6-28-2006 | On May 6, 2006, St. Lucie Unit 2 was in Mode 6, shutdown for the SL2-16 refueling outage. During steam generator eddy current testing ( ECT), FPL determined that an error was made during the previous refueling SG ECT that allowed a defect in a steam generator tube (R100 L96 in SG 2B) tolremain in service during Cycle 15 operation.
This event was caused by an incomplete rotating probe inspection of bobbin probe identified indications during SL2-15.T Corrective actions included plugging of the subject tube, and review of rotating probe data to ensure the entire target location was tested where the data was used to disposition a bobbin indication as "no degradation found"T This review determined (NDF) during the SL2-15 outage inspection.
that one other incomplete rotating probe test resulted in a second tube (R87 L97 in SG 2B) remaining in service during Cycle 15 that was not fully evaluated by Plus Point.T Tube integrity assessment for both tubes and in-situ pressure testing for R100 L96 during the SL2-16 autage, demonstrated that the defective tubes met the structural integrity and ac:Adent induced leakage performance criteria of NEI 97-06, " Steam Generator Program Guidelines." Therefore, there was no impact to the health and safety of the public. |
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FACILITY NAME (1) NUMBER (2)___ DOCKET� LER NUMBER (6) �
Description of the Event
ECT consists of bobbin probe inspections for general purpose screening, and rotating probe inspections for regions where the bobbin probe is not qualified for detection of degradation (i.e., tubesheet region). Therefore, the rotating probe is used to characterize bobbin indications to ensure compliance with TS SR 4.4.5.4.a.6 "Plugging or Repair Limit.
On May 6, 2006, St. Lucie Unit 2 was in Mode 6 shutdown for the SL2-16 refueling outage.
During steam generator (SG) (EIIS: AB) ECT testing, FPL determined that an error was made during the previous refueling SG ECT. During the previous February 2005 SG inspection, a bobbin indication was reported at the first hot leg tube support in Row 100 Line 96 in SG 2B. Subsequently, FPL performed a diagnostic inspection with a rotating Plus Point probe. No defect was detected and the tube remained in service.
During the May 2006 steam generator inspection, FPL again performed a Plus Point diagnostic test after the same indication was reported during bobbin coil testing, and this time the rotating probe confirmed the presence of a defect in this tube. A routine review of prior inspection data was completed and it was determined on May 6, 2006, that the rotating probe inspection from SL2-15 did not include the entire target location to be tested, i.e., eggcrate tube support, thereby missing the portion that contained the indication. R100 L96 exceeded initial screening limits and was in-situ pressure tested to demonstrate that the structural integrity and accident induced leakage performance criteria of NEI 97-06 (Steam generator Program Guidelines) were maintained. This tube passed in-situ pressure testing without any leakage or burst. This effectively demonstrated that the 2B SG was capable of performing its intended safety function during Cycle 15 operation. However, the maximum depth measured during SL2-16 suggests that the indication likely exceeded the 40% plugging limit of TS 4.4.5.4.a.6 at the time of the SL2-15 inspection.
All SL2-15 rotating probe data was reviewed to ensure that the entire target location was tested where the data was used to disposition a bobbin indication as "no degradation found" (NDF). This review determined that the SL2-15 rotating probe test for a bobbin indication in R87 L97 at the second support in SG 2B was also incomplete. The bobbin indication was observed again at SL2-16 and a rotating probe test confirmed the indication as a crack and the tube was plugged. Based on tube integrity assessment during the SL2-16 outage, there was no structural or leakage integrity issue associated with this tube remaining in service during Cycle 15. The results of the data reviews show this to be an event limited to a single calibration group of data in 2005. No additional incomplete tests were observed.
In summary, two rotating probe inspections during the SL2-15 ECT did not cover the entire target area of the tube support region, thereby missing indications identified by the bobbin probe as potential defects. This event is considered an incomplete surveillance caused by the two incomplete rotating probe inspections of bobbin probe indications identified during SL2-15.
DOCKETFACILITY NAME (1) LER NUMBER (6) PAGE (3)NUMBER (2)
Cause of the Event
The cause for the incomplete inspections is that the data acquisition equipment operator did not recognize that the tube end was incorrectly located and failed to correct the situation. The error occurred only during special interest rotating probe inspection of bobbin indications, and resulted in faulty input to the axial encoder, which determines axial position within the tube. The error appears to be a human performance error. The operator has several years of experience and a good performance record. There were no known extenuating circumstances. The data was properly collected by the same operator before and after the error occurred. In addition, the inspection vendor does have a human performance program that is reviewed with each operator prior to each inspection.
Analysis of the Event
This event is reportable under 10 CFR 50.73(a)(2)(i)(B) as any operation or condition prohibited by the Technical Specifications (TS). TS 3.4.5 states that each steam generator shall be operable or restored to operable status prior to increasing Tavg above 200 degrees F. TS Surveillance 4.4.5.0 states that each steam generator shall be demonstrated operable by performance of the required augmented in service inspection program. Contrary to TS, St. Lucie Unit 2 exceeded 200 degrees F without establishing the operability of the steam generators by surveillance requirements. Although the in situ pressure test performed during the Spring 2006 outage concluded that the degraded SG tube was capable of performing its safety function, the maximum depth measured during SL2-16 suggests that the indication likely exceeded the 40% plugging limit of TS 4.4.5.4.a.6 at the SL2-15 inspection.
