ML040130636
| ML040130636 | |
| Person / Time | |
|---|---|
| Site: | McGuire, Mcguire |
| Issue date: | 01/12/2004 |
| From: | Haag R NRC/RGN-II/DRP/RPB1 |
| To: | Gordon Peterson Duke Energy Corp |
| References | |
| IR-03-005 | |
| Download: ML040130636 (36) | |
See also: IR 05000369/2003005
Text
January 12, 2004
Duke Energy Corporation
ATTN: Mr. G. R. Peterson
Vice President
McGuire Nuclear Station
12700 Hagers Ferry Road
Huntersville, NC 28078-8985
SUBJECT:
MCGUIRE NUCLEAR STATION - NRC INTEGRATED INSPECTION REPORT
05000369/2003005 AND 05000370/2003005
Dear Mr. Peterson:
On December 13, 2003, the US Nuclear Regulatory Commission (NRC) completed an
inspection at your McGuire Nuclear Station. The enclosed report documents the inspection
findings which were discussed on December 18, 2003, with you and members of your staff.
The inspection examined activities conducted under your licenses as they relate to safety and
compliance with the Commissions rules and regulations and with the conditions of your
licenses. The inspectors reviewed selected procedures and records, observed activities, and
interviewed personnel.
This report documents one NRC identified finding of very low safety significance (Green). The
finding was determined to be a violation of NRC requirements. However, because of the very
low safety significance and because it was entered into your corrective action program, the
NRC is treating this finding as a non-cited violation (NCV) consistent with Section VI.A of the
NRC Enforcement Policy. If you deny this non-cited violation, you should provide a response
with the basis for your denial, within 30 days of the date of this inspection report, to the United
States Nuclear Regulatory Commission, ATTN: Document Control Desk, Washington, D.C.
20555-0001, with copies to the Regional Administrator, Region II; the Director, Office of
Enforcement, United States Nuclear Regulatory Commission, Washington, D.C. 20555-0001;
and the NRC Resident Inspector at the McGuire facility.
In accordance with 10 CFR 2.790 of the NRC's "Rules of Practice," a copy of this letter, its
enclosure, and your response (if any) will be available electronically for public inspection in the
NRC Public Document Room or from the Publicly Available Records (PARS) component of
2
NRCs document system (ADAMS). ADAMS is accessible from the NRC Web site at
http://www.nrc.gov/reading-rm/adams.html (the Public Electronic Reading Room).
Sincerely,
/RA/
Robert C. Haag, Chief,
Reactor Projects Branch 1
Division of Reactor Projects
Docket Nos. 50-369, 50-370
Enclosure: NRC Integrated Inspection Report 05000369/2003005 and 05000370/2003005,
w/Attachment - Supplemental Information
cc w/encl:
C. J. Thomas
Regulatory Compliance Manager (MNS)
Duke Energy Corporation
Electronic Mail Distribution
M. T. Cash, Manager
Nuclear Regulatory Licensing
Duke Energy Corporation
526 S. Church Street
Charlotte, NC 28201-0006
Lisa Vaughan
Legal department (PB05E)
Duke Energy Corporation
422 South Church Street
Charlotte, NC 28242
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Winston and Strawn
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Division of Radiation Protection
N. C. Department of Environmental
Health & Natural Resources
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County720 East Fourth Street
Charlotte, NC 28202
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Assistant Attorney General
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UBLIC DOCUMENT (circle one): YES NO
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DATE
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Enclosure
U.S. NUCLEAR REGULATORY COMMISSION
REGION II
Docket Nos:
50-369, 50-370
License Nos:
Report Nos:
05000369/2003005 and 05000370/2003005
Licensee:
Duke Energy Corporation
Facility:
McGuire Nuclear Station, Units 1 and 2
Location:
12700 Hagers Ferry Road
Huntersville, NC 28078
Dates:
September 14 - December 13, 2003
Inspectors:
J. Brady, Senior Resident Inspector
S. Walker, Resident Inspector
M. Morgan, Senior Resident Inspector - North Anna (Sections
1R12, 1R15, 1R19, and 1R20)
S. Shaeffer, Senior Project Engineer (Sections 1R01, 1R04,
1R05, 1R13, 1R15, 1R19, and 1R20)
S. Vias, Senior Reactor Inspector (Section 4OA5.2)
D. Jones, Resident Inspector - Robinson (Sections 1R20 and
1R22)
J. Lenahan, Senior Reactor Inspector (Section 1R08)
J. Fuller, Reactor Inspector (Section 1R08)
R. Carroll, Senior Project Engineer (Sections 1R12 and 4OA1)
P. Fillion, Reactor Inspector (Section 4OA5.1)
Approved by:
Robert C. Haag
Reactor Projects Branch 1
Division of Reactor Projects
SUMMARY OF FINDINGS
IR05000369/2003-005, IR05000370/2003-005; 09/14/2003 - 12/13/2003; McGuire Nuclear
Station, Units 1 and 2; Maintenance Risk Assessment and Emergent Work Evaluation
The report covered a three month period of inspection by resident inspectors and announced
inspections by four regional engineering inspectors and two senior project engineers. One
Green non-cited violation (NCV) was identified. The significance of most findings is indicated
by their color (Green, White, Yellow, Red) using IMC 0609, Significance Determination
Process (SDP). Findings for which the SDP does not apply may be Green or be assigned a
severity level after NRC management review. The NRC's program for overseeing the safe
operation of commercial nuclear power reactors is described in NUREG-1649, Reactor
Oversight Process, Revision 3, dated July 2000.
A. NRC-Identified and Self-Revealing Findings
Cornerstone: Mitigating Systems
Green. A non-cited violation (NCV) was identified by the inspectors for failure to
perform an adequate risk assessment as required by 10 CFR 50.65(a)(4) when the 1B
motor-driven auxiliary feedwater pump containment isolation valve for the 1D steam
generator (1CA42B) was closed to perform maintenance on October 14, 2003 (Section
1R13).
This finding was considered to be more than minor because the inadequate risk
assessment resulted in the assignment of an incorrect risk action level (color) for this
maintenance activity. This finding was considered to be of very low safety significance
because had the error not occurred the only additional action required would have been
management awareness of the additional risk associated with the activity.
B. Licensee-Identified Violations
None.
REPORT DETAILS
Summary of Plant Status:
Unit 1 operated at approximately 100 percent rated thermal power (RTP) during the inspection
period.
Unit 2 began the inspection period shutdown in a refueling outage. Unit 2 was taken critical on
October 5, went on-line October 6, and reached 100 percent power on October 11. The unit
remained at approximately 100 percent RTP for the rest of the period.
1. REACTOR SAFETY
Cornerstones: Initiating Events, Mitigating Systems, Barrier Integrity
1R01
Adverse Weather Protection
a.
Inspection Scope
The inspectors reviewed the licensees implementation of adverse weather preparation
in regard to forecasted adverse weather associated with hurricane Isabel from
September 17 to 18, 2003. The inspectors verified the licensee implemented proper
pre-established measures for forecasted high wind conditions. The inspectors
performed walkdowns of the outside plant areas and roofs of accessible safety-related
structures. Temporary outage structures were verified to be either tied down or in
process of being removed. The inspectors also reviewed the licensees outage activities
to assess whether key activities associated with components utilized during loss of
offsite power events, such as the emergency diesel generators (EDGs), were being
monitored to maximize their availability during the adverse weather conditions.
When a tornado warning was predicted for the site on November 19, 2003, the
inspectors reviewed actions taken by the licensee in accordance with procedure
RP/0/A/5700/006, Natural Disasters, prior to the onset of that weather, to ensure that
the adverse weather conditions would neither initiate a plant event nor prevent any
system, structure, or component (SSC) from performing its design function.
After the licensee completed preparations for seasonal low temperature, the inspectors
walked down the auxiliary feedwater (CA) system and the fueling water storage tank
(FWST). This equipment was selected because their safety related functions could be
affected by adverse weather (freezing conditions). The inspectors observed plant
conditions and evaluated those conditions using criteria documented in procedure
IP/0/B/3250/059, Preventive Maintenance and Operational Check of Freeze Protection.
