IR 05000440/2018002

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NRC Integrated Inspection Report 05000440/2018002
ML18222A437
Person / Time
Site: Perry FirstEnergy icon.png
Issue date: 08/10/2018
From: Billy Dickson
NRC/RGN-III/DRP/B5
To: Hamilton D
FirstEnergy Nuclear Operating Co
References
IR 2018002
Download: ML18222A437 (18)


Text

UNITED STATES August 10, 2018

SUBJECT:

PERRY NUCLEAR POWER PLANTNRC INTEGRATED INSPECTION REPORT 05000440/2018002

Dear Mr. Hamilton:

On June 30, 2018, the U.S. Nuclear Regulatory Commission (NRC) completed a baseline inspection at your Perry Nuclear Power Plant. On July 11, 2018, the NRC inspectors discussed the results of this inspection with you and other members of your staff. The results of this inspection are documented in the enclosed report.

Based on the results of this inspection, the NRC has identified one issue that was evaluated under the risk significance determination process as having very low safety significance (Green). The NRC has also determined that one violation is associated with this issue.

Because you have initiated condition reports to address this issue, the violation is being treated as Non-Cited Violation (NCV), consistent with Section 2.3.2 of the Enforcement Policy. The NCV is described in the subject inspection report.

If you contest the violation or significance of the NCV, you should provide a response within 30 days of the date of this inspection report, with the basis for your denial, to the U.S. Nuclear Regulatory Commission, ATTN: Document Control Desk, Washington, DC 20555-0001; with copies to the Regional Administrator, Region III; the Director, Office of Enforcement; and the NRC Resident Inspectors at the Perry Nuclear Power Plant. If you disagree with a cross-cutting aspect assignment or a finding not associated with a regulatory requirement in this report, you should provide a response within 30 days of the date of this inspection report, with the basis for your disagreement, to the U.S. Nuclear Regulatory Commission, ATTN: Document Control Desk, Washington, DC 20555-0001; with copies to the Regional Administrator, Region III; and the NRC resident inspectors at the Perry Nuclear Power Plant.

This letter, its enclosure, and your response (if any) will be made available for public inspection and copying at http://www.nrc.gov/reading-rm/adams.html and at the NRC Public Document Room in accordance with 10 CFR 2.390, Public Inspections, Exemptions, Requests for Withholding.

Sincerely,

/RA/

Billy Dickson, Chief Branch 5 Division of Reactor Projects Docket No. 50-440;72-069 License No. NPF-58 Enclosure:

Inspection Report 05000440/2018002 cc: Distribution via ListServ

SUMMARY

The U.S. Nuclear Regulatory Commission (NRC) continued monitoring licensees performance by conducting an integrated quarterly inspection at Perry Nuclear Power Plant, Unit 1, in accordance with the Reactor Oversight Process. The Reactor Oversight Process is the NRCs program for overseeing the safe operation of commercial nuclear power reactors. Refer to https://www.nrc.gov/reactors/operating/oversight.html for more information. Findings and violations being considered in the NRCs assessment are summarized in the table below.

List of Findings and Violations Failure to Control Transient Combustible Materials in a Designated Combustible Control Zone Cornerstone Significance Cross-Cutting Report Aspect Section Mitigating Green Finding H.12 - Avoid 71111.05AQ Systems NCV 05000440/2018002-01 Complacency Closed The inspectors identified a finding of very low safety significance (Green) and an associated non-cited violation (NCV) of Perry Operating License Condition 2.C(6), Fire Protection, for the licensees failure to control transient combustible materials in a designated combustible control zone within fire area 1AB-1g on Auxiliary Building elevation 574 - 10. Specifically, on May 16, 2018, the inspectors identified transient combustible materials left unattended in the designated combustible control zone in the corridor outside the emergency core cooling system (ECCS) pump rooms, which exceeded the ten pound limit established in the Fire Protection Program document, PAP-1910, for ordinary combustibles (loose) in designated combustible control zones without a transient combustible permit.

Additional Tracking Items Type Issue Number Title Report Status Section LER 05000440/2016-003-01 Loss of Safety Related 71153 Closed Electrical Bus Results in a Loss of Shutdown Cooling

TABLE OF CONTENTS

PLANT STATUS

INSPECTION SCOPES

................................................................................................................

REACTOR SAFETY

..........................................................................................................

RADIATION SAFETY

........................................................................................................

OTHER ACTIVITIES - BASELINE

...................................................................................

INSPECTION RESULTS

..............................................................................................................

