ML040280110

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IR 05000298-03-007, on 09/28/03 Through 12/31/03, for Cooper: Personnel Performance During Nonroutine Evolutions, Operability Evaluations, Postmaintenance Testing, Refueling and Outage Activities, Identification and Resolution of Problems
ML040280110
Person / Time
Site: Cooper Entergy icon.png
Issue date: 01/27/2004
From: Kennedy K
NRC/RGN-IV/DRP/RPB-C
To: Edington R
Nebraska Public Power District (NPPD)
References
IR-03-007
Download: ML040280110 (28)


See also: IR 05000298/2003007

Text

January 27, 2004

Randall K. Edington, Vice

President-Nuclear and CNO

Nebraska Public Power District

P.O. Box 98

Brownville, Nebraska 68321

SUBJECT: COOPER NUCLEAR STATION - NRC INTEGRATED INSPECTION

REPORT 50-298/03-07

Dear Mr. Edington:

On December 31, 2003, the U. S. Nuclear Regulatory Commission (NRC) completed an

inspection at your Cooper Nuclear Station. The enclosed integrated inspection report

documents the inspection findings which were discussed on January 8, 2004, with

Mr. S. Minahan, Acting Site Vice President, and other members of your staff.

This inspection examined activities conducted under your license as they relate to safety and

compliance with the Commissions rules and regulations and with the conditions of your license.

The inspectors reviewed selected procedures and records, observed activities, and interviewed

personnel.

Based on the results of this inspection, the NRC identified five findings that were evaluated

under the risk significance determination process as having very low safety significance

(Green). The NRC also determined that there were three violations associated with these

findings. These violations are being treated as noncited violations (NCVs), consistent with

Section VI.A of the Enforcement Policy. These NCVs are described in the subject inspection

report. If you contest the violation or significance of these NCVs, you should provide a

response within 30 days of the date of this inspection report, with the basis for your denial, to

the U.S. Nuclear Regulatory Commission, ATTN: Document Control Desk, Washington, DC

20555-0001, with copies to the Regional Administrator, U.S. Nuclear Regulatory Commission,

Region IV, 611 Ryan Plaza Drive, Suite 400, Arlington, Texas 76011-4005; the Director, Office

of Enforcement, U.S. Nuclear Regulatory Commission, Washington, DC 20555-0001; and the

NRC Resident Inspector at the Cooper Nuclear Station facility.

In accordance with 10 CFR 2.790 of the NRC's "Rules of Practice," a copy of this letter, its

enclosure, and your response will be made available electronically for public inspection in the

NRC Public Document Room or from the Publicly Available Records (PARS) component of

NRCs document system (ADAMS). ADAMS is accessible from the NRC Web site at

http://www.nrc.gov/reading-rm/adams.html (the Public Electronic Reading Room).

Nebraska Public Power District -2-

Should you have any questions concerning this inspection, we will be pleased to discuss them

with you.

Sincerely,

/RA/

Kriss M. Kennedy, Chief

Project Branch C

Division of Reactor Projects

Docket: 50-298

License: DPR-46

Enclosure:

NRC Inspection Report 05000298/2003007

w/attachment: Supplemental Information

cc w/enclosure:

Randall K. Edington, Vice President-Nuclear

Nebraska Public Power District

P.O. Box 98

Brownville, Nebraska 68321

John R. McPhail, General Counsel

Nebraska Public Power District

P.O. Box 499

Columbus, Nebraska 68602-0499

P. V. Fleming, Licensing and

Regulatory Affairs Manager

Nebraska Public Power District

P.O. Box 98

Brownville, Nebraska 68321

Michael J. Linder, Director

Nebraska Department of

Environmental Quality

P.O. Box 98922

Lincoln, Nebraska 68509-8922

Chairman

Nemaha County Board of Commissioners

Nemaha County Courthouse

1824 N Street

Auburn, Nebraska 68305

Nebraska Public Power District -3-

Sue Semerena, Section Administrator

Nebraska Health and Human Services System

Division of Public Health Assurance

Consumer Services Section

301 Centennial Mall, South

P.O. Box 95007

Lincoln, Nebraska 68509-5007

Ronald A. Kucera, Deputy Director

for Public Policy

Department of Natural Resources

205 Jefferson Street

Jefferson City, Missouri 65101

Jerry Uhlmann, Director

State Emergency Management Agency

P.O. Box 116

Jefferson City, Missouri 65101

Chief, Radiation and Asbestos

Control Section

Kansas Department of Health

and Environment

Bureau of Air and Radiation

1000 SW Jackson, Suite 310

Topeka, Kansas 66612-1366

Daniel K. McGhee

Bureau of Radiological Health

Iowa Department of Public Health

401 SW 7th Street, Suite D

Des Moines, Iowa 50309

William J. Fehrman, President

and Chief Executive Officer

Nebraska Public Power District

1414 15th Street

Columbus, Nebraska 68601

Chief Technological Services Branch

National Preparedness Division

Department of Homeland Security

Emergency Preparedness & Response Directorate

FEMA Region VII

2323 Grand Blvd., Suite 900

Kansas City, Missouri 64108-2670

Nebraska Public Power District -4-

Electronic distribution by RIV:

Regional Administrator (BSM1)

DRP Director (ATH)

Acting DRS Director (DDC)

Senior Resident Inspector (SCS)

Branch Chief, DRP/C (KMK)

Senior Project Engineer, DRP/C (WCW)

Staff Chief, DRP/TSS (PHH)

RITS Coordinator (NBH)

Jim Isom, Pilot Plant Program (JAI)

RidsNrrDipmLipb

Anne Boland, OEDO RIV Coordinator (ATB)

CNS Site Secretary (SLN)

Dale Thatcher (DFT)

