ML031060288

From kanterella
Jump to navigation Jump to search
IR 05000220-03-003, on 02/10/2003 - 03/08/2003; Nine Mile Point, Unit 1; Special Inspection Team of Degraded Piping in the Reactor Building Closed Loop Cooling System
ML031060288
Person / Time
Site: Nine Mile Point 
(DPR-063)
Issue date: 04/15/2003
From: Lanning W
Division of Reactor Safety I
To: Conway J
Nine Mile Point
References
-nr, EA-03-053 IR-03-003
Download: ML031060288 (30)


See also: IR 05000220/2003003

Text

April 15, 2003

EA-03-053

Mr. John T. Conway

Vice President Nine Mile Point

Nine Mile Point Nuclear Station, LLC

P.O. Box 63

Lycoming, NY 13093

SUBJECT:

NINE MILE POINT NUCLEAR STATION - NRC SPECIAL INSPECTION

REPORT 50-220/03-003 - PRELIMINARY WHITE FINDING

Dear Mr. Conway:

On March 7, 2003, the NRC completed a special inspection of the Nine Mile Point Nuclear

Station, Unit 1. The enclosed report documents the inspection findings which were discussed

at the completion of the inspection with you and other members of your staff during an exit

meeting on March 7, 2003.

This inspection examined activities conducted under your license as they relate to safety and

compliance with the Commissions rules and regulations and with the conditions of your license.

The team reviewed selected procedures and records, observed activities, and interviewed

personnel. In particular, the inspection reviewed event evaluations, including technical

analyses, root cause investigation, relevant performance history, and extent of condition to

assess the significance and potential consequences of the degraded condition of the reactor

building closed loop cooling (RBCLC) system.

This report discusses a finding that appears to have low to moderate safety significance. As

described in Section 4OA3 of this report, this finding involves inadequate implementation of

corrective actions for significantly degraded piping in the RBCLC system. There were

numerous prior opportunities to identify and correct this problem. This finding was assessed

using the reactor safety Significance Determination Process (SDP) as a potentially safety

significant finding that was preliminarily determined to be White (i.e., a finding with some

increased importance to safety, which may require additional NRC inspection). The finding has

low to moderate safety significance because a pipe rupture in the RBCLC system could result in

an initiating event and loss of certain equipment necessary to mitigate plant transients and

accidents.

Following identification of the degraded piping, you implemented appropriate corrective actions

by replacing most of the RBCLC system piping located in the drywell with improved hardware

and design. With these compensatory measures in place while long term corrective actions are

being developed, our inspectors determined that an immediate safety hazard does not exist.

John T. Conway

2

The finding also appears to be an apparent violation of NRC requirements and is being

considered for escalated enforcement action in accordance with the General Statement of

Policy and Procedure for NRC Enforcement Actions (Enforcement Policy), NUREG-1600. The

current Enforcement Policy is included on the NRCs Website at http://www.nrc.gov/what-we-

do/regulatory/enforcement.html.

We believe that we have sufficient information to make our final risk determination for the

performance issue regarding inadequate corrective action for the degraded RBCLC system.

However, before the NRC makes a final decision on this matter, we are providing you an

opportunity to either submit a written response or to request a Regulatory Conference where

you would be able to provide your perspectives on the significance of the finding, the bases for

your position, and whether you agree with the apparent violation. If you choose to request a

Regulatory Conference, we encourage you to submit your evaluation and any differences with

the NRC evaluation at least one week prior to the conference in an effort to make the

conference more efficient and effective. If a Regulatory Conference is held, it will be open for

public observation. The NRC will also issue a press release to announce the Regulatory

Conference.

Please contact Mr. James M. Trapp at (610) 337-5186, within 10 business days of the date of

this letter to notify the NRC of your intentions. If we have not heard from you within 10 days, we

will continue with our significance determination and enforcement decision and you will be

advised by separate correspondence of the results of our deliberations on this matter.

Since the NRC has not made a final determination in this matter, no Notice of Violation is being

issued for this inspection finding at this time. In addition, please be advised that the number

and characterization of the apparent violation described in the enclosed inspection report may

change as a result of further NRC review.

In accordance with 10 CFR 2.790 of the NRC's "Rules of Practice," a copy of this letter and its

enclosures will be available electronically for public inspection in the NRC Public Document

Room or from the Publicly Available Records (PARS) component of NRCs document system

(ADAMS). ADAMS is accessible from the NRC Web site at http://www.nrc.gov/reading-

rm/adams.html (the Public Electronic Reading Room).

If you have any questions, please contact Mr. Trapp at (610) 337-5186.

Sincerely,

/RA/

Wayne D. Lanning, Director

Division of Reactor Safety

Docket No.

50-220

License No.

DPR-63

Enclosures:

1) Inspection Report 50-220/03-003 w/Attachment: Supplemental Information

2) NRC Special Inspection Team Charter

John T. Conway

3

cc w/encl:

M. J. Wallace, President, Nine Mile Point Nuclear Station, LLC

M. Wetterhahn, Esquire, Winston and Strawn

J. M. Petro, Jr., Esquire, Counsel, Constellation Power Source, Inc.

P. D. Eddy, Electric Division, NYS Department of Public Service

C. Donaldson, Esquire, Assistant Attorney General, New York

Department of Law

J. V. Vinquist, MATS, Inc.

W. M. Flynn, President, New York State Energy Research

and Development Authority

Supervisor, Town of Scriba

C. Adrienne Rhodes, Chairman and Executive Director, State Consumer Protection Board

T. Judson, Central NY Citizens Awareness Network

John T. Conway

4

Distribution w/encl:

H. Miller, RA/J. Wiggins, DRA

F. Congel, OE (RidsOeMailCenter)

W. Kane, DEDR (RidsEdoMailCenter)

B. Borchardt, NRR (RidsNrrAdip)

D. Dambly, OGC (RidsOgcMailCenter)

S. Figueroa, OE (RidsOeMailCenter)

D. Holody, ORA

R. Urban, ORA

J. Trapp, DRP

T. McGinty, RI EDO Coordinator

R. Laufer, NRR

P. Tam, PM, NRR

D. Skay/T. Colburn, PM, NRR (Backup)

G. Hunegs, SRI - Nine Mile Point

B. Fuller, RI - Nine Mile Point

N. Perry, DRP

K. Kolek, DRP

Region I Docket Room (with concurrences)

W. Lanning, DRS

R. Crlenjak, DRS

R. Lorson, DRS

S. Pindale, DRS

DOCUMENT NAME: G:\\PEB\\PINDALE\\NMP2003003.WPD

After declaring this document An Official Agency Record it will be released to the Public.

