ML033020363

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IR 05000302-03-005, on 06/29/2003 - 09/27/2003; Crystal River Unit 3; Fire Protection and Event Followup
ML033020363
Person / Time
Site: Crystal River 
Issue date: 10/27/2003
From: Joel Munday
NRC/RGN-II/DRP/RPB3
To: Young D
Florida Power Corp
References
FOIA/PA-2004-0277 IR-03-005
Download: ML033020363 (27)


See also: IR 05000302/2003005

Text

October 27, 2003

Mr. Dale E. Young, Vice President

Crystal River Nuclear Plant (NA1B)

ATTN: Supervisor, Licensing &

Regulatory Programs

15760 West Power Line Street

Crystal River, FL 34428-6708

SUBJECT:

CRYSTAL RIVER UNIT 3 - NRC INTEGRATED INSPECTION REPORT

05000302/2003005

Dear Mr. Young:

On September 27, 2003, the US Nuclear Regulatory Commission (NRC) completed an

inspection at your Crystal River Unit 3. The enclosed integrated inspection report documents

the inspection findings, which were discussed on September 29, 2003, with you and members

of your staff.

The inspection examined activities conducted under your license as they relate to safety and

compliance with the Commissions rules and regulations and with the conditions of your license.

The inspectors reviewed selected procedures and records, observed activities, and interviewed

personnel.

Based on the results of this inspection, there was one inspector identified finding and one self-

revealing finding of very low safety significance (Green). These findings were determined to

involve violations of NRC requirements. However, because of the very low safety significance

and because the violations were entered into your corrective action program, the NRC is

treating these violations as non-cited violations (NCVs) consistent with Section VI.A of the NRC

Enforcement Policy. Additionally, a licensee-identified violation which was determined to be of

very low safety significance is listed in Section 40A7 of this report. If you contest any of these

NCVs, you should provide a response within 30 days of the date of this inspection report, with

the basis for your denial, to the Nuclear Regulatory Commission, ATTN.: Document Control

Desk, Washington DC 20555-001; with copies to the Regional Administrator Region II; the

Director, Office of Enforcement, United States Nuclear Regulatory Commission, Washington,

DC 20555-0001; and the NRC Resident Inspector at Crystal River Unit 3.

FPC

2

In accordance with 10 CFR 2.790 of the NRCs "Rules of Practice," a copy of this letter and its

enclosure will be available electronically for public inspection in the NRC Public Document

Room or from the Publicly Available Records (PARS) component of NRCs document system

(ADAMS). ADAMS is accessible from the NRC Web site at

http://www.nrc.gov/reading-rm/adams.html (the Public Electronic Reading Room).

Sincerely,

/RA/

Joel T. Munday, Chief

Reactor Projects Branch 3

Division of Reactor Projects

Docket No.: 50-302

License No.: DPR-72

Enclosure: Inspection Report 05000302/2003005

w/Attachment: Supplemental Information

cc w/encl: (See page 3)

FPC

3

cc w/encl:

Daniel L. Roderick

Director Site Operations

Crystal River Nuclear Plant (NA2C)

Electronic Mail Distribution

Jon A. Franke

Plant General Manager

Crystal River Nuclear Plant (NA2C)

Electronic Mail Distribution

Richard L. Warden

Manager Nuclear Assessment

Crystal River Nuclear Plant (NA2C)

Electronic Mail Distribution

Donald L. Taylor

Manager Support Services

Crystal River Nuclear Plant (NA2C)

15760 W. Power Line Street

Crystal River, FL 34428-6708

R. Alexander Glenn

Associate General Counsel (MAC - BT15A)

Florida Power Corporation

Electronic Mail Distribution

Steven R. Carr

Associate General Counsel - Legal Dept.

Progress Energy Service Company, LLC

Electronic Mail Distribution

Attorney General

Department of Legal Affairs

The Capitol

Tallahassee, FL 32304

William A. Passetti

Bureau of Radiation Control

Department of Health

Electronic Mail Distribution

Craig Fugate, Director

Division of Emergency Preparedness

Department of Community Affairs

Electronic Mail Distribution

Chairman

Board of County Commissioners

Citrus County

110 N. Apopka Avenue

Inverness, FL 36250

Jim Mallay

Framatome Technologies

Electronic Mail Distribution

Distribution wencl: (See page 3)

FPC

4

Distribution w/encl:

B. Mozafari, NRR

L. Slack, RII EICS

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PUBLIC

OFFICE

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DATE

10/22/2003

10/27/2003

10/27/2003

10/23/2003

10/23/2003

E-MAIL COPY?

YES

NO YES

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NO YES

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PUBLIC DOCUMENT

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OFFICIAL RECORD COPY DOCUMENT NAME: C:\\ORPCheckout\\FileNET\\ML033020363.wpd

Enclosure

U.S. NUCLEAR REGULATORY COMMISSION

REGION II

Docket No.:

50-302

License No.:

DPR-72

Report No.:

05000302/2003005

Licensee:

Florida Power Corporation

Facility:

Crystal River Unit 3

Location:

15760 West Power Line Street

Crystal River, FL 34428-6708

Dates:

June 29, 2003 - September 27, 2003

Inspectors:

S. Stewart, Senior Resident Inspector

R. Reyes, Resident Inspector

N. Merriweather, Senior Reactor Inspector (4OA5)

R. Schin, Senior Reactor Inspector (4OA5)

Approved by:

Joel T. Munday, Chief

Reactor Projects Branch 3

Division of Reactor Projects

SUMMARY OF FINDINGS

IR 05000302/2003-005, 06/29/2003 - 09/27/2003; Crystal River Unit 3; Fire Protection and

Event Followup.

