographs and compared them to their visual inspection.

The inspection showed no signs of debris, silt, moisture or corrosion. The motors

did contain a fine film of dust throughout the stator winding as a normal result of

operation. The inspection showed similar results for all three motors. A cleaner

area was observed near the termination box opening into the motor of the CW-1C

motor. This was indicative of where water entered the motor.

No abnormal degradation was noted in any of the three pump motors. The

refurbishment of CW-1C pump motor will be completed as a result of water

intrusion into the motor oil as described in action items 2.3.1.2 and 2.3.1.3 and

evaluated under Confirmatory Action Letter item 2.3.1.4,

This activity constitutes completion of Action Items 2.3.1.5 and 2.3.1.6 as

described in Confirmatory Action Letter 4-12-002.

ii. Findings

No findings were identified.

(8) CAL Action Item 3.2.1.2

i.

Inspection Scope

- 30 -

The purpose of Action Item 3.2.1.2 was to test maintenance rule low voltage

power cable on cables which had been subjected to wetting/submergence. This

item was required to be completed prior to exceeding 210 degrees Fahrenheit in

the Reactor Coolant System.

The licensee performed megger testing on low voltage (480 volt) cable in

November 2011. The population of cables was those which were exposed to

water, traversing through manholes 5 and 31: the feeder cables for motor control

centers MCC-3B3 and MCC-4C4.

The inspectors observed the licensees megger testing and analyzed the result. A

megger test is performed to ensure the adequacy of the insulation in a cable. In

480 volt cables, 500 volts are applied to the cable for one minute, and the

resistance is measured. The acceptance criteria for 480 volt cables is 1.48

megohms. The inspectors verified that the resistance on the cables for MCC-3B3

were greater than 50,000 megohms, and for MCC-4C4 were greater than 2,000

megohms.

This activity constitutes completion of Action Item 3.2.1.2 as described in

Confirmatory Action Letter 4-12-002.

ii.

Findings

No findings were identified.

(9) CAL Action Item 3.2.1.3

i.

Inspection Scope

The purpose of Action Item 3.2.1.3 was to test maintenance rule low voltage

control and instrumentation on cables which had been subjected to

wetting/submergence. This item was required to be completed prior to exceeding

210 degrees Fahrenheit in the Reactor Coolant System.

The licensee performed megger testing on low voltage instrumentation and

control cables in October, 2011. The population of cables was those which were

exposed to water, traversing through manholes 5 and 31: motor driven fire pump,

FP-1A, control cable; the four raw water pump discharge valve control cables,

HCV-2850, HCV-2851, HCV-2852, and HCV-2853; and the six raw water

discharge header isolation valve control cables, HCV-2874A & B, HCV-2875A & B,

and HCV-2876A & B.

The inspectors observed the licensees megger testing and analyzed the result. A

megger test is performed to ensure the adequacy of the insulation in a cable. In

low voltage control and instrumentation cables, 250 volts are applied to the cable

for one minute, and the resistance is measured. The acceptance criteria for these

cables is 1.13 megohms. The inspectors verified that the resistance on all of the

cables was greater than 2,000 megohms.

- 31 -

This activity constitutes completion of Action Item 3.2.1.3 as described in

Confirmatory Action Letter 4-12-002.

ii.

Findings

No findings were identified.

.3 Adequacy of Significant Programs and Processes

Section 3 of the Restart Checklist addresses major programs and processes in place at Fort

Calhoun Station. Section 3 reviews will also include an assessment of how the licensee

addressed the NRC Inspection Procedure 95003 key attributes as described in Section 6.

.a Corrective Action Program

(1) Inspection Scope

The Corrective Action Program and the use of industry Operating Experience at a

nuclear power plant is a key element in ensuring the licensees ability to effectively

detect, correct, and prevent problems. A properly functioning Corrective Action

Program is also a basis for licensee operation within the Reactor Oversight Process.

Based upon observed problems with Corrective Action Program effectiveness the

licensee is performing a comprehensive review of this program.

The NRC will assess the licensees review and potential changes to the Corrective

Action Program. The NRC will also conduct independent inspections to validate

whether the Corrective Action Program is appropriately functioning.

For the assessment period covered by this inspection report, the onsite activities

included the observation of CAP meetings such as the Department Station Corrective

Action Review Board (DCARB), which was observed for the Operations Department,

and a presentation of the licensees corrective actions taken to date. The presentation

also included an explanation of the root causes identified as a result of the licensees

review of the CAP and what the next steps are for their improvement plan. In

addition, the inspectors interviewed site personnel associated with the Performance

Improvement department to continue to get a better understanding of the site CAP

processes. The in-office activities, which were conducted at the inspectors regular

duty stations, consisted of reviews of root cause analyses and procedures associated

with the Corrective Action Program.