To receive a copy of this document, indicate in the box: "C" = Copy without attachment/enclosure "E" = Copy with attachment/enclosure "N" = No copy

OFFICE

RI/DRS

RI/DRS

RI/DRS

RI/DRP

RI/ORA

NAME

SPindale

RLorson

ECobey

JTrapp

RUrban

DATE

03/27/03

04/15/03

03/27/03

03/27/03

03/27/03

OFFICE

RI/DRS

NAME

WLanning

DATE

04/15/03

04/ /03

04/ /03

04/ /03

04/ /03

OFFICIAL RECORD COPY

ENCLOSURE 1

U.S. NUCLEAR REGULATORY COMMISSION

REGION I

Docket No:

50-220

License No:

DPR-63

Report No:

50-220/03-003

Licensee:

Nine Mile Point Nuclear Station, LLC (NMPNS)

Facility:

Nine Mile Point, Unit 1

Location:

P. O. Box 63

Lycoming, NY 13093

Dates:

February 10, 2003 - March 7, 2003

Inspectors:

S. Pindale, Senior Reactor Inspector (Team Leader)

S. Chaudhary, Reactor Inspector

E. Cobey, Senior Reactor Analyst

E. Knutson, Resident Inspector

Approved by:

James M. Trapp, Chief

Projects Branch 1

Division of Reactor Projects

ii

SUMMARY OF FINDINGS

IR 05000220/2003-003; 02/10/2003 - 03/08/2003; Nine Mile Point, Unit 1; Special Inspection

Team of Degraded Piping in the Reactor Building Closed Loop Cooling System.

The inspection was conducted by two regional inspectors, one resident inspector, and one

regional senior reactor analyst. One preliminary White finding was identified. The significance

of most findings is indicated by their color (Green, White, Yellow, Red) using IMC 0609,

Significance Determination Process (SDP). Findings for which the SDP does not apply may

be Green or be assigned a severity level after NRC management review. The NRCs program

for overseeing the safe operation of commercial nuclear power reactors is described in

NUREG-1649, Reactor Oversight Process, Revision 3, dated July 2000.

A.

Inspector Identified and Self-Revealing Findings

Cornerstones: Initiating Events and Mitigating Systems

Preliminary White. An apparent violation of 10 CFR 50, Appendix B,

Criterion XVI, Corrective Action, was identified by the team associated with the

failure to evaluate significant conditions adverse to quality involving degraded

piping in the reactor building closed loop cooling (RBCLC) system. The failure to

adequately identify and evaluate equipment problems, and correct deficiencies,

resulted in repetitive and continued degraded piping conditions in the RBCLC

system. Specifically, a RBCLC system piping leak occurred on May 15, 2002,

due to significant pipe corrosion, primarily as a result of inadequate piping

design, application and operation. Additionally, numerous RBCLC system leaks

occurred during several preceding years. However, the cause for these leaks

was not determined and appropriate corrective actions were not implemented.

This led to further degradation of the RBCLC system piping such that additional

significant leaks occurred on December 5, 2002, and again on December 12,

2002. These significant leaks in December 2002 were accompanied by a

significant reduction in the pipe wall which degraded the structural integrity of the

affected piping sections.

This finding has low to moderate safety significance, based on the results of the

phase three SDP analysis, because the degraded RBCLC piping resulted in an

increase in the likelihood of the loss of the RBCLC system due to piping failure,

which directly affected the initiating events cornerstone. The loss of the RBCLC

system would also result in the loss of cooling to several other risk significant

systems (e.g., feedwater/condensate pumps, recirculation pumps, shutdown

cooling heat exchangers, etc.) following a loss of coolant accident or a loss of all

AC power event where AC power is recovered prior to core damage, which

directly affected the mitigating systems cornerstone. (Section 4OA3.4; AV 50-

220/03-03-01)

REPORT DETAILS

Summary of Plant Status

The reactor building closed loop cooling (RBCLC) system provides cooling for various reactor

auxiliary equipment, as well as balance of plant equipment. Major components supplied by the

system included the drywell air coolers, reactor recirculation pump coolers, reactor building

equipment drain tank cooler, fuel pool heat exchangers, shutdown cooling system, control room

air conditioning equipment, instrument air compressors, and the high pressure injection system

(i.e., feedwater pumps, feedwater booster pumps, and condensate pumps). The RBCLC

system is a safety-related, risk-significant system that is required to operate during normal plant

operations and accident conditions.

In May 2002, and again on December 5 and 12, 2002, the licensee experienced substantial

leaks in RBCLC small bore (less than 2" diameter) piping. Following evaluation and analysis of

these leaks, the licensee discovered notable and widespread wall thinning in RBCLC piping

sections, which were most severe at threaded mechanical connections (where piping thickness

was the smallest due to the thread roots). This reduction in wall thickness was ultimately

attributed to a combination of general corrosion, flow-assisted corrosion, and galvanic

corrosion.

Prior to 2002, there had been numerous additional small bore piping leaks within the RBCLC

system at threaded mechanical joints. Repair methods for these leaks varied, and included

tightening the connection or fittings, replacing components (such as flow switches), seal

welding the threaded connections, and replacing affected pipe sections. Around May 2000,

chloride and sulfate concentrations in the RBCLC system were found to be elevated. Near the

same time, RBCLC system oxygen levels were found to be significantly below normal levels,

and iron particulate levels were high. These parameters indicated an increased corrosion rate,

however, efforts to identify the cause and correct the abnormal chemistry parameters were

unsuccessful.

The NRC teams review of the event details determined the root and contributing causes for the

degraded RBCLC piping included: inadequate system design, inadequate corrective actions,

and degraded RBCLC system water chemistry. Subsequent to the December 12, 2002, leak,

several immediate corrective actions were implemented, including extensive RBCLC small bore

piping and fitting replacement with improved piping material and design. Longer term similar

actions were also in progress for the remaining RBCLC piping sections that had not been

replaced. In addition, the licensee was continuing their efforts to determine the cause and

corrective actions for the unexpected and unexplained chemistry parameters.

The performance deficiency was the failure, prior to December 12, 2002, to determine the

cause of a significant condition adverse to quality and implement appropriate corrective actions

to prevent further degradation of the RBCLC system. The NRC team determined that the

licensees structural analysis did not provide evidence that the as-found condition of the

degraded piping in the RBCLC system retained sufficient strength, and consequently, the

structural integrity of the affected RBCLC system piping may not have been maintained when

subjected to design loading conditions. The safety significance of the inspection finding, based

on the increase in core damage frequency due to internal and external initiating events, was

determined to be White, which represents a finding of low to moderate safety significance.

2

4.

OTHER ACTIVITIES (OA)

4OA3 Event Followup

1.

Degraded RBCLC Piping Due to Corrosion

a.

Inspection Scope

This inspection was conducted in accordance with NRC Inspection Procedure 93812,

Special Inspection, to assess the licensees actions associated with the December 5

and 12, 2002, discovery of two instances where portions of the RBCLC piping were

significantly corroded such that leaks occurred in the system. The licensee conducted

event evaluations following each incident to determine the root cause and corrective

actions. The team reviewed the associated design basis documents, calculations, and

other related documents. A list of the documents reviewed by the team is provided as

Attachment 1 to this report.

The team reviewed aspects of the historical performance of the RBCLC system relative

to prior leaks and associated licensee actions and evaluations. The team also

examined portions of degraded RBCLC piping that had been removed from the system,

walked down portions of the system, and interviewed licensee personnel.