The report covered a three month period of inspection by resident inspectors and an

announced inspection by region based engineering inspectors. Two Green non-cited Violations

were identified. The significance of most findings is indicated by their color (Green, White,

Yellow, Red) using Inspection Manual Chapter (IMC) 0609, Significance Determination

Process (SDP). Findings for which the SDP does not apply may be Green or be assigned a

severity level after NRC management review. The NRC's program for overseeing the safe

operation of commercial nuclear power reactors is described in NUREG-1649, Reactor

Oversight Process, Revision 3, dated July 2000.

A.

Inspector Identified and Self-Revealing Findings

Cornerstone: Mitigating Systems

Green. A self-revealing non-cited violation of Crystal River 3 Technical Specification 3.7.18 was identified. Following Train B chiller maintenance on

December 19, 2002, and Train A chiller maintenance on February 25, 2003,

neither train of control complex cooling was operable because control complex

chiller motor overload relays had been improperly set below their design values.

The problem was identified on June 11, 2003, when both chiller motors tripped

on overload current, when an overload current condition had not occurred.

The self-revealing finding is greater than minor safety significance because it

resulted in a loss of the control complex cooling safety function and affected the

availability and reliability of the Mitigating Systems Cornerstone of Reactor

Safety that is used to mitigate events. The finding is of very low safety

significance because the alternate non-safety Appendix R cooling system and

feedwater pump (FWP-7) were available to mitigate transients involving systems

that could be affected by the loss of cooling. (Section 4OA3)

Green. The inspectors identified a non-cited violation of 10 CFR Part 50, Appendix R,Section III.G.2, Fire Protection of Safe Shutdown Capability, for

failure to protect certain electrical cables for safe shutdown equipment from fire

damage in three fire areas. The licensee has corrected related identified

procedural deficiencies and plans to resolve the noncompliance with cable

protection through licensing correspondence with the NRC.

This finding is greater than minor safety significance because it involved a lack of

required fire barriers for equipment relied upon for safe shutdown following a fire

and because it affected the objectives of the Mitigating Systems Cornerstone of

Reactor Safety. It affected the availability and reliability of systems that mitigate

initiating events to prevent undesirable consequences. The finding is of very low

safety significance because licensees proceduralized manual actions are

reasonably accomplishable and training would have enabled operators to

2

maintain the makeup function sufficiently to maintain reactor coolant system

process variables within acceptable ranges. Therefore, the inspectors identified

this issue as a Green finding as described in Inspection Procedure 71111.05,

Fire Protection. (Section 4OA5)

B.

Licensee Identified Violations

A violation of very low safety significance, which was identified by the licensee, has been

reviewed by the inspectors. Corrective actions taken or planned by the licensee have

been entered into the licensees corrective action program. The violation and corrective

action tracking number are listed in Section 4OA7 of this report.

REPORT DETAILS

Summary of Plant Status

Crystal River 3 operated at full power during the inspection period until September 6, 2003,

when a reactor power coastdown to refueling outage 13 was started. On September 14, 2003,

reactor power was reduced from 82 percent to 60 percent when a turbine throttle valve went

closed on a spurious signal. The control circuit for the valve was repaired and reactor power

was restored on the same day.

1.

REACTOR SAFETY

Cornerstones: Initiating Events, Mitigating Systems, Barrier Integrity [Reactor-R],

Emergency Preparedness [EP]

1R01

Adverse Weather Protection

a.

Inspection Scope

The inspectors monitored the licensees preparations for Tropical Storm Henri on

September 3 to 6, 2003. The licensee activities were checked to assure that vital

systems and components were protected from severe weather in accordance with

licensee Emergency Instruction EM-220, Violent Weather. During the preparations, the

inspectors walked down portions of the following systems/areas to verify the licensees

mitigation strategy. The inspectors attended a licensee Violent Weather Committee

meeting and reviewed the readiness checklists to verify that preparations were being

tracked to completion. Nuclear condition reports were reviewed to verify that the

licensee was identifying and correcting weather protection issues.

Emergency Feedwater system including EFP-3 and EFP-2

Emergency Diesel Generator Systems

Site Switchyard and Berm areas

b.

Findings

No findings of significance were identified.

1R04

Equipment Alignment

.1

Partial Equipment Walkdowns

a.

Inspection Scope

The inspectors performed the following partial system walkdowns during this inspection

period. The inspectors reviewed the alignment of the selected risk-significant systems to

evaluate the readiness of the redundant trains while one train was out of service for

maintenance. The inspectors checked switch and valve positions using the alignments

specified in the listed operating procedures and checked electrical power alignment to

critical components. The inspectors reviewed applicable sections of the Crystal River 3

2

Final Safety Analysis Report to obtain design and operating requirements. Nuclear

condition reports were reviewed to verify that the licensee was identifying and correcting

component alignment issues.

Emergency Diesel Generator EDG-1B using Operating Procedure OP-707,

Operation Of The ES Emergency Diesel Generators, when EDG-1A was out of

service for testing on August 14, 2003.

B Service Water Train using OP-408, Nuclear Services Cooling System, and

Flow Drawing FD-302-601, Nuclear Services Closed Cycle Cooling, when A

service water train was out of service to replace a timing relay per work order 105120, on July 18, 2003. (NCR 98630)

120 volt AC Vital Distribution using Operating Procedure OP-700D, Operation Of

The 120 Volt AC Vital Buses, when inverter VBIT-1E was out of service for

calibration and circuit replacement on September 8, 2003.

b.

Findings

No findings of significance were identified.

