IR 05000454/1990017
| ML20059B433 | |
| Person / Time | |
|---|---|
| Site: | Byron |
| Issue date: | 08/17/1990 |
| From: | Farber M NRC OFFICE OF INSPECTION & ENFORCEMENT (IE REGION III) |
| To: | |
| Shared Package | |
| ML20059B429 | List: |
| References | |
| 50-454-90-17, 50-455-90-16, NUDOCS 9008290075 | |
| Download: ML20059B433 (17) | |
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U.S. NUCLEAR REGULATORY COMMISSION
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REGION III
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.ReportNos.50-454/90017(DRP);50-455/90016(DRP)l
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., Docket Nos; 50-454; 50-455 License Nos. NPF-37; NPF-66
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- .icensee:
Commonwealth Edison Company
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. Opus West III
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-1400 Opus P1 ace
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Downers Grove, IL 60515
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i Facility'Name:
Byron Station,' Units 1 and 2 h
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Inspction At:
Byron Cite, Byron, Illinois
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Inspection Conductedi-July 1 througli August 11, 1990
' Inspectors:. W. J.;Kropp f
R. N. Sutphiii
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a O. R.;Calhoun
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Approved By:
ar in-J.
ar er, Chief y -
Reactor.
ojectscSection 1A Dat(
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Inspe'ction Summary, I
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- L Inspection from July 1 through August 11, 1990 (Report Nos. 50-454/90017(DRP);
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50-455/90016(DRP))
' Areas-Inspected:
Routine, u.1 announced safety inspection by the resident.
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?. inspectors.of; action on prevfous inspection findings; engineered safety.
l, feature systems; onsite event follow-up; reactor startup; current material-condition;: radiological controls;. security; safety assessment / quality verification; maintenance activities; surveillance activities; follow-up
.on allegation;' backlog; engineering and technical support; and fuel
handling.,
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Results:
Of the 14 areas inspected, no violations or deviations were l
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- identified.' Four open items were identified that pertained to
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(1) methodology used by Westinghouse to determine setpoints; (2) material-
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s condition of the post accident neutron flux instrumentation (paragraph 3.e.);
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(3) ir.stallation of a wrong diaphragm in the pressurizer PORVs (paragraph-5.a); (4) timely calibration ofsa plant installed instrument used for
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L technical specification surveillance acceptsnce criteria (paragraph 5.b.)
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. and ;(5) Jan' issue.of undersized welds on the CV and SI punips (paragraph 6.a).
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,.9008290075 900817
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hDJR ADOCN 0500o454
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' 1The licensee's; activities in this area continua to be considered good.
The materia 1' condition for unit I and Unit 2 components-was considered go '
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ioverall;with increased management. attention needed for the post accident y
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T. neutron flux instrumentation.. The materialicondition for the Unit 0
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' components was considered average with,some improvements noted during the
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inspection period.
The communications between, operations personnel on shift J'
1during the-July 17, 1990 reactor startup was considered good. ;The operator's.
. response to the high level in the 2A steam generator during the, startup that
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resulted'in a feedwater isolation was considered good. The operators alsol f'7 lo
" terfaced well with trainees assigned to.startup duties.
The' licensee's,
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wuservative approach in operations was demonstrated by the shutdown.of Unit 2 "
due to' leakage from Swagelock type fittings even though Technical Specification.
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limits were not exceeded..
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The'11censee also chancad the pressurizer low pressure safety injection
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'setpoint from 182F psi to 1850 psi as a. result of an ongoing Westinghouse-study on setpoint methodology.
Even tho' ugh the final determir-1 for-th'e*
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- setpoint has not beea estaMished, the station initiated the nt change
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as a conservative mt.angre and to prevent entering 3.0.3 of 6
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Specification if tne final determination--of the~setpoint re n is in'a setpoint-
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above~1829 psi.
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Safety Assessmgnt/Qua'ity Verification.
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The 1icensee's. performance in the LER process was considered good'.- 'The rooth
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causeLanalysis and planned corrective actions appeared adequate to preclude:
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y similar^ events in the future.
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A Haintenance and Surveillance
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The licensee'sl performance was mixed during this' inspection perio'., The n 4 +
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p jiicensee's' approach to resolve the unidentified RCS' leakage causbd by,leakincj
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- between maintenance, technical, and operations personnel.
Also,._the initiation; L
- .0:/ -of a'Reliabi.lity Centered Maintenance Study;for the Auxiliary Feedwater:'s9 stem' L l
C was considered an' example of-good management involvement.
However, the L,,lu,/{m Q
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h,y surv'eillance to verify the containment spray additive flowrate"was not d 3The ins
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%W CVisystem and considered the backlog:at an acceptable number ><ith no open
,j gjy NWRs affecting immediate operabifity of the CV system.
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~~ Engineering and Technical Support i.[a s
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The licensee's performance in this area was mixed.
The'Onsite Review.
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3 erformedito determine operability of the pressurizer PORVs was timely and.
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p hi technically" sound.
Also, the support by the station's nuclear ~ engineers and s
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- corporate' Nuclear Fuel' Services for,the1 reactor. startup of' Unit 2 on ^ July 17; s
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criticality.and control of. the axial delta flux which could have been;a s
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problem for~ the operators since Unit 2 was at the.end of core life (refuel
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- outage 3 scheduled' for September
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in the potential (undersire weld issue for the'CVf and'SI pumps wasinot timely.
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~ Until questioned 'by the-resident.. inspectors on July'30,11990,s the welds had
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'_notLbeen inspected for as-built configuration even though the'stationir,eceihed) ?
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notification of the' issue by_ l'etter on July 16,1990.
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. DETAILS-1-<
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R W f'.1k* Persons Contacted
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Commonwealth Edison Company (Ceco)-
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- Ri'Pleniewicz,StatiodManager
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- K. Schwartz - Production Superintendent-l
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- R. Ward. Technical Superintendent
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- J. Kudalis, Service Director
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,O D.; Brindle, Operating Engineer,' Administration
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.T.-lDidier, Operating Engineer, Unit 0-tf y
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T. Gierich, Operating Engineer, Unit 2
- T.'Higgins,
- Assistant Superintendent,-Operating-(-]
J Schrock,;0perating~ Engineer. Unit I
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- Pc Johnson,-Technical' Staff Supervisor
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- M.? Snow,eRegulatory Assurance Superviso_r.
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. 'D. St. Clair Assistant' Superintendent,.WorkJPlanning:
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- T. Tulon,, Assistant Superintendent,, Maintenance
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.'D.sWinchesterl Quality Assurance. Superintendent <
- D. sozniak, ' ENC. Pr9, ject Manager L '
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r*E; Zittle, Regulatory Assurance Staff ic
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'* Denotes 1those attending the exit interview conducted on August 10, 1990,
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~and at other; times throughout the-inspect 1on period.