W. A. Maier, RSLO (WAM)

R:\_CNS\2003\CN2003-07RP-SCS.wpd

RIV:RI:DRP/C SRI:DRP/C C:DRS/PSB C:DRS/OB C:DRP/C

SDCochrum SCSchwind TWPruett ATGody KMKennedy

E - KMKennedy E - KMKennedy MPShnnon for GWJohnston for /RA/

1/27/04 1/27/04 1/21/04 1/21/04 1/27/04

OFFICIAL RECORD COPY T=Telephone E=E-mail F=Fax

ENCLOSURE

U.S. NUCLEAR REGULATORY COMMISSION

REGION IV

Docket.: 50-298

License: DPR 46

Report No.: 05000298/2003007

Licensee: Nebraska Public Power District

Facility: Cooper Nuclear Station

Location: P.O. Box 98

Brownville, Nebraska

Dates: September 28 through December 31, 2003

Inspectors: S. Schwind, Senior Resident Inspector

S. Cochrum, Resident Inspector

P. Elkmann, Emergency Preparedness Inspector

P. Gage, Senior Operations Engineer

Approved By: K. Kennedy, Chief, Project Branch C, Division of Reactor Projects

Enclosure

SUMMARY OF FINDINGS

IR05000298/2003007; 09/28/03 - 12/31/03; Cooper Nuclear Station: Personnel Performance

During Nonroutine Evolutions, Operability Evaluations, Postmaintenance Testing, Refueling and

Outage Activities, Identification and Resolution of Problems.

The report covered a 3-month period of inspection by resident inspectors and announced

inspections by a Region IV emergency preparedness inspector and a senior operations

engineer. Three Green noncited violations and two Green findings were identified. The

significance of most findings is indicated by their color (Green, White, Yellow, Red) using

Inspection Manual Chapter 0609, Significance Determination Process. The NRC's program

for overseeing the safe operation of commercial nuclear power reactors is described in

NUREG-1649, Reactor Oversight Process, Revision 3, dated July 2000.

A. NRC-Identified and Self-Revealing Findings

Cornerstone: Initiating Events

failure to establish an adequate system operating procedure for the turbine oil

purification and transfer system during main turbine lube oil reservoir vapor extractor

maintenance. This caused an oil leak resulting in a fire.

This finding was greater than minor since inadequate system operating procedures

could be reasonably viewed a precursor to a significant event and, if left

uncorrected, could become a more significant safety concern. The finding was

determined have a very low safety significance (Green), since it did not affect the fire

mitigation defense in depth elements in Figure 4-1 of Inspection Manual 0609,

Significance Determination Process, Appendix F. In addition, it had crosscutting

aspects associated with problem identification and resolution, since a number of

opportunities were missed to identify the procedure error and prevent the

subsequent fire (Section 1R14).

  • Green. The failure to correctly rack in a breaker and to establish an adequate

postmaintenance test following corrective maintenance on Station Air Compressor B

was determined to be a self-revealing finding. The air compressor was rendered

inoperable following maintenance as a result of its breaker not being fully racked in,

and this condition was not discovered for 35 days.

This finding was more than minor since it was associated with the increased

likelihood of a loss of instrument air, which is an initiating event, but was determined

to have very low safety significance (Green), since it did not increase the likelihood

of a LOCA, did not contribute to both the likelihood of a reactor trip and the likelihood

that mitigation equipment or functions would not be available, and did not increase

the likelihood of a fire or internal flooding. In addition, this finding had crosscutting

aspects associated with human performance because personnel failed to specify a

postmaintenance test per station procedures and incorrectly racked in the breaker

(Section 1R19).

Enclosure

-2-

  • Green. A self-revealing finding was identified associated with the failure to evaluate

and take corrective actions for a fire on the Booneville 345 kV transmission line in

1997. This led to a similar fire on a transmission tower between the main

transformers and the main generator disconnect switches which induced a plant

transient in October 2003.

This finding was more than minor since it induced a plant transient. Given the

configuration of the switchyard, the fire did not pose a challenge to offsite power. It

was determined to have a very low safety significance (Green) since it did not affect

the fire mitigation defense in depth elements in Figure 4-1 of Inspection

Manual 0609, Significance Determination Process, Appendix F. In addition, it had

crosscutting aspects associated with problem identification and resolution since the

October 2003 fire and transient could have been avoided had the 1997 fire been

more thoroughly evaluated (Section 4AO2).

Cornerstone: Mitigating Systems

identified regarding the failure to take adequate corrective actions for degraded

conditions on the diesel fuel oil transfer system. In February 2003, corrosion

products from the fuel oil storage tank clogged the fuel oil strainer supplying

Emergency Diesel Generator 1. Corrective actions for that event failed to preclude

recurrence of the condition in November 2003.

This finding was more than minor since it was associated with the operability,

availability, and reliability of a mitigating system but was of very low safety

significance (Green), since it did not represent the actual loss of a safety function.

In addition, it had crosscutting aspects associated with problem identification and

resolution since the corrective action only addressed symptoms of the problem and

not the root cause, which was corrosion of the fuel oil storage tank (Section 1R15).

Cornerstone: Barrier Integrity

regarding the failure to establish an adequate procedure for operation of the residual

heat removal system. Within the guidance of the existing procedure, operators

inadvertently established a flow path between the reactor vessel and the condensate

storage tank which resulted in draining 300 gallons of reactor coolant to the

condensate storage tank.

This finding was more than minor, since it was associated with the cornerstone

attribute of procedure quality, but was determined to have very low safety

significance (Green), since the draindown was small and decay heat removal

capabilities were not challenged (Section 1R20).

Enclosure

-3-

B. Licensee-Identified Violation

A violation of very low safety significance, which was identified by the licensee, was

reviewed by the inspectors. Corrective actions taken or planned by the licensee have

been entered into the licensees corrective action program. This violation and corrective

action tracking numbers are listed in Section 4OA7 of this report.

Enclosure

REPORT DETAILS

The plant was operating at full power at the beginning of this inspection period. On

September 28, reactor power was reduced to approximately 25 percent as required by

Technical Specifications (TS) due to failure of a turbine trip device during testing. Full power

operations were resumed on October 1. On October 16, reactor power was reduced to

approximately 65 percent in response to a fire reported underneath a main turbine bearing. Full

power operations were resumed on October 17 following completion of firefighting activities and

a damage assessment. On October 28 the reactor was manually scrammed due to a fire

reported on a tower adjacent to the 345 kV switchyard. Full power operations resumed on

November 3 following completion of repairs. One November 28 the reactor automatically

scrammed on low reactor pressure vessel (RPV) level due to an unexpected decrease in

reactor feed pump speed. Full power operation resumed on December 13 following

troubleshooting on the reactor feed pump.