The inspectors also reviewed the following Problem Investigation Process (PIPs)
documents associated with this area to verify that the licensee identified and
implemented appropriate corrective actions.
2
M-02-05786, NRC Audit of Freeze Protection Found Discrepancies in Monthly
and Annual Heat Trace Procedures
M-03-00352, FWST Level Channel Failed Due to Freezing
M-03-00491, Operator Workarounds Due to FWST Level Channel Freezing
M-03-01580, FW System Requires A(1) Maintenance Status
b.
Findings
No findings of significance were identified.
1R04
Equipment Alignment
a.
Inspection Scope
Partial System Walkdowns
During this inspection period, the inspectors performed the following three partial system
walkdowns, when, as applicable, the indicated SSCs were out of service for
maintenance and testing:
Unit 2 Spent Fuel Pool Cooling with the core fully unloaded in the spent fuel pool
Unit 1A Diesel Generator with 1B Diesel Generator out of service on October 14
Unit 1 train A Residual Heat Removal with train B out of service on November 12
To evaluate the operability of the selected trains or systems under these conditions, the
inspectors verified correct valve and power alignments by comparing observed positions
of valves, switches, and electrical power breakers to the procedures and drawings listed
in the Attachment to this report.
Complete System Walkdown
The inspectors conducted a detailed review of the alignment and condition of the
Residual Heat Removal (ND) system. To determine the proper system alignment, the
inspectors reviewed the procedures, drawings, and Updated Final Safety Analysis
Report (UFSAR) sections listed in the Attachment to this report. In addition, significant
events data in the industry was reviewed to ascertain any similarities to McGuire SSCs.
The inspectors walked down the system, to verify that the existing alignment of the
system was correct. Items reviewed during the walkdown included the following:
Valves are correctly positioned and do not exhibit leakage that would impact the
function(s) of any given valve.
Electrical power is available as required.
Major system components are correctly labeled, lubricated, cooled, ventilated,
etc.
Hangers and supports are correctly installed and functional.
Essential support systems are operational.
Ancillary equipment or debris does not interfere with system performance.
3
Tagging clearances are appropriate.
Valves are locked as required by the licensees locked valve program.
The inspectors reviewed the documents listed in the Attachment to this report, to verify
that the ability of the system to perform its function(s) would not be affected by
outstanding design issues, temporary modifications, operator workarounds, adverse
conditions, and other system-related issues. In addition the inspectors also reviewed
the associated PIPs listed in the attachment to this report to verify that the licensee
identified and implemented appropriate corrective actions.
b.
Findings
No findings of significance were identified.
1R05
Fire Protection
a.
Inspection Scope
For the six areas identified below , the inspectors reviewed the licensees control of
transient combustible material and ignition sources, fire detection and suppression
capabilities, fire barriers, and any related compensatory measures, to verify that those
items were consistent with UFSAR Section 9.5.1, Fire Protection System, and Design
Basis Specification for Fire Protection, MCS-1465.00-00-0008. The inspectors walked
down accessible portions of each area and reviewed results from related surveillance
tests, as well as reviewed the associated pre-fire plan strategy, to verify that conditions
in these areas were consistent with descriptions of the areas in the Design Basis
Specification. Documents reviewed during this inspection are listed in the Attachment to
this report.
The inspected areas included:
Portions of the Unit 2 containment structure during No Mode work activities (fire
area containment)
Unit 2 safety-related switchgear rooms (fire area 18 )
Main control room (fire area 24)
Unit 2 motor-driven CA pump room (fire area 3)
Unit 2 turbine-driven CA pump room (fire area 3A)
120 volt vital AC instrument and electrical area (fire area 13)
b.
Findings
No findings of significance were identified.
4
1R06
Flood Protection Measures
a.
Inspection Scope
External Flooding
The inspectors assessed the licensees flooding mitigation plan and equipment
maintenance program to determine if they were risk informed and consistent with design
requirements. This review entailed: (1) potential flooding affects from probable
maximum flooding on the Auxiliary Building (AB); (2) potential flooding affects of cable
trenches, cable pits, and manholes; (3) potential failure of the Auxiliary Feedwater
Storage Tanks (CAST) and flooding of the Turbine Building, Diesel Generator Area, and
Yard. The inspectors reviewed the operator actions credited in the analysis to verify that
the desired results could be achieved using the plant procedure listed in the Attachment
to this report.
In addition, the inspectors walked down accessible manholes or reviewed digital
photographs taken during licensee inspections of manholes that contain safety-related
cables that are subject to flooding. This was to verify that cables and associated
support equipment described in UFSAR Sections 2.4.10, Flooding Protection
Requirements, and 8.3.1.2.37, Underground Raceway Design, were not damaged by
submergence and would perform their intended function.
The inspectors walked down the cable spreading rooms for both units and reviewed
operating experience to verify safe shutdown equipment in lower elevations would not
be affected by potential leaks from cracks in the floor. In addition, the inspectors
assessed the licensees mitigating actions for a service water (RN) line break in the CA
pump room to verify that the area configuration, features, and equipment functions were
consistent with the descriptions and assumptions used in UFSAR section 3.6.A.6,
Flooding Analysis, and in the supporting basis documents listed in the Attachment to
this report. Maintenance and testing records were examined to ensure necessary
instrumentation and equipment was available and reliable and within Technical
Specifications (TS) requirements where applicable. The inspectors reviewed the
operator actions credited in the analysis, to verify that the desired results could be
achieved using the plant procedure listed in the Attachment.
b.
Findings
No findings of significance were identified.
5
1R07
Heat Sink Performance
a.
Inspection Scope
Biennial Inspection
For the three RN cooled heat exchangers identified below, the inspectors reviewed the
documents listed in the Attachment to this report to verify that testing,
inspection/maintenance, or monitoring of biotic fouling controls were adequate to ensure
proper heat transfer. The inspectors reviewed the heat exchanger test and inspection
records to verify that testing and inspection methods were as described in the licensees
response to Generic Letter 89-13, Service Water System Problems Affecting Safety
Related Equipment. The inspectors verified that test/inspection results were trended,
that degrading trends were identified in the corrective action program, and that
corrective actions were taken to restore acceptable performance when trends were
identified. The inspectors reviewed the design documents listed in the Attachment to
this report to verify that the actual heat exchanger condition related to tube plugging was
within the bounds of the design documents. The inspectors determined whether the
assumed design temperatures, flow rates, and heat transfer factors were being verified
through testing and inspection, and whether current performance met the design.
Unit 2 component cooling water heat exchangers (RN on tube side)
Unit 2 diesel generator engine cooling water heat exchangers (RN on tube side)
Unit 2 containment spray heat exchangers (RN on shell side)
The inspectors reviewed the performance of the ultimate heat sink and sub-components
by reviewing their availability. The inspectors review of the ultimate heat sink involved
review of service water pond dam inspection records and performance of a walkdown,
review of main dam inspection records, and assessment of pump and valve
performance with the licensee system and component engineers to verify that the heat
sink and components were available and accessible to perform their heat sink function.
The inspectors reviewed PIPs for the last two years associated with RN to determine
whether any specific trends existed that were not being acted on by the licensee. For
the PIPs listed in the Attachment to this report, the inspector reviewed corrective actions
to determine if they were adequate and to determine if the problems had recurred.
b.
Findings
No findings of significance were identified.
1R08
Inservice Inspection Activities
.1
Inservice Inspection (ISI)
a.
Inspection Scope
The inspectors observed in-process Unit 2 ISI work activities and reviewed selected ISI
records. The observations and records were compared to the TS and ASME Boiler and
Pressure Vessel Code,Section XI, 1989 Edition, no Addenda, to verify compliance. In
6
addition, nondestructive examination (NDE) procedures for the below listed ISI
examination activities were reviewed. The licensee did not conduct examination of
steam generator U-tubes during the current outage. Examination results with
recordable indications and pressure boundary welding activities were not available for
review. Qualification and certification records for examiners, and equipment for selected
examination activities were reviewed. In addition, a sample of ISI issues in the
licensees corrective action program were reviewed for adequacy. The following Unit 2
ISI activities were reviewed:
Liquid Penetrant (PT) exams of weld numbers 2ND2FW16-21 and 2ND2F-367
on the 12 inch diameter residual heat removal piping located in the elevation 716
auxiliary building pipe chase.