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Thel inspectors also had discussionsiwith other licensee. employees,
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including members ofi hett'echnical and engineering / staffs, reactor and-t
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+> auxiliary operators, shift: engineers and foremen',,and electrical,
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mechanical-and instrument maintenance personnel, and cont lract security
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- 1 Action on Previous Inspection Finding (92701 & 92702)
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a.
-(Closed) Violation 454/90012-01:
Fhiiure to -identify, an inadequate
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. design: assumption, approver a calculation prior to ase.and perform a' +
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design review prior to using a single cellecharger.
The inspectors
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have reviewed the. licensee's corrective: action'and action to-
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T preclude' recurrence., Based on the review, the; inspectors do not
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.have any further concerns and this.violatio'nis~ considered closed. ; 3.;
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b.
(Closed) Open Item 454/90012-02; 455/90011-01f JConcerns: relative to
.use of; proper calibration-of instruments when performing specific
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'e a gravity measurement me on.the frequency.of: equalize charges.
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inspectors have revivded the-. licensee's response in a letterito the#
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NRC Regional Administrator (Region.III),3 dated June 29, 1990 and c
s tw i o, have no further' concerns in this area.
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.:, tw , Plant Operations . . n a3 : . .., , !
, W' R 't , , ., , ., _ s < , , [Q= l Unit,1 operated at" power levelslup to 100hthe lhad following modef F ' '[. l , . sinca July l,:1990. ~ L; p a y,;p,, " ' + , - 3' - - , , , Unit l2 o p rated at power levels commensurate with'coastdown: limits . > w.
_ , l k (refueling outage scheduled to. commence September 1,1 1090)until, July 14.,N,e u
Y 1990 when the# unit was shutdown for. primary leakage from Swagelockl type.
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- i[?m fittings'on the. primary sample lines.
The fittings were repaired,;the % vJ , L.
.% ^ se, unit was return 6d to service on July.17, 1990,'and has sin _ce operated'at nM qu . -@+ + h17 power levels commensurate with coastdown',11mits.
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. . , k i : l' f ) a. ' Operational Safety'(71707) Y ,, t << t, . g ni f, p,: , 40-During'the. inspection' period, the inspectors verifiedithati.
1> Tp))3 ' f y ' @T .V the facility'was being operatedrin conformance with the " +; 's 'p < 711 censes and ~ regulatory requirements and-the. licensee's' N >
a y , 4s management responsibilities were effectively carried outLfori >f ] @T 4. T.
' safe operation.. Verification was based.on. routine. direct, t ' " N W,af& f T - l ~c . ?1 . , W"t .. i observation ~of' activities-and equipment performance,- tours of'the' ~'l 4
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facility, interviews--and discussions with licensee personnel,; N < independent: verification of safety system status and limiting "~ conditions for operation action requirements (LC0ARs),~ corrective t > - " - action',"and. review of facility records'. . a Onla;samplingbasiskheinspectors.dailyverifiedpropercont'rol, " i , room staffing and' access, operator: behavior, and coordination of . plant ^ activities with ongoing control' roca operations; verified ~ ' operator adherenceswith-the latest-revisions of. procedures for - ' ongoing. activities; verified operation.as required by Technical i ' Specifications _(TS); including compliance with LC0ARs,1with emphasis on engineered safety features l(ESF).and ESF electr.ical.. '
- alignment:and' valve positions;. monitored instrumentation recorder
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,' -traces-and duplicate channels for' abnormalities;: veri.fied status 'l p_,' of various ? lit annunciators. for, operator:' understanding,yof f-normal y , l condition,: and compensatory actions;1 examined nuclear'instrumenta- ~ l' tion (NI) and other-protection channels for proper operability: ' v'. m4 reviewed radiation. monitors and' stack monitors for' abnormal - ' ' conditions;!verifiedthat'onsiteand.offsite-powerwasavailable ' ,' as required;7observedithe frequency.of plant / control ~ room visits [M by the station * manager,? superintendents, assistant, operations
superintendent,.and other managers; and observed the Safety - , Parameter Display System (SPDS) for. operability.
No. problems'were- , 'o~ -noted.
i ' p4 , < - ! > y . On August 6 - 7, 1990, the_' station changed the pressurizer low - %, -pressure safety. injection'setpoint,from,1829 psi to:1850 psi for- ~ ~ A-Unit 1]and: Unit 2.
As a' result of. an ongoing Westinghouse studyi-of setpoint ' methodology, a preliminary conclusion was. drawn that thes
gr 1829' psi might not be conservative.
A final determination'has ncte
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- engineering onithe'setpoint. LIn the; interim,.the station' elected? '-
to implement aJconservative approach and raised the setpoint to' ' , ,' J1850 psi.
A' set' oint change record:and 10 CFR:50.59 review'were: ' ' p ' performed prior to the-setpoint change.. Since the Westinghouse study of setpoint methodology could also-affect other setpoints.'- This matter is considered an Open Item pending further NRC-review e ' " (454/900017-01;,455/90016-01).. .! . ' . I .b._ Engineered Safety Feature (ESF) Systems (71710) ' ' , ' c,
.During the inspection, the inspectors selec m Lessible portions d > < 'f an ESF system to verify status.
Consideration was.given to the <y o .;4 plant mode, dpplicable Technical Specifications, Limiting Conditions ! & for OperationfAction Requirements (LC0ARs), and other applicable ~ ' j , . requirements.
'
e , . a ., m Various observationsT where applicab'e,= were.made of hangers and- ! ' ' ' supports; housekeeping; whether valve position locking, -if required,- ' was: installed and proper;'- -valve aosition and conditions;' potential n - > ',
- ignition. sources; major component labeling, lubrication, cooling',71 (7'
^ / etc.;'whetherinstrumentationwasoroperlyinstalledandfunctioning~14 . and significant process parameter values were consistent with.
~. ' expected values; whether instrumenta';An was calibrated;' whethergi: p necessary support systems were operational; andiwheth'eplo'cally and, fb i j(,3
% Q7 remotely indicated breaker and valve positi(ns. agreed! y ' { aQ v. ^During the i.nspection, several; accessible'portdns.of[thesfollonirig' j q 1 %
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m A , fi n U Q(/g ' 'ESF systems were walked down, for each unit: WPf 3~ 1,yd - $j ' , s 493 ' (,; ;j ' %g'- ' ' '
4 y4 f UnitEl-i { , r , .L a , . ,, + !h.
i,' ' Containment Spray, Trains A and B E ' \\n d y - .
