ML062080742

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IR 05000348-06-003, IR 05000364-06-003, 07200042-06-001- Farley Inspection Report 2006003
ML062080742
Person / Time
Site: Farley, 07200042  
Issue date: 07/27/2006
From: Scott Shaeffer
Reactor Projects Branch 2
To: Sumner H
Southern Nuclear Operating Co
References
IR-06-003
Download: ML062080742 (38)


See also: IR 05000348/2006003

Text

July 27, 2006

Southern Nuclear Operating Company, Inc.

ATTN: Mr. H. Lewis Sumner

Vice President - Farley Project

P. O. Box 1295

Birmingham, AL 35201-1295

SUBJECT:

JOSEPH M. FARLEY NUCLEAR PLANT - NRC INTEGRATED INSPECTION

REPORT 05000348/2006003, 05000364/2006003, AND 07200042/2006001

Dear Mr. Sumner:

On June 30, 2006, the U.S. Nuclear Regulatory Commission (NRC) completed an inspection at

your Joseph M. Farley Nuclear Plant, Units 1 and 2. The enclosed integrated inspection report

documents the inspection findings, which were discussed on July 7, 2006, with Mr. Randy

Johnson and other members of your staff.

The inspection examined activities conducted under your license as they relate to safety and

compliance with the Commissions rules and regulations and with the conditions of your license.

The inspectors reviewed selected procedures and records, observed activities, and interviewed

personnel.

This report documents two inspector identified findings and one self-revealing finding, all of very

low safety significance (Green). These findings were determined to involve violations of NRC

requirements. However, because of the very low safety significance and because they were

entered into your corrective action program, the NRC is treating these findings as non-cited

violations (NCVs), in accordance with Section VI.A of the NRCs Enforcement Policy. If you

contest these NCVs, you should provide a response within 30 days of the date of this inspection

report, with the basis for your denial, to the United States Nuclear Regulatory Commission,

ATTN: Document Control Desk, Washington DC 20555-0001; with copies to the Regional

Administrator, Region II; the Director, Office of Enforcement, United States Nuclear Regulatory

Commission, Washington, DC 20555-0001; and the NRC Resident Inspector at the Farley

Nuclear Plant.

In accordance with 10 CFR 2.390 of the NRCs Rules of Practice, a copy of this letter, its

enclosures, and your response (if any) will be available electronically for public inspection in the

2

NRC Public Document Room or from the Publicly Available Records (PARS) component the

NRCs document system (ADAMS). ADAMS is accessible from the NRC Web site at

http://www.nrc.gov/reading-rm/adams.html (the Public Electronic Reading Room).

Sincerely,

/RA/

Scott M. Shaeffer, Chief

Reactor Projects Branch 2

Division of Reactor Projects

Docket Nos. 50-348, 50-364, and 72-42

License Nos. NPF-2 and NPF-8

Enclosure: Inspection Report 05000348/2006003, 05000364/2006003, and

07200042/2006001

w/Attachment: Supplemental Information

cc w/encl: (See page 3)

__ML062080742

OFFICE

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SIGNATURE

PKV /RA/

RCC /RA/

ECM /RA/

LFL /RA/

NAME

KVanDoorn

RChou

EMichel

LLake

DATE

July 28, 2006

July 25, 2006

July 25, 2006

July 26, 2006

E-MAIL COPY?

YES

NO YES

NO YES

NO YES

NO YES

NO YES

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NO

OFFICE

RII:DRS

RII:DRS

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RII:DRS

SIGNATURE

GBK /RA/

AND /RA/

NJG /RA/

MAS /RA/

NAME

GKuzo

ANielsen

NGriffis

MScott

DATE

July 25, 2006

July 25, 2006

July 25, 2006

July 28, 2006

E-MAIL COPY?

YES

NO YES

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3

cc w/encl:

B. D. McKinney, Licensing

Services Manager, B-031

Southern Nuclear Operating

Company, Inc.

Electronic Mail Distribution

J. R. Johnson

General Manager, Farley Plant

Southern Nuclear Operating

Company, Inc.

Electronic Mail Distribution

J. T. Gasser

Executive Vice President

Southern Nuclear Operating

Company, Inc.

Electronic Mail Distribution

Bentina C. Terry

Southern Nuclear Operating Company, Inc.

Bin B-022

P. O. Box 1295

Birmingham, AL 35201-1295

State Health Officer

Alabama Department of Public Health

RSA Tower - Administration

201 Monroe St., Suite 700

P. O. Box 303017

Montgomery, AL 36130-3017

M. Stanford Blanton

Balch and Bingham Law Firm

P. O. Box 306

1710 Sixth Avenue North

Birmingham, AL 35201

William D. Oldfield

Quality Assurance Supervisor

Southern Nuclear Operating Company

Electronic Mail Distribution

Distribution w/encl: (See page 4)

1

Letter to H. Lewis Sumner from Scott Shaeffer dated July 27, 2006

SUBJECT:

JOSEPH M. FARLEY NUCLEAR PLANT - NRC INTEGRATED INSPECTION

REPORT 05000348/2006003, 05000364/2006003, AND 07200042/2006001

Distribution w/encl:

R. Martin, NRR

C. Evans

L. Slack, RII EICS

OE Mail

RIDSNRRDIRS

PUBLIC

U. S. NUCLEAR REGULATORY COMMISSION

REGION II

Docket Nos.:

50-348, 50-364, 72-42

License Nos.:

NPF-2, NPF-8

Report Nos.:

05000348/2006003, 05000364/2006003, and 07200042/2006001

Licensee:

Southern Nuclear Operating Company, Inc.

Facility:

Joseph M. Farley Nuclear Plant

Location:

7388 N. State Highway 95

Columbia, AL 36319

Dates:

April 1- June 30, 2006

Inspectors:

C. Patterson, Senior (Sr.) Resident Inspector

J. Baptist, Resident Inspector

K. VanDoorn, Sr. Reactor Inspector (Section 1R08)

R. Chou, Reactor Inspector (Section 1R08)

E. Michel, Reactor Inspector (Sections 1R08, 4OA2)

M. Scott, Reactor Inspector (Section 4OA2)

L. Lake, Reactor Inspector (Section 4OA2)

G. Kuzo, Sr. Health Physicist (Sections 2OS1, 4OA1)

A. Nielsen, Health Physicist (Sections 2OS2, 4OA1)

N. Griffis, Health Physicist (Sections 2PS2, 4OA5)

Approved by:

Scott M. Shaeffer, Chief

Reactor Projects Branch 2

Division of Reactor Projects

SUMMARY OF FINDINGS

IR 05000348/2006003, 05000364/2006003, and 07200042/2006001; 04/01/2006-06/30/2006;

Joseph M. Farley Nuclear Plant, Units 1 & 2; Problem Identification & Resolution, Refueling and

Other Outage Activities.

The report covered a three-month period of inspection by the resident inspectors, five regional-

based Reactor Inspectors, and three Health Physicists. Three Green non-cited violations were

identified. The significance of most findings are indicated by their color (Green, White, Yellow,

or Red) using Inspection Manual Chapter (IMC) 0609, Significance Determination Process

(SDP). Findings for which the SDP does not apply may be Green or be assigned a severity

level after management review. The NRC's program for overseeing the safe operation of

commercial nuclear power reactors is described in NUREG-1649, Reactor Oversight Process,

Revision 3, dated July, 2000.

A.

NRC-Identified and Self-Revealing Findings

Cornerstone: Mitigating Systems

C Green. A Green non-cited violation (NCV) of 10 CFR 50.55a (a) (2) was identified by

the NRC for the licensee failing to comply with the ASME Boiler and Pressure Vessel

Code,Section XI, for Class 2 Components. The licensee failed to meet the ASME

Code requirements for a Unit 2 Charging Safety Injection pump casing replacement,

when they did not obtain a completed NIS-2 form signed by the Authorized Nuclear

Inservice Inspector (ANII).

The finding is more than minor because it affected the mitigating systems cornerstone

objective to assure the reliability of systems that respond to events to prevent

undesirable consequences and was associated with the design control attribute in that

qualification remains questionable. The finding was evaluated as very low risk

significance (Green) because it was a qualification deficiency confirmed not to result in

a loss of operability. This finding has been entered into the licensees corrective

Action Program. (Section 4OA2.2)

C Green. A Green non-cited violation (NCV) of Technical Specification 5.4, Procedures,

was identified by the NRC for failure to follow procedural guidance associated with

removal of debris in containment. The licensee performed a containment inspection;

however, failed to follow adequate procedural guidance to ensure the containment

environment was acceptable for power operations.

This finding is more than minor because it could be reasonably viewed as a precursor

to a significant event involving debris accumulation on the containment sump screens

and a subsequent impairment to suction flow for Emergency Core Cooling System

(ECCS) pumps. Although it impacted the Mitigating System Cornerstone, it did not

result in a loss of function per Inspection Manual Chapter (IMC) Part 9900, Technical

Guidance, Operability Determination Process for Operability and Functional

Assessment, did not represent an actual loss of safety function, and was not

potentially risk significant due to possible external events. This finding was entered

into the licensees corrective action program. (Section 1R20)

2

Cornerstone: Barrier Integrity

C Green. A Green self-revealing non-cited violation (NCV) of 10 CFR 50, Appendix B,

Criterion VII, Control of Purchased Material, Equipment, and Services, was identified

for failure to control adequately contractors during the Unit 1 refueling outage that

resulted in damage to the fuel transfer system. This was a self-revealing violation

when a pillar block weld broke resulting in damage to the transfer cart, rails, basket,

and dummy fuel assembly. The licensee entered the deficiency into their corrective

action program for resolution.

This finding is more than minor because it could be reasonably viewed as a precursor

to a significant event involving damage to a fuel assembly. Although the damage

occurred to a dummy fuel assembly, the stresses applied to the fuel transfer system

occurred during core offload and it is was fortuitous that the failure happened when a

dummy assembly was in the fuel transfer basket. This finding is of very low safety

significance because no damage to a fuel assembly actually occurred. (Section 1R20)

B.

Licensee-Identified Violations

None.

REPORT DETAILS

Summary of Plant Status

Unit 1 operated at or near Rated Thermal Power (RTP) until April 8, 2006, when the unit was

shutdown to begin a refueling outage. The outage ended on May 24, 2006. The unit operated

at RTP until June 30, 2006 when the unit was shutdown due to an inoperable main steam

isolation valve.

Unit 2 operated at or near 100% RTP for the duration of the reporting period.

