ML042120012

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IR 05000317-04-008, IR 05000318-04-008, on 02/16/2004 - 02/20/2004, 03/22/2004 - 03/23/2004, 05/10/2004 - 05/14/2004, Calvert Cliffs Nuclear Power Plant, Units 1 and 2; Special Inspection Team
ML042120012
Person / Time
Site: Calvert Cliffs  
(DPR-053, DPR-069)
Issue date: 07/29/2004
From: Lanning W
Division of Reactor Safety I
To: Vanderheyden G
Constellation Generation Group
References
EA-04-110 IR-04-008
Download: ML042120012 (57)


See also: IR 05000317/2004008

Text

July 29, 2004

EA-04-110

Mr. George Vanderheyden

Vice President - Calvert Cliffs Nuclear Power Plant

Constellation Generation Group, LLC

1650 Calvert Cliffs Parkway

Lusby, Maryland 20657-4702

SUBJECT:

NRC SPECIAL INSPECTION (SI) TEAM REPORT NO. 05000317/2004008 AND

05000318/2004008, AND PRELIMINARY WHITE FINDING - CALVERT CLIFFS

NUCLEAR GENERATING STATION

Dear Mr. Vanderheyden:

On May 14, 2004, the US Nuclear Regulatory Commission (NRC) completed a Special

Inspection at the Calvert Cliffs Nuclear Power Plant, Units 1 and 2. The enclosed report

documents the inspection findings which were discussed with you and other members of your

staff during an exit meeting on June 18, 2004.

This inspection examined activities conducted under your license as they relate to safety and

compliance with the Commissions rules and regulations and with the conditions of your license.

The team reviewed selected procedures and records, observed activities, and interviewed

personnel. In particular, the inspection reviewed event evaluations (including technical

analyses), root cause investigations, relevant performance history, and extent of condition to

assess the significance and potential consequences of issues related to both reactor trips on

January 23, 2004, (Unit 2) and March 20, 2004, (Unit 1).

The team concluded that the overall response of Constellation to the reactor trips on January

23, 2004, and March 20, 2004, were adequate, in that the plants were taken to a safe shutdown

condition. Nevertheless, the operators were challenged by equipment problems and

implementation of emergency operating procedures. Several of these issues were the result of

human performance issues. During the Unit 2 event, some operator actions, executing

emergency operating procedure 0, Post-trip Immediate Actions, were delayed due to past

operating practices.

This report documents one finding that appears to have low to moderate safety significance.

As described in Section 2.1 of this report, this finding involved a reactor regulating system

(RRS) relay that was not designed for the voltage conditions to which it was exposed and had

been in-place since the original construction of the facility. In addition, when Calvert Cliffs

implemented a modification to the turbine bypass valve and atmospheric dump valve control

system in 1992, they missed an opportunity to identify the inappropriate design. This condition

resulted in the relay failure in the RRS that prevented the system from properly regulating the

Mr. George Vanderheyden

2

reactor coolant temperature after the Unit 2 reactor trip on January 23, 2004. This resulted in a

safety injection actuation signal and steam generator isolation.

This finding was assessed using the reactor safety Significance Determination Process (SDP)

as a potentially safety significant finding that was preliminarily determined to be White for Unit 2

(i.e., a finding with some increased importance to safety, which may require additional NRC

inspection). The finding appears to have low to moderate safety significance because the

likelihood of core damage increased due to the loss of normal decay heat removal and loss of

low pressure feedwater supply. Based on analysis of the failed relay, the RRS condition would

have resulted in a similar uncontrolled cooldown, following a reactor trip any time during the

previous eight months.

We believe that we have sufficient information to make our final risk determination for the

performance issue regarding the RRS relay failure. However, before the NRC makes a final

decision on this matter, we are providing you an opportunity to either submit a written response

or to request a Regulatory Conference where you would be able to provide your perspectives

on the significance of the finding and the bases for your position. If you choose to request a

Regulatory Conference, we encourage you to submit your evaluation and any differences with

the NRC evaluation at least one week prior to the conference in an effort to make the

conference more efficient and effective. If a Regulatory Conference is held, it will be open for

public observation. The NRC will also issue a press release to announce the Regulatory

Conference.

Please contact Mr. Richard Conte at (610) 337-5183 within 10 business days of the date of this

letter to notify the NRC of your intentions. If we have not heard from you within 10 days, we will

continue with our significance determination and enforcement decision and you will be advised

by separate correspondence of the results of our deliberations on this matter.

Additionally, based on the results of this inspection, the team identified seven findings of very

low safety significance (Green). Five of these issues were determined to involve violations of

NRC requirements. However, because of their very low safety significance, and because they

have been entered into your corrective action program, the NRC is treating these issues as

non-cited violations, in accordance with Section VI.A.1 of the NRCs Enforcement Policy. If you

deny the non-cited violations noted in this report, you should provide a response with the basis

for your denial, within 30 days of the date of this inspection report, to the Nuclear Regulatory

Commission, ATTN: Document Control Desk, Washington, D.C. 20555-0001; with copies to the

Regional Administrator, Region I; the Director, Office of Enforcement, United States Nuclear

Regulatory Commission, Washington, D.C. 20555-0001; and the NRC Resident Inspector at

the Calvert Cliffs facility.

In accordance with 10 CFR 2.390 of the NRC's "Rules of Practice," a copy of this letter and its

enclosures will be available electronically for public inspection in the NRC Public Document

Room or from the Publicly Available Records (PARS) component of NRCs document system

(ADAMS). ADAMS is accessible from the NRC Web site at http://www.nrc.gov/reading-rm/

adams.html (the Public Electronic Reading Room).

Mr. George Vanderheyden

3

If you have any questions, please contact Mr. Conte at (610) 337-5183.

Sincerely,

/R.V. Crlenjak for:

Wayne D. Lanning, Director

Division of Reactor Safety

Docket Nos:

50-317, 50-318

License Nos: DPR-53, DPR-69

Enclosure:

Inspection Report 05000317/2004008 and 05000318/2004008

w/Attachments: Supplemental Information

Attachments:

A. Supplemental Information

B. Special Inspection Team Charter

C. Unit 2 Sequence of Events

cc w/encl:

M. J. Wallace, President, Constellation Generation

J. M. Heffley, Senior Vice President and Chief Nuclear Officer

President, Calvert County Board of Commissioners

J. M. Petro, Esquire, Constellation Energy Group, Inc.

J. E. Silberg, Esquire, Shaw, Pittman, Potts and Trowbridge

Director, Nuclear Regulatory Matters

R. McLean, Manager, Nuclear Programs

K. Burger, Esquire, Maryland Peoples Counsel

State of Maryland (2)

Mr. George Vanderheyden

4

Distribution w/encl:

H. Miller, RA/J. Wiggins, DRA (1)

OE Mail

F. Congel, OE

S. Figueroa, OE

C. Miller, RI EDO Coordinator

R. Laufer, NRR

R. Guzman, PM, NRR

R. Clark/P. Tam, PM, NRR (Backup)

J. Trapp, DRP

N. Perry, DRP

M. Giles, SRI - Calvert Cliffs

J. OHara, DRP - RI - Calvert Cliffs

K. Farrar, ORA

D. Holody, ORA

R. Urban, ORA

G. Matakas, ORA

Region I Docket Room (with concurrences)

W. Lanning, DRS

R. Crlenjak, DRS

R. Conte, DRS

A. Blamey, DRP

DOCUMENT NAME: C:\\ORPCheckout\\FileNET\\ML042120012.wpd

After declaring this document An Official Agency Record it will be released to the Public.

To receive a copy of this document, indicate in the box: "C" = Copy without attachment/enclosure "E" = Copy with attachment/enclosure "N" = No copy

OFFICE

RI/DRP

RI/DRS

RI/DRS

RI/DRP

RI/ORA

NAME

ABlamey

RConte

WSchmidt

JTrapp

DHolody

DATE

07/22/04

07/22/04

07/27/04

07/27/04

07/27/04

OFFICE

RI/DRS

NAME

WLanning(RVCfor)

DATE

08/02/04

OFFICIAL RECORD COPY

Enclosure

U.S. NUCLEAR REGULATORY COMMISSION

REGION I

Docket Nos:

50-317, 50-318

License Nos:

DPR-53, DPR-69

Report Nos:

05000317/2004008 and 05000318/2004008

Licensee:

Constellation Generation Group, LLC

Facility:

Calvert Cliffs Nuclear Power Plant, Unit 1 and Unit 2

Location:

1650 Calvert Cliffs Parkway

Lusby, MD 20657-4702

Dates:

February 16, 2004 - May 14, 2004

Inspectors:

A. Blamey, Team Leader

S. Barr, Senior Operations Engineer

G. Cobey, Senior Risk Analyst

M. Giles, Senior Resident Inspector

A. Passerelli, Reactor Engineer

J. Richmond, Resident Inspector

W. Schmidt, Senior Risk Analyst

H. Williams, Operations Engineer

Approved by:

Wayne D. Lanning, Director

Division of Reactor Safety

Enclosure

ii

TABLE OF CONTENTS

SUMMARY OF FINDINGS . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . iv

1.0

Description of Events . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . 1

1.1

Event Summaries . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . 1

Unit 2 January 23, 2004, Excessive Steam Demand Event . . . . . . . . . . . . . . . . 1

Unit 1 March 20, 2004, 11 Steam Generator Low Level Event . . . . . . . . . . . . . . 2

2.0

Equipment Failures and Root Causes . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . 4

2.1

Unit 2 Reactor Regulating System Quick Open Circuit

. . . . . . . . . . . . . . . . . . . 4

1.

Failure to Adequately Implement a Modification Design Review of the

Reactor Regulating System Quick Open Circuit . . . . . . . . . . . . . . . . . . . 4

2.

Administrative Procedure for Control of Maintenance Activities . . . . . . . 9

3.

Maintenance Rule Classification & Monitoring of Quick Open Function

. . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . 9

2.2

Unit 2 SIAS Actuation Signal Failure to Reset from Control Room . . . . . . . . . . 10

1.

Failure to Adequately Implement Modification Work Instructions for

Wiring Terminations . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . 10

2.

Previous Corrective Actions for Compression Style Terminations . . . . 12

3.

Control of Testing Scope and Acceptance Criteria . . . . . . . . . . . . . . . . 13

2.3

Test Records for Safety Related Work Not Retained by Document Control . . . 13

2.4

Unit 1 Digital Feedwater Design Deficiency . . . . . . . . . . . . . . . . . . . . . . . . . . . 15

3.0

Human Factors and Procedural Issues . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . 17

3.1

Failure to Properly Implement Station Emergency Operating Procedures . . . . 17

3.2

Failure to Have Procedures Required by Regulatory Guide 1.33 . . . . . . . . . . . 20

3.3

Simulator Fidelity Issues . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . 21

3.4

Failure to Comply with Station Work Control Procedures . . . . . . . . . . . . . . . . . 22

4.0

Emergency Preparedness . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . 24

4.1

Failure to Recognize and Report an Unusual Event During the January 23, 2004,

Unit 2 Reactor Trip . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . 24

5.0

Cross Cutting Aspects of Findings . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . 26

6.0

Generic Issues

. . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . 27

7.0

Risk Significance of the January and March 2004 Events . . . . . . . . . . . . . . . . . . . . . 27

8.0

Overall Adequacy of Licensee Response . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . 28

9.0

Exit Meeting Summary

. . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . 28

KEY POINTS OF CONTACT . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . A-1

LIST OF ITEMS OPENED, CLOSED AND DISCUSSED . . . . . . . . . . . . . . . . . . . . . . . . . . . A-1

LIST OF DOCUMENTS REVIEWED

. . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . A-3

LIST OF ACRONYMS . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . A-9

SPECIAL INSPECTION TEAM CHARTER . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . B-1

Enclosure

iii

REVISED SPECIAL INSPECTION TEAM CHARTER . . . . . . . . . . . . . . . . . . . . . . . . . . . . . B2-1

UNIT 2 SEQUENCE OF EVENTS

. . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . C-1

Enclosure

iv

SUMMARY OF FINDINGS

IR 05000317/2004-008, 05000318/2004-008; 02/16/04-02/20/04, 03/22/04-03/23/04, 05/10/04-

05/14/04; Calvert Cliffs Nuclear Power Plant, Units 1 and 2; Special Inspection Team.

The inspection was conducted by four regional inspectors, two resident inspectors, and two

regional senior reactor analysts. One finding, assessed as Preliminary White on Unit 2, and

seven other Green findings were identified. The significance of most findings is indicated by

their color (Green, White, Yellow, Red) using IMC 0609, Significance Determination Process

(SDP). Findings for which the SDP does not apply may be Green or be assigned a severity

level after NRC management review. The NRCs program for overseeing the safe operation of

commercial nuclear power reactors is described in NUREG-1649, Reactor Oversight Process,

Revision 3, dated July 2000.

A.

NRC Identified and Self-Revealing Findings

Cornerstone: Mitigating Systems



Preliminary White. A self-revealing event identified a finding of low to moderate safety

significance, because Calvert Cliffs Nuclear Power Plant (CCNPP) did not perform a

modification design review, as required by station procedures. Following a Unit 2

reactor trip on January 23, 2004, the atmospheric dump valves and turbine bypass

valves automatically Quick Opened, as designed. However, the Quick Open signal did

not clear when the reactor coolant temperature dropped below the Quick Open setpoint,

because of a reactor regulating system relay failure. As a result, an uncontrolled

cooldown of the reactor coolant system occurred, which in turn caused a loss of the

normal heat removal system.

This finding was more than minor because it was considered to be a precursor to a

more significant event. A Significance Determination Process Phase-3 risk analysis

determined that this finding was of low to moderate safety significance, based on the

change in core damage frequency. (Section 2.1.b.1)



Green. A self-revealing event identified a non-cited violation of very low safety

significance of Technical Specification 5.4.1, because CCNPP did not adequately

implement modification work instructions. As a result, during a plant event, recovery

actions were delayed because operators were unable to reset the "B" channel of the

safety injection actuation signal (SIAS) system from the control room.

This finding was more than minor because the SIAS system was returned to service,

following modification work, and subsequently became unable to perform its function,

similar to example 5.b in NRC Inspection Manual 0612 Appendix E. This finding had

very low safety significance because the finding did not represent an actual loss of a

safety function.

A contributing cause of this finding was related to the Human Performance cross-cutting

area because maintenance technicians did not adequately implement written work

instructions. (Section 2.2.b.1)

Enclosure

v



Green. The inspectors identified a non-cited violation of very low safety significance of

10 CFR 50 Appendix B, Criterion XVII, "Quality Assurance Records," because CCNPP

did not retain records of test results. From 1999 to March 2004, CCNPP did not retain

wiring verification point-to-point test records for modifications of safety-related circuits.

As a result, after the records are transferred to Records Management, verification of the

work performed cannot be done.

