ML110070347

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IR 05000482-10-008, on 06/21/10 - 11/24/10, Wolf Creek Generating Station, Special Inspection in Response to Component Cooling Water System Gas Accumulation
ML110070347
Person / Time
Site: Wolf Creek Wolf Creek Nuclear Operating Corporation icon.png
Issue date: 01/07/2011
From: Hay M
Division of Reactor Safety IV
To: Matthew Sunseri
Wolf Creek
References
IR-10-008
Download: ML110070347 (41)


See also: IR 05000482/2010008

Text

UNITED STATES

NUCLEAR REGULATO RY COM M I SS I ON

R E G I ON I V

612 EAST LAMAR BLVD, SUI TE 400

ARLI NGTON , TEXAS 76011-4125

January 7, 2011

Mr. M. W. Sunseri, President and

Chief Executive Officer

Wolf Creek Nuclear Operating Corporation

P.O. Box 411

Burlington, KS 66839

SUBJECT: WOLF CREEK GENERATING STATION - NRC SPECIAL INSPECTION

REPORT 05000482/2010008

Dear Mr. Sunseri:

On November 24, 2010, the U.S. Nuclear Regulatory Commission (NRC) completed a special

inspection at your Wolf Creek Generating Station. The inspection examined activities

associated with the discovery of gas accumulation in your component cooling water system on

June 1, 2010 and residual heat removal system on July 1, 2010. The NRCs initial evaluation

satisfied the criteria in the NRC Management Directive 8.3, NRC Incident Investigation

Program, for conducting a special inspection. The NRCs initial evaluation of this issue using

the criteria in NRC Management Directive 8.3, NRC Incident Investigation Program,

determined that the estimated Incremental Conditional Core Damage Probability was in the

overlap region between a special and an augmented inspection. However, it was determined

that the model utilized likely over estimated the risk due to the failure assumptions. Therefore,

based on management discretion, a decision was made that, although the risk for this event

was in the overlap region, a special inspection would be performed since the risk for the issue

was likely over estimated. The basis for initiating this inspection is further discussed in the

inspection charter, which is Enclosure 2 to the report.

The enclosed report documents the inspection results, which were discussed at the exit meeting

on November 24, 2010, with Mr. S. Hedges, Site Vice President, and other members of your

staff. The determination that the inspection would be conducted was made by the NRC on June

15, 2010, and the inspection started on June 21, 2010.

The inspection examined activities conducted under your license as they relate to safety and

compliance with the Commissions rules and regulations and with the conditions of your license.

The inspection team reviewed selected procedures and records, observed activities, and

interviewed personnel.

This report documents three NRC-identified violations and one self-revealing violation of very

low safety significance (Green). Although the safety significance of these issues were

determined to be very low the causes for your delay in identifying, evaluating, and correcting the

voided conditions is of concern. The inspection determined that your operators and engineering

staff missed several opportunities to promptly identify and correct the voiding concerns. These

included missed opportunities during review of operating experience, indications of abnormal

flow oscillations, and abnormal flow control valve operation. In addition, when the voiding

Wolf Creek Nuclear Operating Corporation -2-

conditions were identified your evaluations failed to take into account all plant conditions

affected by the degraded condition.

All of these findings were determined to involve violations of NRC requirements. However,

because of the very low safety significance and because they are entered into your corrective

action program, the NRC is treating these findings as noncited violations, consistent with

Section 2.3.2 of the NRC Enforcement Policy. If you contest any NCV, you should provide a

response within 30 days of the date of this inspection report, with the basis for your denial, to

the Nuclear Regulatory Commission, ATTN: Document Control Desk, Washington, D.C.

20555-0001, with copies to the Regional Administrator, Region IV; the Director, Office of

Enforcement, United States Nuclear Regulatory Commission, Washington, D.C. 20555-0001;

and the NRC Resident Inspector at Wolf Creek Generating Station. In addition, if you disagree

with the crosscutting aspect assigned to any finding in this report, you should provide a

response within 30 days of the date of this inspection report, with the basis for your

disagreement, to the Regional Administrator, Region IV, and the NRC Resident Inspector at

Wolf Creek Generating Station. The information you provide will be considered in accordance

with Inspection Manual Chapter 0305.

In accordance with 10 CFR 2.390 of the NRC's "Rules of Practice," a copy of this letter, its

enclosure, and your response (if any) will be available electronically for public inspection in the

NRC Public Document Room or from the Publicly Available Records (PARS) component of

NRCs document system (ADAMS). ADAMS is accessible from the NRC Web site at

http://www.nrc.gov/reading-rm/adams.html (the Public Electronic Reading Room).

Sincerely,

/RA/

Michael Hay, Chief

Technical Support Branch

Division of Reactor Safety

Docket No: 50-482

License No: NPF-42

Enclosure:

(1) Inspection Report 05000482/2010008

(2) Charter

cc w/Enclosure:

Site Vice President

Wolf Creek Nuclear Operating Corporation

P.O. Box 411

Burlington, KS 66839

Jay Silberg, Esq.

Pillsbury Winthrop Shaw Pittman LLP

2300 N Street, NW

Washington, DC 20037

Wolf Creek Nuclear Operating Corporation -3-

Supervisor Licensing

Wolf Creek Nuclear Operating Corporation

P.O. Box 411

Burlington, KS 66839

Chief Engineer

Utilities Division

Kansas Corporation Commission

1500 SW Arrowhead Road

Topeka, KS 66604-4027

Office of the Governor

State of Kansas

Topeka, KS 66612-1590

Attorney General

120 S.W. 10th Avenue, 2nd Floor

Topeka, KS 66612-1597

Chairman

Coffey County Courthouse

110 South 6th Street

Burlington, KS 66839

Chief, Radiation and Asbestos

Control Section

Bureau of Air and Radiation

Kansas Department of Health and

Environment

1000 SW Jackson, Suite 310

Topeka, KS 66612-1366

Chief, Technological Hazards

Branch

FEMA, Region VII

9221 Ward Parkway

Suite 300

Kansas City, MO 64114-3372

Wolf Creek Nuclear Operating Corporation -4-

Electronic distribution by RIV:

Regional Administrator (Elmo.Collins@nrc.gov)

Deputy Regional Administrator (Art.Howell@nrc.gov)

DRP Director (Kriss.Kennedy@nrc.gov)

DRP Deputy Director (Troy.Pruett@nrc.gov)

DRS Director (Anton.Vegel@nrc.gov)

DRS Deputy Director (Vacant)

Senior Resident Inspector (Chris.Long@nrc.gov)

Resident Inspector (Charles.Peabody@nrc.gov)

WC Administrative Assistant (Shirley.Allen@nrc.gov)

Acting Branch Chief, DRP/B (Don.Allen@nrc.gov)

Senior Project Engineer, DRP/B (Rick.Deese@nrc.gov)

Project Engineer, DRP/B (Greg.Tutak@nrc.gov)

Project Engineer, DRP/B (Nestor.Makris@nrc.gov)

Public Affairs Officer (Victor.Dricks@nrc.gov)

Public Affairs Officer (Lara.Uselding@nrc.gov)

Project Manager (Balwant.Singal@nrc.gov)

Branch Chief, DRS/TSB (Michael.Hay@nrc.gov)

RITS Coordinator (Marisa.Herrera@nrc.gov)

Regional Counsel (Karla.Fuller@nrc.gov)

Congressional Affairs Officer (Jenny.Weil@nrc.gov)

OEMail Resource

ROPreports

OEDO RIV Coordinator (Geoffrey.Miller@nrc.gov)

DRS/TSB STA (Dale.Powers@nrc.gov)

File located: R:\_REACTORS\_WC\2010\WC2010008-RP-MRB.docx ML 110070347

SUNSI Rev Compl. ;Yes No ADAMS ;Yes No Reviewer Initials MCH

Publicly Avail ;Yes No Sensitive Yes ;No Sens. Type Initials

RE:DRS/TSB RI:DRS/EB1 SRI:DRP/B C:DRP/B

MBloodgood MYoung DDumbacher DAllen

/RA/ /RA/ per telecon /RA/ per telecon /RA/ RWD for DBA

01/04/11 01/04/11 01/04/11 01/5/11

C:DRS/TSB

MCHay

/RA/

01/07/11

OFFICIAL RECORD COPY T= Telephone E= E-mail F = Fax

U.S. NUCLEAR REGULATORY COMMISSION

REGION IV

Docket: 50-482

License: NPF-42

Report: 05000482/2010008

Licensee: Wolf Creek Operating Corporation

Facility: Wolf Creek Generating Station

Location: 1550 Oxen Lane SE

Burlington, Kansas

Dates: June 21 through November 24, 2010

Inspectors: M. Bloodgood, Reactor Engineer

M. Young, Reactor Inspector

D. Dumbacher, Senior Reactor Inspector

Approved By: M. Hay, Chief, Technical Support Branch, Division of Reactor Safety

-1- Enclosure 1

SUMMARY OF FINDINGS

IR 05000482/2010008; 06/21/10 - 11/24/2010; Wolf Creek Generating Station; Special

Inspection in Response to Component Cooling Water System Gas Accumulation.

This report covers a ten day period of onsite inspection, with in office review through a

November 24, 2010. The special inspection team consisted of a reactor engineer, a reactor

inspector and a senior resident inspector. The inspection identified four findings; all of the

findings were NCVs. The significance of most findings is indicated by their color (Green, White,

Yellow, or Red) using Inspection Manual Chapter 0609, Significance Determination Process.

The crosscutting aspect is determined using Inspection Manual Chapter 0310, Components

Within the Cross Cutting Areas. Findings for which the significance determination process

does not apply may be Green or be assigned a severity level after NRC management review.

The NRCs program for overseeing the safe operation of commercial nuclear power reactors is

described in NUREG-1649, Reactor Oversight Process, Revision 4, dated December 2006.

Evaluations and Operability Assessments

The inspectors reviewed the licensee evaluations associated with the component cooling water

and residual heat removal systems following the identification of the voiding condition. During

the review of the licensee evaluations, the inspectors identified inadequate assumptions within

the calculations and operability determinations. The assumptions included; the failure to include

the effects of the voided condition in the residual heat removal system on the high head safety

pumps; the use of nonconservative assumptions during the determination of the size of the

initial void contained in the residual heat removal heat exchanger; and the initial troubleshooting

following the start of the standby component cooling water pump during a low discharge

pressure condition focused on the potential failure of the pressure switch, when the licensee

had sufficient information that the pressure switch operated as expected.

In addition, during the inspection the inspectors observed challenges in the licensees ability to

understand abnormal operating conditions, in that, the licensee had multiple opportunities to

identify the presence of voids in the residual heat removal and component cooling water

systems prior to the actual discovery of the adverse conditions. These included missed

opportunities during review of licensee and industry operating experience, indications of flow

oscillations during start of system components, and abnormal cycling of flow control valves.