(2) Assessment

During this assessment period, the inspectors attended one DCARB meeting for the

Operations Department. To be able to reasonably assess these processes, the

inspectors will continue to attend more of these meetings and observe more of the

CAP processes during future on-site inspection weeks. In general, the inspectors

noted a general attitude to follow the CAP procedures and healthy willingness to

- 32 -

express dissenting views during CAP meetings. However, during the course of

interviews, plant tours and interactions with plant personnel, the inspectors have also

noted a general behavioral issue with the threshold to initiating Condition Reports

(CRs). The inspectors have noted that, especially with lower level issues, the workers

opt for an attempt to repair the condition in-place and not writing a condition report to

document the deficiency, and place it in the CAP. The inspectors noted that this

approach could prevent issues from being placed in the CAP at an early stage.

(3) Findings

No findings of significance were identified.

.b Equipment Design Qualifications

This item of the Restart Checklist verifies that plant components are maintained within

their licensing and design basis. Additionally, this item provides monitoring of the

capability of the selected components and operator actions to perform their functions. As

plants age, modifications may alter or disable important design features making the

design bases difficult to determine or obsolete. The plant risk assessment model

assumes the capability of safety systems and components to perform their intended

safety function successfully.

.i

Safety-Related Parts Program

A number of instances have been identified where non-safety-related parts have been

installed into safety-related applications. Fort Calhoun Station is performing reviews

to identify conditions where a non-safety-related component or subcomponent was

improperly used in a safety-related application. The restart checklist includes an NRC

assessment of the licensees equipment design qualifications review for inconsistent

quality classifications and the licensees review of the use of non-safety-related parts

in safety-related applications.

(1) Inspection Scope

NRC inspectors reviewed the licensees procedure, scope of work, and training

material for assessing their safety-related parts program. Inspectors also

interviewed station personnel and contractors that performed the reviews.

Inspectors reviewed a sample of the condition reports generated from the review

and draft revisions of the individual system and collective evaluations, many of

which have not been finalized as of the end of the inspection period covered by

this report.

(2) Assessment

During the inspection period, OPPD completed the discovery phase of its

evaluations of this issue. The discovery phase was designed to identify all work

orders (WOs) where non safety related parts were issued for jobs involving safety-

- 33 -

related SSCs. This process identified 2100 WOs to be evaluated to determine if

non safety related parts were installed in safety-related systems and, if so,

whether these parts impacted the systems functionality and operability. At the

end of the inspection period, the licensee had reviewed approximately 40 percent

of the 2100 WOs, and approximately 15 of those WOs required an evaluation of

the impact on system functionality and operability. The NRC inspectors will

continue to review all instances of WO issues that resulted in system functionality

evaluations, and the team will assess a sampling of the WOs for which further

evaluations were performed to determine the effectiveness of the licensees

review. This restart checklist item will remain open until all WOs have been

screened and questions related to operability of SSCs required for Modes 1 and 2

have been appropriately evaluated and addressed.

During the inspection period, FCS changed its scope expansion criteria for this

project. Originally, FCSs scope expansion was based on criteria related to the

number of WOs discovered in the discovery phase and adding more WOs to the

population to be evaluated. FCS changed this scope expansion criteria to one

based upon components evaluated to have been installed in a safety related

application and requiring further review. When an item is found to meet this

criteria, the scope is expanded to search for additional WOs where this part was

issued beyond the original 5-year scope and in other systems. The change was

made to allow the scope expansion to be more risk based. The inspectors will

assess if the revised scope expansion criteria is as effective as identifying

vulnerabilities which occurred beyond the original 5-year scope.

In addition, FCS is in the process of replacing its CQE/non-CQE terminology

with safety-related/non-safety related terminology. FCS staff expects the

updates to station programs and procedures to be completed in 2012. The CQE-

to-safety related terminology conversion is expected to be completed in October

2013, and the non-CQE-to-non-safety related terminology conversion is

supposed to be completed by January 2014.

(3) Findings

No findings or violations of NRC requirements were identified; however, the NRC

will continue its assessment of this CAL item.

.ii High Energy Line Break (HELB) Program and Equipment Qualifications

Industry experience with extended power up-rates (a method some plants use to

produce more power from the same reactor) highlighted potential problems

associated with HELB effects. In preparations for a postponed extended power up-

rate, Fort Calhoun Station reviewed HELB calculations. FCS personnel found that it

was lacking adequate documentation and calculations for HELB effects in some

areas. The restart checklist includes an NRC assessment of FCSs HELB analyses

and documents to ensure the plant is within its licensing and design basis for HELB

- 34 -

effects. The NRC will also assess the licensees qualifications and documentation for

certifying equipment for harsh environments.