This finding was more than minor because the failure to retain the required records was

not an isolated example, and the records were irretrievably lost, similar to example 1.b in

NRC Inspection Manual 0612 Appendix E. This finding was not suitable for a

Significance Determination Process evaluation, but was reviewed by NRC management

and determined to be of very low safety significance.

A contributing cause of this finding was related to the Human Performance cross-cutting

area because station personnel did not adequately implement written instructions in a

safety-related procedure. (Section 2.3)



Green. A self-revealing finding of very low safety significance was identified because

CCNPP failed to perform an adequate design review which resulted in reduced reliability

of the digital feedwater system during a plant event on March 20, 2004.

This finding was more than minor because it effected the design control attributes of the

Initiating Events cornerstone. Incorrectly specifying the design voltage resulted in

reduced reliability of the digital feedwater control system which increased the likelihood

of an event that upset plant stability during power operation. This finding was of very

low safety significance, because one of two turbine driven feedwater pumps and one of

three condensate and condensate booster pumps remained operable during the Unit 1

March 20, 2004, event. (Section 2.4)

Green. The inspectors identified a non-cited violation of CCNPP Technical Specification

5.4.1.b because the operating crew did not properly implement station emergency

operating procedures during the Unit 2 reactor trip reactor shutdown on January 23,

2004.

The finding was more than minor because it affected the Initiating Events Cornerstone

in that the failures to follow station procedures complicated the plants post-trip response

and the ability of the operators to restore normal plant conditions. This finding had very

low safety significance because the finding did not represent an actual loss of a safety

function, and was not potentially risk significant due to an external initiating event.

A contributing cause of the finding was related to the Human Performance cross-cutting

area because licensed operators did not properly implement station emergency

operating procedures. (Section 3.1)

Green. The inspectors identified a non-cited violation of CCNPP Technical Specification

5.4.1.a because CCNPP did not have a procedure (off-normal) for the failure of the

reactor regulating system (RRS) as required by Regulatory Guide 1.33.

Enclosure

vi

This finding was more than minor because if the operators had switched to the alternate

channel of RRS, after the failure of the RRS relay in the X channel, the atmospheric

dump valves (ADVs) and turbine bypass valves (TBVs) would have properly controlled

reactor temperature and terminated the uncontrolled cooldown. This finding had very

low safety significance because the finding did not represent an actual loss of a safety

function, and was not potentially risk significant due to an external initiating event.

(Section 3.2)

Green. A self-revealing event identified a finding in that CCNPP did not follow

procedural requirements in their risk assessment and control of the work on March 20,

2004, which resulted in an unanticipated reactor trip. Specifically, the provisions and

controls of procedures NO-1-100, Conduct of Operations, NO-1-117, Integrated Risk

Management, and MN-1-100, Conduct of Maintenance, were not followed.

This finding was more than minor because the failures to follow station procedures

affected the Initiating Events cornerstone in that the failure to properly risk-classify and

control the work in the control room on March 20 lead to the reactor trip. This finding

had very low safety significance because the finding did not represent an actual loss of

a safety function, and was not potentially risk significant due to an external initiating

event.

A contributing cause of the finding was related to the Human Performance cross-cutting

area because CCNPP managers and staff did not properly implement station

operations, risk management, and maintenance procedures. (Section 3.4)



Green. The inspectors identified a non-cited violation of 10CFR50.54(q) because the

operating crew did not properly recognize plant conditions commensurate with an

Unusual Event in accordance with the emergency plan and implementing procedures

during the Unit 2 reactor trip on January 23, 2004.

This finding was more than minor because it effected the response organization

performance attribute of the Emergency Preparedness Cornerstone in that failure to

properly recognize plant conditions commensurate with an Unusual Event classification.

This finding was of very low safety significance, because it involved an implementation

problem during an actual event and the CCNPP staff failed to identify the Unusual Event

in the post trip review.

This finding is related to the Human Performance cross-cutting area because the

operating crew did not properly recognize plant conditions commensurate with an

Unusual Event in accordance with the emergency plan during a Unit 2 excessive steam

demand event on January 23, 2004. (Section 4.1)

Enclosure

Report Details

1.0

Description of Events

1.1

Event Summaries

January 23, 2004, Excessive Steam Demand Event (Unit 2)

On January 23, 2004, Calvert Cliffs Unit 2 was operating at 100% power. At 3:26 p.m.,

the 22 steam generator feed pump (SGFP) unexpectedly tripped off. Operators

attempted to reset and restart the 22 SGFP three times but were unable to reset the

pump trip. Without this pump operators were unable to maintain water level in the

steam generators, and they monitored water level approaching the trip criteria. Just

prior to the operators initiating a manual reactor trip, the automatic trip set point was

reached, and the unit experienced a reactor trip at 3:27 p.m. The operators entered

emergency operating procedure (EOP) - 0, Post-Trip Immediate Actions. When the

reactor tripped, the reactor regulating system controlled the removal of stored energy in

the reactor coolant system (RCS) and the secondary system with the quick-open signal

which opened the turbine bypass valves (TBVs) and atmospheric dump valves (ADVs).

The quick open signal is designed to have the TBVs and ADVs initially fully open, then

modulate, to automatically control RCS temperature at 532 degrees Fahrenheit. In this

event however, the TBVs and ADVs remained full open, causing a rapid overcooling and

depressurization of the RCS.

Due to lowering steam generator water levels, an Auxiliary Feedwater Actuation Signal

(AFAS) occurred at 3:28 p.m., and the 21 and 23 Auxiliary Feedwater (AFW) pumps

started and provided water to the steam generators as designed. At 3:28 p.m. RCS

pressure decreased to 1740 psia, causing a Safety Injection Actuation Signal (SIAS).

Equipment which started as a result of the SIAS included the 2A and 2B emergency

diesel generators (EDGs), the high pressure safety injection pumps, the containment

spray pumps and the low pressure safety injection pumps. RCS pressure remained

high enough that the charging pumps were the only source of injection into the RCS.

The SIAS signal also stopped RCS letdown and de-energized the back-up pressurizer

heaters. The operators stopped two reactor coolant pumps (RCPs) per the procedure

requirements following receipt of a SIAS signal.

At 3:28 p.m., a Steam Generator Isolation Signal (SGIS) was received when steam

generator pressure decreased below the setpoint, causing the main steam isolation

valves (MSIVs) to shut. This isolated steam flow through the TBVs. At approximately

nine minutes after the reactor trip, the operators transferred control of the ADVs to the

Auxiliary Shutdown Panel to remove the "quick open" signal which was still present to

the ADVs. Once ADV control was transferred to the Auxiliary Shutdown Panel, the

ADVs closed and the cause of the overcooling and depressurization event was

terminated. RCS pressure was 1523 psia and the RCS temperature was 486 degrees

Fahrenheit. Pressurizer level was below the bottom of the indicating range.

2

Enclosure

Due to post-trip reactor decay heat, the plant parameters began to restore to normal

post-trip values. At 3:39 p.m., pressurizer level instrumentation began to indicate a level

increase as expected.

At 3:55 p.m. the operators transitioned to EOP-1, Reactor Trip. With a SIAS signal still

present, all charging pumps were running and RCS letdown was isolated. The

operators took manual control of pressurizer main spray to control rising RCS pressure.

RCS pressure was stabilized at 2318 psia at approximately 3:56 p.m. At 4:01 p.m., the

operators removed 22 and 23 charging pumps from service because pressurizer level

was still increasing (264-inches). At 4:06 p.m., 21 charging pump was stopped. All

injection had been stopped at this point. At 4:08 p.m., the operators stopped the RCS

heat-up at 515 degrees Fahrenheit by modulating the ADVs, and RCS pressure began

to decrease uncontrollably.

The operators attempted to reset the SIAS signal to allow restoration of plant systems.

Of specific interest to the crew were the back-up pressurizer heaters needed to raise

RCS pressure to normal value and the RCS letdown control valves needed to lower

pressurizer level to the normal operating band. At 4:17 p.m., SIAS channel "A" was

reset from the control room. SIAS channel "B" would not reset from the control room.

The operators were able to reset the SIAS "B" signal at the Engineered Safety Features

Actuation System (ESFAS) cabinet located in the cable spreading room at 4:27 p.m.

At 4:45 p.m., RCS pressure was at 1782 psia, and the operators began heating the RCS

to return parameters to within the normal post-trip temperature band of 525-535 degrees

Fahrenheit. Back-up pressurizer heaters, RCS letdown, and 21 charging pump were

returned to service. Due to the large volume of subcooled water that had been added to

the pressurizer, RCS pressure continued to slowly decrease despite having all

pressurizer heaters in service. At 5:18 p.m., a second SIAS actuation was received at

approximately 1750 psia. At this point, RCS pressure stabilized at approximately 1745

psia for the next 30 minutes. To restore pressurizer heater capacity the operators

blocked and reset SIAS, and pressurizer pressure began to recover to its expected

value.

March 20, 2004, No. 11 Steam Generator Low Level Event (Unit 1)

During the Unit 2 refueling outage in April 2003, CCNPP identified a design deficiency

related to varistors installed in the feedwater regulating valve and feedwater regulating

bypass valve digital feedwater indicators. The same deficiency existed on Unit 1, in that

if a ground occurred on the 1Y09 or 1Y10 bus the potential existed to lose all AC power

to the Unit 1 digital feedwater control system. CCNPP planned for the removal of these

varistors and considered different compensatory measures to be used until that

replacement. Operations management did not want to use an interim fix based on the

risk involved in their implementation and decided the varistor vulnerability could be

controlled by limiting the work done on the 1Y09 and 1Y10 buses. Calvert Cliffs records

indicated that the initial work control strategy was effective in that work was prevented

on the buses through approximately August 2003; however, soon thereafter work on the

3

Enclosure

1Y09 and 1Y10 buses again became routine with no additional controls placed on the

work.

On March 20, 2004, maintenance technicians performed work on 1-ER-101, a 500KV

chart recorder in the control room. As part of that work, at 1:19 p.m., maintenance

technicians were installing the recorder into panel 1C29. As the recorder was being

installed, a power lead to the recorder became pinched between the recorder and its

case, and shorted to ground. This resulted in a large bang in the control room, as well

as a ground on 1Y09.

The technicians notified the control room operators of this issue, and the operators

reviewed their indications and controls for the operating units, and noted no immediate

concerns. The only noted abnormality at that time was that the 12 steam generator

digital feedwater back-up central processing unit had re-booted. Later review of saved

data also showed that the feedwater regulating valve controller had also re-booted.

Unknown to the operators, due to the ground on bus 1Y09 phase C, a potential of 208

volts existed from line to ground on phases A and B of 1Y09 and their associated

components. Due to the known design issue with the Dixson digital feedwater

indicators, this potential caused the Dixsons to attempt to reduce the voltage back to

120VAC through the varistors. The varistors tried to limit the voltage for approximately

19 minutes. At 1:39 p.m., due to the ground that still existed on 1Y09, the varistors

failed, causing a line to neutral fault. This caused the fuses in the digital feedwater

controls to open for the 1Y09 power feed. During this time period, the operators noticed

the flashing of digital feedwater components. The digital feedwater electrical power

feeds are designed to be protected by the use of an automatic bus transfer (ABT) switch

which shifts the input power source from 1Y09 (primary) to 1Y10 (backup) if a fault

appears on 1Y09. The ABT shifted from 1Y09 supply to the 1Y10 supply, but due to the

short existing down stream via the varistors, the fuses for the 1Y10 feed to the digital

feedwater controls also opened.

This resulted in the loss of the 11 digital feedwater ABT bus, which in turn resulted in

the deenergization of the 11 main and 12 backup CPUs for digital feedwater. The 11

FRV positioner selector solenoid, 1-SV-1111B failed to electrically shift to the A position,

because of mechanical binding in the solenoid valve. This resulted in a loss of signal to

the 11 FRV, which immediately began closing. Steam generator water levels dropped

quickly, resulting in a reactor trip at 1:40 p.m. Approximately eight seconds prior to the

trip, the operators had shifted 12 FRV to manual. Additionally during the last 15

seconds of the event, 11 SGFP tripped on high discharge pressure as a result of the 11

FRV closure.

Immediately after the trip the TBVs opened as a result of the quick open signal. They

shut when the quick open signal was clear but did not reopen to modulate TBV flow and

control RCS temperature. The operators placed the TBV controller in manual, but the

valves still remained closed. Since the TBVs were not operating, the ADV controller

was placed in manual and modulated to control the cool down. During the same time,

12 steam generator feed pump was still reacting to the loss of 11 steam generator feed

4

Enclosure

pump, increasing in speed and discharge flow. At approximately 20 seconds post trip,

12 FRV shut due to high 12 steam generator water levels, and 12 steam generator feed

pump tripped on high discharge pressure. When steam generator water levels

decreased to the AFAS setpoint, the system actuated and re-initiated feed to the steam

generators.

2.0

Equipment Failures and Root Causes

2.1

Unit 2 Reactor Regulating System Quick Open Circuit

a.

Inspection Scope

Following a Unit 2 reactor trip on January 23, 2004, the reactor regulating system (RRS)

Quick Open signal did not clear when the reactor coolant temperature dropped below

the setpoint. As a result, an uncontrolled cooldown of the reactor coolant system

occurred.

The inspectors reviewed the design of the RRS, ADVs, and TBVs, and interviewed plant

personnel to independently determine what occurred and evaluate the initiating causal

factors. The inspectors also reviewed the material history and maintenance activities

associated with the RRS system. The inspectors assessed CCNPPs root cause

analysis and corrective actions to evaluate the adequacy of CCNPPs conclusions and

actions.

b.

Findings

One self-revealing preliminary white finding and two inspector observations are

documented in this section. The observations were minor issues that were related to

the human performance cross-cutting area.

1.

Failure to Adequately Implement a Modification Design Review of the Reactor

Regulating System Quick Open Circuit

Introduction. A self-revealing event identified a Preliminary White finding because

CCNPP did not perform a modification design review, as required by station procedures.

A preliminary risk analysis determined the finding to be of low to moderate safety

significance, because the likelihood of core damage had increased due to an RRS relay

failure. Following a reactor trip on January 23, 2004, the ADVs and TBVs automatically

Quick Opened, as designed. However, the Quick Open signal did not clear when the

reactor coolant temperature dropped below the Quick Open setpoint, because of the

RRS relay failure. As a result, an uncontrolled cooldown of the reactor coolant system

occurred, which in turn caused a loss of the normal heat removal system.

Description. Following a reactor trip, the ADVs and TBVs automatically Quick Opened,

as designed. However, the Quick Open signal did not clear when the reactor coolant

temperature dropped below the setpoint of 557 degrees T-Avg. As a result, an

uncontrolled cooldown of the reactor coolant system occurred, which in turn initiated

5

Enclosure

SGIS and SIAS actuations. The SGIS actuation resulted in a main steam isolation valve

closure, which disabled the main feedwater pumps (high pressure feedwater supply)

and the TBVs, and caused a loss of the normal heat removal system.

