ML100360782

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IR 05000382-09-005; on October 8, 2009 Through December 31, 2009; Waterford Steam Electric Station, Unit 3, Identification and Resolution of Problems, Access Control to Radiologically Significant Areas
ML100360782
Person / Time
Site: Waterford Entergy icon.png
Issue date: 02/05/2010
From: Clark J
NRC/RGN-IV/DRP/RPB-E
To: Kowalewski J
Entergy Operations
References
IR-09-005
Download: ML100360782 (59)


See also: IR 05000382/2009005

Text

UNITED STATES

NUC LE AR RE G UL AT O RY C O M M I S S I O N

R E GI ON I V

612 EAST LAMAR BLVD , SU I TE 400

AR LI N GTON , TEXAS 76011-4125

February 5, 2010

Joseph Kowalewski, Vice President, Operations

Entergy Operations, Inc.

Waterford Steam Electric Station, Unit 3

17265 River Road

Killona, LA 70057-0751

SUBJECT: WATERFORD STEAM ELECTRIC STATION, UNIT 3 - NRC INTEGRATED

INSPECTION REPORT 05000382/2009005

Dear Mr. Kowalewski:

On December 31, 2009, the U.S. Nuclear Regulatory Commission (NRC) completed an

inspection at your Waterford Steam Electric Station, Unit 3. The enclosed integrated inspection

report documents the inspection findings, which were discussed on January 11, 2010, with you

and other members of your staff.

The inspections examined activities conducted under your license as they relate to safety and

compliance with the Commissions rules and regulations and with the conditions of your license.

The inspectors reviewed selected procedures and records, observed activities, and interviewed

personnel.

This report documents three self-revealing findings of very low safety significance (Green). All

of these findings were determined to involve violations of NRC requirements. Additionally, a

licensee-identified violation, which was determined to be of very low safety significance, is listed

in this report. However, because of the very low safety significance and because they are

entered into your corrective action program, the NRC is treating these findings as noncited

violations, consistent with Section VI.A.1 of the NRC Enforcement Policy. If you contest the

violations or the significance of the noncited violations, you should provide a response within

30 days of the date of this inspection report, with the basis for your denial, to the U.S. Nuclear

Regulatory Commission, ATTN: Document Control Desk, Washington, D.C. 20555-0001, with

copies to the Regional Administrator, U.S. Nuclear Regulatory Commission, Region IV, 612 E.

Lamar Blvd, Suite 400, Arlington, Texas, 76011-4125; the Director, Office of Enforcement,

U.S. Nuclear Regulatory Commission, Washington, D.C. 20555-0001; and the NRC Resident

Inspector at the Waterford Steam Electric Station, Unit 3 facility. In addition, if you disagree with

the characterization of any finding in this report, you should provide a response within 30 days

of the date of this inspection report, with the basis for your disagreement, to the Regional

Administrator, Region IV, and the NRC Resident Inspector at Waterford Steam Electric Station,

Entergy Operations, Inc. -2-

Unit 3. The information you provide will be considered in accordance with Inspection Manual

Chapter 0305.

In accordance with 10 CFR 2.390 of the NRC's Rules of Practice, a copy of this letter, and its

enclosure, will be available electronically for public inspection in the NRC Public Document

Room or from the Publicly Available Records component of NRCs document system (ADAMS).

ADAMS is accessible from the NRC Web site at http://www.nrc.gov/reading-rm/adams.html (the

Public Electronic Reading Room).

Sincerely,

/RA/

Jeffrey A. Clark, P.E.

Chief, Project Branch E

Division of Reactor Projects

Docket: 50-382

License: NPF-38

Enclosure:

NRC Inspection Report 05000382/2009005

w/Attachment: Supplemental Information

cc w/Enclosure:

Senior Vice President

Entergy Nuclear Operations

P. O. Box 31995

Jackson, MS 39286-1995

Senior Vice President and

Chief Operating Officer

Entergy Operations, Inc.

P. O. Box 31995

Jackson, MS 39286-1995

Vice President, Operations Support

Entergy Services, Inc.

P. O. Box 31995

Jackson, MS 39286-1995

Senior Manager, Nuclear Safety

and Licensing

Entergy Services, Inc.

P. O. Box 31995

Jackson, MS 39286-1995

Entergy Operations, Inc. -3-

Site Vice President

Waterford Steam Electric Station, Unit 3

Entergy Operations, Inc.

17265 River Road

Killona, LA 70057-0751

Director

Nuclear Safety Assurance

Entergy Operations, Inc.

17265 River Road

Killona, LA 70057-0751

General Manager, Plant Operations

Waterford 3 SES

Entergy Operations, Inc.

17265 River Road

Killona, LA 70057-0751

Manager, Licensing

Entergy Operations, Inc.

17265 River Road

Killona, LA 70057-0751

Chairman

Louisiana Public Service Commission

P. O. Box 91154

Baton Rouge, LA 70821-9154

Parish President Council

St. Charles Parish

P. O. Box 302

Hahnville, LA 70057

Director, Nuclear Safety & Licensing

Entergy, Operations, Inc.

440 Hamilton Avenue

White Plains, NY 10601

Louisiana Department of Environmental

Quality, Radiological Emergency Planning

and Response Division

P. O. Box 4312

Baton Rouge, LA 70821-4312

Entergy Operations, Inc. -4-

Chief, Technological Hazards

Branch

FEMA Region VI

800 North Loop 288

Federal Regional Center

Denton, TX 76209

Entergy Operations, Inc. -5-

Electronic distribution by RIV:

Regional Administrator (Elmo.Collins@nrc.gov)

Deputy Regional Administrator (Chuck.Casto@nrc.gov)

DRP Director (Dwight.Chamberlain@nrc.gov)

DRP Deputy Director (Anton.Vegel@nrc.gov)

DRS Director (Roy.Caniano@nrc.gov)

DRS Deputy Director (Troy.Pruett@nrc.gov)

Senior Resident Inspector (Mark Haire@nrc.gov)

Resident Inspector (Dean.Overland@nrc.gov)

Branch Chief, DRP/E (Jeff.Clark@nrc.gov)

Senior Project Engineer, DRP/E (Ray.Azua@nrc.gov)

WAT Site Secretary (Linda.Dufrene@nrc.gov)

Public Affairs Officer (Victor.Dricks@nrc.gov)

Public Affairs Officer (Lara.Uselding@nrc.gov)

Branch Chief, DRS/TSB (Michael.Hay@nrc.gov)

RITS Coordinator (Marisa.Herrera@nrc.gov)

Regional Counsel (Karla.Fuller@nrc.gov)

Congressional Affairs Officer (Jenny.Weil@nrc.gov)

OEMail Resource

Regional State Liaison Officer (Bill.Maier@nrc.gov)

NSIR/DPR/EP (Eric.Schrader@nrc.gov)

NSIR/DPR/EP (Steve.LaVie@nrc.gov)

Inspection Reports/MidCycle and EOC Letters to the following:

ROPreports

Only inspection reports to the following:

DRS/TSB STA (Dale.Powers@nrc.gov)

OEDO RIV Coordinator (Leigh.Trocine@nrc.gov)

R:\File located: R:\REACTORS\_WAT\2009\WAT 2009004 RP-MSH.doc ML 100360782

ADAMS: No  : Yes  : SUNSI Review Complete Reviewer Initials: JAC

Publicly Available  : Non-Sensitive

Non-publicly Available Sensitive

RIV:SRI:DRP/E RI:DRP/E SPE:DRP/E C:DRS/EB1 C:DRS/EB2

MSHaire DHOverland RVAzua TFarnholtz NFOKeefe

/RA/E-mailed /RA/E-mailed /RA/ /RA/ /RA/

01/25/2010 01/25/2010 01/18/2010 01/19/2010 1/19/2010

C:DRS/OB C:DRS/PSB1 C:DRS/PSB2 C:DRP/E

SMGarchow MPShannon GEWerner JAClark

/RA/ /RA/ /RA/ /RA/

01/25/2010 01/25/2010 1/19/2010 02/5/2010

OFFICIAL RECORD COPY T=Telephone E=E-mail F=Fax

U.S. NUCLEAR REGULATORY COMMISSION

REGION IV

Docket: 05000382

License: NFP-38

Report: 05000382/2009005

Licensee: Entergy Operations, Inc.

Facility: Waterford Steam Electric Station, Unit 3

Location: Hwy. 18

Killona, LA

Dates: October 8 through December 31, 2009

Inspectors: M. Haire, Senior Resident Inspector

D. Overland, Resident Inspector

S. Anderson, General Engineer

R. Azua, Senior Project Engineer

M. Bloodgood, Senior Reactor Inspector

T. Buchanan, Reactor Inspector

P. Elkmann, Senior Emergency Preparedness Inspector

L. Ricketson, P.E., Senior Health Physicist

N. Greene, Health Physicist

Approved By: Jeff Clark, P.E., Chief, Project Branch E

Division of Reactor Projects

-1- ENCLOSURE

SUMMARY OF FINDINGS

IR 05000382/2009005; October 8, 2009 through December 31, 2009; Waterford Steam Electric

Station, Unit 3, Identification and Resolution of Problems, Access Control to Radiologically

Significant Areas

The report covered a 3-month period of inspection by resident inspectors and announced

baseline inspections by regional based inspectors. Three Green noncited violations of NRC

requirements were identified. The significance of most findings is indicated by their color

(Green, White, Yellow, or Red) using Inspection Manual Chapter 0609, Significance

Determination Process. Findings for which the significance determination process does not

apply may be Green or be assigned a severity level after NRC management review. The NRC's

program for overseeing the safe operation of commercial nuclear power reactors is described in

NUREG-1649, Reactor Oversight Process, Revision 4, dated December 2006.

A. NRC-Identified Findings and Self-Revealing Findings

Cornerstone: Initiating Events

Criterion XVI, was identified for the licensees failure to promptly correct a

condition adverse to quality. Specifically, the licensee did not promptly correct

reactor coolant pump vapor seal leakage that resulted in boric acid accumulation

on the component cooling water heat exchanger and cover areas of three reactor

coolant pumps. Corrective actions for this condition were implemented during

Refueling Outage 15, but these corrective actions failed to correct the condition

and the vapor seal leakage continued through operating Cycle 16. This resulted

in some additional boric acid corrosion and degradation to reactor coolant pump

covers and carbon steel component cooling water flanges. The licensee

implemented a design modification to correct the condition and documented the

condition in Condition Report CR-WF3-2009-5501.

The licensees failure to promptly correct a condition adverse to quality is more

than minor because it is associated with the equipment performance attribute of

the Initiating Events Cornerstone and affects the cornerstone objective to limit the

likelihood of those events that upset plant stability. The finding has very low

safety significance because, although the finding contributes to the likelihood of a

reactor trip, mitigation equipment was still available. This finding had a

crosscutting aspect in the area of human performance associated with work

control in that the licensee did not effectively plan for the resources necessary to

implement the postmaintenance testing associated with the corrective actions

implemented during Refueling Outage 15, and therefore failed to discover that

those corrective actions were inadequate to correct the condition H.3(a)

(Section 4OA2).

Criterion V, was identified for the licensees failure to prescribe an activity

-2- ENCLOSURE

affecting quality by documented instructions, procedures, or drawings

appropriate to the circumstance. Specifically, for all reactor coolant pump heat

exchanger to pump cover bolted connection gasket replacements between the

refueling outage of 1986 (Refueling Outage 1) and the refueling outage of 2009

(Refueling Outage 16), the licensee prescribed the wrong gasket material, gasket

size, and fastener preload because they had failed to incorporate a design

change implemented during Refueling Outage 1 into their instructions,

procedures, or drawings. Station Modification Package SMP-1427, an

engineering change implemented during Refueling Outage 1 in response to

industry operating experience, called for a thicker gasket, different gasket

material, and an increased bolt preload in order to increase gasket compression

and reduce the probability of leakage. As a consequence of failing to incorporate

Station Modification Package SMP-1427 changes into procedures, all heat

exchanger gasket replacements since Refueling Outage 1, four gasket

replacements in total, have utilized thinner gaskets with less than the vendor

recommended compression. The licensee documented this condition in

Condition Report CR-WF3-2009-5501.

The licensees failure to prescribe appropriate gasket replacement requirements

is more than minor because it is associated with the equipment performance

attribute of the Initiating Events Cornerstone and affects the cornerstone

objective to limit the likelihood of those events that upset plant stability. The

finding has very low safety significance because, although the finding contributes

to the likelihood of a reactor trip, mitigation equipment is still available. This

finding had a crosscutting aspect in the area of problem identification and

resolution associated with operating experience in that the licensee did not

institutionalize operating experience through changes to the station procedures

P.2(b) (Section 4OA2).

Cornerstone: Occupational Radiation Safety

  • Green. The inspectors reviewed a self-revealing noncited violation of Technical

Specification 6.8.1 which resulted from a worker failing to follow radiation

protection procedures. A contract radiation worker went to work near steam

generator 1 rather than the area for which he/she was briefed and received

multiple electronic dosimeter dose rate alarms, but did not leave the area until

receiving a continuous dose alarm. In response, the licensee investigated the

occurrence and restricted the individuals access. Additional actions were being

evaluated. This issue was entered into the licensees corrective action program

as Condition Reports CR-WF3-2009-05648 and WF3-2009-06852.