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High Pres'ure Safety Injection, Trains A and B 1#
' J ~,. l ' ~ s ,, Q,3A( Chemical and Volume Control, Trains A and B _ -[~.,: 6 4i ., Auxiliary Feedwater, Trains A -and B / 'i 'I' V! - '~ 3; J w y ~; .' ,j . 7%3 A Unit:2-g .~ y% ; ., - - .d' Containment Spray,. Trains'A and-B / ' ' ' M High Pressure Safety Injection, Trains A 'and B i4 F d . Chemical and Volume Control,. Trains A and B 'i . - ' ,'. Auxiliary Feedwater, Trains A and B q . ' Onsite Event Follow-up-(93702)
, ' (1).On July 14,-1990, Unit 2 was shutdown due to leaks on Swagelock ! type fittings ~on process sample lines for'the reactor coolant ! ' syst'em (RCS); 'The leakage (.8:gpm) was below the Technical . d' Specification limits of 1 gpm.for unidentified and 10 gpm for 'j , a r $Y
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N4 hw [t U W 4 a ' fthen sent inside thetinner," missile' shield wall 4in' containmentif J
,. , The exact' source of the leak could not beidetermined due to i s N b Howeverl the 11censee' ascertained f * "4 ' '. WN. ~ s accessibilityofLthe' area.
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- d licensee' decided to? shutdown the unit'.
Aft'er theishutdbwn the.
' '
.a _ ; N 'f. licensee determined that 3 out of 6 Swagelock type 2 fittings y ,f q.
. e M J were11eaking on the. process sample. lines from the RCS, 'The V &4
- 1
, - - & ' licensee repaired / replaced all the? fittings 'on the process ( $r dJ , s W :; sample lines andJreturned the unit'to service onl July 17. 1990.
- '% , % The inspectors will review:the Deviatioh Report issued for the- ,% , event lfor proper root cause"and corrective action, p o-3;
, . +
g, +1 ' _ s '(2)L.On July 14, 1990 at 9:22=p.m.^a'n unexpected Unit 2 feedwater
<
, i '~ isolation (FW) from the train "B" reactor. trip breakers (RTB)
-
a was initiated when the RTBs-were closed in order to 1atch the. ~ ' ' ,, turbine.
Attempts to repert the FW-isolation signal could.not-o 1,s sbeLacc>mplished by'the licensee.
However, a subsequent ~, -e ' Linspection.of the RTB "B" breaker and breaker cubicle did ' ' _ .1 identify a potential cause of the FW: isolation signal.
Scme - ' wirint associated with the "33" contcctor-(used in the control '" ' circuit to determine if breaker was racked "in" or "out") was found bent at'the lug and could have caused an inadvertent grotmd.
'A ground could cause a spurious FW i' solation signal ' '
7 when the breaker was closed.
The. inspectors will1 review the
' - associated LER for final cause determination.3 ' s,u , , % d.
Reactor Startup-(71707) ' &y = ' ' , ,1 On July'17, 1990, after the completion of) repairs _on Swagelock type' ] 3 fittingsi the licensee commenced a' Unit 2Jreactor startup:at 10:42'a.m.- t ~; . ,_ g, l T-The. inspectors were in the control, room.to, monitor?the < startup.
A JSome of the startup activities were performed by trainees under-M close supervision.by the licessed~ operators.
The startup was- - performed in a! professional manner with good communicat!ons'between
- , [%
' shift personnel.
There was a feedwaterfisolation'that* occurred dueJ ' u . t
'to a'high level in the 2A Steam Generator-(SG) at,6% reactor power.
j ~ "' I mThe high levelioccurred as a result of. difficulty In/ controlling SG.
! , < o m$ xlevels in manual at low power levels.
All_ equipment responded as~ , ! , , , is expecteo.
The operators respondedfto;the, event properly'and were ' , . t J4 able_to stabilize the plant to allow continue,d plant startup.
' - ,y The inspec' tors di.d observe very good i_nterface between theitechnical i' .
- ~ > '
staff nuclear engineers-and the operators during the startup. 'The
, nuclear enginears of Corporate Nuclear Fuel Services provided !> .. _ excellent support to the operating shi.ft in not only the approach to;
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1^ critical'ity but'also'during power ascens' ion to maintain axial. del'-
" ,nY'~, flux within' limits. TThis support was criticall since Unit'2 wass at' " !
end,offcore life'andithe delta flux.would'be difficult to contro11 ~..
within' limits.
- ' ' , V@ _ _ ,
- < , ' ..*i' et current Material Condition (71707) j l' - c ( < , , l.
,f The inspe: tors performed general plant as well as-selected system -
.f L ,and component walkdowns _ to-assess the general and. specific' material ,, , jf+ b conditiog of the plant, to verify.that Nuclear.. Work-Requests (NWRs) 3.
" had b % n initiated forridentified equipment p'roblems,'and to.
?4 - j - " O ev'aluate-housekeeping.
Walkdowns -included an assessment of the , b f' . buildings,- components, tand systems for proper.. identification a~nd ', . "W~ t'agging, accessibility, fire and security-door integrity, - % ' ' X scaffolding, radiological controls, and any unusual. conditions.- ' Unusual conditions included but were' not limited to water, oil, or
& ' r ' . o other liquids on:the floor or equipment; indications'of. leakage ~ ' ' n through ceiling, walls or floors; loose insulation; corrosion; 's a ' , excessive noise;; unusual temperatures; and abnobmalDventilationiand lighting, ' '
. , " The material condition.of' Unit 1 andLunit 2 was: overall'~considere' - d _.
,above average.. However, a conce'rn was identified with the material M ~ ' condition'of the, neutron flux post accident instrumentation,ywhich y '
' 0- . was identified (in Regulatory Guidel(RG).1.97 as'part of the post . O - accident instrumentation.
During a region based inspection:of: < u , components in the, scope:ofLthe environmental qualification program.
3 f' and RG L 97, the inspectors noted that the Unit 1 post accident i. i
L neutron flux instrumentation did not; agree with the actual power L i' W l
< ' level of the unit. zThe Unit 1 post accident neutron flux j ' h[,9.
- -Instruments indicated:approximately 35%l reactor' power even though - % ~ j the unit was at"98% power.
Also, one train of the Unit:2tpost.. p'N e j <+ . ' '~ _ p/ accident' neutron flux ^ monitoring was out-of-service with thelothern.
- O,1 . train operable with~the indicated: power commensurate with the'actuale L +2 !6 6{1' h
reactor power level of the unit. -Based on these"obsoivations,sthe @d Q ~ O inspectors considered the overall: material condition ~of;the{ post 4,
. hf $, accident neutron _ flux instruments as poor.