.2

Complete System Walkdown: On July 22 and 23, the inspectors conducted a detailed

review of the alignment and condition of the operable B train, emergency core cooling

system, including raw water, decay heat, decay heat removal, and building spray

systems, during a scheduled A train maintenance outage. The inspectors used plant

drawings and procedures, and the operating procedures (OP) and surveillance

procedures (SP) listed below, as well as applicable chapters of the Final Safety Analysis

Report (FSAR), to verify proper system alignment:

OP-700A

4160 ES Bus 3B

OP-404

Decay Heat Removal System

OP-405

Reactor Building Spray System

OP-408

Nuclear Services Cooling System

SP-347

ECCS And Boration Flow Paths

The inspectors verified selected electrical power requirements, labeling, hangers and

support installation, and associated support systems status. Operating pumps were

examined to ensure that vibration was not excessive, pump leakoff was not excessive,

and the pumps were properly ventilated. The walk downs also included evaluation of

system piping and supports against the following considerations:

Piping and pipe supports did not show evidence of water hammer.

Oil reservoir levels indicated normal.

Snubbers did not indicate any observable hydraulic fluid leakage.

Component foundations were not degraded

3

A review of outstanding maintenance work orders was performed to verify that the

deficiencies did not significantly affect the system function. In addition, the inspectors

reviewed the condition report (CR) database to verify that the systems equipment

alignment problems were being identified and appropriately resolved.

b.

Findings

No findings of significance were identified.

1R05

Fire Protection

a.

Inspection Scope

The inspectors walked down the following risk-significant plant areas to verify that

control of transient combustibles and ignition sources were consistent with the licensees

Fire Protection Plan and 10 CFR Part 50, Appendix R. The inspectors also evaluated

the material condition, operational lineup, and operational effectiveness of fire protection

systems and assessed material condition of fire barriers used to contain fire damage.

The inspections were completed using the standards of the Crystal River Fire Protection

Plan; 10 CFR Part 50, Appendix R; the Florida Power Corporation Analysis of Safe

Shutdown Equipment; and the Final Safety Analysis Report. The inspectors reviewed

sections of OP-880, Fire Service System, and checked performance of SP-802, Fire

Hose Hydrostatic Test, and SP-800, Monthly Fire Extinguisher Inspection, to monitor the

operational condition of fire protection equipment. When applicable, the inspectors

checked that compensatory measures for fire system problems were implemented. The

inspectors observed performance of fire alarm checks done in accordance with

surveillance procedure SP-323, Evacuation and Fire Alarm Demonstration.

Boric Acid Storage Tank Areas

Backup Engineered Safeguards Transformer, Start-up Transformer, Auxiliary

Transformer, and the A, B, and C Step-up Transformer areas

480-Volt Switch Gear Rooms

A and B EDG Engine Rooms and Compressor Rooms

Decay Heat Vaults including decay heat pump and heat exchanger areas

Fire Pump House

  1. 3 Emergency Feed Pump Building

Auxiliary Intermediate Building and Turbine Building Intermediate Building Roof

area

Main control room

b.

Findings

No findings of significance were identified.

4

1R06

Flood Protection Measures

a

Inspection Scope

The inspectors walked down the turbine and auxiliary building areas, including the decay

heat removal pump vaults, to ensure that flood protection measures were in accordance

with specifications described in the Final Safety Analysis Report. Specific attributes that

were checked included sealing of penetrations between flood areas, operability of

watertight doors, and the operability of the sump pumps. Additional flood protection

checks were done during severe weather preparations and documented in Section

1R01. The inspectors verified that minor deficiencies involving watertight seals and

other flood protection issues were documented in the licensees corrective action

program and corrected.

b.

Findings

No findings of significance were identified.

1R11

Licensed Operator Requalification

a.

Inspection Scope

On July 29, 2003, the inspectors observed licensed operator actions on the plant

specific simulator to Licensed Operator Continuing Training exercise LOR-1-17, Decay

Heat Removal Operations and LOR-1-05, Loss of Decay Heat Removal. The session

involved crew using plant procedures to establish decay heat removal system operations

from a forced circulation - steam dump condition, shifting decay heat removal system

loops of operations, and a response to a complete loss of the decay heat removal

system. The inspectors specifically evaluated the following attributes related to

operating crew performance.

Clarity and formality of communication including crew briefings

Ability to take timely action to safely control the unit

Prioritization, interpretation, and verification of alarms including a loss of decay

heat removal pump alarm

Correct use and implementation of procedures AP-404, Loss of Decay Heat

Removal, and OP-404, Decay Heat Removal System Operation

Control board operation and manipulation, including operator actions such as

establishing decay heat removal system operation from a two reactor coolant

pump operation configuration

Oversight and direction provided by supervision, including ability to identify and

implement appropriate technical specification actions

Effectiveness of the training oversight and critique

b.

Findings

No findings of significance were identified.

5

1R12

Maintenance Effectiveness

a.

Inspection Scope

The inspectors reviewed the planned maintenance activities listed below to evaluate the

licensees implementation of the maintenance rule (10CFR50.65). The inspectors

checked that licensee personnel monitored unavailability of equipment important to

safety and trended key performance parameters. For the equipment issues described

in the work orders (WO) listed below, the inspectors reviewed the licensees

implementation of the Maintenance Rule (10CFR50.65) with respect to the

characterization of failures, the appropriateness of the associated a(1) or a(2)

classifications, and the appropriateness of either the associated a(2) performance

criteria or the associated a(1) goals and corrective actions. The inspectors checked if

the licensee maintained safety functions when equipment important to safety was out of

service for maintenance. The inspectors also periodically reviewed the licensees

implementation of 10 CFR 50, Appendix B and technical specification requirements

regarding safety system problems. The inspectors routinely checked that the licensee

promptly entered problems with plant equipment into the corrective action program or

the corrective maintenance program. The inspectors checked that the licensee

monitored work practices and when appropriate, documented work problems in the

corrective action program.

The inspectors reviewed the goal settings and verified corrective actions had been

completed for the Substation System which had been entered into the maintenance rule

a(1). On August 27, the inspectors attended the Maintenance Rule expert panel

meeting to assess the licensees goal settings on the SW pump and the Control

Complex Chillers which had entered into the maintenance rule a(1) as a result of

unavailability and functional failures, respectively.