A. NRC-identified and Self-Revealing Findings

Cornerstone: Mitigating Systems

Appendix B, Criterion XVI, Corrective Action, for the failure to promptly identify

voiding conditions in the component cooling water and residual heat removal

system piping. The licensee failed to promptly identify the presence of voids in

both the component cooling water and residual heat removal systems despite

unexpected component cooling water pump auto starts and unexpected audible

water hammer and minimum flow valve (EJ-FCV-610) cycling during component

cooling water and residual heat removal pump surveillances.

This finding was more than minor because the failure to promptly identify

conditions adverse to quality associated with the component cooling water and

-2- Enclosure 1

residual heat removal systems is associated with the equipment performance

attribute of the Mitigating Systems Cornerstone and affects the associated

cornerstone objective to ensure the availability, reliability, and capability of

systems that respond to initiating events to prevent undesirable consequences.

Using Manual Chapter 0609.04, Phase 1 - Initial Screening and

Characterization of Findings, the issue screened as having very low safety

significance because it was a qualification deficiency confirmed not to result in a

loss of operability. The finding had a crosscutting aspect in the human

performance, decision making component, because the licensee failed to use

conservative assumptions during the evaluation of the pressure oscillations

exhibited during the component cooling water pump starts [H.1.(b)](Section 2.1).

  • Green. The inspectors identified a self-revealing noncited violation of Technical

Specification 5.4.1, Procedures, for failure to maintain procedures required for

filling and venting of the component cooling water system. The licensee failed to

ensure that the procedures for filling and venting the component cooling water

system were adequately written to prevent gas accumulation and voids to form in

the system.

This finding was more than minor because the failure to maintain an adequate

procedure for filling and venting the component cooling water system is

associated with the equipment performance attribute of the Mitigating Systems

Cornerstone and affects the associated cornerstone objective to ensure the

availability, reliability, and capability of systems that respond to initiating events

to prevent undesirable consequences. Using Manual Chapter 0609.04,

Phase 1 - Initial Screening and Characterization of Findings, the issue

screened as having very low safety significance because it was a qualification

deficiency confirmed not to result in a loss of operability. No crosscutting aspect

was assigned, as this condition was not reflective of current licensee

performance (Section 2.2).

Appendix B, Criterion V, Instructions, Procedures, and Drawings, regarding the

failure to follow the requirements of Procedures AP 28-001, Operability

Evaluations, and AP 26C-004, Technical Specification Operability, associated

with deficiencies resulting from the presence of voiding in the train A residual

heat removal heat exchanger. This condition resulted in the failure to adequately

address the impact of the voided condition for the high head pumps and the heat

removal capacity of the heat exchanger.

This finding is more than minor because it is associated with the Mitigating

Systems Cornerstone attribute of equipment performance and adversely affects

the objective to ensure equipment availability and reliability. Using Manual

Chapter 0609.04, Phase 1 - Initial Screening and Characterization of Findings,

the issue screened as very low risk significant since the finding did not represent

a loss of system safety function. The inspectors determined that this finding had

a crosscutting aspect in the area of problem identification and resolution

associated with the corrective action program component because the licensee

failed to thoroughly evaluate a similar problem such that extent of condition of the

voiding was considered and the cause was resolved P.1(c)(Section 2.3).

-3- Enclosure 1

Green. The inspectors identified a noncited violation of 10 CFR Part 50,

Appendix B, Criterion XVI, "Corrective Action," for the failure to promptly identify

and take corrective actions to address inadequacies in the residual heat removal

system fill and vent procedure. The licensee failed to perform corrective actions

to incorporate minimum flow rates required to sweep air out of the residual heat

removal heat exchangers into the system fill and vent procedure during

performance of revisions incorporating previous operating experience and

corrective actions associated with NRC inspections.

This finding is more than minor because it affected the Mitigating Systems

Cornerstone attribute of design control for ensuring the availability, reliability, and

capability of safety systems. Using Manual Chapter 0609.04, Phase 1 - Initial

Screening and Characterization of Findings, this finding was determined to be of

very low safety significance because the voided heat exchanger was a design or

qualification deficiency confirmed not to result in loss of operability. The

inspectors determined that the finding has a crosscutting aspect in the area of

problem identification and resolution associated with the corrective action

component because the licensee staff evaluation of previous Performance

Improvement Request 2002 2765 was not thorough enough to result in inclusion

of minimum flows necessary to sweep voids out of the residual heat removal heat

exchanger P.1(c)(Section 2.4).

B. Licensee-Identified Violations

None.

-4- Enclosure 1

Report Details

1.0 Special Inspection Scope

The NRC conducted a special inspection at the Wolf Creek Generating Station to better

understand the identification of a potential safety issue involving gas voiding in the

component cooling water (CCW) and residual heat removal (RHR) systems.

On June 1, 2010, the licensee identified voids in train A of the CCW system following an

automatic start of CCW pump D during the performance of an inservice test of CCW

pump A on May 24, 2010, due to low discharge pressure. On June 2, 2010, the licensee

identified a 22.5 cubic foot void in train B on the CCW system side of the RHR heat

exchanger.

On July 1, 2010, the licensee identified a 9.8 cubic foot void in Train A of the RHR

system located in the RHR heat exchanger u-tubes following the erratic operation of the

mini flow valve EJ-FCV-610 and indications of water hammer.

The NRCs initial evaluation satisfied the criteria in the NRC Management Directive 8.3,

NRC Incident Investigation Program, for conducting a special inspection. The NRCs

initial evaluation of this issue using the criteria in NRC Management Directive 8.3, NRC

Incident Investigation Program, determined that the estimated Incremental Conditional

Core Damage Probability was in the overlap region between a special and an

augmented inspection. However, it was determined that the model utilized likely

overestimated the risk due to the failure assumptions. Therefore, based on

management discretion, a decision was made that, although the risk for this event was in

the overlap region, a special inspection would be performed since the risk for the issue

was likely over estimated. The basis for initiating this inspection is further discussed in

the inspection charter, which is Enclosure 2 to the report.

Background

Gas accumulation or voiding of safety related fluid systems can cause air binding in

pumps or water hammer events in piping systems. Instances of gas accumulation or

voiding in safety related fluid systems have occurred on several instances in the nuclear

industry, and as a result, the NRC published information notices, generic letters, and a

NUREG related to this issue.

It is important that systems relied upon to mitigate accidents and events are able to

perform their designed safety function. Specifically, a fluid system whose successful

operation is dependent upon the proper operation of a pump to be able to supply water

should be sufficiently filled to ensure that it can reliably perform its intended function

under all accident and non-accident conditions as required.

Inadequate control of gas introduction or void formation in a fluid system can have the

following safety implications:

  • The introduction of gases into a pump can cause the pump to become air bound

that results in little to no flow being generated by the pump, rendering the pump

inoperable. An air bound pump can become damaged quickly, thereby

-5- Enclosure 1

eliminating the possibility of recovering the pump during an event by venting the

pump casing and suction piping.

  • Gas introduction into a pump can render a pump inoperable, even if the gas does

not air bind the pump. This occurs when there is gas accumulation in the pump

casing, which reduces the pump's discharge pressure and flow capacity to the

point that the pump can no longer perform its design safety function.

  • Void formation in heat exchangers can result in decreased heat transfer

capability resulting in the inability to remove heat during operation of the system.

This occurs when insufficient flow is present in the system to remove air voids in

the heat exchangers.

  • Void formation and gas accumulation can also result in a system pressure

transient event known as water hammer. This is most commonly seen in the

discharge piping, but can also occur in the suction piping. This phenomenon

occurs when a pressure surge or wave is generated when a fluid in motion is

forced to suddenly stop or change direction. Specifically, when there is a rapid

venting or void collapse in a system, followed by a rapid refill of the piping with

water, there is the potential to have water hammer due to the system

configuration.

1.1 Event Summary

On May 24, 2010, during a planned start of CCW pump A for inservice testing,

operators at Wolf Creek observed a pressure drop and a CCW surge tank level

drop of 68 gallons. During this system transient, standby pump C started as

designed to address the low discharge pressure condition and maintain the

system pressurized. Initially, the licensee attributed the starting of CCW pump C

to a faulty pressure relay. On June 1, 2010, CCW system train A experienced an

additional 65-gallon surge tank level drop following the start of pump C. The

licensee subsequently determined gas pockets caused the level changes in the

CCW system. Follow-up venting on June 1, 2010, uncovered the presence of an

additional 0.4 cubic feet of gas. An extent of condition check of train B on June 2

uncovered the presence of a 22.4 cubic feet void in that piping. On June 2, 2010,

ultrasonic testing of standby CCW train A identified several additional voids in

unvented horizontal piping runs. The licensee declared the train inoperable and

commenced dynamic venting operations to sweep the voids from the piping.

On June 28, 2010, during an inservice RHR system pump test, a licensee

operator observed the cycling of minimum flow valve EJ-FCV-610 concurrent

with indications of water hammer. During troubleshooting conducted on July 1,

2010, the licensee concluded that a 9.8 cubic foot void existed in the RHR heat

exchanger u-tubes.

Sequence of Events

Date Discovery / Action

October 10, 2002 Operating experience from Callaway noted that nitrogen gas

from safety injection accumulators had migrated past leaking

-6- Enclosure 1

check valves and had come out of solution in the lower pressure

RHR cold leg injection lines. This same phenomenon was

documented in NRC Special Inspection

Report 05000482/2008007 and in Wolf Creek Root Cause

Report Incident Investigation Team 08-001 as occurring in the

safety injection system.

November 2002 Performance Improvement Request (PIR) 2002-2765 suggested

an enhancement to the dynamic RHR fill and vent procedure. It

resulted in changing the discharge path for the system fill and

vent to the reactor vessel versus the refueling water storage tank

suction header. The PIR also noted minimum flow rates to

sweep air out of the RHR heat exchanger. Specifically,

3268 gpm of flow was listed as required for an effective heat

exchanger fill and vent evolution. Although extensive procedure

changes were made, the minimum flow requirement was not

added to the procedure.

March 13, 2008 NRC completed the special inspection associated with discovery

of voids in the safety injection system on January 2, 2008.

April 9, 2008 Wolf Creek Condition Report 00008212-03-31, recommended

reviewing/revising the emergency core cooling system fill and

vent procedures against isometric drawings. Despite the vertical

RHR heat exchanger design requiring 3268 gpm of dynamic flow

to sweep the RHR tubes, no minimum flow guidance was added

to the new fill and vent procedures.

November 5, 2009 Plant in Refueling Outage 17

November 2009 As part of fill and venting of the RHR system, air (0.001 cubic

feet) was found and vented off at valve EJ-V-221 in RHR

pump A common suction line. Following maintenance on the

component cooling water system, both trains were filled and

vented in accordance with Procedure SYS EG-400, Revision 17,

Component Cooling Water Fill and Vent.