This finding is greater than minor because it involved the program attribute of

exposure control and affected the cornerstone objective in that the failure of the

worker to follow procedural guidance resulted in the worker being

unknowledgeable to the dose rates in all areas entered. The inspectors used the

Occupational Radiation Safety Significance Determination Process and

determined the finding had very low safety significance because it was not:

(1) an as low as reasonably achievable (ALARA) finding, (2) an overexposure,

-3- ENCLOSURE

(3) a substantial potential for overexposure, or (4) an inability to assess dose.

The finding had a crosscutting aspect in the area of human performance, work

practices component, because the worker failed to use human error prevention

techniques such as self and peer checking H.4(a) (Section 2OS1).

B. Licensee-Identified Violations

A violation of very low safety significance, which was identified by the licensee, has been

reviewed by the inspectors. Corrective actions taken or planned by the licensee have

been entered into the licensees corrective action program. This violation and corrective

action tracking numbers (condition report numbers) are listed in Section 4OA7.

-4- ENCLOSURE

REPORT DETAILS

Summary of Plant Status

The plant began the inspection period on October 8, 2009, at 100 percent power and remained

at approximately 100 percent power until October 19, 2009, when the plant was shutdown in

preparation of the licensees planned Refueling Outage 16. The plant remained shutdown until

December 1, 2009, when the reactor was placed back online and the licensee began increasing

power. On December 6, 2009, the plant reached 100 percent power and continued to operate

at this level for the remainder of the inspection period.

1. REACTOR SAFETY

Cornerstones: Initiating Events, Mitigating Systems, Barrier Integrity, and

Emergency Preparedness

1R01 Adverse Weather Protection (71111.01)

.1 Readiness to Cope with External Flooding

a. Inspection Scope

The inspectors evaluated the design, material condition, and procedures for coping with

the design basis probable maximum flood. The evaluation included a review to check

for deviations from the descriptions provided in the Updated Final Safety Analysis Report

for features intended to mitigate the potential for flooding from external factors. As part

of this evaluation, the inspectors checked for obstructions that could prevent draining,

checked that the roofs did not contain obvious loose items that could clog drains in the

event of heavy precipitation, and determined that barriers required to mitigate the flood

were in place and operable. Additionally, the inspectors performed a walkdown of the

protected area to identify any modification to the site that would inhibit site drainage

during a probable maximum precipitation event or allow water ingress past a barrier.

The inspectors also reviewed the abnormal operating procedure for mitigating the design

basis flood to ensure it could be implemented as written. Specific documents reviewed

during this inspection are listed in the attachment.

These activities constitute completion of one external flooding sample as defined in

Inspection Procedure 71111.01-05.

b. Findings

No findings of significance were identified.

-5- ENCLOSURE

1R04 Equipment Alignments (71111.04)

.1 Partial Walkdown

a. Inspection Scope

The inspectors performed partial system walkdowns of the following risk-significant

systems:

  • October 8, 2009, Essential chiller train B
  • October 14, 2009, Low pressure safety injection train B

The inspectors selected these systems based on their risk significance relative to the

reactor safety cornerstones at the time they were inspected. The inspectors attempted

to identify any discrepancies that could affect the function of the system, and, therefore,

potentially increase risk. The inspectors reviewed applicable operating procedures,

system diagrams, Updated Final Safety Analysis Report, technical specification

requirements, administrative technical specifications, outstanding work orders, condition

reports, and the impact of ongoing work activities on redundant trains of equipment in

order to identify conditions that could have rendered the systems incapable of

performing their intended functions. The inspectors also walked down accessible

portions of the systems to verify system components and support equipment were

aligned correctly and operable. The inspectors examined the material condition of the

components and observed operating parameters of equipment to verify that there were

no obvious deficiencies. The inspectors also verified that the licensee had properly

identified and resolved equipment alignment problems that could cause initiating events

or impact the capability of mitigating systems or barriers and entered them into the

corrective action program with the appropriate significance characterization. Specific

documents reviewed during this inspection are listed in the attachment.

These activities constitute completion of two partial system walkdown samples as

defined in Inspection Procedure 71111.04-05.

b. Findings

No findings of significance were identified.

1R05 Fire Protection (71111.05)

.1 Quarterly Fire Inspection Tours

a. Inspection Scope

The inspectors conducted fire protection walkdowns that were focused on availability,

accessibility, and the condition of firefighting equipment in the following risk-significant

plant areas:

  • November 2, 2009, Fuel handling building
  • November 10, 2009, Fire zones RAB 37, 38, and 39

-6- ENCLOSURE

  • November 28, 2009, Reactor containment building
  • December 15, 2009, Battery and switchgear areas

The inspectors reviewed areas to assess if licensee personnel had implemented a fire

protection program that adequately controlled combustibles and ignition sources within

the plant; effectively maintained fire detection and suppression capability; maintained

passive fire protection features in good material condition; and had implemented

adequate compensatory measures for out of service, degraded or inoperable fire

protection equipment, systems, or features, in accordance with the licensees fire plan.

The inspectors selected fire areas based on their overall contribution to internal fire risk

as documented in the plants Individual Plant Examination of External Events with later

additional insights, their potential to affect equipment that could initiate or mitigate a plant

transient, or their impact on the plants ability to respond to a security event. Using the

documents listed in the attachment, the inspectors verified that fire hoses and

extinguishers were in their designated locations and available for immediate use; that

fire detectors and sprinklers were unobstructed, that transient material loading was

within the analyzed limits; and fire doors, dampers, and penetration seals appeared to

be in satisfactory condition. The inspectors also verified that minor issues identified

during the inspection were entered into the licensees corrective action program.

Specific documents reviewed during this inspection are listed in the attachment.

These activities constitute completion of four quarterly fire-protection inspection samples

as defined in Inspection Procedure 71111.05-05.

b. Findings

No findings of significance were identified.

1R06 Flood Protection Measures (71111.06)

a. Inspection Scope

The inspectors reviewed the Updated Final Safety Analysis Report, the flooding analysis,

and plant procedures to assess susceptibilities involving internal flooding; reviewed the

corrective action program to determine if licensee personnel identified and corrected

flooding problems; and verified that operator actions for coping with flooding can

reasonably achieve the desired outcomes. The inspectors also walked down the area

listed below to verify the adequacy of equipment seals located below the flood line, floor

and wall penetration seals, watertight door seals, common drain lines and sumps, sump

pumps, level alarms, and control circuits, and temporary or removable flood barriers.

  • October 14, 2009, Reactor Auxiliary Building -35 foot elevation

This inspection procedure also requires an annual review of risk-significant cables

located in underground bunkers/manholes. Waterford Steam Electric Station, Unit 3, by

design, does not have any safety-related cables that are located in underground

bunkers/manholes; however, there are 17 manholes in which cables associated with

maintenance rule related equipment were located. The inspectors inspected

-7- ENCLOSURE

Manholes M301-NA, M346-NB, and M347-NA and determined that all three contained

maintenance rule related cables submerged in water. The submerged cables did not

show visible deterioration. The licensee has documented this condition in Condition

Report CR-WF3-2009-3925, and is developing a cable monitoring program. Specific

documents reviewed during this inspection are listed in the attachment.

This activity constitutes completion of two flood protection measures inspection samples

as defined in Inspection Procedure 71111.06-05.

b. Findings

No findings of significance were identified.

1R07 Heat Sink Performance (71111.07)

a. Inspection Scope

The inspectors reviewed licensee programs, verified performance against industry

standards, and reviewed critical operating parameters and maintenance records for the

steam generators. The inspectors verified that performance tests were satisfactorily

conducted for heat exchangers/heat sinks and reviewed for problems or errors; the

licensee utilized the periodic maintenance method outlined in EPRI Report NP 7552,

Heat Exchanger Performance Monitoring Guidelines; the licensee properly utilized

biofouling controls; the licensees heat exchanger inspections adequately assessed the

state of cleanliness of their tubes; and the heat exchanger was correctly categorized

under 10 CFR 50.65, Requirements for Monitoring the Effectiveness of Maintenance at

Nuclear Power Plants. Specific documents reviewed during this inspection are listed in

the attachment.

These activities constitute completion of one heat sink inspection sample as defined in

Inspection Procedure 71111.07-05.

b. Findings

No findings of significance were identified.

1R08 In-service Inspection Activities (71111.08)

Completion of Sections .1 through .5, below, constitutes completion of one sample as

defined in Inspection Procedure 71111.05-05.

.1 Inspection Activities Other Than Steam Generator Tube Inspection, Pressurized Water

Reactor Vessel Upper Head Penetration Inspections, and Boric Acid Corrosion Control

(71111.08-02.01)

a. Inspection Scope

The inspectors reviewed two types of nondestructive examination activities and two

welds on the reactor coolant system pressure boundary.

-8- ENCLOSURE

The inspectors directly observed the following nondestructive examinations:

SYSTEM WELD IDENTIFICATION EXAMINATION TYPE

Safety Injection RCS 2A Safety Injection Nozzle Ultrasonic Testing

System (Weld No.12-009)

Reactor Coolant RCS 1A Cold leg Suction Line Ultrasonic Testing

System (Weld No.07-005)

Reactor Coolant RCS 2A Cold Leg Suction Line Ultrasonic Testing

System (Weld No.11-002)

Reactor Coolant RCS 2A Cold Leg Suction Line Visual Inspection VT-1&2

System (Weld No.11-002)

The inspectors reviewed records for the following nondestructive examinations:

SYSTEM IDENTIFICATION EXAMINATION TYPE

Safety Injection RCS 2A Safety Injection Nozzle Ultrasonic Testing

System (Weld No.12-009)

Reactor Coolant RCS 1A Cold leg Suction Line Ultrasonic Testing

System (Weld No.07-005)

Reactor Coolant RCS 2A Cold Leg Suction Line Ultrasonic Testing

System (Weld No.11-002)

Reactor Coolant RCS 2A Cold Leg Suction Line Visual Inspection VT-1&2

System (Weld No.11-002)

Reactor Coolant RCS 12 Hot Leg Surge Line Ultrasonic Testing

System (Weld No.15-009)

During the review and observation of each examination, the inspectors verified that

activities were performed in accordance with the ASME Code requirements and

applicable procedures. The inspectors also verified the qualifications of all

nondestructive examination technicians performing the inspections were current.

The inspectors verified, by review, that the welding procedure specifications and the

welders had been properly qualified in accordance with ASME Code,Section IX,

requirements. The inspectors also verified, through observation and record review, that

essential variables for the welding process were identified, recorded in the procedure

qualification record, and formed the basis for qualification of the welding procedure

specifications. Specific documents reviewed during this inspection are listed in the

attachment.

These actions constitute completion of the requirements for Section 02.01.

-9- ENCLOSURE

b. Findings

No findings of significance were identified.

.2 Vessel Upper Head Penetration Inspection Activities (71111.08-02.02)

a. Inspection Scope

The inspectors reviewed the results of licensee personnels visual inspection of

pressure-retaining components above the reactor pressure vessel head to verify that

there was no evidence of leaks or boron deposits on the surface of the reactor pressure

vessel head or related insulation. The inspectors verified that the personnel performing

the visual inspection were certified as Level II and Level III VT-2 examiners. Specific

documents reviewed during this inspection are listed in the attachment.

The inspectors also reviewed the results of licensee personnels volumetric inspection of

pressure-retaining components above the reactor pressure vessel head to verify that

there were no flaws in the welds associated with these penetrations. The inspectors

observed data acquisition and analysis of one penetration. The inspector verified that

the personnel performing the inspections were current in their certification as Level II or

Level III ultrasonic testing examiners. Specific documents reviewed during this

inspection are listed in the attachment.

These actions constitute completion of the requirements for Section 02.02.

b. Findings

No findings of significance were identified.

.3 Boric Acid Corrosion Control Inspection Activities (71111.08-02.03)

a. Inspection Scope

The inspectors evaluated the implementation of the licensees boric acid corrosion

control program for monitoring degradation of those systems that could be adversely

affected by boric acid corrosion. The inspectors reviewed the documentation associated

with the licensees boric acid corrosion control walkdown as specified in Procedure

NOECP-107, Boric Acid Corrosion Control Program (BACCP), Revision 1. The

inspectors also reviewed the visual records of the components and equipment. The

inspectors verified that the visual inspections emphasized locations where boric acid

leaks could cause degradation of safety-significant components. The inspectors also

verified that the engineering evaluations for those components where boric acid was

identified gave assurance that the ASME Code wall thickness limits were properly

maintained. The inspectors confirmed that the corrective actions performed for evidence

of boric acid leaks were consistent with requirements of the ASME Code. Specific

documents reviewed during this inspection are listed in the attachment.

- 10 - ENCLOSURE

These actions constitute completion of the requirements for Section 02.03.

b. Findings

No findings of significance were identified.

.4 Steam Generator Tube Inspection Activities (71111.08-02.04)

a. Inspection Scope

The inspectors assessed the in-situ screening criteria to assure consistency between

assumed nondestructive examination flaw sizing accuracy and data from the Electric

Power Research Institute (EPRI) examination technique specification sheets. No

conditions were identified that warranted in-situ pressure testing. The inspectors did,

however, review the licensees Steam Generator Degradation Assessment and Repair

Criteria for RF15, dated April 2008, and compared the in-situ test screening parameters

to the guidelines contained in the EPRI document In Situ Pressure Test Guidelines,

Revision 2. This review determined that the screening parameters were consistent with

the EPRI guidelines.

In addition, the inspectors reviewed both the licensee site-validated and qualified

acquisition and analysis technique sheets used during this refueling outage and the

qualifying EPRI examination technique specification sheets to verify that the essential

variables regarding flaw sizing accuracy, tubing, equipment, technique, and analysis had

been identified and qualified through demonstration. The inspectors reviewed

acquisition technique and analysis technique data sheets.