(1) Inspection Scope

NRC inspectors reviewed the licensees procedure, scope of work, and training

material for assessing the HELB and Equipment Qualification programs.

Inspectors also interviewed station personnel and contractors that performed the

reviews. Inspectors reviewed a sample of the condition reports generated from

the review and a draft revision of the collective evaluation, which has not been

completed as of the end of the inspection period covered by this report.

(2) Assessment

During this inspection period, OPPD continued to evaluate concerns related to

containment electrical penetrations discussed in LER 2852012002, and an overall

review of the Environmental Qualification program and HELB program including a

reassessment of the HARSH environment files and program scope and basis.

These reviews were still in progress at the end of the inspection period.

Therefore, the NRCs review of this restart checklist item is still in progress.

Closure of this restart checklist item will be dependent on, in part, the evaluation

and resolution of the issues discussed in the aforementioned LERs, including any

operability concerns.

(3) Findings

No findings or violations of NRC requirements were identified; however, the NRC

will continue its assessment of this CAL item.

.c Design Changes and Modifications

Modifications to risk-significant structures, systems, and components can adversely affect

their availability, reliability, or functional capability. Modifications to one system may also

affect the design bases and functioning of interfacing systems. Similar modifications to

several systems could introduce potential for common cause failures that affect plant risk.

A temporary modification may result in a departure from the design basis and system

success criteria. Modifications performed during increased risk configurations could

place the plant in an unsafe condition.

This item assesses the effectiveness of the licensees implementation of changes to

facility structures, systems, and components, risk significant normal and emergency

operating procedures, test programs, evaluations required by 10 CFR 50.59, and the

updated final safety analysis report. The NRC will inspect to provide assurance that

changes have been appropriately implemented.

.i

Vendor Modification Control

- 35 -

Past NRC inspections indicated that the licensee failed to ensure critical

characteristics were identified and properly addressed in several modification

packages. FCS is currently reviewing work performed by vendors. The restart

checklist includes an NRC assessment of the effectiveness of the licensees vendor

program, including its oversight of vendor work.

(1) Inspection Scope

NRC inspectors interviewed station personnel and contractors that performed the

reviews. Inspectors also reviewed the collective evaluation condition report.

(2) Assessment

The licensee completed its latest version of the collective evaluation condition

report, which summarized the results of its review of modification packages

prepared by vendors. The condition report mentions that significant issues were

identified; however, the licensee stated that it does not plan to perform a root

cause analysis on this topic. The inspector discussed some discrepancies in the

report in the characterization of identified issues. For example, the overall

conclusion in the report was that the identified issues were administrative;

however, another section of the report mentions significant issues were identified.

The licensee stated that it was aware of the discrepancies and is revising the

report. Inspectors also expressed a concern that the condition report stated what

the causal analysis should conclude instead of allowing the causal analysis

process to come to its own conclusions. The inspectors expressed the concern

that the effort was potentially being biased by the results of the organizational

effectiveness root cause analysis. The licensee stated that a final report for this

issue was still in progress.

(3) Findings

No findings or violations of NRC requirements were identified; however, the NRC

will continue its assessment of this CAL item.

.ii 10 CFR 50.59 Screening and Safety Evaluations

Past NRC inspections indicated that several changes to the facility were not properly

screened or evaluated in accordance with the requirements of 10 CFR 50.59. FCS is

evaluating past 10 CFR 50.59 documents. The restart checklist includes an NRC

assessment of plant and procedure modifications to determine if those modifications

were appropriately evaluated in accordance with 10 CFR 50.59. The NRC will also

evaluate the effectiveness of the licensees 10 CFR 50.59 process to ensure proper

treatment of changes to the facility.

(1) Inspection Scope

- 36 -

NRC inspectors interviewed station personnel and contractors that performed the

reviews. Inspectors reviewed a sample of the condition reports generated from

the review.

(2) Assessment

The licensee stated that they completed their review of 50.59 documents and the

collective evaluation condition report and are in the stage of developing a final

report before commencing a root cause analysis for the identified issues. The

collective evaluation condition report summarizes the results of the licensees

review of 50.59 documents. The report attachment contained the same statement

as the vendor modification report about what the cause analysis should state,

which further supported the inspectors concern that the organization

effectiveness root cause analysis results could bias other root cause analyses.

The licensee stated that they would remove these statements from the condition

reports.

The condition reports documenting the results of each 50.59 document review

contained due dates for when the identified issues would be corrected, if FCS staff

decided the issues had to be corrected. The inspectors noticed that some of the

corrective actions (e.g., updating the 50.59 documents with applicable design

basis information to support the conclusions) were deferred until after restart.