December 2009 Operators performed RHR train A pump quarterly inservice

testing surveillance. During surveillance, the mini flow Valve

EJ-FCV-610 cycled closed and then open due to system flow

collapsing a void in the heat exchanger. The system engineer

noted cycling of the valve but did not address the condition to

operations. In addition, the operators missed the 16 second

valve stroke and loud noise due to water hammer during the

pump start.

March 2010 Performed RHR train A pump quarterly surveillance. During

surveillance, the mini flow valve EJ-FCV-610 cycled closed and

then open due to system flow collapsing a void in the heat

exchanger. The system engineer noted cycling of the valve.

The operators missed the 16 second valve stroke and loud noise

due to water hammer.

May 24, 2010 During surveillance test using Procedure STS-EG-100A,

-7- Enclosure 1

Component Cooling Water Pumps A/C Inservice Pump Test,

the CCW pump C unexpectedly auto started. After the pump

started, the pump vibration technician was leaning against the

CCW discharge line and felt the line vibrate and then stop and

then start vibrating again, indicative of a system flow anomaly.

The operator expressed concern to control room about the piping

vibration. The control room observed that the system was

operating appropriately and continued with the test. Following

the test the licensee declared the system operable.

May 25, 2010 Operations personnel requested maintenance to troubleshoot

the low-pressure switch on CCW train A due to a belief that the

pump auto started because of a faulty switch. Operator

reviewed past pump starts, identifying previous starts with low

amps, discharge pressure, and discharge flow similar to

indications to the pump start on May 24, 2010. The licensee

started troubleshooting plans for the CCW pump discharge

pressure switch even though the pump curves indicated that an

actual low-pressure condition did exist during the pump start.

May 26, 2010 Wolf Creek entered Technical Specification Extended Outage

for maintenance of emergency diesel generator train A. The

licensee performed a risk assessment of having the emergency

diesel generator out of service and a failure of the CCW pump A.

May 28, 2010 The troubleshooting plan for the CCW voiding issue was moved

to June 1.

June 1, 2010 The troubleshooting plan for CCW train A commenced.

Licensee discovered void in EJ-V-0163, RHR HX A, CCW

Outlet Line Vent, and EJ-V-0205, RHR HX A, Vent Outer

Isolation Valve, located on the CCW side of the RHR heat

exchanger. The licensee sampled the gas and determined that it

was 97-99 percent nitrogen. Operators started the CCW train A

pumps in reverse order to identify if the CCW pump A would

exhibit the same low amperage, discharge pressure and flowrate

as previously noted. The pump did in fact exhibit the same

condition identified during the pump start on May 24, 2010.

Operators considered CCW train A operable because the pump

operated normally during steady state condition, however, the

control room requested engineering support for a prompt

operability determination.

June 2, 2010 Operators vented the CCW side of both RHR heat exchangers

and identified 0.45 cubic foot void in train A and 22.4 cubic foot

void in train B. The 22.4 cubic foot void was quantified while

venting the system using a rotometer. Engineering performed

ultrasonic testing on both trains A and B and found both piping

systems water solid.

June 3, 2010 Engineering examined CCW system trains A and B suction

points and the CCW side of the RHR heat exchangers and found

the system water solid. However, ultrasonic testing performed

-8- Enclosure 1

on the train A discharge points identified a total void volume of

2.275 cubic feet. Operators declared CCW train A inoperable

due to voids discovered and initiated Action Requests 25947

and 25948. As a corrective action the licensee wrote temporary

procedures TMP 10-007, "Component Cooling Water Train A

Dynamic Vent," and TMP 10-008, "Component Cooling Water

Train B Dynamic Vent," to vent trains A and B to ensure that all

voids in locations which could not be vented would be swept to

locations which voids could be vented.

June 4, 2010 Operators performed dynamic venting of CCW train A in

accordance with TMP 10-007 three times. Following the venting

engineering performed ultrasonic testing of CCW pump D

discharge piping and discovered a void of 0.0007 cubic feet.

Operators performed an Immediate Operability Determination

and requested engineering to perform a Prompt Operability

Determination in Action Request 25952. Engineering continued

to monitor gas accumulation through periodic ultrasonic testing

and venting of high point locations.

June 5, 2010 Operators performed STS EG-100A, Component Cooling Water

Pumps A/C Inservice Pump Test, satisfactorily. Engineering

completed operability evaluations EG-10-006, train A CCW

system, and EG-10-007, train B CCW system.

June 6, 2010 CCW train A was declared operable. Ultrasonic testing of CCW

Train B found one void on the CCW Pump D discharge piping

and at the RHR heat exchanger A discharge high point vent.

The licensee declared train A CCW inoperable due to discovered

voids.

June 8, 2010 The licensee returned CCW train A to service with compensatory

actions that consisted of periodic ultrasonic testing, monitoring,

and venting.

June 21-25, 2010 NRC special inspection team conducted onsite review of the

CCW system voiding event.

June 28, 2010 During RHR train A pump quarterly surveillance the minimum

flow Valve EJ-FCV-610 unexpectedly cycled closed and then

open due to pump flow collapsing a void in the heat exchanger.

pump ran for 34 minutes. The licensee identified both the water

hammer event and Valve EJ-FCV-610 closing.

July 1, 2010 Troubleshooting Valve EJ-FCV-610 unexpected closure the

licensee checked the calibration of the valve logic. Residual

heat removal train A was declared inoperable and the system

was vented at Valve EJ-FCV-610.

July 2, 2010 Licensee identified voids were present in RHR train A. Found

void at the containment recirculation sump isolation vent

valve EJ-V-0059.

July 4, 2010 Void at valve EJ-V-0059 identified as 133 inches long and

-9- Enclosure 1

0.643 cubic feet. Determined that heat exchanger voids

transporting to high point at valve EJ-V-0059. Ran pump four

times for about 18 hours2.083333e-4 days <br />0.005 hours <br />2.97619e-5 weeks <br />6.849e-6 months <br />. During the pump runs, there was

insufficient flow to sweep void out of heat exchanger.

July 5, 2010 Licensee RHR pump A five times for about eight hours. Based

on strip chart recorder and pump flow measurements

engineering determined the RHR heat exchanger void to be

7.9 cubic. feet and declared the train operable per operating

evaluation EJ-10-009.

July 6, 2010 Voids discovered in the containment spray system during

quarterly containment spray testing at high points. Suction void

was enough to initially declare the train inoperable (0.9 cubic

feet). The voids were vented off and the system was declared

operable.

July 12, 2010 Wolf Creek root cause team for CCW system voiding re-formed

for the emergency core cooling system voiding issue. Root

cause report for the CCW voiding delayed to allow inclusion of

emergency core cooling system voiding causal analysis.

July 19-22, 2010 NRC special inspection performed to follow up on RHR and

containment spray voids.

August 23, 2010 Licensee performed a vacuum fill of RHR train A system. Final

void contained in the RHR heat exchanger is 4.1 cubic feet.

September 2, 2010 Root cause report issued.

November 11, 2010 Licensee completed the engineering disposition for the past

operability of the RHR heat exchanger with 9.8 cubic foot void

and performed a dynamic venting of the RHR system to remove

all remaining gas voids during plant shutdown.

1.2 Operating Experience

The inspectors examined the licensee's program for reviewing industry operating

experience, including reviewing the governing procedure and self-assessments.

Specifically, the inspectors reviewed incorporation of past industry operating

experience pertaining to the component cooling water system voiding issue to

assess whether the licensee had appropriately evaluated the notifications for

relevance to the facility. The inspectors then examined the licensees program

and program procedures when screening and determining applicability of

industry operating experience.

The inspectors determined the Industry Operating Experience Program

previously lacked rigor when evaluating industry operating experience and its

applicability to the facility. Specifically, the licensee performed inadequate

evaluations of system piping configurations, piping arrangements designed with

inappropriate or no high-point vents, and procedural guidance which contribute to

gas intrusion in safety related systems. Below are examples of missed

opportunities to adequately review industry operating experience:

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  • The licensee determined that the evaluation of Condition

Report CR-2008-00091 and the response to Generic Letter 2008-01 was

inadequate and initiated Condition Report 14120 dated January 9, 2010.

The licensees actions focused primarily on essential service water supply

to the auxiliary feedwater and essential service water emergency make-

up to the CCW system because vent valves upstream of the auxiliary

feedwater and CCW systems did not exist. Component cooling water

was not formally evaluated for potential voiding locations. An action that

resulted from Condition Report 14120 was enhancement of training to

engineering, operations, and maintenance for safety systems susceptible

to gas intrusion, but this was implemented differently for each

organization.

  • Self-Assessment SEL 2009-139 did not identify a weakness in the

evaluation of the industry operating experience related to gas voiding.

The assessment provided seven recommendations, but no

recommendations were applied to the CCW system.

  • Incident Investigation Team 08-001 focused primarily on emergency core

cooling system and containment spray systems. The licensee stated in

the root cause that the extent of condition for the Incident Investigation

Team 08-001 was limited due to the initial problems being associated with

the emergency core cooling system and there being no indication of

problems in other systems. This was another missed opportunity for the

licensee to address inadequacies related to the CCW system.

  • Three industry operating experience events that were related to CCW did

not result in any action being taken by the licensee. The events were

OE30299 (St. Lucie event dated October 16, 2008), OE30659 (St. Lucie

event dated November 6, 2009), and a San Onofre event dated

February 9, 2007. All three events involved the CCW system, but Wolf

Creek determined none of the events to be applicable. Even though the

events were not applicable, there was an opportunity for the licensee to

identify that the CCW system was a safety system susceptible to gas

voiding.

Overall, corrective actions were developed to evaluate other safety and balance

of plant systems to ensure the potential for gas voiding will not adversely affect

the systems. The evaluations will utilize the recommendation of industry

operating experience which includes a review of system isometrics, walkdowns

of piping, and other system characteristics that could lead to gas accumulation.

1.3 Assessment of Licensees Root Cause

The inspectors reviewed and assessed the licensees root cause analysis for

technical accuracy, thoroughness, and corrective actions proposed and

implemented. The inspectors reviewed the scope and process used by the

licensee personnel to identify the root and contributing causes that led to the

voiding conditions identified in the CCW and RHR systems. The inspectors

compared information obtained during the conduct of the special inspection and

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review of the root cause analysis. The inspectors interviewed licensee

personnel, reviewed licensee documents, logs and system design information.

The licensee completed on September 2, 2010, a Level 2 root cause analysis as

part of Condition Report 25918 that encompassed three separate conditions

where plant voiding in safety systems was experienced. This evaluation was

conducted to confirm the gas intrusion sources and to determine if there was a

common cause for the three events. The three events included:

  • Component Cooling Water System: On May 24, 2010, during the start of

CCW pump A the CCW pump D unexpectedly started on low discharge

header pressure. Troubleshooting commenced on July 1, 2010, that

identified multiple voids in the suction and discharge piping, and resulted

in the CCW system train A being declared inoperable. On June 2, 2010,

the licensee identified and vented a 22.1 cubic foot void on the CCW side

of the RHR train B heat exchanger.

observed that the minimum flow valve automatically cycled open then

closed upon start of the RHR pump A. On July 7, 2010, the licensee

declared the RHR train A inoperable due to voiding concerns. The

licensee determined that a 9.8 cubic foot void was present in RHR train B

heat exchanger.

during a routine ultrasonic testing surveillance a void in the containment

spray Pump A suction line near the containment sump between the motor

operated Valve ENHV01 and check Valve ENV002. Operators declared

the containment spray system, train A, inoperable.

