ML050120255
| ML050120255 | |
| Person / Time | |
|---|---|
| Site: | Hope Creek |
| Issue date: | 01/12/2005 |
| From: | Lyons J NRC/NRR/DLPM |
| To: | Lanning W Division of Reactor Safety I |
| Collins D S, NRR/DLPM, 415-1427 | |
| References | |
| FOIA/PA-2005-0103, TAC MC5111 | |
| Download: ML050120255 (7) | |
Text
January 12, 2005 MEMORANDUM TO: Wayne D. Lanning, Director Division of Reactor Safety Region I FROM:
James E. Lyons, Deputy Director
/RA/
Division of Licensing Project Management Office of Nuclear Reactor Regulation
SUBJECT:
RESPONSE TO TASK INTERFACE AGREEMENT - TIA 2004-006, REQUEST FOR EVALUATION OF SARGENT AND LUNDY REPORT ON HOPE CREEK GENERATING STATION B REACTOR RECIRCULATION PUMP AND PSEG NUCLEAR, LLC EVALUATION OF HIGH PRESSURE COOLANT INJECTION SYSTEM EXHAUST SNUBBERS (TAC NO. MC5111)
By letter dated December 13, 2004, Region I submitted TIA 2004-006 requesting assistance from the Office of Nuclear Reactor Regulation (NRR) in reviewing PSEG Nuclear, LLCs (PSEG or the licensee) resolution of technical concerns related to the reactor recirculation pump and the high pressure coolant injection (HPCI) system exhaust line. Region I requested NRR review of three specific items.
The first item was to review the Sargent and Lundy (S&L) report, Independent Assessment of Hope Creek Reactor Recirculation System and Pump Vibration Issues, and determine whether operation of Hope Creek Generating Station (Hope Creek) over the next operating cycle represents an unacceptable increase in the probability of a recirculation pump shaft failure or a small break (i.e. seal) loss-of-coolant accident (LOCA) event. The staffs review of the S&L report found that it did not provide sufficient information to completely address the concern.
The licensee subsequently provided additional information to the Nuclear Regulatory Commission (NRC) staff; however, based on its review of the technical information provided by the licensee, the NRC staff concludes that the probability of a pump shaft failure of RR pump B during the next cycle of operation is indeterminate. The licensee proposed enhanced vibration monitoring of the reactor recirculation pumps. The NRR staff found that there is reasonable assurance that the licensees enhanced vibration monitoring program can detect a potential crack in the reactor recirculation pump shaft in time to take appropriate actions to reduce pump speed and remove the pump from service prior to a complete shaft failure. Thus, the NRR staff considers that operation of the recirculation pump for one more cycle does not represent an unacceptable increase in the probability of a shaft failure leading to a small LOCA event. The details of NRRs assessment are contained in Attachment 1.
The second item was to review the S&L report and determine whether PSEGs decision to not perform the recirculation pump shaft inspections for potential shaft cracking as described in General Electric (GE) Service Information Letter (SIL) 459 represents an unacceptable increase in the probability of a recirculation pump shaft failure or small break (i.e. seal) LOCA event.
The licensees survey of the industry indicates that a number of recirculation pumps have successfully operated well past the inspection interval proposed in SIL 459. The purpose of the inspection recommended in SIL 459 was to detect a potential crack in the recirculation pump shaft. The NRR staff found that there is reasonable assurance that the licensees enhanced monitoring program can detect a potential crack in the reactor recirculation pump shaft in time to take appropriate actions to reduce pump speed and remove the pump from service prior to a complete shaft failure. Thus, the NRR staff concludes that PSEGs decision not to perform the pump shaft inspection as recommended in GE SIL 459 does not represent an unacceptable increase in the probability of a shaft failure leading to a small LOCA event. The details of NRRs assessment are contained in Attachment 1.
The third item was to provide a technical assessment of PSEGs engineering evaluation for the failed HPCI system steam exhaust line snubbers and determine whether it provides an adequate basis for the operability of the HPCI system per GL 91-18. The NRR staff found that the licensees evaluation provides an adequate basis for the operability of the HPCI system per GL 91-18. The details of NRRs assessment are contained in Attachment 2.