1. REACTOR SAFETY

Cornerstones: Initiating Events, Mitigating Systems, Barrier Integrity, Emergency

Preparedness

1R01 Adverse Weather Protection

a. Inspection Scope

The inspectors selected four samples representing the review of preparations/protection

for cold weather conditions on two risk significant systems. The four samples included:

  • A review of maintenance work orders completed in order to prepare the systems

for possible freezing temperatures

  • A review of deficiency tags and condition reports associated with heat tracing

and other cold weather protection measures to determine their impact on the

systems

  • A walkdown of the 250 vdc station batteries to determine if room temperatures

were being maintained above 70EF

  • A walkdown of the environmental controls in the intake structure to verify that the

licensee had completed the required actions identified in the work orders

The two systems chosen for this inspection included:

  • Portions of the 250 vdc system including the 250 vdc station batteries.
  • The intake structure, including the sluice gates on the ice control tunnel, the ice

deflector, and environmental controls in the service water pump room

Enclosure

-2-

b. Findings

No findings of significance were identified.

1R04 Equipment Alignment

a. Inspection Scope

Partial Equipment Alignment Inspections

The inspectors performed one partial equipment alignment inspection. The walkdown

verified that the critical portions of the selected systems were correctly aligned per the

system operating procedures (SOPs). The following system was included in the scope

of this inspection:

maintenance on October 27. The walkdown included portions of the system in the

diesel building, the Division I critical switchgear room, and the control room.

Complete Equipment Alignment Inspections

On October 24, the inspectors performed one complete system alignment inspection of

the standby liquid control (SLC) system. The inspectors verified that the system was in

the appropriate configuration per the SOP and that it was installed and capable of

performing its design functions as described in the Updated Final Safety Analysis

Report (USAR). A review of maintenance work orders and corrective actions

documents for the past 12 months was also performed. A walkdown of the system was

performed to assess material condition such as system leaks and housekeeping issues

that could adversely affect system operability.

b. Findings

No findings of significance were identified.

1R11 Licensed Operator Requalification

a. Inspection Scope

The inspector conducted an in-office review of the annual operating examination test

results for 2002. Since this was the first half of the biennial requalification testing cycle,

the licensee had not yet administered the written examination. These results were

assessed to determine if they were consistent with NUREG 1021 guidance and Manual

Chapter 0609, Appendix I, Operator Requalification Human Performance Significance

Determination Process, requirements. This review included examination test results for

7 crews, which included 42 licensed individuals.

Enclosure

-3-

b. Findings

No findings of significance were identified.

1R12 Maintenance Rule Implementation

a. Inspection Scope

The inspectors reviewed two equipment performance issues to assess the licensees

implementation of their maintenance rule program. The inspectors verified that

components that experienced performance problems were properly included in the

scope of the licensees maintenance rule program, and the appropriate performance

criteria were established. Maintenance rule implementation was determined to be

adequate if it met the requirements outlined in 10 CFR 50.65 and Administrative

Procedure 0.27, Maintenance Rule Program, Revision 15. The inspectors reviewed

the following equipment performance problems:

  • Failure of Steam Tunnel Fan Cooling Unit CNS-9-HV-FCU-FC-R-1KA on October 17

(Notification 10276549)

  • Failure of Supply Fan HV-DG-1D to automatically start during testing of EDG 2 on

October 29 (Notification 10278560)

b. Findings

No findings of significance were identified.

1R13 Maintenance Risk Assessments and Emergent Work Evaluation

a. Inspection Scope

The inspectors reviewed four risk assessments for planned or emergent maintenance

activities to determine if the licensee met the requirements of 10 CFR 50.65(a)(4) for

assessing and managing any increase in risk from these activities. Evaluations for the

following maintenance activities were included in the scope of this inspection:

  • Emergency Station Service Transformer outage due to maintenance on the 69 kV

transmission line by Omaha Public Power District on October 15

  • EDG 2 fuel oil strainer planned maintenance on November 24 (Work

Order 4346703)

Enclosure

-4-

  • Station Service Air Compressor (SAC) B 480 V breaker found not fully racked in,

which rendered the compressor inoperable from November 10 through December 15

(Notification 10285815)

b. Findings

No findings of significance were identified.

1R14 Personnel Performance During Nonroutine Evolutions

a. Inspection Scope

For the nonroutine events described below, the inspectors reviewed operator logs, plant

computer data, and strip charts to determine what occurred, how the operators

responded, and if the response was in accordance with plant procedures:

  • On October 16, the inspectors responded to the control room shortly after a fire was

reported in the turbine building. The inspectors observed and evaluated the actions

by the control room, actions required by procedures, and monitoring of plant

conditions during this event.

  • On October 28, the inspectors responded to the control room shortly after operators

manually scrammed the reactor in response to a fire on a transmission tower

between the main transformers and the main generator disconnect switches. The

inspectors observed and evaluated the followup actions by the operators, action

required by procedures, and monitoring of plant conditions during this event. This

event is discussed in Sections 4OA2 and 4OA7 of this report.

b. Findings

Fire in Turbine Building

Introduction. A Green noncited violation (NCV) of TS 5.4.1(a) was identified for a failure

to establish an adequate SOP for the turbine oil purification and transfer system during

main turbine lube oil reservoir vapor extractor maintenance, which caused an oil leak

resulting in a fire.