Ultrasonic Examination (UT) of weld numbers 2ND2FW16-21 and 2ND2FW16-
22 on the 12-inch diameter residual heat removal piping located in the elevation
716 auxiliary building pipe chase. Witnessed calibration of equipment for
examination of dissimilar metal welds.
Radiographic films (RT) for weld numbers 2RHR-2A-2-3 & 2RHR-2A-3-4.
Work record for repair/replacement of three pipe supports.
Results of visual inspections performed on 11 pipe supports.
b.
Findings
No findings of significance were identified.
.2
Containment Vessel Inspection
a.
Inspection Scope
The inspectors examined interior and exterior sections of the steel containment vessel
(SCV) and reviewed selected records. The observations and records were compared to
the TS, ASME Boiler and Pressure Vessel Code, Article IWE of Section XI, 1992 Edition
and 1992 Addenda, as modified by 10 CFR 50.55a(b)(2)(vi).
The inspectors reviewed the licensees ISI procedures for containment inspection to
verify the procedures complied with the above listed requirements and specified
acceptance criteria. The inspectors examined the accessible interior surfaces of the
SCV in the pipe chase area (elevation 725) and at elevation 752 between azimuths 105
to 122 degrees in the seal table area, and the exterior surfaces of the SCV between
elevations 725 and 735 between azimuths 349 to 180 degrees. The inspectors also
reviewed records documenting visual inspection of the SCV and moisture barriers to
verify that the ISI activities were conducted in accordance with program requirements
and the acceptance criteria specified in the licensees procedures. The inspectors also
reviewed records documenting results of UT measurements to determine thickness of
the SCV in February,1999 and during the September 2003 outage to satisfy applicable
requirements of the TS and ASME Section XI.
7
b.
Findings
No findings of significance were identified.
1R11
Licensed Operator Requalification
a.
Inspection Scope
On October 22, the inspectors observed licensed-operators during requalification
simulator training for shift C, to verify that operator performance was consistent with
expected operator performance, as described in Exercise Guide OP-MC-SRT-26 and
27. This training tested the operators ability to perform abnormal and emergency
procedures dealing with load rejection, rod control malfunctions, reactor trip, safety
injection, grid disturbances, loss of electrical power, and safety injection termination.
The inspectors focused on clarity and formality of communication, use of procedures,
alarm response, control board manipulations, group dynamics and supervisory
oversight.
The inspectors observed the post-exercise critique, to verify that the licensee identified
deficiencies and discrepancies that occurred during the simulator training.
b.
Findings
No findings of significance were identified.
1R12
Maintenance Effectiveness
a.
Inspection Scope
The inspectors reviewed the four degraded SSC/function performance problems or
conditions listed below, to verify the licensees appropriate handling of these
performance problems or conditions in accordance with 10CFR50, Appendix B, Criterion
XVI, Corrective Action, and 10CFR50.65, Maintenance Rule.
Erratic steam generator level control/feedwater control
Maintenance on main steam supply to auxiliary equipment valve actuator 2SA-49
actuator resulted in additional damage to mechanical yoke stop and instrument
tubing (PIP M-03-4726)
Repetitive failure of standby shutdown facility (SSF) steam generator 1C level
indication
Lightning induced damage/loss of SSF battery charger SDSP-2
The inspectors focused on the following:
Appropriate work practices
Identifying and addressing common cause failures
Scoping in accordance with 10 CFR 50.65(b)
Characterizing reliability issues (performance)
Charging equipment unavailability (performance)
8
Trending key parameters (condition monitoring)
10 CFR 50,65(a)(1) or (a)(2) classification and reclassification, and
Appropriateness of performance criteria for SSCs/functions classified (a)(2)
and/or appropriateness and adequacy of goals and corrective actions for
SSCs/functions classified (a)(1).
b.
Findings
No findings of significance were identified.
1R13
Maintenance Risk Assessments and Emergent Work Evaluation
a.
Inspection Scope
The inspectors reviewed the licensees risk assessments and the risk management
actions used to manage risk for the plant configurations associated with the six activities
listed below. The inspectors assessed whether the licensee performed adequate risk
assessments, and implemented appropriate risk management actions when required by
10CFR50.65(a)(4). For emergent work, the inspectors also verified that any increase in
risk was promptly assessed, and that appropriate risk management actions were
promptly implemented. The inspectors also reviewed associated PIP M-03-5178,
Unrecognized yellow risk condition entered due to valve 1KC-394A going closed, to
verify that the licensee identified and implemented appropriate corrective actions:
Emergent work activities associated with Work Order (WO) 98620247, failure of
containment spray (NS) valve 1NS12B limit switch (add on pack set up)
Emergent work activities on October 6, which involved: RN water system
alignment changes to reduce 1B reactor coolant (NC) pump stator temperature
and 2A component cooling (KC) heat exchanger service water side differential
pressure increase; a wrong unit human error for mis-positioning of a Unit 1
service water valve; and the effects on 1A diesel generator operability from the
special service water alignment for the KC heat exchanger.
Scheduled work activities on Unit 1 for October 14 involving maintenance on the
1B diesel generator and maintenance on the auxiliary feedwater containment
isolation valve for the 1D steam generator (1CA42B)
Scheduled work activities on Unit 1 for the week of October 20, including
Craighead off-site power line switchyard work and emergent work on the 1A NC
pump thermal barrier component cooling water outlet isolation valve (1KC-394).
Scheduled work activities for November 13, which included 2B CA pump testing
and emergent work for a super flush of the side of the A train control room
ventilation chiller. The super flush made the Unit 1 RN system train A
inoperable, but available, and had interactions with Unit 2 that caused the
licensee to delay the Unit 2 auxiliary feedwater testing.
9
Scheduled work activities for November 19 which included work on the Unit 1
fuel handling building train B exhaust fan motor, 1A CA pump slave start test, 1A
charging pump oil gauge replacement and calibration, and 7300 protection
cabinet 2 testing. An emergent tornado warning resulted in risk management
actions being taken to delay some of the planned work.
b.
Findings
Introduction: A Green non-cited violation (NCV) was identified for failure to perform an
adequate risk assessment when the 1B motor-driven auxiliary feedwater pump
containment isolation valve for the 1D steam generator (1CA42B) was closed to perform
maintenance.
Description: The inspectors discovered, on October 14, that the licensee failed to
adequately evaluate the risk of isolating the auxiliary feedwater supply to the 1D steam
generator from the 1B motor-driven auxiliary feedwater pump. The valve was closed
and power removed on October 14, at 4:23 a.m., and was declared operable after
maintenance at 5:42 a.m., on October 15. The risk assessment assumed that the flow
path to the 1D steam generator through valve 1CA42B was functional for the entire
period of maintenance. Consequently, the risk assessment under estimated the risk
and resulted in a green code for this activity instead of a yellow code.
Analysis: Operator logs indicated that during the time valve 1CA42B was unavailable,
the 1B emergency diesel generator was also unavailable for planned maintenance on
October 14 from 4:15 a.m. until 7:01 p.m. It was returned to a functional status at 4:24
p.m. The 1B EDG activity was coded as yellow. Consequently, the coding of 1CA42B
as yellow would have added a second yellow until the EDG became available, and
would have been the only yellow until the valve was returned to functional. This issue
was considered to be more than minor in the mitigating system cornerstone because the
inadequate risk assessment resulted in the identification of an incorrect risk action level
(color). This issue was considered to be of very low safety significance because had the
error not occurred the only additional action required would have been management
awareness of the additional risk associated with the activity.
