ML090400437

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IR 05000255-08-005; Entergy Nuclear Operations, Inc., on 10/01/2008 - 12/31/2008; Palisades Power Plant; Integrated Inspection Report; Operability Evaluations; Follow-up of Events
ML090400437
Person / Time
Site: Palisades Entergy icon.png
Issue date: 02/09/2009
From: Jack Giessner
NRC/RGN-III/DRP/RPB4
To: Schwartz C
Entergy Nuclear Operations
References
IR-05-005
Download: ML090400437 (40)


See also: IR 05000255/2008005

Text

UNITED STATES

NUCLEAR REGULATORY COMMISSION

REGION III

2443 WARRENVILLE ROAD, SUITE 210

LISLE, IL 60532-4352

February 9, 2009

Mr. Christopher J. Schwarz

Site Vice President

Entergy Nuclear Operations, Inc.

Palisades Nuclear Plant

27780 Blue Star Memorial Highway

Covert, MI 49043-9530

SUBJECT: PALISADES NUCLEAR PLANT INTEGRATED INSPECTION

REPORT 05000255/2008-005

Dear Mr. Schwarz:

On December 31, 2008, the U. S. Nuclear Regulatory Commission (NRC) completed an

inspection at your Palisades Nuclear Plant. The enclosed report documents the inspection

findings, which were discussed on January 22, 2009, with members of your staff.

The inspection examined activities conducted under your license as they relate to safety and

compliance with the Commissions rules and regulations and with the conditions of your license.

The inspectors reviewed selected procedures and records, observed activities, and interviewed

personnel.

Based on the results of this inspection, two NRC-identified violations of very low safety

significance were identified. The findings involved violations of NRC requirements. However,

because of their very low safety significance, and because the issues were entered into your

corrective action program, the NRC is treating the issues as Non-Cited Violations (NCVs)in

accordance with Section VI.A.1 of the NRC Enforcement Policy. Additionally, one licensee

identified violation is listed in Section 4OA7 of this report.

If you contest the subject or severity of an NCV, you should provide a response within

30 days of the date of this inspection report, with the basis for your denial, to the

U.S. Nuclear Regulatory Commission, ATTN: Document Control Desk, Washington,

DC 20555-0001, with a copy to the Regional Administrator, U.S. Nuclear Regulatory

Commission - Region III, 2443 Warrenville Road, Suite 210, Lisle, IL 60532-4352; the

Director, Office of Enforcement, U.S. Nuclear Regulatory Commission, Washington, DC

20555-0001; and the Resident Inspector Office at the Palisades Nuclear Plant.

C. Schwarz -2-

In accordance with 10 CFR 2.390 of the NRC's "Rules of Practice," a copy of this letter and its

enclosure will be available electronically for public inspection in the NRC Public Document

Room or from the Publicly Available Records (PARS) component of NRC's document system

(ADAMS), accessible from the NRC Web site at http://www.nrc.gov/reading-rm/adams.html

(the Public Electronic Reading Room).

Sincerely,

/RA/

John B. Giessner, Chief

Branch 4

Division of Reactor Projects

Docket No. 50-255

License No. DPR-20

Enclosure: Inspection Report 05000255/2008-005

w/Attachment: Supplemental Information

cc w/encl: Senior Vice President

Vice President Oversight

Senior Manager, Nuclear Safety & Licensing

Senior Vice President and COO

Assistant General Counsel

Manager, Licensing

W. DiProfio

W. Russell

G. Randolph

Supervisor, Covert Township

Office of the Governor

T. Strong, State Liaison Officer

Michigan Department of Environmental Quality

Michigan Office of the Attorney General

C. Schwarz -2-

In accordance with 10 CFR 2.390 of the NRC's "Rules of Practice," a copy of this letter and its

enclosure will be available electronically for public inspection in the NRC Public Document

Room or from the Publicly Available Records (PARS) component of NRC's document system

(ADAMS), accessible from the NRC Web site at http://www.nrc.gov/reading-rm/adams.html

(the Public Electronic Reading Room).

Sincerely,

John B. Giessner, Chief

Branch 4

Division of Reactor Projects

Docket No. 50-255

License No. DPR-20

Enclosure: Inspection Report 05000255/2008-005

w/Attachment: Supplemental Information

cc w/encl: Senior Vice President

Vice President Oversight

Senior Manager, Nuclear Safety & Licensing

Senior Vice President and COO

Assistant General Counsel

Manager, Licensing

W. DiProfio

W. Russell

G. Randolph

Supervisor, Covert Township

Office of the Governor

T. Strong, State Liaison Officer

Michigan Department of Environmental Quality

Michigan Office of the Attorney General

DOCUMENT NAME: G:\1-Secy\1-Work In Progress\Pali 2008-005.doc

Publicly Available Non-Publicly Available Sensitive Non-Sensitive

To receive a copy of this document, indicate in the concurrence box "C" = Copy without attach/encl "E" = Copy with attach/encl "N" = No copy

OFFICE RIII RIII

NAME RLerch:dtp JGiessner

DATE 02/06/09 02/06/09

OFFICIAL RECORD COPY

Letter to C. Schwarz from J. Giessner dated February 9, 2009

SUBJECT: PALISADES NUCLEAR PLANT INTEGRATED INSPECTION

REPORT 05000255/2008-005

DISTRIBUTION:

Tamara Bloomer

RidsNrrPMPalisades

RidsNrrDorlLpl3-1

RidsNrrDirsIrib Resource

Mark Satorius

Kenneth Obrien

Jared Heck

Carole Ariano

Linda Linn

Cynthia Pederson

DRPIII

DRSIII

Patricia Buckley

Tammy Tomczak

ROPreports@nrc.gov

U.S. NUCLEAR REGULATORY COMMISSION

REGION III

Docket No: 50-255

License No: DPR-20

Report No: 05000255/2008-005

Licensee: Entergy Nuclear Operations, Inc.

Facility: Palisades Nuclear Plant

Location: Covert, MI

Dates: October 1, 2008, to December 31, 2008

Inspectors: J. Ellegood, Senior Resident Inspector

T. Taylor, Resident Inspector

J. Cassidy, Senior Health Physicist

A. Dahbur, Senior Reactor Inspector

R. Jickling, Senior Emergency Preparedness Inspector

R. Winter, Reactor Inspector

Approved by: J. Giessner, Chief

Branch 4

Division of Reactor Projects

Enclosure

TABLE OF CONTENTS

SUMMARY OF FINDINGS ......................................................................................................... 1

REPORT DETAILS..................................................................................................................... 3

Summary of Plant Status......................................................................................................... 3

1. REACTOR SAFETY ..................................................................................................... 3

1R04 Equipment Alignment (71111.04) ....................................................................... 3

1R05 Fire Protection (71111.05) ................................................................................. 4

1R11 Licensed Operator Requalification Program (71111.11)..................................... 5

1R12 Maintenance Effectiveness (71111.12) .............................................................. 5

1R13 Maintenance Risk Assessments and Emergent Work Control (71111.13).......... 6

1R15 Operability Evaluations (71111.15) .................................................................... 6

1R18 Plant Modifications (71111.18) ........................................................................... 8

1R19 Post-Maintenance Testing (71111.19) ............................................................... 9

1R22 Surveillance Testing (71111.22)....................................................................... 10

1EP4 Emergency Action Level and Emergency Plan Changes (71114.04) ............... 11

1EP6 Drill Evaluation (71114.06) ............................................................................... 11

2. RADIATION SAFETY ................................................................................................. 12

2OS1 Access Control to Radiologically Significant Areas (71121.01) ........................ 12

4. OTHER ACTIVITIES .................................................................................................. 16

4OA1 Performance Indicator Verification (71151) ...................................................... 16

4OA2 Identification and Resolution of Problems (71152) ........................................... 17

4OA3 Follow-Up of Events and Notices of Enforcement Discretion (71153) .............. 22

4OA5 Other Activities................................................................................................. 24

4OA6 Management Meetings .................................................................................... 25

4OA7 Licensee-Identified Violations .......................................................................... 26

SUPPLEMENTAL iNFORMATION ............................................................................................. 1

KEY POINTS OF CONTACT .................................................................................................. 1

LIST OF ITEMS OPENED, CLOSED, AND DISCUSSED ....................................................... 2

LIST OF DOCUMENTS REVIEWED ....................................................................................... 3

LIST OF ACRONYMS USED .................................................................................................. 8

Enclosure

SUMMARY OF FINDINGS

IR 05000255/2008-005; 10/01/2008 - 12/31/2008; Palisades Power Plant; Integrated Inspection

Report; Operability Evaluations; Follow-up of Events.

This report covers a 3-month period of inspection by resident inspectors and announced

baseline inspections by regional inspectors. Two Green findings were identified by the

inspectors. The findings were considered Non-Cited Violations of NRC regulations. The

significance of most findings is indicated by their color (Green, White, Yellow, Red) using

Inspection Manual Chapter (IMC) 0609, Significance Determination Process (SDP). Findings

for which the SDP does not apply may be Green or be assigned a severity level after NRC

management review. The NRCs program for overseeing the safe operation of commercial

nuclear power reactors is described in NUREG-1649, Reactor Oversight Process, Revision 4,

dated December 2006.

A. NRC-Identified and Self-Revealed Findings

Cornerstone: Mitigating Systems

  • Green. The inspectors identified a finding of very low safety significance (Green) and

an associated NCV of 10 CFR 50, Appendix B, Criterion XI, Test Control, for

the inadequate testing of the heat removal capacity of the Control Room Heating,

Ventilation, and Air Conditioning (CR HVAC) system. Specifically, the licensee isolated

refrigerant hot gas bypass flow during the test which increased the heat removal

capability of the chiller. The licensee entered the issue into their corrective action

program as condition report (CR) PLP-2008-3993 and re-performed portions of the

engineering basis calculation to demonstrate margin to account for the hot gas bypass

flow.

The finding is more than minor because, in accordance with IMC 0612, Appendix E,

Examples of Minor Issues, the inspectors determined that the finding was similar to

Example E.3.j and resulted in a reasonable doubt as to the operability of the chiller.