The inspection procedure specified comparing the estimated size and number of tube

flaws detected during the current outage against the previous outage operational

assessment predictions to assess the licensees prediction capability. The inspectors

compared the previous outage operational assessment predictions with the flaws

identified during the current steam generator tube inspection effort. The number of

identified indications fell below the range of prediction but was consistent with historical

predictions.

The inspection procedure specified confirmation that the steam generator tube eddy

current test scope and expansion criteria meet technical specification requirements,

EPRI guidelines, and commitments made to the NRC. The inspectors compared the

recommended test scope to the actual test scope and found that the licensee had

accounted for all known flaws and had, as a minimum, established a test scope that met

technical specification requirements, EPRI guidelines, and commitments made to the

NRC. The scope of the licensees eddy current examinations of tubes in both steam

generators included:

  • 100 percent bobbin examination full length of tubing
  • 100 percent hot leg top of tube sheet
  • 100 percent Rows 1 and 2 u-bend rotating pancake coil
  • 100 percent dented tube supports at egg crates greater than 2 Volts

- 11 - ENCLOSURE

  • 20 percent dented diagonal bar and vertical strap greater than 2 Volts
  • 20 percent free span dings greater than 5 Volts
  • Cold leg top of tube sheet periphery exam for loose parts

The inspection procedure specified that, if new degradation mechanisms were identified,

the licensee would verify the analysis fully enveloped the problem of the extended

conditions including operating concerns and that appropriate corrective actions were

taken before plant startup. No new degradation mechanisms were identified.

The inspection procedure required confirmation that the licensee inspected all areas of

potential degradation, especially areas that were known to represent potential eddy

current test challenges (e.g., top-of-tubesheet, tube support plates, and U-bends). The

inspectors confirmed that all known areas of potential degradation were included in the

scope of inspection and were being inspected.

The inspection procedure further required verification that repair processes being used

were approved in the technical specifications. The inspectors confirmed that the repair

processes being used were consistent with the technical specifications requirements.

The inspection procedure also required confirmation of adherence to the technical

specification plugging limit, unless alternate repair criteria have been approved. The

inspection procedure further requires determination whether depth sizing repair criteria

were being applied for indications other than wear or axial primary water stress corrosion

cracking in dented tube support plate intersections. The inspectors determined that the

technical specification plugging limits were being adhered to (i.e., 40 percent maximum

through-wall indication).

If steam generator leakage greater than 3 gallons per day was identified during

operations or during post shutdown visual inspections of the tubesheet face, the

inspection procedure required verification that the licensee had identified a reasonable

cause based on inspection results and that corrective actions were taken or planned to

address the cause for the leakage. The inspectors did not conduct any assessment

because this condition did not exist.

The inspection procedure required confirmation that the eddy current test probes and

equipment were qualified for the expected types of tube degradation and an assessment

of the site-specific qualification of one or more techniques. The inspectors observed

portions of the eddy current tests. During these examinations, the inspectors verified

that: (1) the probes appropriate for identifying the expected types of indications were

being used, (2) probe position location verification was performed, (3) calibration

requirements were adhered, and (4) probe travel speed was in accordance with

procedural requirements. The inspectors performed a review of site-specific

qualifications of the techniques being used.

These actions constitute completion of the requirements of Section 02.04.

- 12 - ENCLOSURE

b. Findings

No findings of significance were identified.

.5 Identification and Resolution of Problems (71111.08-02.05)

a. Inspection scope

The inspectors reviewed 27 condition reports which dealt with inservice inspection

activities and found the corrective actions were appropriate. The specific condition

reports reviewed are listed in the documents reviewed section. From this review the

inspectors concluded that the licensee has an appropriate threshold for entering issues

into the corrective action program and has procedures that direct a root cause evaluation

when necessary. The licensee also has an effective program for applying industry

operating experience. Specific documents reviewed during this inspection are listed in

the attachment.

These actions constitute completion of the requirements of Section 02.05.

b. Findings

No findings of significance were identified.

1R11 Licensed Operator Requalification Program (71111.11)

a. Inspection Scope

On November 24, 2009, the inspectors observed a crew of licensed operators in the

plants simulator to verify that operator performance was adequate, evaluators were

identifying and documenting crew performance problems, and training was being

conducted in accordance with licensee procedures. The inspectors evaluated the

following areas:

  • Licensed operator performance
  • Crews clarity and formality of communications
  • Crews ability to take timely actions in the conservative direction
  • Crews prioritization, interpretation, and verification of annunciator alarms
  • Control board manipulations
  • Oversight and direction from supervisors

The inspectors compared the crews performance in these areas to pre-established

operator action expectations. Specific documents reviewed during this inspection are

listed in the attachment.

These activities constitute completion of one quarterly licensed-operator requalification

program sample as defined in Inspection Procedure 71111.11.

- 13 - ENCLOSURE

b. Findings

No findings of significance were identified.

1R12 Maintenance Effectiveness (71111.12Q)

a. Inspection Scope

The inspectors evaluated degraded performance issues involving the following risk

significant systems:

  • November 20, 2009, Effects of voiding on the functionality of low pressure safety

injection system

  • December 8, 2009, Effects of excessive leakage on functionality of containment

isolation valves

The inspectors reviewed events such as where ineffective equipment maintenance has

resulted in valid or invalid automatic actuations of engineered safeguards systems and

independently verified the licensee's actions to address system performance or condition

problems in terms of the following:

  • Implementing appropriate work practices
  • Identifying and addressing common cause failures
  • Characterizing system reliability issues for performance
  • Charging unavailability for performance
  • Trending key parameters for condition monitoring
  • Verifying appropriate performance criteria for structures, systems, and

components classified as having an adequate demonstration of performance

through preventive maintenance, as described in 10 CFR 50.65(a)(2), or as

requiring the establishment of appropriate and adequate goals and corrective

actions for systems classified as not having adequate performance, as described

in 10 CFR 50.65(a)(1)

The inspectors assessed performance issues with respect to the reliability, availability,

and condition monitoring of the system. In addition, the inspectors verified maintenance

effectiveness issues were entered into the corrective action program with the appropriate

significance characterization. Specific documents reviewed during this inspection are

listed in the attachment.

- 14 - ENCLOSURE

These activities constitute completion of two quarterly maintenance effectiveness

samples as defined in Inspection Procedure 71111.12-05.

b. Findings

No findings of significance were identified.

1R13 Maintenance Risk Assessments and Emergent Work Control (71111.13)

a. Inspection Scope

The inspectors reviewed licensee personnel's evaluation and management of plant risk

for the maintenance and emergent work activities affecting risk-significant and

safety-related equipment listed below to verify that the appropriate risk assessments

were performed prior to removing equipment for work:

water level reduced to approximately 19 feet to support reactor vessel head

removal during mode 6 operations

and draw a bubble in the pressurizer following the refueling outage

  • December 13, 2009, Scheduled plant protection system channel B functional test

The inspectors selected these activities based on potential risk significance relative to

the reactor safety cornerstones. As applicable for each activity, the inspectors verified

that licensee personnel performed risk assessments as required by 10 CFR 50.65(a)(4)

and that the assessments were accurate and complete. When licensee personnel

performed emergent work, the inspectors verified that the licensee personnel promptly

assessed and managed plant risk. The inspectors reviewed the scope of maintenance

work, discussed the results of the assessment with the licensee's probabilistic risk

analyst or shift technical advisor, and verified plant conditions were consistent with the

risk assessment. The inspectors also reviewed the technical specification requirements

and inspected portions of redundant safety systems, when applicable, to verify risk

analysis assumptions were valid and applicable requirements were met. Specific

documents reviewed during this inspection are listed in the attachment.

These activities constitute completion of three maintenance risk assessments and

emergent work control inspection samples as defined in Inspection

Procedure 71111.13-05.

b. Findings

No findings of significance were identified.

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1R15 Operability Evaluations (71111.15)

a. Inspection Scope

The inspectors reviewed the following issues:

  • October 29, 2009, Log power nuclear instrument channel B
  • November 16, 2009, Station battery train B total allowable resistance
  • November 19, 2009, Broken in-core nuclear instrumentation E-13

The inspectors selected these potential operability issues based on the risk-significance

of the associated components and systems. The inspectors evaluated the technical

adequacy of the evaluations to ensure that technical specification operability was

properly justified and the subject component or system remained available such that no

unrecognized increase in risk occurred. The inspectors compared the operability and

design criteria in the appropriate sections of the technical specifications and Updated

Safety Analysis Report to the licensees evaluations, to determine whether the

components or systems were operable. Where compensatory measures were required

to maintain operability, the inspectors determined whether the measures in place would

function as intended and were properly controlled. The inspectors determined, where

appropriate, compliance with bounding limitations associated with the evaluations.

Additionally, the inspectors also reviewed a sampling of corrective action documents to

verify that the licensee was identifying and correcting any deficiencies associated with

operability evaluations. Specific documents reviewed during this inspection are listed in

the attachment.

These activities constitute completion of three operability evaluations inspection samples

as defined in Inspection Procedure 71111.15-05.

b. Findings

No findings of significance were identified.

1R19 Postmaintenance Testing (71111.19)

a. Inspection Scope

The inspectors reviewed the following postmaintenance activities to verify that

procedures and test activities were adequate to ensure system operability and functional

capability:

  • November 9, 2009, S6X (41 second load block relay for emergency diesel

generator B sequencer) loose terminal adjustments retested during Operating

Procedure OP-903-116

  • November 10, 2009, Removal, inspection, stroke test, and re-installment 3 plus

a safety injection sump outlet header B check valve SI-604B

  • November 17, 2009, Replacement of station battery 3-AB-S due to end of useful

life

- 16 - ENCLOSURE

shutdown cooling outside containment isolation valve SI-407B to correct

excessive leakage

  • November 30, 2009, Emergency feedwater pump AB operability check

(Operating Procedure OP-903-046)

  • December 7, 2009, Replacement of station battery 3-A-S due to end of useful life
  • December 9, 2009, Change setpoints and adjust limit stop setting on containment

vacuum relief differential pressure switch CVRIDPIS5220A

The inspectors selected these activities based upon the structure, system, or

component's ability to affect risk. The inspectors evaluated these activities for the

following (as applicable):

  • The effect of testing on the plant had been adequately addressed; testing was

adequate for the maintenance performed

  • Acceptance criteria were clear and demonstrated operational readiness; test

instrumentation was appropriate

The inspectors evaluated the activities against the technical specifications, the Updated

Final Safety Analysis Report, 10 CFR Part 50 requirements, licensee procedures, and

various NRC generic communications to ensure that the test results adequately ensured

that the equipment met the licensing basis and design requirements. In addition, the

inspectors reviewed corrective action documents associated with postmaintenance tests

to determine whether the licensee was identifying problems and entering them in the

corrective action program and that the problems were being corrected commensurate

with their importance to safety. Specific documents reviewed during this inspection are

listed in the attachment.

These activities constitute completion of seven postmaintenance testing inspection

samples as defined in Inspection Procedure 71111.19-05.

b. Findings

No findings of significance were identified.

1R20 Refueling and Other Outage Activities (71111.20)

a. Inspection Scope

The inspectors reviewed the outage safety plan and contingency plans for the Unit 3

refueling outage, conducted October 19, 2009, through December 4, 2009, to confirm

that licensee personnel had appropriately considered risk, industry experience, and

previous site-specific problems in developing and implementing a plan that assured

maintenance of defense-in-depth. During the refueling outage, the inspectors observed

portions of the shutdown and cooldown processes and monitored licensee controls over

the outage activities listed below.

- 17 - ENCLOSURE

  • Configuration management, including maintenance of defense-in-depth, is

commensurate with the outage safety plan for key safety functions and

compliance with the applicable technical specifications when taking equipment

out of service

  • Clearance activities, including confirmation that tags were properly hung and

equipment appropriately configured to safely support the work or testing

  • Installation and configuration of reactor coolant pressure, level, and temperature

instruments to provide accurate indication, accounting for instrument error

  • Status and configuration of electrical systems to ensure that technical

specifications and outage safety-plan requirements were met, and controls over

switchyard activities

  • Verification that outage work was not impacting the ability of the operators to

operate the spent fuel pool cooling system

alternative means for inventory addition, and controls to prevent inventory loss

  • Controls over activities that could affect reactivity
  • Refueling activities, including fuel handling and sipping to detect fuel assembly

leakage

  • Startup and ascension to full power operation, tracking of startup prerequisites,

walkdown of the primary containment to verify that debris had not been left which

could block emergency core cooling system suction strainers, and reactor

physics testing

  • Licensee identification and resolution of problems related to refueling outage

activities

  • Review of Operating Experience Smart Sample FY2007-03, crane and heavy lift

inspection

  • Review of Operating Experience Smart Sample FY2007-01, related to

Information Notice 2006-20

Specific documents reviewed during this inspection are listed in the attachment.

These activities constitute completion of one refueling outage and other outage

inspection sample as defined in Inspection Procedure 71111.20-05.

- 18 - ENCLOSURE

b. Findings

No findings of significance were identified.