1.

REACTOR SAFETY

Cornerstones: Initiating Events, Mitigating Systems, and Barrier Integrity

1R04

Equipment Alignment

a.

Inspection Scope

Partial System Walkdowns. The inspectors performed partial walkdowns of the following

three systems to verify they were properly aligned when redundant systems or trains

were out of service. The walkdowns were performed using the criteria in licensee

procedures FNP-0-AP-16, Conduct of Operations - Operations Group, and

FNP-0-SOP-0, General Instructions to Operations Personnel. The walkdowns included

reviewing the Updated Final Safety Analysis Report (UFSAR), plant procedures and

drawings, checks of control room and plant valves, switches, components, electrical

power line-ups, support equipment, and instrumentation.

C 1-2A, 2B, 1C, 2C Emergency Diesel Generators (EDGs) while 1B EDG out of service.

C 1B Motor Driven Auxiliary Feedwater (MDAFW) Pump during 1A MDAFW freeze seal

maintenance activities.

C 2B and 2C Service Water (SW) Pumps while 2A SW pump was out of service.

Complete Walk-down. The inspectors conducted a complete walkdown of the

accessible portions of the Unit 1 Residual Heat Removal system (RHR). The inspectors

used licensee procedure FNP-1-SOP-7.0A, Residual Heat Removal System and

drawings D-175038 and D-175041, to verify adequate system alignment of on-service

equipment. The inspectors also interviewed personnel and reviewed control room logs,

Maintenance Rule (MR) monthly reports, condition reports (CRs), quarterly system

health reports, outstanding work orders, and industry operating experience to verify that

alignment and equipment discrepancies were being identified and appropriately

resolved. Documents reviewed are listed in the Attachment.

b.

Findings

No findings of significance were identified. The inspectors did identify one valve that

was improperly sealed. The licensee immediately corrected the valve status and

captured the issue in CR 2006105758. The position of the valve was correct and the

function of the system was not compromised due to this discrepancy.

1R05

Fire Protection

6

a.

Inspection Scope

Fire Area Tours. The inspectors conducted a walk-down of the seven fire areas listed

below to verify the licensees control of transient combustibles, the operational readiness

of the fire suppression system, and the material condition and status of fire dampers,

doors, and barriers. The requirements were described in licensee procedures

FNP-0-AP-36, Fire Surveillance and Inspection; FNP-0-AP-38, Use of Open Flame;

FNP-0-AP-39, Fire Patrols and Watches; and the associated Fire Zone Data sheets.

C Unit 1 and 2 EDG Building, Switchgear Room Train A, Zone 56A

C Unit 1 and 2 EDG Building, Diesel Generator 2C, Zone 57

C Unit 1 and 2 EDG Building, Diesel Generator 1B, Zone 58

C Unit 1 and 2 EDG Building, Diesel Generator 2B, Zone 59

C Unit 1 and 2 EDG Building, Diesel Generator 1C, Zone 60

C Unit 1 and 2 EDG Building, Diesel Generator 1-2A, Zone 61

C Unit 1 and 2 EDG Building, Switchgear Room Train B, Zone 56C

b.

Findings

No findings of significance were identified.

1R08

Inservice Inspection (ISI) Activities

a.

Inspection Scope

Piping Systems ISI. The inspectors reviewed the implementation of the licensees ISI

program for monitoring degradation of the reactor coolant system boundary and the risk

significant piping system boundaries for Unit 1. The inspectors selected a sample of

American Society of Mechanical Engineers (ASME) Boiler and Pressure Vessel Code,

Section XI required examinations and a sample of risk-informed ISI Program

examinations. The inspectors conducted an on-site review of the following

nondestructive examination (NDE) activities to evaluate compliance with Technical

Specifications (TS), ASME Section XI and ASME Section V requirements - 1989 Edition,

and to verify that indications and defects were appropriately evaluated and dispositioned

in accordance with the requirements of ASME Section XI, IWB-3000 acceptance

standards.

Ultrasonic Testing (UT):

The inspectors reviewed the following examination records in addition to the records for

the above observed examinations:

UT:

  • 12"-ALA1-4301-6-RI, Pipe to Elbow
  • 10"-ALA2-4516-28-RI, Elbow to Pipe
  • 3"-ALA2-4540-32-RI, Valve to Pipe

7

Liquid Penetrant (PT):

  • 2"-ALA1-4310-2-RI, Pipe to Elbow
  • 2"-ALA1-4307-5-RI, Elbow to Pipe

The inspectors also observed two visual and two UT examinations of the containment

liner along excavated portions of the containment moisture barrier performed in

accordance with ASME Section XI, IWE, 1992 Edition. This examination was perform in

response to previously discovered indications of moisture barrier degradation observed

by an NRC inspector and recorded in the licensees Corrective Action Program.

Qualification and certification records for examiners, inspection equipment, and

consumables along with the applicable NDE procedures for the above ISI examination

activities were reviewed and compared to requirements stated in ASME Section V and

Section XI.

The inspectors performed a review of piping system related problems that were

identified by the licensee and entered into the corrective action program. The inspectors

reviewed these corrective action documents to confirm that the licensee had

appropriately described the scope of the problems and had implemented effective

corrective actions.

Boric Acid Corrosion Control (BACC) ISI. The inspectors reviewed the licensees Boric

Acid Corrosion Control Program (BACCP) to ensure compliance with commitments

made in response to NRC Generic Letter 88-05, Boric Acid Corrosion of Carbon Steel

Reactor Pressure Boundary, and Bulletin 2002-01, Reactor Pressure Vessel Head

Degradation and Reactor Coolant Pressure Boundary Integrity. The inspectors

conducted an on-site record review and an independent walk-down of the reactor

building, which was not normally accessible during at-power operations, to evaluate

compliance with licensee BACCP requirements and 10 CFR Part 50, Appendix B,

Criterion XVI, Corrective Action, requirements. In particular, the inspectors verified that

licensee visual examinations focused on locations where boric acid leaks can cause

degradation of safety significant components and that degraded or non-conforming

conditions were properly identified in the licensees corrective action system.

The inspectors reviewed the licensees program implementation procedures and a

sample of plant issue reports (corrective action documents) to ensure that leaks were

being identified and addressed at an appropriate threshold. A sample review of

corrosion assessments was also completed for boric acid deposits found on reactor

coolant system piping and other ASME Code Class components to verify that the

minimum design code required section thickness had been maintained for any affected

component(s).

Steam Generator (SG) Tube ISI. The inspectors reviewed activities, plans, pre-outage

degradation assessment and procedures for the inspection and evaluation of the steam

generator Inconel Alloy 690TT tubing for Unit 1 SGs A, B, and C, to determine if the

activities were being conducted in accordance with Technical Specifications and

applicable industry standards. Data gathering, analysis, and evaluation activities were

reviewed. The inspectors reviewed data results for tubes at SG B - R45C59; SG A -

R17C04, R15C10, and R26C10; and SG C - R11C82, R12C82, R10C93, R04C51,

8

R03C56, and R13C81 to verify the adequacy of the licensees primary, secondary, and

resolution analyses. The inspectors observed the licensee perform 100% of the

video/visual inspection for the secondary side on the top of tubesheet area of the steam

generators to determine if foreign materials or loose parts were present and the licensee

was conducting appropriate evaluations. The inspectors also reviewed data operators

and analysts certifications and qualifications, including medical exams.

b.

Findings

No findings of significance were identified.

1R11

Licensed Operator Requalification

a.

Inspection Scope

The inspectors observed portions of the licensed operator training and testing program

to verify implementation of procedures FNP-0-AP-45, Farley Nuclear Plant Training

Program, FNP-0-TCP-17.6, Simulator Training Evaluation Documentation, and FNP-0-

TCP-17.3, Licensed Operator Continuing Training Program. The inspectors observed

scenarios conducted in the licensees simulator for a steam generator tube leak, failed

instrumentation, and load rejection. The inspectors observed high risk operator actions,

overall performance, self-critiques, training feedback, and management oversight to

verify operator performance was evaluated against the performance standards of the

licensees scenario. In addition, the inspectors observed implementation of the

applicable emergency operating procedures listed in the attachment to verify that

licensee expectations in procedures FNP-0-AP-16 and FNP-0-TCP-17.6 were met.

Documents reviewed are listed in the Attachment.

b.

Findings

No findings of significance were identified.

1R12

Maintenance Effectiveness

a.

Inspection Scope

The inspectors reviewed the following two issues to verify implementation of licensee

procedures FNP-0-87, Maintenance Rule (MR) Scoping Manual; NMP-ES-021,

Structural Monitoring Program for the Maintenance Rule; and FNP-0-89, FNP

Maintenance Rule Site Implementation Manual; and compliance with 10CFR50.65. The

inspectors assessed the licensees evaluation of appropriate work practices, common

cause failures, functional failures, maintenance preventable functional failures, repetitive

failures, availability and reliability monitoring, trending and condition monitoring, and

system specialist involvement. The inspectors also interviewed maintenance personnel,

system specialists, the MR coordinator, and operations personnel to assess their

knowledge of the program.

C CR 2006104043, 1C Component Cooling Water (CCW) Pump Did Not Start During

Safety Injection (SI)/Loss of offsite power (LOSP) Test

9

C CR 2006104286, Maintenance preventable functional failure (MPFF) of 1C Service Air

Compressor

b.

Findings

No findings of significance were identified.

1R13

Maintenance Risk Assessments and Emergent Work Control

a.

Inspection Scope

The inspectors assessed the licensees planning and control for the following five

planned activities to verify the requirements in licensee procedures FNP-0-ACP-52.3,

Guidelines for Scheduling of On-Line Maintenance; NMP-GM-006, Work Management;

and FNP-0-AP-16, Conduct of Operations - Operations Group; and the MR risk

assessment guidance in 10CFR50.65a(4) were met.

C CR 2006103167, Outage Risk-Entered Orange Prematurely

C CR 2006102858, Instrument Air Compressor Problems

C CR 2006101909, Significant Axial Flux Oscillations During Derate

C CR 2006103262, 1B EDG Air Receiver Blowdown During Orange Shutdown Safety

Assessment

C CR 2006104091, Damage to Unit 1 Fuel Transfer System

b.

Findings

No findings of significance were identified.

1R15

Operability Evaluations

a.