CCNPP subsequently determined that the Quick Open signal failed to reset because an

RRS X-channel K-7 relay contact failed to open when the relay was de-energized. The

K-7 relay had last functioned properly, following a reactor trip, on May 28, 2003.

CCNPP determined that the degraded relay contacts would probably have failed to open

next time that the relay de-energized, following the May reactor trip. The inspectors

concluded that the degraded RRS relay left the plant susceptible to an over-cooling

event from May 28, 2003 to January 23, 2004.

The failed relay, along with two similar relays, were sent to an independent laboratory

for failure modes and effects analysis. The laboratory analysis report identified that the

failed relay contacts had extensive burning and pitting, consistent with electrical welding

of the contacts. In addition, the report stated that arcing had occurred, as evidenced by

burn marks inside the relay case, and that flash-over had deposited soot on one

adjacent contact. The laboratory concluded that the failure was due to "burning and/or

welding" of the contacts, but could not determine whether (1) inductive-kick, (2)

excessive load, or (3) a one-time event initiated the contact burning that lead to the

contact failure.

The CCNPP Root Cause Analysis Report (RCAR), "Failure of Atmospheric Dump Valve

Quick Open Override Relay (K-7)," concluded that the root cause was a poor design

practice during original plant construction and a subsequent 1992 modification (FCR 85-

0068). The RCAR conclusion was based on the following facts and reasoning:



The relay contacts were not rated for the actual circuit voltage; rated for 29 VDC,

but installed in a 125 VDC circuit, and therefore failed prematurely.



The relay (Allied Controls model MHJLO-12A) was a system interface device

between the RRS system (Combustion Engineering design scope) and the ADV

and TBV valve actuator 125 VDC circuit (Bechtel design scope).



Laboratory failure analysis attributed the failure to an over-current event.



The contacts had not reasonably reached end-of-life, and the steady state load

current was low, compared to the contact current rating (no excessive load).



Other than the failed (welded closed) contact pair, the relay was in good

mechanical and electrical condition.



In 1992, the ADV and TBV valve actuator circuits were modified (FCR 85-0068).

A second load was added into the circuit controlled by the K-7 relay contacts.

The contact ratings for the K-7 relay were not checked to verify that they were

adequate for the additional load.

The RRS modification FCR 85-0068 specified specific design reviews and analysis

requirements. The inspectors determined the specified requirements were not

adequately performed, in that a required electrical analysis for the added loading on the

existing ADV and TBV control circuit did not verify the K-7 contact ratings.

6

Enclosure

CCNPPs interim corrective actions replaced all K-7 relays in both Unit 1 and Unit 2, and

performed targeted reviews, based on function and risk, of similar system interfaces to

identify other underrated relay contacts. The interim action to install new K-7 relays

reduced the likelihood of a premature contact failure, until a plant modification could be

performed to eliminate the design deficiency. No other underrated relay contacts were

identified. CCNPPs longer term corrective actions included a modification to the K-7

circuit to restore proper contact ratings for the circuit.

The inspectors review of CCNPPs RCAR analysis identified several weaknesses:



The RCAR did not consider the third failure possibility that was identified in the

laboratory analysis report, as a "one-time event" which could have initiated the

contact burning that lead to the contact failure. Such a failure mode could have

resulted from a maintenance error during testing activities.



The RCAR did not discuss the testing and examination results of the other three

K-7 relays, which had operated under similar conditions and length of service

time (both Unit-1 K-7 relays and the second Unit-2 K-7 relay). Those relays were

bench tested for contact resistence; two relays appeared to have adequately low

contact resistence. The relays were also opened for an internal contact visual

examination. The inspectors examined those relay contacts and noted evidence

of excessive contact pitting on two relays.



The RCAR did not discuss apparent contradictions in contact rating information

provided by an Allied Controls relay applications engineer (original equipment

manufacturer), and an independent root cause review conducted by an outside

organization.

Overall, the inspectors concluded that while the CCNPP root cause determination was

not thorough, the proposed corrective actions appeared reasonable.

Old Design Issue Considerations

In the original plant design (1977), the Combustion Engineering RRS design provided

the K-7 relays as interface devices for a control signal output to the Bechtel designed

ADV and TBV valve control system. The inspectors concluded that the K-7 relay

contacts were underrated for their application since initial plant construction and startup.

NRC MC 0305, "Operating Reactor Assessment Program," Section 04.07 defines an

"Old Design Issue" as a finding that involved a past design-related problem in an

engineering analysis or installation of plant equipment (e.g., a modification), that does

not reflect a performance deficiency associated with an existing program or procedure.

MC 0305 section 06.06(a) provides guidance for the treatment of Old Design Issues,

and states that the NRC may refrain from considering safety significant findings if the

Old Design Issue satisfies the following criteria:

7

Enclosure



Licensee Identified.



Not likely to have been previously identified by on-going licensee efforts.

Self-revealing issues are not considered to be licensee identified. In addition, CCNPP

had a prior opportunity to identify this issue, during a 1992 modification to the ADV and

TBV control system. Therefore, because this design-related finding did not satisfy the

above criteria, it is not considered to be an Old Design Issue and is being treated similar

to any other inspection finding, in accordance with MC 0305-06.06(a). This guidance is

consistent with Section VII.B.3 of the NRC Enforcement Policy.

Analysis. This finding was a performance deficiency because CCNPP did not perform

an adequate design review, as required by station procedures, during a 1992

modification to the Quick Open circuit. Traditional enforcement does not apply because

the issue did not have any actual safety consequences or potential for impacting the

NRCs regulatory function and was not the result of any willful violation of NRC

requirements or CCNPP procedures. This finding affected the Mitigating Systems

cornerstone objective because it negatively impacted systems that are used to respond

to initiating events to prevent core damage. This finding was more than minor because

it was considered to be a precursor to a more significant event. If auxiliary feedwater

(AFW) had not maintained steam generator level, once-through cooling would have

been necessary to remove reactor decay heat. If once-through cooling and alternate

feed had both failed, the sequence could have proceeded to core damage.

The finding was evaluated in accordance with IMC 0609, Appendix A, "Significance

Determination of Reactor Inspection Findings for At-Power Situations," using Phase 1,

Phase 2, and Phase 3 significance determination process (SDP) analyze. The Phase 1

screening determined that a Phase 2 evaluation was required, because the finding

represented an actual loss of a risk significant function of a non-Technical Specification

equipment train that was classified as Maintenance Rule high safety significant, for

greater than 24 hours2.777778e-4 days <br />0.00667 hours <br />3.968254e-5 weeks <br />9.132e-6 months <br />.

A fault exposure time of 240 days was used for non-ATWS initiating events. On May

28, 2003, a reactor trip occurred, and the RRS quick open circuit and ADVs/TBVs

functioned properly. Based on licensee review, the K-7 relay contacts would have failed

to open on the next relay actuation, following the May reactor trip. There were no other

demands or tests which would have demonstrated whether the quick open function was

operational from May 28, until the reactor trip on January 23, 2004, when the RRS relay

failure was identified by a self revealing event.

A fault exposure time of 28 days was used for ATWS initiating events. During the early

part of an operating cycle, the RCS negative temperature coefficient is not be large

enough (provide sufficient negative reactivity) to allow emergency boration (EB) to

shutdown the unit given an ATWS. Based on licensee information this condition would

last for 7 weeks if ADVs/TBVs operate properly and 11 weeks if ADVs/TBVs failed open.

From a Phase 2 perspective this would equate to a 4 week exposure time where EB

would not have functioned following startup from the May 28, 2003 trip.

8

Enclosure

The internal events Phase 2 analysis, for CDF and LERF, was conducted in

accordance with IMC 0609 Appendix A, using the Risk-informed Inspection Notebook

for Calvert Cliffs Nuclear Power Plant Units 1 and 2, revision 1, dated July 2, 2002 and

with Draft IMC 0609, Appendix H, Containment Integrity SDP, respectively. From a

Phase 2 perspective, the finding had low - moderate CDF safety significance and very

low LERF safety significance.

The Region I senior reactor analyst (SRA) conducted a Phase 3 Risk Assessment, to

refine the Phase 2 analysis and to incorporate external events for both CDF and

LERF. The analysis used an update Calvert Cliffs SPAR model, Rev 3i, dated

November 2001. The assumptions used were that a plant transient would result in an

over-cooling event which would have caused SGIS and SIAS actuations. A SGIS

actuation would close the MSIVs resulting in the loss of the main feedwater pumps as a

high pressure feedwater supply and the inability to remove decay heat with the TBVs.

The SIAS actuation would isolate the turbine building service water cooling system,

resulting in the loss of the CBPs as a low pressure feedwater supply and in a loss of

redundancy in instrument air supplies and in TDAFW room cooling.

The Phase 3 analysis determined that the finding represented low to moderate (WHITE)

CDF safety significance for internal and external initiating events. The internal events

analysis resulted in a CDF of approximately 2E-6 for the 240 day exposure period.

The dominant core damage sequence was a transients with successful reactor trip

followed by a loss of steam generator cooling and failure to initiate once through cooling

(Feed and Bleed). An ATWS was the second dominant sequence, given the increased

time that emergency boration would not be sufficient to shutdown the reactor with the

TBVs/ADVs failing open. The finding represented a very low LERF safety significance

because there were no SGTR sequences identified as part of the SPAR analysis. The

SRA reviewed the licensees risk assessment relative to external events, finding that

both fire and seismically induced transients contributed to the total CDF increase, but

not to a sufficient extent to increase the total risk above low - moderate risk significance.

Using similar assumptions to those used in the Phase 3 analysis CCNPP, using an

integrated internal and external initiating events PRA model, estimated the CDF safety

significance at approximately 7E-6 for the 240 days.

Enforcement. There were no violations of NRC regulatory requirements because the

reactor regulating system, atmospheric dump valves, and turbine bypass valves were

not safety-related. CCNPP entered this finding into their corrective action program as

IR4-025-059. (FIN 50-318/2004008-01, Failure to Adequately Implement

Modification Design Review of the Reactor Regulating System Quick Open

Circuit.)

2.

Administrative Procedure for Control of Maintenance Activities

The inspectors identified that CCNPP did not implement written procedures for the

control and revision of in-process maintenance work instructions. During the Unit 2

2003 refuel outage, MO 2-2002-01126 performed PM Checklist IPM56001, "Functional

9

Enclosure

Test of ADV and TBV Quick Open." That functional test was new, and had not

previously been performed. Extensive pen-and-ink changes were made to the written

work instructions, without utilizing the formal PM revision process, as required by MN-

10-102 section 5.1, "PM Change Process." MN-10-102 section 5.2.B(d) limited pen-

and-ink changes to "Administrative or Editorial" changes. The inspectors determined

that the changes made were technical in nature, in that they changed the method of

performing the test. The inspectors did not identify any additional similar examples, and

concluded that this appeared to be an isolated example of this behavior.

Technical Specification 5.4.1 required, in part, that written procedures shall be

established and implemented as recommended in NRC Regulatory Guide (RG) 1.33

Appendix A. RG 1.33 Appendix A, section 1.d, "Administrative Procedures," required

written procedures for procedure adherence and temporary changes. The inspectors

determined that this was a minor violation of regulatory requirements, because the

failure to adequately review and approve the Checklist procedure change did not, in this

instance, impact the final test results. CCNPP entered this issue into their corrective

action program as IR4-036-977.

3.

Maintenance Rule Classification & Monitoring of Quick Open Function

The Maintenance Rule (MR) basis document stated that the RRS control system (quick

open signal & modulating control signal to ADVs & TBVs) was classified as MR high

safety significant. The TBV and ADV valve control functions were scoped as part of the

main steam system. The TBVs were classified as a MR non-risk function. The ADVs

were classified as a MR high safety significant function. All functions were monitored for

reliability (functional failures) at the system level. Only the ADV function was monitored

for availability. The ADV and TBV functions were identified as "operate on demand"

(i.e., a standby function).

CCNPPs Loss of Normal Heat Removal analysis indicated that component failures

which resulted in a loss of the normal heat removal system were risk significant. The

inspectors noted that there was an apparent discrepancy between the MR classification

and the risk significance, as determined by the stations probability risk assessments.

NRC Regulatory Guide 1.160, "Monitoring the Effectiveness of Maintenance," endorses

NUMARC 93-01, and provided guidance for MR implementation. Both documents

stated that high safety significant functions and standby low safety significant functions

should have performance criteria established to assure reliability and availability are

maintained. The inspectors concluded that the Quick Open function (RRS, ADVs, and

TBVs) should reasonably have been monitored for both functional failures and

availability, at the train level. The inspectors reviewed the systems material history and

concluded that, prior to the January 2004 reactor trip, the Quick Open function would not

reasonably have required goal setting and monitoring under the MR (a)(1) requirements.

The inspectors concluded that, in this instance, not monitoring the Quick Open function

for availability was a minor issue. CCNPP entered this issue into their corrective action

program as IR4-035-902.

10

Enclosure

2.2

Unit 2 SIAS Actuation Signal Failure to Reset from Control Room

a.

Inspection Scope

Following a reactor trip on January 23, 2004, during the plant recovery phase of the

event, the control room operators were unable to reset the "B" channel of SIAS.

The inspectors reviewed the SIAS system design, testing, and surveillance program

elements, and interviewed plant personnel to independently determine what occurred

and evaluate the initiating causal factors. The inspectors assessed CCNPPs cause

determination and corrective actions to evaluate the adequacy of CCNPPs conclusions

and actions.

The inspectors reviewed selected maintenance and modification activities associated

with the SIAS system. The inspectors assessed post-maintenance and modification test

adequacy by comparing the test methodology to the scope of work performed. In

addition, the inspectors evaluated the test acceptance criteria to verify whether the test

demonstrated that the tested components satisfied the applicable design requirements.

The inspectors reviewed the recorded test data to determine whether the acceptance

criteria were satisfied.

b.

Findings

One self-revealing green finding and two inspector observations are documented in this

section. The observations were minor issues that were related to the human

performance cross-cutting area.

1.

Failure to Adequately Implement Modification Work Instructions for Wiring Terminations

Introduction. A self-revealing finding of very low safety significance (Green) identified

that maintenance procedures had not been adequately implemented to terminate a

wiring connection during a modification in the SIAS "B" channel reset circuit, in April

2003. As a result, during a plant event, recovery actions were delayed because

operators were unable to reset the "B" channel SIAS actuation from the control room.

This finding was related to the Human Performance cross-cutting area.

Description. In March 2003, CCNPP performed a modification on the SIAS reset

circuitry. Post-modification testing (PMT) consisted of point-to-point wiring checks to

verify that the newly installed or modified circuits conformed to design requirements. No

operational or functional test of the SIAS reset function was performed. CCNPP

determined that the reset function was not specifically credited in any design basis event

and not identified as a safety function in the FSAR or Technical Specification Basis.

Therefore, CCNPP concluded that logic system functional testing was not required to be

performed on the SIAS reset circuits.