The root/apparent cause identified that personnel had a lack of knowledge

concerning gas voiding and accumulations within piping systems, specifically

with the CCW, RHR, and containment spray systems. The root cause identified

three examples of lack of understanding: (1) Misconception that the CCW

system was self-venting, (2) Failure to identify that dynamic venting of the RHR

system requires a minimum flow rate to completely sweep air voids out of non-

vented locations, and (3) Lack of knowledge in the methods of gas void

formation.

In addition, the licensee included as a contributing cause the failure of operations

and engineering personnel to use conservative decision making when performing

evaluations of current operating conditions. This was identified by the NRC as a

failure to promptly identify conditions adverse to quality and further discussed in

Section 2.1 of this report.

1.4 Operating Practices and Design that Allowed the Voiding Condition to Exist

Operating Practices: The inspectors found the following performance

deficiencies contributed to the voided conditions in piping systems:

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indications of RHR valve cycling and oscillations in CCW pump

amperage, flow, and discharge pressure during pump starts

  • Failure to identify sections of the CCW and RHR systems that due to

configuration required a dynamic vent

  • Failure to maintain an adequate procedure for filling and venting the CCW

and RHR systems

  • Failure to incorporate changes in the RHR venting procedure to fully

address recommendations in 2002 from the Incident Investigation

Team RC-1 00008218

These performance deficiencies are provided in more detail in Sections 2.1, 2.2,

2.3 and 2.4 of this report.

1.5 Licensees Corrective Action and Extent of Condition

The inspectors evaluated the scope, adequacy, and timeliness of the licensees

corrective measures that were planned and implemented in response to the

CCW and residual heat removal system voiding. The inspectors concluded that

the actions both planned and implemented by the licensee were appropriate to

address the identified issue, to prevent recurrence, and were consistent with the

safety significance of the issue. These corrective actions included:

  • Increased monitoring of the RHR and CCW systems for voids using

ultrasonic testing and venting

  • Revisions of the component cooling water fill and vent procedures to

incorporate the use of dynamic venting in addition to improving the valve

operating sequences

incorporate a minimum flow rate required during the dynamic flush of the

system

  • Modifications to the component cooling water system piping which

includes the redesign of the surge tank connection piping and the addition

of high point vents

  • Perform training to increase operations and engineering personnel

knowledge, awareness, and expectations with regard to voiding in safety

and non-safety related systems

1.6 Operability Determinations and Evaluations

The inspectors reviewed the licensees operability assessments and evaluations

resulting from the voiding identified in the CCW, RHR, and containment spray

systems. During the review, the inspectors determined that the licensee

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exhibited challenges in fully evaluating both normal and abnormal plant

conditions.

During the review of the events on May 24, 2010, the inspectors identified that

operations and engineering personnel, after reviewing CCW pump curves and

operator reports, determined that the low-pressure limit switch was the potential

cause of the standby CCW pump automatic start. Review of the pump startup

curves indicated a reduction in motor amperage, discharge pressure and flow,

which are indicative of system voiding. In addition, the reduced discharge

pressure, shown on the curves, revealed that the low-pressure switch acted as

expected and the startup of the standby pump was a result of the voiding not a

failed pressure switch. In addition, it was determined that the personnel at the

pump observed flow oscillations and vibrations during the startup of CCW

pump A. During interviews operations and engineering personnel understood

that gas voids in the system would cause flow oscillations and vibrations, but did

not consider this abnormal due to being a normal occurrence. This was similar to

the failure of the licensee to identify previous cycling of RHR minimum flow

valve EJ-FCV-610, in which, engineering personnel identified the valve cycling

before the June 28, 2010, event without taking any corrective action. This issue

is further discussed in Section 2.1 of this report.

During the review of Operability Evaluation EJ-10-009 for the RHR system

voiding the inspectors identified that the licensee did not consider the possibility

of the void transferring to the high head safety injection pumps (further discussed

in Section 2.4) while evaluating the effects of the 7.9 cubic foot void identified in

the RHR heat exchanger u-tubes. The licensee addressed this concern in

Revision 1 of the operability evaluation. On August 24, 2010, the licensee

performed a vacuum fill of RHR train A and reduced the RHR heat exchanger

void size to 4.1 cubic feet. Revision 2 of the operability evaluation was

completed to account for the smaller void size and a slight calculation error

identified during the revision. The inspectors determined from the review of the

calculations that the RHR system remained functional. This issue is further

discussed in Section 2.3 of this report.

In addition, the inspectors questioned the quantification of the initial void

identified in the RHR heat exchanger. The licensee failed to take into account

the volume of gas vented from the system when calculating the initial volume of

7.9 cubic feet, and determined an actual initial volume of 9.8 cubic feet when

recalculated. The inspectors reviewed the past operability evaluation for the

9.8 cubic foot void size and identified that the licensee did not assess the

reduced heat transfer capability of the heat exchanger due to the larger void size.

On November 11, 2010, the licensee completed an engineering disposition for

the past operability of the RHR heat exchanger. The inspectors determined that

the RHR system maintained functionality during the time that the 9.8 cubic foot

void was present in the RHR heat exchanger.

Overall, the inspectors determined that the licensee failed to thoroughly evaluate

problems when performing operability evaluations.

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1.7 Reportability Review

The inspectors reviewed the licensees evaluation of the voiding conditions

associated with the CCW, RHR, and containment spray systems and determined

that the events were not reportable to the NRC in accordance

with 10 CFR 50.73.

1.8 Generic Issues

The inspectors evaluated the circumstances associated with the potential voiding

issue and assessed the root cause analysis. Along with this, the inspectors

interviewed numerous licensee personnel and reviewed industry operating

experience, evaluations the station had performed to analyze this issue, as well

as NRC generic communications with the goal of identifying any potentially

generic issues that should be addressed because of this event.

The inspectors concluded that, while there is a potential for voiding to occur in

any fluid system at any facility, there are no potentially previously unrecognized

generic concerns associated with the issues reviewed at Wolf Creek.

2.0 NRC Identified and Self Revealing Findings

2.1 Failure to Promptly Identify and Correct a Condition Adverse to Quality

Introduction. The inspectors identified a Green noncited violation of 10 CFR

Part 50, Appendix B, Criterion XVI, Corrective Actions, for the failure to

promptly identify voiding conditions in the CCW and RHR system piping. The

licensee failed to promptly identify the presence of voids in both the CCW and

RHR systems despite unexpected CCW pump auto starts and unexpected

audible water hammer and minimum flow valve EJ-FCV-610 cycling during CCW

and RHR pump surveillances.

Description. The inspectors identified that the licensee failed to promptly identify

and correct voiding condition in the following two examples.

Example 1. On May 24, 2010, during the performance of

Procedure STS EG-100A, Component Cooling Water Pumps A/C Inservice

Pump Test, the licensee observed the automatic start of the CCW pump A pump

due to low discharge pressure. Operations personnel reviewed the pump startup

data and identified that the pumps flow and pressure oscillations had dipped

below the low-pressure setting of 25.5 psig causing the auto start of CCW

pump C. In addition, an operator stated that there were indications of a low flow

condition on the return line of the residual heat removal heat exchanger.

Licensee operation and engineering personnel reviewed data obtained from

previous pump starts. During the review, the licensee identified that there were

previous pump starts that exhibited similar oscillations in the pumps amperage,

flow, and discharge pressure since January 4, 2010. Further inspection identified

that the decreases in amperage, flow, and pressure have occurred since May 9,

2007. The licensee determined that these indications were normal and

consistent with a normal pump start.

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On June 1, 2010, the licensee identified voids in the shell side of the RHR train A

heat exchanger and at vent valve EJ-V-0163 on the CCW return from the RHR

train A heat exchanger to the suction of CCW pumps A and D. On June 2, 2010,

the licensee vented the CCW side of RHR train B heat exchanger and identified

a 22.1 cubic foot void. Subsequent void monitoring identified additional voided

locations resulting in CCW train A being declared inoperable on June 3, 2010, a

week after the initial May 24, 2010, event. The licensee continued periodic

monitoring and venting of the CCW system and restored operability of the system

on June 5, 2010. On June 6, 2010, the licensee identified a larger than the

acceptable void affecting CCW train A and declared the train inoperable. The

licensee restored operability on June 8, 2010, after additional venting.

Example 2. After exiting Refueling Outage 17 in November 2009, at least three

RHR inservice test quarterly pump surveillances and other pump runs were

performed with only a recirculation flowpath. These pump runs exhibited the

abnormal condition of temporary closing and re-opening of the pump minimum

flow motor operated valve EJ-FCV-610. The normal stroke closed time for this

valve was about 8 seconds. Position indication for the valve was provided on the

main control board next to the pump start switch. A system engineer

documented the abnormal valve cycling as part of system monitoring

documentation but did not initiate a condition report as required per Corrective

Action Procedure AP 28 100, Condition Reports. The minimum flow valve is

designed to close on increasing flow above 1700 gpm. Due to an approximately

8 cubic foot void in the heat exchanger, the flow increased to approximately

5000 gpm for about 1 second while collapsing the voided area in the heat

exchanger tubes during a pump start.

During Refueling Outage 17, both trains of the RHR system were drained for

maintenance. Following the maintenance on November 9, 2009, the RHR train A

system was filled and vented per Procedure SYS EJ-110, RHR System Fill and

Vent Including Initial RCS Fill. However, shortly after starting the RHR pump for

the train A fill and vent process, the RHR heat exchanger outlet valve was closed

by the plant operators to allow for heat up of the reactor coolant system. The

impact of closing the heat exchanger outlet valve was that insufficient RHR flow

existed to remove the voided heat exchanger tubing. This condition was not

discovered until seven months after the fill and vent was performed.

On June 28, 2010, during the quarterly inservice pump test, operators at the

pump noted very loud noise and significant shaking of the RHR train A system

suction and discharge piping. This resulted in the troubleshooting efforts that, on

July 1, 2010, concluded that a void existed in the heat exchanger. Due to

potential water hammer concerns, the operators declared the train inoperable

due to water hammer concerns. During the troubleshooting efforts, it was noted

that for each pump start the pump minimum flow valve was closing despite the

expected pump flows being far below the setpoint for the control circuitry to call

for valve closure. Recognition of loud noises and unexpected valve operation on

RHR pump starts was not entered into the corrective action process from

December 2009 until June 28, 2010.