EXIT MEETINGS AND DEBRIEFS

............................................................................................ 11

DOCUMENTS REVIEWED

......................................................................................................... 11

PLANT STATUS

The plant began the inspection period at rated thermal power. On April 12, 2018, reactor power

was lowered to 95 percent to recover reactor recirculating jet pump flow mismatch following the

failure of the B loop flow control valve. The reactor was returned to rated thermal power on

April 12, 2018. On June 2, 2018, reactor power was lowered to 70 percent to perform rod

sequence exchange. The unit was returned to rated thermal power on June 3, 2018. The unit

remained at, or near, rated thermal power for the remainder of the inspection period with the

exception that on several occasions, power was reduced to maintain condensate demineralizer

outlet temperature and/or high condenser circulating water outlet temperatures at or below their

respective upper limits due to environmental conditions. The power reductions varied between

and 14 percent of rated thermal power and lasted from a few hours to several days.

On March 28, 2018, FirstEnergy Solutions (FES) / FirstEnergy Nuclear Operating Company

(FENOC) verbally notified the NRC that they intended to shut down all four of their operating

nuclear power units. Perry Nuclear Power Plant, Unit 1, is scheduled to be shut down

May 31, 2021. On March 31, 2018, FES, FirstEnergy Nuclear Generation (FENGEN), and

FENOC filed for bankruptcy. The NRC continues to maintain focus on public health and safety

and the protection of the environment. This will include a continuous evaluation by inspectors to

determine whether the licensees financial condition is impacting safe operation of the plant.

INSPECTION SCOPES

Inspections were conducted using the appropriate portions of the inspection procedures (IPs) in

effect at the beginning of the inspection unless otherwise noted. Currently approved IPs with

their attached revision histories are located on the public website at http://www.nrc.gov/reading-

rm/doc-collections/insp-manual/inspection-procedure/index.html. Samples were declared

complete when the IP requirements most appropriate to the inspection activity were met

consistent with Inspection Manual Chapter (IMC) 2515, Light-Water Reactor Inspection

Program - Operations Phase. The inspectors performed plant status activities described in

IMC 2515 Appendix D, Plant Status and conducted routine reviews using IP 71152, Problem

Identification and Resolution. The inspectors reviewed selected procedures and records,

observed activities, and interviewed personnel to assess licensee performance and compliance

with Commission rules and regulations, license conditions, site procedures, and standards.

REACTOR SAFETY

71111.01Adverse Weather Protection

Summer Readiness (1 Sample)

The inspectors evaluated summer readiness of offsite and alternate alternating current (AC)

power systems.

Impending Severe Weather (1 Sample)

The inspectors evaluated readiness for impending adverse weather conditions for a high

wind warning in the area on May 4, 2018.

71111.04Equipment Alignment

Partial Walkdown (4 Samples)

The inspectors evaluated system configurations during partial walkdowns of the following

systems/trains:

(1) Low pressure core spray system on May 17, 2018;

(2) Reactor core isolation cooling system on June 22, 2018;

(3) Control room ventilation and control room emergency recirculation system on

June 19 and 20, 2018; and

(4) B train of annulus exhaust gas treatment system on June 20 and 21, 2018.

71111.05AQFire Protection Annual/Quarterly

Quarterly Inspection (5 Samples)

The inspectors evaluated fire protection program implementation in the following selected

areas:

(1) Auxiliary Building 574 foot elevation, fire zones 1AB-1g on May 16, 2018;

(2) Control Complex Division 1 and 3 switchgear rooms, fire zones 1CC-3b and 3c on

May 22, 2018;

(3) Control Complex 638 foot elevation, fire zones 1CC/2CC-4a, b, c, d, e, f, g, h, and i on

April 27, 2018;

(4) Intermediate Building 599 foot elevation; fire zone 0IB-2 and fuel handling building 574

and 599 foot elevations; fire zones 0FH-1 and 2 on June 6 and 7, 2018; and

(5) Division 2 Diesel Generator Room; fire zone 1DG-1A on May 22, 2018.

Annual Inspection (1 Sample)

The inspectors evaluated fire brigade performance on May 10, 2018.

71111.11Licensed Operator Requalification Program and Licensed Operator Performance

Operator Requalification (1 Sample)

The inspectors observed and evaluated an operations crew-evaluated scenario in the plant

training simulator on April 30, 2018.

Operator Performance (1 Sample)

The inspectors observed and evaluated operations crew response to an unexpected increase in

power and subsequent recovery due to the failure of the hydraulic control portion of the B

reactor recirculating loop flow control valve on April 12, 2018.