Principal Contributors: J. Fair W. Poertner S. Unikewicz Docket No. 50-354 cc w/ attachments: C. Casto C. Pederson D. Chamberlain January 12, 2005 successfully operated well past the inspection interval proposed in SIL 459. The purpose of the inspection recommended in SIL 459 was to detect a potential crack in the recirculation pump shaft. The NRR staff found that there is reasonable assurance that the licensees enhanced monitoring program can detect a potential crack in the reactor recirculation pump shaft in time to take appropriate actions to reduce pump speed and remove the pump from service prior to a complete shaft failure. Thus, the NRR staff concludes that PSEGs decision not to perform the pump shaft inspection as recommended in GE SIL 459 does not represent an unacceptable increase in the probability of a shaft failure leading to a small LOCA event. The details of NRRs assessment are contained in Attachment 1.
The third item was to provide a technical assessment of PSEGs engineering evaluation for the failed HPCI system steam exhaust line snubbers and determine whether it provides an adequate basis for the operability of the HPCI system per GL 91-18. The NRR staff found that the licensees evaluation provides an adequate basis for the operability of the HPCI system per GL 91-18. The details of NRRs assessment are contained in Attachment 2.
Principal Contributors: J. Fair W. Poertner S. Unikewicz Docket No. 50-354 cc w/ attachments: C. Casto C. Pederson D. Chamberlain DISTRIBUTION:
PUBLIC RidsOgcRp JFair PDI-2 Reading RidsAcrsAcnwMailCenter SUnikewicz RidsNrrDlpm (TMarsh/JLyons)
RidsNrrDeEmeb (EImbro)
WPoertner RidsNrrDlpmLpdi (CHolden)
RidsNrrDe (RBarrett)
GMiller RidsNrrDlpmLpdi2 (DRoberts)
RidsNrrLACRaynor RFretz RidsNrrPMDCollins KManoly RidsRgn1MailCenter DTerao ADAMS Accession Number:
OFFICE PDI-2/PE PDI-2/PM PDI-2/LA EMEB-B/SC PDI-2/SC PDI/PD DLPM/DD NAME GMiller DCollins (RFretz for)
CRaynor KManoly DRoberts CHolden (DRoberts for)
JLyons DATE 01/12/05 01/12/05 01/12/05 1/11/2005 01/12/05 01/12/05 01/12/05 OFFICIAL RECORD COPY Reactor Recirculation Pump Vibration Review
Background
The B Hope Creek Generating Station (Hope Creek) reactor recirculation (RR) pump has had a historical problem involving high vibration levelsabout double those on the A RR pump.
Past PSEG Nuclear, LLC (PSEG or the licensee) actions to reduce the vibration levels have not been effective. The high vibrations have been attributed, in part, to a slight bowing of the shaft in the area below the seal package area. The vibrations have led to frequent seal replacements (1.5-year intervals versus the expected 6-year intervals).
In addition to the bowing, the A and B RR pump shafts are expected to have some degree of thermally induced stress cracking based on industry operating experience described in General Electric (GE) Service Information Letter (SIL) 459. GE SIL 459 recommends three actions to address this problem: vibration monitoring, shaft inspections after about 80,000 hours0 days <br />0 hours <br />0 weeks <br />0 months <br /> of operation and action to mitigate the thermal stress initiators. Hope Creeks RR pumps have over 130,000 hours0 days <br />0 hours <br />0 weeks <br />0 months <br /> of operation, and PSEG has not performed the recommended inspections.
In addition to the pump vibrations, there are vibrations on the associated RR and residual heat removal system piping which have resulted in damage to system sub-components (motor operated valve handwheel and limit switches). To date, none of the vibration-induced component problems have rendered any safety-related system inoperable.