1R22 Surveillance Testing (71111.22)

a. Inspection Scope

The inspectors reviewed the Updated Final Safety Analysis Report, procedure

requirements, and technical specifications to ensure that the two surveillance activities

listed below demonstrated that the systems, structures, and/or components tested were

capable of performing their intended safety functions. The inspectors either witnessed or

reviewed test data to verify that the significant surveillance test attributes were adequate

to address the following:

  • Preconditioning
  • Evaluation of testing impact on the plant
  • Acceptance criteria
  • Test equipment
  • Procedures
  • Jumper/lifted lead controls
  • Test data
  • Testing frequency and method demonstrated technical specification operability
  • Test equipment removal
  • Restoration of plant systems
  • Fulfillment of ASME Code requirements
  • Updating of performance indicator data
  • Engineering evaluations, root causes, and bases for returning tested systems,

structures, and components not meeting the test acceptance criteria were correct

  • Reference setting data

The inspectors also verified that licensee personnel identified and implemented any

needed corrective actions associated with the surveillance testing.

- 19 - ENCLOSURE

  • November 9, 2009, Train B integrated emergency diesel generator/engineering

safety features test (Operating Procedure OP-903-116)

outside containment isolation valve SI-407B

  • December 14, 2009, Annulus negative pressure valves ANP-101 and ANP-102

surveillance test (Operating Procedure OP-903-120)

Specific documents reviewed during this inspection are listed in the attachment.

These activities constitute completion of three surveillance testing inspection samples as

defined in Inspection Procedure 71111.22-05.

b. Findings

No findings of significance were identified.

Cornerstone: Emergency Preparedness

1EP4 Emergency Action Level and Emergency Plan Changes (71114.04)

.1 Inoffice Review, Revision 23

a. Inspection Scope

The inspector performed an in-office review of Emergency Plan Implementing Procedure

EP-001-001, Revision 23, Recognition and Classification of Emergency Conditions,

submitted August 19, 2009. This revision

  • Added information to emergency action level CU1 to clarify that steam generator

leakage is considered to be identified reactor coolant leakage

  • Added information to emergency action level RCB2 to clarify that manual

initiation of emergency core cooling systems to compensate for a steam

generator tube leak/rupture meets the intent of the emergency action level

  • Added information to emergency action level HU6 to clarify that entry conditions

are not met until hurricane force winds are projected for the site occurring in less

than or equal to twelve hours

This revision was compared to its previous revision, to the criteria of NUREG-0654,

Criteria for Preparation and Evaluation of Radiological Emergency Response Plans and

Preparedness in Support of Nuclear Power Plants, Revision 1, to Nuclear Energy

Institute Report 99-01, Emergency Action Level Methodology, Revision 5, and to the

standards in 10 CFR 50.47(b) to determine if the revision adequately implemented the

requirements of 10 CFR 50.54(q). This review was not documented in a safety

evaluation report and did not constitute approval of licensee-generated changes;

therefore, this revision is subject to future inspection.

- 20 - ENCLOSURE

These activities constitute completion of one sample as defined in Inspection

Procedure 71114.04-05.

b. Findings

No findings of significance were identified.

.2 Inoffice Review, Revision 24

a. Inspection Scope

The inspector performed an in-office review of the Waterford Steam Electric Station

Emergency Plan, Revision 38, and Emergency Plan Implementing

Procedure EP-001-001, Recognition and Classification of Emergency Conditions,

Revision 24, submitted October 23, 2009. These revisions

  • Deleted emergency action level CU4, fuel clad degradation
  • Changed the initiating conditions of Emergency Action Level SU9, Fuel Clad

Degradation, from greater than 1.0 µCi/g DEI or greater than 100 over E-Bar

µCi/g, to greater than 60 µCi/g DEI or greater than 1.0 µCi/g DEI for more than a

continuous 48 hour5.555556e-4 days <br />0.0133 hours <br />7.936508e-5 weeks <br />1.8264e-5 months <br /> period or greater than 100 over E-Bar µCi/g

  • Removed fuel clad degradation from the list of Unusual Event conditions on the

Emergency Plan Table 4-1, Summary of Initiating Conditions, and the index of

initiating conditions for cold shutdown conditions in Procedure EP-001-001

The NRC approved the licensees changes to emergency action levels CU4 and SU9 in

a Safety Evaluation Report and letter dated October 13, 2009 (Agency Document and

Management System Accession Number ML092600263).

These revisions were compared to the Safety Evaluation Report dated

October 13, 2009, to determine if the revisions adequately implemented the

requirements of 10 CFR 50.54(q).

These activities constitute completion of two samples as defined in Inspection

Procedure 71114.04-05.

b. Findings

No findings of significance were identified.

- 21 - ENCLOSURE

1EP6 Drill Evaluation (71114.06)

.1 Training Observations

a. Inspection Scope

The inspectors observed a training evolution for licensed operators on

December 21, 2009, which required emergency plan implementation by a licensee

operations crew. This evolution was planned to be evaluated and included in

performance indicator data regarding drill and exercise performance. The inspectors

reviewed the event scenarios and crew briefings for two scenarios. The inspectors

observed event classification and notification activities performed by the crew. The

inspectors also attended the postevolution critique for the scenario. The focus of the

inspectors activities was to note any weaknesses and deficiencies in the crews

performance and ensure that the licensee evaluators noted the same issues and entered

them into the corrective action program.

These activities constitute completion of one sample as defined in Inspection

Procedure 71114.06-05.

b. Findings

No findings of significance were identified.

2. RADIATION SAFETY

Cornerstone: Occupational and Public Radiation Safety

2OS1 Access Control to Radiologically Significant Areas (71121.01)

a. Inspection Scope

This area was inspected to assess licensee personnels performance in implementing

physical and administrative controls for airborne radioactivity areas, radiation areas, high

radiation areas, and worker adherence to these controls. The inspectors used the

requirements in 10 CFR Part 20, the technical specifications, and the licensees

procedures required by technical specifications as criteria for determining compliance.

During the inspection, the inspectors interviewed the radiation protection manager,

radiation protection supervisors, and radiation workers. The inspectors performed

independent radiation dose rate measurements and reviewed the following items:

  • Performance indicator events and associated documentation packages reported

by the licensee in the Occupational Radiation Safety Cornerstone

  • Controls (surveys, posting, and barricades) of radiation, high radiation, or

airborne radioactivity areas

- 22 - ENCLOSURE

  • Radiation work permits, procedures, engineering controls, and air sampler

locations

  • Conformity of electronic personal dosimeter alarm set points with survey

indications and plant policy; workers knowledge of required actions when their

electronic personnel dosimeter noticeably malfunctions or alarms

areas

  • Physical and programmatic controls for highly activated or contaminated

materials (non-fuel) stored within spent fuel and other storage pools

  • Self-assessments, audits, licensee event reports, and special reports related to

the access control program since the last inspection

  • Corrective action documents related to access controls
  • Licensee actions in cases of repetitive deficiencies or significant individual

deficiencies

  • Radiation work permit briefings and worker instructions
  • Adequacy of radiological controls, such as required surveys, radiation protection

job coverage, and contamination control during job performance

  • Dosimetry placement in high radiation work areas with significant dose rate

gradients

and very high radiation areas

  • Controls for special areas that have the potential to become very high radiation

areas during certain plant operations

  • Posting and locking of entrances to all accessible high dose rate - high radiation

areas and very high radiation areas

  • Radiation worker and radiation protection technician performance with respect to

radiation protection work requirements

Either because the conditions did not exist or an event had not occurred, no

opportunities were available to review the following items:

  • Adequacy of the licensees internal dose assessment for any actual internal

exposure greater than 50 millirem committed effective dose equivalent

- 23 - ENCLOSURE

Specific documents reviewed during this inspection are listed in the attachment.

These activities constitute completion of 21 of the required 21 samples as defined in

Inspection Procedure 71121.01-05.

b. Findings

Introduction. The inspectors reviewed a Green self-revealing, noncited violation of

Technical Specification 6.8.1 which resulted from a worker failing to follow radiation

protection procedures.

Description. On November 17, 2009, a contract radiation worker went to work near

steam generator 1 and received multiple electronic dosimeter dose rate alarms, but did

not leave the area until receiving a continuous dose alarm. In response, the licensee

investigated and found the worker indicated to radiation protection access control

personnel he would be going to the D-ring to work. The radiation protection technician

providing the radiological briefing showed the worker a map of reactor coolant pump 1A

and asked if that was where individual would be working. The worker acknowledged it

was, and the radiation protection technician used the survey map associated with

Radiation Work Permit 618, Task 1, Remove/Replace Insulation in the Reactor

Containment Building, to brief the worker on the radiological conditions. The worker

then signed onto Radiation Work Permit 618, Task 1, which provided a dose alarm

setpoint of 50 millirem and dose rate setpoint of 350 millirem per hour, and went to work

near steam generator 1, where dose rates were higher than the area for which the

worker was briefed. The licensee determined the worker entered a maximum dose rate

of 763 millirem per hour and received a dose of 50.8 millirem. Radiation protection

representatives stated the appropriate radiation work permit for the work area was

Radiation Work Permit 618, Task 2. Through examination of the electronic dosimeter

histogram, the licensee verified the worker received multiple dose rate alarms. The

worker mistakenly thought the dose rate alarms were generated by the workers

powered air purifying respirator signaling low air flow. Additional corrective actions were

being considered at the time of the inspection.

Analysis. The failure to follow radiation protection procedural requirements for entry into

the radiological controlled area was a performance deficiency. This finding is greater

than minor because it involved the program attribute of exposure control and affected

the cornerstone objective in that the failure of the worker to follow procedural guidance

resulted in the worker being unknowledgeable of the dose rates in all areas entered.

The inspectors used the Occupational Radiation Safety Significance Determination

Process and determined the finding had very low safety significance because it was not:

(1) an as low as reasonably achievable (ALARA) finding, (2) an overexposure,

(3) a substantial potential for overexposure, or (4) an inability to assess dose. The

finding had a crosscutting aspect in the area of human performance, work practices

component, because the worker failed to use human error prevention techniques such

as self and peer checking H.4.a].

- 24 - ENCLOSURE

Enforcement. Technical Specification 6.8.1 requires written procedures be established,

implemented, and maintained covering the applicable procedures recommended in

Appendix A of Regulatory Guide 1.33, Revision 2, February 1978. Appendix A lists

procedures for access control to radiation areas. Procedure EN-RP-100, Radworker

Expectations, Revision 3, Section 5.3[9], requires the radiation work permit to be read,

understood, and obeyed as a condition of radiologically controlled area access.

Section 5.4[3](h) requires the worker know where to properly perform his/her task.

Section 5.3[17] requires the worker be briefed and sign on the appropriate radiation work

permit. Section 5.3[11] requires the worker know the radiological conditions in the work

area. The contract worker violated these requirements when the worker did not know

where to perform his/her task, did not sign the appropriate radiation work permit and

task, and did not know the radiological conditions in the work area as evidenced by the

multiple electronic dosimeter dose rate alarms. Because this failure to follow radiation

protection procedural guidance when entering the radiological controlled area was of

very low safety significance and has been entered into the licensees corrective action

program in Condition Reports WF3-2009-05648 and WF3-2009-06852, this violation is

being treated as an noncited violation, consistent with Section VI.A of the NRC

Enforcement Policy: NCV 05000382/2009005-01; Failure to Follow Radiation

Protection Procedural Requirements.

2OS2 ALARA Planning and Controls (71121.02)

a. Inspection Scope

The inspectors assessed licensee personnels performance with respect to maintaining

individual and collective radiation exposures as low as is reasonably achievable. The

inspectors used the requirements in 10 CFR Part 20 and the licensees procedures

required by technical specifications as criteria for determining compliance. The

inspectors interviewed licensee personnel and reviewed the following:

  • Integration of ALARA requirements into work procedure and radiation work

permit (or radiation exposure permit) documents

  • Shielding requests and dose/benefit analyses
  • Use of engineering controls to achieve dose reductions and dose reduction

benefits afforded by shielding

  • Workers use of the low dose waiting areas
  • Radiation worker and radiation protection technician performance during work

activities in radiation areas, airborne radioactivity areas, or high radiation areas

  • Corrective action documents related to the ALARA program and follow-up

activities, such as initial problem identification, characterization, and tracking

Specific documents reviewed during this inspection are listed in the attachment.

- 25 - ENCLOSURE

These activities constitute completion of two of the required 15 samples and four of the

optional samples as defined in Inspection Procedure 71121.02-05.

b. Findings

No findings of significance were identified.

4. OTHER ACTIVITIES

4OA1 Performance Indicator Verification (71151)

.1 Data Submission Issue

a. Inspection Scope

The inspectors performed a review of the data submitted by the licensee for the third

quarter 2009 performance indicators for any obvious inconsistencies prior to its public

release in accordance with Inspection Manual Chapter 0608, Performance Indicator

Program.

This review was performed as part of the inspectors normal plant status activities and,

as such, did not constitute a separate inspection sample.

b. Findings

No findings of significance were identified.

.2 Reactor Coolant System Specific Activity

a. Inspection Scope

The inspectors sampled licensee submittals for the reactor coolant system specific

activity performance indicator for the period from the third quarter 2008 through the third

quarter 2009. To determine the accuracy of the performance indicator data reported

during those periods, the inspectors used definitions and guidance contained in NEI

Document 99-02, Regulatory Assessment Performance Indicator Guideline, Revision 5.

The inspectors reviewed the licensees reactor coolant system chemistry samples,

technical specification requirements, issue reports, event reports, and NRC integrated

inspection reports for the period of the third quarter 2008 through the third quarter 2009

to validate the accuracy of the submittals. The inspectors also reviewed the licensees

issue report database to determine if any problems had been identified with the

performance indicator data collected or transmitted for this indicator and none were

identified. In addition to record reviews, the inspectors observed a chemistry technician

obtain and analyze a reactor coolant system sample. Specific documents reviewed are

described in the attachment to this report.