Inspection Scope

The inspectors reviewed the following five operability evaluations to verify they met the

requirements of licensee procedures FNP-0-AP-16, Conduct of Operations and

FNP-0-ACP-9.2, Operability Determination for Technical Adequacy, Consideration of

Degraded Conditions, and Identification of Compensatory Measures. The inspectors

reviewed the evaluations against the design bases, as stated in the UFSAR and

Functional System Descriptions (FSDs) to verify system operability was not affected.

C CR 2006103043, Unit 2 Main Steam Isolation Valves (MSIVs)

C CR 2006104130, OD 6-04, 2B EDG minor leakage Service Water Piping

C CR 2006104389, OD 6-05, 1-2A EDG service water leakage at Expansion joint

C CR 2006104942, Turbine Driven Auxiliary Feedwater (TDAFW) Pump Check Valve

Flow Verification test failure

C CR 2006105386, OD 6-06, 2A MDAFW Pump miniflow line vent piping leak

b.

Findings

No findings of significance were identified.

10

1R17

Permanent Plant Modifications

a.

Inspection Scope

The inspectors reviewed the following plant modification to verify the implementation of

procedure FNP-0-AP-8, Design Modification Control. This included verification that the

design bases, licensing bases, and performance capability or risk significant systems,

structures, and components would not be degraded through the modifications and the

modifications would not place the plant in an unsafe condition. The inspectors also

discussed the modifications with engineering and operations personnel, and reviewed

the related procedures and drawings.

C DCP 03-1-9976, Unit 1 Containment Scaffolding Storage Modification

b.

Findings

No findings of significance were identified.

1R19

Post Maintenance Testing

a.

Inspection Scope

The inspectors reviewed the criteria contained in licensee procedures FNP-0-PMT-0.0,

Post Maintenance Test Program, to verify post-maintenance test procedures and test

activities for the following five systems/components were adequate to verify system

operability and functional capability.

C WO 2061229101, VT-2 check of SW Leak

C FNP-1-STP-45.7, MSIV and Bypass Valves Cold Shutdown Inservice Test

C FNP-0-ETP-3643, Verification of Rod Control System Operability

C FNP-2-STP-22.23, TDAFW Pump Trip and Throttle Valve Mechanism and Indicator

Operability Test

C FNP-0-STP-80.1, Diesel Generator 1-2A Operability Test .

b.

Findings

No findings of significance were identified

1R20

Refueling and Other Outage Activities

a.

Inspection Scope

Refueling Activities. The inspectors reviewed the following activities related to the Unit 1

refueling outage for conformance to licensee procedure FNP-0-UOP-4.0, General

Outage Operations Guideline, and FNP-1-UOP-4.1, Controlling Procedure for Refueling.

Surveillance tests were reviewed to verify results were within the TS required

specification. Shutdown risk, management oversight, procedural compliance, and

operator awareness were evaluated for each of the following activities. Documents

reviewed are listed in the attachment.

11

C Outage Risk Assessment

C Cooldown

C Core offload and reload

C Reactor coolant instrumentation

C Electrical system alignments and bus outages

C Reactor vessel disassembly and assembly activities

C Outage-related surveillance tests

C Containment Closure

C Low Power Physics Testing and Startup Activities

C Clearance Activities

C Decay Heat Removal and Spent Fuel Pool Cooling

b.

Findings

.1

Failure to Follow Established Procedures Regarding Debris in Containment

Introduction: A Green non-cited violation (NCV) for failure to follow procedural guidance

associated with removal of debris in containment was identified by the NRC.

Description: On May 20, 2006, the licensee implemented procedures FNP-1-STP-34.1,

Containment Inspection (Maintenance) and FNP-1- STP-34.0, Containment Inspection

(General). The Containment Inspection (Maintenance) procedure is maintained open

until all work is completed to track work items as they enter and exit containment. The

Containment Inspection (General) procedure was performed by the licensee as a

general walkdown to verify that containment was acceptable. The licensee completed

the Containment Inspection (General) procedure and documented it as satisfactorily

finished. The acceptance criteria is to ensure that there is No loose debris (rags, trash,

clothing, etc.) present in the containment which could be transported to the containment

sump and cause restricted pump suctions during LOCA conditions.

On May 21, 2006, after Unit 1 plant entry into Mode 4, the resident inspectors

performed a containment closeout tour to determine the status of housekeeping and

equipment storage in containment. In general, the inspectors found that the

containment was clean and free of items of a substantial size that may impact the

performance of the containment sumps. However, the inspectors identified an

appreciable quantity of smaller debris consisting of wires, foam insulation, a spray

bottle, mopheads, and a plastic garbage bag that were not removed. A majority of the

articles identified by the inspectors were located on the 105' level and were apparently

left behind from untracked work occurring on May 20, 2006. These items would have

had access to the containment sump screens during loss of coolant accident (LOCA)

conditions; however, could only have partially affected one of the containment sump

screens while the remaining two would have been fully functional.

Based on the amount, characterization, and location of the debris, the inspectors

concluded that in the aggregate, the licensee failed to follow adequate procedural

guidance to ensure the containment environment was acceptable for power operations.

The specific corrective action document initiated by the licensee associated with the

inspector identified issues/discrepancies is CR 2006104914.

12

Analysis: The performance deficiency associated with this issue is the failure to meet

the acceptance criteria of FNP-1- STP-34.0, Containment Inspection (General). The

procedure requires the containment general area to be free of foreign objects unless

they are identified on a tracking log sheet in procedure FNP-1-STP-34.1. The items

found by the inspectors were present at the time of FNP-1- STP-34.0 completion and

inadequate measures were taken to ensure their removal. The inspectors referenced

Inspection Manual Chapter (IMC) 0612 and determined the finding is more than minor

because it could be reasonably viewed as a precursor to a significant event involving

debris accumulation on the containment sump screens and a subsequent impairment to

suction flow for Emergency Core Cooling System (ECCS) pumps. Although the amount

of debris identified would not have a significant impact on the operability of all three

containment sump screens, the continued accumulation of debris could impact long-

term post accident sump functionality. The inspectors further referenced IMC 0609 for

the SDP review and determined the finding was of very low safety significance.

Although it impacted the Mitigating System Cornerstone, it did not result in a loss of

function per Part 9900, Technical Guidance, Operability Determination Process for

Operability and Functional Assessment, did not represent an actual loss of safety

function, and was not potentially risk significant due to possible external events. No

specific cross-cutting areas were identified.

Enforcement: Technical Specification 5.4, Procedures, requires that written procedures

be implemented for those systems referenced in Regulatory Guide 1.33, Revision 2,

Appendix A, February 1978, which would include the Emergency Core Cooling System.

Contrary to the above, on May 20, 2006 the licensee performed FNP-1-STP-34.0,

Containment Inspection (General) and identified satisfactory completion, even though

the acceptance criteria was not met regarding debris in containment. The debris was

not tracked by any mechanism and remained in the general containment areas until

identified by the resident inspectors on May 21, 2006. This resulted in items being left

behind that could have had an adverse impact on post-accident containment sump

recirculation flow. Because this finding is of very low safety significance and because it

was entered into the licensees corrective action program (CR 2006104914), this

violation is being treated as a NCV, consistent with Section VI.A of the NRC

Enforcement Policy: NCV 05000348/200600301, Failure to Follow Established

Procedures Regarding Debris in Containment.

.2

Failure to Control Contractors Results in Fuel Transfer System Damage

Introduction: A Green non-cited violation (NCV) was identified for failure to control

contractors during the refueling outage that resulted in damage to the fuel transfer

system. This was a self-revealing violation when a pillar block weld broke resulting in

damage to the transfer cart, rails, basket, and dummy fuel assembly.

Description: During the Unit 1 refueling outage, contractor support personnel were

asked to respond to a slack upender cable issue in the spent fuel pool area during core

offload. Core offload occurred during April 15-17, 2006. Using a digital control box,

vendor support personnel made several adjustments to the transfer system cable travel

length. The impact of these adjustments was not understood. These adjustments

caused the pivot points of the upender and basket to be misaligned such that one

13

contacted the other when taken to the vertical position. Because of the adjustments, the

upender and transfer carts alignment marks were misaligned by several inches. Over

time stresses were put on the welds until one failed resulting in the damage to the

system. The failure occurred during checks of the system with a dummy fuel assembly.

The dummy assembly was damaged. The Unit 2 dummy assembly was used to check

the system out following repairs.

Analysis: The inspectors referenced Inspection Manual Chapter (IMC) 0612 and

determined the finding is more than minor because it could be reasonably viewed as a

precursor to a significant event involving damage to a fuel assembly. Although the

damage occurred to a dummy fuel assembly the stresses applied to the fuel transfer

system occurred during core offload and it is was fortuitous that the failure happened

when a dummy assembly was in the basket. The inspectors reviewed IMC 0609 for the

SDP review and determined the finding to be of very low safety significance. Although it

impacted the Barrier Integrity Cornerstone, there was no damage to a fuel assembly.

Enforcement: 10 CFR 50, Appendix B, Criterion VII, Control of Purchased Material,

Equipment, and Services, requires that the effectiveness of the control of contractors

shall be assessed at intervals consistent with the importance, complexity, and quantity

of the product or services. Contrary to the above, Unit 1 contractor support personnel

for refueling activities during April 2006, were not adequately assessed to understand

the impact of adjustments the contractor personnel made to the transfer system cable

travel during core offload to prevent damage to the fuel transfer system. Because this

finding is of very low safety significance and because it was entered into the licensees

corrective action program (CR 2006104091), this violation is being treated as a NCV,

consistent with Section VI.A of the NRC Enforcement Policy: NCV

05000348/200600302, Failure to Control Contractors Results in Fuel Transfer System

Damage.

1R22

Surveillance Testing

a.

Inspection Scope

The inspectors reviewed surveillance test procedures and either witnessed the test or

reviewed test records for the following eight surveillance tests to determine if the tests

adequately demonstrated equipment operability and met the TS requirements. The

inspectors reviewed the activities to assess for preconditioning of equipment, procedure

adherence, and valve alignment following completion of the surveillance. The

inspectors reviewed licensee procedures FNP-0-AP-24, Test Control; FNP-0-M-050,

Master List of Surveillance Requirements; and FNP-0-AP-16, Conduct of Operations;

and attended selected briefings to determine if procedure requirements were met.