Further investigation; 4 o W - i % ' im - N, N 4 y~ hK by-the inspectors determined that the post accident. neutron? flux!W L ' 'lt j , 'y','; Therefore, any survbill'ance.activitie!E, ;j.. es5 ' ' -instruments were not in Technical Specifications as other pc::t M V-accident instruments.
' i ti i associated with post accident neutron flux instruments 9as performedi J ,g6 v ;. l" ';to:a non-technical specification procedure that-did'not 9pecify;af f /@<, - l NAM frequency for the performance. of the sur(eillance.. The(inspectors,
h e.Br expressed concern to the plant management that sufficient contrcls.
'" '! LQ%8% L' ' did nat exist to ensure the. material condition of theJpost:accidentf L i neutren flux instruments was maintained at a level co'mmensurate' with i
if other post. accident instruments identified in RG ol.97.
This matter U , a.
&,~ is considered an open item pending further review by the NRC and.
, ~ ~ licensee (454/90017-02(DRP); 455/90016-02(DRP)); ~ ~ ' j Mr ] ' , g
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- The mat'erial: condition of Unit _0" equipment was= considered: average. N hi;jkl$$f
' overall with" continued ef fort-by,' management. tot strjve, for above' ','f '(Q ~ " " ygw pe average. status.
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Radiological Controls -(71707)f f! -g;
? ~ 3* , V ./ q&* .. = The inspectors' verified that, personnel were followhg health lphysk:s # ^w > 'j i + > y %,; A __ . w . _ ,., , .. 4L %NQi D = , : procedures for dosimetry, protective cloth' ig, frisking'3 posting lg T ~*'l ' , %, x NS etc.]and randomly examined radiation' protection"i'dtrument'ation~,*ri i use,<operabili_ty, and calibration.. ~ ' ' ' f.. , ~ . , -b - t M f.
q3; . g. : Security (81064): > < Each week during. routine activities or tours, Ethednspectors : ' A me m
. . , , ' ~ 0-monitored the licensee'stsecurity program to ensure:that}observedi~ _ y% 7e .. _. " " ^ ' ~ IM b actions were:.being implemented according;to ;the _ approved security! .. fn '
- plan.' ;The inspectors noted that persons within the protected area. '
- displayed proper ph_oto.-identification badges; and those individuals , ' requiring escorts,were' properly-escorted.
The inspectors also.. m verified that checked.vitalJareas were locked and alarmed.
'f. y(j% - y ' Additional,1y,Lthe. inspectors also' verified that observed. personnel- _ q ,. and packages entering the protected area were searched by-7-
, appropriate equipment:or by hand,
- a x
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0SHA- "
'
,
, ~
, The Byron' Station exceeded 5 million hours without a lost 1.ime 'T accident on August 7,1990. iByron' was the first Commowealth Edisons 'l ' ' <" . %j i station to exceed-5'million tours, sThe inspections d ying-tours;did- . . s _not-. identify any personnel safety issues.
' , ! -
- d No violations orideviation's were id'entified, h
J - s.
. . v , ,w ~ t-
<< 4;
- Safety Assessment / Quality Verification (40500, 90712, 92700)
( U ..g y . , , Licensee Event Report (LER) Fo',10w-upi(90712, 92700) ',
- j , >s , STnrough direct observations, discussions with'licenseeipersonnel, Jand' ; m. p ' ' review of records, the followipg event reports were reviewed to determine h , that"reportability requirements were fulfilled, that immediate corrective J ~ ' action was accomplished,7and that corrective action:to prevent. recurrence ~ , had been or would be: accomplished in accordance with' Technical'
& Specifications (TS): b" p e
. ,
a.
(Closed) 454/90002-LL: Reactor trip when'2 out if14 coincidence.was) % ' '
y, satisfied on Overtemperature-(OT)Jdelta Temperature (^T).
This;esent i B ' was discussed in Inspection Reports 50-454/90010; 50-455/90009, ' ' *
, . paragraph 2.c.
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-~(Closed) 454/90007-LL:- Failure,toxtest-the steam line isolation ' y handswitch on main control = board panel,s1(2)PM06J during the past " , i 4%
- refueling:; outages forfboth ' units...Technicalyspecificationt3.3/2:
, < C?
- Table 4.3-2,Jitem 4.a.2 required the' tests on the main:stepm
, isolation handswitch,on a refueling-outage-interval.
For.further-e , t _- . ., , 'f;' ~ ' details _seeilnspection' Report 50-454/90014[ 50-455/90013,
- ' y a paragraph 4 b.
> . - ,n
- ..
. .. h..;'. j - .. f f ; * ::c. '. W1osed)L 454/90008-LLi. Unit l'was: shutdowa duelto containmentja'ir: , temperature /was above the technical specification limit.
TheicauseE f ' l
hy . l 'f' " of the'nighLtemperature was both Unit 1 ca tainment chillers out of? " , , L <o '
services For further details see Inspecti9n Reports 50,454/90014; J W " y , ' 50-455/90013,. paragraph 2c.
'(I? ~" i - ,:s.,, ., y ,.a -, y y n,. + . . +, - n .y ' ,' .^ an; dC E No' violations or deviations were identified. ' > ' .~i.
- - ,v _ p c v' . _ . a. - _ - - a., . , Q R~ ;, , ',' . _ . , ., ', ,_, r g, 5.
Maintenance /$urveillance (62703 & 61726) I.A,# l,
- <H J v r .t s n
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Maintenance' Activities ('62703) '
' n '% L > , " U ' ' WJ c v < ,.
,
, , , ! Station maintenance activities that~ af fected;the safety relatEd, yyj '" , andindustrycodesJorstandards,and=inconformance 1' (1Y and associated systems'and components were observed or reviewed to + }M a,. k [( ,ascer a n complia'nce with approved procedures, regulatory guides! fg ^- ti d' . a . ' 1, Specifications.f, by ' < - , . .. , , - a - ,] ... m
- s,1 ! P g ' A,,
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__ e A '1w The following i bms-were considered during this re' view; :the ' .N_ . ' limiting conditions for operation wereJmet while ccaponents ort \\!. ~ ' ._ obtained. prior _to; initiating _the work;. activities 1were accomplished' ' O _systemswereremovedfromandrestoredtoservice;approya.lswerei q '.e - (
m _ /V W using approved procedures and were inspected as_ applicable; - = mg f unctional.. testing rand /or cal _ibrations were performed prior to-q < . , ' returning components or systems to service; quality;cdntrol records _
' = <, , , _ ' g Wt were maintained;; activities were accomplished by qualifled - > . , ',. . d , = personne'l; parts and materials used were: properly certified; a,
radiological controls were implemented; and fire prevention controls
,, > -- F ' 'were implemented.. Work * requests.were' reviewed to. determine the- -
~' ' - status of; outstanding jobs ~and to assure that' priority is' assigned, . '
y, .to safety-relatsd' equipment 1 maintenance which may aflect system-l F , , ', -performance.
q . - , e" a Portions of the:following maintenance activities were observed: ' - = .< and/or reviewed: . ^ ' , . , , _ 2, . , s < > , - NWR 43184 - Repair 11eak 'on-union 'in Unit 2 Loop D, ?/8", Process A s g , '* _ Sample Line.