Based upon a review of the licensees revised calculation for the CR HVAC system

acceptance criteria and the Technical Specification (TS) requirements, the finding

screens as very low safety significance (Green) using the Phase 1 SDP worksheets.

The inspectors determined that the finding included a cross-cutting aspect in the area of

human performance, resources, and complete and accurate procedures (H.2(c))

because the surveillance procedure unacceptably preconditioned the chiller. (1R15)

  • Green. A self-revealed finding of very low safety significance (Green) and an associated

NCV for failure to comply with TS 3.8.1 requirements when metal fragments were found

in the valve assembly area of the 1-2 Emergency Diesel Generator (EDG) cylinder 2L.

The source of the fragments was a failed spring lock for one of the exhaust valves. This

resulted in the EDG being inoperable for a period greater than allowed by TSs.

Subsequently, the licensee inspected the remaining spring locks on the 1-2 EDG.

Inspections of the 1-1 EDG spring locks are planned.

The finding is more than minor because it affected the equipment performance attribute

of the mitigating system cornerstone and adversely affected the objective of ensuring the

availability, reliability, and capability of systems that respond to initiating events to

prevent undesirable consequences. A failure analysis performed by the vendor in

1 Enclosure

conjunction with an apparent cause analysis by the licensee led to an evaluation that the

diesel could perform its safety function for at least the 24-hour Probabilistic Risk

Assessment mission time. In consultation with the regional Senior Risk Analyst, the

finding screens as Green using the significance determination process phase 1. No

cross-cutting aspect was assigned because this issue is not indicative of current plant

performance. (4OA3)

B. Licensee-Identified Violations

A violation of very low safety significance that was identified by the licensee has been

reviewed by inspectors. Corrective actions planned or taken by the licensee have been

entered into the licensees corrective action program. This violation and corrective

action tracking numbers are listed in Section 4OA7 of this report.

2 Enclosure

REPORT DETAILS

Summary of Plant Status

Throughout the inspection period, the plant operated at or near 100 percent power.

1. REACTOR SAFETY

1R01 Adverse Weather Protection (71111.01)

a. Inspection Scope

Since extreme cold conditions were forecast in the vicinity of the facility for

December 2008, the inspectors reviewed the licensees overall preparations/protection

for the expected weather conditions. On December 17, the inspectors walked down the

condensate storage tanks and safety injection and refueling water tank system(s)

because their safety-related functions could be affected or required as a result of the

extreme cold conditions forecast for the facility. The inspectors observed insulation,

heat trace circuits, and weatherized enclosures to ensure operability of affected

systems. The inspectors reviewed licensee procedures. Specific documents reviewed

during this inspection are listed in the Attachment.

This inspection constituted one readiness for impending adverse weather condition

sample as defined in IP 71111.01-05.

b. Findings

No findings of significance were identified.

1R04 Equipment Alignment (71111.04)

a. Inspection Scope

The inspectors performed partial system walkdowns of the following risk-significant

systems:

  • High Pressure Safety Injection (HPSI)-A with HPSI-B out of service for

maintenance;

maintenance;

  • HPSI-B with HPSI-A out of service for maintenance;
  • 1-2 EDG with the 1-1 EDG out of service for maintenance.

The inspectors selected these systems based on their risk significance relative to the

reactor safety cornerstones at the time they were inspected. The inspectors attempted

to identify any discrepancies that could impact the function of the system, and, therefore,

potentially increase risk. The inspectors reviewed applicable operating procedures,

system diagrams, Updated Final Safety Analysis Report (UFSAR), Technical

Specification (TS) requirements, outstanding work orders, condition reports, and the

impact of ongoing work activities on redundant trains of equipment in order to identify

conditions that could have rendered the systems incapable of performing their intended

3 Enclosure

functions. The inspectors also walked down accessible portions of the systems to verify

system components and support equipment were aligned correctly and operable. The

inspectors examined the material condition of the components and observed operating

parameters of equipment to verify that there were no obvious deficiencies. The

inspectors also verified that the licensee had properly identified and resolved equipment

alignment problems that could cause initiating events or impact the capability of

mitigating systems or barriers and entered them into the Corrective Action program

(CAP) with the appropriate significance characterization. Documents reviewed are listed

in the Attachment.

These activities constituted four partial system walkdown samples as defined in

IP 71111.04-05.

b. Findings

No findings of significance were identified.

1R05 Fire Protection (71111.05)

a. Inspection Scope

The inspectors conducted fire protection walkdowns which were focused on availability,

accessibility, and the condition of firefighting equipment in the following risk-significant

plant areas:

  • 1-D Switchgear Room (during/following emergent Post Maintenance Testing for

Auxiliary Feed Water (AFW) -C power supply);

  • Component Cooling Water Room;
  • North and Southwest Penetration Rooms;
  • Charging Pumps Room.

The inspectors reviewed areas to assess if the licensee had implemented a fire

protection program that adequately controlled combustibles and ignition sources within

the plant, effectively maintained fire detection and suppression capability, maintained

passive fire protection features in good material condition, and had implemented

adequate compensatory measures for out of service, degraded, or inoperable fire

protection equipment, systems, or features in accordance with the licensees fire plan.

The inspectors selected fire areas based on their overall contribution to internal fire risk

as documented in the plants Individual Plant Examination of External Events with later

additional insights, their potential to impact equipment which could initiate or mitigate a

plant transient, or their impact on the plants ability to respond to a security event. Using

the documents listed in the Attachment, the inspectors verified that fire hoses and

extinguishers were in their designated locations and available for immediate use; that

fire detectors and sprinklers were unobstructed; that transient material loading was

within the analyzed limits; and fire doors, dampers, and penetration seals appeared to

be in satisfactory condition. The inspectors also verified that minor issues identified

during the inspection were entered into the licensees CAP. Documents reviewed are

listed in the Attachment to this report.

4 Enclosure

These activities constituted five quarterly fire protection inspection samples as defined in

IP 71111.05-05.

b. Findings

No findings of significance were identified.

1R11 Licensed Operator Requalification Program (71111.11)

a. Inspection Scope

On November 17, the inspectors observed a crew of licensed operators in the plants

simulator during licensed operator requalification examinations to verify that operator

performance was adequate, evaluators were identifying, and documenting crew

performance problems, and training was being conducted in accordance with licensee

procedures. The inspectors evaluated the following areas:

  • licensed operator performance;
  • crews clarity and formality of communications;
  • ability to take timely actions in the conservative direction;
  • prioritization, interpretation, and verification of annunciator alarms;
  • correct use and implementation of abnormal and emergency procedures;
  • control board manipulations;
  • oversight and direction from supervisors; and
  • ability to identify and implement appropriate TS actions and Emergency Plan

actions and notifications.

The crews performance in these areas was compared to pre-established operator action

expectations and successful critical task completion requirements. Documents reviewed

are listed in the Attachment to this report.

This inspection constituted one quarterly licensed operator requalification program

sample as defined in IP 71111.11.

b. Findings

No findings of significance were identified.

1R12 Maintenance Effectiveness (71111.12)

a. Inspection Scope

The inspectors evaluated degraded performance issues involving the following risk

significant systems:

The inspectors assessed performance issues with respect to the reliability, availability,

and condition monitoring of the system. In addition, the inspectors verified maintenance

effectiveness issues were entered into the corrective action program with the appropriate

significance characterization. Documents reviewed are listed in the Attachment.

5 Enclosure

This inspection constitutes one quarterly maintenance effectiveness samples as defined

in IP 71111.12-05.

b. Findings

No findings of significance were identified.

1R13 Maintenance Risk Assessments and Emergent Work Control (71111.13)

a. Inspection Scope

The inspectors reviewed the licensee's evaluation and management of plant risk for the

maintenance and emergent work activities affecting risk-significant and safety-related

equipment listed below to verify that the appropriate risk assessments were performed

prior to removing equipment for work:

  • HPSI-B bearing oil change with hot leg injection valve breaker work and

switchyard work (yellow risk);

  • Unplanned AFW right train inoperability.

These activities were selected based on their potential risk significance relative to the

reactor safety cornerstones. As applicable for each activity, the inspectors verified that

risk assessments were performed as required by 10 CFR 50.65(a)(4) and were accurate

and complete. When emergent work was performed, the inspectors verified that the

plant risk was promptly reassessed and managed. The inspectors reviewed the scope

of maintenance work, discussed the results of the assessment with the licensee's

probabilistic risk analyst or shift technical advisor, and verified plant conditions were

consistent with the risk assessment. The inspectors also reviewed TS requirements and

walked down portions of redundant safety systems, when applicable, to verify risk

analysis assumptions were valid and applicable requirements were met.

These maintenance risk assessments and emergent work control activities constituted

two samples as defined in IP 71111.13-05.

b. Findings

No findings of significance were identified.

1R15 Operability Evaluations (71111.15)

a. Inspection Scope

The inspectors reviewed the following issues:

  • CR HVAC chiller capacity with hot-gas bypass isolated;
  • CR HVAC fittings found not in-accordance with design;
  • EDG 1-2 due to increased load from Containment Air Coolers.

The inspectors selected these potential operability issues based on the risk-significance

of the associated components and systems. The inspectors evaluated the technical

6 Enclosure

adequacy of the evaluations to ensure that TS operability was properly justified, and the

subject component or system remained available such that no unrecognized increase in

risk occurred. The inspectors compared the operability and design criteria in the

appropriate sections of the TS and UFSAR to the licensees evaluations, to determine

whether the components or systems were operable. Where compensatory measures

were required to maintain operability, the inspectors determined whether the measures

in place would function as intended and were properly controlled. The inspectors

determined, where appropriate, compliance with bounding limitations associated with the

evaluations. Additionally, the inspectors also reviewed a sampling of corrective action

documents to verify that the licensee was identifying and correcting any deficiencies

associated with operability evaluations. Documents reviewed are listed in the

Attachment.

This inspection constitutes four samples as defined in IP 71111.15.-05.

b. Findings

Introduction: The inspectors identified a finding of very low safety significance (Green)

and an associated NCV of 10 CFR 50, Appendix B, Criterion XI, Test Control, for

the inadequate testing of the heat removal capacity of the CR HVAC system.