Enforcement: 10 CFR 50.65(a)(4) requires that before performing maintenance
activities, the licensee shall assess and manage the increase in risk that may result from
the proposed maintenance activities. Contrary to the above, on October 14, the
licensee failed to properly assess the increase in risk from isolating the auxiliary
feedwater supply to the 1D steam generator from the 1B motor-driven auxiliary
feedwater pump in that the licensees risk assessment assumed that the function was
available when it was not. Consequently, the risk assessment was inaccurate. The
failure to have an adequate risk assessment as required by 10 CFR 50.65(a)(4) is being
treated as an NCV, consistent with Section VI.A.1 of the NRC Enforcement Policy and is
identified as NCV 05000369/2003005-01: Inadequate Risk Assessment For 1CA42B
Out-of-service. This issue is in the licensees corrective action program as PIP M-03-
5115.
10
1R14
Personnel Performance During Nonroutine Plant Evolutions
a.
Inspection Scope
During the non-routine evolutions associated with Unit 2 plant startup from refueling
outage, the inspectors observed plant instruments and operator performance to verify
that operator performance was in accordance with procedure OP/2/A/6100/003,
Controlling Procedure for Unit Operations, and related training.
b.
Findings
No findings of significance were identified.
1R15
Operability Evaluations
a.
Inspection Scope
The inspectors reviewed the five operability determinations associated with the PIPs
listed below. The inspectors assessed the accuracy of the evaluations, the use and
control of any necessary compensatory measures, and compliance with the TS. The
inspectors verified that the operability determinations were made as specified by
Nuclear System Directive (NSD) 203, Operability. The inspectors compared the
arguments made in the determination to the requirements in TS, the UFSAR, and
associated design-basis documents, to verify that operability was properly justified and
the subject component or system remained available, such that no unrecognized
increase in risk occurred.
M-03-2668
Evaluate settlement of the 1A EDG exhaust missile barrier
M-03-4260
Unit 2 in mast sipping failed to identify suspect fuel defect
M-03-2861
Unanalyzed thermal transient on Unit 2 pressurizer power
operated relief valve (PORV) piping and components
M-03-5405
Low magnitude pressure surge occurred when valve 2RN-162B
was closed during service water flush of supply lines to the
auxiliary feedwater system (also PIP M-01-01573, previous similar
occurrence)
M-03-5055
Unit 2 pressurizer PORV piping temperatures lower than assumed
in previous operability evaluation
b.
Findings
No findings of significance were identified.
11
1R16
Operator Work-Arounds
a.
Inspection Scope
The inspectors reviewed the cumulative effects of the operator work-arounds listed in
the attachment to this report, to verify that those effects would not increase an initiating
event frequency, affect multiple mitigating systems, or affect the ability of operators to
respond in a correct and timely manner to plant transients and accidents.
b.
Findings
No findings of significance were identified.
1R19
Post-Maintenance Testing
a.
Inspection Scope
For the post-maintenance tests listed below, the inspectors witnessed the test and/or
reviewed the test data, to verify that test results adequately demonstrated restoration of
the affected safety function(s) described in the UFSAR and TS. The tests included the
following:
PT/2/A/4350/002A, Diesel Generator 2A Operability Test (outage maintenance)
PT/2/A/4350/002B, Diesel Generator 2B Operability Test (outage maintenance)
PT/2/A/4401/013, KC to NC pump Flow Balance Test (repair of various KC
valves)
PT/2/A/4403/005A, RN Train 2A Head Curve Verification (repair of various RN
components and 2A pump bearing repair)
OP/2/A/6200/009, Adjustment of Accumulator Pressures (reseating of C cold leg
accumulator check valve 2NI-81)
PT/2/A/4204/005B, ND Train B Valve Stroke Timing - Shutdown (replacement of
2ND-15B actuator)
b.
Findings
No findings of significance were identified.
1R20
Refueling and Outage Activities
a.
Inspection Scope
The inspectors evaluated licensee outage activities to verify that the licensee considered
risk in revising outage schedules, adhered to administrative risk reduction
methodologies they developed to control plant configuration, adhered to operating
license and TS requirements that maintained defense-in-depth, and developed
mitigation strategies for losses of the key safety functions identified below:
Inventory control
12
Power availability
Reactivity control
Containment
The inspectors observed the items or activities described below, to verify that the
licensee maintained defense-in-depth commensurate with the outage risk control plan
for key safety functions and applicable TS when taking equipment out of service. The
inspectors reviewed the licensees responses to emergent work and unexpected
conditions to verify that resulting configuration changes were controlled in accordance
with the outage risk control plan, and to verify that control room operators were kept
cognizant of plant configuration.
Clearance Activities
Reactor Coolant System (RCS) Instrumentation
Electrical Power
Spent Fuel Pool Cooling
Inventory Control
Reactivity Control
Containment Closure
The inspectors also observed fuel handling operations (insertion) and other ongoing
activities including Control Rod Latching, to verify that those operations and activities
were being performed in accordance with TS and approved procedures. Additionally,
the inspectors observed refueling activities to verify that the location of the fuel
assemblies was tracked, including new fuel, from core offload through core reload.
Prior to mode changes and on a sampling basis, the inspectors reviewed system lineups
and/or control board indications to verify that TS, license conditions, and other
requirements, commitments, and administrative procedure prerequisites for mode
changes were met prior to changing modes or plant configurations. Also, the inspectors
periodically reviewed RCS boundary leakage data, and observed the setting of
containment integrity, to verify that the RCS and containment boundaries were in place
and had integrity when necessary. Prior to reactor startup, the inspectors walked down
containment to verify that debris has not been left which could affect performance of the
containment sumps. The inspectors reviewed reactor startup and unit synchronization
to the grid to verify procedure compliance and that systems performed as designed.
The inspectors reviewed reactor physics testing results to verify that core operating limit
parameters were consistent with the design.
Periodically, the inspectors reviewed the items that had been entered into the licensees
corrective action program, to verify that the licensee had identified problems related to
outage activities at an appropriate threshold and had entered them into the corrective
action program. For the significant problems documented in the corrective action
program and listed on the Attachment to this report, the inspectors reviewed the results
of the licensees investigations to verify that the licensee had determined the root cause
13
and implemented appropriate corrective actions, as required by 10CFR50, Appendix B,
Criterion XVI, Corrective Action.
b.
Findings
No findings of significance were identified.
1R22
Surveillance Testing
a.
Inspection Scope
For the surveillance tests identified below, the inspectors witnessed testing and/or
reviewed the test data, to verify that the systems, structures, and components involved
in these tests satisfied the requirements described in the Technical Specifications, the
UFSAR, and applicable licensee procedures, and that the tests demonstrated that the
SSCs were capable of performing their intended safety functions.
PT/2/A/4350/004A, 2A D/G [Diesel Generator] Periodic and Load Sequencer
Test
PT/2/A4200/009 A, Engineered Safety Features Actuation Periodic Test Train A,
on September 26
PT/2/A4200/009 B, Engineered Safety Features Actuation Periodic Test Train B,
on September 27
SM/0/A/8510/006, Ice Condenser Intermediate Deck Doors Inspection and
Corrective Maintenance
PT/0/A/4200/032, Periodic Inspection of Ice Condenser Lower Inlet Doors
PT/2/A/4403/001A, 2A RN Pump Performance Test*
PT/2/A/4252/001A, 2A CA Pump Performance Test*
PT/2/A/4200/001 N, VP Valve Leak Rate Test**
- This procedure included inservice testing requirements.
- This procedure included testing of a large containment isolation valve.
The inspectors reviewed associated PIP M-03-2880, Cylinder 1 on Unit 2 A EDG
exhibited low exhaust temperature for one minute during 24 hour2.777778e-4 days <br />0.00667 hours <br />3.968254e-5 weeks <br />9.132e-6 months <br /> run, to verify that the
licensee identified and implemented appropriate corrective actions.
b.
Findings
No findings of significance were identified.
1R23
Temporary Plant Modifications
a.
Inspection Scope
The inspectors reviewed the temporary modifications described in the McGuire
Temporary Modifications (MGTM) listed below, to verify that the modifications did not
affect the safety functions of important safety systems, and to verify that the
modifications satisfied the requirements of 10CFR50, Appendix B, Criterion III, Design
Control.