' i 't,> . . < NWR 15409 Disassemble, Inspect and Clean _, or Replacep the Oil w
, ' Cooler for Safety In,iectio_n Pump, 2SIO15B* _ g _ aJW NWR 75460 Clean air side of Cubicle Cooler for Safety Injection I Puinp 28.
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.c393 s ~ d7V NWR 770631. Disassemble, Inspect, and Clean Water-Side ofi L . N i(, y ' ' . (e i'J
'D Containment Spray Pump 20 Cubicle Cooler, y l . NWRi77729.- Ruptured Diaphragm in 10RV, 4 - W . a ~ > . NWR.78250.- Investigate,: Calibrate, and Repairiequipnient associated: N*O ' '
W - with UH t 1-- IF steam Generator PORV.t ' , ~ Y ' '
7.
NWR;78264 - Repair leak in ' /8" tube ~ fittings, Parke'r' CPI L . ' , o 2i . (SwagelockiType 4 3/8" . . . . ' . NWR'78275'-; Investigate'Un; ain 8 Feedwater Isolation Signal . . caused byfa Reactor trip Breaker.. . ,, ' ,
- NWR 78379; Replace and Calibrate Card for-Unit 2-Cold Leg 2A WR:
' ' ? Temperature Indicator.
' . . , '% The i nspectors' periodically monitored the licensee's work in
o < ' progress and. verified performance was in accordance with' proper-. j ' proc 6duresf, and approved work packages, that'10 CFR'50.59 and.other.
' .M' applicable drawing. updates were madeLand/or planned, and that.
' d , !", operator trainingy;asiconducted inta reasonable' period of time., +- s ,.
Duringj.hemaintenanceactivitiest(NWR77729and<77723)'onthel l ' ' [
Unit 1 pressuriter power operated relief valves (PORV) 1RY455A and J t , - 1RY456 on June'14,'1990,' wrong diaphragms.were installed, Instead ;
' F , [ of, ethylene propylene. material. the diaphragms' installed were BUNA-NJ j d material.
Since the PORVs.were EQ valves, the'ticensee performed an' " s . ~0nsite Review-(OSR)'to' determine operability of'1RY455A and 1RY456., M ( , ' The OSR;(90-151) is discussed in paragraph 7b.iof this' report.- The < ' , licensee identified this issue ducing a rev'iew of;the maintenance ' < o " * package 1after the completion?of the maintenance activities on 1; 1RY455A and 1RY456.
Further investigation by the' licensee ! > ' s , identified that a Unit-2 PCRV 2RY455A,salso had the wrong diaphragm
' . installed in November,1999. >The licensee.has issued Discrepancy
r e
A . Record;(DR) 90-148 and Deviation: Report (DVR) 90-092, ;to acidress
- j
.,e >1 root cause(s)-of thenincorrect-installation,'. corrective action j.
. i, ' (required and action.to prevent' recurrence.- This. matter i.s n 1.
" considered an~openfitem pending review of DR'90-148.
' lI , ? _;
- (454/90017-03(DRP);455/90016-04(DRP))(*
o* '
- U nP'
'. . . . _.. ~ ~ .
- The lice necihas initiated a. Reliability Centered Maintenance-(RCM)
' . , Study of the Auxiliary Feedwater System (AFW) by an-independent;g. ' > party.' LThe"results.of. the study wi1T be reviewed by the insp,ectors. ; j , w' v C-Theistudy will include an onsite.isit by the" independent; party inh q late August 1990'and will utilize-work history,; vendor < manuals etc.. j , m , f' insiinput to the RCH program for AFW.
'
/ X:j, ' m , , -D & . 3'
- ,.
. y b.
Surveillance hetivities (61726) 3Y /
, Ag %
3 , , - ~ m ,.. ,, kW, Theinspectorsobservedorreviewed~3urveillandetests, req 0iredb'yli /, j i ! k1; Technical Specifications during the inspection p,eriod an.d verified! q $ ]
KT, g that'testsiwere performed.in accordance with adequate procedures,+ q y 'r > ' L test instrumentation was calibrated,. limiting conditions for d < , =cperation were met, removal and restoration.of-the.affected j
~ k d.i components were accomplished, results conformed withiTechnical.
,. , '
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d, '.f' s
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]y;W$ Q T '.,"40 4 [o s, ht-we wo . ,' - o a, < _ ', ! ' n , , ' . 't , - , , . ,. .e,mn . . ,, }") l ,F j; ' ' ~< ' I
q + , , q ,. > ._ ~ . 't 3: e
f Specifications.and procedure requirements and were. reviewed by/ H '
, 3 f;, ', i, 3. '
- per'sonnel other;than the individual: directing-the. test, and anyj l
- 4
- deficienciesiidentified duringsthe tests were properly, reviewed!and-
-
'Mg resolved by appropriate, management _ personnel.
- "
f g4 , ,,,, , , . _ I . a o . j, 'The' irispectors: alsolwitness'ed/ reviewed portions. of the following ' ' 'p' . 7.- activities: ' ' ' ' '
'i . ' + t m ,, .. . - . . . ._ j 1;BOS 3'1.1-20? "! Train A Solid State ProtectioncSystem.Bi-Monthly < g" ' .' . .. Surveillance", Rev.:8; - n a s 1( 1 BOS-3.'2.1-860 --i "ESFAS Instrumentation Slave Relay. Surv'eillance . c ,
- (Train'A-Containment Isolation Phase B-K618,1
' ' < - . W , K626)", Rev. 2.
.. . ' ' ' ' - > ~ Sf?f, 1 BOS;3.2.1-900.-'"ESFAS Instrumentation' Slave. Relay Surveillance, ' ' , % ~(Train; A Steam Line Isolation-K616)"., Rev. 2. N, '. ' ~
- y.TE
,l'BVS 6.2.2;d-1.
" Containment 15 pray. Additive Flowrate . l m ' j . _. Verification", Rev. 2 ..