Following a reactor trip in January 2004, a SIAS actuation occurred, per plant design.

Approximately 49 minutes into the event, operators attempted to reset the SIAS

11

Enclosure

actuation signal, to allow recovery of pressurizer level and pressure control. However,

"B" channel of SIAS could not be reset from the control room. At approximately 60

minutes into the event, an operator reset the "B" channel SIAS modules individually in

the cable spreading room.

During post-event troubleshooting, a visual inspection in control room panel 2C10

identified a wire hanging free in the air. The loose wire was determined to have come

off of hand-switch 2HS-6901 terminal 7, which was part of the daisy chain circuit for the

SIAS "B" channel reset. CCNPP determined that the wire probably pulled off the hand-

switch terminal during one of two maintenance activities, performed in the same panel in

close proximity to the affected hand-switch (MOs 2200302348 and 2200302349, to

replace containment air cooler fan control hand-switches), in August or October 2003.

The inspectors reviewed the modification installation work order 2-2000-00544,

"Remove SIAS Contacts from Containment Purge Isolation and Hydrogen Purge." The

inspectors were unable to evaluate the adequacy of the PMT because CCNPP had not

retained the test record data (see 2.3 below). The inspectors were initially unable to

determine whether the wire had mistakenly not been terminated during the modification

installation process, or whether the wire had subsequently come loose during adjacent

work in the panel. However, the inspectors determined that the SIAS panel wiring was

safety related and seismic category-1. Therefore, the inspectors concluded that CCNPP

did not properly terminate a wire to hand-switch 2HS-6901 during a previous

modification, and the subsequent quality inspection process failed to identify the faulty

termination.

Analysis. This finding was a performance deficiency because written work instructions

were not adequately followed. Traditional enforcement does not apply because the

issue did not have any actual safety consequences or potential for impacting the NRCs

regulatory function and was not the result of any willful violation of NRC requirements or

CCNPP procedures. This finding was more than minor because the SIAS system was

returned to service, following modification work, and subsequently became unable to

perform its function as a result of the deficiency, similar to example 5.b in NRC

Inspection Manual 0612 Appendix E, "Examples of Minor Issues." This finding affected

the Mitigating Systems cornerstone objective to ensure availability, reliability, and

capability of mitigating systems, because it was associated with the cornerstone

attributes for human performance.

This finding was determined to have very low safety significance, and screened out as

Green, using the NRC Significance Determination Process (SDP) Phase-1 screening

worksheet for NRC MC 0609 Appendix A, "Reactor Inspection Findings for At-Power

Situations." This finding had very low safety significance because the finding did not

represent an actual loss of a safety function, and was not potentially risk significant due

to an external initiating event. CCNPP entered this finding into their corrective action

program as IR4-025-652 and IR4-028-080.

12

Enclosure

A contributing cause of the finding was related to the Human Performance cross-cutting

area because maintenance technicians did not adequately implement written work

instructions.

Enforcement. Technical Specification 5.4.1 required, in part, that written procedures

shall be established and implemented as recommended in NRC Regulatory Guide (RG)

1.33 Appendix A. RG 1.33 Appendix A, section 9.a, "Procedures for Performing

Maintenance," required pre-planned maintenance activities be performed in accordance

with written procedures for maintenance that can affect the performance of safety

related equipment. CCNPP modification work order 2-2000-00544 required, in part, that

wires were properly terminated, in accordance with E-406, "Installation Standard - Main

Control Board Wiring."

Contrary to the above, on January 23, 2004, a self-revealing event identified that on

March 20, 2003, CCNPP did not adequately implement work order 2-2000-00544

instruction steps to terminate wiring added by the modification. Because this violation

was of very low safety significance, and CCNPP entered this finding into their corrective

action program (IR4-025-652 and IR4-028-080), this violation is being treated as a

non-cited violation (NCV), consistent with Section VI.A of the NRC Enforcement Policy.

(NCV 05000318/2004008-02, Failure to Adequately Implement Modification Work

Instructions for Wiring Terminations.)

2.

Previous Corrective Actions for Compression Style Terminations

In 1997, Unit 1 had a reactor trip (LER 50-317/1997-009) which was a direct result from

an improper compression style termination, on a similar, but non-safety related, control

panel hand-switch. Calvert Cliffs root cause analysis report (CCER 9701) had a

corrective action (IR1-053-484) to evaluate the use of a different type of termination

(such as a crimped lug, under the switchs termination screw), to replace the

compression style termination currently used. CCNPP engineering subsequently

determined that the compression style termination was more reliable (ES 1998-00394).

CCNPP's review of the current issue also contains a corrective action to evaluate use of

a non-compression style termination. The inspectors concluded that CCNPP may have

missed an opportunity to have prevented this failure.

3.

Control of Testing Scope and Acceptance Criteria

The SIAS reset circuit PMT consisted of wiring continuity checks, performed by ME-001,

"Wiring Verification." No functional or operational test of the SIAS reset circuit was

performed. ME-001 required that a supervisor verify the list of "circuits or drawings" to

be checked, prior to the wiring continuity checks. The inspectors identified that the

supervisor's "circuit identification" was designated by drawing number. The inspectors

determined that the designated drawings contained numerous circuits, cables, and

schemes, many of which were not involved with the modification. The test points, for

the point-to-point continuity checks, were not pre-planned and were only required to be

performed on the portion of the circuit that was new or modified. The selection of the

13

Enclosure

test points was considered a skill-of-the-craft attribute. The inspectors concluded that

allowing the maintenance technicians to select the test points may not test all aspects of

the modification that are required to be tested. In addition, the inspectors identified that

the test procedure (ME-001) did not require supervisory review or approval of the test

results.

10 CFR 50 Appendix-B Criterion XI, "Test Control," required, in part, that testing

required to demonstrate that systems will perform satisfactorily shall be performed in

accordance with written procedures which incorporate requirements and acceptance

limits. In the instance of the SIAS reset circuit modification, the ME-001 wiring

verification test was the only PMT performed. The inspectors determined that ME-001

did not contain adequate written requirements or acceptance criteria, because the

testing scope was designated at the drawing level, not the individual circuit or wire level.

The inspectors determined that this was a minor violation of regulatory requirements,

because the inspectors did not identify any instance where this performance deficiency

had impacted the final test results. CCNPP entered this issue into their corrective action

program as IR4-023-641.

2.3

Test Records for Safety Related Work Not Retained by Document Control

a.

Scope

The inspectors reviewed selected post-maintenance and post-modification test records

to evaluate whether the retained quality assurance records were adequate to verify that

the associated tests demonstrated that safety related systems could perform their

intended functions, after completion of maintenance or modification activities.

b.

Findings

Introduction. The inspectors identified a non-cited violation of very low safety

significance (Green) because CCNPP did not retain records of test results, as required

by 10 CFR 50 Appendix B, Criterion XVII, "Quality Assurance Records." Specifically,

CCNPP did not retain wiring verification point-to-point test records for modifications of

safety related circuits. As a result, after the records were transferred to Records

Management, verification of the work performed could not be done. This finding was

related to the Human Performance cross-cutting area.

Description. In February 2004, the inspectors were unable to independently verify

whether post-modification testing (PMT) had been adequately performed for

modification work order 2-2000-00544, "Remove SIAS Contacts from Containment

Purge Isolation and Hydrogen Purge." CCNPP Records Management did not retain

individual point-to-point wiring verification documents, as required by ME-001, "Wiring

Verification." Without the required test records, there was no documentation to identify

which circuits, wires, or schemes had been checked, and no documentation to identify

from where-to-where that the continuity checks had been performed.

14

Enclosure

For the SIAS reset circuit modification, no additional operational testing of the SIAS

reset function was performed. The PMT relied entirely on the point-to-point wiring

verification tests to verify SIAS reset circuit functionality. ME-001 section 6.3 required

schematic drawings to be highlighted with the actual circuit locations where the point-to-

point wiring checks had been performed. ME-001 section 7 required that all highlighted

drawings and data sheets be attached to the initiating maintenance work order. ME-001

section 9 required that the records generated by the procedure were to be identified as

permanent and retained for the lifetime of the plant.

CCNPP retained quality assurance safety related paper records by converting them into

electronic records through an optical imaging process. The inspectors identified that in

1999, a revision to a CCNPP Records Management checklist excluded the ME-001

highlighted drawings as records which were required to be optically imaged. The

marked-up drawings were highlighted in color, but the imaging system could not image

color.

Analysis. This finding was a performance deficiency because written procedure

instructions were not implemented. Traditional enforcement does not apply because the

issue did not have any actual safety consequences or potential for impacting the NRCs

regulatory function and was not the result of any willful violation of NRC requirements or

CCNPP procedures. This finding was more than minor because the failure to retain the

required records was not an isolated example, and the records were irretrievably lost,

similar to example 1.b in NRC Inspection Manual 0612 Appendix E, "Examples of Minor

Issues."

This finding was not suitable for an NRC Significance Determination Process evaluation,

but was reviewed by NRC management and determined to be of very low safety

significance (Green). This finding would have been considered as potentially greater

than very low safety significance if the missing test records had been associated with

inadequate testing that had been linked to subsequent equipment failures which

resulted in an event of greater than very low safety significance. CCNPP entered this

finding into their corrective action program as IR4-025-931.

A contributing cause of this finding was related to the Human Performance cross-cutting

area because station personnel did not adequately implement written instructions in a

safety related procedure.

Enforcement. 10 CRF 50 Appendix B, Criterion XVII, "Quality Assurance Records,"

required, in part, that sufficient records shall be maintained to furnish evidence of

activities affecting quality, including results of tests. The CCNPP Quality Assurance

(QA) Policy, revision 57, stated that the QA Program satisfied the requirements of

American National Standards Institute (ANSI) N18.7-1976 for administrative controls

and quality assurance of safety related plant activities. ANSI N18.7 section 5.2.17,

"Inspections," required that records shall be kept in sufficient detail to permit adequate

confirmation of the inspection program. CCNPP safety related procedure ME-001,

"Wiring Verification," section 7 and 9, required all highlighted drawings and records

generated by the procedure to be retained for the life of the plant. Contrary to the

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Enclosure

above, on March 26, 2004, the inspectors identified that CCNPP had not retained test

records, as required by ME-001, since approximately 1999.

Because this violation was of very low safety significance, and CCNPP entered this

finding into their corrective action program (IR4-025-931), this violation is being treated

as a non-cited violation (NCV), consistent with Section VI.A of the NRC Enforcement

Policy. (NCV 05000318/2004008-03, Test Records for Safety Related Work Not

Retained by Document Control)

2.4

Unit 1 Digital Feedwater Design Deficiency

a.

Inspection Scope

The inspectors reviewed the design deficiency in the digital feedwater system and its

effect on the loss of feedwater to the 11 steam generator which resulted in a Unit 1

reactor trip on March 20, 2004. The inspectors reviewed the digital feedwater control

system design, interviewed plant personnel to independently determine what occurred

and evaluated the initiating causal factors. The inspectors assessed CCNPPs cause

determination and corrective actions to evaluate the adequacy of CCNPPs conclusions

and actions.

b.

Findings

Introduction. A self-revealing event identified a finding because CCNPP failed to

perform an adequate design review, as required by station procedures. This resulted in

reduced reliability of the digital feedwater system and subsequently caused the Unit 1

reactor trip on March 20, 2004.

Description. On March 20, 2004, during maintenance on the 1-ER-101, 500 KV Bus

Voltage chart recorder technicians created a short circuit on the C phase of

instrument bus 1Y09. Instrument bus 1Y09 is a three phase ungrounded AC system

and since this is a three-phase ungrounded system the voltage on the other phases (A

& B) increased. The normal AC power for the 11 steam generator digital feedwater

control system is supplied by the B phase from instrument bus 1Y09. The increase in

voltage on the B phase resulted in metal oxide varistor (varistor) failures in the digital

feedwater position indicators for the feedwater regulating valve. These failed varistors

acted as a short circuit and opened a fuse in the normal power supply to the digital

feedwater control processor. The power supply automatically transferred to the backup

AC power supply from instrument bus 1Y10, but since the failed varistors were still in the

circuit, the fuse from the backup power supply opened which removed both the normal

and backup AC power to the 11 steam generator digital feedwater control system. The

digital feedwater regulating valve failed to automatically transfer to DC control, which

resulted in closing the regulating valve, reducing the level in 11 Steam generator

resulting in a subsequent reactor trip.

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Enclosure

Calvert Cliffs had previously determined that the design of the digital feedwater position

indicators for the feedwater regulating valve and bypass valves were not designed for

the higher voltages that a three-phase ungrounded system could sustain with one phase

shorted. Calvert Cliffs failed to correctly specify the power supply voltages on the digital

feedwater position indicators as required by ES-021, Design Input Requirements

Preparations. The design input requirement evaluation concluded that the power supply

for the position indicators, which include the varistors, were approximately 115 VAC.

However, since the power supply is a three-phase ungrounded system the varistors

could be expected to experience voltages as high as 208 VAC during a fault condition.

Therefore, under the conditions experienced, the varistors failed, which resulted in

reduced reliability of the feedwater digital control system and resulted in the reactor trip.

Analysis. This finding was a performance deficiency because CCNPP did not perform

an adequate design review, as required by station procedures ES-020, Impact Screens

for the Engineering Service Process, and ES-021, Design Input Requirements

Preparation. Calvert Cliffs did not properly identify and evaluate critical aspects of the

electrical power supply. Traditional enforcement does not apply because the issue did

not have any actual safety consequences or potential for impacting the NRCs

regulatory function and was not the result of any willful violation of NRC requirements or

CCNPP procedures. This finding affected the Initiating Events cornerstone objective

because it contributed to increasing both the likelihood of a reactor trip and the

likelihood that mitigating equipment or functions will not be available. This finding was

more than minor because it effects the design control attributes of the Initiating Events

cornerstone. Incorrectly specifying the design voltage resulted in reducing the reliability

of the digital feedwater control system which increased the likelihood of an event that

upset plant stability during power operation.

The finding was determined to be of very low safety significance (Green), using the NRC

Significance Determination Process (SDP). The Phase-1 screening determined that a

Phase-2 evaluation was required because the finding affected both the Initiating Event

and Mitigating Systems Cornerstones. In the Phase 2 risk analysis, the Transient and

Loss of Component Cooling Water (LOCCW) initiating events were reviewed, as

specified the Calvert Cliffs Plant Specific Risk Notebook. For Transients, the initiating

event frequency was increased by one order of magnitude, because the digital

feedwater control issue increased the likelihood of a loss of feedwater. For both the

Transient and LOCCW SDP worksheets, the mitigation credit for the power conversion

system (PCS) was decreased by one order of magnitude, because the feedwater

system was less redundant with only one feed path available. The dominant core

damage sequence was a transient, with successful reactor trip, followed by a loss of

steam generator cooling and failure to initiate once through cooling (Feed and Bleed).