Inspectors also noticed a condition report that identified that design basis

information was not adequately incorporated or referenced in a 50.59 for an

engineering change (EC); however, FCS staff responded to the condition report

that there was no benefit to correcting the EC package because the summary of

the modification was already sent to the NRC, and the result of the 50.59 would

have been the same. The licensee stated that the contractors performing the

reviews were relying on experience and judgment to gauge whether NRC

approval would have been needed for determining the due dates for correcting

issues.

NRC inspectors attended a portion of 50.59 training that was provided by a

contractor to FCS staff. The training was thorough and of high quality.

The NRC will continue its review of the 50.59 documentation and associated

condition reports evaluated by the licensee. The NRC will also review the final

report, root cause analysis, corrective actions, and the effectiveness of those

corrective actions when completed by the licensee. This restart checklist item

remains open.

(3) Findings

No findings or violations of NRC requirements were identified; however, the NRC

will continue its assessment of this CAL item.

.d Maintenance Programs

- 37 -

Inadequate maintenance activities that are not detected prior to returning the equipment

to service can result in a significant increase in unidentified risk for the subject system.

The Maintenance Rule (10 CFR 50.65) requires licensees to monitor the performance or

condition of structures, systems and components within the scope of the rule against

licensee-established goals to provide reasonable assurance that these structures,

systems, and components are capable of fulfilling their intended functions. These goals

are to be commensurate with safety and, where practical, should take into account

industry-wide operating experience.

The NRC will assess the licensees maintenance programs, including preventative

maintenance, compliance with vendor recommendations, post-maintenance testing

programs, and establishing and controlling equipment service life.

(1) Inspection Scope

.i

Vendor Manuals and Vendor Informational Control Programs

NRC inspections determined vendor manuals and information have not been

adequately maintained, which has resulted in adverse conditions at Fort Calhoun

Station. The licensee will perform a review to identify and incorporate updates to

vendor manual technical documentation. This review applies to all equipment and

components classified as a Critical Quality Element (safety-related). Changes in

vendor guidance will be evaluated to determine what impact, if any, the new

information has on scheduled work, work completed since the last vendor manual

update was made, and changes to plant documentation. The NRC will evaluate

the effectiveness of the licensees incorporation of vendor information into

applicable plant procedures and design documents to ensure proper maintenance

and operation of facility equipment.

.ii Equipment Service Life

NRC inspections determined that the licensee opted to keep some plant

equipment in service beyond the vendor recommended service life or standard

industry guidelines. Operating equipment past the recommended replacement

timeline has resulted in age-related failures at Fort Calhoun Station. In response,

the licensee will perform an assessment to evaluate the service life of

safety-related plant equipment and the effectiveness of programs used to

implement service life requirements. The NRC will inspect and assess the

adequacy of this evaluation and the associated corrective actions.

(2) Assessment

The team noted that a new apparent cause analysis is being performed for the vendor

manual area and the targeted completion date for this new analysis is October 30,

2012. The licensee does not currently have a schedule for completion of all

corrective actions. The NRC will close out this issue for restart after the inspections

- 38 -

verify that the station has 1) completed the new apparent cause analysis, 2)

completed the corrective actions from the apparent cause analysis, and 3) completed

all actions necessary to prevent re-occurrence. Additionally, because the vendor

manuals contain the service life requirements for most equipment and their

subcomponents, the inspectors will need to complete the service life corrective

actions as well to ensure proper reconciliation of these programs was accomplished.

The licensee wrote Condition Report CR 2012-09215 to address the reconciliation

issue.

The team noted that the root cause analysis being performed for the equipment

service life issue is scheduled to be completed on November 28, 2012. The licensee

does not currently have a schedule for completion of all corrective actions. The NRC

will close out this issue for restart after the inspections verify that the station has

1) completed the root cause analysis, 2) completed the corrective actions from the

root cause analysis, and 3) completed all actions necessary to prevent re-occurrence.

As mentioned above, proper reconciliation will need to be verified for this issue as

well (Condition Report CR 2012-09215).

(3) Findings

No Findings of significance were identified.

.e Operability Process

Improper evaluations of degraded and/or non-conforming conditions may result in

continued operation with a structure, system, or component that is not capable of

performing its design function.

(1) Inspection Scope

.i

Operability Determination Process

NRC inspections determined that Fort Calhoun Station did not consistently

conduct adequate Operability Evaluations to ensure that the impacts of degraded

conditions on plant operations are fully understood. In response, the licensee will

assess their operability evaluation program and develop corrective actions to

improve performance. The NRC will assess the licensees operability

determination process reviews. The NRC will inspect a sample of operability

determinations to ensure proper implementation of the licensees process and

ensure evaluations were correct.

