05000244/LER-2012-001, Regarding Automatic State of B Emergency Disesel Generator Caused by Loss of Offsite Circuit 767 Due to Wildlife

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Regarding Automatic State of B Emergency Disesel Generator Caused by Loss of Offsite Circuit 767 Due to Wildlife
ML12212A214
Person / Time
Site: Ginna Constellation icon.png
Issue date: 07/26/2012
From: Dean E
Constellation Energy Nuclear Group, EDF Development, Ginna
To:
Document Control Desk, Office of Nuclear Reactor Regulation
References
LER 12-001-00
Download: ML12212A214 (6)


LER-2012-001, Regarding Automatic State of B Emergency Disesel Generator Caused by Loss of Offsite Circuit 767 Due to Wildlife
Event date:
Report date:
Reporting criterion: 10 CFR 50.73(a)(2)(viii)(A)

10 CFR 50.73(a)(2)(iv)(A), System Actuation
2442012001R00 - NRC Website

text

Sonny Dean Plant General Manager CENG.

a joint venture of Constellation eD O

'Ene eD R.E. GINNA NUCLEAR POWER PLANT R.E. Ginna Nuclear Power Plant, LLC 1503 Lake Road Ontario, New York 14519-9364 585.771.5205 585.771.3943 Fax sonny.dean*.cenqllc.com July 26, 2012 U.S. Nuclear Regulatory Commission Washington, DC 20555-0001 ATTENTION:

SUBJECT:

Document Control Desk R.E. Ginna Nuclear Power Plant Docket No. 50-244 LER 2012-001, Automatic Start of "B" Emergency Diesel Generator Caused by Loss of Offsite Circuit 767 Due to Wildlife The attached Licensee Event Report (LER) 2012-001 is submitted under the provisions of NUREG-1022, Event Reporting Guidelines. There are no new commitments contained in this submittal. Should you have any questions regarding the information in this letter, please contact Mr. Thomas Harding at (585) 771-5219.

Very truly yours, Edwin D. Dean III Attachments: (1) LER 2012-001 cc:

W.M. Dean, NRC M.C. Thadani, NRC Resident Inspector, NRC (Ginna)

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LER 2012-001 July 26, 2012 Page 2 bcc:

J. Pacher S. Dean T. Harding J. Jackson E. P. Perkins C.W. Fleming COMMITMENTS IDENTIFIED IN THIS CORRESPONDENCE:

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ATTACHMENT 1 I

LER 2012-001

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ABSTRACTIA;(Llitfia 40sas.W. prkmti 15 ;ingle-sacedl typewfl ten lines)

On Sunday, 06/03/2012 at approximately 0239, offsite power circuit 767 tripped offline resulting in a loss of Bus 12B. Upon investigation, the cause was determined to be a fault caused by a raccoon. With the electrical system in the normal 50%/50% alignment, the loss of circuit 767 caused the 480v safeguards buses 16 and 17 to momentarily lose power until the B emergency diesel generator automatically started and reenergized the safeguards buses as designed.

The cause of the loss of power to Circuit 767 was determined to be a temporary fault caused by a raccoon, no damage to the plant equipment occurred. Additional Animal Deterrent Devices are b~ing developed for installation.

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2012 001 0

NAýRRATIVE, L""". "DESCRIPTION OF EVENT A.

PRE-EVENT PLANT CONDITIONS:

- On June 03, 2012 the plant was in Mode 1 at approximately 100% reactor power. Reactor Coolant System (RCS) pressure was 2235 psig and RCS temperature was 574F. The offsite electrical system was in the 50%/50% lineup, meaning that each offsite circuit was providing power to two (2) of the four (4) 480 Volt Safeguards Busses.

B.