14
MGTM-0302, Leak repair pipe cap for 2NI-465, unit 2 NV to 2B NC cold leg high
point vent valve
MGTM-0306, Bypass FWST trench sump pump high level cutoff switch until
new switch arrives.
The inspectors also reviewed tag outs open on December 10, 2003, to verify that tag
outs were not being used to implement temporary modifications.
b.
Findings
No findings of significance were identified.
4.
OTHER ACTIVITIES
4OA1 Performance Indicator Verification
a.
Inspection Scope
For the performance indicators (PIs) listed below, the inspectors sampled licensee PI
data for the period from July 2002 through September 2003. To verify the accuracy of
the PI data reported for both units during that period, the inspectors compared the
licensees basis in reporting each data element to the PI definitions and guidance
contained in NEI 99-02, Regulatory Assessment Indicator Guideline, Rev. 2.
Mitigating Systems Cornerstone
Safety System Unavailability, High Pressure Safety Injection
The inspectors reviewed Licensee Event Reports, records of inoperable equipment, and
Maintenance Rule records, to verify that the licensee had adequately accounted for
unavailability hours that the subject systems had experienced during the previous four
quarters. The inspectors also reviewed the number of hours those systems were
required to be available and the licensees basis for identifying unavailability hours. In
addition, the inspectors interviewed licensee personnel associated with the PI data
collection, evaluation, and distribution.
Integrity Cornerstone
Reactor Coolant System Specific Activity
The inspectors observed licensee sampling and analysis of reactor coolant system
samples, and compared the licensee-reported performance indicator data with records
developed by the licensee while analyzing previous samples. The inspectors also
reviewed the following PIPs associated with this area to verify that the licensee identified
and implemented appropriate corrective actions:
M-03-05536, 3 Primary Chemistry Samples Analyzed With Incorrect Sample
Times, dated 11/12/03
M-03-05686, Chemistry HPRC Procedure Benchmarking Project, dated 11/12/03
15
b.
Findings
No findings of significance were identified
4OA2 Problem Identification and Resolution
As required by Inspection Procedure 71152, Identification and Resolution of Problems,
and in order to help identify repetitive equipment failures or specific human performance
issues for follow-up, the inspectors performed a daily screening of items entered into the
licensees corrective action program. This review was accomplished by reviewing hard
copies of each condition report, attending daily screening meetings, and accessing the
licensees computerized database.
4OA5 Other Activities
.1
(Closed) Unresolved Item (URI) 50-369, 370/2003007001: Fire Suppression System for
Dedicated Shutdown Areas Not in Accordance with 10 CFR 50, Appendix R, Section
III.G.3
This URI was opened pending evaluation of whether a backfit was warranted to require
that the existing partial suppression capability be expanded to whole area suppression.
Though the URI writeup describes the partial suppression system in Fire Area 4, the
report alludes to other III.G.3 areas with similar partial suppression.
The inspector used the significance determination process to determine the change in
risk that would result from expanding the existing suppression system from partial
coverage to area wide coverage. This analysis indicated no significant difference in risk
between the normal suppression and degraded suppression cases. Hence, the
inspector concluded that backfitting to provide area wide suppression was not
warranted. This analysis considered the worst case of post-fire shutdown with only the
standby shutdown system available. Both the transient worksheet and the loss of
nuclear service water worksheets were evaluated. Insights gained from this analysis,
which focused on Fire Area 4, led to the conclusion that the same result would be
obtained for any auxiliary building III.G.3 area at McGuire. This is primarily due to the
small difference in initiating event likelihood between the normal suppression and
degraded suppression cases and the relatively low likelihood values. There were only
three other III.G.3 areas. Two were the cable spreading rooms which had misty fog type
suppression systems. The other was the control room, which is a generic exception to
the requirement to have a fixed suppression system.
.2
Reactor Pressure Vessel Lower Head Penetration Nozzle Inspection
a.
Inspection Scope (TI 2515/152)
The inspectors observed activities associated with the inspection of the Unit 2 reactor
vessel lower head penetrations in response to NRC Bulletin 2003-02. The guidelines for
the inspection are provided in NRC temporary instruction (TI) procedure 2515/152,
Reactor Pressure Vessel (RPV) Lower Head Penetration Nozzle Inspection (NRC
16
The inspection included review of nondestructive examination (NDE) procedures,
assessment of NDE personnel training and qualification, and observation and
assessment of Remote Visual (VT) examinations. Discussions were also held with
contractor representatives and other licensee personnel. The inspectors reviewed
results of the licensees 100% Bare Metal Visual (BMV) and VT examination. The
inspectors also performed a visual inspection of the lower head to verify items on the
video tape prior to licensee cleaning of the lower head. The activities and documents
listed below were examined to verify licensee compliance with regulatory requirements
and gather information to help the NRC staff identify possible further regulatory
positions and generic communications.
Specifically, the inspectors reviewed and observed:
-MP/0/A/7150/165, Rx Vessel Bottom Head Bare Metal Inspection, Rev 0
-MP/0/A/7700/080, Inspection, Evaluation and Cleanup of Boric Acid on Plant
Materials.
-QAL-15, Inservice Inspection (ISI) Visual Exam, VT-2, Pressure Test, Rev 20.
-PIP M-03-04004 U2 Rx Vessel Bottom Head Bare Metal Inspection Results
-PIP M-03-04096 Count Room Analysis of Smear Samples
-Video results of VT-2 exam of U2 Rx Bottom Head Inspection
b.
Findings
TI 2515/152 Reporting Requirements:
1.1
Was the examination performed by qualified and knowledgeable personnel?
The Bare Metal Visual (BMV) examination of the reactor vessel (RV) lower head
was conducted by certified visual inspectors to QAL-15, Inservice Inspection
(ISI) Visual Exam, VT-2, Pressure Test. The qualification documentation for the
Level II & Level III VT-2 personnel performing the inspection was verified. The
inspectors also reviewed the inspection standards, acceptance criteria,
calibration requirements of the camera and lighting, the resolution and sensitivity
requirements for the inspection equipment. The inspectors found that the
licencees inspection personnel were very knowledgeable with the requirements
in all of these areas.
1.2
Was the examination performed in accordance with demonstrated procedures?
The inspectors reviewed the applicable inspection procedures and verified they
had been reviewed and approved through the licensees procedure review
process.
The Bare Metal Visual (BMV) examination was performed in accordance with
licensee procedure number MP/0/A/7150/165, Rx Vessel Bottom Head Bare
Metal Inspection.
17
1.3
Was the examination able to identify, disposition, and resolve deficiencies?
The inspectors reviewed the procedures controlling the 100% Bare Metal VT-2
examination techniques and determined that they provided adequate guidance to
ensure that they would be able to identify, disposition and resolve relevant
deficiencies in the RV lower head penetration materials.
1.4
Was the examination capable of identifying pressure boundary leakage and/or
RPV lower head corrosion as described in BL 2003-02?
Based upon review of the results for the BMV examination, procedures,
qualifications, appropriate lighting, and sensitivity requirements, the inspectors
determined that the licensee was capable of identifying and dispositioning
pressure boundary leakage and boric acid corrosion, if present.
2.0
What was the condition of the reactor vessel lower head (debris, insulation, dirt,
boron from other sources, physical layout, viewing obstructions)?
Prior to the RPV lower head inspection all the insulation was removed, and the
reactor vessel bottom head was entirely accessible for the BMV inspection.
Minor boron deposits and metal corrosion were identified on the bottom reactor
vessel and incore guide tubes. In all cases there were visible leak tracks running
down the side of the vessel that originated from previous cavity seal and
sandbox cover seal leaks. Each of the 58 penetrations was videoed twice, one
pass from each side. The combination of the two passes provided a complete
360 degree view of each penetration. No significant boron buildup at the annular
areas around the bottom mounted instrumentation (BMI) penetrations was found
that would indicate a leakage. The inspectors did not see any popcorn type
boric acid crystals surrounding the penetrations. There was no wastage,
corrosion or cracks that needed repair. The inspection results were documented
in PIP M-03-04004, U2 Rx Vessel Bottom Head Bare Metal Inspection Results,
09/07/2003. The inspectors reviewed the video of the bottom head inspection to
verify the licensees inspection results, and held discussions with the appropriate
engineering and examination staff.