Description. On October 16 at 12:19 p.m., a station operator discovered a small fire

located beneath Main Turbine Bearing 1. The operator had been sent inside the main

turbine shield wall to evaluate earlier reports of smoke observed by a remote camera in

the turbine building. Control room operators immediately entered Emergency Procedure

5.4FIRE, General Fire Procedure, Revision 5. The fire brigade responded, but their

initial attempts to extinguish the fire with portable CO2 and dry chemical extinguishers

were unsuccessful. At 12:30 p.m., a Notice of Unusual Event was declared, since the

duration of the fire had exceeded 10 minutes. The fire was extinguished using water

and foam at 1:36 p.m. No offsite assistance was requested. Due to elevated dose

Enclosure

-5-

rates in the fire affected area and the extended time required to fight the fire, reactor

power was reduced to 65 percent to maintain the fire brigades dose as low as is

reasonably achievable. Damage was limited to discoloration of piping underneath the

affected area. There were no injuries and the Notice of Unusual Event was terminated at

3:41 p.m. after the licensee determined that the fire was completely extinguished and

there was no risk of re-ignition.

The licensee determined that the fire was caused by an oil leak from the seals of the

Main Turbine 1 bearing, which came into contact with hot piping in the area. Securing

both turbine lube oil vapor extractors allowed oil to leak out of the journal bearing seals.

The vapor extractors are designed to maintain a slightly negative pressure on the

turbine bearing oil return system, which prevents oil from leaking out of the bearing

seals. Both vapor extractors were secured for planned maintenance per SOP 2.2.81,

Turbine Oil Purification and Transfer System, Revision 29, and were out of service for

approximately 6 hours6.944444e-5 days <br />0.00167 hours <br />9.920635e-6 weeks <br />2.283e-6 months <br />. They had been restored to service 45 minutes prior to the fire.

Multiple reports were made to the control room of an oil mist on the turbine deck prior to

restoring the vapor extractors to service.

In 1986, a design modification added a redundant vapor extractor as recommended by

Westinghouse Bulletin 8504. This bulletin also recommended that the main turbine be

shutdown if both vapor extractors were out of service. The Westinghouse vendor

manual recommended limiting the time both vapor extractors are out of service to the

time necessary to transfer operation from one to the other. The recommendations of

the bulletin were translated into Design Change 86-84, Installation of Redundant Vapor

Extractor, which stated that a failure of the vapor extractors would require shutdown of

the turbine generator;, however, SOP 2.2.81 was changed in July 2002 to allow

operation of the main turbine with both vapor extractors secured. This condition was

allowed for an unspecified period of time.

Analysis. This finding had crosscutting aspects associated with problem identification

and resolution. This assessment was based on industry operating experience that was

provided to the work planner and discussed at the plan-of-the-day meeting on

October 15, indicating that fire events had occurred at other nuclear power stations

when both lube oil vapor extractors were secured during turbine operation. Also, there

were several opportunities to address the oil leak prior to the fire based on multiple

reports made to the control room of an oil mist on the turbine deck. This assessment

was also based on the licensees root cause investigation, which determined that a

number of opportunities were missed to identify the error in SOP 2.2.81 during the

procedure change review.

This finding was more than minor, since it affected the Initiating Events Cornerstone, the

inadequate SOPs could be reasonably viewed as a precursor to a significant event and,

if left uncorrected, it could become a more significant safety concern. Inspection

Manual Chapter 0609, Significance Determination Process, Appendix F, was used to

assess the safety significance of this finding. Phase 1 of the significance determination

Enclosure

-6-

process (SDP) concluded that the finding was of very low safety significance (Green),

since it did not affect the fire mitigation defense in depth elements in Figure 4-1.

Enforcement. TS 5.4.1(a) requires that licensees establish, implement, and maintain

written procedures recommended in Regulatory Guide 1.33, Revision 2, Appendix A,

February 1978. Appendix A recommends operating procedures for the turbine-

generator system. Contrary to the above, adequate operating procedures were not

established for the turbine-generator system, since the licensees procedures for the

operation of the lube oil vapor extractors did not minimize the time that both vapor

extractors could be secured and allowed turbine-generator operation with both vapor

extractors secured for an unspecified period of time. This finding is being treated as an

NCV (50-298/0307-01) consistent with Section VI.A of the NRC Enforcement Policy.

The licensee entered this issue into their corrective action program (CAP) as significant

condition report (SCR) 2003-1808. Procedure 2.2.81 was revised to correct the

procedural inadequacy.

1R15 Operability Evaluations

a. Inspection Scope

The inspectors reviewed four operability determinations regarding mitigating system

capabilities to ensure that the licensee properly justified operability and that the

component or system remained available so that no unrecognized increase in risk

occurred. These reviews considered the technical adequacy of the licensees evaluation

and verified that the licensee considered other degraded conditions and their impact on

compensatory measures for the condition being evaluated. The inspectors referenced

the USAR, TS, and the associated system design criteria documents to determine if

operability was justified. The inspectors reviewed the following equipment conditions

and associated operability evaluations:

  • Inservice Test (IST) failure of Diesel Fuel Oil Transfer Pump A due to debris buildup

on the inlet strainer for Fuel Oil Day Tank 2 (Notification 10279881)

10277107)

  • Inadvertent removal of riprap during dredging operations adjacent to the intake

structure (Notification 10280113)

  • Failure of the main turbine mechanical trip device on high reactor vessel level during

testing (Notification 10272894)

b. Findings

Introduction: A Green NCV was identified regarding the failure to take adequate

corrective actions for degraded conditions on the diesel fuel oil transfer system.

Enclosure

-7-

Description: On November 5, Fuel Oil Transfer Pump A failed to develop the required

flowrate during Surveillance Procedure 6.1DG.401, Diesel Generator Fuel Oil Transfer

Pump IST Flow Test (Div 1), Revision 13. Troubleshooting indicated that the fuel oil

strainer on the inlet float valve for Fuel Oil Day Tank 1 had accumulated sufficient

corrosion product debris from the fuel stream as to restrict flow. The licensee cleaned

the strainer, and the transfer pump subsequently passed the surveillance test. In

addition, an operability determination was performed which concluded that the corrosion

products were being transported from the fuel oil storage tank, which was a slow

process that could be managed through the preventive maintenance (PM) program.

The operability determination also stated that, if the strainer became clogged during

diesel operation, there would be a sufficient volume of fuel in the day tank to allow for

cleaning or replacement of the strainer without interruption of engine operation.