Surveillance Tests

C FNP-2-SOP-17.0, Appendix 4, MSIV Functional Test

C FNP-1-STP-11.15, Residual Heat Removal (RHR) Heat Exchange Discharge Valve

Mechanical Stop Verification

C FNP-1-STP-40.0, SI with LOSP Test

C FNP-1-STP-22.13, TDAFW Pump Check Valve Flow Verification

14

In-Service Tests (ISTs)

C FNP-1-STP-45.7, MSIV and Bypass Valves Cold Shutdown Inservice Test

Reactor Coolant System (RCS) Leak Detection

C FNP-1-STP-9.0, RCS Leakage

Containment Isolation Valves

C FNP-2-STP-627, Local Leak Rate Testing of Containment Penetrations, Pen 64A

C FNP-2-STP-627, Local Leak Rate Testing of Containment Penetrations, Pen 93

b.

Findings

No findings of significance were identified

1R23

Temporary Plant Modifications

a.

Inspection Scope

The inspectors reviewed the following temporary modification (TM) and associated

10CFR50.59 screening criteria against the system design bases information and

documentation and the licensees temporary modifications procedure FNP-0-AP-8,

Design Modification Control. The inspectors reviewed implementation, configuration

control, post-installation test activities, drawing and procedure updates, and operator

awareness for this TM.

C TM 10613319102, Unit 1 Upender Car Traveler Seismic Clips

b.

Findings

No findings of significance were identified.

Cornerstone: Emergency Preparedness

1EP6 Drill Evaluation

a.

Inspection Scope

The inspectors evaluated one emergency plan drill on June 28, 2006, to verify the

licensee was properly classifying the event, making required notifications, making

protective action recommendations, and conducting self-assessments. The inspectors

used procedure FNP-0-EIP-15.0, Emergency Drills, as the inspection criteria and

observed the drill on June 28 in the Technical Support Center (TSC). The inspectors

reviewed FNP-0-EIP-9.0, Emergency Classification and Actions, and other supporting

procedures to validate the classification of the event made by the licensee. The

inspectors subsequently observed and reviewed the notifications made, communications

between emergency response team members, team work of licensee personnel,

licensee identification of weaknesses and deficiencies, corrective action documentation,

and overall performance.

15

b.

Findings

No findings of significance were identified.

2.

RADIATION SAFETY

Cornerstones: Occupational Radiation Safety and Public Radiation Safety

2OS1 Access Control To Radiologically Significant Areas (21 Samples)

a.

Inspection Scope

Access Controls Licensee activities for controlling and monitoring worker access to

radiologically significant areas and tasks were evaluated. The inspectors evaluated

changes to and adequacy of procedural guidance; directly observed implementation of

established administrative and physical radiological controls; appraised radiation worker

and health physics technician (HPT) knowledge of and proficiency in implementing

radiation protection activities; and assessed occupational exposures to radiation and

radioactive material.

The inspectors directly observed controls established for workers and HPT staff in

airborne radioactivity area, radiation area, high radiation area (HRA), locked-high

radiation area (LHRA), and very high radiation area (VHRA) locations. Controls and

their implementation for HRA keys and for storage of irradiated material within U1 and

U2 spent fuel pool (SFP) areas were reviewed and discussed in detail. The inspectors

reviewed and evaluated U1 refueling outage tasks including under vessel bare metal

inspection activities; reactor vessel head disassembly; snubber inspection and

maintenance; fuel off-load; valve maintenance and replacement; reactor coolant pump

maintenance; steam generator primary and secondary side maintenance; radioactive

waste (radwaste) handling and storage; and transportation activities. The inspectors

attended pre-job briefings and reviewed radiation work permit (RWP) details to assess

communication of radiological control requirements to workers. Occupational workers

adherence to selected RWPs and HPT proficiency in providing job coverage were

evaluated through direct observations and interviews with licensee staff. Electronic

dosimeter (ED) alarm set points and worker stay times were evaluated against area

radiation survey results and actual dose rates encountered and doses received.

Worker exposure as measured by ED and by licensee evaluations of potential skin

doses resulting from discrete radioactive particle or dispersed skin contamination events

during the 1R20 activities were reviewed and assessed independently. For HRA tasks

involving potentially significant dose rate gradients, e.g., steam generator maintenance

activities, the inspectors evaluated the potential for use of dosimeter multi-badging to

monitor worker exposure.

Postings for access to radiologically controlled areas (RCAs) and physical controls for

the U1 reactor containment and for U1 and U2 reactor auxiliary building (RAB) locations

designated as LHRAs and VHRAs were evaluated during facility tours. The inspectors

independently measured radiation dose rates or directly observed conduct of licensee

16

radiation surveys and results for U1 containment equipment and work locations, U2

drumming/storage room, outside radioactive material storage areas, and selected U1

and U2 RAB locations. All results were compared to current licensee surveys and

assessed against established postings and radiological controls.

Licensee controls for airborne radioactivity areas with the potential for individual worker

internal exposures of greater than 30 millirem (mrem) Committed Effective Dose

Equivalent were evaluated. For selected RWPs identifying potential airborne areas

associated with 1R20 activities, e.g., under vessel maintenance, valve maintenance, U1

seal table equipment maintenance, and reactor vessel stud cleaning activities, the

inspectors evaluated the implementation and effectiveness of administrative and

physical controls including air sampling, barrier integrity, engineering controls, and

postings. Licensee identification and assessment of potential radionuclide intakes by

workers between April 1, 2005 through April 20, 2006, were reviewed and evaluated.

Radiation protection activities were evaluated against Updated Final Safety Analysis

Report (UFSAR), Technical Specification (TS), and 10 Code of Federal Regulations

(CFR) Parts 19 and 20 requirements. Specific assessment criteria included UFSAR

Section 11, Radioactive Waste Management, and Section 12, Radiation Protection;

10 CFR 19.12; 10 CFR 20, Subpart B, Subpart C, Subpart F, Subpart G, Subpart H, and

Subpart J; TS Sections 5.4, Procedures, and 5.7, High Radiation Area Controls; and

approved procedures. Detailed procedural guidance and records reviewed for this

inspection area are listed in Sections 2OS1, 2OS2, 2PS2, 4OA1, and 4OA5 of the report

Attachment.

Problem Identification and Resolution Licensee Corrective Action Program (CAP)

documents associated with access control to radiologically significant areas were

reviewed and assessed. The inspectors evaluated the licensees ability to identify,

characterize, prioritize, and resolve the identified issues in accordance with Nuclear

Management Procedure (NMP)-GM-002, Corrective Action Program, Version (Ver.) 4.

Licensee Condition Report (CR) documents and audits associated with access controls,

personnel monitoring instrumentation, and personnel contamination events were

reviewed. Licensee CAP documents reviewed and evaluated in detail during inspection

of this program area are identified in Section 2OS1 of the report Attachment.

b.

Findings

No findings of significance were identified.

2OS2 ALARA Planning and Controls (15 Samples)

a.

Inspection Scope

As Low As Reasonably Achievable (ALARA) The inspectors reviewed ALARA program

guidance and its implementation for ongoing refueling outage job tasks. The inspectors

evaluated the accuracy of ALARA work planning and dose budgeting, observed

implementation of ALARA initiatives and radiation controls for selected jobs in-progress,

assessed the effectiveness of source-term reduction efforts, and reviewed historical

dose information.

17

ALARA planning documents and procedural guidance were reviewed and projected

dose estimates were compared to actual dose expenditures for the following high dose

jobs: steam generator (S/G) maintenance, reactor head assembly/disassembly,

scaffolding construction, and work on valves LCV-459/460 near the regenerative heat

exchanger. Differences between budgeted dose and actual exposure received were

discussed with cognizant ALARA staff. Changes to dose budgets relative to changes in

radiation source term and/or job scope were also discussed. The inspectors attended

pre-job briefings and evaluated the communication of ALARA goals, RWP requirements,

and industry lessons-learned to job crew personnel.

The inspectors made direct field or closed-circuit-video observations of outage job tasks

involving S/G maintenance and reactor head disassembly. For the selected tasks, the

inspectors evaluated radiation worker (radworker) and HPT job performance; surveys of

the work areas; appropriateness of RWP requirements; and adequacy of implemented

engineering controls.

Implementation and effectiveness of selected program initiatives with respect to source-

term reduction were evaluated. Chemistry program ALARA initiatives, including crud

burst/cleanup activities, and their effect on U1 containment and auxiliary building dose

rate trends were reviewed. The effectiveness of temporary shielding installed near the

U1 regenerative heat exchanger was assessed through review of pre-shielding versus

post-shielding dose rate data and expected person-rem saved.

Plant exposure history for calendar year (CY) 2002 through CY 2004 (three year rolling

average) was reviewed. The inspectors also reviewed selected monthly dose reports

and daily RWP dose tracking worksheets. In addition, the inspectors examined dose

records of selected declared pregnant workers to evaluate assignment of gestation

dose.

ALARA program activities and their implementation were reviewed against 10 CFR

Part 20, and approved licensee procedures. In addition, licensee performance was

evaluated against guidance contained in Regulatory Guide (RG) 8.8, Information

Relevant to Ensuring that Occupational Radiation Exposures at Nuclear Power Stations

will be As Low As Reasonably Achievable and RG 8.13, Instruction Concerning Prenatal

Radiation Exposure. Procedures and records reviewed within this inspection area are

listed in Sections 2OS2 of the report Attachment.

Problem Identification and Resolution The inspectors reviewed selected CRs and a

licensee self-assessment in the area of exposure control. The inspectors evaluated the

licensees ability to identify, characterize, prioritize, and resolve the identified issues in

accordance with NMP-GM-002, Corrective Action Program Ver. 4. Specific CAP

documents reviewed in detail for this inspection area are identified in Section 2OS2 of

the report Attachment.

b.

Findings

No findings of significance were identified.

18

2PS2 Radioactive Material Processing and Transportation (6 Samples)

a.

Inspection Scope

Waste Processing and Characterization Selected liquid and solid radwaste processing

system components were inspected for material condition and for configuration

compliance with the UFSAR and Process Control Program (PCP). Inspected equipment

included the recycle hold-up tanks; supplemental demineralizer system; resin transfer

piping; resin and filter packaging components; and abandoned waste evaporator

equipment. The inspectors discussed component function, equipment operability, and

changes to radwaste storage areas with licensee staff.

The 2004 Annual Radioactive Effluent Release Report and radionuclide

characterizations from January 1, 2005 through Year-to-Date 2006 for each major waste

stream were reviewed and discussed with radioactive waste (radwaste) staff. For

Reactor Coolant System (RCS) filters, SFP filters, and Dry Active Waste (DAW); the

inspectors evaluated analyses for hard-to-detect nuclides, reviewed the use of scaling

factors, and examined comparison results between gamma emitting radionuclides

reported in the licensee waste stream characterizations and the vendor laboratory data.