The Phase-2 analysis determined that this finding was of very low safety significance

(Green), because the finding did not affect the auxiliary feedwater system, and one of

two turbine driven feedwater pumps remained available.

Enforcement. There were no violation of NRC regulatory requirements because the

affected equipment was not safety-related. Calvert Cliffs entered this finding into their

corrective action program as IR200400168. (FIN 50-317/2004008-04, Failure to

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Enclosure

Adequately Implement a Modification Design Review of the Digital Feedwater

Control System)

3.0

Human Factors and Procedural Issues

3.1

Failure to Properly Implement Station Emergency Operating Procedures

a. Inspection Scope

The inspectors reviewed the licensed operator performance following the Unit 2 reactor

trip on January 23, 2004. Specifically, the inspectors looked at operator use of the

emergency operating procedures (EOPs) and previous related training provided to the

operators, and compared operator actions to procedural requirements.

b. Findings

Introduction. The inspectors identified a Green finding because CCNPP did not follow

procedural requirements in their implementation of EOP-0, Post-trip Immediate

Actions, and EOP-1, Reactor Trip. The operators mis-diagnosed plant conditions in

EOP-0 and incorrectly proceeded to EOP-1 rather than EOP-4, Excess Steam Demand

Event. Further, once in EOP-1, the operators failed to comply with the direction of that

procedure. These failures to follow station procedures complicated the plants post-trip

response and the ability of the operators to restore normal plant conditions.

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Enclosure

Description

Procedure Implementation

Following the Unit 2 reactor trip on January 23, the control room operators entered

procedure EOP-0. This procedure is organized around critical safety functions which

must be satisfied when a reactor trip occurs, to ensure that the plant is placed in a

stable, safe condition or that the plant is configured to further respond to a continuing

casualty. When the ADVs and TBVs remained open following the trip, RCS

temperature, pressurizer pressure and pressurizer level deviated from the acceptance

values in EOP-0. While in EOP-0, operators attempted to recover these parameters to

the values expected after a normal reactor trip. As part of that effort, the operators

implemented steps of EOP-4 out of sequence in order to attempt to restore RCS

parameter values. Following the SIAS, the safety injection compounded these out-of-

sequence operator actions, and the pressurizer was overfilled with a large mass of cold

water. RCS pressure was then dominated by this large volume of cold water, not the

smaller-than-usual steam vapor bubble. The pressurizer bubble slowly lost its energy to

the colder water volume, and pressure began to decrease, leading to the second SIAS.

In addition, the operators also incorrectly exited EOP-0 to go to EOP-1 when both the

RCS Pressure/Inventory Safety Function and the Core/RCS Heat Removal Safety

Function were not met. The diagnostic flowchart in EOP-0 directs the use of EOP-1

only when all safety functions are met. In this case, with two safety functions not met,

EOP-0 directs the implementation of EOP-4. However, the operators should have been

able to correctly enter EOP-4 even after entering EOP-1. Procedure EOP-1 requires

that the diagnosis of an uncomplicated trip is correct by verifying the Safety Function

Status Checks Intermediate Acceptance Criteria are satisfied. If any parameter does

not satisfy the Intermediate Acceptance Criteria, and cannot be readily returned to within

the Acceptance Criteria, the operator should perform EOP-8, Functional Recovery

Procedure, or re-diagnose the event using the EOP-0 diagnostic flowchart and

implement the appropriate procedure. On January 23, 2004, the Unit 2 operators

identified that the RCS Pressure and Inventory parameters and the Core and RCS Heat

Removal parameters did not satisfy the safety function status checks for at least the first

12 intermediate checks, yet the operators remained in EOP-1 and did not re-diagnose

the event and did not implement the appropriate procedure, which in this case was

EOP-4.

Also contributing to the improper use of the EOPs was the operators implementation of

the provisions of procedure NO-1-201, Calvert Cliffs Operating Manual. Section 5.1C

of that procedure allows deviation from controlling technical procedures to prevent

conditions directly adverse to personnel safety, plant safety, plant stability, or the safety

of the public. The procedure does not include a required condition that no other

approved procedure is available (as is required by 10CFR50.54(x) and ANSI Standard

N18.7/ANS 3.2-1976, Section 5.2.2). On January 23, operators used the provision of

NO-1-201 to deviate from EOP-0 and EOP-1 when in fact other procedures were

available to be used to mitigate this event.

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Enclosure

Licensed Operator Training

Calvert Cliffs has increased the time allowed to execute EOP-0, to allow the operators to

concurrently implement procedure steps from other EOPs, without executing the entire

EOP. Calvert Cliffs allows this practice while in EOP-0, so that key plant parameters

can be restored to normal operating bands. This philosophy resulted in the operators

performing actions using knowledge-based skills as opposed to procedure-base skills

during high stress condition. This practice significantly increased the potential for

operator errors, and in the case of the January 23, 2004 event, it resulted in improper

transitions in the EOP procedures.

Analysis. This finding was a performance deficiency because the operating crew did not

follow procedural requirements in their implementation of EOP-0, Post-trip Immediate

Actions, and EOP-1, Reactor Trip. Traditional enforcement does not apply because

the issue did not have any actual safety consequences or potential for impacting the

NRCs regulatory function and was not the result of any willful violation of NRC

requirements or CCNPP procedures. The finding is greater than minor because it

affected the Human Performance attribute of the Mitigating Systems cornerstone

objective. This finding was determined to have very low safety significance, and

screened out as Green, using the NRC Significance Determination Process (SDP)

Phase-1 screening worksheet for NRC MC 0609 Appendix A, "Reactor Inspection

Findings for At-Power Situations." This finding had very low safety significance because

the finding did not represent an actual loss of a safety function, and was not potentially

risk significant due to an external initiating event. CCNPP entered this finding into their

corrective action program as IR4-025-167.

A contributing cause of the finding was related to the Human Performance cross-cutting

area because licensed operators did not properly implement station emergency

operating procedures.

Enforcement. Calvert Cliffs Technical Specification 5.4.1.b, states that written

procedures shall be established, implemented, and maintained covering the emergency

operating procedures required to implement the requirements of NUREG-0737. EOP-0

requires, when safety functions are not met following a reactor trip, the transition to the

appropriate optimal recovery procedure EOP. EOP-1 requires, when Safety Function

Status Checks Intermediate Acceptance Criteria are not satisfied, the return to EOP-0 or

the use of EOP-8.

Contrary to the above, on January 23, 2004, licensed operators at Calvert Cliffs Unit 2

improperly implemented EOP-0, Post-trip Immediate Actions, and EOP-1, Reactor Trip.

With several safety functions still not satisfied, the operators improperly went to EOP-1

from EOP-0 instead of proceeding to EOP-4 as required by EOP-0. Further, with Safety

Function Status Checks Intermediate Acceptance Criteria not satisfied, the operators

improperly remained in EOP-1 instead of returning to EOP-0 to re-diagnose the event.

Because this violation was of very low safety significance, and CCNPP entered this

finding into their corrective action program (IR4-025-167), this violation is being treated

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Enclosure

as a non-cited violation (NCV), consistent with Section VI.A of the NRC Enforcement

Policy. (NCV 05000318/2004008-05, Failure to Properly Implement Station

Emergency Operating Procedures)

3.2

Failure to Have Procedures Required by Regulatory Guide 1.33

a.

Inspection Scope

The inspectors reviewed CCNPP procedures following the Unit 2 reactor trip on January

23, 2004. Specifically, the inspectors looked at procedures available to operators for the

use of the Reactor Regulating System (RRS) and for contingency measures for use

upon that systems failure.

b.

Findings

Introduction: The inspectors identified a Green finding because CCNPP did not have

any procedural guidance for the failure of the RRS during their implementation of EOP-

0, Post-trip Immediate Actions. Upon the reactor trip and the subsequent failure of the

K7 relay in the X channel of the RRS, if the operators had switched to the alternate Y

channel of RRS, the ADVs and TBVs would have properly controlled the RCS

temperature and terminated the uncontrolled cooldown event.

Description: Calvert Cliffs Unit 2 did not have procedures specifically designed to

combat the malfunction of the RRS. Although the station had procedural direction on

how to change RRS channels, that direction was contained in the precautions of

operating instruction OI-7, Reactor Regulating System, rather than an alarm response

procedure or abnormal operating procedure used to combat a malfunction. The RRS is

designed to provide control functions for the steam dump valves (TBVs and ADVs) for

quick opening to remove stored energy upon a reactor trip, using RCS T-ave and

turbine trip as initiating signals. This quick open feature provides for automatic control

of RCS T-ave and pressurizer pressure following a reactor trip. On January 23, when

the RRS failed and incorrectly kept the TBVs and ADVs open, Unit 2 operators did not

have proper procedural guidance direct their response to the RRS malfunction event,

forcing them to improperly use parts of different EOPs to combat the resulting off-

normal RCS T-ave and pressurizer pressure and level parameters.

Analysis: This finding was a performance deficiency because the CCNPP is required to

have a written procedure to combat the malfunction of a pressure control system.

Traditional enforcement does not apply because the issue did not have any actual safety

consequences or potential for impacting the NRCs regulatory function and was not the

result of any willful violation of NRC requirements or CCNPP procedures. The finding is

greater than minor because it affected the Procedure Quality attribute of the Mitigating

Systems cornerstone objective. This finding was determined to have very low safety

significance, and screened out as Green, using the NRC Significance Determination

Process (SDP) Phase-1 screening worksheet for NRC MC 0609 Appendix A, "Reactor

Inspection Findings for At-Power Situations." This finding had very low safety

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Enclosure

significance because the finding did not represent an actual loss of a safety function,

and was not potentially risk significant due to an external initiating event. CCNPP

entered this finding into their corrective action program as IR4-018-361.

Enforcement: Calvert Cliffs Technical Specification 5.4.1.a, states that written

procedures shall be established, implemented, and maintained covering the applicable

procedures recommended in Regulatory Guide 1.33, Revision 2, Appendix A, February

1978. That Regulatory Guide specifies procedures for abnormal, offnormal, or alarm

conditions and procedures for combating emergencies and other significant events,

including the malfunction of a pressure control system.

Contrary to the above, on January 23, 2004, licensed operators at Calvert Cliffs Unit 2

did not have a specific procedure to respond to the abnormal condition created by the

malfunction of the RRS, a pressure control system. Because this violation was of very

low safety significance, and CCNPP entered this finding into their corrective action

program (IR4-018-361), this violation is being treated as a non-cited violation (NCV),

consistent with Section VI.A of the NRC Enforcement Policy. (NCV 05000318/2004008-

06, Failure to Have Procedures Required by Regulatory Guide 1.33)

3.3

Simulator Fidelity Issues

a.

Inspection Scope

Through operator and training department interviews, and through licensee document

review, the inspectors reviewed the licensed facilitys control room simulator and its

ability to accurately reproduce the events of January 23, 2004. Specifically, the

inspectors looked at the simulator model replication of the RCS pressure and

temperature transients observed that day by the control room operators.

b.

Findings

No findings of significance were identified.

Observations

Calvert Cliffs identified a difference between the plants RCS pressure and pressurizer

temperature parameter response when the Unit 2, January 23 reactor trip was replicated

on the plant specific simulator. Calvert Cliffs validates plant trips on their simulator to

verify simulator fidelity. The validation of the January 23 reactor event, including the

reactor trip and post-trip equipment and operator actions, revealed substantial

differences in actual and predicted RCS pressure and temperature during the initial

depressurization and subsequent repressurization. Specifically, after the TBVs and

ADVs were shut, a plant heat-up occurred, and pressurizer level and RCS pressure

increased in both the plant and the simulator. Operator action was required in the plant

to stop the RCS pressure increase, but no operator action was required in the simulator

to stop and control the RCS pressure. This contributed to the operators not fully

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Enclosure

comprehending the behavior of pressurizer parameters, particularly the pressurizer

bubble-water mass energy interface.

Calvert Cliffs identified the cause of the fidelity issue as deficiencies in the original

simulator software model that was installed in 1985. The licensee identified that the

discrepancy between plant and simulator responses was due to three simulator model

coefficient deficiencies. The Calvert Cliffs plant specific simulator did not correctly

replicate RCS pressure and pressurizer temperature for this excess steam demand

event. The differences between the actual plant response and the response previously

experienced by the operators in their simulator training confused the operators and

complicated the recovery of plant parameters following the Unit 2 reactor trip. However,

enforcement action was not pursued due to the apparent cause of the issue being an

original design issue, the identification of which was beyond the scope of expected and

required testing.

3.4

Failure to Comply with Station Work Control Procedures

a.

Inspection Scope

The inspectors reviewed CCNPP work control practices and decision-making processes

which led up to the reactor trip on March 20, 2004, at Unit 1. Specifically, the inspectors

interviewed licensed operators, managers, and maintenance staff who had been

involved in the decisions to defer the replacement of vulnerable components in the

digital feedwater system, those who had been involved in the scheduling of electrical

work during the week of March 14, and those who were immediately involved on March

20. The inspectors reviewed CCNPP work control procedures and compared CCNPP

actions against those procedural requirements and expectations.

b.

Findings

Introduction. This self-revealing event identified a Green finding because CCNPP did

not follow procedural requirements in their risk assessment and control of the work that

was performed March 20, 2004, on Unit 1. Specifically, the provisions and controls of

procedures NO-1-100, Conduct of Operations, NO-1-117, Integrated Risk

Management, and MN-1-100, Conduct of Maintenance, were not followed. These

failures to follow station procedures impacted the Initiating Events cornerstone in that

the failure to properly classify and control the work in the control room on March 20 lead

to an unanticipated reactor trip.

Description. In February 2004, a maintenance order was generated to repair the 500KV

Bus Voltage Recorder 1ER-101 because the chart paper was not advancing. This piece

of equipment is owned by the Generation Protections and Test Unit (GPTU), and that

group was scheduled to be onsite March 20 to perform other site work. Based on that

scheduling, the work on the recorder was placed on that weeks work schedule as

emergent work. Calvert Cliffs records and NRC interviews of CCNPP staff show that

the NO-1-117 work control/risk assessment process was implemented during the week

of 3/14, yet a number of barriers failed or were bypassed:

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Enclosure

1)

No one involved in the scheduling or performance of the 1ER-101 recorder work

recognized that the work involved the 1Y09 bus, and that the work should have

gotten additional management attention, per the prior management decision

made last year. The exact nature of the intended 1Y09/10 work prohibition or

control was not clear due to the lack of documentation.

2)

No one involved in the scheduling or performance of the 1ER-101 recorder work

recognized that the work involved a trip sensitive area as defined in NO-1-100.

Therefore, the additional preparation and oversight required by NO-1-100 were

not implemented. The inspector also identified that the current revision of NO-1-

100 directs the requirements of MN-1-124, Conduct of Integrated Work

Management, be followed for work in trip sensitive areas, yet those

requirements in essence had been relocated to NO-1-117 without a change to

the NO-1-100 procedure direction.