The diesel fuel oil system at Cooper Nuclear Station consists of two underground

storage tanks, two transfer pumps, and a day tank for each EDG. Each transfer pump

takes a suction approximately 3 inches from the bottom of its respective storage tank,

and the pump discharge headers are normally cross-connected. Although either

transfer pump can supply fuel to either day tank, a single transfer pump does not have

sufficient capacity to supply fuel to two fully loaded EDGs. Therefore, each transfer

pump is required to support operability of its respective EDG.

A similar event occurred in February 2003, when Fuel Oil Transfer Pump A failed a

surveillance test due to corrosion products in the strainer. The licensees response to

that event was similar; the strainer was cleaned and an operability determination was

performed which concluded that the debris buildup could be managed by the PM

program. The PM to clean and inspect the strainer was increased from a 72-week

frequency to a 24-week frequency and the contents of both fuel oil storage tanks were

filtered in May 2003 in an attempt to reduce the amount of sediment in the tanks. Based

on trend data from past engine runs and the current condition of the fuel oil storage

tanks, the licensee concluded that the fuel strainer would become blocked by debris

after approximately 30 to 35 hours4.050926e-4 days <br />0.00972 hours <br />5.787037e-5 weeks <br />1.33175e-5 months <br /> of run time. The 24-week PM frequency was

considered adequate to prevent this. At the time of the failure in November, EDG 1 had

approximately 40 hours4.62963e-4 days <br />0.0111 hours <br />6.613757e-5 weeks <br />1.522e-5 months <br /> of run time and the strainer clogged prior to the end of the

24-week maintenance interval.

Analysis: This finding had crosscutting aspects associated with problem identification

and resolution. This assessment was based on the fact that the licensee had performed

an analysis that indicated the failure would repeat itself at approximately 30 to 35 hours4.050926e-4 days <br />0.00972 hours <br />5.787037e-5 weeks <br />1.33175e-5 months <br />

of engine run time, yet the corrective action for the February 2003 failure was to change

the PM frequency based on calendar time rather than engine run time. In addition, the

corrective actions primarily dealt with the symptoms caused by increased fuel storage

tank corrosion, not the root causes. This approach also created an operator

workaround, since manual action would be required to maintain an EDG operable during

its 7-day mission time.

Enclosure

-8-

This finding affected the Mitigating Systems Cornerstone and was considered more than

minor, since it was associated with the operability, availability, and reliability of a

mitigating system. Based on the results of an SDP Phase 1 evaluation, this finding was

determined to have very low safety significance, since it did not represent the actual loss

of a safety function.

Enforcement: Appendix B, Criterion XVI, of 10 CFR Part 50 states that measures shall

be established to assure that conditions adverse to quality are promptly identified and

corrected. In the case of significant conditions adverse to quality, the measures shall

assure that the cause of the condition is determined and corrective actions taken to

preclude repetition. Failure of Fuel Oil Transfer Pump A was considered a significant

condition adverse to quality, since it adversely impacted the ability of a risk significant

safety system to perform as designed. Corrective actions for the transfer pump failure

in February 2003 failed to preclude an additional failure in November 2003. This

violation of 10 CFR Part 50, Appendix B, Criterion XVI, is being treated as an NCV,

consistent with Section VI.A of the NRC Enforcement Policy (50-298/0307-02). The

licensee entered this issue into their CAP as SCR 2003-1876.

1R16 Operator Workarounds

a. Inspection Scope

The inspectors reviewed eight operator workaround items to evaluate their cumulative

affect on mitigating systems and the operators ability to implement abnormal or

emergency procedures. In addition, open operability determinations and selected

condition reports were reviewed and operators were interviewed to determine if there

were additional degraded or nonconforming conditions that could complicate the

operation of plant equipment.

b. Findings

No findings of significance were identified.

1R19 Postmaintenance Testing

a. Inspection Scope

The inspectors reviewed or observed seven selected postmaintenance tests to verify

that the procedures adequately tested the safety function(s) that were affected by

maintenance activities on the associated systems. The inspectors also verified that the

acceptance criteria were consistent with information in the applicable licensing basis and

design basis documents and that the procedures were properly reviewed and approved.

Postmaintenance tests for the following maintenance activities were included in the

scope of this inspection:

Enclosure

-9-

  • Replacement of scram solenoid pilot valves from September 12 to October 28 (Work

Order 432210)

  • Leak repair on moisture separator for Station Air Compressor (SAC) B on

November 10 (Work Order 4338511)

  • Cleaning and inspection of Diesel Fuel Oil Strainer DGDO-STRN-FLTV11 on

November 24 (Work Order 4343940)

741AV on December 11 (Work Order 4172876)

  • Cleaning and inspection of Service Water Strainer A on December 16 (Work

Order 4323349)

  • Control board replacement in 250 vDC Battery Charger A on December 17 (Work

Order 4314331)

b. Findings

Introduction: A Green finding was identified regarding the failure to correctly rack in a

breaker and to specify an adequate postmaintenance test following corrective

maintenance on SAC B.

Details: On November 10, SAC B was removed from service to repair a leak on the

moisture separator. The tagging order specified that the breaker for the compressor

(EE-CB-480G) be racked to the test position and specified the restoration configuration

as racked in. The corrective maintenance on the moisture separator was completed,

the tags were cleared, and the system was restored to a standby configuration. Work

Order 4338511 did not specify any postmaintenance test following this job.

SAC B remained in standby until December 15 when operators attempted to start it as

part of their normal equipment rotation routine. The compressor failed to start and,

upon further investigation, it was determined that Breaker EE-CB-480G was not fully

racked in. Once the breaker had been fully racked in, operators were successful in

starting SAC B.

Analysis: This finding had crosscutting aspects associated with human performance.

This assessment was based on the fact that personnel failed to follow station

procedures regarding work planning and control. Administrative Procedure 0.40, "Work

Control Program," Revision 39, Section 6.7.1, requires that postmaintenance testing be

specified to demonstrate satisfactory completion of work and verify that no new

deficiencies have been created. This was not done. In addition, station personnel failed

to correctly restore the breaker for SAC B following maintenance.