Specifically, the licensee isolated refrigerant hot gas bypass flow during the test which

increased the heat removal capability of the chiller.

Description: On August 26, 2008, the licensee performed a surveillance test, RT-202, to

determine the heat removal capability of the A chiller. The test assessed the capability

of chiller to remove heat load during design basis conditions. The inspectors reviewed

the procedure and conduct of the test and noted that step 5.1.3.d of the procedure

manually isolated the hot gas bypass valve of the chiller. Under normal and design

conditions, the hot gas bypass flow control valve regulates automatically to open and

bypass refrigerant from the condensing unit to maintain compressor suction pressure

under low load condition. At full load conditions the valve is closed, but by design there

is a small amount of refrigerant that flows. Therefore, isolating the hot gas bypass

increases the heat removal capability of the chiller. Since hot gas bypass would not be

isolated during normal operation nor during an event, the inspectors concluded that

isolating hot gas bypass was preconditioning. As part of the corrective actions, the

licensee reviewed test data going back approximately 3 years and adjusted the data to

account for hot gas bypass flow. For the July 2007 test on the A train of the CR HVAC

system, taking hot gas bypass flow into consideration would have resulted in a

measured capacity approximately 9200 BTU/hr below the acceptance criteria of RT-202.

Based on discussions with the system engineer and a review of previous revisions of

RT-202, the inspectors determined that RT-202 was being performed with hot gas

bypass flow isolated since the year 2000.

In order to determine current operability of the CR HVAC system, the licensee adjusted

the most recent results of RT-202 to account for hot gas bypass flow. The licensee

determined that the B CR HVAC train was operable and that the A CR HVAC train

would remain operable below an outside air temperature of 87 degrees. Upon further

questioning by the inspectors regarding the TS requirements, the licensee later declared

the A train of CR HVAC inoperable. As part of the licensees corrective actions, the

RT-202 basis calculation was revised. By using margin included in the analysis

regarding allowable control room temperature, the licensee provided a basis to restore

7 Enclosure

the A chiller to operable status and demonstrate operability for the previous tests that

were reviewed.

Analysis: The inspectors concluded that the failure to properly demonstrate the

capability of the chillers warranted an evaluation using the SDP. Specifically, the

manual isolation of the hot gas bypass line provided an erroneous value for chiller

capacity. On one occasion, isolation of the flow path masked a condition where the

chiller would not have been able to meet surveillance requirements. Although the

licensee was able to revise an underlying calculation to show the chiller could maintain

control room temperatures within the TS requirements, the failure to meet the

requirements prior to the calculation markup created a reasonable doubt of the

operability of the chiller. Using IMC 0612, Appendix E, Examples of Minor Issues, the

inspectors determined that the finding was similar to Example E.3.j and was more than

minor because the error resulted in reasonable doubt as to the operability of the chiller.

This finding affects the Procedure Quality attribute of the Mitigating Systems cornerstone

objective of ensuring the availability, reliability, and capability of systems that respond to

initiating events to prevent undesirable consequences in that the licensee used

inadequate testing to demonstrate operability of the system. To further assess the

significance of the finding, the inspectors used IMC 0609, Appendix A, Determining the

Significance of Reactor Inspection Findings for At-Power Situations. Based upon a

review of the licensees revised calculation for the CR HVAC system acceptance criteria

and the TS requirements, the finding screens as very low safety significance (Green)

using the Phase 1 worksheets due to answering no to each of the screening questions.

The inspectors determined that the finding included a cross-cutting aspect in the area of

human performance, resources, and complete and accurate procedures (H.2(c))

because the surveillance procedure unacceptably preconditioned the chiller. The finding

reflects current performance because the licensee revised the steps in question in

July 2007 but failed to identify and correct the preconditioning.

Enforcement: Appendix B of 10 CFR Part 50, Criterion XI, Test Control, requires, in

part, that a test program be established to assure that all testing required to

demonstrate that structures, systems, and components will perform satisfactorily in

service is identified and performed in accordance with written test procedures which

incorporate the requirements and acceptance limits contained in the applicable design

documents. Contrary to this requirement, during the performance of TS Surveillance

Procedure RT-202, Control Room HVAC Heat Removal Capability in August 2008, the

inspectors identified that the procedure does not adequately test the chillers to ensure

bypass flow of refrigerant is accounted for in the capacity of the unit. In addition,

potential degradation in the hot gas bypass flow line is not analyzed. Because the

finding is of very low safety significance and has been entered into the licensees

CAP as CR-2008-03993, this violation of 10 CFR 50, Appendix B, Criterion XI, is being

treated as a NCV, consistent with Section VI.A of the NRC Enforcement Policy.

(NCV 05000255/2008005 01, Inadequate Testing of Control Room Chillers)

1R18 Plant Modifications (71111.18)

a. Inspection Scope

The inspectors reviewed the following temporary modification(s):

8 Enclosure

The inspectors compared the temporary configuration changes and associated

10 CFR 50.59 screening and evaluation information against the design basis, the

UFSAR, and the TS, as applicable, to verify that the modification did not affect the

operability or availability of the affected system(s). The inspectors also compared the

licensees information to operating experience information to ensure that lessons learned

from other utilities had been incorporated into the licensees decision to implement the

temporary modification. The inspectors, as applicable, performed field verifications to

ensure that the modifications were installed as directed; the modifications operated as

expected; modification testing adequately demonstrated continued system operability,

availability, and reliability; and that operation of the modifications did not impact the

operability of any interfacing systems. Lastly, the inspectors discussed the temporary

modification with operations, engineering, and training personnel to ensure that the

individuals were aware of how extended operation with the temporary modification in

place could impact overall plant performance.

This inspection constituted one temporary modification sample as defined in

IP 71111.18-05.

b. Findings

No findings of significance were identified.

1R19 Post-Maintenance Testing (71111.19)

a. Inspection Scope

The inspectors reviewed the following post-maintenance activities to verify that

procedures and test activities were adequate to ensure system operability and functional

capability:

  • Uninterruptible power supply following installation;
  • Primary rod position indication following power supply replacement;
  • AFW Right Train Power Supply Replacement.

These activities were selected based upon the structure, system, or component's ability

to impact risk. The inspectors evaluated these activities for the following (as applicable):

the effect of testing on the plant had been adequately addressed; testing was adequate

for the maintenance performed; acceptance criteria were clear and demonstrated

operational readiness; test instrumentation was appropriate; tests were performed as

written in accordance with properly reviewed and approved procedures; equipment was

returned to its operational status following testing (temporary modifications or jumpers

required for test performance were properly removed after test completion); and test

documentation was properly evaluated. The inspectors evaluated the activities against

TS, the UFSAR, 10 CFR Part 50 requirements, licensee procedures, and various

NRC generic communications to ensure that the test results adequately ensured that the

equipment met the licensing basis and design requirements. In addition, the inspectors

reviewed corrective action documents associated with post-maintenance tests to

determine whether the licensee was identifying problems and entering them in the CAP

and that the problems were being corrected commensurate with their importance to

safety. Documents reviewed are listed in the Attachment to this report.

9 Enclosure

This inspection constituted three post-maintenance testing samples as defined in

IP 71111.19-05.

b. Findings

No findings of significance were identified.

1R22 Surveillance Testing (71111.22)

a. Inspection Scope

The inspectors reviewed the test results for the following activities to determine whether

risk-significant systems and equipment were capable of performing their intended safety

function and to verify testing was conducted in accordance with applicable procedural

and TS requirements:

  • RPS-I-7, Anticipated Transient Without Scram Calibration/Functional Test
  • QO-1, Safety Injection Test;
  • RO-52, Fire Pump Capacity Test;
  • QO-15, Component Cooling Water-B Pump In-Service Test.

The inspectors observed in-plant activities and reviewed procedures and associated

records to determine the following:

  • did preconditioning occur;
  • were the effects of the testing adequately addressed by control room personnel

or engineers prior to the commencement of the testing;

  • were acceptance criteria clearly stated, demonstrated operational readiness, and

consistent with the system design basis;

  • plant equipment calibration was correct, accurate, and properly documented;
  • as-left setpoints were within required ranges; and the calibration frequency were

in accordance with TSs, the UFSAR, procedures, and applicable commitments;

  • measuring and test equipment calibration was current;
  • test equipment was used within the required range and accuracy; applicable

prerequisites described in the test procedures were satisfied;

  • test frequencies met TS requirements to demonstrate operability and reliability;

tests were performed in accordance with the test procedures and other

applicable procedures; jumpers and lifted leads were controlled and restored

where used;

  • test data and results were accurate, complete, within limits, and valid;
  • test equipment was removed after testing;
  • where applicable for inservice testing activities, testing was performed in

accordance with the applicable version of Section XI, American Society of

Mechanical Engineers Code, and reference values were consistent with the

system design basis;

  • where applicable, test results not meeting acceptance criteria were addressed

with an adequate operability evaluation or the system or component was

declared inoperable;

  • where applicable for safety-related instrument control surveillance tests,

reference setting data were accurately incorporated in the test procedure;

10 Enclosure

  • where applicable, actual conditions encountering high resistance electrical

contacts were such that the intended safety function could still be accomplished;

  • prior procedure changes had not provided an opportunity to identify problems

encountered during the performance of the surveillance or calibration test;

  • equipment was returned to a position or status required to support the

performance of its safety functions; and

  • all problems identified during the testing were appropriately documented and

dispositioned in the CAP.

Documents reviewed are listed in the Attachment to this report.

This inspection constituted four routine surveillance testing sample(s) and one inservice

testing sample.

b. Findings

No findings of significance were identified.

1EP4 Emergency Action Level and Emergency Plan Changes (71114.04)

a. Inspection Scope

Since the last NRC inspection of this program area, Emergency Plan Revision 17 and

Implementing Procedure EI-1, "Emergency Classification and Actions," Revision 49,

were implemented based on your determination, in accordance with 10 CFR 50.54(q),

that the changes resulted in no decrease in effectiveness of the Plan, and that the

revised Plan as changed continues to meet the requirements of 10 CFR 50.47(b) and

Appendix E to 10 CFR Part 50. The inspectors conducted a sampling review of the

Emergency Plan changes and a review of the Emergency Action Level changes to

evaluate for potential decreases in effectiveness of the Plan. However, this review does

not constitute formal NRC approval of the changes. Therefore, these changes remain

subject to future NRC inspection in their entirety.