For selected shipments of spent resin and Low Specific Activity (LSA) waste, the

methodology used for waste stream mixing and concentration averaging was evaluated.

The inspectors also reviewed the licensees procedural guidance for monitoring changes

in waste stream isotopic mixtures.

Radwaste processing activities were reviewed for compliance with 10 CFR Part 50.59

and consistency with the licensees current PCP and UFSAR, Chapter 11. Waste

stream characterization analyses and selected shipping records were reviewed against

regulations detailed in 10 CFR Part 20, 10 CFR Part 61, 49 CFR Part 173, and guidance

provided in the Branch Technical Position (BTP) on Waste Classification and Waste

Form. Reviewed documents are listed in Section 2PS2 of the report Attachment.

Transportation The inspectors directly observed preparation activities for a shipment of

contaminated laundry. The inspectors noted package markings and placarding, and

interviewed shipping technicians regarding Department of Transportation (DOT)

regulations. The inspectors observed dose rate surveys of the shipping packages and

compared the results to DOT limits.

Five shipping records were reviewed for consistency with licensee procedures and

compliance with NRC and DOT regulations. The inspectors reviewed emergency

response information, DOT shipping package classification, radiation survey results, and

evaluated whether receiving licensees were authorized to accept the packages. The

licensees procedures for use of Type B shipping casks were compared to

recommended vendor protocols and Certificate of Compliance (CoC) requirements. In

addition, training records for individuals currently qualified to ship radioactive material

were reviewed.

Transportation program implementation was reviewed against regulations detailed in

10 CFR Parts 20 and 71, 49 CFR Parts 172-178; as well as the guidance provided in

NUREG-1608. Training activities were assessed against 49 CFR Part 172 Subpart H.

19

Documents reviewed during the inspection are listed in Section 2PS2 of the report

Attachment.

Problem Identification and Resolution. The inspectors reviewed and discussed with HP

supervision selected CRs and audits associated with transportation and radioactive

waste processing program activities. The inspectors assessed the licensees ability to

characterize, prioritize, and resolve the identified issues in accordance with licensee

procedure NMP-GM-002, Corrective Action Program, Ver. 4.0.

b.

Findings

No findings of significance were identified.

4.

OTHER ACTIVITIES

4OA1 Performance Indicator (PI) Verification

a.

Inspection Scope

The inspectors sampled licensee submittals for the PIs listed below to verify the

accuracy of the data reported. The PI definitions and the guidance contained in NEI 99-

02, Regulatory Assessment Performance Indicator Guideline, Rev. 2, and licensee

procedure FNP-0-AP-54, Preparation and Review of NRC Performance Indicator Data,

were used to verify procedure and reporting requirements were met.

Mitigating Systems Cornerstone

  • Unit 1 and Unit 2 Safety System Functional Failures

The inspectors reviewed samples of raw PI data, Licensee Event Reports (LERs), and

Monthly Operating Reports for the period covering April 2004 through March 2006. The

data reviewed from the LERs and Monthly Operating Reports was compared to

graphical representations from the most recent PI report. The inspectors also examined

a sampling of operations logs and procedures to verify the PI data was appropriately

captured for inclusion into the PI report as well as insuring that the individual PIs were

calculated correctly.

Barrier Integrity Cornerstone

The inspectors reviewed raw PI data for the period from October 2004 through March

2006 consisting of daily chemistry analysis and daily leak rate logs. The inspectors

reviewed the recent PI report to verify the data was accurately reflected in the report.

Occupational Radiation Safety Cornerstone

20

  • Occupational Exposure Control Effectiveness

The inspectors reviewed PI data collected from October 1, through March 30, 2006.

The inspectors assessed CAP records to determine if HRA, VHRA, or unplanned

exposures, which resulted in TS or 10 CFR 20 non-conformances, had occurred during

the review period. In addition, the inspectors reviewed selected personnel

contamination event data, internal dose assessment results, and ED alarms for

cumulative doses and/or dose rates exceeding established setpoints. Documents

reviewed are listed in the Attachment.

Public Radiation Safety Cornerstone

  • Radiological Control Effluent Release Occurrences

The inspectors reviewed the PI results for the period of July 1, 2005 through March 31,

2006. For the assessment period, the inspectors reviewed dose totals to the public, out-

of-service (OOS) effluent radiation monitors and selected compensatory sampling data,

and selected CRs related to Radiological Effluent Technical Specific/ Offsite Dose

Calculation Manual issues. The inspectors also reviewed licensee procedural guidance

for collecting and documenting PI data. Documents reviewed are listed in the

Attachment.

b.

Findings

No findings of significance were identified.

4OA2 Identification and Resolution of Problems

.1

Daily Review

As required by Inspection Procedure 71152, "Identification and Resolution of Problems,"

and to help identify repetitive equipment failures or specific human performance issues

for follow-up, the inspectors performed a daily screening of items entered into the

licensees corrective action program. This review was accomplished by reviewing daily

hard copy summaries of CRs and by reviewing the licensees electronic CR database.

.2

Annual Sample Review

Work-Around Review

a.

Inspection Scope

As required by Inspection Procedure 71152, Identification and Resolution of Problems,

the inspectors performed a detailed review of the work-around lists for Unit 1 and 2

shared and Unit 2 that were in effect on May 7, 2006. The inspectors reviewed the

proposed corrective action and schedule for each item on the work-around list. The

inspectors reviewed the compensatory action and cumulative effects on plant operation.

21

The inspectors verified each item was being dispositioned in accordance with plant

procedure ACP-17, Operator Work-Around.

b.

Findings and Observations

The inspectors found that operator work-arounds were being identified at an appropriate

threshold. Items were entered into the corrective action program or actions taken were

appropriate.

Review of High Head Safety Injection pump replacement issue

a.

Inspection Scope

As a result of NRC awareness that the replacement High Head Safety Injection pump

casing and discharge head had not been stored or controlled in accordance with an

approved 10CFR50 Appendix B Quality Assurance program, inspectors verified

compliance of the replacement activity with applicable portions of the American Society

of Mechanical Engineers (ASME) Boiler and Pressure Vessel Code,Section XI.

b.

Findings and Observations

Introduction: A Green NCV of 10 CFR 50.55a(a)(2) was identified by the inspectors for

the licensee failing to comply with the ASME Boiler and Pressure Vessel Code, Section

XI, for Class 2 Components. IWA-7520 of the 1989 edition of Section XI requires that as

part of replacement activities, a completed Owners Report for Repairs or

Replacements, Form NIS-2, be maintained; and subsequently submitted in accordance

with the requirements of IWA-6000.

Description: During the scheduled Unit 2 Fall 2005 outage, the licensee replaced

Charging/High Head Safety Injection Pump 2B casing and discharge head with

replacements that had been previously used in a test facility without an approved quality

assurance program. The replacement pump casing and discharge head, originally

designated and N Stamped per ASME Section III for Code Class 2 service, had not

been continuously controlled as a safety-related ASME Code Class 2 part since 1984 in

accordance with the requirements of an approved quality assurance program.

Therefore, the level of quality had to be re-established in order for the pump to be used

as an ASME Section XI replacement. Methods on how to re-establish quality levels

were not addressed in the ASME Code.

After discussions with the NRC staff, (refer to [SNC] letter to the NRC dated December

2, 2005), SNC considered methods to address the question related to control of pump

pressure retaining parts which would allow returning the 2B Charging / High Head

Safety Injection pump to service. After consideration of submitting a relief request, the

use of Generic Letter 89-09, or to disposition the issue within the SNC corrective action

program, SNC determined that the appropriate process to disposition this issue and

return the 2B charging pump to service was for SNC to document an evaluation for the

pump casing and discharge head acceptability within their corrective action program.

Subsequently the pump was replaced using a design change under Job Number E21-

2051013013.

22

As identified in SNCs letter to the NRC dated March 1, 2006, that transmitted Farley

Nuclear Plant Unit 2 Inservice Inspection Summary Report, SNCs evaluation consisted

of a code reconciliation that addressed the use of different codes, evaluated any

differences between design specification requirements and design, and evaluated the

potential effects of the uncontrolled storage of parts. The evaluation included a

conclusion that the parts retained an acceptable level of quality and safety. SNC

considered the Code requirements of the casing and discharge head to be confirmed.

Also identified in the March 1, 2006 letter transmitting the Inservice Inspection Summary

was information that due to the Authorized Nuclear Inservice Inspectors (ANII)

interpretation of Code requirements, the ANII decided not to sign the NIS-2 form for the

Charging / High Head Safety Injection Pump replacement. It was SNCs position that,

based on an ASME Section XI response to SNCs request for a code interpretation, the

replacement parts are fully qualified to be used as permanent ASME Section XI Class 2

replacement parts. The interpretation requested a response to the question Is it a

requirement of IWA-2110 (h) [1989 Edition of ASME Section XI] that the ANII approve

owners corrective action performed under the owners Appendix B program? The reply

from ASME was No.

The inspectors performed an in-house review of available information provided by the

licensee on the replacement pump. The performance of non-destructive inspection,

visual inspection, and reconciliation evaluation details were reviewed by the inspectors,

and satisfactory inservice testing of the replacement pump was observed. The

inspectors reviewed the following documents associated with the Charging / High Head

Safety Injection Pump 2B replacement and did not identify any immediate safety

concerns with the use of the pump, and that except for the ANIIs signature, those

requirements of ASME Section XI, 1989 Edition affecting the structural integrity of the

replacement pump have been essentially met.

  • DOEJ-SS-2052666001-001, Documentation of Engineering Judgment 001 Code

Reconciliation

  • DOEJ-SM-2052666001-002, Documentation of Engineering Judgment 002 Storage

Issue for Pump Casing

  • DOEJ-SS-2052666001-003, Documentation of Engineering Judgment 003 Design

Deficiencies Evaluation

  • RER 2052666001, Design Verification Summary
  • NDR-05-003 Attach. 5, Nonconformance Disposition Report
  • SNCs response to inspectors questions transmitted in e-mail dated 2/21/06.