- 7 t a
'"
, . , , q
' 2 BOS 3.1.1-21
- " Train B Solid-State Protection System _ Bi-Monthly-
, @M' , ? e L Surveillance",'Rev. 5.
w '
,J , N j 2180S ?3.2.1-12 " Reactor? Trip :- P-4 Contacts", Rev. 51.- Q .. " - '> d, L J N ? 2 BOS 8.1.1.2.La-2 -1"2B Diesel. Generator Operability Month'ly and! ", 't / - , am +, i ;,4 JSemi-Annual Surveillance", Rev. 2.
3'W'
, m
' ,
E, s L 72'BVS 3.3;2-1 X"Mo.veable-Incore Detectors' Operability Check"i I( ! A . - TRev. 2.
M i . ' ~ ~ '
M" V;7,lh' NThe' inspectors did identify:two concerns' withisurveillanc'eb1BVS o Ut - M Iff j l'p"H, 4. ' _. _ . .. .., E > WM % e?t . , ' f, 6 '3M / [6.2.2.d-1, "Conta'inment Spray Additive Flowrate Ve'rification"., 2 m+ " My e ? W N LThe' surveillance was: required to be performed every five-years;by2
4 s + 0~ ~ Technical-Specifications:(TS)' The review of the surieillance' t % Li ' , - . & 6 4-resultsafor Train "A'E performed on 0ctober 11 and.12,1988 j, j' ' 4' ' J t , J t % t_ $' 'i_dentified the following concerns: ' - u-(- ' / ' 'f + . f N i;4 -< y ,f .e >
% %% , i . The installed, flow transmitter,1FTCS015, ~ utilizedTiri"the - - i " ' U< ~
- '
surveillance to' determine that the additive floe meets'TS m$l limits wastlast calibrated in" June,-1984. 'The calibration } '
y y Y frequency;for the transmitter and associated. loop was :also r t ' - , /M ' -five years.
However, the_duesdate was not' adjusted,to)fallt !vi .due at the'same time the surveillance, 1BVS 6.2.2Jd-1 was due.
,J o %.,, J Instead the last calibration' oft 1FTCS015 was' performed over ' > W ' ' ,t four years prior to performance of surveillance,:1BVS" ' ,
G.2.2.d-l', in October,1988. The inspectors reviewed the data M, for the IFTCS015, April 29, 1987, calibration,;and determined '
that the "as-found" data did not adversely affect the rtsults J > of' surveillance.1BVS 6.2.2.d-1 performed in October',198t'. '
_ . .t , , il, r .Howevery the insper,. tors 'still have a ! concern with -the , ' ht 4'- timelitiess of the calibration _of plant installed instruments: ' C utilized for TS: acceptance datac ~ l , + , ,+ , b ' (w r s
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.n . ,, , (gyg[,,' - ' gp 7*; T N surveillanci procedure,,1BVS 6.'2T2.d-1.id}d'.not identifyh. , theN erification of< proper. calibration of the.plantainsta11ed W o Eh e m*s iflow0ransmitter and associated loop that was utilized fortTS c .1- ' C" gW.g acceptance criteria.
The, surveillance procedure did require...' ' the identification of other test instruments-that was not plant '/'. n (installed used during the. surveillance 1by identifi, cation number.
A": '~ ' -
, , ~ and calibration due date.' ' ' ww ^ q, , x , - , _ l
- The above two concerns are considered open items' pending further,
~i h , '
W~ < review by the NRC.(454/90017-04(DRP); 455/90016-04(DRP)). e
c L pWQ sp ,, Follow-up on Allegation Involving a Fuel Handling Foreman Activ'ites '
2 /? " 4 < c.
, Rfg.
M (RIII-90-A-0011) , , + p
- e 1<
j . , W m ~0n January 29,.1990, an individual telephoned the.NRC Region III ." , '7% < ' Allegation 7 Coordinator with information that concerned a 'sel > , handling foreman (FHF) and the lubrication program at1tht ;yron .< @: m Station.=' The individual provided'the following linfrirmation: " ' ' y . . . f . y r .
- , ' e . Op # ' '~ (1)4 LThe: FHF f abricated,.in' a home ; workshop,.a 1 thimble-plug' t'ool .' 7
l
C4 ' that was;. utilized, withcut certification or quality assurance,
(tests'during'thejUnit1outageinJanuary,E1990.. A ' " ,, y , . n . . s.
. , , O (2) Three times' within the last 30 -days the FHF reeked of Alcohol ' - ,, ~ 1,d while'onsite. -The dates given were January-28, 1990, . . ' o s ,
- December 4,,1989 and'either the day,before or after>the FHFs:
W 'y, . . .NRC licensee examination.- 10n; one occasion,' Januaryf28#1990, ' ~ ' the indi'idual' stated that: security was notified and tne only ' v s - . ' assessment performed was akobservation while on opposite ~ sides
- t.
ofsthe glass a't the;gatehouse.1 The individual.proviced the; ,s-
' -
names ofTthree 0ther individualsithatishould be:able tot.. ,
- T W; G
'substantiatehthel allegation. ; >x m -
- 6Y M4,
' - During slow peridds, fue1 handlersi(FH) were givenLduties to @q t < -'r s , p p g_ , Vi ' ' I (3) ~ i . { . lubricate plant' equipment..The assignments.wereigenerat'ed byJa ' ' Lcompute't? printout and the: FHs. initialed the printout ~ after they a H. ; <
- .
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f .C P v" 3 f '. $ [ y% b Lcompletion of.the job, The individual stated that.the FHF:. ; 9i:k'f"f , a routinelyfalsifiedtheprintoutbyplacing=FHinitialsfonthe(g k ge h"% fg , printout for jobs not' completed.
The individua). stated tha.ty; 4 g' yy the data from the printouts were logged into the compute,rjand; L, N y WLp ghg.
i y %
the printouts -with the initials were then destroyedA."
, ~ . . g_ c._ AM (* - > Nw
y g, ' (4)' Two years. ago,' the in-core' detector was raised out. of.the' waterf .-t.m
- (b #rA yY 'j, S -
Eby the FHF even though the radiation technicians warnedithe4HF 'nn . g not to perform such an^ activity. The FHF still performed the% + T ' * g M F 9; - as a' joke and set off the electronic' dosimetry d $ N W j < g, N J ?activitys - nvi g~ ',O [Y g . [p. 4 L ' j - Qw
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- ~The'NRC' requested;theTlicensee;toLinvestigate the parts of t W,g,'
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eg%pn 4 allegation idenMfiedcin paragraphs'(1) and (2) above.TThr,other. f ' Ci i , 1y + parts'ofithe allegation were investigated by;the'NRCL lThe-results( a, . Q i d, Fof thesel investigations were: ', ' ' *
' .