3)

The risk assessments performed by the responsible group supervisor (RGS) and

outage work control (OWC) in accordance with NO-1-117 incorrectly rated the

1ER-101 work as low risk. Due to the work being performed in a trip sensitive

area and due to the previously identified vulnerability of the feedwater control

system to work involving the 1Y09 bus, this work should have been rated as

medium risk. The additional controls associated with a higher risk assessment

were not implemented.

4)

The actual 1ER-101 work was not performed in accordance with the

expectations of MN-1-100, in that the pre-job briefing committed to using STAR,

supervisory oversight, and peer checks as defenses to prevent errors. The

failure to implement these practices directly led to the pinching of the power

supply wire during the reinstallation of the 1ER-101 and the creation of the

ground which initiated the reactor trip event.

When work was done on the 1ER-101 recorder, a piece of equipment powered by the

1Y09 bus, the lack of increased oversight and control of the work allowed a ground to be

created, and all AC power to the Unit 1 digital feedwater control system was lost. This

failure, combined with a latent failure in the DC power control system, led to an actual

partial loss of feedwater event and a Unit 1 reactor trip.

Analysis. This finding was a performance deficiency because CCNPP did not properly

risk-assess the work planned for March 20 nor did they put in place the proper

precautions for the work, as required by station procedures. Traditional enforcement

does not apply because the issue did not have any actual safety consequences or

potential for impacting the NRCs regulatory function and was not the result of any willful

violation of NRC requirements or CCNPP procedures. This finding was more than

minor because the combination of procedural non-compliances was considered to be a

precursor to a more significant event, and it affected the Significance Determination

Process Initiating Event Cornerstone by being a transient initiator contributor (i.e.,

directly led to an unplanned reactor trip). The finding screened to Green because the

procedural non-compliances did not contribute to a LOCA initiator, contribute to the

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Enclosure

likelihood mitigation equipment would not be available, or increase the likelihood of a fire

or flood.

A contributing cause of the finding was related to the Human Performance cross-cutting

area because CCNPP managers and staff did not properly implement station

operations, risk management, and maintenance procedures.

Enforcement. No violation of regulatory requirements occurred. The inspectors

determined that the finding did not represent a noncompliance because it occurred on

non-safety-related secondary plant equipment. CCNPP entered this finding into their

corrective action program as IR4-028-774. (FIN 50-317/2004008-07 Failure to Comply

with Station Work Control Procedures)

4.0

Emergency Preparedness

4.1

Failure to Recognize and Report an Unusual Event During the January 23, 2004, Unit 2

Reactor Trip

a.

Inspection Scope

The inspectors reviewed the CCNPP implementation of the emergency plan during the

January 23, 2004, Unit 2 reactor trip. The inspectors conducted interviews with licensed

senior reactor operators (SRO), reactor operators (RO) and station support staff. The

inspector reviewed station procedures and industry guidance and then compared the

operators performance to station procedures and industry guidance documents.

b.

Findings

Introduction. The inspectors identified a non-cited violation of very low safety

significance (Green) because the CCNPP operating staff and post trip review did not

recognize that plant conditions required an emergency level classification (Unusual

Event) in accordance with station procedures. As a result, CCNPP did not correctly

implement the station emergency plan as required by 10CFR50.54(q). This finding was

related to the Human Performance cross-cutting area.

Description. During the Unit 2 reactor trip and subsequent failure of the Reactor

Regulating System, the ADVs and the TBVs failed open for approximately nine minutes.

This resulted in an uncontrolled RCS cooldown which emptied the pressurizer, resulted

in an automatic SIAS actuation, and a SGIS isolation. This excessive cooldown event

was partially terminated by the SGIS isolation which isolated the TBVs and was finally

terminated when the operators regained local control of the ADVs.

During this event the operators identified that the open TBVs and ADVs were not

responding as designed. However, when evaluating plant conditions, the operators did

not correctly conclude that the cause of the conditions (failed open TBVs and ADVs)

were unexplained. Since the operators did not understand why the valves had failed to

25

Enclosure

reclose they should have concluded that the condition was unexplained. This would

have resulted in a determination that plant conditions met the entry conditions for EOP-

4, Excessive Steam Demand Event, and required an Unusual Event classification.

The CCNPP emergence action level (EAL) classification matrix specified that EOP-4,

Excess Steam Demand Event is Implemented, met the criteria for an Unusual Event.

Unexplained lowering of one or both steam generator pressure are entry conditions into

EOP-4, Excessive Steam Demand Event. These plant conditions were present, and

Station procedure NO-1-201, Calvert Cliffs Operating Manual, requires classification

of an event when the plant condition meets the emergency classification criteria.

Therefore, the licensed operators should have reasonablely identified that an Unusual

Event classification was required.

During the post-trip review, CCNPP concluded that an Unusual Event declaration was

not required because EOP-4, Excessive Steam Demand Event, entry conditions were

not met. The review concluded that the source of the excessive steam demand was the

failed open TBVs and ADVs, and because the cause of the excessive steam demand

was known, the entry condition for EOP-4 was not met. Therefore, this review

concluded that EOP-4 was not entered and no Unusual Event declaration was required.

The post trip review incorrectly concluded that the cause of the failed open TBV and

ADVs was explained. The failed open TBVs and ADVs were not responding as

designed and met the entry conditions for EOP-4. Therefore, these plant conditions

were commensurate with an Unusual Event. During the week of January 17, 2004, the

inspectors discussed the Unusual Event classification with CCNPP. On May 28, 2004,

CCNPP completed a 1-hour report in accordance with 10 CFR 50.72(a)(1)(i) for this

event.

Analysis. The inspectors determined that this finding was a performance deficiency

because CCNPP operating staff did not recognize plant conditions commensurate with

an Unusual Event and therefore, the plant operating staff did not declare an Unusual

Event nor did the post-trip review identify the Unusual Event. Traditional enforcement

does not apply because the issue did not have any actual safety consequences or

potential for impacting the NRCs regulatory function and was not the result of any willful

violation of NRC requirements or CCNPP procedures. This finding was more than

minor because it effects the response organization performance attribute of the

Emergency Preparedness Cornerstone in that failure to recognize plant conditions

indicative of an Unusual Event resulted in not identifying the Unusual Event. The finding

was assessed using MC 0609, Appendix B, Emergency Preparedness Significant

Determination Process, sheet 2, Actual Event Implementation Problem. The finding

was determined to be of very low safety significance (Green) because the operators

failed to identify Unusual Event conditions during an actual plant event.

This finding is related to the Human Performance cross-cutting area because reactor

operators and the Unit 2 post trip review did not recognize plant conditions

commensurate with an Unusual Event and did not report the Unusual Event prior to

prompting by the NRC.

26

Enclosure

Enforcement. This was a violation of 10CFR50.54(q) which states in part that licensees

shall follow their emergency plans. The CCNPP Emergency Response Plan, Section

4.0, Emergency Measures, states "Emergency Response Plan Implementing

Procedures contain procedures and guidance for accident assessment and emergency

classification." ERPIP-3.0, Immediate Actions, Attachment 2 entitled "Emergency

Classification" directs operators to evaluate plant conditions against EAL Criteria.

Specifically, EAL QU5 states the conditions for an unusual event: "EOP-4, Excess

Steam Demand Event is implemented." NO-1-201, "Calvert Cliffs Operating Manual"

states "During EOP-0, should it become apparent that an EAL condition is met, the

classification should begin right away without waiting for the next EOP to be

implemented."

Contrary to the above, the operating crew, in response to the January 23, 2004, reactor

trip event, did not recognize plant conditions that were commensurate with an Unusual

Event. The CCNPP post-event review did not identify that an Unusual Event should

have been identified based on plant conditions. This violation has been entered in

CCNPP corrective action program as IR4-023-606 and is being treated as a non-cited

violation (NCV), consistent with Section VI.A of the NRC Enforcement Policy. (NCV

05000318/2004008-08, Failure to Recognize an Unusual Event During the Unit 2

Reactor Trip)

5.0

Cross Cutting Aspects of Findings

Section 2.2 describes a finding where maintenance technicians did not adequately

implement written work instructions. As a result, during a plant event, recovery actions

were delayed because operators were unable to reset the "B" channel SIAS actuation

from the control room.

Section 2.3 describes a finding where station personnel did not adequately implement

written instructions in a safety related procedure to maintain records that can be used to

determine the scope of work performed on safety related components. The failure to

retain the required records, as required by ME-001, since approximately 1999 resulted

in the records being irretrievably lost

Section 3.1 describes a finding where licensed operators did not properly implement

station emergency operating procedures. These actions resulted in the operators

performing actions using knowledge-based information as opposed to skill-based

information. This resulted in the operators selecting what actions should be performed

out of station procedures based on plant indications, under high stress conditions which

significantly increased the potential for operator errors, and in the case of the January

23, 2004 event, it resulted in improper transitions in the EOP procedures.

Section 3.4 describes a finding where CCNPP managers and staff did not properly

implement station operations, risk management, and maintenance procedures. This

resulted in a precursor to Unit 1 reactor trip on March 20, 2004.

27

Enclosure

Section 4.1 describes a finding where licensed operators and the post-trip review failed

to recognize plant conditions commensurate with an Unusual Event during the January

23, 2004, Unit 2 excessive steam demand event.

6.0

Generic Issues

During this inspection, no significant issues were identified requiring the issuance of

generic communications to the nuclear industry.

7.0

Risk Significance of the January and March 2004 Events

The team conducted an initiating event assessments and concluded that each event

resulted in a moderate risk significance conditional core damage probability (CCDP)

(between E-6 and E-5 per event). These risk assessments were conducted using the

NRCs standardized plant analysis risk (SPAR) model for Calvert Cliffs. The model was

updated to reflect the licensees operating experience and procedures. The licensee

also performed an initiating event assessments for these events and reached similar

conclusions.

Unit 2 January Reactor Trip

The team concluded that this event resulted in a conditional core damage probability

(CCDP) in the mid E-6 range. The following assumptions were used:



A general plant transient occurred due to a partial loss of feedwater.



The failure of the K-7 relay in the reactor regulating system resulted in the

turbine bypass valves and the atmospheric dump valves remaining full open and

not modulating to control reactor plant parameters, which resulted in an

uncontrolled cooldown of the reactor coolant system. As a result, steam

generator isolation and safety injection actuation signals were generated to

mitigate the event.

The dominant accident sequences for this transient event were: 1) failure of steam

generator cooling and Failure of once through core cooling; 2) failure of the reactor

protection system to shutdown the reactor and failure to limit reactor coolant system

pressure; and 3) failure of the reactor coolant pump seals and failure of high pressure

recirculation.

Unit 1 March Reactor Trip

The team concluded that this event resulted in a CCDP in the low E-6 range. The

following assumptions were used:



A general plant transient occurred due to a partial loss of feedwater. The main

feedwater flow path to SG11 was unavailable due to the digital feedwater control

system failure.

A-1

Enclosure

Attachment



Turbine bypass valves fast opened but failed to stay open to control pressure.

This resulted in the need to use the atmospheric dump valves.

The dominant accident sequences for this transient event were: 1) failure of steam

generator cooling and Failure of once through core cooling; 2) failure of the reactor

coolant pump seals and failure of high pressure recirculation; and 3) failure of the

reactor protection system to shutdown the reactor and failure to limit reactor coolant

system pressure.

8.0

Overall Adequacy of Licensee Response

The team concluded that the overall response of CCNPP to the January 23, 2004, Unit

2 reactor trip and the March 20, 2004, Unit 1 reactor trip were adequate because the

plants were taken to a safe shutdown condition. However, during both events the

operators were challenged by equipment malfunctions that were the result of less than

adequate design review and maintenance work. In addition, the operators had

problems implementing emergency operating procedures during the Unit 2 reactor trip.

The Unit 1 trip was the result of not correctly implementing work management control

procedures. CCNPP had an opportunity in both cases to previously address the issues.

CCNPPs corrective actions regarding equipment and procedures for this event have

been appropriate. However, the CCNPP identification and reporting of the Unusual

Event condition was delayed and had to be prompted by the NRC. These events show

the need for improvements in the human performance areas.

9.0

Exit Meeting Summary

The NRC presented the results of this special inspection to Mr. George Vanderheyden,

and other members of CCNPP management on June 18, 2004, via conference call.

Calvert Cliffs management acknowledged the findings presented. No proprietary

information was identified.

ATTACHMENT A

SUPPLEMENTAL INFORMATION

KEY POINTS OF CONTACT

Licensee Personnel:

T. Roberts, Supervisor - Electrical & Control Systems

M. McMahon, Supervisor - FIN Team

C. Yoder, Engineer - Electrical & Control Design

R. Stark, Senior Engineer - Electrical & Control Design

H. Winters, System Engineer

D. Lenker, Supervisor - Electrical and I&C Design

J. Kilpatrick, Senior Engineer - 50.59 Program

H. Daman, General Supervisor - Electrical and I&C Maintenance

A-2

Attachment

R. Simmons, Supervisor - I&C Maintenance

S. Collins, System Engineer

E. Roach, Lead Assessor

NRC Personnel:

M. Giles, Senior Resident Inspector - Calvert Cliffs

R. Fuhrmeister, Senior Reactor Inspector

A. Della Greca, Senior Reactor Inspector

E. McKenna, NRR

LIST OF ITEMS OPENED, CLOSED AND DISCUSSED

Opened

05000318/2004008-01

FIN

Failure to Adequately Implement Modification Design

Review of the Reactor Regulating System Quick Open

Circuit (Section 2.1.b.1)

Closed

05000318/2004008-02

NCV

Failure to Adequately Implement Modification Work

Instructions for Wiring Terminations (Section 2.2.b.1)05000318/2004008-03

NCV

Test Records for Safety Related Work Not Retained by

Document Control (Section 2.3)05000317/2004008-04

FIN

Failure to Adequately Implement a Modification Design

Review of the Digital Feedwater Control System (Section

2.4)05000318/2004008-05

NCV

Failure to Properly Implement Station Emergency

Operating Procedures (Section 3.1)05000318/2004008-06

NCV

Failure to Have Procedures Required by Regulatory Guide

1.33 (Section 3.2)05000317/2004008-07

FIN

Failure to Comply with Station Work Control Procedures

(Section 3.4)05000318/2004008-08

NCV

Failure to Recognize an Unusual Event During the Unit 2

Reactor Trip (Section 4.1)

A-3

Attachment

LIST OF DOCUMENTS REVIEWED

Section 2.1 Reactor Regulating System Quick Open Circuit Failure

Issue Reports

IR4-025-059

IR4-028-151

Work Orders

MO 2-2004-00291

Design Bases

CCNPP Quality Assurance Policy, revision 57

FSAR Section 7.4.1, "Reactor Regulating System"

Procedures

Checklist IPM56001, "Functional Testing of ADV and TBV Quick Open"

Drawings

86924SH0001X, "Unit 2 RRS Channel-X Schematic"

86924SH0001Y, "Unit 2 RRS Channel-Y Schematic"