Chronology of System Leakage

The RBCLC system piping was designed and installed in accordance with the B31.1-

1955 Code for Pressure Piping. The pipe was Schedule 40 carbon steel and threaded

connections were used for many of the small bore piping connections. The nominal wall

thickness for 1-1/2 inch diameter Schedule 40 and 80 pipe is 0.145 and 0.200 inches,

respectively. The use of threaded connections reduces the nominal wall thickness as

the threads are cut into the pipe, thereby further reducing the pipe wall thickness at the

root of the threads. In addition, the system also contained several dissimilar metal joints

(e.g., carbon steel to stainless steel; and carbon steel to bronze) at several of the piping

connections. While this was not prohibited by the piping design code, direct connection

(without insulating barriers) of dissimilar metals can lead to galvanic corrosion.

The team reviewed documentation of RBCLC system leaks dating back to 1991. In July

1991, the unit was shut down to investigate increased drywell leakage. The source of

the leakage was RBCLC from the recirculation pump seal coolers. At that time, a total

of seven out of ten recirculation pump seal cooler threaded pipe connections were found

to be leaking. These connections consisted of threaded pipe joints, as opposed to

welded pipe sections. The licensee attributed the leakage, as documented in deviation

event report (DER) 1991-0560, to thermal expansion and vibration which caused the

mechanical connections to loosen. The licensee determined the root cause of the event

to be an inadequate system design.

3

In February 1992, DER 1992-0480 documented that the long term corrective actions of

DER 1991-0560 had not been implemented. The corrective action in this DER

recommended that the long term corrective actions from DER 1991-0560 should be

implemented prior to closing DER 1992-0480. Despite continuing issues with

recirculation pump seal cooler leaks through the 1990s (as documented in DER 2002-

2383), this recommendation was not implemented, and modification N1-80-83 was

subsequently canceled in 1994.

In September 2000, two recirculation pump seal cooler leaks were identified and

documented in DER 2000-3268. Both leaks were from threaded connections between

the RBCLC piping and the coolers. The cause of the leaks (i.e., whether the leakage

was through the mechanical joints or through-wall degradation of the piping) was not

positively identified. However, the DER noted that attempts to stop the leak by

tightening the connections were unsuccessful. Both leaks were repaired by seal

welding.

During a mid-cycle outage in May 2002 to investigate drywell leakage, two significant

RBCLC leaks were identified in the drywell, as documented in DER 2002-2383. One

leak was from a recirculation pump seal cooler mechanical joint. Again, the cause of the

leak was not positively identified, although attempts to tighten the joint did not stop the

leakage. This leak was repaired by seal welding. The other leak was from the

downstream threaded connection to a flow switch in RBCLC piping to the 14

recirculation pump. This leak was repaired by replacing the flow switch and the

immediate upstream and downstream piping. Subsequent vendor analysis identified the

apparent cause of the flow switch leak as galvanic corrosion of the downstream pipe,

due to dissimilar metals in the flow switch and the piping. Flow turbulence downstream

of the flow switch continually exposed fresh metal and allowed the galvanic action to

progress to failure. Although the results of the vendor analysis results were available in

July 2002, they were not factored into the corrective action process and, consequently,

were not addressed until after the subsequent RBCLC leaks were identified in

December 2002.

On December 5, 2002, Unit 1 shut down to investigate an increase in unidentified

drywell leakage. The source was found to be RBCLC system leakage from the

threaded joint on the downstream side of the outlet check valve from the 11 drywell

equipment drain tank cooler. The apparent cause, as identified in DER 2002-5166, was

a combination of galvanic corrosion between dissimilar metal components (bronze

check valve, carbon steel piping) and turbulent flow downstream of the check valve.

The leak was repaired by eliminating the check valve and replacing the associated

piping. Additional actions associated with this DER included the following:

Eliminating the outlet check valve from the other (12) drywell equipment drain

tank cooler;

Replacing susceptible pipe assemblies at the outlet of the recirculation pump

motor and seal cooler lines, and eliminating check valves and dissimilar metal

joints;

4

Completing seal welding of RBCLC lines to the recirculation pump seal coolers;

and

Replacing flow switches and connecting piping for the two recirculation pumps

that had not had this done within the last four years.

One week later, on December 12, 2002, a leak was identified at the RBCLC inlet

connection to the 11 drywell cooler heat exchanger. The leak was from the threaded

connection of a pipe nipple to a threaded elbow, originating in a pinhole at the root of the

exposed portion of the threads. The licensee (DER 2002-5280) identified that the

apparent cause for this leak was general corrosion combined with the tapered threads

on the original construction Schedule 40 piping. This threaded joint was not a dissimilar

metal joint (it was all carbon steel).

In response to the most recent problem, the unit was shut down. The corrective action

for this leak was to replace all drywell air cooler inlet and outlet piping. Additional

actions associated with DER 2002-5280 included replacement of the majority of RBCLC

piping inside the drywell with Schedule 80 piping using welded (rather than threaded)

connections. The recirculation pump motor cooler piping was determined to be in good

condition and was not replaced; and the upstream piping to the equipment drain tank

was determined to be acceptable until the refueling outage scheduled for Fall 2004.

RBCLC Chemistry Control

In early 2000, unexplained changes in the RBCLC water chemistry parameters began to

occur. Over a period of several months, the dissolved oxygen concentration decreased

from its normal value of about 3000 ppb (parts per billion) to essentially zero.

Subsequently, in June 2000, DER 2000-2139 was written to document an increase in

RBCLC water conductivity, and chloride and sulfate concentrations. Typically, such

changes are the result of service water system leakage into the RBCLC system.

Attempts to identify the source of the chloride and sulfate contamination have been

unsuccessful to date. Contaminant concentrations have, for the most part, been

maintained within specification by performing system feed-and-bleeds (i.e., purging the

water volume in the system). The cause for the oxygen depletion has not been

determined. The feed-and-bleed evolution used aerated water (oxygen concentration

on the order of 3000 ppb), however, the RBCLC oxygen concentration remained

approximately zero. This indicated that some process was continuing to consume the

dissolved oxygen. The licensee had also identified elevated concentrations of soluble

and insoluble iron in the RBCLC water since the year 2000, which was consistent with

the oxygen depletion mechanism being the result of corrosion.

5

2.

Root and Contributing Causes of Degraded RBCLC Piping

a.

Inspection Scope

The team reviewed the licensees event evaluation reports and cause analyses

associated with the RBCLC system pipe leaks and degraded piping. The team also

independently assessed the root and causal factors for the event. The team reviewed

data and corrective action program documents, conducted plant tours, and interviewed

personnel, including station management.

b.

Findings

The team concluded that the licensees cause evaluations prior to the December 12,

2002, leak did not effectively evaluate the observed degraded piping. The licensees

actions, subsequent to this leak, have included a comprehensive cause investigation

and also an evaluation to determine how the organizational and cultural environment

affected previous attempts to correct this problem. The licensee appropriately identified

that general corrosion, galvanic cells, and flow-assisted corrosion degraded the RBCLC

system integrity and led to the leaks.

The licensees investigation identified several preliminary findings, including: station

personnel did not use effective problem solving techniques; weaknesses in technical

rigor/justification; high standards for thorough problem solving were not reinforced; and

personnel did not demonstrate judicial use/application of failure analysis examinations.

The NRC teams review of the event details determined the following regarding the root

and contributing causes for the degraded RBCLC piping:

Inadequate System Design: The use of threaded (vs. welded) connections with

Schedule 40 piping (nominal wall thickness of 0.145") resulted in a thin base

material at the piping connections, particularly at the roots of the threads.