However, the inspectors did not consider that the code case interpretation provided by

ASME resolved the lack of signature by the ANII. ASME Section XI, Article IWA-7520 of

ASME Section XI, 1989 Edition also requires a completed Owners Report for Repairs or

Replacements, Form NIS-2, be maintained by the owner, and article IWA-6000 requires

that the NIS-2 form be submitted to regulatory authorities with the Inservice Inspection

Summary Report within 90 days of the completion of the Inservice inspection conducted

during each refueling outage. As identified in SNCs letter to the NRC dated March 1,

2006, that transmitted FNP Unit 2 Inservice Inspection Summary Report, the NIS-2 form

was not completed. The NIS-2 form was not signed by the ANII, and SNC did not fully

23

explain why. Review of the documentation by the inspectors suggested that the ANII

remains concerned with the replacement part being out of control of an Appendix B

program for many years. The NRC holds the signature of the ANII in high regard and

relies on the ANII approval of such actions to assure Code compliance. An incomplete

NIS-2 form, indicates that all requirements of the Code have not been complied with.

Analysis: The performance deficiency was that the licensee did not meet Code by not

having the NIS-2 form completed. The finding is more than minor because it affects the

Mitigating Systems Cornerstone objective to assure the reliability of systems that

respond to events to prevent undesirable consequences and is associated with the

design control attribute in that qualification remains questionable because there is a lack

of assurance that all code requirements have been met.

The inspectors processed the finding using Appendix A of Inspection Manual Chapter 0609. The finding was evaluated using the Phase 1 screening worksheet and because

it represents a qualification deficiency confirmed not to result in a loss of operability, it

was determined that the deficiency is of very low risk significance (Green). This finding

has been entered into the licensees Corrective Action Program as CR 2006104737.

Enforcement: 10CFR50.55a(a)(2) requires Nuclear Class 1, 2 and 3 components meet

the requirements of the Section XI of the ASME Code. The 1989 Edition of Section XI

requires a completed NIS-2 Form signed by an ANII that documents that the owner has

performed examinations and taken corrective measures in accordance with all the

requirements of ASME Section XI. Contrary to the above, for the Unit 2B Charging/High

Head Safety Injection pump replacement, the licensee did not have a completed NIS-2

Form.

Because this finding is of very low safety significance and has been entered into the

licensees corrective action program as CR 2006104737, this violation is being treated

as a non-cited violation (NCV) consistent with Section VI.A of the NRC Enforcement

manual (NCV 05000364/2006003-03, Failure to Meet Pump Code

/Requirements/Details).

.3

Semi-Annual Trend Review

a.

Inspection Scope

As required by Inspection Procedure 71152, Identification and Resolution of Problems,

the inspectors performed a review of the licensees CAP and associated documents to

identify trends that could indicate the existence of a more safety significant safety issue.

The inspectors review focused on CRs with corrective action that were not sufficiently

comprehensive to reduce the likelihood or prevent recurrence of the condition. The

review also considered the results of the daily inspector CAP item screening discussed

in Section 4OA2.1, licensee trending efforts, and licensee human performance results.

The inspectors reviewed the licensee quarterly trend reports for November 2005 -

January 2006, and February - April 2006, daily CRs, selected completed CRs,

Maintenance Rule (a)(1) list, equipment health reports, and quality assurance reports to

identify issues not recognized by the licensee. The inspectors compared and contrasted

their results with the results contained in the licensees quarterly trend reports.

Corrective actions associated with a sample of the issues identified in the licensees

trend report were reviewed for adequacy. The inspectors also evaluated the reports

24

against the requirements of the licensees CAP procedures FNP-0-AP-30.0, Corrective

Action Reporting and NMP-GM-002-GL05, Corrective Action Program Trend Coding and

Analysis Guideline, and the requirements of 10 CFR 50, Appendix B.

b.

Findings and Observations

No findings of significance were identified. The inspectors noted that the licensee had

identified adverse trends with quality of physical work and events related to 4160V

breakers. These were the two most significant issues noted by the inspectors during the

semi-annual review period. Quality of physical work is currently being addressed by the

Maintenance department with action item due dates of August 2006. The events

surrounding 4160V breakers will continue to be evaluated into the next quarter (May

2006, June 2006) and have not been analyzed by the licensee as its trend quarter has

not ended. A separate observation was noted by the inspectors. During a review of the

last two quarters of the Farley Key Performance Indicators, there has been little

increase in the Reactivity Management Index (RMI) with a significant number of

reactivity events. The RMI has remained in a Green overall status over the last twelve

months in the presence of twenty-two level 3 and 4 reactivity management events.

When input to the RMI calculation, the severity level 3 and 4 reactivity issues do not

have significant worth. This would require 20-40 incidents over a twelve month period to

change RMI color and require additional licensee attention. The inspectors identified

this to the licensee and the licensee is evaluating a potential change to the RMI

calculation (SNC fleet wide) that could improve the threshold for monitoring these

events to be more useful in recognizing and addressing potential problem areas. The

licensee has addressed this issue in CR 2006105917.

4OA5 Other Activities

.1

Operation of an Independent Spent Fuel Storage Installation (ISFSI)

a.

Inspection Scope

Inspectors reviewed selected ISFSI operations records to verify that the licensee had

properly identified each fuel assembly in the two latest casks placed on the ISFSI pad.

The inspectors also reviewed Technical Specifications to verify that the fuel placed in

these casks met the requirements. The inspectors also reviewed ISFSI document

control practices to verify that the required records were being retained and duplicate

records were being kept at a separate location. The inspectors walked down the ISFSI

pads to assess the material condition of the casks, the installation of security

equipment, and the performance of the monitoring systems.

b.

Findings

No findings of significance were identified.

.2

Independent Spent Fuel Storage Installation (ISFSI) Radiological Controls

a.

Inspection Scope

The inspectors reviewed gamma-ray, neutron, and contamination surveys of the ISFSI

facility. Inspectors also observed routine gamma-ray surveys and compared the results

25

to previous surveys and TS limits. The inspectors evaluated implementation of

radiological controls, including labeling and posting, and discussed controls with an HP

Technician and HP supervisory staff. Environmental monitoring for direct radiation from

the ISFSI was reviewed, and inspectors observed placement of thermoluminescent

dosimeters.

Radiological control activities for ISFSI areas were evaluated against 10 CFR Part 20,

10 CFR Part 72, and Admentment 2 to the Certificate of Compliance No. 1014 TS

details. Documents reviewed are listed in the Attachment.

b.

Findings

No findings of significance were identified.

.3

(Closed) NRC Temporary Instruction (TI) 2515/165: Operational Readiness of Offsite

Power and Impact on Plant Risk

The inspectors reviewed licensee procedures and controls and interviewed operations

and maintenance personnel to verify these documents contained specific attributes

delineated in the TI to ensure the operational readiness of offsite power systems in

accordance with plant Technical Specifications; the design requirements provided in 10 CFR 50, Appendix A, General Design Criterion 17, "Electric Power Systems;" and the

impact of maintenance on plant risk in accordance with 10 CFR 50.65(a)(4),

"Requirements for Monitoring the Effectiveness of Maintenance at Nuclear Power

Plants." Documents reviewed are listed in the Attachment. Appropriate documentation

of the results of this inspection was provided to NRC headquarters staff for further

analysis, as required by the TI. This completes the Region II inspection TI requirements

for the Joseph M. Farley Nuclear Station.

.4

(Closed) Unresolved Item [URI] 50-348, 364/2004-04-02, Non-conservative Acceptance

Criteria Used For Service Water Pump Testing

The above URI was opened because the licensee was testing the Component Cooling

Water (CCW) heat exchangers just prior to refueling outages after they had been

cleaned. Therefore, they were potentially getting incorrect as-found performance data

on heat exchanger capability.

In August, 2005, the licensee tested the worst case Unit 2 heat exchanger at the end of

an operating cycle, prior to cleaning. The inspectors reviewed the data and discussed

the data collection methods and results with the licensee. Farley corrective action

Condition Report 2004102818 documented the result and the technical justification,

RER C051797501. The licensees conclusion was that the CCW exchangers are fully

capable of performing their function under worst case conditions between their

scheduled once-per-cycle cleanings. With the attendant changes the licensee had

made to their preventive maintenance program regarding cleaning of the river intake

structure and ultimate heat sink pond, the inspectors concluded the licensees response

to CR 2004 102818 was acceptable.

26

4OA6 Meetings, Including Exit

On July 7, 2006, the inspectors presented the inspection results to Mr. Randy Johnson

and the other members of his staff who acknowledged the findings. The inspectors

confirmed that proprietary information was not provided or examined during the

inspection.

ATTACHMENT: SUPPLEMENTAL INFORMATION

Attachment

SUPPLEMENTAL INFORMATION

KEY POINTS OF CONTACT

Licensee personnel

W.L. Bargeron, Assistant General Manager - Operations

W. R. Bayne, Performance Analysis Supervisor

S. H. Chestnut, Engineering Support Manager

P. Harlos, Health Physics Manager

L. Hogg, Security Manager

J. Horn, Training and Emergency Preparedness Manager

J.R. Johnson, Plant General Manager

T. Livingston, Chemistry Manager

B. L. Moore, Maintenance Manager

W. D. Oldfield, Quality Assurance Supervisor

J. Swartzwelder, Work Control Superintendent

R. J. Vanderbye, Emergency Preparedness Coordinator

R. Wells, Operations Manager

T. L. Youngblood, Assistant General Manager - Plant Support

NRC personnel

S. Shaeffer, Division of Reactor Projects, Branch Chief

D. Simpkins, Division of Reactor Projects, Acting Branch Chief

LIST OF ITEMS OPENED, CLOSED, AND DISCUSSED

Opened and Closed

05000348/2006-003-01

NCV

Failure to Follow Procedures for Containment Closeout

(Section 1R20)

05000348/2006-003-02

NCV

Failure to Control Contractors Results in Fuel Transfer

System Damage (Section 1R20)

05000364/2006-003-03

NCV

Failure to Meet Pump Code Requirements/Details (Section

4OA2.2)

Closed

05000348, 364/2515/165

TI

Operational Readiness of Offsite Power and Impact on

Plant Risk (Section 4OA5.3)

05000348, 364/2004-04-02 URI

Non-conservative Acceptance Criteria Used For Service

Water Pump Testing (Section 4OA5.4)

Discussed

None

2

Attachment

LIST OF DOCUMENTS REVIEWED

Section 1R04: Equipment Alignment

UFSAR Section 5.5.7

Technical Specification Section 3.5.2

Student Lesson Plan OPS-52102B-40302C Emergency Core Cooling

RHR Function System Description A-181002

Section 1R08: Inservice Inspection Activities

NMP-ES-024-502, PDI Generic Procedure for the Ultrasonic Examination of Ferritic Pipe Welds