.ii Degraded and Non-conforming Conditions

NRC inspection determined that some equipment identified as operable but

degraded remained degraded until subsequent failure occurred. Fort Calhoun

Station processes did not adequately identify degraded equipment or restore

equipment from a degraded condition to full qualifications in a timely manner. In

- 39 -

response, Fort Calhoun Station will assess their controls for the review of

operable but degraded equipment. The NRC will evaluate the effectiveness of

the changes made to the licensees tracking and treatment of operable but

degraded equipment.

(2) Assessment

The team noted that the root cause analysis being performed for the two issues of

operability and degraded and non-conforming conditions is scheduled to be

completed on November 16, 2012. The licensee does not currently have a schedule

for completion of all corrective actions. The NRC will close out these two issues for

restart after the inspections verify that the station has 1) completed the root cause

analysis, 2) completed the corrective actions from the root cause analysis, and 3)

completed all actions necessary to prevent re-occurrence.

The team reviewed several condition reports related to issues with containment spray

pumps, component cooling water pumps, and the emergency diesel generators. The

team also performed interviews and attended discussions with the licensee regarding

the operating experience program. A detailed write up on these systems,

components, and programs will be completed during the next six-week inspection

period.

(3) Findings

No Findings of significance were identified.

4OA5 Other Inspection Activities (TI 2515/188)

.1 (Opened and Closed) Temporary Instruction 2515/188 - Inspection of Near-Term Task Force

Recommendation 2.3 Seismic Walkdowns

NRC inspectors performed inspection activities to independently verify that Fort Calhoun Station

conducted seismic walkdown activities using an NRC-endorsed seismic walkdown methodology.

The seismic walkdowns are being performed at all sites in response to Enclosure 3 of a letter

from the NRC to licensees entitled, Request for Information Pursuant to Title 10 of the Code of

Federal Regulations 50.54(f) Regarding Recommendations 2.1, 2.3, and 9.3, of the Near-Term

Task Force Review of Insights from the Fukushima Dai-ichi Accident, dated March 12, 2012

(ADAMS Accession No. ML12053A340).

(1) Inspection Scope

The inspectors accompanied the licensee on their seismic walkdowns of :

The Motor Driven Auxiliary Feedwater Pump and associate equipment in Room

19 on August 8, 2012.

The B EDG and associated equipment on August14, 2012.

- 40 -

Walk down of the 1A2/1A4 switchgear area and inspection of the 1A4-9 breaker

cubicle.

The inspectors verified that the licensee confirmed that the following seismic features

associated with the above equipment and systems were free of potential adverse seismic

conditions by verifying:

Anchorages were free of bent, broken, missing or loose hardware.

Anchorages were free of corrosion that is more than mild surface oxidation.

Anchorages were free of visible cracks in the concrete near the anchors.

Anchorage configurations were consistent with plant documentation.

SSCs will not be damaged from impact by nearby equipment or structures.

Overhead equipment, distribution systems, ceiling tiles and lighting, and masonry

block walls are secure and not likely to collapse onto the equipment.

Attached lines have adequate flexibility to avoid damage.

The area appears to be free of potentially adverse seismic interactions that could

cause flooding or spray in the area.

The area appears to be free of potentially adverse seismic interactions that could

cause a fire in the area.

The area appears to be free of potentially adverse seismic interactions associated

with housekeeping practices, storage of portable equipment, and temporary

installations (e.g., scaffolding, lead shielding).

The inspectors independently performed their walkdown and verified that the following

areas were inspected and seismic features verified:

Walkdown of the Component Cooling Water Pump Area and associated

equipment on September 18, 2012.

Walk by of the Charging Pump Room and associated equipment on

September 19, 2012.

Additionally, inspectors verified that items that could allow the spent fuel pool to drain

down rapidly were added to the SWEL and these items were walked down by the

licensee.

(2) Findings and Observations:

No NRC-identified or self-revealing findings were identified.

The walkdowns were performed by contract personnel with support from OPPDs

operations and security departments. FCS appropriately conducted the walkdowns in

accordance with the industry guidance. Observations were documented in the corrective

action program as condition reports, as appropriate. The inspectors observed that FCS

completed walkdowns of all accessable equipment. For equipment which was

inaccessible (such as energized electrical busses) or equipment for which full walkdowns

- 41 -

could not be completed, the walkdowns were documented as not completed and followup

inspections were scheduled for system outage windows. The inspection of these items is

expected to be completed prior to plant restart.

4OA6 Meetings, Including Exit

Exit Meeting Summary

On October 18, 2012, the inspectors presented the inspection results to Mr. Mike Prospero, Plant

Manager, and other members of the licensee staff. Additionally, on November 7, 2012 one

finding was recharacterized as an Severity Level IV, cited violation. The licensee acknowledged

the issues presented. The inspector asked the licensee whether any materials examined during

the inspection should be considered proprietary. No proprietary information was identified.