This Emergency Action Level and Emergency Plan Changes inspection constituted one

sample as defined in IP 71114.04-05.

b. Findings

No findings of significance were identified.

1EP6 Drill Evaluation (71114.06)

a. Inspection Scope

The inspectors evaluated the conduct of a routine licensee emergency drill on

November 5, 2008, and a table top drill for the emergency operations facility on

December 17, 2008, to identify any weaknesses and deficiencies in classification,

notification, and protective action recommendation development activities. The

inspectors observed, as applicable, emergency response operations in the simulator

control room, technical support center, and emergency operations facility to determine

whether the event classification, notifications, and protective action recommendations

11 Enclosure

were performed in accordance with procedures. The inspectors also attended the

licensee drill critique to compare any inspector-observed weakness with those identified

by the licensee staff in order to evaluate the critique and to verify whether the licensee

staff was properly identifying weaknesses and entering them into the corrective action

program. As part of the inspection, the inspectors reviewed the drill package and other

documents listed in the Attachment to this report.

These emergency preparedness drill inspections constituted two samples as defined in

IP 71114.06-05.

b. Findings

No findings of significance were identified.

2. RADIATION SAFETY

Cornerstone: Occupational Radiation Safety

2OS1 Access Control to Radiologically Significant Areas (71121.01)

.1 Plant Walkdowns and Radiation Work Permit (RWP) Reviews

a. Inspection Scope

The inspectors reviewed licensee controls and surveys in the following radiologically

significant work areas within radiation areas, high radiation areas, and airborne

radioactivity areas in the plant to determine if radiological controls including surveys,

postings, and barricades were acceptable:

  • Auxiliary Building;
  • Containment Building; and
  • Spent Fuel Pool Area.

This inspection constitutes one sample as defined in IP 71121.01-5.

The inspectors reviewed the RWPs and work packages used to access these areas and

other high radiation work areas. The inspectors assessed the work control instructions

and control barriers specified by the licensee. Electronic dosimeter alarm set points for

both integrated dose and dose rate were evaluated for conformity with survey indications

and plant policy. The inspectors interviewed workers to verify that they were aware of

the actions required if their electronic dosimeters noticeably malfunctioned or alarmed.

This inspection constitutes one sample as defined in IP 71121.01-5.

The inspectors walked down and surveyed (using an NRC survey meter) these areas to

verify that the prescribed RWP, procedure, and engineering controls were in place; that

licensee surveys and postings were complete and accurate; and that air samplers were

properly located.

This inspection constitutes one sample as defined in IP 71121.01-5.

12 Enclosure

The inspectors also reviewed the licensees physical and programmatic controls for

highly activated and/or contaminated materials (non-fuel) stored within the spent fuel

pool or other storage pools.

This inspection constitutes one sample as defined in IP 71121.01-5.

b. Findings

No findings of significance were identified.

.2 Problem Identification and Resolution

a. Inspection Scope

The inspectors reviewed a sample of the licensees self-assessments, audits, Licensee

Event Reports (LERs), and Special Reports related to the access control program to

verify that identified problems were entered into the CAP for resolution.

This inspection constitutes one sample as defined in IP 71121.01-5.

The inspectors evaluated the licensees process for problem identification,

characterization, and prioritization and verified that problems were entered into the

CAP and resolved. For repetitive deficiencies and/or significant individual deficiencies

in problem identification and resolution, the inspectors verified that the licensees

self-assessment activities were capable of identifying and addressing these deficiencies.

This inspection constitutes one sample as defined in IP 71121.01-5.

The inspectors reviewed licensee documentation packages for all performance indicator

(PI) events occurring since the last inspection to determine if any of these PI events

involved dose rates in excess of 25 R/hr at 30 centimeters or in excess of 500 R/hr at

1 meter. Barriers were evaluated for failure and to determine if there were any barriers

left to prevent personnel access. Unintended exposures exceeding 100 millirem total

effective dose equivalent (or 5 rem shallow dose equivalent or 1.5 rem lens dose

equivalent) were evaluated to determine if there were any regulatory overexposures or if

there was a substantial potential for an overexposure.

This inspection constitutes one sample as defined in IP 71121.01-5.

b. Findings

No findings of significance were identified.

.3 Job-In-Progress Reviews

a. Inspection Scope

The inspectors observed the following two jobs that were being performed in radiation

areas, airborne radioactivity areas, or high radiation areas for observation of work

activities that presented the greatest radiological risk to workers:

13 Enclosure

  • Troubleshooting Pressurizer Heater Breaker; and
  • Negative Reactivity Testing of the Spent Fuel Pool Racks.

The inspectors reviewed radiological job requirements for these activities, including

RWP requirements and work procedure requirements.

This inspection constitutes one sample as defined in IP 71121.01-5.

Job performance was observed with respect to the radiological control requirements to

assess whether radiological conditions in the work area were adequately communicated

to workers through pre-job briefings and postings. The inspectors evaluated the

adequacy of radiological controls, including required radiation, contamination, and

airborne surveys for system breaches; radiation protection job coverage, including any

applicable audio and visual surveillance for remote job coverage; and contamination

controls.

This inspection constitutes one sample as defined in IP 71121.01-5.

a. Findings

No findings of significance were identified.

.4 High Risk Significant, High Dose Rate, High Radiation Area, and Very High Radiation

Area Controls

a. Inspection Scope

The inspectors held discussions with the Radiation Protection Manager concerning high

dose rate, high radiation area, and very high radiation area controls and procedures,

including procedural changes that had occurred since the last inspection, in order to

assess whether any procedure modifications substantially reduced the effectiveness and

level of worker protection.

This inspection constitutes one sample as defined in IP 71121.01-5.

The inspectors discussed with radiation protection supervisors the controls that were in

place for special areas of the plant that had the potential to become very high radiation

areas during certain plant operations. The inspectors assessed if plant operations

required communication beforehand with the radiation protection group, so as to allow

corresponding timely actions to properly post and control the radiation hazards.

This inspection constitutes one sample as defined in IP 71121.01-5.

The inspectors conducted plant walkdowns to assess the posting and locking of

entrances to high dose rate, high radiation areas, and very high radiation areas.

This inspection constitutes one sample as defined in IP 71121.01-5.

b. Findings

No findings of significance were identified

14 Enclosure

.5 Radiation Worker Performance

a. Inspection Scope

During job performance observations, the inspectors evaluated radiation worker

performance with respect to stated radiation safety work requirements. The inspectors

evaluated whether workers were aware of any significant radiological conditions in their

workplace, of the RWP controls and limits in place, and of the level of radiological

hazards present. The inspectors also observed worker performance to determine if

workers accounted for these radiological hazards.

This inspection constitutes one sample as defined in IP 71121.01-5.

The inspectors reviewed radiological problem reports for which the cause of the event

was due to radiation worker errors to determine if there was an observable pattern

traceable to a similar cause and to determine if this perspective matched the corrective

action approach taken by the licensee to resolve the reported problems. Problems or

issues with planned or completed corrective actions were discussed with the Radiation

Protection Manager.

This inspection constitutes one sample as defined in IP 71121.01-5.

b. Findings

No findings of significance were identified.

.6 Radiation Protection Technician Proficiency

a. Inspection Scope

During job performance observations, the inspectors evaluated radiation protection

technician performance with respect to radiation safety work requirements. The

inspectors evaluated whether technicians were aware of the radiological conditions in

their workplace, the RWP controls and limits in place, and if their performance was

consistent with their training and qualifications with respect to the radiological hazards

and work activities.

This inspection constitutes one sample as defined in IP 71121.01-5.

The inspectors reviewed radiological problem reports for which the cause of the event

was radiation protection technician error to determine if there was an observable pattern

traceable to a similar cause and to determine if this perspective matched the corrective

action approach taken by the licensee to resolve the reported problems.

This inspection constitutes one sample as defined in IP 71121.01-5.

b. Findings

No findings of significance were identified.

15 Enclosure

4. OTHER ACTIVITIES

4OA1 Performance Indicator Verification (71151)

.1 Reactor Coolant System Leakage

a. Inspection Scope

The inspectors sampled licensee submittals for the Reactor Coolant System

Leakage performance indicator for the period from the fourth quarter 2007 through

the third quarter 2008. To determine the accuracy of the PI data reported during those

periods, PI definitions and guidance contained in the Nuclear Energy Institute (NEI)

Document 99-02, Regulatory Assessment Performance Indicator Guideline,

Revision 5, was used. The inspectors reviewed the licensees operator logs and verified

the accuracy of a sample of calculations for the period of October 2007 through

September 2008 to validate the licensees submittals. Documents reviewed are listed in

the Attachment to this report.

This inspection constituted one reactor coolant system leakage sample as defined in

IP 71151-05.

b. Findings

No findings of significance were identified.

.2 Unplanned Transients per 7000 Critical Hours

a. Inspection Scope

The inspectors sampled licensee submittals for the Unplanned Transients per

7000 Critical Hours performance indicator for the period from the fourth quarter 2007

through the third quarter of 2008. To determine the accuracy of the PI data reported

during those periods, PI definitions and guidance contained in the NEI Document 99-02,

Regulatory Assessment Performance Indicator Guideline, Revision 5, was used. The

inspectors reviewed the licensees operator narrative logs and NRC Integrated

Inspection Reports for the period of October 2007 through September 2008 to validate

the accuracy of the submittals. Documents reviewed are listed in the Attachment to this

report.

This inspection constituted one unplanned transients per 7000 critical hours sample as

defined in IP 71151-05.

b. Findings

No findings of significance were identified.