3.0
Could small boron deposits, as described in the bulletin, be identified and
characterized?
With the available lighting on the remote visual equipment and the clarity of the
picture, the inspectors were able to verify that the boric acid present on the
bottom head would not mask any indications of penetration leakage. Boron
deposits, as described in the bulletin, could have been readily identified and
characterized.
4.0
What materiel deficiencies (associated with the concerns identified in the
bulletin) were identified that required repair?
18
There was no wastage, corrosion or cracks that needed repair. The licensee was
planning to conduct an additional BMV examination upon completion of hydro-
cleaning the reactor vessel bottom head. This will provide the licensee with
appropriate baseline documentation for future inspections.
5.0
What, if any, impediments to effective examinations were identified.
There were no significant items that could impede effective examinations. The
licensee was able to inspect 360 degrees around each of the 58 lower head
penetration nozzles.
6.0
Did the licensee perform appropriate follow-up examinations for indications of
boric acid leaks from pressure-retaining components above the RPV lower
head?
The Licensee was aware of cavity seal leaks from previous outages. The
licensee plans to hydro-clean the bottom vessel head in order to establish a
baseline visual inspection record for any future BMV examinations.
The licensee obtained residue samples at various locations on the reactor
bottom vessel head, and performed an isotopic analysis. The results verified the
source of the deposits to be from past cavity seal leaks greater than 18 months
old. These results are described in PIP M-03-04096, Count Room Analysis of
Smear Samples.
4OA6 Meetings, Including Exit
On December 18, 2003, the resident inspectors presented the inspection results to
Mr. G. Peterson and other members of his staff. The inspectors confirmed that
proprietary information was not provided or examined during the inspection.
Attachment
SUPPLEMENTAL INFORMATION
KEY POINTS OF CONTACT
Licensee
D. Black, Security Manager
S. Bradshaw, Superintendent, Plant Operations
J. Bramblett, Chemistry Manager
S. Brown, Manager, Engineering
K. Crane, Technical Specialist
B. Dolan, Manager, Safety Assurance
K. Evans, Manager, Mechanical and Civil Engineering (MCE)
T. Harrall, Station Manager, McGuire Nuclear Station
B. Johanson, SSF System Engineer
R. Kirk, Plant Systems Engineer - PI
L. Loucks, Radiation Protection Manager
R. Parker, Superintendent, Maintenance
G. Peterson, Site Vice President, McGuire Nuclear Station
P. Smith, Maintenance Rule Engineer
J. Thomas, Manager, Regulatory Compliance
K. Thomas, Manager, RES Engineering
B. Travis, Superintendent, Work Control
R. Branch, QA/QTeam Leader
J. Bryant, Regulatory Compliance
D. Caldwell, Inservice Inspection
F. Grass, Insevice Inspection
NRC personnel
R. Haag, Chief, Reactor Projects Branch 1
LIST OF ITEMS OPENED, CLOSED, AND DISCUSSED
Opened and Closed
50-369/03-05-01
Failure to perform an adequate risk assessment for
removing from service the auxiliary feedwater isolation
valve to the 1D steam generator (Section 1R12)
Closed
50-369, 370/03-07-01
Fire Suppression System for Dedicated Shutdown Areas
Not in Accordance with 10 CFR 50, Appendix R, Section
III.G.3 (Section 4OA5)
Discussed
None
2
LIST OF DOCUMENTS REVIEWED
Section 1R01: (Adverse Weather Protection)
Procedures:
IP/0/B/3250/059, Preventive Maintenance and Operational Check of Freeze Protection, Rev. 15
IP/1/B/3050/013C, FWST Area Temperature Loop Calibration, Rev. 4
IP/0/B/3250/059A, Monthly Check of Freeze Protection, Rev. 14,15
Work Orders:
98585977, Freeze Protection Heat Trace Inspection, dated 8/29/03
98618219, U2 High Temp Normal Heat Trace Control Board Replacement, dated 11/12/03
98289914, U2 Re-Terminate T/C Input Wiring for HT Control, dated 11/19/03
98617629, U1 High Temp Normal Heat Trace Control Board Replacement, dated 11/12/03
98289648,U2 Heat Trace Panel Channel 2 Alarm dated 9/13/03
98606092, Redesign FWST Heat Trace System U2 (Work Order Report), dated 9/4/03
98585977, Inspect Heat Trace, (Work Order Report), dated 10/30/03
PIPs Generated During This Inspection
M-03-05700, Determine If SSF Duct Heaters Needed for Freeze Protection and PMd
M-03-05696, Area Heaters for U1 FWST Instrument Room Not Listed in IP/0/B/3250/095
Section 1R04: (Equipment Alignment)
Partial System Walkdown
Spent Fuel Cooling System Drawing MCFD 1570-01.01
Diesel Generator Engine Flow Diagrams: MCFD-1609-03, Fuel Oil System;
MCFD-1609-01, Cooling Water System; MCFD-1609-04, Starting Air System;
MCFD-1609-02, Lubricating Oil System
Residual Heat Removal Flow Diagram: MCFD-2561-01.00
Complete System Walkdown
Procedure OP/2/A/6200/004, Residual Heat Removal , Revision 071
Training OP-MC-PS-ND, Residual Heat Removal (ND) Lesson Plan, Revision 29
Design Basis Specification -MCS-1561.ND-00-0001, ND System, Revision 8
Drawing MCFD-2561-01.00, Flow Diagram of ND System", Revision10
UFSAR section 6.3, Emergency Core Cooling System
UFSAR section 5.5.7, Residual Heat Removal
WR 98623147 2NDPS5040: Top Left T-Valve Has Leak
WR 98624377 2NDTE7500: Reinstall Upper Thermocouple
WR 98618960 2NDTE7500: Check Upper Bearing T/C
WR 98618403 2ND-19A: Replace Add-On Pack of Actuator
3
PIP M-03-04545, Miniflow Recirc via 2ND-68A has decreased from 667 to 587 gpm
PIP M-03-02170, 2NDPS 5040 Locking Screw for Low Switch Found Stripped
PIP M-01-04677, 1/2ND-14,29, & 34 Present Special System Vulnerabilities
PIP M-03-01236, Operating Experience Evaluation of IN 2003-03, Part 21 Inadequately Staked
Capscrew Renders Residual Heat Removal Pump Inoperable
IN-2003-03, Part 21 - Inadequately Staked Capscrew Renders Residual Heat Removal Pump
2003T2, ND - Residual Heat Removal and Low Head Safety Injection Health Report
2003T2, Air Operated Valves Health Report
Section1R05: (Fire Protection)
Procedures:
McGuire Nuclear Station IPEEE Submittal Report dated June 1, 1994
McGuire Nuclear Station Supplemental IPEEE Fire Analysis Report dated August 1, 1996
MCS-1465.00-00-0008, R4, Design Basis Specification for Fire Protection
Drawings: MC-1384-07-17-01, MC-1384-07-13-01, MC-1384-07-15-01, MC-1384-07-15-01
Section 1R06: (Flood Protection Measures)
UFSAR Sections
2.4.10, Flooding Protection Requirements.
3.6A.6, Flooding Analysis.