NCR 76622, Reactor Trip Due to Opening of the Main Generator Output Breaker

a(1)

NCR 95966, Control Complex Chilled Water System Failures a(1)

NCR 105249, Hi Vibrations on Air Handling Fan AHF-8B a(2)

b.

Findings

No findings of significance were identified.

1R13

Maintenance Risk Assessments and Emergent Work Evaluation

a.

Inspection Scope

The inspectors reviewed the following work risk assessments to assess the

effectiveness of licensees risk assessment and emergent work evaluation in

accordance with plant procedural requirements. The inspectors reviewed daily

maintenance schedules and observed work controls to check risk management while

maintenance was conducted. The inspectors assessed operability of equipment using

technical specifications, the Final Safety Analysis Report, licensee procedures, and

regulatory information such as NRC Generic Letter 91-18, Revision 1, Information to

6

Licensees Regarding NRC Inspection Manual Section on Resolution of Degraded And

Nonconforming Conditions. The inspectors also reviewed maintenance schedules to

check that overall risk was minimized through preservation of safety functions such as

decay heat removal capability, reactor coolant system inventory control, electric power

availability, reactivity control, and primary containment control. The inspectors checked

if licensee personnel were managing risk by assuring that key safety functions were

preserved and that upon identification of an unplanned situation, the resulting emergent

work was evaluated by the licensee for risk and controlled as described in technical

specifications, licensee Compliance Procedure CP-253, Power Operations Risk

Assessment and Management, and Administrative Instruction AI-500, Conduct of

Operations. The inspectors checked that risk significant emergent work was

documented in the corrective action program and that risk management actions were

promptly initiated.

Work Week 03W27, Risk assessment for planned B train ECCS outage revised

for emergent repairs to raw water pump RWP-130 (NCR 98198)

Work Week 03W28, Risk assessment for the EGDG-1A engine surveillance,

revised to repair the EGDG-1B jacket cooling water heater relay after failure

(NCR 98987)

Work Week 03W29, Risk assessment for Emergency Core Cooling System train

outage and piping replacement per clearance 55395 and work order 228448;

Elevated Risk Condition Yellow

Work Week 03W31, Risk assessment for Inspection and Lubrication of auxiliary

steam valve ASV-204, revised when makeup pump MUP-1A was removed from

service to troubleshoot and repair the bearing thermocouople MU-36-TE per

work request 339430

Work Week 03W32, Risk assessment revised when the 1A Control Complex

Chiller failed a post-maintenance test after maintenance had been performed per

work request 222359-01

Work Week 03W35, Risk assessment for planned maintenance on battery

charger DPBC-1B revised when main generator output breaker 1661 opened

and required troubleshooting and repairs (NCR103415)

b.

Findings

No findings of significance were identified.

1R14

Personnel Performance During Non-routine Plant Evolutions

a.

Inspection Scope

For the non-routine event described below, the inspectors observed the activity,

reviewed operator logs and plant computer data to determine that the evolution was

conducted safely and in accordance with plant procedures.

7

Reactor power reduction and withdrawal of Axial Power Shaping Rods (APSR)

completed on August 13, 2003, using operating procedure OP-502A, End of

Cycle APSR Withdrawal and Operations Department Communication 0308-03,

APSR Withdrawal.

b.

Findings

No findings of significance were identified.

1R15

Operability Evaluations

a.

Inspection Scope

The inspectors reviewed the following degraded or nonconforming conditions to

determine if operability of systems or components important to safety was consistent

with technical specifications, the Final Safety Analysis Report, 10 CFR Part 50

requirements, and when applicable, NRC Generic Letter 91-18, Revision 1, Information

to Licensees Regarding NRC Inspection Manual Section on Resolution of Degraded and

Nonconforming Conditions. The inspectors monitored licensee nuclear condition reports

(NCRs), work schedules, and engineering documents to check if operability issues were

being identified at an appropriate threshold and documented in the corrective action

program, consistent with 10 CFR 50, Appendix B requirements, and licensee procedure

NGGC-200, Corrective Action Program. The inspectors checked that when plant

problems were identified, the resulting change in plant risk was identified and managed.

The following issues, including the related nuclear condition reports (NCRs), were

specifically checked:

NCR 97889, Debris Found In The Reactor Building

NCR 98198, Through wall leak in raw water Socket Weld Between Pipe And

Valve RWV-130

NCR 98511, Ultimate Heat Sink Temperature High

NCR103426, Small Leak in service water pipe downstream of service water heat

exchangers

NCR 100231, Service Water Heat Exchanger SWHE-1D, divider plate is

degraded

b.

Findings

No findings of significance were identified.

1R16

Operator Workarounds

a.

Inspection Scope

On July 10, there were four operator work arounds (OWA) listed in the licensee OWA

list. The inspectors reviewed the activities associated with Operator Work Around

(OWA) SCV-23 Temperature Controller, and discussed it in detail with Operations

personnel. The recent work that had been completed in which a new controller had

8

been installed was reviewed with engineering. The planned post maintenance tests

associated with installation of the new controller were reviewed as well. The inspectors

reviewed the OWA list with reactor operators to determine if they were familiar with the

OWA and the required operational activities relating to each OWA.

Cumulative Effects

The inspectors performed a semi-annual evaluation of the potential cumulative effects of

all outstanding OWAs. At the time of the inspection, there were four OWAs. The

inspectors evaluated all outstanding OWAs for their cumulative effects, and discussed

these potential effects with control room supervision and operators. Furthermore, the

inspectors reviewed the current OOS logs and walked down the control room and plant

areas to verify OWAs were being identified and properly entered into the corrective

action program.

b.

Findings

No findings of significance were identified.

1R20

Refueling and Outage Activities

a.