.3 Safety System Functional Failures

a. Inspection Scope

The inspectors sampled licensee submittals for the Safety System Functional Failures

performance indicator for the period from the fourth quarter 2007 through the third

16 Enclosure

quarter 2008 to determine the accuracy of the PI data reported during those periods,

PI definitions and guidance contained in the NEI Document 99-02, Regulatory

Assessment Performance Indicator Guideline, Revision 5, and NUREG-1022, Event

Reporting Guidelines 10 CFR 50.72 and 50.73," definitions and guidance, were used.

The inspectors reviewed licensee event reports for the period of October 2007 through

September 2008 to validate the accuracy of the submittals. Documents reviewed are

listed in the Attachment to this report.

This inspection constituted one safety system functional failures sample as defined in

IP 71151-05.

.4 Mitigating Systems Performance Index - Cooling Water Systems

a. Inspection Scope

The inspectors sampled licensee submittals for the Mitigating Systems Performance

Index (MSPI) - Cooling Water Systems performance indicator for the period from the

fourth quarter 2007 through the third quarter of 2008 to determine the accuracy of the

PI data reported during those periods, PI definitions and guidance contained in the

NEI Document 99-02, Regulatory Assessment Performance Indicator Guideline,

Revision 5, were used. The inspectors reviewed the licensees operator narrative logs,

condition reports, MSPI derivation reports, event reports, and NRC Integrated Inspection

Reports for the period of October 2007 through September 2008 to validate the accuracy

of the submittals. The inspectors reviewed the MSPI component risk coefficient to

determine if it had changed by more than 25 percent in value since the previous

inspection, and if so, that the change was in accordance with applicable NEI guidance.

The inspectors also reviewed the licensees issue report database to determine if any

problems had been identified with the PI data collected or transmitted for this indicator

and none were identified. Documents reviewed are listed in the Attachment to this

report.

This inspection constituted one MSPI cooling water system sample as defined in

IP 71151-05.

b. Findings

No findings of significance were identified.

4OA2 Identification and Resolution of Problems (71152)

Cornerstones: Initiating Events, Mitigating Systems, Barrier Integrity, Emergency

Preparedness, Public Radiation Safety, Occupational Radiation Safety, and

Physical Protection

.1 Routine Review of items Entered Into the Corrective Action Program

a. Inspection Scope

As part of the various baseline inspection procedures discussed in previous sections of

this report, the inspectors routinely reviewed issues during baseline inspection activities

and plant status reviews to verify that they were being entered into the licensees CAP at

17 Enclosure

an appropriate threshold, that adequate attention was being given to timely corrective

actions, and that adverse trends were identified and addressed. Attributes reviewed

included: the complete and accurate identification of the problem; that timeliness was

commensurate with the safety significance; that evaluation and disposition of

performance issues, generic implications, common causes, contributing factors, root

causes, extent of condition reviews, and previous occurrences reviews were proper and

adequate; and that the classification, prioritization, focus, and timeliness of corrective

actions were commensurate with safety and sufficient to prevent recurrence of the issue.

Minor issues entered into the licensees CAP as a result of the inspectors observations

are included in the attached List of Documents Reviewed.

These routine reviews for the identification and resolution of problems did not constitute

any additional inspection samples. Instead, by procedure they were considered an

integral part of the inspections performed during the quarter and documented in

Section 1 of this report.

b. Findings

No findings of significance were identified.

.2 Daily Corrective Action Program Reviews

a. Inspection Scope

In order to assist with the identification of repetitive equipment failures and specific

human performance issues for follow-up, the inspectors performed a daily screening of

items entered into the licensees CAP. This review was accomplished through

inspection of the stations daily condition report packages.

These daily reviews were performed by procedure as part of the inspectors daily plant

status monitoring activities and, as such, did not constitute any separate inspection

samples.

b. Findings

No findings of significance were identified.

.3 Semi-Annual Trend Review

a. Inspection Scope

The inspectors performed a review of the licensees CAP and associated documents to

identify trends that could indicate the existence of a more significant safety issue. The

inspectors review was focused on repetitive equipment issues, but also considered the

results of daily inspector CAP item screening discussed in Section 4OA2.2 above,

licensee trending efforts, departmental performance reports and metrics, and licensee

human performance results. The inspectors review nominally considered the 6 month

period of July 2008 through December 2008, although some examples expanded

beyond those dates where the scope of the trend warranted.

18 Enclosure

The inspectors compared and contrasted their results with the results contained in the

licensees assessments. Corrective actions associated with a sample of the issues

identified in the licensees trending reports were reviewed for adequacy.

This review constituted a single semi-annual trend inspection sample as defined in

IP 71152-05.

b. Findings

No findings of significance were identified.

.4 Annual Sample: Review of Operator Workarounds

a. Inspection Scope

The inspectors evaluated the licensees implementation of their process used to identify,

document, track, and resolve operational challenges. Inspection activities included, but

were not limited to, a review of the cumulative effects of the Operator Work Arounds on

system availability and the potential for improper operation of the system, for potential

impacts on multiple systems, and on the ability of operators to respond to plant

transients or accidents.

The inspectors performed a review of the cumulative effects of Operator Work Arounds.

The documents listed in the Attachment were reviewed to accomplish the objectives of

the inspection procedure. The inspectors reviewed both current and historical

operational challenge records to determine whether the licensee was identifying operator

challenges at an appropriate threshold, had entered them into their CAP, and proposed

or implemented appropriate and timely corrective actions which addressed each issue.

Reviews were conducted to determine if any operator challenge could increase the

possibility of an Initiating Event, if the challenge was contrary to training, required a

change from long-standing operational practices, or created the potential for

inappropriate compensatory actions. Additionally, all temporary modifications were

reviewed to identify any potential effect on the functionality of Mitigating Systems,

impaired access to equipment, or required equipment uses for which the equipment was

not designed. Daily plant and equipment status logs, degraded instrument logs, and

operator aids or tools being used to compensate for material deficiencies were also

assessed to identify any potential sources of unidentified operator workarounds.

This review constituted one operator workaround annual inspection sample as defined in

IP 71152-05.

b. Findings

No findings of significance were identified.

.5 Selected Issue Follow-Up Inspection: Criticality Controls in the Spent Fuel Pool

a. Inspection Scope

In July of 2008, the licensee tested some spent fuel storage rack locations to determine

if the neutron poison built into the storage rack continued to meet assumptions in the

19 Enclosure

criticality analysis. The testing revealed that the neutron absorption capability of the

Spent Fuel Pool racks had degraded and in some cases no longer met assumptions

contained within the criticality analysis. The licensee implemented additional criticality

controls in the spent fuel pool and informed the NRC of the controls by letter dated

August 27, 2008. After reviewing the controls, the NRC issued Confirmatory Action

Letter (CAL) RIII-08-003 to confirm the commitments made by Entergy Nuclear

Operations.

During this inspection period, the inspectors validated that the licensee implemented the

requirements of the CAL. Specific actions included:

  • review of the licensees basis for criticality safety for proposed fuel moves;
  • verification that fuel moves complied with CAL requirements;
  • observation of additional testing of the spent fuel pool neutron absorption

capability.

The inspectors concluded that the licensee complied with the requirements of the CAL.

This review constituted one in-depth problem identification and resolution sample as

defined in IP 71152-05.

b. Findings

No findings of significance were identified.

.6 Selected Issue Follow-Up Inspection: Deviation between Estimated and Actual Critical

Positions for the August 9, 2008, Startup

a. Inspection Scope

The inspectors reviewed the data and associated procedures for the August 9, 2008,

reactor startup from a forced outage. The inspectors also interviewed licensee staff and

searched for relevant operating experience and past similar issues identified by the NRC

at other plants. Corrective action documents related to the issue were reviewed for

appropriate categorization and action. During the August 9, 2008, reactor startup, the

reactor attained criticality with rods withdrawn to a position of 0.28 percent delta rho

above that predicted by the estimated critical position. Although the deviation was below

the TS limit of 1 percent delta rho and the licensee administrative limit of 0.5 percent

delta rho, the deviation was abnormally high. The licensee reviewed the error in

condition report CR-PLP-2008-3439. The cause evaluation concluded the error

occurred due to boron 10 depletion in the primary coolant system. B-10 depletion

occurs due to B-10 burnup via neutron absorption. Naturally occurring boron contains

19.8 atom percent B-10 with the remainder B-11. As B-10 (which has a much larger

neutron absorption cross-section) absorbs neutrons, the ratio of B-10 to B-11 decreases.

This change alters the effective boron poison strength of the primary coolant for a given

boron concentration. When fresh boron is added, the effective boron concentration

changes. In this instance, the licensee added fresh boron during the shutdown but did

not account for it while determining an estimated critical position. As part of the

corrective actions, the licensee identified several items to help address this issue. The

licensee did have some guidance in EM-04-24, their Critical Prediction and Critical

Approach procedure, in regards to when to apply a B-10 correction. The licensee plans

20 Enclosure

to enhance this portion of the procedure for clarity and ease of conducting a B-10

correction, if deemed necessary. In addition, the licensee benchmarked other fleet

plants to determine an optimum isotopic sampling frequency to track the depletion of

B-10. The licensee is proceeding with plans to obtain and ship samples for analysis

more frequently.

Based on data provided by the licensee, the last time there was a deviation of this

magnitude or greater was June 1998 with a 0.393 percent delta rho error. Beyond that,

in October 1997 there was a 0.437 percent deviation. The October 1997 deviation was

determined to be mostly due to B-10 depletion. A search for relevant operating

experience and previous findings was conducted with no relevant results. The

inspectors reviewed the licensees reactivity management event classification guidelines

and corrective action process procedure to validate appropriate categorization of the

issue. No deficiencies were identified.

This review constituted one in-depth problem identification and resolution sample as

defined in IP 71152-05.