These activities constitute completion of one reactor coolant system specific activity

sample as defined in Inspection Procedure 71151-05.

- 26 - ENCLOSURE

b. Findings

No findings of significance were identified.

.3 Reactor Coolant System Leakage

a. Inspection Scope

The inspectors sampled licensee submittals for the reactor coolant system leakage

performance indicator for the period from the third quarter 2008 through the third quarter

2009. To determine the accuracy of the performance indicator data reported during

those periods, the inspectors used definitions and guidance contained in NEI Document

99-02, Regulatory Assessment Performance Indicator Guideline, Revision 5. The

inspectors reviewed the licensees operator logs, reactor coolant system leakage

tracking data, issue reports, event reports, and NRC integrated inspection reports for the

period of the third quarter 2008 through the third quarter 2009 to validate the accuracy of

the submittals. The inspectors also reviewed the licensees issue report database to

determine if any problems had been identified with the performance indicator data

collected or transmitted for this indicator and none were identified. Specific documents

reviewed are described in the attachment to this report

These activities constitute completion of one reactor coolant system leakage sample as

defined in Inspection Procedure 71151-05.

b. Findings

No findings of significance were identified.

.16 Occupational Exposure Control Effectiveness (OR01)

a. Inspection Scope

The inspectors sampled licensee submittals for the Occupational Radiological

Occurrences performance indicator for the third quarter 2009. To determine the

accuracy of the performance indicator data reported during those periods, performance

indicator definitions and guidance contained in NEI Document 99-02, Regulatory

Assessment Performance Indicator Guideline, Revision 5, was used. The inspectors

reviewed the licensees assessment of the performance indicator for occupational

radiation safety to determine if indicator related data was adequately assessed and

reported. To assess the adequacy of the licensees performance indicator data

collection and analyses, the inspectors discussed with radiation protection staff, the

scope and breadth of its data review, and the results of those reviews. The inspectors

independently reviewed electronic dosimetry dose rate and accumulated dose alarm and

dose reports and the dose assignments for any intakes that occurred during the time

period reviewed to determine if there were potentially unrecognized occurrences. The

inspectors also conducted walkdowns of numerous locked high and very high radiation

area entrances to determine the adequacy of the controls in place for these areas.

- 27 - ENCLOSURE

These activities constitute completion of the occupational radiological occurrences

sample as defined in Inspection Procedure 71151-05.

b. Findings

No findings of significance were identified.

.17 Radiological Effluent Technical Specifications/Offsite Dose Calculation Manual

Radiological Effluent Occurrences (PR01)

a. Inspection Scope

The inspectors sampled licensee submittals for the Radiological Effluent Technical

Specifications/Offsite Dose Calculation Manual Radiological Effluent Occurrences

performance indicator for the third quarter 2009. To determine the accuracy of the

performance indicator data reported during those periods, performance indicator

definitions and guidance contained in NEI Document 99-02, Regulatory Assessment

Performance Indicator Guideline, Revision 5, was used. The inspectors reviewed the

licensees issue report database and selected individual reports generated since this

indicator was last reviewed to identify any potential occurrences such as unmonitored,

uncontrolled, or improperly calculated effluent releases that may have impacted offsite

dose.

These activities constitute completion of the radiological effluent technical

specifications/offsite dose calculation manual radiological effluent occurrences sample

as defined in Inspection Procedure 71151-05.

b. Findings

No findings of significance were identified.

4OA2 Identification and Resolution of Problems (71152)

Cornerstones: Initiating Events, Mitigating Systems, Barrier Integrity, Emergency

Preparedness, Public Radiation Safety, Occupational Radiation Safety, and

Physical Protection

.1 Routine Review of Identification and Resolution of Problems

a. Inspection Scope

As part of the various baseline inspection procedures discussed in previous sections of

this report, the inspectors routinely reviewed issues during baseline inspection activities

and plant status reviews to verify that they were being entered into the licensees

corrective action program at an appropriate threshold, that adequate attention was being

given to timely corrective actions, and that adverse trends were identified and

addressed. The inspectors reviewed attributes that included the complete and accurate

identification of the problem; the timely correction, commensurate with the safety

- 28 - ENCLOSURE

significance; the evaluation and disposition of performance issues, generic implications,

common causes, contributing factors, root causes, extent of condition reviews, and

previous occurrences reviews; and the classification, prioritization, focus, and timeliness

of corrective. Minor issues entered into the licensees corrective action program

because of the inspectors observations are included in the attached list of documents

reviewed.

These routine reviews for the identification and resolution of problems did not constitute

any additional inspection samples. Instead, by procedure, they were considered an

integral part of the inspections performed during the quarter and documented in

Section 1 of this report.

b. Findings

No findings of significance were identified.

.2 Daily Corrective Action Program Reviews

a. Inspection Scope

In order to assist with the identification of repetitive equipment failures and specific

human performance issues for follow-up, the inspectors performed a daily screening of

items entered into the licensees corrective action program. The inspectors

accomplished this through review of the stations daily corrective action documents.

The inspectors performed these daily reviews as part of their daily plant status

monitoring activities and, as such, did not constitute any separate inspection samples.

b. Findings

No findings of significance were identified.

.3 Selected Issue Follow-up Inspection

a. Inspection Scope

During a review of items entered in the licensees corrective action program, the

inspectors reviewed conditions surrounding reactor coolant system leakage and boric

acid corrosion related to reactor coolant pumps. The inspectors considered the following

during the review of the licensees actions: (1) complete and accurate identification of

problems in a timely manner; (2) evaluation and disposition of operability/reportability

issues; (3) consideration of extent of condition, generic implications, common cause, and

previous occurrences; (4) classification and prioritization of the resolution of the problem;

(5) identification of root and contributing causes of the problem; (6) identification of

corrective actions; and (7) completion of corrective actions in a timely manner.

These activities constitute completion of one in-depth problem identification and

resolution sample as defined in Inspection Procedure 71152-05.

- 29 - ENCLOSURE

b. Findings

i. Introduction. A self-revealing Green noncited violation of 10 CFR Part 50,

Appendix B, Criterion XVI, was identified for the licensees failure to promptly correct

a condition adverse to quality. Specifically, the licensee did not promptly correct

reactor coolant pump vapor seal leakage that resulted in boric acid accumulation on

the component cooling water heat exchanger and cover areas of three reactor

coolant pumps. Corrective actions for this condition were implemented during

Refueling Outage 15, but these corrective actions failed to correct the condition and

the vapor seal leakage continued through Operating Cycle 16. This resulted in some

additional boric acid corrosion and degradation to reactor coolant pump covers and

carbon steel component cooling water flanges.

Description. The reactor coolant pumps are designed to direct vapor stage seal

leakage to the reactor drain tank via installed piping which includes a check valve to

prevent back flow from the drain line to the vapor seal. For several cycles, the

licensee has recognized that vapor stage seal leakage has not been draining to the

reactor drain tank as designed but has instead been backing up in the line and

spilling into the pump shroud region. It was theorized that this failure of the vapor

stage leakage to flow to the reactor drain tank was due to the normally positive

pressure in the reactor drain tank and that a design change was needed. During

Refueling Outage 15, the licensee implemented Engineering Change EC-6256 to

redirect all reactor coolant pump vapor seal leakage flow to a floor drain instead of

the reactor drain tank. However, the design change did not consider the flow

restriction effects of an existing check valve in each of the reactor coolant pump

vapor stage leakage piping, and made the modification downstream of each of those

existing check valves such that vapor stage leakage no longer faced the back

pressure from the reactor drain tank, but still had to pass through the existing check

valves in order to reach the target floor drain.

The postmaintenance test prescribed by Engineering Change EC-6256 to verify flow

through the modified vapor stage leakage piping from the seal, through the leak-off

piping (including the installed check valve) to the floor drain was not implemented as

specified. Instead, because of schedule and resource impacts (it would have been

difficult, resource intensive, and intrusive to conduct the test as prescribed), a

substitute postmaintenance test was performed that only verified flow through the

portion of the piping that was modified. This meant that the postmaintenance test did

not verify that water would actually flow from the vapor stage seal, through the

existing check valves, through the new piping modification and into the floor drain.

Operating Cycle 16 proceeded following Refueling Outage 15 with the newly

modified and inadequately tested vapor stage leakage line in operation. At the

conclusion of Operating Cycle 16, Mode 3 walkdowns at the beginning of Refueling

Outage 16 identified more boric acid accumulation on three of four reactor coolant

pumps, indicating continued reactor coolant pump vapor stage leakage out onto the

heat exchanger and pump cover. The licensees root cause analysis determined that

Engineering Change EC-6256 was ineffective. A test similar to the postmaintenance

test originally prescribed by Engineering Change EC-6256 was performed on reactor

- 30 - ENCLOSURE

coolant pump 2B (which had experienced the most boric acid accumulation) and it

identified that the installed check valve RC-511B was incapable of passing flow as

intended by design. The valve was a 3/4 Velan spring loaded check valve in which

the pressure required to overcome the spring load was more than the static head of

water between the vapor stage seal and the check valve could develop. Both the

original design and the subsequent design modification implemented by Engineering

Change EC-6256 were incapable of passing flow as intended by design because the

vapor stage leakage line between the seal and the check valve could not develop

enough static head to lift the check valve before backing up and spilling over onto the

pump heat exchanger and cover. If the postmaintenance test prescribed by

Engineering Change EC-6256 had been implemented as prescribed during Refueling

Outage 15, this design flaw associated with the check valve would have been

detected and the design could have been modified to correct this condition at that

time. However, because that postmaintenance test was not properly implemented,

the condition adverse to quality (the vapor stage leakage onto the reactor coolant

pump heat exchanger and pump cover and associated boric acid accumulation and

associated corrosion) continued to exist for another operating cycle.

Analysis. The licensees failure to promptly correct a condition adverse to quality is a

performance deficiency. The finding is more than minor because it is associated with

the equipment performance attribute of the Initiating Events Cornerstone and affects

the cornerstone objective to limit the likelihood of those events that upset plant

stability. Using the Manual Chapter 0609, Attachment 4, Phase 1 screening

worksheet, the issue screened as having very low safety significance because,

although the finding contributes to the likelihood of a reactor trip, mitigation

equipment is still available. This finding had a crosscutting aspect in the area of

human performance associated with work control in that the licensee did not

effectively plan for the resources necessary to implement the postmaintenance

testing per Engineering Change EC 6256 H.3(a).

Enforcement. Title10 CFR Part 50, Appendix B, Criterion XVI, requires, in part, that

measures shall be established to assure that conditions adverse to quality are

promptly identified and corrected. Contrary to the above, the licensee failed to

promptly correct a condition adverse to quality. Specifically, the licensee failed to

correct the reactor coolant pump vapor seal leakage with the corrective actions it

implemented during Refueling Outage 15 (ending May 31, 2008), and the vapor seal

leakage continued through operating cycle 16 until corrected during Refueling

Outage 16 (ending December 4, 2009). Because this finding was of very low safety

significance and has been entered into the licensees corrective action program as

Condition Report CR-WF3-2009-5501, it is being treated as a noncited violation

consistent with Section VI.A.1 of the NRC Enforcement Policy:

NCV 05000382/2009005-02, Reactor Coolant Pump Vapor Seal Leakage.

ii. Introduction: A self-revealing Green noncited violation of 10 CFR Part 50,

Appendix B, Criterion V, was identified for the licensees failure to prescribe an

activity affecting quality by documented instructions, procedures, or drawings

appropriate to the circumstance. Specifically, for all reactor coolant pump heat

exchanger to pump cover bolted connection gasket replacements between the

- 31 - ENCLOSURE

refueling outage of 1986 (Refueling Outage 1) and the refueling outage of 2009

(Refueling Outage 16), the licensee prescribed the wrong gasket material, gasket

size, and fastener preload because they had failed to incorporate a design change

implemented during Refueling Outage 1 into their instructions, procedures, or

drawings. Station Modification Package SMP-1427, an engineering change

implemented during Refueling Outage 1 in response to industry operating

experience, called for a thicker gasket, different gasket material, and an increased

bolt preload in order to increase gasket compression and reduce the probability of

leakage. As a consequence of failing to incorporate Station Modification

Package SMP-1427 changes into procedures, all heat exchanger gasket

replacements since Refueling Outage 1, four gasket replacements in total, have

utilized thinner gaskets with less than the vendor recommended compression.

Description. After the licensees first operating cycle, industry operating experience

indicated that the reactor coolant pump heat exchanger to pump cover bolted

connection had a high probability of leakage as designed and warranted a design

modification to increase gasket compression to reduce the likelihood of reactor

coolant leakage at that interface. As a result, the licensee implemented a design

modification, Station Modification Package SMP-1427, to change the required

gasket material from stainless steel/asbestos to inconel/grafoil, to change the gasket

thickness from 0.125 inches to 0.135 inches, and to change the fastening method

from 2200-foot pounds of torque (roughly equivalent to 30 ksi tensioned) to 38.7 ksi

tensioned.

All four reactor coolant pump bolted connections were modified to the new gaskets

and fastening method as prescribed in Station Modification Package SMP-1427.