Inspection Scope

The inspectors reviewed the Crystal River Unit 3, Refuel 13 Outage Risk Assessment

for the refueling outage planned to begin on October 3, 2003. The inspectors checked

that the risk assessment was based on the licensees outage schedule and consistent

with licensee requirements in Administrative Instruction AI-504, Guidelines for Cold

Shutdown and Refueling. The inspectors verified that during evolutions identified as

high risk, plans had been established for maintaining key safety functions such as

electrical power, reactivity control, reactor inventory control, and decay heat removal.

The inspectors checked that the risk assessment included industry experience and

previous site-specific problems and had been reviewed by management.

b.

Findings

No findings of significance were identified.

1R23

Temporary Plant Modifications

a.

Inspection Scope

The inspectors reviewed temporary modifications listed below to ensure that they did not

adversely affect the operation of a system that was altered. The inspectors screened

temporary plant modifications for systems that were ranked high in risk for departures

from design basis and for inadvertent changes that could challenge the systems to fulfill

their safety function. The inspectors conducted plant tours and discussed system status

with engineering and operations personnel to check for the existence of temporary

modifications that had not been appropriately identified and evaluated.

9

Engineering Change EC 49716, Reduce flow induced vibration for main steam

safety valves, MSV-33 through 48, by using a clamp to connect adjacent coils of

valve springs

Engineering Change EC 48830, Perform a sealant injection to reduce or

eliminate external leakage from the pressure seal ring of Decay Heat Valve

DHV-4

b.

Findings

No findings of significance were identified.

1RST Post-Maintenance and Surveillance Testing - Pilot

This pilot inspection procedure combines both post-maintenance and surveillance

testing activities.

a.

Inspection Scope

The inspectors observed or reviewed the following post-maintenance and surveillance

testing activities for risk significant systems to check the following (as applicable): (1)

the effect of testing on the plant had been adequately addressed; (2) testing was

adequate for the maintenance performed; (3) acceptance criteria were clear and

demonstrated operational readiness; (4) test instrumentation was appropriate; (5) tests

were performed as written; and (6) equipment was returned to its operational status

following testing. The inspectors evaluated the licensee activities against the technical

specifications, the Final Safety Analysis Report, 10 CFR Part 50 requirements, licensee

procedures, and various NRC generic communications. The inspectors routinely

checked that post maintenance testing and surveillance testing issues were resolved

and documented in the licensees corrective action program.

Inservice test (IST) activities were reviewed to ensure testing methods, acceptance

criteria, and corrective actions were in accordance with the ASME Code,Section XI, and

Florida Power Corporation ASME Section XI, Ten Year Inservice Testing Program,

dated May 4, 1998.

Post- Maintenance Testing

Work Order 339430-01, MUP-1A Radial Inboard Bearing Thermocouple

Replacement, testing of thermocouple and oil leak test

Surveillance Procedure SP-375A, CHP-1 And Valve Surveillance, after

performing preventive maintenance on the 1A Chiller

Surveillance Procedure SP-206, Visual Examination for Leakage, after replacing

raw water spool piece RW-84, including RWV-133 using work order WO 228448

Work Order 456040, data collection and engineering evaluation of vibration

following repair of air handling fan AHF-8B

10

Surveillance Testing

SP-130, Engineered Safeguards Monthly Functional Tests, performed on July 7,

2003

SP-349B, EFP-2 And Valve Surveillance, performed on August 6, 2003 (IST)

SP-363, Fire Protection System Tests, performed on August 6, 2003

SP-521, Quarterly Battery Check for 3B1 and 3B2 Station Batteries performed

on August 25, 2003

b.

Findings

No findings of significance were identified.

Cornerstone: Emergency Preparedness (EP)

1EP6

Drill Evaluation

a.

Inspection Scope

On July 23, 2003, the inspectors observed the site emergency response organization

respond to a tabletop scenario of a security threat to the Crystal River Nuclear Plant.

The tabletop was held in the emergency offsite facility, and participants included

representatives of the Federal Bureau of Investigation, Florida Department of Law

Enforcement, Florida Division of Emergency Management, and Citrus County and Levy

County emergency management personnel. During this scenario, the inspectors

assessed the licensees ability to classify an emergent situation, and make timely

notification to state and federal officials in accordance with 10 CFR Part 50.72.

Emergency activities were checked to be in accordance with the Crystal River

Radiological Emergency Response Plan, Section 8.0, Emergency Classification System,

and 10 CFR Part 50, Appendix E.

b.

Findings

No findings of significance were identified.

4.

OTHER ACTIVITIES

4OA1 Performance Indicator Verification

.1

Initiating Event and Mitigating Systems Cornerstone

a.

Inspection Scope

The inspectors checked the accuracy of the performance indicators for reactor coolant

system activity and leakage. Performance indicator data submitted from June 2002, to

June 2003, was compared for consistency to data obtained through the review of

chemistry department records, monthly operating reports, and control room records.

Surveillance Procedure SP-317, Reactor Coolant System Water Inventory Balance and

11

Chemistry Department Procedure, CHA-263, Dose Equivalent Iodine were reviewed.

Data gathering using both procedures was monitored. During routine plant tours, the

inspectors checked proper controls for plant personnel exposure and radioactive

releases. The inspectors checked the licensees compliance with station procedure CP-

155, Fuel Integrity Program and Failed Fuel Action Plan.

b.

Findings

No findings of significance were identified.

4OA2 Problem Identification and Resolution

Routine Problem Review

a.