71111.12Maintenance Effectiveness

Quality Control (1 Sample)

The inspectors evaluated maintenance and quality control activities associated with the

following equipment performance issue:

(1) High pressure core spray elbow replacement activities due to a through wall leak on

May 15 through 23, 2018.

71111.13Maintenance Risk Assessments and Emergent Work Control (6 Samples)

The inspectors evaluated the risk assessments for the following planned and emergent

work activities:

(1) Ground detection and isolation activities on the 125 VDC load center, D-1-B;

(2) A average power range monitor power supply card replacement;

(3) Replacement of the reactor recirculation hydraulic power unit B subloop 1 servo valve

amphenol connector cable;

(4) Spent fuel pool moves in preparation for the 1R17 refueling outage;

(5) Division 3 outage for high pressure core spray minimum flow line elbow replacement,

Division 3 diesel generator and emergency service water preventive maintenance

activities; and

(6) Plant risk evaluation for work activities while interbus transformer LH-1-B and

B essential service water sluice gate removed from service.

71111.15Operability Determinations and Functionality Assessments (4 Samples)

The inspectors evaluated the following operability determinations and functionality

assessments:

(1) Division 2 diesel generator exhaust temperature thermocouple failure;

(2) Division 3 diesel generator operability determination following woodward governor lube

oil replacement;

(3) A control rod drive pump; and

(4) A Emergency service water and A residual heat removal system assessment following

the discovery of a pin hole leak from the A emergency service water system.

71111.18Plant Modifications (1 Sample)

The inspectors evaluated the following temporary modification:

(1) Plant modification to clear the electrical ground on the 125 VDC load center, D-1-B, and

prevent further plant upset due to the ground.

71111.19Post Maintenance Testing (7 Samples)

The inspectors evaluated the following post maintenance tests:

(1) Testing following the replacement of the power supply for the power monitoring card

associated with the A average power range monitor on April 23, 2018;

(2) Testing following the replacement of the reactor recirculation hydraulic power unit B

subloop 1 servo valve amphenol connector cable on April 24 through 26, 2018;

(3) Testing of the 13.8 kilovolt bus L20 supply and crosstie breakers following breaker

replacement on May 8 and 9, 2018;

(4) B reactor protection system motor generator following cleaning, inspection, lubrication,

and motor analysis on May 9 and 10, 2018;

(5) Division 3 diesel generator testing following maintenance window on May 21, 2018;

(6) Testing following the replacement of the high pressure core spray recirculation line

elbow on June 12, 2018; and

(7) Division 1 diesel generator 2A supply fan testing following structural inspections on

June 25 through 28, 2018.

71111.22Surveillance Testing

The inspectors evaluated the following surveillance tests:

Routine (5 Samples)

(1) 'A' Average power range monitor channel calibration for 1C51-K605A on April 23, 2018;

(2) High pressure core spray diesel generator monthly surveillance test on May 11, 2018;

(3) Safety relief valve and Low-Low set pressure actuation channel functional for

1B21- N668E on May 24, 2018;

(4) 'B' Fuel pool cooling and cleanup pump and valve surveillance test on June 20, 2018;

and

(5) 'A' Standby liquid control pump and valve operability test on June 27, 2018.

In-service (1 Sample)

(1) 'B' residual heat removal system pump and valve surveillance on April 30 through

May 2, 2018.

71114.06Drill Evaluation

Emergency Planning Drill (1 Sample)

The inspectors evaluated an emergency response organization drill on June 6, 2018.

RADIATION SAFETY

71124.03In-Plant Airborne Radioactivity Control and Mitigation

Engineering Controls (1 Sample)

The inspectors evaluated airborne controls and monitoring.

Use of Respiratory Protection Devices (1 Sample)

The inspectors evaluated respiratory protection.

71124.04Occupational Dose Assessment

Source Term Characterization (1 Sample)

The inspectors evaluated the licensees source term characterization.

External Dosimetry (1 Sample)

The inspectors evaluated the licensees external dosimetry program.

Internal Dosimetry (1 Sample)

The inspectors evaluated the licensees internal dosimetry program.

Special Dosimetric Situations (1 Sample)

The inspectors evaluated the licensees performance for special dosimetric situations.