-16- Enclosure 1

Analysis. The licensees failure to promptly identify a condition adverse to quality

was a performance deficiency. Specifically, the licensee failed to promptly

identify voided conditions in the RHR train A heat exchanger and CCW system

piping and CCW side of both RHR heat exchangers. This finding was more than

minor because the failure to correct these conditions adverse to quality affects

the associated cornerstone objective to ensure the availability, reliability, and

capability of systems that respond to initiating events to prevent undesirable

consequences. Using Manual Chapter 0609.04, Phase 1 - Initial Screening and

Characterization of Findings, the issue screened as having very low safety

significance because it was a qualification deficiency confirmed not to result in a

loss of operability. The finding had a crosscutting aspect in the human

performance, decision making component, because the licensee failed to use

conservative assumptions following indications of gas voiding in the RHR and

CCW systems during pump starts [H.1.(b)].

Enforcement. Title 10 of the Code of Federal Regulations, Part 50, Appendix B,

Criterion XVI, Corrective Action, requires, in part, that measures shall be

established to assure that conditions adverse to quality, such as failures,

malfunctions, deficiencies, deviations, defective material and equipment, and

nonconformance are promptly identified and corrected. Contrary to the above,

engineering personnel failed to promptly identify and correct gas accumulation

and voiding conditions in the CCW and RHR systems. Specifically, from May 24

to June 1, 2010, the licensee failed to promptly identify that voids were adversely

affecting the CCW system following an unexpected start of a CCW pump. In

addition, from November 9, 2009 to July 1, 2010, the licensee failed to promptly

identify that voids in the RHR system were causing abnormal conditions.

Because this finding is of very low safety significance and has been entered into

the licensees corrective action program as Condition Report 26417 and 27107,

this violation is being treated as a noncited violation, consistent with

Section 2.3.2 of the NRC Enforcement Policy: NCV 05000482/2010008-01,

Failure to Promptly Identify and Correct a Condition Adverse to Quality.

2.2 Inadequate Procedure for Fill and Vent of the Component Cooling Water System

Introduction. The inspectors identified a self-revealing Green noncited violation

of Technical Specification 5.4.1, Procedures, involving the failure to maintain

adequate procedures required for fill and venting of the component cooling water

system to prevent gas accumulation and voids to form in the system.

Description. During the fall 2009 outage, the licensee filled and vented both

trains A and B CCW systems in accordance with Procedure SYS EG-400,

Component Cooling Water System Fill and Vent, Revision 17.

On May 24, 2010, during the performance of STS EG-100A, Component

Cooling Water Pumps A/C Inservice Pump Test, the licensee observed the

automatic start of CCW pump A due to low discharge pressure. Operations

personnel reviewed the pump startup data and identified that the pumps flow

and pressure oscillations had dipped below the low-pressure setting of 25.5 psig

causing the auto start of CCW pump C. In addition, an operator at the pump

stated that there were indications of a low flow condition on the return of the

residual heat removal heat exchanger. The licensee operations and engineering

-17- Enclosure 1

personnel reviewed past pump start data and determined that the characteristics

identified during the pump start had previously occurred.

On June 1, 2010, the licensee identified voids in the shell side of RHR train A

heat exchanger and vent valve EJ-V-0163 on the CCW return from the heat

exchanger to the suction of CCW pumps A and D. On June 2, 2010, the licensee

vented the CCW side of the RHR train B heat exchanger and identified a

22.1 cubic foot void.

On June 3, 2010, the licensee engineering personnel examined CCW trains A

and B suction points and the CCW side of the RHR heat exchangers and found

the system water solid. However, ultrasonic testing performed on the train A

discharge points identified a total void volume of 2.275 cubic feet. The licensee

conducted ultrasonic testing and identified a total of 33 void locations throughout

the CCW system. In addition, the CCW train A pump discharge piping contained

an inverted U section of piping that could not be statically vented due to the lack

of high point vents. Due to the inability of the system to be statically vented, the

licensee wrote temporary procedures TMP 10-007, "Component Cooling Water

Train A Dynamic Vent," and TMP 10-008, "Component Cooling Water Train B

Dynamic Vent," to dynamically vent the system. These procedures were written

to ensure that all voids in locations that could not be vented are swept to

locations which voids could be vented.

Analysis. The licensees failure to ensure that adequate procedures were

available for the filling and venting of the component cooling water system was a

performance deficiency. This finding is more than minor because the failure to

maintain adequate fill and vent procedures affected the equipment performance

attribute of the Mitigating Systems Cornerstone and affects the associated

cornerstone objective to ensure the availability, reliability, and capability of

systems that respond to initiating events to prevent undesirable consequences.

Using Manual Chapter 0609.04, Phase 1 - Initial Screening and

Characterization of Findings, Phase 1 Screening Worksheet, the issue screened

as having very low safety significance because it was a qualification deficiency

confirmed not to result in a loss of operability. No crosscutting aspect was

assigned, as this condition was not reflective of current licensee performance.

Enforcement. Technical Specification 5.4.1, Procedures, requires, in part, that

written procedures shall be established, implemented, and maintained covering

the applicable procedures recommended in Regulatory Guide 1.33, Revision 2,

Appendix A, dated February 1978. Regulatory Guide 1.33, Appendix A,

Section 3.e, requires, in part, that instructions for filling and venting the

component cooling water system should be covered by written procedures.

Contrary to the above, from October 2009 until June 1, 2010, the licensee failed

to provide adequate instructions for filling and venting the component cooling

water system. Specifically, station procedures allowed for gas accumulations in

the component cooling water system, which affected the proper operation of the

pumps during startup. Because this violation was of very low safety significance

and it was entered into the licensees corrective action program as Condition

Report 26420, this violation is being treated as a noncited violation, consistent

with Section 2.3.2 of the NRC Enforcement Policy: NCV 05000482/2010008-02,

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Inadequate Procedure for the Fill and Vent of the Component Cooling Water

System.

2.3 Failure to Perform an Adequate Operability Evaluation

Introduction. The inspectors identified a Green noncited violation of 10 CFR

Part 50, Appendix B, Criterion V, Instructions, Procedures, and Drawings,

regarding the failure to follow the requirements of Procedures AP 28-001,

Operability Evaluations, and AP 26C-004, Technical Specification Operability,

associated with deficiencies resulting from the presence of voiding in the train A

RHR heat exchanger. This condition resulted in the failure to adequately

address the impact of the voided condition for the high head pumps and the heat

removal capacity of the RHR heat exchanger.

Description. Following the November 2009 Wolf Creek refueling outage three

train A RHR quarterly pump tests exhibited water hammer symptoms related to

heat exchanger voiding. On June 28, 2010, during the quarterly inservice pump

test, operators at the pump noted very loud noise and significant shaking of the

system suction and discharge piping. This resulted in the troubleshooting efforts

that, on July 1, 2010, concluded that a void existed in the RHR heat exchanger.

The void size in the RHR heat exchanger was initially determined to be 7.9 cubic

feet. Wolf Creek engineering staff determined that none of the possible void

effects resulted in a loss of component or system operability. On July 4, 2010,

Wolf Creek operators declared the RHR system degraded but operable with the

still existing void in the RHR heat exchanger because of the relative small void

size and insufficient flows needed for transport out of the heat exchanger.

An NRC special inspection team reviewed the licensee Operability

Evaluation OE EJ-10-009, Revision 0, associated with Condition Report 26463

description of the heat exchanger void. The operability evaluation considered

many possible effects of the void including: (1) pump operation, (2) water

hammer affecting the RHR piping, valves, nozzles, and pipe supports, (3) the

reactor coolant system, (4) heat transfer through the heat exchanger, (5) the

combined effects of voiding on both sides of the RHR heat exchanger tubing, and

(6) the effects of this gas being injected into the safety injection and charging

system pump suctions. The licensee concluded that the RHR system was

degraded but operable and the void could remain in the RHR heat exchanger.

The NRC inspectors noted that the operability evaluation assumed that

insufficient design basis accident flows existed to allow the void to travel to the

suction of the safety injection and charging system pumps. The inspectors

challenged this assumption. With an unavailable RHR train B pump, cold leg

recirculation would require the RHR train A pump to provide flow to both charging

pumps and both safety injection pumps. The licensee re-reviewed this aspect of

the design basis loss of coolant accidents and determined that the gas in the

heat exchanger would transport to the cold leg recirculation path to the suction of

the high-pressure pumps. An analyses was performed to determine the

distribution of the gas to the various flow paths and the resulting void fractions at

the pump inlets. This analysis input assumed a 7.9 cubic foot void and the Wolf

Creek emergency core cooling system to the GOTHIC 2-phase flow model. The

GOTHIC model determined that the 7.9 cubic foot void size would never result in

-19- Enclosure 1

greater than the operability limit for void fraction at any of the high-pressure

pumps. The void was only able to transport out of the RHR heat exchanger at

RCS pressures less than 160 psig. At this pressure, the RHR pump itself was

able to deliver about 1000 gpm and provide the necessary cooling in this cold leg

recirculation mode. At lower reactor coolant system pressures, most of the void

bubble would go directly to the reactor coolant system and not affect the suction

of the high-pressure pumps.

Revision 1 of Operability Evaluation OE EJ-10-009 addressed the inspectors

concerns and determined all void fractions were below the operability limit.

Revision 2 of the operability evaluation addressed a slight calculation error and

justified the void condition after the vacuum fill and vent reduced the void to

4.1 cubic feet. Another assumption error noted by the inspectors was that the

original measurement of the RHR heat exchanger void size should have been

9.8 cubic feet. This also resulted in acceptable void fractions at the high-

pressure pumps.

After the NRC inspection, short-term corrective actions were implemented to

perform a vacuum fill and vent of the heat exchanger on August 23, 2010. Long-

term corrective actions were addressed by the actions associated with the root

cause evaluation performed by Wolf Creek.

Analysis. The licensees failure to perform an adequate operability evaluation for

the train A emergency core cooling system voiding discovered on June 28, 2010,

was a performance deficiency. This finding is more than minor because it is

associated with the Mitigating Systems Cornerstone attribute of equipment

performance and adversely affects the objective to ensure equipment availability

and reliability. Using Manual Chapter 0609.04, Phase 1 - Initial Screening and

Characterization of Findings, the issue screened as having very low risk

significance since the finding did not represent a loss of system safety function.

The inspectors determined that this finding had a crosscutting aspect in the area

of problem identification and resolution associated with the corrective action

program component because the licensee failed to thoroughly evaluate a similar

problem such that extent of condition of the voiding was considered and the

cause was resolved P.1(c).

Enforcement. Title 10 of the Code of Federal Regulations, Part 50, Appendix B,

Criterion V, Instructions, Procedures, and Drawings, requires, in part, that

activities affecting quality shall be prescribed by documented instructions or

drawings of a type appropriate to the circumstances and shall be accomplished

in accordance with these instructions or drawings. Contrary to the above,

following discovery of voiding in RHR train A heat exchanger on June 28, 2010,

the licensee failed to provide a reasonable basis for operability as required by

Step 6.1.4 of Procedure AP 26C-004, Technical Specification Operability.