Calculations:
MCC-1223.42-00-0037, Evaluation of the Use of Non-Safety Water Sources for the Auxiliary
Feedwater System, Sec. 10.8, Rev. 6
MCC-1206.47-69-1001, Auxiliary Building Flooding Analysis, Sec.9.2-9.2.1, Rev. 11
Procedures:
AP/0/A/5500/44, Plant Flooding, Rev. 3
IP/0/A/3215/004, Magnetrol Liquid Level Control Switch Calibration, Rev. 15
Other Documents:
PIP M-02-04591, Steel Plate Trench Cover at Unit 2 FWST Not Bolted Down
PIP M-02-04582, Flood Curbing Around Exterior Auxiliary Building Doors
PIP M-02-04569, FWST Sump System Calibration and Labeling
PIP M-02-04578, SSF Control and Annunciator for WZ Sump Pumps
PIP M-02-04592, WZ C Sump HI Setpoint Set at 6.5 Instead of 7.0 Feet
PIP M-02-03265, Evaluate Applicability of Columbia Station Water Spill Event Report
PIP M-03-02564, Water Filling in Cable Trench on U2 TB SE Side in Gravel
WO 98549870, Magnetrol Liquid Level Control Switch Calibration 5000, dated 4/1/03
WO 98253960, Magnetrol Liquid Level Control Switch Calibration 5000, dated 4/8/00
4
WO 98549871, Magnetrol Liquid Level Control Switch Calibration 5010, dated 4/1/03
WO 98253961, Magnetrol Liquid Level Control Switch Calibration 5010, dated 4/8/00
WO 98253962, Magnetrol Liquid Level Control Switch Calibration 5020, dated 4/3/00
WO 98547819, Magnetrol Liquid Level Control Switch Calibration 5020, dated 4/4/03
WO 98253963, Magnetrol Liquid Level Control Switch Calibration 5030, dated 4/3/00
WO 98547820, Magnetrol Liquid Level Control Switch Calibration 5020, dated 4/4/03
WO 98253964, Magnetrol Liquid Level Control Switch Calibration 5040, dated 4/5/00
WO 98476920, Rad Monitor EMF-31 U1 Flow Calibration, dated 4/23/02
WO 98562946, Rad Monitor EMF-31 U1 Flow Calibration, dated 3/24/03
WO 98498788, Rad Monitor EMF-31 U2 Flow Calibration, dated 10/9/02
WO 98551649, Rad Monitor EMF-31 U2 Flow Calibration, dated 4/23/02
MN32104U, System Description for WP & WU Systems, dated 12/19/85
PIPs Generated During Inspection
PIP M-03-05352, Incorrect Tolerance for WZ Sump Level Switch LS0500
1R07: Heat Sink Performance
Procedures:
MP/0/A/7700/013, Component Cooling System Heat Exchanger Corrective Maintenance:
performed 9/12/2203 for 2B KC, 9/17-19/2003 for 2A KC
MP/0/A/7650/087, Documenting Heat Exchanger Tube Plugs In Safety Related Heat
Exchanger: performed 9/19/2003 for 2A KC
MP/0/A/7650/101, Diesel Generator Cooling Water (KD) Heat Exchanger Corrective
Maintenance: performed 9/17/2003 for 2A KD, 9/12-13/2003 for 2B KD
OP/2/A/6400/006, Enclosure 4.9, KC Heat Exchanger Flush and Realignment: performed
11/02/2003 for 2B KC heat exchanger high velocity flush, performed 11/10/2003 for 2A KC
heat exchanger high velocity flush and super flush
Calculations:
MCC-123.24-00-0072, RN/KD Heat Exchanger Tube Plugging Analysis
MCC-123.24-00-0075, RN/KC Heat Exchanger Tube Plugging Analysis
MCC-123.24-00-0076, RN/NS Heat Exchanger Tube Plugging Analysis
Drawings:
SNSWP intake structure sketch (C-4 & C-5)
Main Dam intake structure sketch (Figure 1-9)
5
PIPs:
M-01-4406, M-01-5099, M-02-3497, M-02-4182, M-03-1762, M-03-2112, M-03-2678, M-03-
4962, M-03-5253, M-03-5434
Other documents:
Duke Power Generic Letter 89-13 response dated 9/30/1996
Licensees service water heat exchanger spread sheet/data base
Licensees service water flow balance data base from 1992 until present
Work Order 98091368: Inspection of LLI, SNSP intake and discharge, main intake and
discharge (last performed 6/2-3/99, due in 2004) .
Work Orders for inspection of containment spray heat exchangers: 96052306 (1A); 96052317
(1B); 97007785 (2A); 97007793 (2B)
2003 Annual Inspection of SNSW Dam and WWCB Dikes, performed February 3, 2003
NRC Dam Safety Audit transmitted March 24, 1999 for FERC inspection conducted October 14,
1998
Service Water Profile Data report dated November 5, 2003
Digital pictures of the RN tube side inspections of Unit 2 KC and 2KD heat exchangers during
2EOC15
RN-Nuclear Service Water Health Report for report period 2003T2
UFSAR section 9.2.2, Nuclear Service Water System and Ultimate Heat Sink
Section 1R08:Inservice Inspection Activities
Procedures
Procedure QAL-13, Inservice Inspection (ISI) Visual Examination, VT-1 and VT-1C, Rev. 18,
dated 8/15/02, and Field Change FC F31, dated 9/11/02
Procedure QAL-14, Inservice Inspection (ISI) Visual Examination, VT-3 and VT-3C, Rev. 24,
dated 8/15/02, and Field Change FC F32, dated 9/11/02
Procedure NDE-600, Ultrasonic Examination of Similar Metal Welds in Ferric and Austenitic
Piping, Rev. 15, dated 9/2/03
Procedure NDE-35 Liquid Penetrant Examination, Rev 19, dated 1/31/02, Field Changes FC
02-30, dated 11/21/02 and FC 03-19, dated 7/7/03
Procedure PDI-UT-10, PDI Generic Procedure for the Ultrasonic Examination of Dissimilar
Metal Piping Welds, Rev. A 12/20/2002, approval date 1/28/03
Drawings
Drawing numbers MC-ISIC-1042-002 & -003, Reactor Building Unit 1, Steel Containment
Vessel, Inside Surfaces, ISI Areas, Sheet 1, Rev. 2, & Sheet 2, Rev. 1
Drawing Number MC-ISIC-2042-004 & -005, Reactor Building Unit 1, Steel Containment
Vessel, Outside Surfaces, ISI Areas, Sheet 1, Rev. 0 and Sheet 2, Rev. 1
6
Drawing Number MC-ISIC-1042-006, Reactor Building Unit 1, Steel Containment Vessel, Dome
Plan & Elevation, Rev. 0
Drawing Number MC-ISIC-1042-015, Reactor Building Unit 1, Steel Containment Vessel,
Penetration Details, Rev. 2
Drawing Number MC-ISIC-1042-016, Reactor Building Unit 1, Steel Containment Vessel,
Outside Surfaces, Augumented Examination Areas, Details, Sheet 1, Rev. 0
Drawing Number MC-ISIC-1042-017, Reactor Building Unit 1, Steel Containment Vessel,
Outside Surfaces, Augumented Examination Areas, Details, Sheet 2, Rev. 2
Drawing Number MC-ISIC-1042-018, Reactor Building Unit 1, Steel Containment Vessel,
Outside Surfaces, Augumented Examination Areas, Details, Sheets 3, Rev. 2
Drawing Number MC-ISIC-1042-019, Reactor Building Unit 1, Steel Containment Vessel,
Outside Surfaces, Augumented Examination Areas, Details, Sheet 4, Rev. 3
Other Documents:
Problem Investigation Process (PIP) PIP M-03-02452, Failure to Include Head to Flange Welds
on the Excess Letdown Heat Exchanger in the Unit 1 and Unit 2 Second Inservice Inspection
Plan
PIP M-03-04270, Identification of Indication during UT Exam of Weld Number 2NI2FW24-6
Liquid penetrant examination reports for weld numbers 2ND2FW16-22, and -367 dated 9/18/03
Ultrasonic calibration report numbers CAL-03-160, 162 and -163, for 3/17/03
Ultrasonic examination reports for weld numbers 2ND2FW16-22, -22, and -367, dated 9/19/03
Repair of Hanger # 2MCY-FW-5048
Replacement of Mechanical Snubber on Hanger 2-MCA-S-RN-533-01-S
Replacement of Mechanical Snubber on Hanger 2-MCR-NC-4285
Records for Visual inspection of Unit 2 Containment Moisture Barriers completed on 9/8/03,
9/9/03, and 9/11/03
Visual Inspection Reports for pipe support numbers 2-MCA-KC-3324, 2-MCA-CA-H141, 2-
MCA-CA-H145, 2-MCA-ND-6127, -6130, -6220, -6280, and -5502, 2-MCA-SV-H53, 2-MCA-