86924SH0002X, "Unit 2 RRS Channel-X Schematic"

86924SH0002Y, "Unit 2 RRS Channel-Y Schematic"

63069, "Turbine Steam Dump and Bypass Control Schematic"

12017-0101, "RRS Block Diagram"

12132-0050, "RRS Reactor Program Unit Calculator Function and Wiring Diagram"

86-922-E, "RRS Test Panel Schematic Wiring Diagram"

Other Documents

Modification Package FCR 85-0068

System Descriptions, System 56 and 83A

System Health Report, System 56 and 83A

Maintenance Rule Scoping Document, System 56 and 83A

Main Steam System Risk Significant Components Report, revision 0, dated 03/19/1998

NUMARC 93-01, revision 2, "Monitoring the Effectiveness of Maintenance"

Section 2.2 SIAS Actuation Signal Failure to Reset from Control Room

Issue Reports

IR4-025-652, "ESFAS SIAS "B" Would Not Reset from the Control Room"

IR4-028-080, "Signal for SIAS Reset is Not Tested from Control Room"

IR4-022-941, "Unexpected Second SIAS Actuation"

A-4

Attachment

Work Orders

MO 2200000544, "Remove SIAS Contacts from Ctmt Purge Iso & H2 Purge"

MO 2200400304, "Check for Open Switch Contacts"

MO 2200302348, "Replace 23 CAC Hand Switch 2HS5301"

MO 2200302349, "Replace 24 CAC Hand Switch 2HS5302"

Design Bases

FSAR section 7.3, ESFAS

E-406, "Installation Standard - Main Control Board Wiring"

NRC Generic Letter 1996-01, "Testing of Safety Related Logic Circuits"

RG 1.187, "Guidance for Implementation of 10 CFR 50.59"

Procedures

ME-001, revision 0, "Wiring Verification"

STP-M-220B-2, "Engineered Safety Features Actuation System Channel ZE Functional Test"

PR-1-101, revision 20, "Preparation and Control of Technical Procedures"

EN-1-102, revision 8, "10 CFR 50.59 / 72.48 Reviews"

ES-017, revision 5, "10 CFR 50.59 Reviews"

Drawings

63076SH0042, "Schematic Diagram for Containment Vent & Hydrogen Purge"

63059, "Schematic Diagram for ESFAS"

63059A, "Schematic Diagram for ESFAS"

87310SH00002, "Wiring Diagram for Panel 2C10"

Other Documents

System Description No. 048, revision 2, "Engineered Safety Features Actuation System"

System Health Report for Systems 48 and 52

NEI 1996-07, revision 1, "Guidelines for 10 CFR 50.59 Implementation"

Section 2.3 Safety Related Test Records Not Retained

Issue Reports

IR4-025-652, "ESFAS SIAS "B" Would Not Reset from the Control Room"

IR4-028-080, "Signal for SIAS Reset is Not Tested from Control Room"

Work Orders

MO 2200000544, "Remove SIAS Contacts from Ctmt Purge Iso & H2 Purge"

MO 2200400304, "Check for Open Switch Contacts"

Design Bases

E-406, "Installation Standard - Main Control Board Wiring"

CCNPP Quality Assurance Policy, revision 57

ANSI N18.7-1976, "Administrative Controls and Quality Assurance for the Operational Phase of

Nuclear Power Plants"

Procedures

A-5

Attachment

ME-001, revision 0, "Wiring Verification"

Drawings

61036, Rev. 62, "Schematic Diagram 208/120V Instrumentation Buses 11 & 12 Unit #1"for

Containment Vent & Hydrogen Purge"

63059, "Schematic Diagram for ESFAS"

63059A, "Schematic Diagram for ESFAS"

87310SH00002, "Wiring Diagram for Panel 2C10"

Section 2.4 Unit 1 Digital Feedwater Design Deficiency

Issue Reports

IR200400168, March 20, 2004, Unit 1 Reactor Trip During Scheduled Maintenance

Procedures

ES-020, Rev. 10, Impact Screens for the engineering Service Process

ES-021, Rev. 04, Design Input Requirements (DIR) Preparation

EN-1-100, Rev. 16, Engineering Services Process Overview

EN-1-101, Rev. 06, Design Change and Modification Implementation

Analysis

ESP-199602497, Rev. 01, dated 11/27/2001

ESP-200001092. Rev. 03, dated 8/27/01

Drawings

61036, Rev. 62, "Schematic Diagram 208/120V Instrumentation Buses 11 & 12 Unit #1"

Simplified Drawing - Digital Feedwater Power Distribution System

Simplified Drawing - Digital Feedwater Power Scheme, Unit One Post 2002 RFO

Section 3.1

Failure to Properly Implement Station Emergency Operating Procedures

Issue Reports

IR200400053 23 Steam Generator Feed Pump Trip Resulting in Unit 2 Plant Trip, Root Causal

Analysis (Issue Report IR4-028-786)

IR200400056, Unplanned SIAS Actuation Following Unit 2 Trip, Root Causal Analysis (Issue

Report IR4-025-167)

IR4-025-059, Unit 2 Atmospheric Dump Valves Appear to Have Erroneous Open Signal From

RRS Channel X

IR4-025-165, -166 & -167, POSRC Recommendations During 1/24/04 Post-Trip Review

Meeting

IR4-028-786, Unit 2 Trip: Loss of 22 SGFP Resulted in Low SG Level Trip

A-6

Attachment

Procedures

AOP-7K, Overcooling Event in Mode One or Two (Unit 2), Rev. 2

AOP-7K, Overcooling Event in Mode One or Two, Basis Document (Unit 1 & 2), Rev. 1

EOP-0, Post-Trip Immediate Actions (Unit Two), Rev. 8

EOP-0, Post-Trip Immediate Actions Technical Basis Document, Rev. 14

EOP-1, Reactor Trip (Unit Two), Rev. 12

EOP-4, Excess Steam Demand Event (Unit Two), Rev. 15

NO-1-100, Conduct of Operations, Rev. 23

NO-1-111, Post-Trip Review, Rev. 6

NO-1-200, Control of Shift Activities, Rev. 29

NO-1-201, Calvert Cliffs Operating Manual, Rev. 15

Training Materials

Lesson Plan LOI-201-0-9, EOP-0 Post-Trip Immediate Actions Scope and Basis for the

Licensed Operator Initial Training Program

Lesson Plan LOR-63-1-02, ESFAS for the Licensed Operator Requalification Program

Lesson Plan LOR-201-0, 4-S-0-2, EOP-0, -1, and -4 Simulator Exercises for the Licensed

Operator Training Program

Lesson Plan LOR-201-0-8-02, EOP Basis Review for the Licensed Operator Training Program

Lesson Plan LOR-348-1-04, Calvert Cliffs Operating Experience, With Thermodynamic Review,

Unit 2 Trip 1/23/04

Other Documents

Unit 2 Control Room Operator Logs for January 23, 2004

Unit 2 Equipment Control Logs for January 23, 2004

Section 3.2

Failure to Have Procedures Required by Regulatory Guide 1.33

Design Bases

Regulatory Guide 1.33, Quality Assurance Program Requirements (Operation)

Calvert Cliffs - Unit 2 Technical Specifications

Procedures

OI-7, Reactor Regulating System, Rev. 9

NO-1-100, Conduct of Operations, Rev. 23

Training Materials

Reactor Regulating System Description No. 56, Rev. 0

LOI-58-1-13, Reactor Regulating System for the License Operator Initial Training Program

Simulator Operating Examinations for the Licensed Operator Training Program (various)

A-7

Attachment

Section 3.3

Simulator Fidelity Issues

Issue Reports

IR200400066, Simulator Fidelity Deficiency Root Causal Analysis (Issue Report IR4-020-078)

Procedures

AOP-7K, Overcooling Event in Mode One or Two (Unit 2), Rev. 2

Training Materials

Simulator Requal Session V, Scenario 03-03, Rapid Downpower with Expeditious Return to Full

Power

Lesson Plan LOR-348-1-04, Calvert Cliffs Operating Experience, With Thermodynamic Review,

Unit 2 Trip 1/23/04

Section 3.4

Failure to Comply with Station Work Control Procedures

Issue Reports

IR200400168, March 20 Unit 1 Reactor Trip Root Causal Analysis (Issue Report IR4-028-774)

IR4-000-887, Potential for Loss of AC Power to SG Level Control if Ground Occurs on 1Y09/10

IR4-028-847, 500KV Bus Voltage Recorder (1ER-101) Chart Paper Does Not Advance

Maintenance Orders

MO 1200400687, Replace 500KV Sensitive Voltage Recorder 1ER-101

Procedures

MN-1-100, Conduct of Maintenance, Rev. 22

MN-1-124, Conduct of Integrated Work Management, Rev. 6

NO-1-100, Conduct of Operations, Rev. 23

NO-1-117, Integrated Risk Management, Rev. 11

NO-1-200, Control of Shift Activities, Rev. 29

NO-1-201, Calvert Cliffs Operating Manual, Rev. 15

PR-1-103, Use of Procedures, Rev. 4

Section 4.0 Emergency Preparedness

Issue Reports

IR4-023-606, Event 4092, Reactor Trip on 1/23/04 Met the Conditions of ERPRP UE Due to

Excessive Steam Demand for 9 Minutes Following the Trip.

Procedures:

NO-1-201, Calvert Cliffs Operating Manual

EOP-4, Rev. 15, Excess Steam Demand Event

EOP-4 Basis Document

Calvert Cliffs EAL Technical Basis Manual, Rev. 10

A-8

Attachment

Other:

Information Notice 85-80,

Timely Declaration of an Emergency Class, Implementation of an

Emergency Plan, and Emergency Notification.

Information Notice 89-72,

Failure of Licensed Senior Operators to Classify Emergency

Events Properly.

A-9

LIST OF ACRONYMS

ABT

Automatic Bus Transfer

ADV

Atmospheric Dump Valve

AFAS

Auxiliary Feedwater Actuation System

ANSI

American National Standards Institute

ARC

Alarm Response Card

AV

Apparent Violation

CBP

Condensate Booster Pump

CCDP

Conditional Core Damage Probability

CCNPP

Calvert Cliffs Nuclear Power Plant

CDF

Core Damage Frequency

CR

Condition Report

CRS

Control Room Supervisor

CST

Condensate Storage Tank

CDF

Delta Core Damage Frequency

EDG

Emergency Diesel Generator

EOP

Emergency Operating Procedure

FRV

Feedwater Regulating Valve

FSAR

Final Safety Analysis Report

GPTU

Generation Protection and Test Unit

LER

Licensee Event Report

MR

Maintenance Rule

MSIV

Main Steam Isolation Valve

NCV

Non-Cited Violation

NLO

Non-Licensed Operator

NRC

Nuclear Regulatory Commission

OWC

Outage Work Control

PMT

Post Modification Test

PORC

Plant Operations Review Committee

QA

Quality Assurance

RCAR

Root Cause Analysis Report

RG

[NRC] Regulatory Guide

RGS

Responsible Group Supervisor

RHR

Residual Heat Removal

RRS

Reactor Regulating System

SGFP

Steam Generator Feedwater Pump

SDP

[NRC] Significance Determination Process

SGIS

Steam Generator Isolation Signal

SIAS

Safety Injection Actuation Signal

SRV

Safety Relief Valve

STAR

Stop, Think, Act, Review

TBV

Turbine Bypass Valve

TS

Technical Specification

UE

Unusual Event

UFSAR

Updated Final Safety Analysis Report

B-1

ATTACHMENT B

SPECIAL INSPECTION TEAM CHARTER

February 5, 2004

MEMORANDUM TO:

Richard J. Conte, Team Manager

Division of Reactor Safety

Alan J. Blamey, Team Leader

Special Inspection

FROM:

Wayne D. Lanning, Director

Division of Reactor Safety

SUBJECT:

SPECIAL INSPECTION CHARTER - CALVERT CLIFFS

NUCLEAR POWER PLANT UNIT 2

A special inspection has been established to inspect and assess the automatic reactor trip that

occurred at Calvert Cliffs Unit 2 on January 23, 2004. The special inspection will be conducted

onsite during the week of February 17, 2004, to allow Calvert Cliffs to complete the root cause

analysis for this event. The apparent cause review was completed prior to restart of the unit on

January 25, 2004. The team will include:

Manager:

Richard J. Conte, Chief, Operational Safety Branch

Leader:

Alan Blamey, Senior Operations Engineer

Members:

John Richmond, Resident Inspector at Susquehanna

Steve Barr, Operations Engineer

Herb Williams, Operations Engineer

Mark Giles, Senior Resident Inspector at Calvert Cliffs - Part Time

Eugene Cobey, Senior Reactor Analyst - Part Time

Unit 2 was operating at 100% power when the 22 steam generator feed pump spuriously

tripped. Operators were unable to reset and restart the pump, so they manually tripped the

reactor. Just prior to the manual trip, the reactor automatically tripped due to low steam

generator water level. The steam dump valves (atmospheric and condenser) fast opened as

designed, but did not modulate to properly control RCS temperature. Operators had difficulty

stabilizing RCS pressure such that a safety injection actuation signal occurred a second time

during the first two hours after the reactor trip. Additionally, operators were unable to reset the

safety injection actuation signal from the main control board, and some of the pressurizer back-

up heaters were previously removed from service due to a leaking pressurizer spray valve, a

known problem. The basis for this inspection is to independently evaluate equipment and

human performance, and to assess Constellations root cause evaluation and corrective

actions.

B-2

This special inspection was initiated in accordance with NRC Inspection Procedure 71153

Event Follow-up and NRC Management Directive 8.3, NRC Incident Investigation Program.

The decision to perform this special inspection was based on the initial risk assessment

coupled with the various complications that occurred following the trip. The inspection will be

performed in accordance with the guidance of NRC Inspection Procedure 93812, Special

Inspection, and the inspection report will be issued within 30 days following the exit meeting for

the inspection. If you have any questions regarding the objectives of the attached charter,

please contact me at (610) 337-5191.

Attachment:

Special Inspection Charter

Distribution:

H. Miller, RA/J. Wiggins, DRA

J. Trapp, DRP

M. Giles, DRP

N. Perry, DRP

E. Cobey, DRS

J. Jolicoeur, RI EDO Coordinator

R. Laufer, NRR

G. Vissing, PM, NRR

R. Clark/P. Tam, PM, NRR (Backup)

W. Lanning, DRS

R. Crlenjak, DRS

B. Holian, DRP

D. Screnci, ORA

B-3

Special Inspection Charter

Calvert Cliffs Nuclear Power Plant Unit 2

Automatic Reactor Trip - With Equipment and Potential Human

Performance Problems

The objectives of the inspection are to verify the facts and assess the issues surrounding the

automatic reactor trip that occurred at Calvert Cliffs Nuclear Power Plant Unit 2 on January 23,

2004. Specifically the inspection should:

1.