- 1 -

Attachment

SUPPLEMENTAL INFORMATION

KEY POINTS OF CONTACT

Licensee Personnel

C. Cameron, Supervisor Regulatory Compliance

L. Cortopassi, Site Vice President

K. Erdman, Supervisor, Engineering Programs

M. Ferm, Manager, Site Performance Improvement

M. Frans, Manager, Engineering Programs

W. Hansher, Supervisor, Nuclear Licensing

K. Ihnen, Manager, Manager, Site Nuclear Oversight

J. James, Manager, Outage

R. King, Director, Site Maintenance

K. Kingston, Manager, Chemistry

T. Maine, Manager, Radiation Protection

E. Matzke, Senior Licensing Engineer

S. Miller, Manager, Design Engineering

V. Naschansy, Director, Site Engineering

T. Orth, Director, Site Work Management

A. Pallas, Manager, Shift Operations

M. Prospero, Division Manager, Plant Operations

T. Simpkin, Manager, Site Regulatory Assurance

M. Smith, Manager, Operations

LIST OF ITEMS OPENED, CLOSED, AND DISCUSSED

Opened

05000285-2011-010-00 LER Fire Causes a Circuit Breaker to Open Outside Design

Assumptions

05000285-2012-014-00 LER Containment Beam 22 Loading Conditions outside of the

Allowable Limits

05000285-2012-015-00 LER Electrical Equipment Impacted by High Energy Line Break

Outside of Containment

05000285-2012-016-00 LER

Unanalyzed Charging System Socket Welds to the Reactor

Coolant System 05000285/2012005-01

NOV Failure to Update the Safety Analysis Report - Solid Waste

- 2 -

Opened and Closed 05000285/2012005-02

NCV Untimely Corrective Actions for 480 VAC Breaker Issues

2515/188

TI

Inspection of Near-Term Task Force Recommendation 2.3

Seismic Walkdowns

- 3 -

LIST OF DOCUMENTS REVIEWED

Section 1R08: Inservice Inspection Activities

CONDITION REPORTS

2012-01123

PROCEDURES

NUMBER

TITLE

REVISION /

DATE

CFTC-09-108

Field Service Report Steam Generator Secondary Side

Services 2009 Outage

December

18, 2009

MRS-SSP-2229-

CFTC1

Analysis of Eddy Current Data

0

DRAWINGS

NUMBER

TITLE

REVISION /

DATE

E-925-096

Primary Piping Layout (Plan View)

18

MISCELLANEOUS DOCUMENTS

NUMBER

TITLE

REVISION /

DATE

CFTC-09-108

Field Service Report Steam Generator Secondary Side

Services 2009 Outage

December

18, 2009

89361

Steam Generator Services April 2008 Refueling Outage

May 5, 2008

Steam Generator Eddy Current Test Report - 2008

Refueling Outage

December 9,

2008

Revised License Amendment Request, Application for

Technical Specification Improvement Regarding Steam

Generator Tube Integrity Using the Consolidated Line Item

Improvement Process and Deletion of Sleeving as a Steam

Generator Tube Repair Method

August 30,

2006

FC06968

FCS RSG - Evaluation for the Impact of the RSG on FCS

0

EC31589

Replacement Steam Generators (Component)