.7 Selected Issue Follow-Up Inspection: Licensee Compliance with the Station Blackout

(SBO) Rule Assumptions

a. Inspection Scope

While performing an operability evaluation on inadequate testing of the CR HVAC

system (discussed in Section 1R15 of this report), the inspectors noted that the

licensees revision to the underlying calculation for the systems surveillance test may

not have taken into account SBO Rule (10 CFR 50.63) requirements. The inspectors

interviewed licensee personnel and reviewed design basis documents, the UFSAR, and

docketed correspondence between the NRC and the licensee. The inspectors review

included the analysis performed by the licensee to demonstrate compliance with the

SBO rule. Based on the review, the inspectors concluded the licensee remained

compliant with the license condition for SBO but noted weaknesses in the licensees

program. Noted weaknesses included:

  • Lack of operations staff awareness of impacts on SBO rule compliance with

elevated temperatures in the control room

  • Lack of programmatic controls for maintaining compliance with the plants SBO

assumptions

The licensee generated two condition reports (CR-PLP-2008-5023 and

CR-PLP-2008-5074) to address the issue.

This review constituted one in-depth problem identification and resolution sample as

defined in IP 71152-05.

b. Findings

No findings of significance were identified.

21 Enclosure

4OA3 Follow-Up of Events and Notices of Enforcement Discretion (71153)

.1 (Closed) LER 05000255/2008-05-00, Completion of Plant Shutdown Required by TSs

On August 5, 2008, the licensee began a planned shutdown to replace leaking Control

Rod Drive Mechanism seals. At 97 percent power, a relief valve, RV-2006, in the

letdown system lifted resulting in primary coolant leakage in excess of the TS limit of

1 gallon per minute of unidentified leakage. The licensee made a 4-hour report to the

NRC and completed a plant shutdown as required by TSs. The licensee determined that

the relief valve lifted when a second charging pump started per the pressurizer level

control program. Historically, the licensee has experienced difficulties with control of

pressure in the letdown system during operation of charging pumps due to performance

of controllers in the system. In addition, the licensee determined that the setpoint of the

relief valve will drift as a result of previous relief valve lifts. During the outage, the

licensee replaced the relief valve. In this event, leak rates of approximately 4 gallons per

minute occurred when the relief valve lifted. Because the line discharged into a quench

tank with multiple sources, the licensee treated the leakage as unidentified leakage. The

licensee exited the Limiting Condition for Operation (LCO) when the plant entered

Mode 5 and the LCO no longer applied. Documents reviewed as part of this inspection

are listed in the Attachment. The inspectors did not identify any additional safety issues.

This LER is closed.

This event follow-up review constituted one sample as defined in IP 71153-05.

.2 (Closed) LER 05000255/2008-06-00, Emergency Diesel Generator Inoperable in Excess

of TSs Requirements

a. Inspection Scope

On February 19, 2008, during performance of planned maintenance on the 1-2 EDG,

licensee personnel discovered foreign material (metal fragments) in the valve assembly

area of the 1-2 EDG cylinder 2L. The metal fragments were identified to be broken

pieces of the valve seat spring lock associated with the cylinder 2L inboard exhaust

valve. These fragments were discovered by workers during an unrelated maintenance

activity involving the snubber valves. Due to some physical interference between

components during work, the valve cover for cylinder 2L needed to be removed to

complete some of the snubber valve maintenance. When the cover was removed,

workers noted the spring lock material described above. The licensee performed an

apparent cause evaluation that included a failure analysis performed by Fairbanks

Morse Engine. The licensee determined that the spring lock was damaged due to a

condition discovered in March 2000. While performing maintenance on March 21, 2000,

licensee personnel discovered that the valve yoke retaining lock nut had fallen off one of

the valve assemblies for cylinder 2L. The licensee determined that because of this, the

adjusting screw backed out such that the valve yoke was able to strike the spring seat

instead of the adjusting nut striking the valve stem, as designed. This resulted in cyclical

side loading of the valve assembly which initiated a fatigue crack on the inside diameter

of the spring lock. Eventually it failed, resulting in the pieces discovered on

February 19, 2008. The licensee inspected the other spring locks on the 1-2 EDG and

found no discrepancies. An extent-of-condition review was performed for the 1-1 EDG

by the licensee. The licensee concluded that there was high assurance that a similar

22 Enclosure

condition does not exist on the 1-1 EDG. The licensee plans to inspect valve seat spring

locks for the 1-1 EDG during the next scheduled preventative maintenance outage.

The licensee reviewed the corrective actions for the March 2000 discovery of the lock

nut that fell off and the associated backing-out of the adjusting screw. To resolve the

issue, the nut was returned to the proper position and torqued. In addition, the other

retaining nuts were inspected and found to be acceptable. There were no documented

inspections of any other components in the valve assembly area under the valve cover.

Following the discovery, the licensee did not change the routine preventative

maintenance requirements. The inspectors identified one finding. This LER is closed.

This event follow-up review constituted one sample as defined in IP 71153-05.

b. Findings

Introduction: On February 19, 2008, a Green self-revealed finding and associated NCV

of TS requirement 3.8.1.b became evident when licensee personnel discovered metal

fragments in the valve assembly area of the 1-2 EDG cylinder 2L. Subsequent

evaluation by the licensee determined that the diesel would not be able to function for its

30-day mission time and was inoperable for a period of time greater than allowed by TS.

Description: While performing maintenance on the 1-2 EDG, licensee personnel noted

metal fragments in the valve cover for the 1-2 EDG. The licensee investigated the

source of the metal fragments and discovered that the spring lock for an exhaust valve

had failed. The licensee reviewed maintenance history for the diesel and determined

that a lock nut had backed off an adjustment screw in 2000. The licensee contracted the

diesel vendor to evaluate the condition of the cylinder head in order to determine the

cause of the spring lock failure. The vendor concluded that the loss of the lock nut

caused the adjusting screw to drift and allowed the yoke arm to contact the valve spring

seat. The abnormal operating condition likely created cracks in the spring lock that

propagated even after replacement of the lock nut. In 2000, the licensee limited

corrective actions to replacing the lock nut and checking the lock nuts on other cylinders.

The licensee did not evaluate potential degradation of other components due to the

abnormal operation of the valve.

The licensee evaluated the as-found condition and concluded that a sufficient amount of

the spring lock remained on the valve to assure continued operation of the EDG for at

least 24 hours2.777778e-4 days <br />0.00667 hours <br />3.968254e-5 weeks <br />9.132e-6 months <br />. However, the wear rates could not be determined to assure the EDG

would operate for 30 days. The licensee identified that a potential failure mode was loss

of the valve into the associated cylinder and subsequent damage to the turbo charger

through transport of generated debris. As corrective action, the licensee replaced the

spring lock and inspected the others on the 1-2 EDG. An extent of condition was

performed for the 1-1 EDG, and inspections are planned for the 1-1 EDG as well. The

condition was entered into the licensees CAP as CR-PLP-2008-0822.

Analysis: The inspectors determined that the inoperability of the diesel generator for

longer than TS allowed outage time represented a performance deficiency that

warranted a significance determination. Through review of the condition reports related

to the missing lock nut in 2000, the inspectors determined that the licensee could

reasonably be expected to foresee and correct the condition of the cylinder/valve

operating mechanism. In 2000, the licensee did not evaluate potential adverse effects

23 Enclosure

on the valve and related components. Corrective actions at the time also indicated the

remaining lock nuts were only checked hand-tight. The inspectors determined the issue

is more than minor because it affected the mitigating system cornerstone objective of

ensuring the reliability and capability of mitigating systems. The inspectors performed a

phase 1 screen on the issue in accordance with IMC 0609 and determined that since the

EDG was inoperable for greater than the TS allowed outage time, support from the

region-based senior risk analyst was needed to determine risk significance. Based on

vendor analysis, the licensee concluded that the EDG would likely operate in excess of

24 hours2.777778e-4 days <br />0.00667 hours <br />3.968254e-5 weeks <br />9.132e-6 months <br />, but not for the 30-day mission time required by the license. Since the EDG

would function for the Probable Risk Assessment mission time, the senior risk analyst

determined the issue would screen as Green using the phase 1 worksheets. No cross-

cutting aspect was assigned because the review dated back to 2000, therefore, this

issue is not indicative of current plant performance.

Enforcement: Technical Specification LCO 3.8.1 states, in part, that two diesel

generators each capable of supplying one train of the Class 1E AC electrical power

distribution system shall be operable. The TS action requirement requires a plant

shutdown if the associated EDG is inoperable for greater than 7 days. Contrary to the

required action statements, on February 19, 2008, a failed spring lock for one of the

exhaust valves on the 1-2 EDG was discovered. This resulted in an EDG inoperability

beyond the allowed required action times. The failure was determined to have been the

result of an issue discovered in 2000 involving a lock nut that had fallen off of the

exhaust valve assembly. Further analysis led to a conclusion by the licensee that the

condition would likely allow the EDG to run for the 24-hour Probabilistic Risk

Assessment mission time but not the 30-day mission time. Because the finding is of

very low safety significance and has been entered into the licensees CAP as

CR-2008-0822, this violation of TS requirement 3.8.1.b is being treated as an NCV,

consistent with Section VI.A of the NRC Enforcement Policy.

(NCV 05000255/2008005-02 Emergency Diesel Generator Inoperable in Excess of

TS Requirements).

4OA5 Other Activities

.1 Observations of Security

a. Inspection Scope

During the inspection period, the inspectors conducted observations of security force

personnel and activities to ensure that the activities were consistent with licensee

security procedures and regulatory requirements relating to nuclear plant security.

These observations took place during both normal and off-normal plant working hours.

These quarterly resident inspector observations of security force personnel and activities

did not constitute any additional inspection samples. Rather, they were considered an

integral part of the inspectors' normal plant status review and inspection activities.

b. Findings

No findings of significance were identified.

24 Enclosure

.2 Implementation of Temporary Instruction (TI) 2515/176, Emergency Diesel generator

Technical Specification Surveillance Requirements Regarding Endurance and Margin

testing

a. Inspection Scope

The objective of TI 2515/176 was to gather information to assess the adequacy of

nuclear power plant emergency diesel generator endurance and margin testing as

prescribed in plant-specific TSs. The inspectors reviewed the licensee's TS,

procedures, and calculations, and interviewed licensee personnel to complete the TI.

The information gathered for this TI was forwarded to the Office of Nuclear Reactor

Regulation for further review and evaluation on December 17, 2008. This TI is

complete at Palisades Nuclear Plant; however, this TI 2515/176 will not expire until

August 31, 2009. Additional information may be required after review by the Office of

Nuclear Reactor Regulation.

b. Findings

No findings of significance were identified.