Inspection Scope

The inspectors selected the following nuclear condition report (NCR) for detailed review

and discussion with the licensee. The report was examined to verify whether problem

identification was timely, complete and accurate; safety concerns were properly

classified and prioritized for resolution; technical issues were evaluated and

dispositioned to address operability and reportability; root cause or apparent cause

determinations were sufficiently thorough; extent of condition, generic implications,

common causes, and previous history were adequately considered; and appropriate

corrective actions were implemented or planned in a manner consistent with safety and

technical specification compliance. The inspectors evaluated the report against the

requirements of the licensees corrective action program in Administrative Procedures

CAP-NGGC-0200, Corrective Action Program and 10 CFR 50, Appendix B. Nuclear

Condition Reports 68148 and 68365 involving non-conforming conditions with the

station batteries, the January to June 2003 System Health Report regarding DC Electric

Power System, and the licensees (10 CFR 50.65) maintenance rule event data base

were also reviewed.

Nuclear Condition Report 64202: During performance of surveillance procedure,

SP-522, Station Battery Inspection, the inspection criteria could not be met due

to connection cleanliness and copper contamination

b.

Findings and Observations

There were no significant licensee performance issues or NRC violations identified by

the inspectors regarding the condition report. The inspectors verified that the apparent

cause evaluation and initial corrective actions were appropriate and timely in relation to

the safety significance of the problem. Long term corrective actions were appropriately

planned to maintain system readiness.

12

4OA3 Event Followup

(Closed) Licensee Event Report 05000302/2003-001-00, Incorrectly Set Motor Overload

Relays Result in Loss of Both Control Complex Chillers

a.

Inspection Scope The inspectors reviewed the LER and the associated nuclear

condition report (NCR 95966) to verify that the cause of the June 11, 2003, failure of

both trains of control complex chillers had been identified and that the corrective actions

were reasonable. The failure was caused when technicians incorrectly calibrated the

chiller motor overload relays due to inadequate work instructions. CHHE-1A motor

overload relays had been incorrectly set on February 25, 2003, and CHHE-1B on

December 19, 2002. The two units operated successfully until June 11, 2003, when a

failed component on the 1B chiller initiated a transient that resulted in both machines

being concurrently tripped on overload. Maintenance was required to return the chillers

to operation. The inspectors reviewed the licensees corrective actions described in the

LER, reviewed the nuclear condition report, and discussed the status of continuing

corrective actions with appropriate personnel. Florida Power letter 3F0902-06, License

Amendment Request #271, Revision 1, Revised Improved Technical Specification 3.7.18, for Two Inoperable Control Complex Chillers, dated September 20, 2002, was

used in the inspectors review.

b.

Findings

Introduction: A Green self-revealing finding of TS 3.7.18 was identified for failure to

maintain two operable control complex cooling trains due to incorrectly calibrated chiller

motor overload relays.

Description: The licensee determined that the root cause of the failure of both control

complex chillers was the incorrect calibration of the chiller motor overload relays. The

incorrect calibration was attributed to inadequate work instructions.

Analysis: The inspectors determined that the licensee failed to meet the requirement of

Technical Specification, Limiting Condition for Operability (LCO) 3.7.18, that states:

Two Control Complex Cooling trains shall be operable, when on December 19, 2002,

and February 25, 2003, overload protection relays for CHHE-1B, and CHHE-1A,

respectively were set below the design range. Because the incorrect calibration resulted

in the failure to meet a technical specification requirement and was attributed to

inadequate work instructions, it was a performance deficiency. The finding was greater

than minor because it was associated with the equipment performance attribute of the

mitigating systems cornerstone and affected the cornerstone objective of equipment

reliability. Because the finding involved a loss of safety function for the safety related

control complex cooling system, a Phase 2, Significance Determination was completed

using NRC Manual Chapter 0609, Appendix A. The most dominant core damage

sequences involved plant transients. For this finding, the inspectors assumed that the

Emergency Feedwater Isolation and Control (EFIC) system could be affected by the

loss of room cooling, and further assumed that no loss of emergency feedwater function

would occur because 1) the redundant Appendix R cooling system was available for

alignment to the EFIC control system room coolers, and 2) alternate feedwater was

13

available using either the main feedwater system, or the Feedwater Pump FWP-7

system. The finding was determined to be of very low safety significance (Green).

Enforcement: Technical Specification LCO 3.7.18, requires Two Control Complex

Cooling Trains shall be Operable. A cooling train consists of a chiller, a chill water

pump, and ducting to deliver cooling to safety related areas. Contrary to the above,

following Train B chiller maintenance on December 19, 2002, and Train A chiller

maintenance on February 25, 2003, neither train of control complex cooling was

operable because control complex chiller motor overload relays had been improperly set

below their design values. The problem was identified on June 11, 2003, when both

chiller motors tripped on overload current, when a design overload current condition had

not occurred. The licensee entered Technical Specification 3.0.3, and initiated a plant

shutdown when the problem was found. Maintenance was promptly conducted and the

A train chiller was returned to service on the same day. Chiller CHHE-1B was repaired

and returned to service on June 13, 2003. Because the failure to maintain an operable

control complex cooling train requirement was of very low safety significance and had

been entered into the licensees corrective action program (NCR 95966), this violation is

being treated as a Non Cited Violation (NCV), consistent with Section VI.A of the NRC

Enforcement Policy: NCV 05000302/2003005-01, Failure to Maintain Two Operable

Control Complex Cooling Trains. At the end of the inspection period, in addition to

having returned both trains of equipment to service, the licensee had completed an

extent of condition review and had summarized the occurrence to maintenance

personnel to prevent similar problems. Additional corrective actions were being tracked

in the licensees corrective action program. The LER is closed.

4OA5 Other

(Closed) Unresolved Item (URI)05000302/2002005-01, Failure to Protect One Train of

Safe Shutdown Equipment From Fire Damage in Accordance with Appendix R, Section

III.G.2 (Three Examples)

a.

Inspection Scope

This inspection followed up on URI 05000302/2002005-01, which had been opened for

NRC review of the local manual operator actions for three fire areas. The licensee had

relied on these operator actions instead of physically protecting electrical cables for the

makeup (high pressure injection) and emergency electrical power systems from fire

damage. The URI also described a concern with unprotected cables for a fire service

valve that could potentially degrade the response of the fire brigade. The URI was also

open for NRC review of the overall safety significance of the potential finding.