(Appendix VIII), Ver 1.0

NMP-ES-024-501, PDI Generic Procedure for the Ultrasonic Examination of Austinetic Pipe

Welds (Appendix VIII), Ver 1.0

FNP-0-NDE-100.34, Nondestructive Examination Procedure

Boric Acid Corrosion Control Program Quarterly Report 4th Quarter - October 1, 2005 -

December 31, 2005

NMP-ES-019, Boric Acid Corrosion Control Program, Ver 1.0

NMP-ES-019-GL01, Boric Acid Corrosion Control Implementation Guideline, Ver 1.0

FNP-0-M-101, Boric Acid Corrosion Control Program, Ver 10

FNP-0-EPT-4496, Corrosion Assessment, Ver 2.0

Westinghouse MRS-SSP-1169-ALA/APR, Rev. 2, Farley Units 1 & 2 In-Service Steam

Generator Eddy Current Analysis Guidelines

Westinghouse MRS-SSP-1052-ALA/APR, Rev. 6, Secondary Side Tubesheet Inspection -

Westinghouse Model 54F Sgs

Westinghouse MRS 2.4.2 GEN-35, Rev. 11, Eddy Current Inspection Of Preservice and

Inservice Heat Exchanger Tubing

MIS-FNP-5-17, Review of Farley 1R19 Steam Generator Secondary Side Loose Parts for Next

Cycle of Operation, Dated November 4, 2004

Steam Generator Degradation Assessment for Farley 1R20 Inservice Inspection for Model 54F

RSGs

Steam Generator History and Operating Assessment

Eddy Current Analyses Calibration Nos. 19 for SG B tube R45C59; 9 for SG A tubes R17C04;

11 for SG A tubes R15C10 and R26C10; 41 for SG C tubes R11C82, R12C82, and R10C93;

and 43 for SG C tubes R04C51, R03C56, and R13C81

Specific Assessment of Potential Degradation Mechanism Developed for the Upcoming Outage

Data Acquisition and Analysis Personnel Qualification for Level II Data Operators, Level II A

and Level III A Analysts

Farley Unit 1, ALA R20 Steam Generator Inspection Reference Manual

Westinghouse Reference Letter LTR-SGDA-04-326, Evaluation of Loose Parts for Farley Unit 1

Fall 2004 Outage, Dated October 29, 2004

RER C049635101, to initiate, Implement, and Resolve Loose Parts in the Secondary Side of

Steam Generators Due to Flex Gaskets from the Broken Spiral Wound Gaskets Used in Valves

CRs: 2005112010, 2004000259, 2004104601, 2005111036, 2004104465, 2006103677,

2006103737, 2006103680, 2006103746, 2005200863

3

Attachment

Section 1R11: Licensed Operator Requalification

FNP-1-AOP-2.0, Steam Generator Tube Leakage

FNP-1-AOP-4.0, Loss of Reactor Coolant Flow

FNP-1-AOP-17.0, Rapid Load Reduction

FNP-1-AOP-100, Instrumentation Malfunction

FNP-1-UOP-3.1, Power Operation

FNP-0-ESP-0.1, Reactor Trip Response

FNP-0-EIP-9.0, Emergency Classification and Actions

Section 1R20: Refueling and Outage Activities

FNP-0-UOP-4.0, General Outage Operations Guidance

FNP-0-AP-52, Equipment Status Control and Maintenance Authorization

FNP-1-UOP-4.1, Refueling Outage Operation

FNP-0-AP-94, Outage Nuclear Safety

FNP-1-UOP-4.3, Mid-Loop Operations

FNP-0-ACP-47.3, Outage Preparation

FNP-1-STP-35.0, Reactor Coolant System Pressure and Temperature/Pressurizer

Temperature Limits Verification

FNP-1-UOP-2.1, Shutdown of Unit From Minimum Load to Hot Standby

FNP-1-UOP-2.2, Shutdown of Unit From Hot Standby to Cold Shutdown

FNP-1-SOP-1.6, Draining th Reactor Coolant System

FNP-1-SOP-1.3, Reactor Coolant System Filling and Venting-Vacuum Method

FNP-1-STP-18.4, Ctmt Mid-Loop and/or Refueling Integrity Verification and Ctmt Closure

FNP-1-IMP-201.45, Refueling Reactor Coolant System Level Calibration Q1B21FT0416

FNP-1-STP-35.1, Unit Startup Technical Specification Verification

FNP-0-ETP-3643, Verification of Rod Control System Availability

FNP-1-STP-101, Zero Power Reactor Physics Testing

FNP-1-STP-29.6, Calculation of Estimated Critical Condition

Section 2OS1: Access Controls to Radiologically Significant Areas

Procedures, Manuals, and Guidance Documents

Farley Nuclear Plant (FNP) Dosimetry Procedure (DOS)-1, Personnel Monitoring, Version

(Ver) 43.0

FNP-1- FHP - 1.0, Refueling Operations, Ver. 8.0

FNP-0-ACP- 7.0, Foreign Material Exclusion Program, Ver. 16.0

FNP -0-RPC -0.1, Key Control Program and Health Physics Guidance for Control of High

Radiation Areas, Exclusion Areas (Locked High Radiation Areas) and Very High Radiation

Areas, Ver. 9.0

FNP-1-RPC -0.2, Unit 1 Reactor Vessel Maintenance Sump Entry, Ver. 2.0

FNP 0-RPC-4, Refueling Survey, Ver. 18.0

FNP-0-RPC-26, Radiological Surveys and Monitoring, Ver. 32.0

FNP-0-RCP-26, Temporary Change Notice Form (TCNF), Radiological Surveys and Monitoring,

Ver. 32.1

FNP-0-RPC-29, Contamination Guidelines, Ver. 38.0

FNP-0-RPC-29.1, Guidelines for Personnel Decon and Response to Personnel Contamination

4

Attachment

Events, Ver. 5.0

FNP-0-RCP-57, Radioactive and Potentially Radioactive Material Handling, Ver. 28

FNP-0-RPC-114, Operation and Care of Safety and Supplys Model RC 2095, LANCS Model

LI-520Y Series All Clear Air-Fed Hood, and Defense Apparels HSQ-10 Supplied Air Hood

Assembly, Ver. 7.0

FNP-0-RPC-367, Radiological Control Associated with Primary Steam Generator

Channelheads, Ver. 36.0

Records and Data Reviewed

Unit 1 (U1) and Unit 2 (U2) Spent Fuel Pool (SFP) Trash (Non-Fuel Items Inventory), as of

04/20/2006

U1 ICA-3, U1 SFP Inventory Map, as of 04/20/2006

U2 ICA-6, U2 SFP Inventory Map, as of 04/20/2006

U1 SFP Debris Canister Stack Sequence: Long Term and Short Term Storage Items (Data as

of 04/21/2006).

U2 SFP FSDC Stack Sequence: Long Term and Short Term Storage Items as Loaded for

FATF 02-99-021, (Data as of 04/21/2006)

Radiation Work Permit (RWP) 06-0501, Operations: Routine Inspections, Activities and

Training Within Radiation Controlled Areas by Operations Personnel. CAUTION: Do Not use

this RWP for Containment (CTMT) Entries, Rev. 0

RWP 06-0703, Engineering Support (ES): All Work Associated with Fuel Inspections, Fuel

Oxide Measurements, Top Nozzle Replacement, etc., in the Unit 1 (U1) or Unit 2 (U2) Spent

Fuel Pool (SFP). NOTE: Not for New Fuel Receipt. CAUTION: Do Not Use this RWP for

CTMT Entries, Rev. 0

RWP 06-0705, ES: All Work Associated with SFP Inventory Classification in the U1 or U2 SFP.

Caution: Do Not Use this RWP for CTMT Entries, Rev. 0

RWP 06-1444, Maintenance - All; All Work Associated with Repairs, Inspections, and

Observations in the Unit 1 Reactor Vessel Maintenance Sump to Support the 1R20 Outage.

No Entry While Incore Thimbles are Withdrawn or While Driving Detectors, Rev. 0

RWP 06-1453, Maintenance-MM; All Work Associated with Maintenance on Valves Reading

1000 mRem/hr or Greater Contact and not Specifically Covered by Other RWPs in the

Auxiliary Building and Unit 1 CTMT to Support the 1R20 Outage, Rev. 0

RWP 06-1467, Maintenance-MM, FAC,HP,WMS; All Work Associated with Cleanout and

Maintenance of the U1 Reactor Cavity Transfer Canal to Support the 1R20 Outage. (To

Include Decon of the Upender Sump, Blind Flange Work, and all Repairs). Rev. 0

RWP 06-1488, Maintenance-MM, WMS, Wyle; All Work Associated with Routine Snubber Work

in the Auxiliary Building, the Unit 1 Containment, and the Snubber Trailer/Building to Support

the 1R20 Outage, Rev. 0

RWP 06-1504, Operations-OPS, ES, Westinghouse; All work to Support for Refueling Activities

in the U1 Containment and the U1 SFP Room during the 1R20 Outage, Rev.0

RWP 06-1707, Maintenance - All: All Work Associated with Visual Bottom Mounted

Instrumentation (BMI) Penetration Inspection of the U1 Containment Reactor Vessel

Maintenance Sump during the 1R20 Outage. No Entry While Incore Thimbles are Withdrawn

or While Driving Detectors, Rev. 0.