4OA6 Management Meetings

.1 Exit Meeting Summary

On January 22, 2009, the inspectors presented the inspection results to Thomas Kirwin

and other members of the licensee staff. The licensee acknowledged the issues

presented. The inspectors confirmed that none of the potential report input discussed

was considered proprietary. A follow-up phone exit meeting was held by the NRC with

Ms. B. Dotson and Mr. C. Sherman on February 2, 2009 to discuss additional inspection

results.

.2 Interim Exit Meetings

Interim exits were conducted for:

  • The annual review of emergency action level and emergency plan changes with

the licensee's Senior Emergency Planning Coordinator, Mr. M. Sweet via

telephone on December 30, 2008.

  • The results of the access control to radiologically significant areas inspection with

the Plant Manager, Mr. T. Kirwin, and other members of your staff, on

December 12, 2008.

  • A telephone exit for TI 2515/176 was conducted with John Broschak,

Entergy/Engineering Director and other Licensee staff on December 2, 2008.

The inspectors confirmed that none of the potential report input discussed was

considered proprietary.

25 Enclosure

4OA7 Licensee-Identified Violations

The following violation of very low significance (Green) were identified by the licensee

and are violations of NRC requirements which meet the criteria of Section VI of the

NRC Enforcement Policy, NUREG-1600, for being dispositioned as an NCV.

100 mR/hr to be posted as a High Radiation Area and barricaded. Contrary to this,

on October 18, 2008, the high radiation area posting and barricade did not provide

an adequate barricade around areas of the room having dose rates greater than

100 mR/hr in the west engineered safeguards room. This was identified in the

licensees corrective action program as CR-PLP-2008-04310. The finding was

determined to be of very low safety significance because it was not an ALARA

planning issue, there was no overexposure nor substantial potential for

overexposure, and the licensees ability to assess dose was not compromised.

ATTACHMENT: SUPPLEMENTAL INFORMATION

26 Enclosure

SUPPLEMENTAL INFORMATION

KEY POINTS OF CONTACT

Licensee

C. Schwarz, Site Vice President

V. Beilfuss, Project Manager

J. Broschak, Engineering Director

N. Brott, Emergency Preparedness Coordinator

J. Burnett, RETS/REMP Specialist

T. Davis, Regulatory Compliance

B. Dotson, Regulatory Compliance

J. Fontaine, Senior Emergency Planning Coordinator

J. Ford, Corrective Action Manager

T. Kirwin, Plant General Manager

L. Lahti, Licensing Manager

B. Nixon, Assistant Operations Manager

T. Shewmaker, Chemistry Manager

C. Sherman, Radiation Protection Manager

M. Sicard, Operations Manager

G. Sleeper, Assistant Operations Manager

E. Williams, Radiation Protection Supervisor

Nuclear Regulatory Commission

J. Giessner, Chief, Branch 4

1 Attachment

LIST OF ITEMS OPENED, CLOSED, AND DISCUSSED

Opened

05000255/2008005-01 NCV Inadequate Testing of Control Room Chillers (Section 1R15)05000255/2008005-02 NCV Emergency Diesel Generator Inoperable in Excess of

Technical Specification Requirements (Section 4OA3)

Closed

05000255/2008005-01 NCV Inadequate Testing of Control Room Chillers (Section 1R15)05000255/2008005-02 NCV Emergency Diesel Generator Inoperable in Excess of

Technical Specification Requirements (Section 4OA3)

05000255/2008005 LER Completion of Plant Shutdown Required by Technical

Specifications (Section 4OA3)

05000255/2008006 LER Emergency Diesel Generator Inoperable in Excess of

Technical Specification Requirements (Section 4OA3)

2 Attachment

LIST OF DOCUMENTS REVIEWED

The following is a partial list of documents reviewed during the inspection. Inclusion on this list

does not imply that the NRC inspector reviewed the documents in their entirety, but rather that

selected sections or portions of the documents were evaluated as part of the overall inspection

effort. Inclusion of a document on this list does not imply NRC acceptance of the document or

any part of it, unless this is stated in the body of the inspection report.

1R01 Adverse Weather Protection

- CR-PLP-2007-5672, 1-3 DG cold weather vent covers fall out of the vents, November 7, 2007

- CR-PLP-2007-5934, The Insulating Box for SIRW Tank Level Instrument LT-0331 is Bent,

November 21, 2007

- SOP-23, Plant Heating System, Revision 27

1R04 Equipment Alignment

- Drawing M-204, Safety Injection, Containment Spray, and Shutdown Cooling System

- Drawing M-208, Service Water System

- Drawing M-213, Service Water, Screen Structure, and Chlorinator

- FSAR Chapter 9.1.1, Service Water System, Revision 25

- Procedure No. 4.02, Control of Equipment, Revision 47

- SOP-15, Service Water System, Revision 47

- SOP-22, Emergency Diesel Generators, Revision 45

- SOP-3, High Pressure Safety Injection System, Revision 75

1R05 Fire Protection

- Fire Hazard Analysis, Palisades Plant, Revision 7

1R11 Licensed Operator Requalification Program

- Procedure SEP, Site Emergency Plan, Revision 16

- Simulator Exercise Guide for November 17, 2008 Licensed Operator Requalification Drill

1R12 Maintenance Effectiveness

- CR-PLP-2007-01807, K-6B Placed in Maintenance Rule Category a(1), May 3, 2007

- CR-PLP-2007-01145, K-6B exceeds Maintenance Rule Unavailability Hours, March 13, 2007

- CR-PLP-2008-01424, EG-30A, 1-2 Emergency Diesel Generator Alarm Panel Failure (K-6B),

March 28, 2008

- CR-PLP-2008-03141, During the Performance of MO-7A-2, Emergency Diesel Generator 1-2,

Difficulties were Encountered in Attempting to Match Generator Output Voltage to Match Bus

1D Voltage, July 21, 2008

- CR-PLP-2008-03142, While Increasing Load on 1-2 Diesel Generator, the Cyclinder Petcock

for 9R Came Open, July 21, 2008

- CR-PLP-2008-0822, Broken Valve Keeper (Spring Seat Lock) Found on Cylinder 2-L of the 1-

2 Emergency Diesel Generator, February 19, 2008

- EGAD-EP-10, Maintenance Rule Scoping Document, Revision 5

- EM-20-01, Emergency Diesel Generator Reliability Program, Revision 2

3 Attachment

- Emergency Diesel Generator Related Plant Operating Log Entries from May 2007 thru

September 2008

- Emergency Diesel Generators Palisades Plant Health Report, 3rd Quarter 2008

- EN-DC-198, Emergency Diesel Generator Reliability Program, Revision 1

- EN-DC-203, Maintenance Rule Program, Revision 1

- EN-DC-204, Maintenance Rule Scope and Basis, Revision 1

- EN-DC-205, Maintenance Rule Monitoring, Revision 2

- EN-DC-206, Maintenance Rule (a)(1) Process, Revision 1

- NUMARC 93-01, Industry Guideline for Monitoring the Effectiveness of Maintenance at

Nuclear Power Plants, Revision 2

- Palisades Plant Maintenance Rule Unavailability Performance Indicator Data thru

September 2008

1R13 Maintenance Risk Assessments and Emergent Work Control

- Procedure No. 4.02, Control of Equipment, Revision 47

- SOP-3, High Pressure Safety Injection System, Revision 75

- FSAR Chapter 9.7, Auxiliary Feedwater System, Revision 26

1R15 Operability Determinations

- Calculation 022-M-001, Control Room Required Cooling Load, Revision 0 and markup

- CR-4580, Diesel Load Calculation, November 11, 2008

- CR-PLP-2008-03993, RT-202, Control Room Heat Removal Capability Test Operability Issue,

September 24, 2008

- CR-PLP-2008-04344, Control room HVAC mounting configuration of solenoid valves to their

positioners not in accordance with design drawings, October 21, 2008

- CR-PLP-2008-04580, Diesel Load Calculation did not Account for Worst Case Containment

Air Cooler Load, November 11, 2008

- CR-PLP-2008-4431, Containment Spray Header Pressure Indicator Indicating Below

Technical Specification Limit after Maintenance, October 28, 2008

- DBD 1.06, Control Room HVAC System, Revision 7

- DBD-2.03, Containment Spray System, Revision 7

- EA-SBO-1, Station Blackout Coping Evaluation for 10CFR50.63, Revision 2

- EC Markup EC-10988, Control Room Cooling Load, Revision 0

- ESSO-1, Containment Spray Header Fill, Revision 12

- FSAR Chapter 6.2, Containment Spray, Revision 26

- FSAR Chapter 9.8, Heating, Ventilation, and Air Conditioning System, Revision 26

- MO-29, Engineered Safety System Alignment, Revision 36

- RT-202, Control Room HVAC Heat Removal Capability, Revisions 3, 9, and 10

1R18 Plant Modifications

- EC-10638, Disable Fast Transfer

1R19 Post Maintenance Testing

- CR-PLP-2006-2485, Control Rods Failed RO-19, May 2, 2006

- CR-PLP-2480, CRD-8 Failed to Drive CRD-8, May 1, 2006

- DBD-1.03, Auxiliary Feedwater System Design Basis Document, Revision 7

- FSAR Chapter 9.7, Auxiliary Feedwater System, Revision 26

4 Attachment

- Procedure No. 9.20, Attachment 3, Process Control Sheet dtd 11/5/08 for Auxiliary Feedwater

System 18-Month Test Procedure, Revision 24

- RO-127, Auxiliary Feedwater System, 18-Month Test Procedure, Revision 7

- WO #51634185, P/S-0737A, Replace Power Supply During 1R20

- WO 00168249, MC1000-03 has Failed, October 12, 2008

- WO 0019168, RO-19 Control Rod Position Verification, May 2, 2006

- WO 51631052, Control Rod Position Verification, October 12, 2007

- WO002981980, Control Rod Position Verification, May 3, 2006

- EC-9282, Provide UPS Power for Perimeter Intrusion Detection and Monitoring Equipment,