However, Technical document TD-B580.0025 was not updated with the design

change at that time. As a result, all gasket replacements conducted between

Refueling Outage 1 and Refueling Outage 16 were accomplished in accordance with

the outdated and inadequate specifications that remained in TD-B580.0025. The

result was that, by the beginning of Refueling Outage 16, only reactor coolant

pump RCP-1B still retained the modifications prescribed by Station Modification

Package SMP-1427 and implemented in Refueling Outage 1.

It is noteworthy that the inspection of reactor coolant pump 1A during the midcycle

outage on October 9, 2007, identified a sizable quantity of boric acid crystals

contained in the pump shroud. The root cause analysis concluded that the boric

acid accumulation was primarily due to leakage past the reactor coolant pump heat

exchanger to pump cover gasket. However, the root cause analysis for this leakage

did not identify that operating experience associated with leakage past these gaskets

had caused the licensee to implement Station Modification Package SMP-1427 in

Refueling Outage 1, and neither did the root cause analysis identify that the thicker

gasket and modified fastening method were needed to achieve the vendors

recommended compression. Therefore, the gasket replacement on reactor coolant

pump RCP-1A was not performed in accordance with Station Modification

Package SMP-1427. In addition, it is noteworthy that boric acid accumulation

discovered on reactor coolant pump RCP-2B on October 20, 2009, prompted

another root cause analysis by the licensee which concluded that leakage past the

- 32 - ENCLOSURE

heat exchanger to pump cover gasket may have been a possible cause of a portion

of that boric acid accumulation. The root cause analysis performed in 2007 for

reactor coolant pump RCP-1A was a missed opportunity to identify the licensees

past failure to include the Station Modification Package SMP-1427 design

modifications into plant procedures. Had that opportunity not been missed, it is

postulated that the inadequate gasket and fastener configuration on reactor coolant

pump RCP-2B may have been identified and corrected before the discovery of

significant boric acid accumulation on it during Operating Cycle 16, which may have

reduced the accumulation of boric acid on that pump.

Analysis. The licensees failure to prescribe appropriate gasket replacement

requirements in instructions, procedures, or drawings is a performance deficiency.

The finding is more than minor because it is associated with the equipment

performance attribute of the Initiating Events Cornerstone and affects the

cornerstone objective to limit the likelihood of those events that upset plant stability.

Using the Manual Chapter 0609, Attachment 4, Phase 1 screening worksheet, the

issue screened as having very low safety significance because, although the finding

contributes to the likelihood of a reactor trip, mitigation equipment is still available.

This finding had a crosscutting aspect in the area of problem identification and

resolution associated with operating experience in that the licensee did not

institutionalize operating experience through changes to the station procedures

P.2(b).

Enforcement. Title10 CFR Part 50, Appendix B, Criterion V, requires that activities

affecting quality shall be prescribed by documented instructions, procedures, or

drawings, of a type appropriate to the circumstances. Contrary to the above, the

licensee failed to prescribe an activity affecting quality by instructions, procedures, or

drawings, of a type appropriate to the circumstances. Specifically, for all reactor

coolant pump heat exchanger to pump cover bolted connection gasket replacements

between the refueling outage of 1986 (Refueling Outage 1) and the refueling outage

of 2009 (Refueling Outage 16), the licensee prescribed the wrong gasket material,

gasket size, and fastener preload because they had failed to incorporate a design

change implemented during Refueling Outage 1 into their instructions, procedures,

or drawings. Because this finding was of very low safety significance and has been

entered into the licensees corrective action program as Condition

Report CR-WF3-2009-5501, it is being treated as a noncited violation consistent with

Section VI.A.1 of the NRC Enforcement Policy: NCV 05000382/2009005-03,

Failure to Update Drawings after Design Change.

4OA5 Other Activities

.1 Temporary Instruction 2515-172, Reactor Coolant System Dissimilar Metal Butt Welds

a. Inspection Scope

The reactor coolant system for this unit is carbon steel with stainless steel cladding and

has the following dissimilar metal welds subject to the requirements of the Materials

Reliability Program 139:

- 33 - ENCLOSURE

1. One 12-inch pressurizer surge line nozzle was mitigated during a previous

outage using a weld overlay process. The weld was classified as Category F per

materials reliability program guidelines.

2. Three 6-inch pressurizer safety nozzles were mitigated during a previous outage

using a weld overlay process. The welds were classified as Category F per

materials reliability program guidelines.

3. One 4-inch pressurizer spray nozzle was mitigated during a previous outage

using a weld overlay process. The weld was classified as Category F per

materials reliability program guidelines.

4. Two 14-inch hot leg shutdown cooling nozzles were mitigated during a previous

outage using a weld overlay process. The welds were classified as Category F

per materials reliability program guidelines.

5. One 12-inch hot leg surge nozzle was mitigated during a previous outage using a

weld overlay process. The weld was classified as Category F per materials

reliability program guidelines.

6. One 2-inch hot leg drain nozzle was mitigated during a previous outage using a

weld overlay process. The weld was classified as Category F per materials

reliability program guidelines.

7. Four 12-inch safety injection nozzles were previously left unmitigated. The

licensee performed a volumetric inspection of each nozzle during the current

outage and classified the welds as Category E per materials reliability program

guidelines.

8. Four 30-inch reactor coolant pump suction piping (unmitigated as of this outage).

The licensee performed a volumetric inspection of each pipe during the current

outage and classified the welds as Category E per materials reliability program

guidelines.

9. Four 30-inch reactor coolant pump discharge piping (unmitigated as of this

outage). The licensee performed a volumetric inspection of each pipe during the

current outage and classified the welds as Category E per materials reliability

program guidelines.

All of the pressurizer and hot-leg welds have been mitigated, in previous outages, using

a full-structural overlay weld. The cold-leg-temperature welds have not been mitigated

as of this outage. The cold-leg welds have been volumetrically inspected and any

decision to mitigate these welds will be made on the basis of these and/or future

inspections.

- 34 - ENCLOSURE

03.01 Licensees Implementation of the Materials Reliability Program (MRP-139) Baseline

Inspections

a. The inspector reviewed records of structural weld overlays and nondestructive

examination activities associated with the licensees hot leg surge nozzles

structural weld overlay mitigation effort.

b. The licensee was not planning to take any deviations from the baseline

inspection requirements of Materials Reliability Program MRP-139, and all other

applicable dissimilar metal butt welds were scheduled in accordance with

Materials Reliability Program MRP-139 guidelines.

03.02 Volumetric Examinations

a. The inspector observed the phased array ultrasonic examination of two cold leg

welds that were not scheduled to be overlaid. This examination was conducted

in accordance with ASME Code,Section XI, Supplement VIII Performance

Demonstration Initiative requirements regarding personnel, procedures, and

equipment qualifications. No relevant conditions were identified during this

examination.

b. The inspector reviewed records for the nondestructive evaluations performed on

the hot leg surge nozzle weld overlay. Inspection coverage met the requirements

of Materials Reliability Program MRP-139 and no relevant conditions were

identified.

c. The certification records of ultrasonic examination personnel were reviewed for

those personnel that performed the examinations of the cold-leg welds. All

personnel records showed that they were qualified under the EPRI Performance

Demonstration Initiative.

d. No deficiencies were identified during the nondestructive examinations.

03.03 Weld Overlays

a. The inspector reviewed the welding activities associated with the weld overlay

performed on the hot leg surge nozzle.

b. The licensee submitted and received NRC authorization for the use of relief

request from the ASME code to apply weld overlays on their dissimilar metal butt

welds. Using this, the licensee performed weld overlays on all of the dissimilar

metal butt welds associated with pressurizer and hot leg temperatures. This

welding took place in previous outages. The inspector reviewed the weld records

for one of these welds to ensure the welding was performed in accordance with

the ASME code as modified by the approved relief requests.

c. No deficiencies were identified in the completed full structural weld overlays.

- 35 - ENCLOSURE

03.04 Mechanical Stress Improvement

This item was not applicable because the licensee did not have plans to employ a

mechanical stress improvement process.

03.05 Inservice Inspection Program

The inspector reviewed the licensees risk informed inservice plan and verified that all

dissimilar metal butt welds have been entered into the plan and will be examined on a

schedule consistent with Materials Reliability Program MRP-139.

b. Findings

No findings of significance were identified.

4OA6 Meetings

Exit Meeting Summary

On October 1, 2009, the inspector conducted a telephonic exit meeting to present the results of

the in-office inspection of changes to the Waterford Steam Electric Station, Unit 3s, emergency

action levels to Mr. J. Lewis, Manager, Emergency Preparedness. He acknowledged the issues

presented. The inspector asked whether any materials examined during the inspection should

be considered proprietary. No proprietary information was identified

On November 9, 2009, the inspector conducted a telephonic exit meeting to present the results

of the in-office inspection of changes to the Waterford Steam Electric Station, Unit 3, emergency

plan and emergency action levels to Mr. R. Perry, Acting Emergency Preparedness Manager.

He acknowledged the issues presented. The inspector asked whether any materials examined

during the inspection should be considered proprietary. No proprietary information was

identified.

On November 13, 2009, the inspectors presented the results of the inservice inspection to you

and other members of your staff. You acknowledged the issues presented. The inspectors

returned proprietary material examined during the inspection.

On November 20, 2009, the inspectors presented the inspection results to Mr. C. Arnone,

General Manager, Plant Operations, and other members of your staff. They acknowledged the

issues presented. The inspector asked whether any materials examined during the inspection

should be considered proprietary. No proprietary information was identified.

On January 11, 2010, the inspectors presented the quarterly inspection results to you and other

members of your staff. You acknowledged the issues presented. The inspectors asked whether

any materials examined during the inspection should be considered proprietary. No proprietary

information was identified.

- 36 - ENCLOSURE

4OA7 Licensee-Identified Violations

The following violations of very low safety significance (Green) were identified by the licensee

and are violations of NRC requirements which meet the criteria of Section VI of the NRC

Enforcement Policy, NUREG-1600, for being dispositioned as noncited violations.

Technical Specification 6.8.1 requires written procedures be established, implemented, and

maintained covering the applicable procedures recommended in Appendix A of Regulatory

Guide 1.33, Revision 2, February 1978. Appendix A lists procedures for access control to

radiation areas. Procedure EN-RP-100, Radworker Expectations, Revision 3, Section 5.3[9]

requires the radiation work permit to be read, understood, and obeyed as a condition of

radiologically controlled area access. Procedure EN-RP-100, Radworker Expectations,

Revision 3, Section 5.4[3](h) requires the worker know where to properly perform his/her task.

Section 5.3[17] requires the worker be briefed and sign on the appropriate radiation work permit.

Section 5.3[11] requires the worker know the radiological conditions in the work area. The

licensee identified an example of a worker entering a high radiation area using an inappropriate

radiation work permit and without knowing the dose rates in the area. On October 24, 2009, a

security officer entered shutdown heat exchanger Room B and received an electronic dosimeter

dose rate alarm. The room was posted as a high radiation area and dose rates within the area

were as high as 140 millirem per hour. The officer entered the radiological controlled area using

Radiation Work Permit 2009005, Tours and Inspection in All Radiological Controlled Areas,

Except High Radiation Areas, Locked High Radiation Areas, Very High Radiation Areas, and the

Reactor Containment Building. Because the radiation work permit did not allow entry into high

radiation areas, radiation protection personnel did not anticipate the officer would enter the room

and did not brief the officer on the dose rates in the area. In response, the licensee conducted a

human performance error review and counseled the officer. This finding was of very low safety

significance because it did not involve an actual or substantial potential of an overexposure.

This finding was entered into the licensees corrective action program as Condition

Report CR-WF3-2009-05648.