Because of the very low safety significance and Wolf Creeks action to place this

issue in their corrective action program as Condition Report 27109, this violation

is being treated as a noncited violation in accordance with Section 2.3.2 of the

Enforcement Policy: NCV 05000482/2010008-03, Failure to Perform an

Adequate Operability Evaluation.

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2.4 Failure to Identify and Correct Inadequate RHR Fill and Vent Procedures

Introduction. The inspectors identified a Green noncited violation of 10 CFR

Part 50, Appendix B, Criterion XVI, "Corrective Action," for the failure to identify

and take prompt corrective actions to address inadequacies in the RHR fill and

vent procedure. The licensee failed to perform corrective actions to incorporate

minimum flow rates required to sweep air out of the RHR heat exchangers into

the system fill and vent procedure during performance of revisions incorporating

previous operating experience and corrective actions associated with NRC

inspections.

Description. Performance Improvement Report 2002-2765, a Wolf Creek 2002

corrective action document, noted after reviewing industry Callaway Plant

operating experience that the Wolf Creek dynamic RHR fill and vent procedure

needed improvements. Changes were made to reroute the discharge path for

the system fill and vent to the reactor vessel versus the refueling water storage

tank suction header. The performance improvement report also noted minimum

flow rates to sweep air out of the RHR heat exchanger. Specifically 3268 gpm of

flow was listed as required for a heat exchanger fill and vent to achieve a Froude

number > 1. Although extensive procedure changes were made, the minimum

flow requirement was not added to the procedure.

On January 2, 2008, the NRC Special Inspection Report 05000482/2008007

discussed discovery of voids in the Wolf Creek emergency core cooling systems.

Wolf Creek Condition Report 8212-03-31, Action 3694 recommended

reviewing/revising emergency core cooling system fill and vent procedures

against isometric drawings. Despite the vertical RHR heat exchanger design

requiring 3268 gpm of dynamic flow to sweep the RHR tubes, no minimum flow

guidance was added to the new fill and vent procedures. Condition Report 8212

was generated as a result of the 2008 voiding in the safety injection system and

the NRC follow-up special inspection.

During the 2009 refueling outage, both trains of the RHR system were drained for

maintenance. Following the maintenance, the trains were to be filled and vented

per Procedure SYS EJ-110, RHR System Fill and Vent Including Initial RCS

Fill. However, shortly after starting the RHR pump for the train A fill and vent,

the RHR heat exchanger outlet valve was closed by the plant operators to allow

heat up of the reactor coolant system. The impact of closing the heat exchanger

outlet valve was that insufficient RHR flow existed to remove the void in the heat

exchanger tubing. This voided condition was not discovered until seven months

after the fill and vent was performed.

After exiting the refueling outage in November 2009, at least three RHR quarterly

pump surveillances and other pump runs were performed with only a

recirculation flow path. These pump runs exhibited the abnormal condition of

temporary closing and re-opening of the pump minimum flow motor operated

Valve EJ-FCV-610. Due to an approximately 8 cubic foot void in the heat

exchanger the RHR pump flow increased to approximately 5000 gpm for about

1 second while collapsing the voided area in the heat exchanger tubes. On

June 28, 2010, during the quarterly pump test, operators at the pump noted very

loud noise and significant shaking of the RHR train A system suction and

-21- Enclosure 1

discharge piping. This resulted in the troubleshooting efforts that, on July 1,

2010, concluded that a void existed in the heat exchanger. This led to the

operators declaring the RHR train A system inoperable due to water hammer

concerns.

The licensee determined on July 4, 2010, that the RHR system was degraded

but operable with the still existing void in the RHR heat exchanger because of the

relative small void size and insufficient flows needed for transport out of the heat

exchanger.

Analysis. The licensees failure to promptly identify and correct a condition

adverse to quality was a performance deficiency. Specifically, the licensee failed

to identify and correct the RHR system fill and vent procedures. This finding is

more than minor because it affected the Mitigating Systems Cornerstone attribute

of design control for ensuring the availability, reliability, and capability of safety

systems. Using Manual Chapter 0609.04, Phase 1 - Initial Screening and

Characterization of Findings, this finding was determined to be of very low safety

significance because the voided heat exchanger was a design or qualification

deficiency confirmed not to result in loss of operability. The inspectors

determined that the finding has a crosscutting aspect in the area of problem

identification and resolution associated with the corrective action component

because the licensee staff evaluation of previous Performance Improvement

Report 2002-2765 was not thorough enough to result in inclusion of minimum

flows necessary to sweep voids out of the RHR heat exchanger P.1(c).

Enforcement. Title 10 of the Code of Federal Regulations, Part 50, Appendix B,

Criterion XVI, Corrective Action, requires, in part, that measures be established

to assure conditions adverse to quality are promptly identified and corrected.

Contrary to the above, the licensee failed to correct the adverse condition of

inadequate fill and vent procedures related to removing voiding in the RHR heat

exchangers. Specifically, following draining of the RHR trains in November 2009,

Procedure SYS EJ-110, RHR System Fill and Vent Including Initial RCS Fill,

was inadequate in that it did not specify the minimum flows necessary to remove

the void existing in the heat exchangers. Because this violation is of very low

safety significance and has been entered into the licensee's corrective action

program as Wolf Creek Condition Report 27106, this violation is being treated as

a noncited violation, consistent with Section 2.3.2 of the NRC Enforcement

Policy: NCV 05000482/2010008-04, Failure to Identify and Correct Inadequate

RHR Fill and Vent Procedures.

AOA6 Meetings

Exit Meeting Summary

On June 25, 2010, prior to the teams departure from the facility, an inspection debrief was

conducted with Mr. M. W. Sunseri, President and CEO, and other members of the licensee staff

to apprise them of the teams results to date and to explain that the inspection would continue

with in office review pending resolution of all questions.

On July 23, 2010, prior to the teams departure from the facility, an inspection debrief was

conducted with Mr. M. W. Sunseri, President and CEO, and other members of the licensee staff

-22- Enclosure 1

to apprise them of the teams results to date and to explain that the inspection would continue

with in office review pending resolution of all questions.

On November 24, 2010, the team conducted a telephonic exit meeting to present the inspection

results to Mr. S. Hedges, Site Vice President, and other members of the licensee staff. The

licensee acknowledged the issues presented. The team acknowledged review of proprietary

material, as part of the inspection but no proprietary information was retained or included in the

report.

-23- Enclosure 1

SUPPLEMENTAL INFORMATION

KEY POINTS OF CONTACT

Licensee Personnel

T. Card, Supervisor Engineer

J. Harris, Engineer, Void Management Program

J. Harvey, Manager Engineering NSSS

J. Lowery, Engineer

G. Pendergrass, Manager, Systems Engineering

T. Wilson, Root Cause Evaluator (Lead)

NRC Personnel

C. Long, Senior Resident Inspector

C. Peabody, Resident Inspector

M. Hay, Branch Chief, TSB

D. Loveless, Senior Risk Analyst

ITEMS OPENED, CLOSED AND DISCUSSED

Opened and Closed

05000482/2010008-01 NCV Failure to Promptly Identify and Correct a Condition Adverse to

Quality

05000482/2010008-02 NCV Inadequate Procedure for Fill and Vent of the Component

Cooling Water System

05000482/2010008-03 NCV Failure to Perform an Adequate Operability Evaluation

05000482/2010008-04 NCV Failure to Identify and Correct Inadequate RHR Fill and Vent

Procedures

LIST OF DOCUMENTS REVIEWED

PROCEDURES

NUMBER TITLE REVISION

STS EG-100A Component Cooling Water Pumps A/C Inservice Pump Test 24

STS EG-100B Component Cooling Water Pumps B/D Inservice Pump Test 21

STS EG-201A EG RV-9, CCW Surge Tank A Vent Valve Inservice Valve Test 8

STS EG-201B EG RV-10, CCW Surge Tank B Vent Valve Inservice Valve Test 10

AP 20E-001 Industry Operating Experience Program 14

SYS SJ-002 Void Sampling Using A Sample/Purge Rig 1

A-1 Attachment

ALR 00-052B CCW PMP A/C Press Lo 6

ALR 00-051C CCW PMP A Flow Lo 6A

ALR 00-051D CCW SRG TK A LEV HiLo 6A

ALR 00-067F OSA No. 3 3

OP1610102 SOER 97-1, Gas Intrusion Into Safety Injection Systems 0

(Operations Training)

SY1300600 Emergency Core Cooling System (Training) 19

ES1310101 ESP Continuing Training 09-Q2 30

ES1310101 ESP Continuing Training 08-Q1 27

ES1350400 Gas Intrusion/Voiding Events Wolf Creek 0

TMP 10-007 Component Cooling Water Train A Dynamic Vent 0

TMP 10-008 Component Cooling Water Train B Dynamic Vent 0

TMP 10-009 CCW Train A Supplying Service Loop with CCW to Radwaste 0

Isolated

AP 28-001 Operability Evaluations 17

AP 28-011 Resolving Deficiencies Impacting SSCs 1B

AP 26C-004 Technical Specification Operability 20

AP 28A-100 Condition Reports 12

AI 28A-007 Level 2 CR Evaluation 3

SYS EG-401 Component Cooling Water System Drain Procedure 24

SYS EG-400 Component Cooling Water System Fill and Vent 17

SYS EG-400 Component Cooling Water System Fill and Vent 17A

AI 21-100 Operations Guidance and Expectations 18

AP 26A-003 10 CFR 50.59 Reviews 10A

STN EJ-003A RHR Train A & Common Void Monitoring & Venting 2

STS BG-002 ECCS Valve Check and System Vent 17

STS BG-007A ECCS Valve Check and Train A & Common Void Monitoring and 3

Venting

STS BG-007B ECCS Train B Void Monitoring and Venting 3

SYS EJ-110 RHR System Fill and vent Including Initial RCS Fill 48

SYS EJ-110 RHR System Fill and vent Including Initial RCS Fill 52

SYS EJ-120 Startup of a Residual Heat Removal Train 56

SYS EN-400 Containment Spray System Fill and Vent 5

A-2 Attachment

SYS EN-400 Containment Spray System Fill and Vent 10

SYS EJ-110 RHR System Fill and Vent 10

AI-28A-003 Rapid Response to Events of Significance 6A

AI-28A-004 Incident Investigation Team (IIT) Guidance 3A

AI-28A-010 Screening Condition Reports 5

DRAWINGS

NUMBER TITLE REVISION

M-13EG01 Piping Isometric Component Cooling Water Sys. Aux. Bldg. A 7

Train

M-11EG01 System Flow Diagram Component Cooling Water 2

M-13EG02 Piping Isometric Component Cooling Water Sys. A Train to 1

Fuel Bldg.