Dissimilar metals in various system components resulted in galvanic corrosion

which, in some cases, accelerated the wall loss of the internal piping surface to

the point of loss of adequate structural integrity and through-wall leakage.

Inadequate Corrective Actions: In 1991, DER 1991-0560 identified threaded

connections at the recirculation pump seal coolers as a system design deficiency

and recommended corrective action to implement a previously identified

modification (N1-80-83) to redesign the connections. However, this corrective

action was initially not acted upon, as identified by DER 1992-0480, and

ultimately was canceled. Corrective actions associated with several of the leaks

consisted, in part, of seal welding at the threaded pipe joints. This action was

superficial in that it only eliminated the immediate symptom (the leak) and made

no attempt to identify the root cause of this significant condition adverse to

quality. In addition, the failure analysis for the leaking flow switch, which

identified galvanic corrosion and turbulent flow as the cause of failure, was not

factored into the corrective action program, and therefore, was not promptly

acted upon. Corrective actions associated with the December 5, 2002 leak,

while more extensive than in previous cases, were still not adequate to identify

6

the root cause of the system degradation and to prevent the additional failure,

that occurred one week later.

Degraded RBCLC System Water Chemistry: Actions over about two years have

been unsuccessful in identifying the source of chloride and sulfate

contamination, and the cause for the oxygen depletion. While the cause of

these issues remains unknown, they apparently have contributed to accelerated

system degradation through corrosion, as evidenced by the coincident increase

in soluble/insoluble iron content of the water. Attempts to identify the source of

dissolved hydrogen and nitrogen have also been unsuccessful.

While the licensees recent efforts to identify the root and contributing causes of

degraded RBCLC piping were acceptable after the December 12, 2002 leak, some of

the causes remained undetermined. In particular, the licensee has not yet been able to

identify the source of the abnormal chemistry parameters in the RBCLC system. The

licensees efforts were continuing in this area to identify and diagnose the RBCLC

system abnormal chemistry parameters.

3.

Structural Integrity of RBCLC Degraded Piping

a.

Inspection Scope

The team interviewed personnel, conducted a partial system walkdown, and reviewed

the licensees engineering evaluations associated with the structural integrity of the as-

found condition of the 1-1/2" diameter degraded piping in the RBCLC system to

independently assess the condition of the degraded RBCLC system piping. In

particular, the team reviewed the licensees preliminary evaluation of the system

structural integrity as documented in engineering report NER-1S-031, Rev. 00A. The

licensee evaluated the condition that they determined represented the worst case

condition. This evaluation considered the pipe degradation, and RBCLC system static

and dynamic loading (including additional loading potentially caused by transients

initiating in other systems).

The limiting location was the circumferential ligament adjacent to the section where the

December 5, 2002, leak occurred. It was located in the threaded area of the RBCLC

piping one thread adjacent to the leak. Engineering report NER-1S-031 documented

evaluations pertaining to the following:

Failure analysis of a section of 1-1/2" diameter pipe installed at the RBCLC

return line from the 11 drywell sump cooler (105-04) between check valve CKV-

70-362 and ball valve VLV-70-363;

7

Collapse load analysis for the above pipe to determine the collapse moment

capacities for various temperature conditions and sustained loads (dead weight

plus operating loads). The method used in calculating collapsing moment were

per Appendix F of ASME Code,Section III;

Piping analysis for pipe between line No. 105-04 and the 4" diameter header

pipe; and

A comparison of applied moments to the calculated collapsing moment

capacities for the applicable loading conditions:

-

Load Case a: Dead weight, design pressure 125 psig, normal RBCLC

system operating temperature 100F, and 0.05 maximum ground

acceleration for seismic loads.

-

Load Case b: Dead weight, design pressure 125 psig, and a drywell

temperature of 240F as a result of a small break loss of coolant

accident.

-

Load Case c: Dead weight, transient pressure of 142 psig, combined

with a drywell temperature of 215F as a result of a loss of offsite power

event.

The results of the piping analysis documented in NER-1S-031 were used as input to an

inelastic finite element analysis using the ANSYS Computer Program for the various

load conditions. This analysis was used to evaluate the structural integrity of the

existing ligament geometry in the threaded piping section.

b.

Findings

The licensee determined the collapse moment capacity and the applied moment for

each of the three load cases. The collapse moment capacity relates to the calculated

strength of the RBCLC piping, based upon material properties. Inherent in the

licensees analysis was that they assumed the remaining material in the measured

ligament (after the significant corrosion occurred), retained the properties of the original

piping/metal material. The applied moments were calculated for each of the loads that

would result in these cases. The analysis assumed that the integrity of the pipe would

not be maintained if the applied moment exceeded the collapse moment.

The calculated collapse moment capacities (criteria) and applied moments are

summarized in the following table (Note: all units are ft-lbs).

8

Load Case

Calculated collapse moment

capacity (Criterion)

Criterion, including

measurement tolerance

Applied

moment

a

37.8

36.6

37

b

42

40.7

40

c

42

40.7

38

Although the applied moment exceeded the collapse moment capacity for load case a,

the licensee stated that the applied moment was within 1% of the reduced collapse

moment capacity (criteria above).

The licensee stated that there was no leak evident at the ligament that was analyzed

(downstream of bronze check valve CKV-70-362). They concluded that this location

and configuration was a critical section and was the worst case (and bounding) for the

purpose of analysis. They also concluded that the critical piping section would retain

sufficient structural integrity to prevent collapse of the piping when subjected to the

design loading conditions. While the team did not identify a location or configuration

that would be more bounding, the team determined the absence of leak was not an

indication of structural integrity and/or loading capacity. Further, a leak can be

prevented by a barrier that does not have any significant structural capacity.

The team identified several additional concerns associated with the licensees analysis,

assumptions, and methodology. For example, the pipe wall thickness assumed in the

finite element analysis was a very thin ligament at the root of the pipe thread, and in

some cases, only a few thousandths of an inch. The material behavior in thin ligaments

may be significantly different than that assumed in the analysis. Very thin carbon steel

material may not exhibit the homogenous isotropic behavior assumed in the licensees

analysis; the grain size of the metal significantly affects the structural properties. The

material properties assumed in the analysis was based on the original certified material

test report (CMTR) supplied with the piping purchase order.

In addition to the above uncertainties in the material properties, there are potential of

negative cumulative errors in wall thickness measurements, i.e. magnification and

calibration tolerance/error in the electron microscope, and the caliper or other measuring

tools and equipment.

The removed section of the pipe was visually examined by the inspection team to

assess the material condition. The removed sections indicated a highly corroded piping

section with missing thread root. Even where the material was not missing, a flash light

illumination indicated a material ligament so thin that it appeared nearly translucent.

The team also learned that a full section of the pipe was able to be broken apart

manually following removal by maintenance personnel.

Finally, the team noted that the licensees analyses and evaluations were based on

assumptions that had not been substantiated by test and/or verifiable data. As such, the

licensees results were considered preliminary by the licensee and their consultants.

9

In summary, although the RBCLC system remained in operation and functional during

the operating cycle, the team concluded that the licensees evaluation did not provide an

adequate basis to demonstrate that the piping in the RBCLC system retained sufficient

structural strength/integrity when subjected to loading conditions during postulated

events. In addition, the team concluded that a passive failure of the degraded RBCLC

piping was a dominant failure mode, which resulted in an increased likelihood of a loss

of RBCLC initiating event.