0

- 4 -

CFTC1_SG-B_20080401_ADI-ADH-CALLS

9/5/2012

CFTC1_SG-A_20080401_ADI-ADH-CALLS

9/5/2012

MHI Presentation on FCS Steam Generators

9/5/2012

Page 11 from Final ECTReport08 R1 1364

4/2008

CFTC1_SGA_Pri_sec_res_abs_channels_minus-ndf

9/25/2012

CFTC1_SGB_Pri_sec_res_abs_channels_minus-ndf

9/25/2012

LTR-AMER-

MKG-12-1715

Westinghouse Steam Generator Operational Assessment

Scope

1

Tubes looked at:SG11HCALROD00005 65 tubes

4/27/2008

SG21HCALROD00002 181 tubes

4/30/2008

Section 1R15: Operability Evaluations

CONDITION REPORTS

2012-00550

2012-00551

2012-00552

2012-00657

2012-07085

2012-07143

2012-11933

PROCEDURES

NUMBER

TITLE

REVISION /

DATE

OP-12

Fueling Operations

64

DRAWINGS

NUMBER

TITLE

REVISION /

DATE

11405-S-17

Reactor Plant Basement Floor Plan El 994-0 Outline

17

11405-S-18

Reactor Plant Ground Floor Plan El 1013-0 Outline

4

11405-S-19

Reactor Plant Operating Fl Plan El 1045-0 and 1060-0

Outline

15

11405-S-20

Reactor Plant Reactor Foundation and Fuel Pit - Sheet 1

2

11405-S-23

Reactor Plant Section & Details Outline - Sheet 2

5

11405-S-24

Reactor Plant Section & Details Outline - Sheet 3

4

11405-S-39

Reactor Plant Ground Fl Plan El 1013-0 Reinf - Sheet 1

5

- 5 -

11405-S-41

Reactor Plant Operating Fl Plan El 1045-0 and 1060-0

Reinforcement - Sheet 1

4

11405-S-43

Reactor Plant Reactor Foundation & Fuel Pit Reinforcement

- Sheet 1

2

11405-S-44

Reactor Plant Reactor Foundation & Fuel Pit Reinforcement

- Sheet 2

2

11405-S-49

Auxiliary Building Misc Details

1

E-57

Refueling Area Crane Rail, Angle, Frame, Containment Plan

1038 Fy 6 In

1

CALCULATIONS

NUMBER

TITLE

REVISION /

DATE

FC01420

Reactor Plant Operating Floor Design

0

FC03230

Containment Structural Design: Columns, Beams,

Reinforcement, Various Elevations - Construction

2

FC06916

Seismic Analysis Calculation for the ReFueling Machine

(FH-1)

0

FC06971

Past Operability Evaluation: RV Head Laydown Area

Seismic Analysis

1

FC07176

Assessment of Concrete Beams at Elev. 1045'-0" in

Containment for Rx Vessel Head Load

2

MISCELLANEOUS DOCUMENTS

NUMBER

TITLE

REVISION /

DATE

USAR 5.11

Structures Other Than Containment

10

USAR App F

Classification of Structures and Equipment and Seismic

Criteria

9

Section 1R22: Surveillance Testing

WORK ORDERS

436013

436014

436015

PROCEDURES

- 6 -

NUMBER

TITLE

REVISION /

DATE

OP-ST-FH-0001

Refueling System Fuel Handling Machine (FH-1) Interlocks

Test

33

OP-ST-FH-0002

Refueling System Fuel Transfer System Interlocks Test

25

OP-ST-FH-0005

Refueling System Spent Fuel Handling Machine Refueling

Interlocks Test

28

Section 4OA4: IMC 0350 Inspection Activities

CONDITION REPORTS (CR)

2011-8955

2011-8950

2011-8957

2011-7319

2011-8956

2011-5718

2011-5831

2011-5930

2011-5963

2011-5830

2011-5834

2012-12612

2012-13491

2011-2865

2011-6726

2011-7675

2011-5433

2011-8109

2012-03734

2001-02933

2011-09384

2012-09795

2005-01815

2008-05695

2010-06905

2011-00814

2012-02063

2012-03886

2012-04299

2012-04973

2012-09865

2012-09771

2012-09865

2012-10480

2012-06714

2012-13444

2012-08177

2012-05253

2012-05382

2012-05383

2012-05256

2012-06715

2012-05383

2012-06715

2012-06714

2012-07827

2012-07878

2012-05385

2012-07367

2012-06707

2012-07350

2012-04499

2012-05384

2012-13281

2012-11064

2012-10382

2012-07279

2011-5553

2012-12780

2011-2790

2010-2387

2012-11201

2012-10977

2012-11215

2012-04425

2012-09265

2012-00307

2012-04492

2012-02331

2012-10963

2012-00986

2012-4315

2012-03819

WORK ORDERS (WO)

418123

424263

400199

396921

421701

421702

421703

417681

417698

PROCEDURES

NUMBER

TITLE

REVISION

- 7 -

PROCEDURES

NUMBER

TITLE

REVISION

OP-ST-FP-0001A

Fire Protection System Inspection and Test

17

OP-ST-FP-0002

Fire Protection Water Suppression System Valve

Cycling Test

33

OP-ST-FP-0011

Fire Protection System Hose Station Operability Test

8

OCAG-1

Operational Contingency Action Guideline

17

SE-ST-FP-0002

Fire Protection System Motor Driven Fire Pump Full

Flow Test

21

SE-ST-FP-0003

Fire Protection System Diesel Driven Fire Pump Full

Flow Test

25

FCS-65-2

Recovery Checklist Issue Closure

0

FCS-65-3

Restart Classification and Management of recovery

Action Items under MC 0350 Restart Oversight

1

NP 95003 Admin C

Admin Controls for 95003 Work Scope for Station

Recovery

1

PLDBD-CS-56

External Flooding

1

EPIP-OSC-7

Emergency Response Organization (ERO) Activation

at the Emergency Operations Facility (EOF)