Enclosure

-10-

This finding affected the Initiating Events Cornerstone and was considered more than

minor, since it was associated with the increased likelihood of a loss of instrument air,

which is an initiating event. Based on the results of an SDP Phase 1 evaluation, this

finding was determined to have very low safety significance, since it did not increase the

likelihood of a LOCA, a fire, or internal flooding and did not contribute to either the

likelihood of a reactor trip or that mitigation equipment or functions would not be

available.

Enforcement: Although SAC B is a risk significant component, it is not considered

safety related. Therefore, no violation of NRC requirements was identified. The

licensee entered this issue into their CAP as Notification 10285815.

1R20 Refueling and Outage Activities

a. Inspection Scope

The inspectors observed outage-related activities during Forced Outage 03-05.

Activities included the scram recovery actions following a manual reactor scram on

October 28, plant cooldown, placing the residual heat removal (RHR) system in the

shutdown cooling mode of operation, and startup activities.

b. Findings

Introduction: An inadequate procedure, which led to an RPV draindown event while

placing RHR in shutdown cooling, was considered to be a self-revealing, Green NCV.

Description: On October 29, operators were in the process of flushing Division 1 of the

RHR system in preparation for placing it in shutdown cooling. During the flushing and

venting process, SOP 2.2.69.2, RHR System Shutdown Operations, Revision 42,

directed operators to open the RHR shutdown cooling condensate supply valves, RHR-

96 and RHR-97, and then to open the inboard and outboard shutdown cooling isolation

valves, RHR-MO-17 and RHR-MO-18. This established a drain path from the RPV to

the condensate system and, subsequently, to the condensate storage tank (CST).

Control room operators noted that RPV level decreased by 1.5 inches during this

evolution and that RHR-96 and RHR-97 were hot, which indicated they were passing

reactor coolant. At this point, the drain path was isolated. It was estimated that 300

gallons were inadvertently transferred from the reactor coolant system to the CST at a

flow rate of approximately 60 gallons per minute.

Analysis: This finding affected the Barrier Integrity Cornerstone since it represented the

unintentional bypass of two fission product barriers (reactor coolant system and

containment system) and was more than minor, since it was associated with the

cornerstone attribute of procedure quality. This finding degraded the safety of a

shutdown reactor; therefore, MC 0609, Appendix G, "Shutdown Operations Significance

Determination Process," was used to assess its signficance. A quantitative assessment

was not performed since an RPV level change of 1.5 inches does not represent a loss of

Enclosure

-11-

control. Pages T-14 through T-16 of Appendix G were used to assess the significance

since the reactor was in hot shutdown, time to boil was less than 2 hours2.314815e-5 days <br />5.555556e-4 hours <br />3.306878e-6 weeks <br />7.61e-7 months <br />, and initial

conditions for RHR operations had been met. The guidelines for core heat removal,

inventory control, and power availability were met. In addition, the containment

guidelines were met, since the automatic containment isolation function for RHR on low

RPV level (7.81 inches on the wide-range instrument) was operable. Although this

finding did increase the likelihood of a loss of reactor coolant inventory, a Phase 2

analysis was unnecessary because level instrumentation was unaffected and this was

not considered rapid loss of inventory. Based on these results, this finding was

determined to have very low safety significance.

Enforcement: TS 5.4.1(a) requires written procedures to be established, implemented,

and maintained as recommended by Regulatory Guide 1.33, Revision 2, Appendix A,

February 1978. Appendix A recommends operating procedures for the shutdown

cooling system. SOP 2.2.69.2, RHR System Shutdown Operations, Revision 42, did

not meet this requirement in that it directed operators to align the system in a manner

which established a drain path from the RPV to the CST. This violation is being treated

as an NCV (50-298/0307-03) consistent with Section VI.A of the NRC Enforcement

Policy. The licensee entered these issues into their CAP as Notifications 10249930 and

10249920.

1R22 Surveillance Testing

a. Inspection Scope

The inspectors observed or reviewed the following three surveillance tests to ensure that

the systems were capable of performing their safety function and to assess their

operational readiness. Specifically, the inspectors verified that the following surveillance

tests met TS requirements, the USAR, and licensee procedural requirements:

  • 15.TG.302, Main Turbine Trip Functional Test, Revision 5, performed on

September 29

  • 6.2ADS.303, ADS [alternate depressurization system] Logic System Functional

Test (Div 2), Revision 7, performed on October 17

  • SLC pump discharge relief valve testing under Work Orders 4285654 and 4338440.

b. Findings

No findings of significance were identified.

Enclosure

-12-

1R23 Temporary Plant Modifications

a. Inspection Scope

The inspectors reviewed Temporary Configuration Change 4347948, dated

December 2, 2003, which installed temporary diagnostic equipment in the controller

cabinet for Reactor Feed Pump B and installed an additional supervisory alarm for the

feed pump turbine in the control room. The inspectors verified that the change did not

require NRC approval prior to implementation and that adequate controls on the

installation existed.

b. Findings

No findings of significance were identified.

1EP4 Emergency Action Level and Emergency Plan Changes

a. Inspection Scope

The inspector performed an in-office review of Revision 44 to the Cooper Nuclear

Station Emergency Plan, submitted September 17, 2003. This revision:

  • Clarified responsibility for on-shift dose assessment
  • Revised documentation requirements for Letters of Agreement
  • Revised the description of the conduct of emergency response organization training
  • Updated titles

The revision was compared to its previous version, to the criteria of NUREG-0654,

Criteria for Preparation and Evaluation of Radiological Emergency Response Plans and

Preparedness in Support of Nuclear Power Plants, Revision 1, and to the requirements

of 10 CFR 50.47(b) and 50.54(q) to determine if the revision decreased the

effectiveness of the plan. The inspector completed the required one sample during this

inspection.

b. Findings

No findings of significance were identified.