4.

Corrective Actions

a.

Inspection Scope

The team interviewed licensee personnel, reviewed related corrective action program

documents, and reviewed associated licensee evaluations associated with the degraded

piping. The adequacy, extent and timeliness of the licensees corrective actions were

also assessed.

b.

Findings

Corrective Actions Implement for RBCLC Leakage

In December 2002, the licensee identified significant and widespread degradation of the

RBCLC system piping due to corrosion. This degradation occurred despite numerous

prior opportunities to identify, determine the root causes and correct the condition.

Leaks had occurred over the previous several years due to significant degradation of

small bore piping (less than 2" diameter), and a failure of this size line would result in

failure of the RBCLC system.

The team determined that the leaks that occurred on May 15, 2002, represented an

opportunity to recognize the potential significant degradation of the RBCLC system.

The more significant of the two leaks occurred at a threaded connection on the

downstream side of a flow switch associated with one of the five recirculation pump

coolers. The second leak at a threaded mechanical pipe connection associated with

another recirculation pump cooler was seal welded. At that time, the licensee attributed

those leaks to inherent leakage associated with threaded connections and noted that

leaks at the pipe connections for the seal cooling piping to and from the recirculation

pumps had been a chronic problem for many years. They failed to adequately evaluate

the cause and extent of the degraded condition. Further, the licensee failed to evaluate

an associated flow switch failure analysis report (performed by a vendor), which was

dated July 29, 2002, and provided relevant insights regarding the nature and extent of

the corrosion in the RBCLC system. This failure analysis was not included in the

licensees corrective action process, and therefore, was not adequately reviewed.

The December 5, 2002, leak also represented an opportunity for the licensee to perform

a detailed cause analysis and implement comprehensive corrective actions. This leak

was located adjacent to the 11 equipment drain cooler discharge check valve. The

licensee concluded that the carbon steel pipe was experiencing wall thinning on the

downstream side at and near threaded connections to either bronze or austenitic

stainless steel components, and that this degradation due to galvanic corrosion was

10

accelerated due to turbulent flow conditions. The area at the threaded connection that

showed the most severe degradation consisted of a very thin ligament of corroded

metal. Although the licensee identified several RBCLC pipe areas for further inspection

and repair, these actions failed to properly identify and characterize the cause and

extent of the degradation mechanism. Specifically, the licensee failed to recognize that

general internal pipe corrosion contributed substantially to the pipe wall thinning, and

that the inspection scope for susceptible piping areas should have extended beyond

dissimilar metal, turbulent flow interfaces.

Soon after the startup from the December 5, 2002, forced outage, another leak occurred

on December 12, 2002. The investigation of this leak revealed additional RBCLC piping

that was substantially degraded. During the extent of condition evaluation, the licensee

again identified wall thinning due to corrosion. However, in this instance, a dissimilar

metal and galvanic corrosion mechanism was not present. The licensee had not

previously considered that the carbon steel to carbon steel connections may also exhibit

significant corrosion. Further, the effect of threads on pipe wall thickness in conjunction

with the pipe wall thinning (absent a galvanic mechanism) had not been considered

during the previous evaluations.

Assessment of Corrective Actions

In evaluating the RBCLC system leak history and associated licensee corrective actions,

the team made several observations. In particular, the team determined that the

licensees efforts in response to the problems over the years were focused on fixing

symptoms (leaks) rather than identifying causes, determining extent of condition, and

implementing effective corrective actions. For example, the team observed the

following:



For the RBCLC system leaks identified in May 2002 and earlier, the apparent

causes did not consider mechanisms other than leakage across the threads.

DER 2002-2383 stated that it is expected that threaded piping connections that

are not seal welded will leak over an extended period of time. The cause

analysis was not sufficiently rigorous to identify that the Schedule 40 pipe wall

thickness at the threaded area was significantly less than the rest of the system.

Therefore, the cause analysis, extent of condition assessment and scope of

repairs were not sufficient to preclude additional RBCLC leakage.



Seal welding was proposed and implemented on threaded connections as a

housekeeping measure. This activity could potentially stop an active leak as a

temporary measure. However, because seal welding is not designed or credited

to restore structural integrity, it could also mask significant internal degradation

and allow continued internal corrosion to further degrade the structural integrity

of the pipe.



The licensee recognized the degraded chemistry parameters in the RBCLC

system (high chloride and sulfate concentration, low oxygen, high iron), existed

for over two years, however, the cause of these conditions had not been

identified. The licensees feed-and-bleed activities of the system only

temporarily and marginally improved the chemistry conditions.

11



In 1980, a modification was initiated to eliminate certain RBCLC threaded

connections in the drywell (in particular, threaded joints in recirculation pump

coolers to eliminate a possible leakage source). However, the modification was

not installed, and was canceled in 1994 based on low priority and continued

satisfactory system performance (two successful operating runs).

The team reviewed the licensees corrective actions following the December 12, 2002

leak (after the licensee fully recognized the cause and extent of condition). Several

immediate corrective actions were implemented. These activities included extensive

replacement of RBCLC piping and fittings inside the drywell. The majority of RBCLC

fittings and pipe (about 90%) was replaced with the more robust schedule 80 piping.

The remaining piping was determined to be acceptable through calculations in

combination with ultrasonic and visual inspections. Also, the new piping sections were

connected by welded joints (except in some cases, where prohibited by physical

interference problems).

Longer term similar actions are also in progress for RBCLC piping located outside the

drywell. The licensee similarly evaluated the existing condition of the RBCLC piping

outside the drywell by ultrasonic and visual inspections, and concluded that there was

sufficient pipe wall thickness and structural integrity to support interim continued

operation of the RBCLC system. Current licensee plans are to replace all 3" and

smaller diameter RBCLC system piping (inside and outside the drywell) with Schedule

80 welded joint piping within two years. The licensee performed testing and conducted

an evaluation and determined that the larger than 3" piping was not subject to a similar

type of failure mechanism. Regarding the chemistry issues, the licensee has been

developing an action plan to identify the source of loss of oxygen (oxygen injection and

detection), and the source of the other elevated parameters. The team found the

licensees completed and planned corrective actions to be appropriate.

Performance Assessment

The licensees failure, prior to December 12, 2002, to determine the cause of a

significant condition adverse to quality and implement corrective action to prevent

repetition, despite prior opportunities to do so, was a performance deficiency. This

failure allowed the RBCLC system to continue to degrade due to several factors,

including inadequate design and poor system chemistry. The system degraded

significantly due to general corrosion, galvanic corrosion, and flow-assisted corrosion.

In accordance with Inspection Manual Chapter (IMC) 0612, Appendix B, Issue

Disposition Screening, the team determined that the issue was more than minor

because the issue was associated with the equipment performance attribute of both the

initiating events and mitigating systems cornerstones. The significantly degraded

RBCLC piping resulted in an increase in the likelihood of the loss of the RBCLC system

due to piping failure, which directly affected the initiating events cornerstone. The loss

of the RBCLC system would also result in the loss of cooling to the feedwater and

condensate pumps, the recirculation pumps, the drywell coolers, the shutdown cooling

heat exchangers, and two of three instrument air compressors following a loss of

coolant accident or a loss of all AC power (SBO) event where AC power is recovered

12

prior to core damage, which directly affected the mitigating systems cornerstone.