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4 s < . + m %; k;.y ', 'y 1)$FabhicationofL. fool- - ,- e , , ( ,,,A ~ ;
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?[L N, Afy;; ' ' [ v This',partoftheallegationwasinvestighedby'the, licensee,~
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- . , N" 3 Q " GJ i
- and the'results' documented in aFletter~to;the,NRC Regional'
-% M , 'Administstion,on May 25, 1990.. The inspectors reviewed the .
' i +
(resultyof.O.Qnvestigation.
TheLlicensee'.s1 investigation g i' fr , AT . - could not substantiate the alleger's concern that a^tooln.
i , fj T,, . JfabricatM in the FHF home' workshop'was utilized duringethe - >0 o , ., % %y = Unit;1; refueling outage without proper tests pndicertification.
i
'
- . , %t^ 4; Thellicensee's' investigation determined,,through interviews' 't Vj ' MR with:FHs and review of documentation that a new tool was' . t, i ' fabricated but prior to use. the. tool wasitestedG'Also, prior,, N + i ~' f to'use as50.59 review and alon-site. review wascperformed.
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, $"- ,(2)[FitnessforDuty(FFD)-FHFreekedof'alcoholwhileonsite Vq ' ' lW
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- This-paYt?of the allegation was.also investigated by.the
j! ' ,. , ? licemee,and,the results documented to the' NRC Region,III d6 - ' n[t ' # ' ' , fI: AdministrationDin'a' letter dated April 30,t 1990. ' The " ' , Einspectors reviewed-the results of the licensee's
, . investigation. The licensee; could: not'substantiateithat the
> - J FHFehad reeked ofsalcohollon the days stated'by the-' alleger. J ,
. < V6 The licensee) interviewed the individuals the alleger'had stated " M > QN
could substantiateithe allegation.- The interviews considered
.. 1% 3' not only specific referenced" dated,:but also' addressed any past ' t , , Q% s /= FFD concerns _ for :'e. individual.
None of the three' individuals y ' 1W" V interviewed coulo provide anyLinformation,to support the wa ' . _ t W allegaticns..Alsofon one of the' dates of concern identified 'oy , ,% the. all eger, ' January. 28', 1990, the station received an f j ^ l anonymous FFD allegation against. the same individualsidentified-J ~Y is this allegation, LThe1 Shift Engineer had the individual , screened for.FFD.'iThe result was negative..Also,1the - ~. a individual's supervisor' assessed the individual's behavior-and' ' . l
+ performance of duty-in the' individual's work environment and '
' ~ .i , M there'were.no FFD! concerns observed.
Sincelthe NRC, Region III , , office received the same= allegation on.the morning'of'
~ s9 January 29,1.1990,.the Senior Resident" Inspector was immediately i , f notified of: the allegation and observed the individual e C ' ' , ., ', . ' ' performing his duties.
The. inspector didinot identifytany - -t ' ' behavior,of-the individual that(would. indicate he was unfit
~
- ,.
' V-i for' duty.. l ' ' , ED (3) Falsification of Lubrication Records ~ ' ' ' t 1 j - ,
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' ~ c.. !. ,t .. ,,.. .. fiH 3Q + > t TheLinSpec'tsrs investigated this portion of the allegation.
. , 'A " ' ' d g ( f a: m /The -investigation' consisted Jof.several' phases that includedh , '
, W*p , interviewing FHs,/the review of the-lubrication programLat . J , V.
Byrun, review of tlubrication records, and a sample of Lequipment" I? $
- in iht plant 'where the lubrication oil, by visual' inspection,N,'3 <
@# 'i'6 appearsd suspect.1to. verify the component's current lubricati_on u ,, . statusW Also, the inspector interviewed six individuals-o ,j .# - s, from the FH organization.~ The,FH organization has" eleven'
[" ,6r uindividuals and not all individuals'were; interviewed since some-tc . ' ' Y individuals were in training,-vacation,'or on the second shift.
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- Each individual interviewed described the' administrative
' , m , s' controls;for,the lubrication program. The individuals' stated
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ccomputer' sheets /were initialed and dated-by the FH:that N
' performed the lubrications.: The_ data on the computer sheets 1 a , Fw
., were then transferred to the mc ter.fi_le'by one the FHFs.
C'& ,e ,* The. individuals interviewed. sere not: aware of any occurrences
- y where falsification;of lubrication-records were! suspect.
The- ' inspectors reviewed <a sample of the lubrication records and '
, , did not identify anyLanomalies that could-be potentia 11 ' '
, . falsification of-records.
Also,;the inspectors selected
- '
e,
several components in the plant that_upon visual inspection, a '
- a ~@ ' appeared to need an oil' change due_to thercolor of.the oil (dark)e The inspectors: identified no anomalies that: j , , " substantiated falsification of' lubrication: records.
The ' ' O inspectors did substantiate that the records FHs initiated ' < > - , ~ after trt performance _of'a lubrication activity.were destroyed' ' , ,
after the data was transferred by one of the FHF to the; master '.- '" a
- file.
The'inspectorsdidnotconsiderthismethodofrecordy.
, , ,W ' keeping as a problem.
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11 In Core detector raised out of the water : -
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- 'This part of
- the allegation ~ wast reviewed by NRC6 region.alc nj
> gg specialists. The review!was ' documented <in Inspection 'i R1, _.. reportsE50-454/90007;'50-455/90006.
The inspectors could [ j %d 5:M1 *' not su,bstantiateithat the incore detector was liftedLout , .s.
' 'of thawaterlintentionally, For further -details see_ ! " , . .
- f
dP referenced reports.
' ' ' ":
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, , , l; 4 A d.1 ~ ' Backlog ' "" # s1 - - ~, ~
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! Q@i._ .* The inspectors reviewed the licensee's backlog of non-outage ;NWRse,g% f ! A ~ .
.
- (
p'L'@ associated with the Unit 1 Chemical and Volume Control Systems-(CV) 3 ' Eto 'determinef tf maintenance was accomplished. cThe' inspectors'
e& ' 3 E -' '., sselec.ted three NWRs from a" computer' listing,off the' licensee's i fm , , ~ @ f' backlog as of July 24,-1990..TheiNWRs were evaluated'for safety 'r' ' s %[ 'W 5. w" " -impact :of deferrals, and causes*uch as lack of per,sonnel,- lack-of .. _ trained / qualified personnel, 1 e* parts'or. engineering, support.
! ' T the three!NWRs reviewed were: . < 'j B78346 "0il Leaking From Piping To Auxiliary Oil-Pump".
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? W B72599 - " Replace Existing Transmitter With Barton Model 764".
$~ ' - B77149 " Perform Votes Testing %
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+ , . , ll W ;, gi +, L & ' Gj ;ff 's r 'y- %' ~j,j' ?' ' i aEthe basklog for the Unit 1 CV and the specific three hit; iThe! - p 4 $y e d'6, CWRs , h i identify ~any concerns.