- 37 - ENCLOSURE

SUPPLEMENTAL INFORMATION

KEY POINTS OF CONTACT

Licensee Personnel

C. Arnone, General Manager Plant Operations

D. Bauman, Senior Project Manager

M. Bratton, Manager, Senior Lead Technical Specialist

J. Brawley, ALARA Supervisor, Radiation Protection

B. Celeste, Lead Level III, Contractor, C&S Engineers, Inc.

K. Cook, Acting General Manager Plant Operations

L. Dauzat, Supervisor, Radiation Protection

D. Dufrene; Technician, Radiation Protection

G. Ferguson, PE, IWE Examination

J. Gobell, Project Manager

J. Houghtaling, Senior Project Manager

C. Hunsaker, Technical Specialist II

J. Kowalewski, Vice President, Operations

J. Lewis, Manager, Emergency Preparedness

R. Luter, Technical Specialist IV

M. Mason, Engineer, Licensing

R. McGaha, Technical Specialist II

M. Mason, Engineer, Licensing

R. Murillo, Manager, Licensing

K. Nichols, Director, Engineering

R. OQuinn, Senior Staff Engineer

C. Pickering, Supervisor, Mechanical Maintenance

B. Piluti, Manager, Radiation Protection

J. Polluck, Engineer, Licensing

R. Redmond, Technical Specialist, Boric Acid Corrosion Control Program

W. Sims, Manager, Major Projects I

B. Williams, Technical Specialist IV

R. Williams, ASME Section XI/ISI Senior Lead

NRC Personnel

M. Haire, Senior Resident Inspector

D. Overland, Resident Inspector

LIST OF ITEMS OPENED, CLOSED, AND DISCUSSED

Opened and Closed

Failure to follow radiation protection procedural

05000382/2009005-01 NCV

requirements05000382/2009005-02 NCV Reactor Coolant Pump Vapor Seal Leakage

A-1 Attachment

Opened and Closed

Failure to follow radiation protection procedural

05000382/2009005-01 NCV

requirements05000382/2009005-02 NCV Reactor Coolant Pump Vapor Seal Leakage

05000382/2009005-03 NCV Failure to Update Drawings after Design Change

LIST OF DOCUMENTS REVIEWED

Section 1R01: Adverse Weather Protection

PROCEDURES/DOCUMENTS

NUMBER TITLE REVISION

WSES-FSAR- Final Safety Analysis Report - Section 2.4, Hydrologic 10

UNIT-3 Engineering

OP-901-521 Off-Normal Procedure for Severe Weather and Flooding 301

Section 1R04: Equipment Alignment

PROCEDURES/DOCUMENTS

NUMBER TITLE REVISION /

DATE

OP-002-004 Chilled Water System 303

OP-903-063 Chilled Water Pump Operability Verification 302

SD-CHW Essential Chilled Water System Description 6

G853 Sheet 3 Chilled Water flow Diagram SH-1 December 4,

1975

SD-SI Safety Injection System Description 13

OP-009-008 Safety Injection System Operating Procedure 26

A-2 Attachment

Section 1R05: Fire Protection

PROCEDURES/DOCUMENTS

NUMBER TITLE REVISION

OP-009-004 Fire Protection 305

MM-004-424 Building Fire Hose Station Inspection and Hose 10

Replacement

MM-007-010 Fire Extinguisher Inspection and Extinguisher Replacement 302

FP-001-014 Duties of a Fire Watch 14

FP-001-015 Fire Protection Impairments 302

DBD-018 Appendix R/Fire Protection

FP-001-015 Fire Protection Impairments 302

FP-001-018 Pre-fire Plan Strategies, Development, And Revision 300

UNT-007-006 Housekeeping 301

EN-DC-161 Control of Combustibles 003

UNT-007-060 Control of Loose Items 302

UNT-005-013 Fire Protection Program 010

SD-FP Fire Protection System Description 2

Section 1R06: Flood Protection Measures

CONDITION REPORTS

CR-WF3-2005-03338 CR-WF3-1996-00930 CR-WF3-2009-3925

PROCEDURE/DOCUMENTS

NUMBER TITLE REVISION /

DATE

WSES-FSAR- February

Appendix 3.6A Pipe Rupture Analysis

UNIT-3 2002

WSES-FSAR- February

Water Level (Flood) Design

UNIT-3 2002

WSES-FSAR-

System Description Plant Sumps 6

UNIT-3

OP-901-521 Severe Weather and Flooding 301

G-349 Yard Duct Runs and Outdoor Lighting Drawing 18

A-3 Attachment

Section 1R07: Heat Sink Performance

PROCEDURES/DOCUMENTS

NUMBER TITLE DATE

NOECP-257 Steam Generator Secondary Side Inspections 4

LTR-SGDA-08-129 Acceptability of Loose Batwing Section found in the May 12, 2008

Upper Central Stay Cavity Region during RF15

LTR-SGDA-09-189 Acceptability of SG Operation As a Result of an November 16,

Unattached Steam Vent and Observed Feedwater Ring 2009

Erosion

LTR-SGDA-09-188 Acceptance Criteria for Waterford Feedwater November 13,

Discharge Elbows 2009

Section 1RO8: Inservice Inspection Activities

DOCUMENTS/PROCEDURES/REPORTS

NUMBER TITLE REVISION / DATE

EN-DC-317 Entergy Steam Generator Administrative 4

Procedure

NOECP-257 Steam Generator Secondary Side Inspection 4

NOECP-252 Steam Generator Eddy Current Inspection 11

Testing

CEP-NDE-0955 Alloy 600 Visual Examination (VE) of 301

Bare-Metal Surfaces

EN-DC-319 Inspection and Evaluation of Boric Acid Leaks 4

NOECP-107 Boric Acid corrosion Control Program 3

WF3-CHEM-SEC-001- Strategic Secondary Water Chemistry Plan 6

06

WDI-PJF-1304321- Waterford 3 - RF16 - Reactor Vessel Head 0

FSR-001 Penetration Inspection Final Report.

WDI-SSP-1002 Reactor Vessel Head Penetration Inspection 3

Tool Operation for ANO 2 and Waterford 3 -

ROSA

WCAL-002 Pulser/Receiver Linearity Procedure 10

WDI-ET-003 IntraSpect Eddy Current Imaging Procedure 14

for Inspection of Reactor Vessel Head

Penetrations

WDI-ET-004 IntraSpect Eddy Current Analysis Guidelines 14

A-4 Attachment

Section 1R07: Heat Sink Performance

PROCEDURES/DOCUMENTS

NUMBER TITLE DATE

WDI-STD-1040 IntraSpect Ultrasonic Procedure for Inspection 2

of Reactor Vessel Head Penetrations, Time of

Flight Ultrasonic, Longitudinal Wave and

Shear Wave

WDI-STD-1041 IntraSpect UT Analysis Guidelines 1

WDI-STD-101 RVHI Vent Tube J-Weld Eddy Current 8

Examination

WDI-STD-114 RVHI Vent Tube ID & CS Wastage Eddy 10

Current Examination

CEP-NDE-0404 Manual Ultrasonic Examination of Ferritic 4

Piping Welds (ASME XI)

ISI-UT-09-019 UT Calibration/Examination (WO 157687) - October 31, 2009

RCS Cold Leg Loop 1A - Weld No.07-005

L-09-006 Ultrasonic Instrument Linearity - Krautkramer October 22, 2009

USN 60 SW (Serial No. 01VNCT); Transducer

Frequency 4.0 MHz (Serial No. 5746222529);

Calibration Standard (Serial No. 9634);

Couplant - Ultragel II (Batch No. 06225)

ISI-VT-09-194 Visual Examination for Boric Acid Detection October 27, 2009

(WO 159119) - RCS Loop 1A Cold Leg -

Weld No.07-002

MRP-139 Material Reliability Program: Primary System 1

Piping Butt Weld Inspection and Evaluation

Guideline

CEP-NDE-0901 VT-1 Examination 4

CEP-NDE-0902 VT-2 Examination 7

CEP-NDE-0903 VT-3 Examination 5

SI-UT-130 Procedure for the Phased Array Ultrasonic 3

Examination of Dissimilar Metal Welds

SI-NDE-06 Calibration of Ultrasonic NDE Equipment 4

SI-NDE-08 Qualification and Certification of NDE 1

Personnel for Nuclear Applications

WF3 11-002 RCP 2A Structural Integrity Associates - Phased Array October 30, 2009

Suction Nozzle Ultrasonic Examination Record Data Sheet for

Weld No. 11-002: Reactor Coolant Pump 2A

Cold Leg Suction Nozzle

A-5 Attachment

Section 1R07: Heat Sink Performance

PROCEDURES/DOCUMENTS

NUMBER TITLE DATE

WF3 11-002 RCP 2A Structural Integrity Associates - Ultrasonic October 30, 2009

Suction AX SH Phased Array Calibration Record for Weld

No. 11-002: Reactor Coolant Pump Suction

Nozzle Dissimilar Metal Weld - Wedge

Angle 36.2o (Axial Scan)

WF3 11-002 RCP 2A Structural Integrity Associates - Ultrasonic October 30, 2009

Suction Circ - 10 RL Phased Array Calibration Record for Weld

No. 11-002: Reactor Coolant Pump Suction

Nozzle Dissimilar Metal Weld - Wedge

Angle 4.0o (Circumferential Scan)

WF3 11-002 RCP 2A Structural Integrity Associates - Ultrasonic October 30, 2009

Suction Circ + 10 RL Phased Array Calibration Record for Weld No.

11-002: Reactor Coolant Pump Suction

Nozzle Dissimilar Metal Weld - Wedge

Angle 14.0o (Circumferential Scan)

WF3 11-002 RCP 2A Structural Integrity Associates - Ultrasonic October 30, 2009

Suction Flat RL Phased Array Calibration Record for Weld

No. 11-002: Reactor Coolant Pump Suction

Nozzle Dissimilar Metal Weld - Wedge Angle

14.0o (Axial & Circumferential Scan)

WF3-LIN-09-002 Structural Integrity Associates - Ultrasonic October 21, 2009

Linearity Record - Zetec/RD Tech OmniScan

MX - Version 1.4R3 (Serial No. ONMI-1983);

Transducer 115-000-613 (Serial

No. 01VTVW); Reference Block 16 AX (Serial

No. SI-16-AX-03).

Product Code 115-000- Krautkramer Phased Array Transducer September 02, 2008

566 Certificate of Compliance (Serial

No. 01VM4k-1)

SII006-07-09-28155-1 Laboratory Testing Inc. - Certified Test Report July 27, 2007

for Sonotech Ultragel II

WF3 12-009 RCP 2A Structural Integrity Associates - Phased Array October 29, 2009

Safety Injection Nozzle Ultrasonic Examination Record Data Sheet for

Weld No. 12-009: RCP 2A Safety Injection

Nozzle

WF3 12-009 RCP 2A Structural Integrity Associates - Ultrasonic October 29, 2009

Safety Injection AX SH Phased Array Calibration Record for Weld

No. 12-009: Reactor Coolant Pump 2A Safety

Injection Nozzle Dissimilar Metal Weld -

Wedge Angle 36.2o (Axial Scan)

A-6 Attachment

Section 1R07: Heat Sink Performance

PROCEDURES/DOCUMENTS

NUMBER TITLE DATE

WF3 12-009 RCP 2A Structural Integrity Associates - Ultrasonic October 29, 2009

Safety Injection AX RL Phased Array Calibration Record for Weld

No. 12-009: Reactor Coolant Pump 2A Safety

Injection Nozzle Dissimilar Metal Weld -

Wedge Angle 16.2o (Axial Scan)

WF3 12-009 RCP 2A Structural Integrity Associates - Ultrasonic October 29, 2009

Safety Injection CIRC Phased Array Calibration Record for Weld

RL No. 12-009: Reactor Coolant Pump 2A Safety

Injection Nozzle Dissimilar Metal Weld -

Wedge Angle 16.2o (Circumferential Scan)

Contract No. C-08-422 Sonaspection - Structural Integrity of December 17, 2009

Calibration Block No. SI-16-AX-03 & SI-16-

CIRC-03

WF3-LIN-09-003 Structural Integrity Associates - Ultrasonic October 21, 2009

Linearity Record - Zetec/RD Tech OmniScan

MX - Version 1.4R3 (Serial No. ONMI-1590);

Transducer 115-000-613 (Serial No.

01VTW0); Reference Block 16 AX (Serial

No. SI-16-AX-03).

Product Code 115-000- Krautkramer Phased Array Transducer August 26, 2008

613 Certificate of Conformity (Serial

No. 01VTW0-1)