Enclosure

-13-

1EP6 Drill Evaluation

a. Inspection Scope

The inspectors observed the licensee perform an emergency preparedness drill on

December 17. Observations were conducted in the control room, technical support

center, and emergency operations facility. During the drill, the inspectors assessed the

licensees performance related to classification, notification, and protective action

recommendations. Following the drill, the inspectors reviewed the licensees critique to

determine if issues were appropriately identified and documented. The following

documents were reviewed during this inspection:

b. Findings

No findings of significance were identified.

4. OTHER ACTIVITIES (OA)

4OA1 Performance Indicator (PI) Verification

a. Inspection Scope

The inspectors sampled licensee PIs listed below for the period October 01, 2002,

through September 30, 2003. The definitions and guidance of NEI 99-02, Regulatory

Assessment Indicator Guideline, Revision 2, were used to verify the licensees basis for

reporting each data element in order to verify the accuracy of PI data reported during

the assessment period. Licensee PI data were reviewed against the requirements of

Procedures 0-PI-01, Performance Indicator Program, Revision 13.

Reactor Safety Cornerstone

The inspectors reviewed a selection of licensee event reports (LERs), portions of

operator log entries, monthly reports, and PI data sheets to determine whether the

licensee adequately collected, evaluated, and distributed PI data for the period

reviewed.

Enclosure

-14-

b. Findings

No findings of significance were identified.

4OA2 Identification and Resolution of Problems

.1 Reactor Scram Due to a Fire on a 345 kV Transmission Tower

a. Inspection Scope

The inspectors performed a review of SCR 2003-1844, which documented the root

cause investigation into a fire on a wooden transmission tower between the main

transformers and the main generator disconnect switches. The inspectors also

conducted interviews with selected licensee engineers and the personnel who

conducted the investigation. Other aspects of this event are discussed in Section 4OA7

of this report.

b. Findings

Introduction: A Green, self-revealing finding was identified associated with the failure to

evaluate and take corrective actions for a fire on the Booneville 345 kV transmission

line. This led to a similar fire on a transmission tower between the main transformers

and the main generator disconnect switches, which induced a plant transient.

Description: On October 28 at 1:30 a.m., control room operators were notified by

security of a fire on the crossarm of a wooden 345 kV transmission tower adjacent to

the 345 kV switchyard. The tower supported the main generator output lines and was

located between the main transformers and the main generator disconnect switches. At

1:45 a.m. operators began a rapid shutdown of the plant in anticipation of losing the

main generator output line. In addition, the Emergency Response Organization was

activated as a precautionary measure, even though no emergency declaration was

required or had been made. At 1:59 a.m., operators manually scrammed the reactor

when the crossarm of the tower failed, allowing one phase of the main generator output

lines to fall. This phase remained suspended above the ground and no generator

grounds or phase-to-ground arcing occurred. The inspectors arrived in the control room

at approximately 2:20 a.m. to observe operator response to the reactor scram. The fire

was extinguished and the plant was stable in Mode 3 by 6:47 a.m.

The licensees root cause investigation concluded that the fire on the crossarm was

caused by the lack of grounding straps on the crossarm insulators. In addition, the

crossarm showed signs of age-related deterioration due to the loss of wood

preservative. This was evidenced by moss growth on the crossarm and cracks in the

wood. These factors, combined with light rain several hours prior to the event,

established a high resistance current path across one of the insulators, through the

wooden crossarm, and across the tower poles to ground. This high resistance current

path eventually heated the wood sufficiently to ignite the crossarm.

Enclosure

-15-

The licensee evaluated the extent of this condition and determined that the Booneville

345 kV transmission line had a similar configuration as the main generator output line.

The insulators on the wooden tower supporting this line were not properly grounded;

however, the wooden crossarm was in better material condition since it had been

replaced in 1997 following a similar fire. The licensee entered that event into their CAP

as Department Disposition 2-18586; however, no root cause investigation or extent of

condition evaluation was performed and the only corrective action implemented was to

repair the damaged crossarm.

Following the more recent fire event, the licensee implemented a number of corrective

actions, including a modification to the main generator output line which removed the

wooden transmission tower and the installation of grounding straps on the wooden tower

supporting the Booneville 345 kV transmission line.

Analysis: This finding had crosscutting aspects associated with problem identification

and resolution. This assessment was based on the licensees failure to question the

causes and extent of condition regarding a similar fire event in 1997. A thorough

evaluation of that fire could have prevented the fire in 2003 and the associated plant

transient.

This finding was more than minor, since it affected an Initiating Events Cornerstone

attribute by increasing the likelihood of a transient. Although this fire induced a

transient, it did not pose a challenge to offsite power due to the configuration of the

switchyard and did not challenge mitigating equipment. Inspection Manual

Chapter 0609, Significance Determination Process, Appendix F, was used to assess

the safety significance of this finding. Phase 1 of the SDP concluded that the finding

was of very low safety significance (Green), since it did not affect the fire mitigation

defense in depth elements in Figure 4-1.

Enforcement: The portion of the electrical distribution system affected by this fire was

nonsafety-related; therefore, no violation of NRC requirements was identified. This

finding was entered into the licensees CAP as SCR 2003-1844.

.2 Cross-References to Problem Identification and Resolution Findings Documented

Elsewhere

Section 1R14 describes that the licensee missed a number of opportunities to identify

procedure errors, which resulted in a turbine lube oil leak.

Section 1R15 describes that the licensees corrective actions dealt primarily with the

symptoms rather than the root causes for a clogged diesel fuel oil strainer. This

condition repeated itself 9 months later.

Section 4OA2 describes that the licensee failed to thoroughly evaluate a fire on a

345 kV transmission line in 1997. This contributed to a similar fire in 2003, which

induced a plant transient.