EVENT:

- On June 03, 2012 at approximately 0239, offsite power circuit 767 was lost due to a fault caused by a raccoon. This resulted in a momentary loss of safeguards busses 16 and
17. The B emergency diesel generator automatically started and supplied power to busses 16 and 17 as designed.
- Off site power circuit 7T remained operable during this event. The offsite power configuration was later changed to a 100%/0% lineup, with circuit 7T supplying offsite power requirements.
- The plant remained at approximately 100% power throughout the event.

C.

INOPERABLE STRUCTURES, COMPONENTS OR SYSTEMS THAT CONTRIBUTED TO THE EVENT:

- None.

D.

DATES AND APPROXIMATE TIMES OF MAJOR OCCURRENCES

06/03/2012, 0239 EST Event Date and Time, Loss of Off-site power circuit 767 and B Emergency Diesel Generator automatic start supplying power to busses 16 and 17 06/03/2012, 0318 EST Busses 16 and 17 returned to off-site power (Circuit 7T) 06/03/2012, 0448 EST B Emergency Diesel Generator shut down 06/03/2012, 0607 EST Notification of B Emergency Diesel Generator start, event # 47988 under 10CFR50.72(b)(3)(iv)(A)

E.

OTHER SYSTEMS OR SECONDARY FUNCTIONS AFFECTED

- None.

F.

METHOD OF DISCOVERY

- Main Control Board Alarms associated with loss of offsite power and Emergency Diesel Generator start.

G.

MAJOR OPERATOR ACTION:

- Operations responded to the loss of circuit 767 using abnormal operating procedure AP-ELEC.1 "Loss of 12A and/or 12B Busses"
- Offsite power was restored to bus 12 B using ER-ELEC.1 "Restoration of Off-site Power"
- Restored offsite power to pre-event lineup with 0-6.9.2 1

NRC FORM i64 (I 10-2010)

ILICENSEEEVENTREPORT (AER) U.S.NUCLEAREGUlTORY COMMISSION (14~O1O)CONTIUTION'SHIEET

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3., PAGE NUMBERý

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R.E. Ginna Nuclear Power Plant

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NARRAT:IVE H.

SAFETY SYSTEM RESPONSES:

- The B Emergency Diesel Generator operated properly and as expected.

II.

CAUSE OF EVENT

- The cause is raccoon interaction with power lines causing a temporary fault (CR-2012-003664). The raccoon caused a line to ground fault. Pilot wire differential and overcurrent relays operated, opening primary and secondary side transformer breakers for circuit 767.

Ill.

ANALYSIS OF THE EVENT

- This event is reportable as an LER under 10CFR50.73(a)(2)(iv)(A) due to the automatic start of B Emergency Diesel Generator and loading onto its safeguards buses not being part of a pre-planned sequence during testing.
- There were no safety consequences as the redundant offsite circuit and Emergency Diesel Generators were operable and performed as designed.

IV

CORRECTIVE ACTIONS

A.

ACTION TAKEN TO RETURN AFFECTED SYSTEMS TO PRE-EVENT NORMAL STATUS

- Offsite power configuration was changed to 100%/0% lineup with Circuit 7T supplying power to all four (4) safeguards buses. B Emergency Diesel Generator was later stopped and aligned for auto standby
- Control room personnel were contacted by RG&E stating that circuit 767 was available. They then returned offsite power to 50%/50% lineup power using procedure 0-6.9.2.
- Inspection of equipment revealed no damage B.

ACTION TAKEN TO PREVENT RECURRENCE

- Development and installation of additional Animal Deterrent Devices is planned.

V.

ADDITIONAL INFORMATION

A.

FAILED COMPONENT(s)

- None.

B.

PREVIOUS LERs ON SIMILAR EVENTS

- A review of recent Ginna events involving the start of B Emergency.Diesel Generator revealed only one other event (LER 1997-002) that was caused by an animal, and all the events occurred external to Ginna and Station 13a:
- LER 2005-002
- LER 2005-003
- LER 2003-006
- LER 1997-002 1

N4RC FOR'k 3616A (0201ý06)