The number of NWRs.in the= ,9 M a N og for;the CV system was 37, which was-not considered; ' , t. ec y g excessive.- m; ' tl w - m . .. t" % _ . . . . , ' ' - +f j m
- No violations or deviations were identified;
- - . L A
- (,
, g, g i , [ $ 4, j. Engine'ering'& Technical: Support _(37700) -l'
- D 1 T.y o
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i d, C f ,V bi 'a.1 On July 16,11990,. the station received a letter dat'ed July,2,T1990; Q from the: Nuclea'rs Steam Supply System vendor,- Westinghouse,? that-M; / identified a potential' problem with welds on the Chemical andi 'Fg1 M kpp<E $ L A Q s Volume Control System (CV) and Safety Injection;(SI) pump,p.,,Thet* Mhp A w.- ',N"4 mproblem pertained to the potential for. failure oflthe welds.on the, 7 ' V y, ', ' :of the welds could cause misalignment offCV and S 4,+ o3 - A alignment dowels and keyways during a' seismic event /.' 6The failure [ O3 y
'N.
. #+3
- N
1 ' . 7 %' -, subsequent; fail _ure of the pumps. L On July 30, 1990, the, inspectors"
- %
e 'requestedEthe status of:the welds on the CV and SI pumps;for both!t! iM (c0
'?- ' - . uni _ ts. The incpectors determined that the welds had not,yet"been 1 1' P s; W/4 - Inspectedito the criteria in the July 2,,1990 Westinghouse letter. > * Q^ 11 g, % ~ ' < . 'O M Investigation by the inspectors determined that the We'stinghouse,
' ! ' +[- C letter had been sent to the licensee's corporate engineeri_ngf y iorganization with-copies sent to.the licensee's pressurized water- ^ ~ . . reactor'(PWR)' facilities.
As previously stated,'theiletter was ? ! - , received by the' station on' July 16, 1990 and'sent*toitheDstation's i " . LTechnical' Staff..The inspectors were concerned that the"as-built' ' J configurati_on off the welds for the' CV and SI pumps alignment dowels- ~ 'and keyways were not ascertained'by the station until-the inspectors P; s ._ questioned the station of the welds.,The licensee inspected the
welds on July 31, and August.1, 1990,xand' determined that three of M . the dowel welds.did not' meet the requirements of the1 Westinghouse
J' J ' July 2,' 1990 letter for proper size.
The pumps that had-undersize . M L ' 'i welds were the IA and.1B CV pumps'and the 2A CV pump. ;The + . g tlicensee's engineer.ing organization-bas'the as-buiJt weld ' configuration and was assessing'the acceptability'of:the welds; based ' y , T-on thefspecific-seismic criteria of Byron instead of the morei !! ' ._4 stpingent seismic: criteria used-in'the. July 2,'1990 Westinghouse 1 . c 11etter.
This matter is considered open.pending further review by i v".
, 1, -the licensee and the NRC-(454/90017-05(DRP)'; 455/90016-05)DRP))~. j ' g , ,5 ' g S4 4, ' b.
The inspectors reviewed"On-Site Review (OSR)s90-151 performed:"on i
June 27,1990, to docume'nt the continued operability of: pressurizer , ~ i ' power operated valves, IRf455A,JRY456'and 2RY455A that had the -!
wrong diaphragm installed.(BUNA-h) instead.of the' required' ethylene- !, . c - propylene. LThe PORVs, 1RY455A, 13Y456'and 2RY455A were classified A yas EQ valves and therefore'OSR 90 151 was initiated to document the ~ 'g . , . operability of the valves with the BUNA-N. material for the
7 . diaphra*gm. + The OSR. was~ reviewed by regional-EQ specialists. and ' " , . determined to.be' acceptable.
' , . [Noviolationsorideviationswereidentified.
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. " _ , , ya y , a., , i _ A 7? FueliHandling-X 'i " "
. ',s ; ' tn e ~' "On~severaloccasions!the"inspectorswitnessedtherech,ipPandIstdrage'of ^ ^ , u . dw ~ W.._ o. enew fuel within the. fuel handling building., The.inspecto'rs: verified the( y M f appropriate' documentation of new fuel and that station procedures'were:. Al : & ?a- - ?
- followed in' unloading,; lifting, moving, lowering; and inspecting'new fuel d
- d_ f f ' assemblies.L Appropriate cleanliness controls _were implementedt . . ' - A Efficient communications between fuel-handlers,icrane; operators, radcheml 'it 4 " o ' . f.Jf i + technicians, and the;. fuel handling foremen facilitated fuel; handling - ~'%, . j; o. %
- operations.,
.
+ , , ' ' ' v, Noiviolations or deviations were identified. de l' _/
y ~ ; . - ' < ' y W ' C_ < 8, Open Items , , ' h
- )
, , . + . ,e f0 pen items are matters ~which have been discussed:with'the, licensee,3which Y l ~ ~ ' ' . M C.
will be reviewed by the inspector- .d which involve some action on~the" '
, s "linspectico are. discussed ~iniParagraphs 3a, 3e,- Sa',15b, and 6a.1 . J '.'part,of the'NRC'or licensee or both.
Open Items disclosed during the.
4^ > ,
' n . ~ a c q, . ' y -.. g n-o .
i , ' 59. L Meetings"ahd Other 'AEtivities ' g)'yw!n D - . e w - .- .. _ < , , ._ L a.' .Mancoament Meetings (30702) . . . 'v. N;m w . a il,E k s, '. t' f e t On Jul'y 11, 1990, CommissionerKennethRogers,accompaniedbyl.
. ' Wf "' (* 4^. , , b =h - T., Martin. Deputy Director, Division ofr Reactor-Safety, toured-the - l o Byronplantandmetwithlicensee,managementto;discussp~1 anti y,,, t % -,,i ' t' . performance and plant material condition.
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Exit:Inte"rview;(30703) , r.' ' - s+i 'ny ~ 3 : :
- , ;
+ . ., 9Y The' inspectors met with theilicensee representativesidenoted inL Qd ' ' ' - 4M 4 ;; -
- j, paragraph,1 during the inspection. period and'at-the conclusionJ'of '*
" N?
- thelinspection onLAugust
- 10 [ 19901-The, inspectors summarized the1 ?
' fp (;M W , sscope and!results of the inspection and' discussed t'he likely coptenti fwv T W b % of this inspection report.
The. licensee acknowledged the ' - O N disclosed during;did not; indicate;thatHany_ of-the:informati n! j V(y' ~ .> - QQ k % information and -
' the1inspectioncould,beconsideredproprietarp.in pQg g , W ,
nature.
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