SV-H55, and 2-MCA-SA-5086
7
Section 1R12: Maintenance Effectiveness
Feedwater Control
Screened 357 PIPs related to the feedwater system and reviewed 40 that dealt with aspects of
feedwater/steam generator level control
Discussed system history (including 40 related PIPs) with the system engineer
S/G Level Control Improvement plan dated 10/28/2002
CF-Feedwater Health Report for period 2003T1
CF system maintenance rule scoping document
Preventive maintenance work order tasks on CF Reg valves: 92027512, 85055329, 98384459,
8505526, 9852483,898418540
Preventive maintenance work order tasks on CF Reg valves: 85055531, 90056974
SSF Health Report 2003T2
Engineering Directives Manual EDM-210, Engineering Responsibilities for the Maintenance
Rule, Revision 16
AP/1/A/5500/024, Loss of Plant Control Due to Fire or Sabotage, Revision 21
SLC 16.9.7, Standby Shutdown System
SSF steam generator 1C level indication
PIPs M-02-01969 (Unit 2), M-02-06075 (Unit 1), and M-03-00762 (Unit 1) - SSF standby
makeup pump flow indication (NVP6420) deficiencies/failures
PIPs M-02-04211 (Unit 1), M-02-04299 (Unit 1), and M-02-05261 (Unit 1) - SSF 1C steam
generator wide range level indication (1CFP6100) deficiencies/failures
Modification MGMM13978 and associated Work Order 98565527, Replacement of Foxboro
flow transmitter 1NVFT6420 with Rosemount Model 1153HB4RCN0037
Modification MGMM13604 and associated Work Order 98538684, Replacement of Foxboro
level transmitter 1CFLT6100 with Rosemount Model 1153DB5RC
Modification MGMM14396 (scheduled 1EOC17), Replacement of Foxboro level transmitters
1CFLT6080, 1CFLT6090, and 1CFLT6110 with Rosemount Model 1153DB5RC
Modification MGMM14397 (scheduled 2EOC16), Replacement of Foxboro level transmitters
2CFLT 6100, 2CFLT6080, 2CFLT6090, and 2CFLT6110 with Rosemount Model
1153DB5RC, and Replacement of Foxboro flow transmitter 2NVFT6420 with Rosemount
Model 1153HB4RCN0037
7-Year Work Order History for 1CFLP6080, 1CFLP6090, 1CFLP6100, 1CFLP6110,
1NVLP6420, 2CFLP6080, 2CFLP6090, 2CFLP6100, 2CFLP6110, 2NVLP6420, and
1LGPT5090 (Unit 1 main generator seal oil pump d/p)
SSF battery charger SDSP-2
7-Year Work Order History for SSF chargers SDSP-1, SDSP-2 and SDSS
PIP M-03-03042 (SDSP-2; lightning trip - control board damage)
8
PIP M-02-02461 (SDSP-1; lightning trip - no damage)
PIP M-03-00733 (SDSP-1; trip following deep discharge battery test - no damage)
PIP M-99-03656 (SDSP-2; trip following deep discharge battery test - no damage)
PIP M-98-01003 (SDSS; trip following deep discharge battery test - control board damage)
IEE Transactions on Energy Conversions, Volume 5, No. 1, March 1990 (Analytical Technical of
Lightning Surges Induced on Grounding Mesh of PWR Nuclear Power Plant)
IEE Transactions on Energy Conversions, Volume 9, No. 3, September 1994 (A Review of
Lightning-Related Operating Events at Nuclear Power Plants)
Drawing MC-1716-02.03, Connection Diagram - SSF Control Panel, Revision 37
Drawing MC-1705-03.01, One and Three Line Diagram - SSF 250/125VDC Auxiliary Power
System, Revision 24
Drawing MC-1778-01.01, Connection Diagram - SSF Diesel Generator, Revision 12
Section 1R16: Operator Work-Arounds
Work-arounds reviewed for cumulative affect
98-03, EFA zones
99-01, S/G chart recorder ink problems
99-12, excessive leakage of 1RL-18 causes improper LT oil temperature
01-01, S/G level control at low power levels
03-01, frequency changes to grid cause reactor power to exceed 100%
03-02, 1NV-124 in manual control due to erratic control in auto
03-03, 1CA-42B may have a problem reopening against d/P and will not be cycled to control CA
flow to 1D S/G during a loss of VI or vital bus events
03-04, Ongoing problems with both the U-1 and U-2 FWST level heat tracing systems have
resulted in numerous malfunctions, alarms and eventually resulting in all 3 U-1 FWST level
channels freezing and failing high
03-05, Due to tripping problems associated with the A train VC/YC chiller during startup,
Engineering Guidance # 03-16 was generated providing compensatory actions locally at the
chiller by a designated maintenance technician to prevent chiller from tripping.
03-06, control room operators must take turbine to manual to perform governor valve
movement portion of PT/1(2)/A/4250/004A (turbine valve movement test), to prevent other
governor valves from swinging drastically (20%)
Section 1R20: Refueling and Outage Activities
Procedures and Reports
MCEI-0400-41, McGuire 2 Cycle 16 Final Core Map, Rev. 11
PT/0/A/4150/033, Core Verification, Rev. 15
PT/0/A/4150/033, Total Core Reloading, Rev. 43
MP/2/A/7150/073, Rod Cluster Control Assembly Heavy Drive Rod Unlatching and Latching,
Rev. 14
OP/2/A/6100/003, Controlling Procedure For Unit Operation
PT/0/A/4150/021, Post Refueling Controlling procedure for Criticality, Zero Power Physics, &
Power Escalation Testing
PT/0/A/4150/028, Criticality Following a Change in Core Nuclear Characteristics
PT/0/A/4150/013, Boron Endpoint, Dynamic Rod Worth and Isothermal Temperature
Coefficient Measurement
MCEI-0400-47, Unit 2 Cycle 16 Core Operating Limits Report
9
PIP M-03-4868, ND discharge cross-connect valve 2ND-15 actuator failure and acceptability of
Mode 4 entry with valve functional but inoperable.
PIP M-03-4911, Unit 2 reactivity computer loss of configuration control resulting in the need to
return to Mode 3, reconfigure, and restart the reactor.
Section 4OA5.2 Other Activities (TI 2515/152)
Procedures
MP/0/A/7150/165, Rx Vessel Bottom Head Bare Metal Inspection, Rev. 0
MP/0/A/7700/080, Inspection, Evaluation and Cleanup of Boric Acid on Plant Materials.
QAL-15, Inservice Inspection (ISI) Visual Exam, VT-2, Pressure Test, Rev 20, 7/22/02.
Other Documents
PIP M-03-04004 U2 Rx Vessel Bottom Head Bare Metal Inspection Results, 09/07/2003
PIP M-03-04096 Count Room Analysis of Smear Samples, 09/10/2003
LIST OF ACRONYMS
-
American Society of Mechanical Engineers
CA
-
-
CFR
-
Code of Federal Regulations
-
-
-
End-Of-Cycle
-
Emergency Procedure
-
Electric Power Research Institute
FWST
-
Fueling Water Storage Tank
GPM
-
Gallons Per Minute
-
Interim Compensatory Measures
IR
-
Inspection Report
-
Inservice Inspection
KC
-
Component Cooling Water
LER
-
Licensee Event Report
LCO
-
Limiting Condition of Operation
MGTM
-
-
Non-Cited Violation
ND
-
-
NEI
-
Nuclear Energy Institute
NS
-
NSD
-
Nuclear Site Directive
NV
-
Chemical and Volume Control
-
Performance Indicator
-
Problem Investigation Process Report
-
Power Operated Relief Valve
-
-
Pressurized Water Reactor
10
-
Quality Control
RN
-
Nuclear Service Water
SCV
-
Steel Containment Vessel
-
Significance Determination Process
-
Structures, Systems, Components
SSF
-
Standby Shutdown Facility
TI
-
Temporary Instruction
TS
-
Technical Specifications
-
Updated Final Safety Analysis Report
-
Unresolved Item
-
Ultrasonic Testing
WA
-
Work Around
-
Work Order
YC
-
Ventilation Chiller