Analysis of Safety Significance The tube at R100 L96 in SG 2B was in-situ pressure tested to demonstrate that the structural integrity and accident induced leakage performance criteria of NEI 97-06 (Steam Generator Program Guidelines) was maintained. The tube passed in-situ pressure testing without any leakage or burst. Based on tube integrity assessment during SL2-16, R87 L97 did not exceed initial tube integrity screening criteria for in-situ pressure testing, therefore, there was no structural or leakage integrity issue associated with this tube remaining in service during Cycle 15. This effectively demonstrated that the 2B SG was capable of performing its intended safety function during Cycle 15 operation.
However, the maximum depths measured during SL2-16 suggest that the indications in these tubes likely exceeded the 40% plugging limit of TS 4.4.5.4.a.6 at the SL2-15 inspection.
Based on the satisfactory in-situ pressure testing, performance of 100% ECT during the SL2-16 outage, and subsequent process verification, FPL concludes this event had no impact on the health and safety of the public.
FACILITY NAME (1) NUMBER DOCKET(2) LER NUMBER (6) PAGE (3) St. Lucie Unit 2 05000389
Corrective Actions
The proposed corrective actions and supporting actions listed below are entered into the site corrective action program.� Any changes to the proposed actions will be managed under the commitment management change program.
1.R100 L96 in SG 2B was in-situ pressure tested to verify that structural and leakage integrity was maintained during Cycle 15.�Tube integrity assessment for R87 L97 in SG 2B at SL2-16 verified that structural and leakage integrity was maintained during Cycle 15.� Both tubes were plugged at SL2-16 (Complete).
2.All rotating probe data was reviewed to ensure that the entire target location was tested where the data was used to disposition a bobbin indication as "no degradation found (NDF)" during SL2-16.� No additional incomplete tests were observed (Complete).
3.Revise the FPL steam generator program procedure to capture the lessons learned from St. Lucie 2, regardless of the vendor used for future inspections, to include attributes for verification of vendor training on location of tube ends using auto-locating software, verification that FPL data analysis guidelines provide effective methods to ensure that the extent of examination is obtained for rotating probe inspection of bobbin indications, including a requirement that lead personnel review results where a bobbin indication was resolved as a NDF, and verification that vendor has a human performance program and training as part of their inspection preparations.� (08/15/06).
Similar Events Inspection.
In-Service.
Failed Components
None
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Box 249 Buchanan, N.Y. 10511-0249Entergy Tel (914) 734-6700 Fred Dacimo Site Vice President Administration September 13, 2006 Indian Point Unit No. 3 Docket No. 50-286 N L-06-084 Document Control Desk U.S. Nuclear Regulatory Commission Mail Stop O-P1-17 Washington, DC 20555-0001 Subject:L Licensee Event Report # 2006-002-00, "Manual Reactor Trip as a Result of Arcing Under the Main Generator Between Scaffolding and Phase A&B of the Isophase Bus Housing" Dear Sir: The attached Licensee Event Report (LER) 2006-002-00 is the follow-up written report submitted in accordance with 10 CFR 50.73. This event is of the type defined in 10 CFR 50.73(a)(2)(iv)(A) for an event recorded in the Entergy corrective action process as Condition Report CR-IP3-2006-02255. There are no commitments contained in this letter. Should you or your staff have any questions regarding this matter, please contact Mr. Patric W. Conroy, Manager, Licensing, Indian Point Energy Center at (914) 734-6668. Fred R. Dacimo Site Vice President Indian Point Energy Center Docket No. 50-286 NL-06-084 Page 2 of 2 Attachment: LER-2006-002-00 CC: Mr. Samuel J. Collins Regional Administrator — Region I U.S. Nuclear Regulatory Commission U.S. Nuclear Regulatory Commission Resident Inspector's Office Resident Inspector Indian Point Unit 3 Mr. Paul Eddy State of New York Public Service Commission INPO Record Center NRC FORM 366 U.S. NUCLEAR REGULATORY COMMISSION APPROVED BY OMB NO. 3150-0104 EXPIRES: 06/30/2007
(6-2004)
. Estimated burden per response to comply with this mandatory collection request: 50 hours.DReported lessons learned are incorporated into the licensing process and fed back to industry. Send comments regarding burden estimate to the Records and FOIA/Privacy Service Branch (T-5 F52), U.S. Nuclear Regulatory Commission, Washington, DC 20555-0001, or by internetLICENSEE EVENT REPORT (LER) e-mail to infocollects@nrc.gov, and to the Desk Officer, Office of Information and Regulatory Affairs, NEOB-10202, (3150-0104), Office of Management and Budget, Washington, DC 20503. If a means used to impose an information collection does not display a currently valid OMB control number, the NRC may not conduct or sponsor, and a person is not required to respond to, the information collection. ■ 1. FACILITY NAME 2. DOCKET NUMBER I 3. PAGE
INDIAN POINT 3 05000-286 1 OF 6
4.TITLE: Manual Reactor Trip as a Result of Arcing Under the Main Generator Between
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