Independently evaluate the equipment and human performance issues to assess the

adequacy of the scope of Constellations investigation. This evaluation will:

Assess the adequacy of Constellations investigation and root cause evaluation

of the circumstances surrounding the cause of the automatic reactor trip and the

post trip response from the perspective of the equipment performance and

human performance.

Assess the adequacy of Constellations plans for corrective actions and extent of

condition review for the equipment and human performance issues.

2.

Independently evaluate the quality of operator response, and their implementation of

procedures, including Emergency Operating Procedures.

3.

Assess the adequacy of testing activities, prior to the event, to verify equipment

operability after maintenance or modification activities.

4.

Assess the adequacy of programs (i.e., workarounds, configuration control, corrective

action program) to address known equipment issues.

5.

Independently evaluate the risk significance of the event.

6.

Assess the effectiveness of related simulator and training issues.

7.

Document the inspection findings and conclusions in a special inspection report in

accordance with Inspection Procedure 93812 within 30 days of the exit meeting for the

inspection.

B2-1

ATTACHMENT B2

REVISED SPECIAL INSPECTION TEAM CHARTER

April 13, 2004

MEMORANDUM TO:

Richard J. Conte, Team Manager

Division of Reactor Safety

Alan J. Blamey, Team Leader

Special Inspection

FROM:

Wayne D. Lanning, Director

Division of Reactor Safety

SUBJECT:

SPECIAL INSPECTION CHARTER - CALVERT CLIFFS

NUCLEAR POWER PLANT UNIT 2 - SUPPLEMENTAL TO

INCLUDE UNIT 1 TRIP

A special inspection had been established to inspect and assess the automatic reactor trip that

occurred at Calvert Cliffs Unit 2 on January 23, 2004. As a result of a comparable conditional

core damage probability, and similar deterministic factors related to operator performance, the

Calvert Cliffs Unit 1 reactor trip of March 20, 2004, is now included in your teams review.

The special inspection will be conducted onsite on or about May 10, 2004, on a not to interfere

basis with the Unit 1 startup from a refueling outage scheduled to start April 9, 2004. This is to

allow Constellation Energy to complete the root cause analysis for Calvert Cliffs Unit 1

March 20, 2004, event. The apparent cause review was completed prior to restart of the unit on

March 22, 2004. The team remains the same per the previous charter but implementation

should be with less resources and less scope. For example since the post trip response for

Unit 1 was less severe than Unit 2, the main focus of the Unit 1 review will be the 20 minutes

before the trip when digital feedwater controls adversely responded to the loss of an instrument

bus.

Unit 1 was operating at 100% power when technicians inadvertently grounded an instrument

when reinstalling an instrument recorder. The grounding effected digital steam generator

feedwater control system, eventually causing a loss of feedwater and an almost simultaneous

automatic and manual reactor trips. Operators were unable to manually control the turbine

bypass valves and the main condenser was lost for 10 hours1.157407e-4 days <br />0.00278 hours <br />1.653439e-5 weeks <br />3.805e-6 months <br />. Just prior to the trip signal, the

operators dealt with diagnosing the effect of the ground on digital feedwater control. No safety

injection signals occurred and the post trip response was relatively benign, but there is a

question on how procedures were implemented in the 20 minutes prior to the trip. The risk for

this event increased due to the loss of the main condenser. The basis for this inspection is to

independently evaluate equipment and human performance, and to assess Calvert Cliffs root

cause evaluation and corrective actions.

B2-2

This special inspection was initiated in accordance with NRC Inspection Procedure 71153

Event Follow-up and NRC Management Directive 8.3, NRC Incident Investigation Program.

The decision to perform this special inspection was based on the initial risk assessment

coupled with our knowledge of preliminary performance deficiencies for the Unit 2 trip of

January 2004 and some uncertainty on how procedures were implemented in the 20 minutes

prior to the Unit 1 trip. The inspection will be performed in accordance with the guidance of

NRC Inspection Procedure 93812, Special Inspection, and the inspection report will be issued

within 30 days following the exit meeting for the inspection. If you have any questions

regarding the objectives of the attached charter, please contact me at (610) 337-5126.

Attachment:

Special Inspection Charter

Distribution:

H. Miller, RA/J. Wiggins, DRA

J. Trapp, DRP

M. Giles, DRP

N. Perry, DRP

E. Cobey, DRS

J. Jolicoeur, RI EDO Coordinator

R. Laufer, NRR

G. Vissing, PM, NRR

R. Clark/P. Tam, PM, NRR (Backup)

W. Lanning, DRS

R. Crlenjak, DRS

B. Holian, DRP

D. Screnci, ORA

R. Conte, DRS

A. Blamey, DRP

B2-3

Special Inspection Charter - Supplemental

Calvert Cliffs Nuclear Power Plant Unit 1

Automatic Reactor Trip - With Equipment and Potential Human

Performance Problems

The objectives of the inspection are to verify the facts and assess the issues surrounding the

manual and automatic reactor trip that occurred at Constellations Calvert Cliffs Nuclear Power

Plant Unit 1 on March 20, 2004. Specifically, the inspection should:

1.

Independently evaluate the equipment and human performance issues to assess the

adequacy of the scope of Constellations investigation. This evaluation will:

Assess the adequacy of Constellations investigation and root cause evaluation

of the circumstances surrounding the cause of the automatic reactor trip and the

post trip response from the perspective of the equipment performance and

human performance.

Assess the adequacy of Constellations plans for corrective actions and extent of

condition review for the equipment and human performance issues.

2.

Independently evaluate the quality of operator response, and their implementation of

procedures, including the hierarchal implementation of Emergency and Abnormal

Operating Procedures along with Alarm Response Procedures.

3.

Assess the adequacy of maintenance activities, prior to the event, to verify if an

adequate assessment of trip potential and risk was conducted prior to the instrument

recorder work.

4.

Independently evaluate the risk significance of the event.

5.

Assess the effectiveness of related training issues.

6.

Document the inspection findings and conclusions in a special inspection report in

accordance with Inspection Procedure 93812 within 30 days of the exit meeting for the

inspection.

C-1

Attachment

ATTACHMENT C

UNIT 2 SEQUENCE OF EVENTS

Unit 2 January 23, 2004 Excess Steam Demand Event

15:26.02

Initial Conditions

100% Reactor Power. 24 CWP secured for planned maintenance. RTCBs 1&5

open due to problems experienced earlier in the day during the performance of

an IM STP Reactor Reg System selected to Channel X.

15:26.37

22 SGFP Trips (With direction from the CRS, the CRO attempts multiple resets

of the 22 SGFP per plant stabilizing actions IAW AOP-3G. None of the resets

are successful and the CRS orders a manual reactor trip when S/G Low Level

Pre-Trips are received (coincident with -40 S/G levels per narrow range level

indication).)

15:27.48

RPS Steam Generator Low Level Channel A & D Trip. RTCBs 2, 3, 4, 6, 7, 8

open. RPS manual reactor trip from 1C05 due to action of RO.

15:28.20

ADVs and TBVs are not responding as designed as they are still full open and

RCS average temperature is well below 557oF.

15:28.26

All pressurizer backup and proportional heater banks automatically secure due to

pressurizer level falling below 101". The RO places all heater hand switches in

OFF shortly afterwards.

15:28.34

AFAS B actuation. ESFAS SIAS A & B actuation.

15:28.52

2B EDG, 21 & 22 LPSI pumps, 21 & 22 CS pumps, 21 HPSI pump all start.

15:28.53

22 Component cooling pump starts, 23 HPSI pump all start.

15:28.54

21 & 22 Boric acid pumps, 21/22/23 IRU, 24 CAC Fan all start.

15:28.57

ESFAS SGIS A & B Actuation.

15:28.59

Letdown secured. 2A & 2B EDG start.

15:29.00

21 & 22 MSIVs shut (with the MSIVs shut due to the SGIS actuation, the TBVs

are no longer contributing to the excess steam demand event. For approximately

the next seven minutes the RCS continues to cooldown at a rate of

approximately 160oF/hr.

15:29.13

Pressurizer level goes off-scale low.

C-2

Attachment

15:32.15

21B & 22A RCP secured in accordance with RCP Trip Strategy for SIAS

actuation.

15:37.00

The Quick Open Dump Signal from RRS is removed from both ADVs when the

TBO shifts the hand transfer valves in the 45 switchgear room to align ADV

control to 2C43. Over the next 32 minutes, an RCS heatup at approximately

57oF/hr takes place until RCS cold leg temperatures are restored to 515oF.

15:39.50

Pressurizer level returns to scale

15:47.30

The operating crew reduces AFW flow to each S/G from 300gpm to 150gpm.

Summary of EOP-O, Post Trip Immediate Actions:

Safety Function Status

Reactivity Control - Complete

Vital Auxiliaries - Complete

RCS Pressure and Inventory Control - Not Met

Core and RCS Heat Removal - Not Met

Containment Environment - Complete

Rad Levels External to Containment - Complete

Safety System Actuations

AFAS - Verified

SIAS - Verified

SGIS - Verified

15:55.00

EOP-1, Reactor Trip, is implemented from EOP-0. Upon entry, the crew

recognizes the high RCS pressure and the rapidly rising pressurizer level and

prepares to take stabilizing actions.

15:56.00

The RO takes manual control of the Main Spray Controller, 2HIC100, (which has

been greatly reduced due to only having one RCP operating in the spray line

loops) and places the output at approximately 30-35% to stop the RCS pressure

rise at 2335 psia. Subsequent minor manual Main Spray Controller

manipulations results in a stable RCS pressure at around 2318psia. Note - the

main spray valves, 1CV100E and 1CV100F, did not start to open until 2300psia

(based on a pressurizer controller setpoint of 2250 psia).

15:58.00

Due to the insurge from the RCS heatup, along with approximately 4100 gallons

of injection from the Charging system, Pressurizer level has reached ~210 and

the Pressurizer temperature has reached a minimum value of 514°F (saturation

for 771 psia).

15:59.00

The Pressurizer insurge continues as full Charging is still present at 128 GPM

and the 57°F/hr RCS heatup continues. At this point, due to the large volume of

cold water in the Pressurizer and the lack of full heater capability, RCS

pressure begins to rapidly drop from ~2318 to ~1800 psia over the next 22

minutes.

C-3

Attachment

16:01.46

22 & 23 charging pump are secured (H/S placed in PTL).

16:05.00

Based on Operator recall, the Main Spray Controller, 2HIC100, output signal is

lowered from 30 - 35% to approximately -2% (although 2HIC100 can be driven

to an output as low as -20%, an output of 0% should represent a signal at which

both Main Spray valves are full shut).

16:06.50

21 Charging pump is secured.

16:08.00

The RCS heatup is temporarily secured per the operating crews decision to hold

RCS cold leg temperature at 515oF.

16:09.00

Based on Operator recall, both Pressurizer Proportional Heaters are returned to

AUTO and Backup Heaters 22 and 24 are placed in ON. Backup Heater 24 only

has a capacity of 225 KW (normal capacity is 300 KW) due to a previous CMF

that had one bank of heaters removed from service. Backup Heaters 21 and 23

can not be returned to service at this time due to the active SIAS signals.

16:17.28

SIAS A is reset remotely from the Control Room. SIAS B can not be reset from

the Control Room due to a problem with the reset pushbutton.

16:27.36

SIAS B is reset locally from the Cable Spreading Room.

16:33.35

21 Charging Pump is started per OI-2A in an effort to restore Letdown to restore

Pressurizer level. For approximately the next five minutes, the Operating Crew

attempts to restore Letdown, but problems associated with the Control Room

position indication for one of the Letdown isolation valves, 2-CV-516, delays the

successful restoration.

16:38.50

21 Charging Pump is secured when the Operating Crew believes that the

Letdown isolation valve, 2-CV-516, is not opening when attempts are made

using the hand switch.

16:39.00

Based on Operator recall, Pressurizer Backup Heaters 21 and 23 are restored

and placed in ON now that SIAS has been reset and both heater breakers have

been closed locally.

16:45.30

A second heatup of the RCS at approximately 35°F/hr is commenced to return

RCS cold leg temperatures to the EOP-1 acceptable range of 525 - 535°F. The

heatup and resulting Pressurizer insurge contributes to RCS pressure lowering

from ~1800 psia to ~1750 psia over the next 30 minutes. The combination of

Letdown and the RCS heatup result in the RCS Pressure lowering to 1750 psia

and a second SIAS actuation.

16:48.29

21 Charging pump is started per OI-2A in a second effort to restore Letdown to

restore pressurizer level.

C-4

Attachment

16:48.40

Letdown is successfully placed in service and raised to approximately 105gpm

over the next nine minutes.

16:57.23

Letdown is maintained between 100 & 115gpm until about 17:14.34.

17:04.00

Per CRS/SM direction, the RO lowers the Main Spray Controller, 2HIC100,

output signal to -20% (lowest possible output signal) to ensure that the Main

Spray valves are fully closed in an attempt to minimize any leakby on the valves.

17:14.34

Letdown flow is reduced to ~70 GPM as the Operating Crew recognizes that

RCS pressure is steadily lowering and re-approaching the SIAS setpoint.

17:18.01

ESFAS SIAS B actuation (lose capability to use pressurizer backup heater 23).

17:18.02

ESFAS SIAS A actuation (lose capability to use pressurizer backup heater 21).

17:20.53

21 charging pump is secured.

17:49.00

After using procedure guidance from EOP-4 and blocking SIAS, the Operating

Crew resets SIAS A remotely from the Control Room. The decision to block and

reset SIAS is made in order to recover full Pressurizer heater capability in an

attempt to restore RCS pressure which has remained between 1750 and 1780

psia for the previous 50 to 60 minutes.

17:53.29

SIAS B is reset locally from the Cable Spreading Room.

17:58.00

Based on Operator recall, Pressurizer Backup Heaters 21 and 23 are restored

and placed in ON now that SIAS has again been reset and both heater breakers

have been closed locally. The Operating Crew now has full Pressurizer heater

output. The Operating Crew decides to not attempt to reinitiate Charging and

Letdown until RCS pressure reaches 2100 psia in order to assure that another

RCS depressurization does not occur.

18:22.00

Based on Operator recall, the Main Spray Controller, 2HIC100, is returned to

automatic control.

18:25.00

SGIS is reset using guidance from EOP-3.

18:29.20

AFAS A & B are reset in accordance with OI-32B.

18:32.29

21 Charging pump is started in preparation for restoring letdown.

18:33.35

Charging and Letdown is restored in attempt to return Pressurizer level to the

EOP-1 acceptable band of 130 to 180. Letdown is established at approximately

45 - 50 GPM.

19:26.00

The Operating Crew exits EOP-1 and implements OP-2 and OP-4.

C-5

Attachment

19:30.00

The 21B and 22A RCPs are restarted in accordance with OI-1A. The 21 AFW

pump is secured.

19:50.00

Both MSIVs are reopened in accordance with OP-2.

19:55.00

Secured 21 AFW pump.

20.00.00

RCS parameters have reached normal post-trip levels and are considered

steady state.