Sargent and Lundy (S&L) performed an independent assessment for PSEG which concluded that return of Hope Creek to service for the next operating cycle was acceptable given the current level of RR pump and piping vibrations. S&Ls conclusion was based upon data which indicated that the vibration level for Hope Creeks B RR pump was consistent with RR pumps at other facilities and also based on an assumption that operators would be able to respond to an increasing vibration trend and take action to remove the pump from service prior to shaft failure.
The S&L assessment is summarized in the report, Independent Assessment of Hope Creek Reactor Recirculation System and Pump Vibration Issues, dated November 12, 2004. The NRC staff reviewed the S&L report and developed a number of questions which were provided to the licensee on December 1, 2004. PSEG responded to the questions during a December 17, 2004, public meeting with the Nuclear Regulatory Commission (NRC). PSEG provided additional responses to the NRC staffs questions in letters dated December 29, 2004, January 4, 2005, January 7, 2005, and January 9, 2005. In addition, numerous teleconferences were held between PSEG and the NRC in December 2004 and January 2005 to discuss the B RR pump vibration issue.
The S&L report concluded that there is no immediate need to replace the B pump rotor during the current refueling outage. S&L recommended that both pumps be monitored for vibrations and that a rapid rise in vibrations would be a sufficient reason to shut the pump down immediately for an internal inspection and shaft replacement, as the window between the rise in vibration and potential shaft failure is expected to be small.
PSEG also provided additional background information in Report H-1-BB-MEE-1878, Hope Creek B Recirculation Pump Vibration Analysis, Revision 1, dated December 16, 2004. The report concluded that, while the B RR pump has elevated vibrations when compared to the industry average, these vibration levels are not detrimental to the operation or reliability of the pump. The report also indicated that, although the risk of an RR pump shaft cracking event during any given cycle cannot be quantified, the operating experience of 29 RR pumps in operation longer than the Hope Creek B RR pump provides sufficient data to conclude that the risk of a shaft cracking event during the next cycle is minimal.
NRC Staff Review The NRC staffs review focused on the following key issues regarding the RR pump operation:
(1)
Does PSEG have a technical evaluation which shows that the RR pumps can be operated for another cycle without failure of the shafts considering the identification of shaft cracks that have been observed at other facilities with the same design RR pumps?
(2)
Can PSEG provide data which demonstrates that shaft cracks have been detected at other facilities with the same design RR pumps using vibration monitoring? Can the cracks be detected in time for the operators to take appropriate actions?
(3)
What are the consequences of an RR pump failure during plant operations?
GE SIL 459 indicates that all Byron Jackson RR pump shafts inspected have shown some degree of thermally-induced cracking. The cracking occurs near the pump thermal barrier where mixing of cold seal purge system water and the hot reactor coolant water occur. The cracks initiate as axial cracks in the pump shaft. The licensee indicated that, if the cracks remain axial, the cracks will grow slowly and not affect the operation of the pump. However, the licensee also indicated that given sufficient mechanical loads, the cracks can become circumferential. The circumferential cracks can propagate to shaft failure under mechanical loading. The time it takes to transition from slow growing axial cracks to more rapidly growing circumferential cracks depends on the magnitude of the mechanical loads acting on the pump shaft. Since the licensee does not know the magnitude of the mechanical loads, it is difficult to predict the shaft life based on the magnitude of the operational loads.
The licensee cited operating experience of other boiling water reactors (BWRs) with similar Byron Jackson RR pumps. The licensee indicates that the age of the Hope Creek RR pumps is about average for the pumps of similar design at other BWRs. The NRC staff notes that a number of the older pumps included in the licensees comparison are much smaller than the Hope Creek pumps. While the operating experience provides some confidence that the pumps can be safely operated beyond the time interval recommended in GE SIL 459, the crack growth analyses provided by the licensee indicates that the time is highly dependent on the magnitude of the mechanical loads, which is not well known.