October 17, 2008

- WO 00160408, Upgrade to Security UPS System, October 17, 2008

1R22 Surveillance Testing

- ASME OM Code 2001, Subsection ISTB

- EM-09-04, Inservice Testing of Selected Safety-Related Pumps, Revision 23

- QO-15 Basis Document for Inservice Test Procedure-Component Cooling Water Pumps,

Revision 14

- QO-15, Inservice Test Procedure, Component Cooling Water Pumps, Revision 26

- RO-146, Comprehensive Pump Test Procedure, Component Cooling System Pumps P-52A,

P-52B, and P-52C, Revision 1

- RO-52, Fire Suppression Water System Functional Test; Fire Pump Capacity Test,

Revision 27

- RPS-I-7, Anticipated Transient Without Scram (ATWS) Calibration/Functional Test,

October 22, 2008

- WO 51662292, Fire Suppress Wtr Sys Pump Capacity Func, September 23, 2008

1EP4 Emergency Action Level and Emergency Plan Changes

- Attachment 9.2, 10 CFR 50.54(q) Evaluation/Screening, Revisions 17 and 49

- EI-1, Emergency Classification and Actions, Revisions 48 and 49

- Palisades Nuclear Plant Site Emergency Plan, Revisions 16 and 17

1EP6 Drill Evaluation

- Procedure SEP, Site Emergency Plan, Revision 16

- NEI-99-02, Regulatory Assessment Performance Indicator Guideline, Revision 5

- Fourth Quarter Integrated Training Drill, November 5, 2008

- Tabletop Drill, December 17, 2008

2OS1 Access Control to Radiologically Significant Areas

- CR-PLP-2007-04378, Ensure that all Requirements Associated with Control of Very High

Radiation Areas are Properly Assessed, dated September 23, 2007

- CR-PLP-2007-4383, Concerns Have Been Made Regarding Use of the New Fuel Elevator,

dated September 24, 2007

- CR-PLP-2008-04310, West Engineered Safeguards Room Dose Rates Warranted High

Radiation Area Posting, dated October 18, 2008

- EAR 2001-0518, Evaluate Current Mechanical Stop on New Fuel Elevator for Design

Function, Revision 0

- EN-RP-100, Radworker Expectations, Revision 2

5 Attachment

- EN-RP-101, Access Control For Radiologically Controlled Areas, Revision 4

- EN-RP-108, Radiation Protection Posting, Revision 7

- EN-RP-141, Job Coverage, Revision 4

- EN-RP-151, Radiological Diving Revision 2

- QA-14-2008-PLP-01, Quality Assurance Report, Radiation Protection, dated May 14, 2008

- Radiation Work Permit 20080015 and Associated ALARA File, Containment Activities During

Power Operations, Revision 3

- Radiation Work Permit 20080108 and Associated ALARA File, Badger Testing in the Spent

Fuel Pool, Revision 0

- SC-91-095-07, New Fuel Elevator Travel Limit Switch and Control Console Modification,

Revision 1

- Snapshot Assessment, Incorporation of Radiation Protection Hold Points and Radiation

Protection Notification into Palisades Operation Procedures, June 13, 2008

4OA1 Performance Indicator Verification

- Cooling Water System Mitigating System Performance Indicator Validation Packages, Fourth

Quarter 2007 thru Third Quarter 2008

- DWO-1, Operators Daily/Weekly Items Modes 1,2,3, and 4 Basis Document, Revision 53

- DWO-1, Operators Daily/Weekly Items Modes 1,2,3, and 4, Revision 84

- MSPI Margin Report for Cooling Water System, Period ending September 2008

- LER 05000255/2008-002-00, Breaker Cubicle Failure Results in High Pressure Safety

Injection Pump Inoperability

- LER 05000255/2007-007-00, Fuel Handling Area Ventilation System Inoperable

- LER 05000255/2007-008-00, Auxiliary Feedwater Pump Inoperable in excess of technical

Specification Limits Due to a Postulated steam Line Break

- Log Entries associated with Cooling Water System Equipment, 1 October 2007 thru 30

September 2008

- Selected Palisades Plant Operating Logs from Fourth Quarter 2007 thru Third Quarter 2008

- NEI-99-02, Regulatory Assessment Performance Indicator Guideline, Revision 5

4OA2 Problem Identification and Resolution

- 06-01 OWA, Auxiliary Feedwater Pumps P-8A, B, C Suction Source, May 23, 2008

- 07-02 OWA, 2400VAC Busses 1C, 1D, 1E, May 14, 2007

- 08-01 OB, 2400/4160VAC MOC Switch Required Inspections, May 14, 2008

- 08-01 OWA, Condensate Pump P-2B Degraded Pressure, December 6, 2007

- Corrective Action X, Basis for Fuel Assembly Moves in Palisades Spent Fuel Pool,

November 6 2008

- CR-PLP-2008-3439, The Estimated Critical Position, although Well Within Acceptance

Criteria, was not as Accurate as Typical for Palisades, August 9, 2008

- CR-PLP-2008-01748, 1-1 Diesel Fuel Oil Supply Line Rubbing, April 19, 2008

- CR-PLP-2008-01749, 1-1 Diesel Fuel Oil Supply Line Rubbing, April 19, 2008

- CR-PLP-2008-05023, NRC has questioned the basis, justification, and control of initial control

room temperature assumption in the heatup analysis of the Palisades station blackout (SBO)

event, December 12, 2008

- CR-PLP-2008-05074, An Administrative Issue was Identified During Review of Documents

Provided to the NRC Related to Palisades Compliance with SBO Rule, December 17, 2008

- EA-APR-95-023, Room heatup after loss of ventilation under Appendix R scenario in the

control room, 1C and 1D switchgear rooms, battery rooms, containment area, and EDG rooms

- EM-04-24, Palisades Critical Prediction and Critical Approach, Revision 8

6 Attachment

- EN-LI-102, Corrective Action Process, Revision 10

- EN-OP-103, Reactivity Management Program, Revision 3

- FSAR Chapter 8.1.5, Station Blackout, Revision 25

- Letter to Gerald Slade, Palisades Plant Station Blackout Analysis, Safety Evaluation

(TAC No. 68578), May 20, 1991

- Letter to Gerald Slade, Palisades Plant-Station Blackout Analysis-Safety Evaluation

(TAC No. M68578), June 25, 1992

- Letter to John Ellegood, Notification of Fuel Moves Planned -Palisades Spent Fuel Pool

Region 1 to Region 2, November 6, 2008

- Letter to the NRC, Palisades Plant-Station Blackout Analysis, Safety Evaluation

(TAC No. 68578), August 1, 1991

- NET-299-01, BADGER Test Campaign at Palisades Nuclear Plant, October 8, 2008

- NUMARC 87-00, Guidelines and Technical Bases for NUMARC Initiatives Addressing Station

Blackout at Light Water Reactors, Revision 1

- ODMI Implementation Action Plan, P-2B Condensate Pump Degraded Performance,

November 18, 2007

- Operator Work Arounds / Burdens, October 14, 2008 Index

- Palisades Administrative Procedure 4.12, Operator Work-Around Program, Revision 5

- Palisades Operator Aggregate Index Reports, July through October 2008

- CR-PLP-2006-04702, Adverse Trend in Power Supply Reliability, October 3, 2006

- EN-LI-121, Entergy Trending Process Third Quarter Report, Revision 7

- CR-PLP-2008-04279, Adverse Trend in Power Supplies, October 16, 2008

- CR-PLP-2008-03203, Emerging Trend in Control of Equipment Positioning, July 25, 2008

- SOP-24, Ventilation and Air Conditioning System, Revision 52

- Letter to NRC, Commitments to Address degraded Spent Fuel Pool Storage Rack Neutron

Absorber, August 27, 2008

- Spent Fuel Pool Shuffle Sequence, November 7, 2008

- Letter to John Ellegood, Notification of Fuel Moves Planned -Palisades Spent Fuel Pool

region 1 to region 2, November 17, 2008

4OA3 Follow-up of Events and Notices of Enforcement Discretion

- CR-PLP-2008-03328, Plant Exceeded Technical Specification Limit for Unidentified Leak

Rate, August 5, 2008

- LER 05000255/2008-05-00, Completion of Plant Shutdown required by Technical

Specifications, Revision 0

- LER 05000255/2008-06-00, Emergency Diesel Generator Inoperable in Excess of Technical

Specification Requirements, Revision 0

- CR-PLP-2008-00822, Broken Valve Keeper (Spring Seat Lock) Found on Cylinder 2L of the

1-2 Emergency Diesel Generator, February 19, 2008

- CR-PLP-2000-00556, EDG 1-2 Valve Yoke Retaining Nut on Cylinder 2L Was Not Attached,

March 21, 2000

- EPS-M-14, Diesel Generator Periodic Maintenance, Revision 17

- EPS-M-15, Diesel Generator 1-2 Refueling Frequency Maintenance, Revision 1

4OA5 Other Activities

- Procedure No. RO-128-1; Diesel Generator 1-1 24 Hour Load Run; Revision 13

- Procedure No. RO-128-2; Diesel Generator 1-2 24 Hour Load Run; Revision 12

- Calculation No. EA-ELEC-LDTAB-005; Emergency Diesel Generator 1-1 & 1-2 Steady State

Loading; Revision 8

7 Attachment

LIST OF ACRONYMS USED

AFW Auxiliary Feed Water

CAL Confirmatory Action Letter

CAP Corrective Action Program

CFR Code of Federal Regulations

CR Condition Report

CR HVAC Control Room Heating, Ventilation and Air Conditioning

EDG Emergency Diesel Generator

HPSI High Pressure Safety Injection

IMC Inspection Manual Chapter

LCO Limiting Condition for Operations

LER Licensee Event Report

MSPI Mitigating Systems Performance Index

NEI Nuclear Energy Institute

NCV Non-Cited Violation

NRC U.S. Nuclear Regulatory Commission

PI Performance Indicator

RWP Radiation Work Permits

SBO Station Black Out

SDP Significance Determination Process

TS Technical Specification

UFSAR Updated Final Safety Analysis Report

8 Attachment