3

EPIP-EOF-1

Activation of the Emergency Operations Facility

18

EPIP-TSC-2

Catastrophic Flooding Preparations

15

PE-RR-AE-1000

Flood Barrier Inspection and Repair

9

PE-RR-AE-1001

Flood Barrier and Sandbag Staging and Installation

16

PE-RR-AE-1002

Installation of Portable Steam Generator Make-up

Pumps

5

FCSG-64

External Flooding of Site

2

SO-G-124

Flood Barrier Impairment

2

AOP-01

Acts of Nature

31

AOP 38

Blair Water Main Trouble

4

AOP-36

Loss of Spent Fuel Cooling

8

AOP-19

Loss of Shutdown Cooling

17

- 8 -

PROCEDURES

NUMBER

TITLE

REVISION

OI-CW-1

Circulating Water System Normal Operation

67

EOP/AOP Floating Steps

3

CALCULATIONS

NUMBER

TITLE

REVISION

FC 08030

Intake Structure Cell Level Control Using the Intake

Structure Sluice Gates

11

MISCELLANEOUS DOCUMENTS

NUMBER

TITLE

REVISION

ACA 2011-3019

Equipment Service Life Apparent Cause Analysis

1

ACA 2011-09276 Apparent Cause Analysis for Missed Vendor Manual

1

RCA 2012-03986 Organizational Effectiveness Root Cause Analysis

0

ACA 2008-05695 Apparent Cause Analysis for SI-3A-M Pump Side Motor

Bearing Oil Level Found Low on Sight Glass

0

USAR 9.8

Auxiliary Systems: Raw Water System

31

RCA 2011-10135 Root Cause Analysis: Cultural Weaknesses in Problem

Identification and Resolution

0

RCA 2010-2387

Root Cause Analysis: External Flooding Protection

1

LIC-11-0011

OPPD Reply to Notice of Violation EA-10-084 (Revision 1)

June 7, 2011

Business Continuity Plan

June 11,

2011

Section 4OA5: Other Activities

DRAWINGS

NUMBER

TITLE

REVISION /

DATE

11405-E-61

Reactor Auxiliary Building Tray and Conduit Layout Plan

Basement FL EL 9890 West,

Rev 51

- 9 -

Section 4OA5: Other Activities

DRAWINGS

NUMBER

TITLE

REVISION /

DATE

11405-M-112

Containment & Auxiliary Building Miscellanious Piping Sh1,

Rev 17.

11405-M-66

Auxiliary Building RWD Vents, Drains, & Valve leak Offs EL

971-0 and 989-0,

Rev 19

303.130-M-001

CH-1A Oil Drain

Rev 1

70665-1 Sh1

Component Cooling Water Pump Specification,

Rev 7

A-6039 Sh 11

Safe Shutdown Target Drawing-Auxiliary Building basement

Level, Room 19

Rev 0.

A-6039 Sh 20

Safe Shutdown Target Drawing -Auxiliary Building Ground

Floor Level, Room 56

Rev 1

A-6039 Sh 25

Safe Shutdown Target Drawing-Auxiliary Building Ground

Floor Level, Room 63

Rev 0

A-6039 SH3

Safe Shutdown Target Drawing-Auxiliary building Basement

Level Room 6,

Rev 0

C 1845-833391

Installation & Assy 5 gallion 75 PSIG Suction Stabilizer.

Rev A

C-4055

Charging Pump A Flushing Line Vibration Restraints

Rev 1

D-12627

Cylinder Assembly PIB-STPS,

Rev 7

D-12629

Base Outline- P18

Rev 6

D-12742

Packing Cooling System

Rev 19

D-4112,

Addition of Suction Stabilizer & Discharge Pulsation

Dampener to Charging Pumps,

Rev 1

D-4228 Sh 2

CQE Piping Isometrics Seismic subsystem #CH-283-A

FC 259

Auxiliary Building Equipment Supports,

Rev 2

FIG 8.1.1

P&ID Plant Electrical System,

Rev 142

S-53, Auxiliary

Building

Intermediate Fl

EL 1025-0

Outline Sheet 1,

Rev 4

- 10 -

MISCELLANEOUS DOCUMENTS

TITLE

REVISION /

DATE

Electric Power Research Institute document 1025286, Seismic Walkdown

Guidance,

(ML12188A031)

IPEEE USI A46 ,Seismic Inspections.

List of FCS SWEL Items

9/17/12

NRC Request for Information Pursuant to Title 10 of the Code of Federal

Regulations 50.54(f) Regarding Recommendations 2.1, 2.3, and 9.3, of the

Near-Term Task Force Review of Insights from the Fukushima Dai-ichi

Accident, dated March 12, 2012

(ML12053A340).

Pre- Job Brief for Fukushima NTTF 2.3 Seismic Walkdowns.

Seismic Walkdown Checklist for AC-3B, CCW Pump.

Seismic Walkdown Checklist for AC-3C, CCW Pump.

Seismic Walkdown checklist for CH-1A, Charging Pump