Section 4OA3.5 discusses the risk analysis and assessment associated with this finding.

Enforcement

Title 10 to CFR Part 50, Appendix B, Criterion XVI, Corrective Action, requires, in part,

that measures shall be established to assure that conditions adverse to quality are

promptly identified and corrected. In the case of significant conditions adverse to

quality, the measures shall assure that the cause of the condition is determined and

corrective action taken to prevent repetition. Contrary to this requirement, when

significant conditions adverse to quality occurred prior to, and on May 15, 2002,

involving degraded RBCLC system piping, the licensee failed to determine the cause

and the extent of the condition and failed to take appropriate corrective actions to

prevent recurrence. Specifically, an RBCLC system piping leak occurred on May 15,

2002, due to significant pipe corrosion, primarily as a result of a inadequate piping

design, application and operation. Additionally, numerous RBCLC system leaks

occurred during several preceding years. However, the cause of this condition was not

determined and corrective actions were not taken, and as a result, corrosion continued

to further degrade RBCLC system piping such that additional significant leaks occurred

on December 5, 2002, and again on December 12, 2002. These significant leaks in

December 2002 exhibited severe pipe wall loss and degraded the structural integrity of

the affected piping sections. This was an apparent violation of 10 CFR 50, Appendix B,

Criterion XVI. (AV 50-220/03-003-01)

5.

Risk Significance and Analysis of Event

a.

Inspection Scope

The team evaluated the licensees safety and availability assessment of the degraded

condition of the RBCLC system, including the associated assumption and evaluation

criteria, analysis methodology, and design inputs. The team also performed an

independent risk assessment of the finding related to the degraded RBCLC system.

The team evaluated the duration of the degraded condition, and the safety implications

associated with the cause of the degradation. The team also interviewed the cognizant

licensee risk, engineering, and operations personnel.

13

b.

Findings

SDP Phase 1:

In accordance with NRC IMC 0609, Appendix A, Significance Determination of Reactor

Inspection Findings for At-Power Situations, the team conducted a significance

determination process (SDP) Phase 1 screening and determined that the finding

degraded both the initiating event and mitigating systems cornerstones. Therefore, a

SDP Phase 2 evaluation was required.

SDP Phase 2:

The SDP Phase 2 process was not designed to estimate the risk significance of a

finding that resulted in an initiating event that induces a second initiating event.

SDP Phase 3:

Internal Initiating Events:

The NRCs Standardized Plant Analysis Risk (SPAR) model, Revision 3.01, was used to

evaluate the significance of this finding. The team determined that the SPAR model

needed to be revised to link the loss of RBCLC event tree and the anticipated transient

without scram (ATWS) event tree and to reflect the possibility of a recirculation pump

seal leak following the loss of the RBCLC system. This revision resulted in an increase

in the baseline core damage frequency from 7.88E-6 per year to 7.91E-6 per year.

Assumptions:

1.

The performance deficiency existed for in excess of a year. Therefore, the team

used an exposure time of 1 year.

2.

The RBCLC system piping was significantly degraded and lacked adequate

structural integrity. Therefore, the dominant failure mode of the RBCLC system

involved a passive failure of the piping which resulted in an increase in the

likelihood of a loss of RBCLC initiating event. The initiating event frequency was

determined by taking into account the existing failure modes of the system, the

lack of structural integrity of the piping, the numerous leaks from the RBCLC

piping over the years, and the likelihood of a leak before break in the piping.

Applying engineering judgement, the team concluded that the loss of RBCLC

initiating event frequency was approximately 5.0E-2 per year.

3.

Loss of coolant accidents and SBO events result in drywell temperatures that

induce thermal stresses in the RBCLC piping in excess of the structural

capability of the piping. Therefore, the team used a conditional failure probability

of 1.0 for the RBCLC system in these events.

4.

Failure of the RBCLC piping would result in the inability to remove heat from the

recirculation pump seals. Without cooling, the likelihood of a recirculation pump

seal leak increased substantially. Therefore, the team used a seal failure

14

probability of 0.5, which was based on the licensees recirculation pump seal

package test results.

5.

Failure of the RBCLC piping would result in system leakage in excess of the

automatic makeup capability for the system. Consequently, the RBCLC

expansion tank level would be lost and the operating RBCLC pumps would fail

due to inadequate net positive suction head (NPSH).

The team did not credit recovery of the RBCLC system because under certain

entry conditions, Annunciator Response Procedure N1-ARP-H1, Control Room

Panel H1, directed the starting of the standby RBCLC pump; and Annunciator

Response Procedure N1-ARP-H1, Special Operating Procedure N1-SOP-8,

RBCLC Failure, and Operating Procedure N1-OP-11, Reactor Building Closed

Loop Cooling System, did not provide guidance to secure the operating RBCLC

pumps when inadequate NPSH existed. Also, no procedural guidance existed to

isolate an RBCLC leak and recover the RBCLC system. In addition, because

each of the dominant accident sequences involved the failure of operator actions

prior to when RBCLC would have been recovered, the likelihood of the failure of

the operators to recover RBCLC would be dependent on those prior failures.

Consequently, the team considered the likelihood of the operators failure to

recover the RBCLC system too high to credit.

The team revised the SPAR model to reflect these assumptions, determined a revised

core damage frequency for the exposure period (1.32E-5 per year) and calculated the

change in core damage frequency ( CDF) for this finding due to internal initiating

events.

CDF = [(1.32E-5 per year) - (7.91E-6 per year)]

= 5.29E-6 per year (White)

15

This result was dominated by the following accident sequences.

Contributio

n

to CDF

Core Damage Sequence Description

4.03E-6

 IE - Loss of RBCLC due to the degraded piping condition

 Instrument air (IA) fails following the loss of RBCLC

 RCS inventory is lost via either a stuck open SRV or unisolated

recirculation pump seal leaks

 Condensate and feedwater fail due to loss of RBCLC

 Operators successfully depressurize to low pressure

 Core Spray successfully provides inventory control

 Suppression Pool Cooling fails due to loss of IA

 Shutdown Cooling fails due to loss of RBCLC

 Containment spray fails

 Containment venting fails due to loss of IA

5.71E-7

 IE - Small break loss of coolant accident (SLOCA)

 RBCLC fails due to the degraded piping condition following the SLOCA

 IA fails following the loss of RBCLC

 Condensate and feedwater fail due to loss of RBCLC

 Operators successfully depressurize to low pressure

 Core Spray successfully provides inventory control

 Suppression Pool Cooling fails due to loss of IA

 Containment spray fails

 Containment venting fails due to loss of IA

5.26E-7

 IE - Loss of RBCLC due to the degraded piping condition

 IA fails following the loss of RBCLC

 Condensate and feedwater fail due to loss of RBCLC

 Emergency condensers fail

 Operators successfully depressurize to low pressure

 Core Spray successfully provides inventory control

 Suppression Pool Cooling fails due to loss of IA

 Shutdown Cooling fails due to loss of RBCLC

 Containment spray fails

 Containment venting fails due to loss of IA

6.80E-8

 IE - Loss of RBCLC due to the degraded piping condition

 IA fails following the loss of RBCLC

 RCS inventory is lost via two or more stuck open SRVs

 Condensate and feedwater fail due to loss of RBCLC

 Core Spray successfully provides inventory control

 Suppression Pool Cooling fails due to loss of IA

 Shutdown Cooling fails due to loss of RBCLC

 Containment spray fails

 Containment venting fails due to loss of IA

16

External Initiating Events:

The Nine Mile Point Unit 1 probabilistic risk assessment (PRA) model U1PRA01B, dated

February 2002, includes external initiating events (e.g., seismic and fire initiating

events). Therefore, the team evaluated the results obtained using the licensees PRA

model to determine the risk contribution of the significantly degraded RBCLC piping due

to external initiating events.