RWP 06-1730, Engineering-ES; Westinghouse, ES, HP; All Work Associated with the

Installation and Removal of Nozzle Dam/Nozzle Covers in the Primary Steam Generators to

Support the 1R20 Outage, Rev. 0

RWP 06-1731, Engineering-ES; Westinghouse, ES, HP; All Work Associated with the Primary

Steam Generator Eddy Current Testing and Repairs to Support the 1R20 Outage, Rev. 0

5

Attachment

Survey Number (No.) 13991, Unit 1 Reactor Cavity (1CB155), Dose Rate Data, 11/11/04

Survey No. 22708, U-1 Auxiliary Building 83 foot elevation (1AB83), Dose Rate and

Contamination Data, 03/19/06

Survey No. 23275, 1AB83, Dose Rate and Contamination Data, 04/09/2006

Survey No. 23317, 1AB83, Dose Rate and Contamination Data, 04/10/2006

Survey No. 23360, 1Auxiliary Building RHR Pump Room (1AB83131) Dose Rate and

Contamination Data, 04/10/06

Survey No. 23403, U1 Containment Sump (1CB) Dose Rate and Contamination Data,

04/11/2006

Survey No. 23371, HP Derived Air Concentration Report, U1 Reactor Sump Air Sample,

04/11/2006

Survey No. 23457, U1 Containment Transfer Canal (1CB155) Dose Rate Data, 04/12/2006

Health Physics Survey (HPS) Data (Airborne) Associated with Reactor Stud Cleaning Activities:

HPS No. 23541, 04/15/2006; No. 23611, 04/15/2006; No. 23701, 04/16-17/2006; No. 23654,

04/16/2006;

Record of Dose Rates During Initial Fuel Assembly Transfer, 04/15/2006

Health Physics Locked High Radiation Area (LHRA) Control Log, Data 04/10-11/2006

Dose Report Data for: RWP 06-1444, Containment Reactor Vessel Maintenance Sump

Activities, 04/11/2006; RWP 06-1453, Maintenance on Valves $1000 mRem/hr, 04/20/2006;

RWP 06-1467, Cleanout and Maintenance of the U1 Rx Cavity Transfer Canal to Support the

1R20 Outage, 04/20/2006; RWP: 06-1707, Containment Reactor Vessel Maintenance

Sump Activities, 04/11/2006; RWP 06-1731, Primary Steam Generator Eddy Current Testing

and Repairs, 04/20/2006; RWP 06-1739, Installation & Removal of Nozzle Dam/Nozzle

Covers in Primary Steam Generator, 04/20/2006

Corrective Action Program (CAP) Documents

Nuclear Management Procedure (NMP) General Management ((GM) - 002, Corrective Action

Program, Ver. 4

Farley Nuclear Plant Health Physics Self Assessment, INPO 03-004 Guide (Radiation

Protection), 12/06-10/2004

Review of Locked High Radiation Area (LHRA) Administrative Controls, 08/09-12/2005

Condition Report (CR) 2005104299, HP Individual Logged-in on the Wrong RWP , 04/28/2005

CR 2005110573, Containment Entry Made on Auxiliary Building RWP, 10/24/2005

CR 2005110695, Inadvertent Sign-In to Wrong RWP, 10/26/2005

CR 2005105623, Maintenance Worker Direct Alarming Dosimeter Not Operating During RCA

Entry, 06/09/2006

CR 2005107891, Loss of Controls Securing Tri-Nuke Equipment Within the U1 Spent Fuel

Pool, 08/05/2005

CR 2005111645, Very High Radiation Area Key Lost, 11/15/2005

Section 2OS2: As Low As Reasonably Achievable (ALARA)

Procedures, Manuals, and Guidance Documents

FNP-0-RCP-7, Coordinated Exposure Reduction Program, Ver. 2.0

FNP-0-RCP-15, Temporary Shielding, Ver. 35.0

FNP-0-RCP-19, Pre and Post Job ALARA Planning for Work in Radiation Controlled Areas of

the Plant, Ver. 19.0

Chemical Degassing/Crud Burst 1RFO20

NMP-GM-002, Corrective Action Program, Ver. 4.

6

Attachment

Records and Data Reviewed

RWP Dose Tracking Records, 4/10/06 - 4/21/06

Plant ALARA Review Committee meeting minutes, 4/6/06

Monthly ALARA Report, March 2006

Declared Pregnant Worker Dosimetry Records, 2003 - 2004

1R20 ALARA Planning Checklists: Steam Generator Eddy Current Testing and Reactor Head

Assembly/Disassembly

RWP 06-1731, Steam Generator Eddy Current Testing, Rev. 0

RWP 06-1461, Reactor Head Assembly/Disassembly, Rev. 0

RWP 06-1481, All Work Inside U1 Regenerative Heat Exchanger Fence, Rev. 1

Survey 23241, U1 Regenerative Heat Exchanger Valves (Pre-Shield), 4/8/06

Survey 23427, U1 Regenerative Heat Exchanger Valves (Post-Shield), 4/11/06

Survey 23779, U1 C Steam Generator Hot Leg, 4/18/06

Crud Burst/Cleanup Survey Point Data, 1R17 - 1R20

CAP Documents

Health Physics Self-Assessment, INPO 03-004 Guide (Radiation Protection), 12/6/04 - 12/10/04

CR 2005111491, Improvement needed in determining the total job scope of scaffold

requirements for an outage, 11/11/05

CR 2005102060, Plant dose is at 161% of budget dose for the first month of the year, 2/18/06

CR 2004104041, Request an engineering evaluation to consider permanent shielding on U1

regenerative heat exchanger, 10/10/04

CR 2006101009, Increased dose to replace 1A incore detector due to new equipment issues,

2/3/06

Section: 2PS2 Radioactive Material Processing and Transportation

Procedures, Manuals, and Guidance Documents

FNP UFSAR, Chapter 11, Radioactive Waste Management

Joseph M. Farley Nuclear Plant Annual Radioactive Effluent Release Report for 2004, 04/25/05

FNP-0-030, Process Control Program, Rev. 15

FNP-0-RCP-801, Disposable Demineralizer System Operation (Hittman), Ver. 16.0

FNP-0-RCP-809, Isotopic Characterization, Scaling Factor Utilization, and Waste Classification

of Radioactive Waste Streams for Offsite Shipments and/or Near Surface Disposal, Ver.16.0

FNP-0-RCP-810, Shipment of Radioactive Waste, Ver. 44.0

FNP-0-RCP-811, Shipment of Radioactive Material, Ver. 34.0

FNP-0-RCP-839, Segregation of Low Level Solid Wastes, Rev. 6

FNP-1-SOP-49.0, Solid Waste Processing System, Ver. 23.0

FNP-1-SOP-50.0, Liquid Waste Processing System, Ver. 52.0

FNP-1-SOP-50.4, Demineralizer Resin Removal and Addition, Ver. 32.0

FNP-0-SOP-50.7, Liquid Waste Processing using the Supplemental Demineralizer System,

Ver. 36

Records and Data

U1 Waste Processing System Piping and Instrumentation Diagram (P&ID) No. D-175042,

Sheets 1, 2, 3,4 and 7

U2 Waste Processing System P&ID No. D-205042, Sheets 1, 2, 3,4 and 7

Radioactive Waste Shipment (RWS) 06-11, Primary Resin, 02/18/06

7

Attachment

RWS 05-24, LWP Mixed Media, 12/02/05

RWS 05-11, DAW Sealands, 07/15/05

RWS 05-05, Primary Resin, 04/21/05

RWS 05-02, Filter HIC, 02/23/05

10 CFR Part 61 Radioactive Waste Stream Analysis Reports, SFP filters, RCS filters, and

DAW, 2004 and 2005

10 CFR Part 61 Radioactive Waste Stream Analysis Report, Filter Smears, HIC C in shipment

RWS 05-02

10 CFR Part 61 In-House to Industrial Laboratory Comparison and Data Set Validation for SFP

filters, RCS filters and DAW, 2005

CoC no. 9208, Model No.10-142 Shipping Package, Rev. 15

Hazardous Material/Waste Handler Training Certificates for shipping staff

CAP Documents

CR 2004106550, FNP QA discovered a weight discrepancy in Radwaste Shipping

paperwork, 12/02/04.

CR 2005100836, QA Audit F-CRW-2004, Comment # 2: Potential misclassification of

radioactive waste shipments, 01/21/05

CR 2005108566, Challenges in cleaning sludge from Floor Drain Tank, 08/26/05

CR 2005111241, When loading DAW found 2 bags of trash with incorrect dose rates marked

on the bags, 11/06/05

CR 2006101693, Written to document contamination issues at the OSGSF fenced RCA

associated with preparations to ship 2 degraded sealand containers, 02/23/06

CR2006102506, Active leaks in the roof of the LLRWB, 03/21/06

CR2006102504, Fire Protection System has leak at the area center of the northern most aisle

in main bay of LLRWB, 03/21/06

Health Physics Self Assessment, December 06, 2004 to December 10, 2004

QA Surveillance # 2004-04, Primary Spent Resin Cask Shipment, 02/17/04

Section: 4OA1 Performance Indicator Verification

Procedures

FNP-0-AP-54, Preparation and Reporting of NRC Performance Indicator Data and NRC

Operating Data, Ver. 6.0

Records and Data Reviewed

Access Control Alarms, Cumulative Dose and Dose Rate Data; October 1, 2005 through

April 18, 2006

Special Report 2005-001-00, Inoperable Radiation Monitor R-29B

OOS effluent monitor logs, 6/1/05 - 3/6/06

Gaseous effluent release permits 50387.027.057.G and 60071.017.010.G

Liquid effluent release permits 50874.021.162.L and 60208.021.023.L

CAP Documents

CR 2005105520, 2B turbine building sump auto sampler failed to collect sample, 6/7/05

CR 2005112468, R-29B inoperable for greater than 7 days, 12/7/05

CR 2006100073, Isolation valve RCV-23B failed to close on high radiation signal from steam

generator blow down monitor R23B during surveillance test, 1/5/06

8

Attachment

Section 4OA2: Identification and Resolution of Problems

April 12, 2006 SNC Letter to Farley Engineering Manager, File: RER C051797501: Log: PS-

06-0117

Section 4OA5: Other Activities

A-173444, Power Quality Guide

BPO-1, Bulk Power Operations

FNP-1-SOP-28.1, Turbine Generator Operations

FNP-0-SOP-38.0, Diesel Generators

FNP-0-ACP-4, Switchyard control

FNP-1-STP-27.1, A.C. Source verification

FNP-0-ACP-52.3, On-Line Risk Assessment

FNP-1-AOP-5.2, Degraded Grid

FNP-2-ECP-0.0, Loss of All AC Power

ISFSI Radiological Controls Procedures, Manuals, and Guidance Documents

FNP-0-STP-822, Hi-Storm Overpack Surface Dose Rates, Ver. 2.0

Certificate of Compliance (CoC) No. 1014 for the Holtec International Hi-Storm 100 Cask

System, Amendment No. 2

Holtec Report No. HI-2053364, Hi-Storm CoC Radiation Protection Program Dose Rate Limits

for SNC, 03/01/05

Surveys, Data, and Records Reviewed

ISFSI Pad Survey # 18151, 08/25/05

ISFSI Pad Survey # 20156, 11/05/05

ISFSI Perimeter TLD Exposure Report - 2nd quarter 2005, 01/27/06

CR 2005110575, Discrepancy in neutron dose measured with DAD versus TLD for worker

involved in the spent fuel dry cask storage campaign, 10/24/05