M-12EG01 Piping & Instrumentation Diagram Component Cooling Water 16

System

M-12EG02 Piping & Instrumentation Diagram Component Cooling Water 19

System

M-12EG03 Piping & Instrumentation Diagram Component Cooling Water 9

System

M-13EG08(Q) Piping Isometric Component Cooling Water Sys. Surge Tank 0

Area

M-13EG03(Q) Piping Isometric Component Cooling Water Sys. Auxiliary Bldg. 2

B Train

M-13EG04 Piping Isometric Component Cooling Water Sys. Auxiliary Bldg. 6

B Train

M-13EG05 Piping Isometric Component Cooling Water Sys. B Train to 2

Fuel Bldg.

M-13EG06 Piping Isometric Component Cooling Water Sys. Aux. Bldg. 9

Common Header

M-13EG07 Piping Isometric Component Cooling Water Sys. Aux. Bldg. 2

Common Header

M-13EG09 Piping Isometric Component Cooling Water System Reactor 3

Building

M-13EG18 Piping Isometric Component Cooling Water System Fuel 5

Building

M-13EG19 Piping Isometric Component Cooling Water System Radwaste 6

Building

A-3 Attachment

M-13EG20 Piping Isometric Component Cooling Water System Radwaste 0

Building

M-13EG24 Piping Isometric Component Cooling Water Sys. Auxiliary 2

Building

M-13EG26 Piping Isometric Component Cooling Water Sys. Aux. Bldg. A 2

Train

M-12AN01 Piping and Instrumentation Diagram Demineralized Water 27

Storage and Transfer System

M-12EF01 Piping & Instrumentation Diagram Essential Service Water 21

System

M-12EF02 Piping & Instrumentation Diagram Essential Service Water 26

System

E-11005 List of Loads Supplied by Emergency Diesel Generator 33

J-02EG01A(Q) Control Logic Diagram Component Cooling Water System 5

Pumps

5739 Vertical Residual Heat Exchanger Details 3

5736 Vertical Residual H.E. Outline Dwg. 5

5737 Vertical Residual Heat Exchanger Assembly 4

5738 Vertical Residual Heat Exchanger Details 4

5740 Vertical Residual Heat Exchanger Details 4

M-01EJ01 RHR System Flow Diagram in Final Safety Analysis Report Voided

M-12EJ01 Piping and Instrumentation Diagram Residual Heat Removal 43

System

M-12EJ01 Piping and Instrumentation Diagram Containment Spray System 12

M-01EJ01 FSAR System Flow Diagram 6 (Voided)

M-13EJ01 Piping Isometric Residual Heat Removal System, Auxiliary 15

Building A

M-13EJ02 Piping Isometric Residual Heat Removal System, Auxiliary 11

Building B

M-13EJ03 Piping Isometric Residual Heat Removal System, Auxiliary 8

Building A and B

M-13EJ04 Piping Isometric Residual Heat Removal System, Reactor 6

Building

M-13EJ08 Small Piping Isometric Residual Heat Removal System, Auxiliary 0

Building

M-13EJ09 Small Piping Isometric Residual Heat Removal System, Auxiliary 1

Building

A-4 Attachment

M-13 EN01 Piping Isometric Containment Spray System, Auxiliary Building A 7

M-13EN02 Piping Isometric Containment Spray System, Auxiliary Building B 7

CALCULATIONS

NUMBER TITLE REVISION

EG-M-040 Evaluation for the maximum void fraction and transient 0

duration to preclude pump mechanical damage for the

Component Cooling Water (CCW) EG System

EG-M-42 Pump Start up Pressure Surge Due to Gas in CCW RHR 0

Piping

EG-M-43 Transport of Non-Condensable Gas in the Wolf Creek CCW 0

System

EJ-M-049 Calculate Volume of RHR Heat Exchanger (EEJ01A/B) Above 1

the Top of the Inlet Nozzle (Inside the Shell). (Ref.

CR 00025859)

EG-M-041 Water Hammer due to Voids in Component Cooling Water 0

(CCW) EG System Piping

EG-S-019 Pipe Stress and Support Review Due to Water Hammer 0

Loads in CCW System

EJ-M-050 Evaluation of Void at EJ-V-0163 0

M-EG-5 Calculate NPSH Available to the Component Cooling Water 1

Pumps

EJ-M-18 Rate of Heat Up of RHR System in Recirculation Mode due to 2

Pump Heat with no CCW

EJ-M-013 Thrust/Torque Calculation for EJHV8811A and EJHV8811B December 12,

2005

EJ-M-051 External Pressure Capacities, Tube, Channel, and Piping 0

Vacuum for RHR Heat Exchanger

EJ-M-053 Evaluation of Gas Void in Tube Side of RHR Heat Exchanger 0

EJ-M-054 Transport of RHR HX Bubble to the Charging Pumps 0

CONDITION REPORTS (Formerly Performance Improvement Reports)

00011261 00014120 00024847 00025918 00025947

00025948 00025859 00025860 00026210 00026231

00026232 00026240 00026462 00026562 00026565

00011261 00024847 00025918 00026462 00026562

00026774 00026822 00008212 00026565 00028301

A-5 Attachment

00027543 00027575 00026417 00026420 00026492

00027110 00027108 00027109 00027107 00027112

00027106

PERFORMANCE IMPROVEMENT REPORTS

2002-2765 2008-000861

WORK ORDER

10-329334-000 10-329334-044 10-329565-012 06-290742-000 10-329308-000

10-329565-014 10-329334-001 10-329565-003 10-329334-010 10-329334-011

10-329334-012 10-329334-013 10-329334-014 10-329334-016 10-329334-018

10-329334-049 10-329565-013 10-329334-002 10-329334-003 10-329334-004

10-329334-006 10-329334-007 10-329334-008 10-329334-009 10-329334-020

10-329334-047 10-329334-048 10-329334-055 10-329334-056 10-329334-059

10-329565-001 10-329565-004 10-329565-005 10-329565-011

SURVEILLANCE TEST

NUMBER TITLE DATE

STS EG-100A Component Cooling Water Pumps A/C Inservice Pump Test May 28, 2009

STS EG-100A Component Cooling Water Pumps A/C Inservice Pump Test August 26,

2009

STS EG-100A Component Cooling Water Pumps A/C Inservice Pump Test August 27,

2009

STS EG-100A Component Cooling Water Pumps A/C Inservice Pump Test November 25,

2009

STS EG-100A Component Cooling Water Pumps A/C Inservice Pump Test February 23,

2010

STS EG-100A Component Cooling Water Pumps A/C Inservice Pump Test February 24,

2010

STS EG-100A Component Cooling Water Pumps A/C Inservice Pump Test May 24, 2010

STS EG-100A Component Cooling Water Pumps A/C Inservice Pump Test June 5, 2010

STS EG-100A Component Cooling Water Pumps A/C Inservice Pump Test June 7, 2010

STS EG-100A Component Cooling Water Pumps A/C Inservice Pump Test June 8, 2010

STS EG-100B Component Cooling Water Pumps B/D Inservice Pump Test November 15,

2009

A-6 Attachment

STS EG-100B Component Cooling Water Pumps B/D Inservice Pump Test November 16,

2009

STS EG-100B Component Cooling Water Pumps B/D Inservice Pump Test December 17,

2009

STS EG-100B Component Cooling Water Pumps B/D Inservice Pump Test March 16,

2010

STS EG-100B Component Cooling Water Pumps B/D Inservice Pump Test March 17,

2010

STS EG-100B Component Cooling Water Pumps B/D Inservice Pump Test June 17,

2010

STS EG-100B Component Cooling Water Pumps B/D Inservice Pump Test June 18,

2010

TMP 10-007 Dynamic Vent of Train A CCW June 5, 2010

TMP 10-007 Dynamic Vent of Train A CCW June 6, 2010

TMP 10-009 CCW Train A Supplying Service Loop with CCW to Radwaste June 17,

Isolated 2010

STS EG-201A EG RV-9, CCW Surge Tank A Vent Valve Inservice Valve March 8,

Test 2010

STS EG-201A EG RV-9, CCW Surge Tank A Vent Valve Inservice Valve June 8, 2010

Test

STS EG-201B EG RV-10, CCW Surge Tank B Vent Valve Inservice Valve May 23, 2010

Test

MISCELLANEOUS

NUMBER TITLE REVISION /

DATE

OE EG-10- A Component Cooling Water System Voids June 3, 2010

006 Revision 1

OE EG-10- B Component Cooling Water System Voids June 4, 2010

007 Revision 1

OE EJ-10-009 RHR System, Train A 2

OE EJ-10-010 RHR System, Train A July 27, 2010

Revision 1

WCAP 16717- Wolf Creek Generating Station (SAP) MSIV/MFIV February 7,

P Replacement Project Small Break LOCA Analysis 2007

Engineering Report

FAI/09-130 Technical Basis for Gas Transport to the Pump Suction December 2009

M-10EJ Residual Heat Removal 4

A-7 Attachment

M-10EN Containment Spray 4

Cycle 17 ECCS 31 day Surveillance Void Trend

Cycle 18 ECCS 31 day Surveillance Void Trend

Cycle 17 Containment Spray Void Trend

Cycle 18 Containment Spray Void Trend

Strip Chart Recorder data of B RHR pump flow vs. time for

July 2, 2010 troubleshooting

Table of RHR run times since November 2008

RHR pump PEJ01A pump performance (graph) since RF17

Engineering Disposition on Gas Voids in ECCS Piping

On the Spot Change (OTSC) 10-0037, STS EJ-100A, RHR

System Inservice Pump A Test

Applicability Determination for Procedure STS EJ-100A,

RHR System Inservice Pump A Test, OTSC 10-0037

Event and Causal Factors Chart for Condition Report July 19, 2010

00024847, B Train ECCS Voiding

Barrier (HBT) Analysis for Condition Report 00024847, B July 19, 2010

Train ECCS Voiding

Nine Month Response to NRC Generic Letter 2008-001, October 10,

Managing Gas Accumulation in Emergency Core Cooling, 2008

Decay Heat Removal, and Containment Spray Systems

Wolf Creek response to NRC Request for Additional August 17,

Information RE: Response to NRC Generic Letter 2008-001, 2009

Managing Gas Accumulation in Emergency Core Cooling,

Decay Heat Removal, and Containment Spray Systems

Engineering Disposition, Past Operability of RHR Heat November 11,

Exchanger with 9.8 Cubic Foot Void 2010

A-8 Attachment

June 15, 2010

MEMORANDUM TO: Michael Bloodgood, Inspector, Team Leader

Technical Support Branch

Division of Reactor Safety

Matthew Young, Inspector

Engineering Branch 1

Division of Reactor Safety

FROM: Roy Caniano, Director

Division of Reactor Safety

SUBJECT: CHARTER FOR SPECIAL INSPECTION TO EVALUTE GAS

ACCUMULATION IN THE COMPONENT COOLING WATER SYSTEM

AT WOLF CREEK GENERATING STATION

In response to the discovery of voiding in portions of the Component Cooling Water (CCW)

System piping, a Special Inspection will be performed. You are hereby designated as the

Special Inspection Team Leader. Matthew Young, Inspector, is designated as a team member.