Seismic:

The Nine Mile Point Unit 1 PRA model has six categories of seismic events. The model

uses the EPRI seismic hazards curves to estimate the frequencies of each of these

events. The baseline seismic-induced CDF is approximately 1.25E-6 per year. The

licensees PRA documentation stated that the model results using the Lawrence

Livermore National Laboratory seismic hazard curves would be higher by approximately

a factor of five.

The team concurred with the licensees conclusion that the significantly degraded

RBCLC piping would fail during any seismic event of 0.05g or greater in magnitude.

The licensee revised their PRA model to reflect this degraded condition and determined

that the increase in seismic-induced CDF was approximately 1.03E-7 per year. This

result was dominated by a seismic-induced loss of offsite power, failure of the RBCLC

piping, failure of instrument air, and failure to remove decay heat from containment.

The team reviewed the results and concluded that the results were reasonable and that

seismic events did not contribute significantly to CDF.

Fire:

The team determined that there were no fire scenarios that would result in conditions

that would fail the significantly degraded RBCLC piping. In addition, the team

determined that the significantly degraded RBCLC piping did not adversely impact the

mitigation of any fire events. Therefore, the team concluded that fire events did not

contribute significantly to CDF.

High Winds, Floods, and Other External Events (HFO):

The team determined that there were no HFO events that would result in conditions that

would fail the significantly degraded RBCLC piping. In addition, the team determined

that the significantly degraded RBCLC piping did not adversely impact the mitigation of

any HFO events. Therefore, the team concluded that HFO events did not contribute

significantly to CDF.

17

Potential Risk Contribution due to Large Early Release Frequency:

In BWR Mark I containments, only a subset of core damage accidents can lead to large,

unmitigated releases from the containment that have the potential to cause prompt

fatalities prior to population evacuation. Core damage sequences of concern for BWR

Mark I containments are inter-system loss of coolant accident, ATWS, SLOCA, and

transient sequences. Because the dominant accident sequences for the case involving

the significantly degraded RBCLC piping were transient and SLOCA sequences, the

finding was screened for its potential risk contribution to large early release frequency

(LERF). Using NRC Inspection Manual Chapter 0609, Appendix H, Containment

Integrity SDP, the team determined that the dominant accident sequences did not result

in a contribution to LERF because these sequences resulted in core damage following

containment failure due to a loss of containment heat removal. Thus, evacuation of the

population would have been carried out in sufficient time so that these accident

sequences would not have resulted in a contribution to LERF.

Licensees Risk Assessment:

The licensee performed a risk evaluation of the degraded RBCLC piping and concluded

that the CDF was 9.0E-7 per year and the LERF was 7.5E-8 per year. The team

reviewed the licensees results and concluded that the differences were primarily

attributable to a difference in three assumptions.

First, the licensee assumed that the RBCLC piping was degraded, but it retained

structural integrity for all initiating events except loss of coolant accidents, loss of drywell

cooling events, and seismic events greater than 0.05g in magnitude. The licensee did

not assume that the likelihood of the loss of RBCLC initiating event increased due to the

condition of the RBCLC piping. The team evaluated the licensees assumption and

concluded that it was not the most appropriate assumption for the condition.

Second, the licensee assumed that the RBCLC system would fail at one preferential

location and that the recirculation pump seals would be cooled by the boil off of the

water that would remain in the system following the pipe rupture. As a result, the

licensee assumed that the likelihood of the recirculation pump seal leak remained

unchanged. The team evaluated the licensees assumption and concluded that there

was no basis to assume that the RBCLC piping would fail at one preferential location

and that the remaining water in the system would adequately cool the recirculation pump

seals. As a result, the team evaluated the licensees assumption and concluded that it

was not the most appropriate assumption for the condition.

Lastly, the licensee assumed that recovery of the RBCLC and IA systems was possible

to provide long term heat removal from containment. The licensee assumed that the

likelihood of the operators failure to recover the RBCLC system was 0.1. The licensee

based this assumption largely on the time available to perform the recovery actions and

reliance on assistance from the Technical Support Center and the Emergency

Operations Facility. The team evaluated the licensees assumption and concluded that

it was not the most appropriate assumption for the condition for the reasons described

above (Phase 3 Assumption 5).

18

Analysis - Conclusion:

The safety significance of the inspection finding based on the increase in core damage

frequency due to internal and external initiating events is White ( CDF = 5.39E-6 per

year). The safety significance of the inspection finding based on the increase in large

early release frequency is Green ( LERF < 1.0E-7 per year). Therefore, the safety

significance of the inspection finding is White. A White finding represents a finding of

low to moderate safety significance.

4OA5 Other

(Closed) URI 50-220/2002-06-02: RBCLC System Piping Degradation Due to

Corrosion. This item was opened to evaluate the safety and risk significance of the

degraded condition of the RBCLC system. This NRC special inspection team performed

this evaluation, and identified associated licensee performance deficiencies as

documented in this inspection report. Therefore, this item is closed, and further tracking

and follow-up of this issue will be accomplished via the enforcement tracking/violation

open item identified in this report (See Section 4OA3.4 of this report).

4OA6 Meetings, including Exit

The inspectors presented the inspection results to Mr. J. Conway, Vice President, Nine

Mile Point, and other members of licensee management at the conclusion of the onsite

inspection on February 14, 2003, and on March 7, 2003, upon completion of the

combined onsite and in-office inspection activities. The licensee acknowledged the

findings presented. The team reviewed some proprietary documents during the

inspection, and these documents were identified and discussed by the NRC at the exit

meeting. Based upon subsequent discussions with the licensee, none of the information

presented at the exit meeting and included in this report was considered proprietary.

ATTACHMENT 1

KEY POINTS OF CONTACT

Licensee Personnel

M. Alvi, Lead Engineer, Design Structural

K. Churchill, System Engineer

K. Embry, Licensing Engineer

T. Kulczycky, Principle Engineer, Reliability Engineering

T. Kurtz, Engineering Services

B. Montgomery, Manager, Engineering Services

J. Murphy, Engineer, Mechanical Design

B. Randall, General Supervisor, System Engineering

J. Richards, Manager, Chemistry

NRC Personnel

G. Hunegs, Senior Resident Inspector, NMP

J. Trapp, Chief, Projects Branch 1, Region I

LIST OF ITEMS OPENED, CLOSED, AND DISCUSSED

Opened

50-220/2003-03-01

AV

Failure to Determine the Cause of a Significant Condition Adverse

to Quality and Implement Corrective Action to Prevent Repetition,

Associated with Severe Corrosion of the RBCLC System.