OTHER ACTIVITIES - BASELINE

71151Performance Indicator Verification (3 Samples)

The inspectors verified licensee performance indicators submittals listed below:

(1) MS05: Safety System Functional Failures (SSFFs) Sample-1 Sample (April 1, 2017,

through March 31, 2018);

(2) MS06: Emergency AC Power Systems-1 Sample (April 1, 2017, through

March 31, 2018); and

(3) MS07: High Pressure Injection Systems-1 Sample (April 1, 2017, through

March 31, 2018).

71153Follow-Up of Events and Notices of Enforcement Discretion

Events (1 Sample)

The inspectors evaluated the B recirculating flow control valve failure which resulted in jet

pump flow mismatch and the licensees response on April 12, 2018.

Licensee Event Reports (1 Sample)

The inspectors evaluated the following licensee event reports which can be accessed at

https://lersearch.inl.gov/LERSearchCriteria.aspx:

(1) Licensee Event Report (LER) 05000440/2016-003-01 - Loss of Safety Related

Electrical Bus Results in a Loss of Shutdown Cooling. A finding and associated

non-cited violation (NCV) was previously documented in NRC Integrated Inspection

Report 05000440/2017001 dated May 15, 2017, (ADAMS Accession No. ML17131A207)

as NCV 05000440/2017001-01, Failure to Implement Procedures for Combating a Loss

of Shutdown Cooling. This LER is closed.

INSPECTION RESULTS

71111.05AQFire Protection Annual/Quarterly

Failure to Control Transient Combustible Materials in a Designated Combustible Control Zone

Cornerstone Significance Cross-Cutting Report Section

Aspect

Mitigating Green [H.12] - Avoid 71111.05AQ

Systems NCV 05000440/2018002-01 Complacency

Closed

The inspectors identified a finding of very low safety significance (Green) and an associated

NCV of Perry Operating License Condition 2.C(6), Fire Protection, for the licensees failure to

control transient combustible materials in a designated combustible control zone within fire

area 1AB-1g on Auxiliary Building elevation 574 - 10. Specifically, on May 16, 2018, the

inspectors identified transient combustible materials left unattended in the designated

combustible control zone in the corridor outside the emergency core cooling system (ECCS)

pump rooms, which exceeded the ten pound limit established in the Fire Protection Program

document, PAP-1910, for ordinary combustibles (loose) in designated combustible control

zones without a transient combustible permit.

Description:

On May 16, 2018, the inspectors identified transient combustible materials left unattended in

the designated combustible control zone in the corridor outside the ECCS pump rooms on

Auxiliary Building elevation 574 10 and within fire area 1AB-1g. The combustible control

zone was marked off with red and white tape and had an overhead sign designating the area

as a combustible control zone with additional instructions detailing the requirements for

storing combustible material within the boundaries of the combustible control zone. The

combustible materials consisted of two large plastic laundry/trash carts filled with flexible

ventilation ducting, catch containment devices, plastic bags filled with zip ties, mop heads,

rags, and other loose combustibles. In the licensees engineering evaluation, the licensee

estimated the weight of the ordinary combustibles, based on the photographs taken, to be,

very near the 150 pounds of margin identified in the calculation P54-024. The calculated

weight was 149.5648 pounds, rounded to 149.6 pounds.

Corrective Actions: Immediately following notification by the NRC of the combustible

materials being stored in the combustible control zone without an approved transient

combustible permit, the licensee had the materials removed from the combustible control

zone and entered the issue into its corrective action program.

Corrective Action References: CR-2018-04561 and CR-2018-04568

Performance Assessment:

Performance Deficiency: The inspectors determined that the licensees failure to control

transient combustible materials in a designated combustible control zone within fire area

1AB-1g on Auxiliary Building elevation 574 - 10 was a performance deficiency that was

reasonably within the licensees ability to foresee and should have been prevented.

Specifically, on May 16, 2018, the inspectors identified transient combustible materials left

unattended in the designated combustible control zone in the corridor outside the ECCS

pump rooms, which exceeded the ten pound limit established in PAP-1910 for ordinary

combustibles (loose) in designated combustible control zones without a transient combustible

permit.

Screening: The inspectors determined the performance deficiency to be more than minor

because it was related to the Mitigating Systems cornerstone attribute of protection against

external factors (fire) and adversely affected the cornerstone objective to ensure the

availability, reliability, and capability of systems that respond to initiating events to prevent

undesirable consequences (i.e., core damage). Specifically, the failure to properly control

combustible materials in safety-related and risk significant plant areas could challenge the

availability, reliability and capability of systems that respond to initiating events to prevent

undesirable consequences, such as core damage. Furthermore, the inspectors reviewed the

examples of minor issues in IMC 0612 Appendix E dated August 11, 2009, and determined

the finding was similar to example 4.k. for an issue of concern involving transient

combustibles in a designated combustible control zone, which is defined in the licensees Fire

Protection Program (PAP-1910) as an area within the plant containing redundant trains of

equipment and/or circuits required for the safe shutdown of the plant.