The licensee also provided the level of vibration recorded at other BWRs with similar Byron Jackson RR pumps. The licensee concluded that measured vibration levels of the Hope Creek RR pumps are within the range of the vibration levels measured at other BWRs. However, the level of vibration of the B pump is toward the high end of the range of vibration levels measured at other BWRs. Therefore, the B pump is experiencing higher vibratory loadings than most of the pumps in the licensees survey. In addition, the licensee cited a history of problems in its attempt to balance and align the pump shaft. These problems caused additional mechanical loadings on the pump shaft which could increase the potential for circumferential cracks to have developed in the shaft. On the basis of the above discussion, the NRC staff concludes that the probability of a pump shaft failure of RR pump B during the next cycle of operation is indeterminate based on PSEGs evaluation of the potential thermal and mechanical loads on the pump shaft.
The licensee relies on vibration monitoring to detect circumferential cracking of the RR pump shaft with sufficient lead time for operators to secure the pump prior to complete shaft failure.
The licensee developed a plan for monitoring the vibration levels of the RR pumps. The key elements of the plan involve continuous basic monitoring of the overall level of vibration and continuous monitoring of the vibration harmonics for enhanced detection capability of potential shaft cracking.
The licensees continuous basic vibration level monitoring by the operations department consists of a pump vibration alarm and pump speed reduction if the B pump vibration level reaches 11 mils (0.011 inch), and removal from service if the pump vibration level reaches 16 mils (0.016 inch). The continuous monitoring of the vibration harmonics consists of pump vibration alarms and pump speed reduction if the synchronous speed (1X) vibration amplitude, two times synchronous speed (2X) vibration amplitude, 1X phase angle, or 2X phase angle exceed defined allowable limits. If the monitored values do not fall within their allowable limits at the reduced pump speed, the licensee will remove the RR pump from service. The allowable limits are established using the Operations and Maintenance Committee of the American Society of Mechanical Engineers standard, Reactor Coolant and Recirculation Pump Condition Monitoring. The licensee will record baseline data to establish these allowable limits during plant startup. The licensee provided two technical papers in support of the proposed vibration monitoring criteria.
The first technical paper is entitled, Case History Reactor Recirculation Pump Shaft Crack, Machinery Messages, December 1990. The paper discusses the RR pump shaft cracking experience at the Grand Gulf nuclear power plant. The paper indicates that the vibration level increased rapidly over a three-hour period before the pump was secured at slow speed.
Although the shaft did not experience a complete failure, subsequent inspection revealed the shaft was cracked approximately 320 degrees around the circumference. The paper indicates that it is necessary to monitor the 1X and 2X steady state vectors (1X and 2X amplitudes and phase angles) on a continuous basis and to compare these monitored values to an acceptance criteria. The paper also indicates that alarms are necessary to alert the user to amplitude and phase deviations that are outside the acceptance criteria.
The second paper is a technical bulletin from Bently, Nevada, Early Shaft Crack Detection on Rotating Machinery Using Vibration Monitoring and Diagnostics. The technical bulletin indicates that shaft cracking can be detected by monitoring the 1X and 2X vectors. The technical bulletin also recommends continuous monitoring of machines that are susceptible to shaft cracking.
These papers recommend using continuous monitoring of the 1X and 2X vectors as a predictive method to detect significant shaft cracking. The NRC staff requested that the licensee provide some evidence that vibration monitoring was effective for detecting shaft cracks in RR pumps similar to the Hope Creek RR pumps. The licensee cited the experience at Grand Gulf discussed above. The Grand Gulf RR pump shafts are hollow shafts as opposed to the solid shafts used in the Hope Creek RR pumps. Therefore, the Grand Gulf experience may not be directly applicable to Hope Creek. The licensee provided additional information which indicates that cracks in reactor coolant pump shafts were identified at Sequoyah (technical presentation to non-destrictive examination Steering Committee by G. Wade, July 12, 2002) and Palo Verde Unit 1 (Palo Verde Nuclear Generating Station Cracked Reactor Coolant Pump Shaft Event, H. Maxwell, 1996) using vibration monitoring. Although these plants are pressurized water reactors (PWRs), the reactor coolant pumps have solid shafts. The licensee indicated that these pumps had operated for a significant period of time after the first indication of shaft cracks by vibration monitoring. The NRC staffs review of related pump shaft vibration concerns also identified that vibration monitoring successfully identified a reactor coolant pump shaft cracking at St. Lucie Unit 2 (licensee event report (LER) Number: 1993-005). The PWR reactor coolant pump experience provides some indication that a solid pump shaft will provide better early crack detection capability than the hollow pump shafts, such as those used at Grand Gulf. PSEG has provided data which demonstrates that shaft cracks in pump shafts similar to those used at Hope Creek have been detected at other facilities, and that these cracks were detected in time for operators to take appropriate actions.