During this inspection, the inspectors reviewed the potential findings that were described

in the URI and also reviewed the licensees proceduralized local manual operator

actions for the three fire areas of concern for feasibility, using the guidance of NRC

Inspection Procedure 71111.05, Enclosure 2. To accomplish this review, the inspectors

inspected the three fire areas of concern and walked down all of the local manual

operator actions for the three fire areas. The inspectors also reviewed cable routings of

concern in the three fire areas, design information for affected equipment, fire brigade

procedures, and records of previous fire drills in the fire areas of concern. In addition,

14

the inspectors discussed the plant design, procedures, and staffing with licensee

operators and engineers and evaluated the safety significance of identified deficiencies

and findings.

b.

Findings

Introduction. A Green non-cited violation (NCV) of 10 CFR 50, Appendix R,

Section III.G.2, Fire Protection of Safe Shutdown Capability, was identified for failure to

protect certain electrical cables for safe shutdown equipment from fire damage in three

fire areas.

Description. The inspectors identified that the licensee had failed to protect certain

electrical cables, for equipment that was relied upon for safe hot shutdown, from fire

damage. The affected equipment included:

Electrical control cables for makeup system motor-operated valves (MOVs)

MUV-23, -24, -25, and -26 (which were in parallel in the required flowpath) were

not protected from fire damage in fire areas CC-108-102 [hallway and remote

shutdown room on the 108 foot elevation of the control complex] and CC-108-

107 [3B 4160 volt engineered safeguard switchgear room on the 108 foot

elevation of the control complex]. At least one of these valves should have been

protected from fire damage because one was needed to establish and maintain

a makeup flowpath to the reactor coolant system (RCS) for safe hot shutdown.

Electrical control cables for makeup pump (MUP) 1A, 1B, and 1C were not

protected from fire damage in fire area CC-108-106 [battery charger room 3A on

the 108 foot elevation of the control complex]. MUP 1C should have been

protected as it was relied upon, per the licensees safe shutdown analysis and

procedures, to supply makeup to the RCS for safe hot shutdown.

Electrical control cables for MUP flow recirculation MOVs MUV-53 and MUV-257

(which were in series in the required flowpath and affected all three MUPs) were

not protected from fire damage in fire areas CC-108-102 and CC-108-107,

respectively. Both valves should have been protected from fire damage to

ensure that the MUP minimum flow recirculation flowpath would be available as

needed for safe hot shutdown.

After reviewing the potential effects of cable damage due to fire, the system design, and

the operating procedures, the inspectors found that even with these unprotected

electrical cables and some deficient operator actions, licensee procedures and training

would have enabled operators to maintain the makeup function as needed for safe

shutdown following a fire in fire areas CC-108-102, -106, or -107. [The deficient

operator actions involved locally manually repositioning MOVs that were vulnerable to

spurious actuations and failing to open the power supply breakers to the MOVs, leaving

the MOVs still vulnerable to spurious actuations.] The inspectors evaluated that with the

proceduralized operator actions, the makeup function would have been sufficient to

maintain reactor coolant system process variables within acceptable ranges. The

inspectors also noted that the licensee had corrected all of the identified deficient

operator actions in the current revision of the procedure. In addition, the licensee

15

planned to resolve the noncompliance with cable protection through licensing

correspondence with the NRC. These factors limited the safety significance of the

licensees failure to physically protect the cable from fire damage as required by 10 CFR 50, Appendix R,Section III.G.2.

The inspectors determined that some other concerns described in the URI should not be

considered as findings, as described below:

Electrical cables for emergency diesel generators (EDGs) 1A and 1B were not

protected from fire damage in fire area CC-108-106; however, the licensees

safe shutdown analysis and procedures did not rely on the EDGs. The licensee

had determined that offsite power would not be affected by a fire in fire area CC-

108-106 and would be available for safe shutdown. Inspector review of selected

electrical circuits did not identify any flaws in the licensees determination that

offsite power would be unaffected by the fire.

Electrical cables for fire service valve FSV-257 were not protected from fire

damage in the fire areas of concern. The inspectors verified that this could delay

the fire brigade by about three minutes in pressurizing a fire hose from a fire

station in the control building. However, by procedure and also by actual

practice during fire drills, the fire brigade brought a second fire hose that would

be pressurized from the turbine building. That hose would be unaffected by

FSV-257. Since the fire brigade needed only one hose, they would not be

delayed by damage to FSV-257 cables. The inspectors verified that the hose

from the turbine building, plus an additional 50 feet of hose from the fire brigade

cart, would provide sufficient length and water pressure to fight fires in all of the

fire areas of concern. The inspectors also verified that fire brigade response

time during drills was less than the acceptance criteria, such that a three-minute

delay to locally manually open FSV-257 would not result in the fire brigade being

considered degraded.

Analysis. The inspectors determined that the licensees failure to protect the electrical

cables for certain makeup system components from fire damage was a performance

deficiency because the licensee failed to comply with the requirements of 10 CFR 50, Appendix R,Section III.G.2. This finding is greater than minor safety significance

because it involved a lack of required fire barriers for equipment relied upon for safe

shutdown following a fire and because it affected the objectives of the Mitigating

Systems Cornerstone of Reactor Safety. The finding affected the availability and

reliability of systems that mitigate initiating events to prevent undesirable consequences.

The inspectors determined that manual actions are reasonably accomplishable and

licensee procedures and training would have enabled operators to maintain the makeup

function sufficiently to maintain reactor coolant system process variables within

acceptable ranges. Therefore, the inspectors identified this issue as a Green finding as

described in Inspection Procedure 71111.05, Fire Protection.