ENGINEERING CHANGE REQUEST

NUMBER TITLE DATE

0000004490 Steam Generator Degradation Assessment and Repair April 2008

Criteria for RF15

0000005544 Waterford 3 Cycle 16 Steam Generator Operational April 2008

Assessment

0000005544 Waterford 3 Cycle 16 Steam Generator Operational August 2008

Assessment

0000008593 Waterford-3 RF16 Steam Generator Eddy Current Probe Revision 0

Equivalency Report

A-7 Attachment

ENGINEERING CHANGE REQUEST

NUMBER TITLE DATE

0000008594 Waterford-3 RF16 Steam Generator Inspection ECT

Data Analyst Training Manual

0000008592 RF16 Waterford-3 Steam Generator Analysis Guidelines Revision 0

0000008591 Steam Generator Degradation Assessment and Repair October 2009

Criteria for RF16

MISCELLANEOUS DOCUMENTS

NUMBER TITLE DATE

ECR-WF3-4490 Steam Generator Degradation Assessment and Repair April 2008

Criteria

W3F1-2008-0039 Steam Generator Conditions Observed at Waterford 3 May 20, 2008

During Refueling Outage 15

ECR-WF3-8593 Waterford -3 RF16 Steam Generator Eddy Current Probe November 3,

Equivalency Report 2009

ECR-WF3-8594 Document the Analysts Training Manual for RF16 SG November 6,

Eddy Current Analysts per the Requirements of NEI 97- 2009

06 and EN-DC-317

ECR-WF3-8592 RF16 Waterford-3 Steam Generator Analysis Guidelines November 5,

2009

ECR-WF3-8591 Steam Generator Degradation Assessment and Repair October 2009

Criteria for RF16

WF3-CHEM- Strategic Secondary Water Chemistry Plan 6

SEC-001-06

Inspection Report for Bare Metal Visual of Reactor

Vessel Head

BOP-VT-09-020 Visual Examination of Boric Acid Detection November 12,

2009

LTR-SGMP-09- Estimate of Through-Tube Depth of Intrados Wear Scar November 10,

179 in Waterford Steam Generator 32 2009

LO-WLO-2008- WF3 Boric Acid corrosion Control Program Self- October 6-16,

00068 Assessment 2008

LO-WLO-2006- Waterford 3 Strategic Secondary Water Chemistry Plan March 27-30,

00046 Self-Assessment 2006

A-8 Attachment

LO-WLO-2008- Benchmark of: Point Beach (PBNP) Nuclear Plant July 16-17,

0091 2009

W3F1-2008-0039 Steam Generator Conditions Observed at Waterford 3 May 20, 2008

WDI-PJF- Waterford 3 RF16 Reactor Vessel Head Penetration 0

1304321-FSR- Inspection Final Report

001

DWG U.T. Calibration Standard UT-6 (Contract No.74470) March 14,

C-246-392-2 1974

CNRO-2007-002 Mitigating Actions and Associated Schedule for Alloy

600/82/182

Weld No.12-009 Waterford 3 Dissimilar-Metal Weld Walk-Down Data

Sheet 4: 12 SI Nozzle to Safe-End

Various Personnel Certifications and Certification

Reviews

Bare Metal Visual Inspections Scheduled for RF-16

RF-16 Steam Generator Scope Summary

WELDING DATA RECORDS

2009-4293 2009-4528 2009-4588

CONDITION REPORTS

CR-WF3-2006-3966 CR-WF3-2008-2283 CR-HQN-2009-1068 CR-WF3-2009-5194

CR-WF3-2009-5501 CR-WF3-2009-5502 CR-WF3-2009-5509 CR-WF3-2009-5511

CR-WF3-2009-5514 CR-WF3-2009-5515 CR-WF3-2009-5516 CR-WF3-2009-5553

CR-WF3-2009-5554 CR-WF3-2009-5555 CR-WF3-2009-5556 CR-WF3-2009-5585

CR-WF3-2009-5662 CR-WF3-2009-5671 CR-WF3-2009-5679 CR-WF3-2009-5700

CR-WF3-2009-5716 CR-WF3-2009-5735 CR-WF3-2009-5757 CR-WF3-2009-5765

CR-WF3-2009-5769 CR-WF3-2009-5770 CR-WF3-2009-5774 CR-WF3-2009-5836

CR-WF3-2009-5838 CR-WF3-2009-5899 CR-WF3-2009-5941 CR-WF3-2009-5944

CR-WF3-2009-6486 CR-WF3-2009-6504 CR-WF3-2009-6514 CR-WF3-2009-6620

A-9 Attachment

Section 1R11: Licensed Operator Requalification Program

PROCEDURES/DOCUMENTS

NUMBER TITLE REVISION /

DATE

EN-TQ-114 Licensed Operator Requalification Training Program 0

Description

O-JITDIL Simulator Scenario for Dilution JIT 3

Section 1R12: Maintenance Effectiveness

CONDITION REPORTS

WF3-CR-2008-2637 WF3-CR-2008-2641 WF3-CR-2008-2689 WF3-CR-2008-2721

WF3-CR-2008-3103 WF3-CR-2008-3976 WF3-CR-2008-4012 WF3-CR-2008-4033

WF3-CR-2008-4635 WF3-CR-2008-4953 WF3-CR-2009-2189 WF3-CR-2009-2762

WF3-CR-2009-2796 WF3-CR-2009-3507 WF3-CR-2009-4066 WF3-CR-2009-4088

WF3-CR-2009-4093 WF3-CR-2009-4098 WF3-CR-2009-4155 WF3-CR-2009-5335

WF3-CR-2008-3217 WF3-CR-2008-4992 WF3-CR-2009-1901 WF3-CR-2009-2485

WF3-CR-2008-4453 WF3-CR-2008-5266 WF3-CR-2009-2077 WF3-CR-2009-4499

WF3-CR-2008-4583 WF3-CR-2009-0214 WF3-CR-2009-2096 WF3-CR-2009-5804

PROCEDURES/DOCUMENTS

NUMBER TITLE REVISION

EN-DC-206 Maintenance Rule 1

NUMARC 93-01 Industry Guideline for Monitoring the Effectiveness of 3

maintenance at Nuclear Power Plants

Section 1R13: Maintenance Risk Assessment and Emergent Work Controls

PROCEDURES/DOCUMENTS

NUMBER TITLE REVISION /

DATE

EOOS Version 3.3a Schedulers Evaluation for Shutdown Version Waterford November 5,

3 Rev 3 Model 2009

A-10 Attachment

N/A RF16 Daily Outage Status Report October 24,

2009

OP-903-107 Surveillance Procedure for Plant Protection System 303

Channel Functional Test

EOOS Version 3.3a Schedulers Evaluation for Shutdown Version 12/03/2009

Waterford 3 Rev 3 Model

Section 1R15: Operability Evaluations

CONDITION REPORTS

CR-WF3-2009-6101 CR-WF3-2008-2684 CR-WF3-2008-2705 CR-WF3-2008-2730

PROCEDURES/DOCUMENTS

NUMBER TITLE REVISION /

DATE

EN-OP-104 Operability Determination 4

MI-003-126 Core Protection Calculator Functional 14

SD-PPS Plant Protection System Description 0

OP-903-107 Plant Protection System Channel A, B, C, D, Functional Test 303

TSTF-324 Correct logarithmic power vs. RTP 1

ECE98-001 Calculation of Maximum Allowable Battery Inter Cell 0

Connection Resistance

ECE98-001 Calculation of Maximum Allowable Battery Inter Cell 1

Connection Resistance

ME-003-220 Station Battery Bank & Charger (18 month) 303

ME-003-220 Station Battery Bank & Charger (18 month) 301

SD-NI Nuclear Instrumentation System Description 6

Section 1R19: Postmaintenance Testing

CONDITION REPORTS

CR-WF3-2009-6095 CR-WF3-2009-6412 CR-WF3-2008-2381 CR-WF3-2009-6461

CR-WF3-2009-6449 CR-WF3-2008-4179 CR-WF3-2009-6506 CR-WF3-2009-4499

WORK ORDERS

1517161 213478 187774 152910

161402 122097 212157

A-11 Attachment

PROCEDURES/DOCUMENTS

NUMBER TITLE REVISION /

DATE

STA-001-004 Local Leak Rate Test 303

ICE-37718 Siemens Motor Driven Relay Observed Contact Behavior 02/05/1999

OP-903-116 Train B Integrated Emergency Diesel Generator/Engineering 013

Safety Features Test

ME-003-230 Battery Service Test 306

ME-003-240 Battery Performance Test 306

ME-004-213 Battery Intercell Connections 14

ME-004-231 Station Battery Charging 19

ME-003-210 Station Battery Bank and Charger (Quarterly) 16

ME-003-220 Station Battery Bank and Charger (18 month) 303

OP-903-046 Emergency Feed Pump Operability Check - Attachment 10.3 305

Section 1R20: Refueling and Other Outage Activities

PROCEDURES/DOCUMENTS

NUMBER TITLE REVISION /

DATE

OP-903-027 Inspection of Containment 301

PLG-009-014 Conduct of Planned Outages 303

OP-001-003 Reactor Coolant System Drain Down 306

OI-037-000 Operations Risk Assessment Guideline 2

MM-004-201 Containment Building Polar Crane PM 303

WF3-CS-08-01 NEI Heavy Load Drop Initiative 0

UNT-007-008 Control of Loads and Lifting 302

RF-001-009 Reactor Head 303

NEI 08-05 Industry Initiative on Control of Heavy Loads 0

MM-007-003 Containment Building Polar Crane Testing 5

A-12 Attachment

Section 1R22: Surveillance Testing

PROCEDURES/DOCUMENTS

NUMBER TITLE REVISION /

DATE

OP-903-116 Train B Integrated Emergency Diesel Generator/Engineering 013

Safety Features Test

OP-903-120 Section 7.10 Annulus Negative Pressure Surveillance Test 9

Section 2OS1: Access Controls to Radiologically Significant Areas

CONDITION REPORTS

CR-WF3-2009-5492 CR-WF3-2009-5648 CR-WF3-2009-5878 CR-WF3-2009-5880

CR-WF3-2009-6767 CR-WF3-2009-6792 CR-WF3-2009-6834 CR-WF3-2009-6852

CR-WF3-2009-6856

PROCEDURES/DOCUMENTS

NUMBER TITLE REVISION

EN-RP-100 Radworker Expectations 3

EN-RP-101 Access Control for Radiologically 4

Controlled Areas

EN-RP-102 Radiological Control 2

EN-RP-105 Radiation Work Permits 6

EN-RP-108 Radiation Protection Posting 7

EN-RP-121 Radioactive Material Control 4

EN-RP-123 Radiological Controls for Highly 0

Radioactive Particles

HP-001-114 Control of Temporary Shielding 10

UNT-001-016 Radiation Protection 301

UNT-007-001 Control of Miscellaneous Material in the 5

Spent Fuel Pool

A-13 Attachment

AUDITS, SELF-ASSESSMENTS, AND SURVEILLANCES

PROCEDURE/DOCUMENTS

NUMBER TITLE DATE

QA-14/15-2009- Radiation Protection/Radwaste Audit September

WF3-1 2009

RADIATON WORK PERMITS

NUMBER DESCRIPTION

2009-0401 Perform UDS/Viper/Votes and/or AOV/MOV testing of contaminated

system valves

2009-0510 Install/Remove Steam Generator Nozzle Dams, Pin verification, &

closeout

2009-0512 Remove/Install Steam Generator Secondary Manways/Handholes

2009-0513 RCP 1A Motor and Driver Mount removal and replacement

2009-0603 Entries into posted LHRA of the Reactor Containment Building to

perform minor maintenance activities, walkdowns, surveillances, and

inspections

2009-0606 Perform minor maintenance activities, walkdowns, surveillances, and

inspections

2009-0628 Entries into Containment Sump to perform transmitter calibrations,

Weir Box cleaning and Under Vessel inspections

2009-0721 Entries into posted LHRA of the Reactor Containment Building to

install/remove shielding on the ICI stalks

2009-0805 Refuel 16 - Tours and inspections in all RCAs except HRA, LHRA,

VHRA

A-14 Attachment

SAMPLE RESULTS AND SURVEYS

MISCELLANEOUS

NUMBER TITLE DATE

WF3-0910-0398 Survey of RAB -35 Shutdown Heat Exchangers October 23, 2009

WF3-0910-0431 Survey of RAB -35 Shutdown Heat Exchangers October 24, 2009

Section 2OS2: ALARA Planning and Controls

PROCEDURES

NUMBER TITLE REVISION

HP-002-201 Radiological Survey Techniques and Frequencies 302

EN-RP-104 Personnel Contamination Events 4

EN-RP-106 Radiological Survey Documentation 2

EN-RP-131 Air Sampling 7

EN-RP-203 Dose Assessment 3

MISCELLANEOUS

NUMBER TITLE DATE

2009-0020 Personnel Contamination Event Record October 29, 2009

2009-0045 Personnel Contamination Event Record November 3, 2009

2009-0049 Personnel Contamination Event Record November 5,2009

Section 4OA1: Performance Indicator Verification

PROCEDURES/DOCUMENTS

NUMBER TITLE REVISION

NEI 99-02 Regulatory Assessment Performance Indicator Guideline 5

EN-LI-114 Performance Indicator Process 4

EN-DIR-RP-002 Radiation Protection Performance Indicator Program 0

MISCELLANEOUS DOCUMENTS

Radiological controlled area entries greater than 100 millirem

A-15 Attachment

Section 4OA2: Identification and Resolution of Problems

CONDITION REPORTS

CR-WF3-2009-5501 CR-WF3-2009-5502 CR-WF3-2009-5509 CR-WF3-2009-5511

CR-WF3-2009-5514 CR-WF3-2009-7166 CR-WF3-2009-7159

Section 4OA5: Other Activities

DOCUMENTS

NUMBER TITLE REVISION /

DATE

CEP-NDE-0955 Alloy 600 Visual Examination (VE) of Bare-Metal Surfaces 301

EC-1830 Waterford Steam Electric Station, Unit 3, Dissimilar Metal 0

Weld Overlays

Drawing No. Hot Leg Surge Nozzle Weld Overlay Design 5

WSES-19Q-05

SI-UT-130 Procedure for the Phased Array Ultrasonic Examination of 3

Dissimilar Metal Welds

SI-NDE-06 Calibration of Ultrasonic NDE Equipment 4

SI-NDE-08 Qualification and Certification of NDE Personnel for 1

Nuclear Applications

CEP-NDE-0901 VT-1 Examination 4

CEP-NDE-0902 VT-2 Examination 7

CEP-NDE-0903 VT-3 Examination 5

WF3 11-002 Structural Integrity Associates - Phased Array Ultrasonic October 30,

RCP 2A Suction Examination Record Data Sheet for Weld No. 11-002: 2009

Nozzle Reactor Coolant Pump 2A Cold Leg Suction Nozzle

WF3 11-002 Structural Integrity Associates - Ultrasonic Phased Array October 30,

RCP 2A Suction Calibration Record for Weld No. 11-002: Reactor Coolant 2009

AX SH Pump Suction Nozzle Dissimilar Metal Weld - Wedge

Angle 36.2o (Axial Scan)

WF3 11-002 Structural Integrity Associates - Ultrasonic Phased Array October 30,

RCP 2A Suction Calibration Record for Weld No. 11-002: Reactor Coolant 2009

Circ + 10 RL Pump Suction Nozzle Dissimilar Metal Weld - Wedge

Angle 14.0o (Circumferential Scan)

WF3 11-002 Structural Integrity Associates - Ultrasonic Phased Array October 30,

RCP 2A Suction Calibration Record for Weld No. 11-002: Reactor Coolant 2009

Flat RL Pump Suction Nozzle Dissimilar Metal Weld - Wedge

Angle 14.0o (Axial & Circumferential Scan)

A-16 Attachment

WF3-LIN-09-002 Structural Integrity Associates - Ultrasonic Linearity October 21,

Record - Zetec/RD Tech OmniScan MX - Version 1.4R3 2009

(Serial No. ONMI-1983); Transducer 115-000-613 (Serial

No. 01VTVW); Reference Block 16 AX (Serial No. SI-16-

AX-03).

Contract No. C- Sonaspection - Structural Integrity of Calibration Block May 18, 2009

09-089 R1 No. SI-Flat-SS-4inchT-01

A-17 Attachment