On the basis of the available operating experience, the NRC staff concludes that continuous monitoring of the 1X and 2X amplitudes and phase angles provides reasonable assurance that circumferential shaft cracking can be detected with sufficient time for the plant operators to take appropriate actions. The licensee will either reduce the RR pump speed or remove the pump from service if the monitoring system detects vibration levels that exceed the limits specified in the vibration monitoring plan.
The NRC staff also reviewed the licensees assessment of the potential consequences of an RR pump shaft failure. The RR pump shaft axial cracking that has been reported occurred below the seal area and above the pump hydrostatic bearing. This is the region where a potential RR pump shaft failure would be expected to occur. The pump impeller would be expected to settle at the bottom of the pump casing, which could potentially result in some damage to the pump casing. The unsupported end of the upper part of a broken shaft may damage the shaft seal. A seal failure would result in leakage of reactor coolant through clearances around the upper half of the broken pump shaft. This leakage would be bounded by the design basis small loss-of-coolant event. If such an event were to occur, the licensee would be able to isolate the pump using the RR loop isolation valves, thereby terminating any reactor coolant system leakage.
Conclusion The NRC staff concludes that the licensees continuous monitoring program for the Hope Creek RR pumps, as discussed above, provides reasonable assurance that a potential crack in the RR pump shaft can be detected in time for operators to take appropriate actions to reduce the pump speed or remove the RR pump from service prior to a complete shaft failure.
High Pressure Coolant Injection (HPCI) Exhaust Line Review
Background
On November 1, 2004, with Hope Creek Generating Station in Mode 5 for refueling outage 12, tandem snubbers from the HPCI turbine exhaust piping failed during dynamic testing. A followup inspection of the HPCI piping resulted in the observation of a damaged pipe support and a snubber anomaly that could have been the result of a water hammer event in the HPCI turbine exhaust line. A subsequent evaluation by PSEG Nuclear, LLC (the licensee) of the reported observations found that there was no conclusive evidence that a water hammer had occurred in the HPCI turbine exhaust line.
Nuclear Regulatory Commission (NRC) Staff Review The licensee provided an assessment of the tandem snubber failures performed by the snubber manufacturer, Lisega. The snubber failures occurred in the fluid reservoirs. Lisega indicated that the fluid reservoir failures were caused by stuck poppet valves that allowed fluid to leak into the reservoir during testing. Lisega concluded that repeated testing of the HPCI snubbers in compression resulted in over-pressurization of the reservoirs. Lisega also indicated that the snubbers would have functioned in response to a seismic event. The licensees assessments of the other observations, identified during the initial inspection of the HPCI exhaust line, provided reasonable dispositions of the observed conditions.
A licensee inspection of the accessible portions of the HPCI exhaust line in the turbine room and the torus room found no evidence of large pipe distortion or excessive pipe movement at support locations which likely would have been present if a water hammer had occurred. This was confirmed by the NRC inspectors. The licensee also performed non-destructive examination (NDE) of all field welds on the 20-inch HPCI exhaust line. All welds were found to be satisfactory. The inspections and weld examinations performed by the licensee are the type of actions the NRC staff would require after a water hammer event.
Conclusion The licensee provided plausible explanations for the snubber failures that occurred during snubber testing and for the identified support damage and snubber anomaly identified during the followup HPCI inspection. In addition, the licensee performed the type of inspections and NDE examinations that the NRC would require after a water hammer event and found no adverse results. Therefore, the NRC staff concluded that there was reasonable assurance that the integrity of the HPCI exhaust line had not been challenged by a water hammer event.