Closed

50-220/2002-06-02

URI

RBCLC System Degradation

LIST OF DOCUMENTS REVIEWED

Drawings:

C-18011-C

Instrument Air System P&I Diagram, Sheet 1, Rev. 48

C-18018-C

Reactor Shutdown Cooling System P&I Diagram, Sheet 1, Rev. 25

C-18022-C

RBCLC System P&I Diagram, Sheet 2, Rev. 43

C-18022-C

TBCLC System P&I Diagram, Sheet 3, Rev. 30

C-18298-C

RBCLC System Piping at Drywell Air Coolers and Equipment Drain Sump Pit

Coolers, Rev. 6

C-18299-C

RBCLC System Piping at Drywell Air Coolers and Equipment Drain Sump Pit

Coolers, Rev. 5

C-26855-C

RBCLC System No. 70 Piping Isometric, Rev. 2

Attachment 1 (contd)

2

Calculations:

S13.4-70-TP15

RBCLC, Rev. 0

Licensing Documents:

Nine Mile Point Unit 1 Technical Specifications

Updated Safety Analysis Report - Nine Mile Point Unit 1 Nuclear Station

Deviation Event Reports (DER):

1991-560

1992-480

1993-339

2000-2139

2000-3268

2001-5201

2002-2383

2002-3143

2002-5166

2002-5193

2002-5193

2002-5280

2002-5305

Procedures:

N1-OP-11

Reactor Building Closed Loop Cooling System, Rev. 20

N1-MRM-REL-0104

Maintenance Rule Manual, Rev. 16

N1-MRM-REL-0105

Maintenance Performance Criteria, Rev. 14

Miscellaneous Documents:

Failure Analysis of Flow Switch from the RBCLC to Recirculation Pump 32-190 Cooling Water,

NMP-1, dated July 29, 2002

Design Change Package N1-02-219

Drywell Equipment Drain Tank Coolers RBCLC

Outlet Re-design, Rev. 0

Draft Evaluations

DER 2002-5305 Category 1 Root Cause Evaluation (Organizational and Cultural Assessment -

Unit 1 RBCLC System Events)

Safety and Availability Assessment - Unit 1 - RBCLC Pipe Leakage Inside Primary Containment

Reliability Group Technical Report - Unit 1 Drywell Heatup and RBCLC Drain Unit Cooler Piping

Temperature Response Evaluation

Safety and Availability Assessment - Unit 1 - RBCLC Leak Study

Attachment 1 (contd)

3

LIST OF ACRONYMS USED

AC

Alternating Current

ASME

American Society of Mechanical Engineers

ATWS

Anticipated Transient Without Scram

AV

Apparent Violation

BWR

Boiling Water Reactor

CDF

Core Damage Frequency

CFR

Code of Federal Regulations

CMTR

Certified Material Test Report

DER

Deviation Event Report

ECCS

Emergency Core Cooling System

EPRI

Electric Power Research Institute

FW

Feedwater

HFO

High Winds, Floods, and Other External Events

IA

Instrument Air

IE

Initiating Events

IMC

Inspection Manual Chapter

LERF

Large Early Release Frequency

MDC

Mechanical Design Criteria

MS

Mitigating Systems

MSIV

Main Steam Isolation Valve

NEI

Nuclear Energy Institute

NPSH

Net Positive Suction Head

NRC

Nuclear Regulatory Commission

ppb

Parts Per Billion

PRA

Probabilistic Risk Assessment

RBCLC

Reactor Building Closed Loop Cooling

RCS

Reactor Coolant System

SBO

Station Blackout

SDP

Significance Determination Process

SLOCA

Small Break Loss of Coolant Accident

SPAR

Standardized Plant Analysis Risk

SRV

Safety Relief Valve

TBCLC

Turbine Building Closed Loop Cooling

URI

Unresolved Item

CDF

Change in Core Damage Frequency

LERF

Change in Large Early Release Frequency

ENCLOSURE 2

February 4, 2003

MEMORANDUM TO:

James Trapp, Manager

Special Inspection

Steve Pindale, Leader

Special Inspection

FROM:

A. Randolph Blough, Director

/RA/

Division of Reactor Projects

SUBJECT:

SPECIAL INSPECTION CHARTER - NINE MILE POINT

UNIT NO. 1

A special inspection has been established to inspect and assess the reactor building closed

loop cooling (RBCLC) system piping degradation that was identified at Nine Mile Point Unit 1 in

December 2002. The special inspection will be conducted onsite during the week of

February 10, 2003, and will include:

Manager:

James Trapp, Chief, Projects Branch 1

Leader:

Steve Pindale, DRS

Members:

Suresh Chaudhary, DRS

Edward Knutson, Resident Inspector at Nine Mile Point

Eugene Cobey, Senior Risk Analyst - Part Time

On December 5, Unit 1 was shut down due to unidentified system leakage inside the drywell.

Leakage was subsequently identified from the RBCLC system. The piping degradation resulted

in system leaks and potentially adversely impacted the structural integrity of the system. The

RBCLC system is cooled by service water and provides demineralized water to cool auxiliary

equipment located in the reactor, turbine and waste disposal building. The RBCLC system

provides cooling water to major components including equipment drain tank coolers, drywell air

coolers and recirculation pump coolers located in the drywell in addition to fuel pool heat

exchangers, instrument air compressors, feedwater pumps, condensate pumps and feedwater

booster pumps.

2

This special inspection was initiated in accordance with NRC Inspection Procedure 71153

Event Follow-up and NRC Management Directive 8.3, NRC Incident Investigation Program.

The decision to perform this special inspection was based largely on the postulated loss of

safety function of the feedwater coolant injection system (high pressure reactor makeup source

is dependent on RBCLC) and the increased conditional core damage probability (CCDP) for this

condition. The inspection will be performed in accordance with the guidance of NRC Inspection

Procedure 93812, Special Inspection, and the inspection report will be issued within 45 days

following the exit meeting for the inspection. If you have any questions regarding the objectives

of the attached charter, please contact James Trapp at 610-337-5186.

Attachment: Special Inspection Charter

Special Inspection Charter

Nine Mile Point Unit No. 1

Reactor Building Closed Loop Cooling System Piping Degradation

The objectives of the inspection are to determine the facts and assess the conditions

surrounding the reactor building closed loop cooling system piping degradation that occurred at

Nine Mile Point Unit 1 on December 2002. Specifically the inspection should:

a.

Assess the adequacy of the licensees root cause evaluation of the condition.

b.

Assess the adequacy of the licensees extent of condition review and corrective actions

for the condition.

c.

Assess the effectiveness of prior corrective actions for the previous leaks in the reactor

building closed loop cooling system.

d.

Evaluate the licensees assessment of the risk significance of the condition, including

evaluation of all input assumptions.

e.

Independently evaluate the risk significance of the condition.

f.

Assess the applicability/effectiveness of the licensees piping inspection program.

g.

Assess the design adequacy of the RBCLC piping material compatibility.

h.

Document the inspection findings and conclusions in a special inspection report in

accordance with Inspection Procedure 93812 within 45 days of the exit meeting for the

inspection.