Enclosure

-16-

4OA3 Event Followup

.1 (Closed) LER 50-298/03-001-00 Inadequate Communication Results if Both Diesel

Generators Inoperable Simultaneously

On February 28, 2003, the licensee declared EDG 2 inoperable due to a question

regarding the qualified life of an Agastat time delay relay in the diesel room ventilation

system. This ventilation system was required to support operability of EDG 2. EDG 1

had previously been declared inoperable on February 24 due to a clogged strainer in the

fuel oil system. The reactor was in cold shutdown (Mode 4) at the time both EDGs were

inoperable. During this period of time, only one EDG was required to be operable per

TS and at no time were both EDG simultaneously unable to perform their safety

function. The time delay relay was replaced on February 28 and EDG 2 was declared

operable. On March 2, maintenance on the fuel oil system was complete and EDG 1

was declared operable. The enforcement aspects associated with this event are

discussed in Section 1R15 of this report and Section 4OA2 (Example 2) of NRC

Inspection Report 05000298/2003002. This LER is closed.

.2 (Closed) LER 50-298/03-005-00 Turbine Trip Failure During Testing Due to Ester

Contamination of Turbine Lube Oil

On September 28, during turbine trip testing, the turbine trip block failed to actuate as

designed while testing the solenoid and low vacuum trip portions of the device.

Troubleshooting indicated binding in the auto stop oil dump valve which is mechanically

linked to the trip block. This rendered the high reactor water level (Level 8) turbine trip

feature inoperable, which required reactor power to be reduced below 25 percent per

TS. After the valve was exercised, the trip block operated properly and full power

operation was resumed. The probable cause of the auto stop oil dump valve binding

was the presence of trace amounts of hydrolyzed ester contaminants in the turbine lube

oil. The source of the ester could not be determined; however, compensatory

measures, such as regularly exercising the auto stop oil dump valve, were implemented

to ensure the condition did not recur. In addition, the turbine lube oil purification system

has been effective in removing the hydrolyzed ester contaminants. Since the source of

lube oil contamination could not be determined, the inspectors were unable to identify

any licensee performance deficiency and no findings of significance were identified.

This LER is closed.

4OA6 Meetings, Including Exit

On November 12, 2003, the inspector presented the results of the emergency plan

inspection to Mr. J. Bednar, Emergency Preparedness Manager, and other members of

his staff who acknowledged the findings.

On January 8, 2004, inspectors presented the results of the resident inspector activities

to Mr. S. Minahan, General Manager, Site Operations, and other members of his staff

who acknowledged the findings.

Enclosure

-17-

In all cases, the inspectors confirmed that proprietary information was not provided or

examined during the inspection.

4OA7 Licensee Identified Violations

The following violation of very low safety significance (Green) was identified by the

licensee and is a violation of NRC requirements which met the criteria of Section VI of

the NRC Enforcement Policy, NUREG-1600, for being dispositioned as an NCV.

  • TS 5.4.1(a) requires that the licensee establish and implement written procedures

recommended in Regulatory Guide 1.33, Revision 2, Appendix A, February 1978.

Appendix A recommends procedures for combating emergencies and other

significant events, such as reactor scrams. Contrary to this requirement, operators

failed to take manual control of reactor feed pumps as required by General

Operating Procedure 2.1.5, Reactor Scrams, Revision 44, during scram recovery

actions performed on October 28, 2003. This contributed to level control problems

following the scram. This finding was identified by the licensee during their

postscram review and was entered into their CAP as Resolve Condition Report

2003-1846. This finding was of very low safety significance, since it did not

represent the loss of any safety function.

ATTACHMENT: SUPPLEMENTAL INFORMATION

Enclosure

SUPPLEMENTAL INFORMATION

KEY POINTS OF CONTACT

Licensee Personnel

J. Bednar, Emergency Preparedness Manager

C. Blair, Engineer, Licensing

M. Boyce, Corrective Action Program Senior Manager

D. Cook, Senior Manager of Emergency Preparedness

J. Christensen, Acting Nuclear Site Vice President

T. Chard, Radiological Manager

K. Chambliss, Operations Manager

J. Edom, Risk Management

R. Estrada, Performance Analysis Department Manager

M. Faulkner, Security Manager

J. Flaherty, Site Regulatory Liaison

P. Fleming, Risk & Regulatory Affairs Manager

C. Kirkland, Nuclear Information Technology Manager

W. Macecevic, Work Control Manager

L. Schilling, Administrative Services Department Manager

R. Shaw, Shift Manager

J. Sumpter, Senior Staff Engineer, Licensing

K. Tanner, Shift Supervisor, Radiation Protection

D. Knox, Maintenance Manager

A. Williams, Manager, Engineering Support Division

LIST OF ITEMS OPENED, CLOSED, AND DISCUSSED

Opened and Closed

05000298/2003007-001 NCV Inadequate Procedure Results in Oil Fire Underneath Main

Turbine (Section 1R14)05000298/2003007-002 NCV Inadequate Corrective Actions Result in Repetitive

Degraded Condition on EDG (Section 1R15)05000298/2003007-003 NCV Inadequate Procedure Results in Inadvertent RPV

Draindown (Section 1R20)

Finding FIN Inadequate Postmaintenance Test of SAC (Section 1R19)

Finding FIN Inadequate Corrective Actions Result in Fire and Plant

Transient (Section 4OA2)

A-1 Attachment

Closed

05000298/2003-001-00 LER Inadequate Communication Results in Both Diesel

Generators Inoperable Simultaneously (Section 4OA3.1)

05000298/2003-005-00 LER Turbine Trip Failure During Testing Due to Ester

Contamination of Turbine Lube Oil (Section 4OA3.2)

LIST OF DOCUMENTS REVIEWED

Miscellaneous Documents Reviewed

Cooper Nuclear Station 2002 Operating Examination Results

LIST OF ACRONYMS

ADS alternate depressurization system

CAP Corrective Action Program

CFR Code of Federal Regulations

CST condensate storage tank

EDG emergency diesel generator

IST inservice test

LER licensee event report

NCV noncited violation

NEI Nuclear Energy Institute

PI performance indicator

PM preventive maintenance

RHR residual heat removal

RPV reactor pressure vessel

SAC station air compressor

SCR significant condition report

SDP Significance Determination Process

SLC standby liquid control system

SOP system operating procedure

TS Technical Specification

USAR Updated Final Safety Analysis Report

A-2 Attachment