The Senior Reactor Analyst assigned to support the team is David Loveless.

A. Basis

Specifically, on May 24, 2010, during a planned start of CCW Pump A for inservice

testing, operators at Wolf Creek observed a pressure drop and a surge tank level drop of

68 gallons. During this system transient, Pump C started unexpectedly on a feature

designed to maintain the system pressurized. At the time, the licensee attributed the

anomalous system response to a potentially faulty pressure relay. On June 1, 2010,

Train A of CCW experienced a 65-gallon surge tank level drop following the start of

Pump C. The licensee subsequently determined the May 24 and June 1 level changes

were caused by gas pockets in the CCW system. Follow-up venting on June 1, 2010,

uncovered the presence of an additional 0.4 cubic feet of gas in the RHR A heat

exchanger shell. Also, an extent of condition check of Train B on June 2 uncovered the

presence of a 22.4 cubic foot void in that piping. On June 3, 2010, ultrasonic testing of

standby CCW Train A identified several additional voids in unvented horizontal piping

runs. The licensee declared the standby train inoperable and commenced dynamic

venting operations to sweep the voids from the piping. The gas voids are believed to

have come from the use of nitrogen saturated fill water after maintenance conducted on

the system during the fall 2009 refueling outage. Between that outage and the time the

nitrogen gas was vented, the CCW system was degraded and may not have been able

to perform its safety functions.

-1- Enclosure 2

A regional Senior Reactor Analyst (SRA) estimated the Maximum Conditional Core

Damage Probability for this issue to be between 1E-5 and 1E-4, which is in the overlap

region between a special inspection and an augmented inspection team. Based on

current available information, the NRC staff recommends that the appropriate level of

NRC response is the performance of a special inspection. The special inspection

activities will include information gathering to determine whether an augmented

inspection is warranted, as well as inspections to understand the extent of condition,

source of the gas intrusion, past operability, and to assess the adequacy of the

licensees corrective actions.

B. Scope

The team is expected to address the following:

1. Throughout the inspection coordinate with the regional SRA to ensure the NRC

response to the event is consistent with the potential safety significance.

2. Develop a complete sequence of events related to the discovery of the voided

conditions and follow-up actions taken by the licensee.

3. Review operating experience involving voiding of CCW System piping and evaluate

actions implemented at Wolf Creek as a result of operating experience.

4. Review the current status of the licensees root cause analysis and determine if it is

being conducted at a level of detail commensurate with the significance of the

problem.

5. Review the potential cause or causes of any design deficiencies and/or operating

practices that allowed the voiding condition to exist. Independently verify key

assumptions and facts.

6. Determine if the licensees immediate corrective actions have addressed the extent

of condition for voiding of safety systems and assess whether these actions are

adequate to prevent recurrence. Review the adequacy of any long term corrective

actions being implemented or planned that address voiding of safety systems.

7. Review the calculations the licensee used to evaluate the voided conditions. Assess

the key factors associated with the total volume of the voids including the expected

flow rates of the CCW pumps and the potential impact of voids affecting the pumps,

valves, and piping systems.

8. Review the licensees compliance with the Technical Specifications.

9. Verify the licensee met the proper reporting requirements of 10 CFR 50.72 and

10 CFR 50.73. Also determine if the licensee has plans to issue a Licensee Event

Report to document this issue.

10. Evaluate the potential for any generic issues related to the discovery of the voided

conditions and promptly communicate any potential generic issues to regional

management.

-2- Enclosure 2

11. In concert with the SRA, collect data as necessary to support a significance

determination of issues.

C. Guidance

Inspection Procedure 93812, Special Inspection, will be used during this inspection.

The inspection should emphasize fact-finding in its review of the circumstance

surrounding this event. It is not the responsibility of the team to examine the regulatory

process. Safety concerns identified that are not directly to the event should be reported

to the Region IV office for appropriate action.

The team will report to the site, conduct an entrance, and begin inspection no later than

June 21, 2010. While onsite, you will provide daily status briefings to Region IV

management, starting on Tuesday, June 22, 2010. Regional management will

coordinate with the Office of Nuclear Reactor Regulation to ensure that all other parties

are kept informed. The inspection results will be documented in Special Inspection

Report 05000482/2010008. This report will be issued within 45 days of the completion

of the inspection.

This charter may be modified should the team develop significant new information that

warrants review. Should you require support for the final determination of the risk

significance of any issue, contact David Loveless at 817-860-8161. If you have any

questions concerning this guidance, contact Michael Hay at (817) 276-6527.

-3- Enclosure 2

July 14, 2010

MEMORANDUM TO: Michael Bloodgood, Reactor Engineer, Team Leader

Technical Support Branch

Division of Reactor Safety

Matthew Young, Reactor Inspector

Engineering Branch 1

Division of Reactor Safety

David Dumbacher, Senior Resident Inspector

Projects Branch B

Division of Reactor Projects

FROM: Roy Caniano, Director

Division of Reactor Safety

SUBJECT: AMENDED CHARTER FOR SPECIAL INSPECTION TO EVALUTE GAS

ACCUMULATION IN THE COMPONENT COOLING WATER SYSTEM

AT WOLF CREEK GENERATING STATION

In response to the discovery of voiding in portions of the Component Cooling Water (CCW)

System piping, a Special Inspection was initiated. Subsequent to the occurrence of voiding in

the CCW system, and while the special inspection to review that event was still ongoing,

additional voiding was detected in the Train A Residual Heat Removal (RHR) and

Containment Spray (CS) systems. Consequently, additional inspection is warranted and the

charter dated June 15, 2010, is being amended. David Dumbacher, Senior Resident Inspector,

Callaway Plant, has been assigned as an additional team member to review the circumstances

related to the voiding identified in the RHR and CS systems. David Loveless, Senior Reactor

Analyst (SRA) will continue to support the team.

A. Basis

Specifically, on May 24, 2010, during a planned start of CCW Pump A for inservice

testing, operators at Wolf Creek observed a pressure drop and a surge tank level drop of

68 gallons. During this system transient, Pump C started unexpectedly on a feature

designed to maintain the system pressurized. At the time, the licensee attributed the

anomalous system response to a faulty pressure relay. On June 1, 2010, Train A of

CCW experienced a 65-gallon surge tank level drop following the start of Pump C. The

licensee subsequently determined the May 24 and June 1 level changes were caused by

gas pockets in the CCW system. Follow-up venting on June 1, 2010, uncovered the

presence of an additional 0.4 cubic feet of gas in the RHR Train A heat exchanger

shell. Also, an extent of condition check of Train B on June 2, 2010, uncovered the

presence of a 22.4 cubic foot void in that piping. On June 3, 2010, ultrasonic testing of

standby CCW Train A identified several additional voids in unvented horizontal piping

runs. The licensee declared the standby train inoperable and commenced dynamic

venting operations to sweep the voids from the piping. The gas voids are believed to

have come from the use of nitrogen saturated fill water after maintenance conducted on

-4- Enclosure 2

the system during the fall 2009 refueling outage. Between that outage and the time the

nitrogen gas was vented, the CCW system was degraded and may not have been able

to perform its safety functions.

A regional SRA estimated the Maximum Conditional Core Damage Probability for this

issue to be between 1E-5 and 1E-4, which is in the overlap region between a special

inspection and an augmented inspection team. Based on current available information,

the NRC staff recommends that the appropriate level of NRC response is the

performance of a special inspection. The special inspection activities will include

information gathering to determine whether an augmented inspection is warranted, as

well as inspections to understand the extent of condition, source of the gas intrusion,

past operability, and to assess the adequacy of the licensees corrective actions.

During the weeks of June 28, 2010, and July 5, 2010, additional voids were discovered

in Train A of the RHR and CS Systems. Initial causal determinations indicate that the

source on the voids discovered in these systems are the same as for the voiding initially

discovered in the CCW system. A follow-up estimate of the Conditional Core Damage

Probability by a regional SRA, informed by the inspection team for the condition of CCW

after their June 21-25, 2010, onsite inspection, combined with the RHR and CS

inoperability showed no appreciable change in the risk values.

B. Scope

The team is expected to address the following:

12. Throughout the inspection coordinate with the regional SRA to ensure the NRC

response to the event is consistent with the potential safety significance.

13. Develop a complete sequence of events related to the discovery of the voided

conditions for each system with voids and follow-up actions taken by the licensee.

14. Review operating experience involving voiding of CCW, RHR and CS System piping

and evaluate actions implemented at Wolf Creek as a result of operating experience.

15. Review the current status of the licensees root cause analysis and determine if it is

being conducted at a level of detail commensurate with the significance of the

problem.

16. Review the potential cause or causes of any design deficiencies and/or operating

practices that allowed the voiding condition to exist in each system. Independently

verify key assumptions and facts.

17. Determine if the licensees immediate corrective actions have addressed the extent

of condition and extent of cause for voiding of safety systems and assess whether

these actions are adequate to prevent recurrence. Review the adequacy of any long

term corrective actions being implemented or planned that address voiding of safety

systems, including any actions enacted for Generic Letter 2008-01, Managing Gas

Accumulation in Emergency Core Cooling, Decay Heat Removal, and Containment

Spray Systems, and the NRC inspection detailed in Inspection Report 05000482/2008007.

-5- Enclosure 2

18. Review the calculations the licensee used to evaluate the voided conditions. Assess

the key factors associated with the total volume of the voids including the expected

flow rates of the pumps and the potential impact of voids affecting the pumps, valves,

and piping systems.

19. Review the licensees compliance with the Technical Specifications.

20. Verify the licensee met the proper reporting requirements of 10 CFR 50.72 and

10 CFR 50.73. Also determine if the licensee has plans to issue a Licensee Event

Report to document this issue.

21. Evaluate the potential for any generic issues related to the discovery of the voided

conditions and promptly communicate any potential generic issues to regional

management.

22. In concert with the SRA, collect data as necessary to support a significance

determination of issues. This includes determinations on the functionality of the

CCW, RHR, CS, and any other systems with the presence of indicated voids.

C. Guidance

Inspection Procedure 93812, Special Inspection, will be used during this inspection.

The inspection should emphasize fact-finding in its review of the circumstance

surrounding this event. It is not the responsibility of the team to examine the regulatory

process. Safety concerns identified that are not directly to the event should be reported

to the Region IV office for appropriate action.

The team will report to the site, conduct an entrance, and begin inspection no later than

June 21, 2010. While onsite, you will provide daily status briefings to Region IV

management, starting on Tuesday, June 22, 2010. Regional management will

coordinate with the Office of Nuclear Reactor Regulation to ensure that all other parties

are kept informed. The inspection results will be documented in Special Inspection

Report 05000482/2010008. This report will be issued within 45 days of the completion

of the inspection.

This charter may be modified should the team develop significant new information that

warrants review. Should you have any questions concerning this guidance, contact

Michael Hay at (817) 276-6527.

-6- Enclosure 2