Enforcement. 10 CFR 50, Appendix R,Section III.G.2 requires in part that where cables

or equipment, that could prevent operation or cause maloperation due to hot shorts,

open circuits, or shorts to ground, of redundant trains of systems necessary to achieve

and maintain hot shutdown conditions are located within the same fire area outside of

16

primary containment, one of the following means of ensuring that one of the redundant

trains is free of fire damage shall be provided: a) physical protection by a three-hour fire

barrier, b) physical protection by a separation of more than 20 feet, with no intervening

combustibles or fire hazards, plus fire detectors and automatic suppression, or c)

physical protection by a one-hour fire barrier plus fire detectors and automatic

suppression.

Contrary to the above, the licensee failed to protect cables that could prevent operation

or cause maloperation due to hot shorts, of redundant trains of systems necessary to

achieve and maintain hot shutdown conditions, from fire damage by one of the

prescribed methods. This nonconforming design was identified by NRC inspectors in

July 2002 and had been in existence for years. Because this failure to protect cables is

of very low safety significance and has been entered into the licensees corrective action

program as Non-Conformance Report (NCR) No. 061781; this violation is being treated

as an NCV, consistent with Section VI.A of the NRC Enforcement Policy: NCV 0500302/2003005-02, Failure to Protect One Train of Safe Shutdown Equipment From

Fire Damage.

4OA6 Meetings, Including Exit

Exit Meeting Summary

The fire protection specialist inspectors presented their inspection results (Section

4OA5) to Mr. D. Young and other members of the licensees staff on September 12,

2003. The licensee acknowledged the findings presented. Proprietary information is

not included in the inspection report.

The resident inspectors presented the inspection results to Mr. Young and other

members of licensee management at the conclusion of the inspection on September 29,

2003. The inspectors asked the licensee whether any of the material examined during

the inspection should be considered proprietary. The licensee did not identify any

proprietary information.

4OA7 Licensee Identified Violation

The following violation of very low safety significance (Green) was identified by the

licensee and is a violation of NRC requirements which meets the criteria of Section VI of

the NRC Enforcement Policy, NUREG-1600, for being dispositioned as an Non-Cited

Violation.

Crystal River 3 Technical Specification 5.6.1, requires that the procedures

recommended in Regulatory Guide 1.33, Revision 2, Appendix A, be implemented. The

regulatory guide, in Paragraph 9.a, specifies procedures for performing maintenance on

safety related equipment. Crystal River 3, Work Order 456040 required for the post-

maintenance test on safety-related air handling fan, AHF-8B, vibration analysis by

engineering. Contrary to the above, on September 23, 2003, AHF-8B was returned to

service following maintenance under Work Order 456040, without completion of

vibration analysis by engineering. Instead, engineering evaluated the running AHF-8A

and reported the results to plant operators. The discrepancy was identified during the

17

next operations shift turnover, plant status review. The vibration analysis was then

conducted the same day, and when evaluated, it was determined to be unsatisfactory

for vibrations and re-work was authorized. The finding was of very low safety

significance because it was identified within a few hours of occurrence and the

redundant fan, AHF-8A, remained available. There was no actual safety consequence.

The occurrence is documented in the licensee corrective action program as NCR

105249.

Attachment

SUPPLEMENTAL INFORMATION

KEY POINTS OF CONTACT

Licensee personnel:

J. Huegel, Acting Manager, Operations

S. Bernhoft, Supervisor, System Engineering

W. Brewer, Manager, Work Controls

R. Davis, Manager, Training

J. Franke, Plant General Manager

J. Kreuhm, Manager, Maintenance

D. Roderick, Director Site Operations

S. Glenn, Supervisor, Corrective Actions Program

S. Powell, Supervisor, Licensing

M. Rigsby, Radiation Protection Manager

J. Stephenson, Supervisor, Emergency Preparedness

J. Terry, Manager, Engineering

R. Warden, Manager, Nuclear Assessment

D. Young, Vice President, Crystal River Nuclear Plant

S. Young, Security Manager

NRC personnel:

J. Munday. Chief, Reactor Projects Branch 3, NRC Region II

J. Riveria-Ortiz, NRC Intern

LIST OF ITEMS OPENED AND CLOSED

Opened and Closed

05000302/2003005-01

NCV

Failure to Maintain Two Operable Control Complex

Cooling Trains (Section 4OA3)05000302/2003005-02

NCV

Failure to Protect One Train of Safe Shutdown

Equipment From Fire Damage (Section 4OA5)

Closed

05000302/2002005-01

URI

Failure to Protect One Train of Safe Shutdown

Equipment From Fire Damage in Accordance with

Appendix R,Section III.G.2 (Three Examples)

(Section 4OA5)

05000302/2003-001-00

LER

Incorrectly Set Motor Overload Relays Result in

Loss of Both Control Complex Chillers (Section

4OA3)

2

LIST OF DOCUMENTS REVIEWED

Section 4OA5, Other

Procedures

AR-801, Fire System Annunciator Response, Rev. 17

AP-880, Fire Protection, Rev. 15

AP-880, Fire Protection, Rev. 19

Emergency Plan Implementing Procedure, EM-216, Duties of the Fire Brigade, Rev. 23

OP-880A, Appendix R Post-Fire Safe Shutdown Information, Rev. 0

OP-880A, Appendix R Post-Fire Safe Shutdown Information, Rev. 3

Drawings

E-213-013, 10 CFR 50 Appendix R Protected Raceways, Control Complex El. 108-0, Rev. 13

FD-302-661, Make-up & Purification, Sheet 2 of 5, Rev. 74

FD-302-661, Make-up & Purification, Sheet 3 of 5, Rev. 76

FD-302-661, Make-up & Purification, Sheet 4 of 5, Rev. 76

Analyses and Calculations

Crystal River Unit 3 Fire Hazards Analysis, Rev. 11

Crystal River 3 Individual Plant Examination of External Events, Rev. 1