Significance: Using IMC 0609, Significance Determination Process (SDP), and Appendix F,

dated May 2, 2018, and Attachment 1, Fire Protection SDP Phase 1 Worksheet, and

2, Degradation Rating Guidance, both dated May 2, 2018, the inspectors

determined that the safety significance of the finding was very low because of a low

degradation rating, since the quantity of transient combustibles exceeded the ten pound limit

for ordinary combustibles in a combustible control zone without a combustible permit and

challenged the combustible loading calculation (P54-024) for the fire area 1AB-1g, of 150

pounds, but did not challenge the safe shutdown of the plant by affecting redundant trains.

Cross-cutting Aspect: The finding had a cross-cutting aspect in the Avoid Complacency

component of the Human Performance cross-cutting area, which states that the licensee will

recognize and plan for the possibility of mistakes, latent issues, and inherent risk, even while

expecting successful outcomes. Specifically, individuals involved did not recognize and plan

for the possibility of mistakes and did not implement appropriate error reduction tools, in that

they were not able to determine where the combustible control zone started and ended and,

therefore, moved the two large laundry carts filled with ordinary combustibles into the

combustible control zone rather than removing the small metal cart out of the combustible

control zone as requested by the field supervisor. [H.12]

Enforcement:

Violation: License condition 2.C(6) requires the licensee to implement and maintain in effect

all provisions of the approved fire protection program as described in the Final Safety

Analysis Report, as amended, and as approved through Safety Evaluation Report (NUREG-

0887) dated May 1982 and supplemental numbers 1 through 10. Perry Fire Protection

Program, PAP-1910, Section 4.6.5.3e, Table 1 states in part that ordinary combustibles

(loose) cotton, rags, paper, cardboard and anti-contamination clothing at step-off pads, up to

lbs do not require a combustible permit. Attachment 1 of PAP-1910 describes

combustible control zones and defines the area outside the ECCS rooms on Auxiliary Building

574 as a combustible control zone.

Contrary to the above, on May 16, 2018, the licensee failed to implement and maintain in

effect all provisions of the approved fire protection program. Specifically, the licensee failed

to control transient combustible materials in a designated combustible control zone within fire

area 1AB-1g on Auxiliary Building elevation 574 - 10 in accordance with the Fire Protection

Program when its operators placed approximately 150 pounds of ordinary combustibles

(loose) into the combustible control zone without an approved transient combustible permit

and left those combustibles inside the combustible control zone unattended.

Disposition: This violation is being treated as an NCV, consistent with Section 2.3.2 of the

Enforcement Policy.

EXIT MEETINGS AND DEBRIEFS

The inspectors confirmed that proprietary information was controlled to protect from public

disclosure. No proprietary information was documented in this report.

  • On April 27, 2018, the inspector presented the radiation protection program inspection

results to Mr.

F. Payne, Plant Manager, and other members of the licensee staff.
  • On July 11, 2018, the inspector presented the quarterly integrated inspection results to

Mr.

D. Hamilton, Site Vice President, and other members of the licensee staff.

DOCUMENTS REVIEWED

71111.01Adverse Weather Protection

- CR 2018-04175; NRC ID: Items Identified during Outside Walkdown Prior to Wind Advisory;

May 4, 2018

- Letter from Perry Site Vice President to Senior Vice President Chief Operations Officer of

FENOC; Site Certification Letter for Summer Readiness; May 31, 2018

- NOP-OP-1003; Grid Reliability Protocol; Revision 9

- NOP-WM-2001; Work Management Scheduling, Assessment and Seasonal Readiness

Processes; Revision 22

- ONI-ZZZ-1; Tornado or High Winds; Revision 29

- PAP-0102; Interface with the Transmission System Owner; Revision 18

- eSOMS Plant Narrative Log; May 4, 2018

- Perry Nuclear Power Plant; Summer Work List; June 1, 2018

71111.04Equipment Alignment

- VLI-E21; Low Pressure Core Spray System; Revision 11

- VLI-E51; Reactor Core Isolation Cooling System; Revision 10

- VLI-M15; Annulus Exhaust Gas Treatment System (Unit 1); Revision 4

- VLI-M25/2; Control Room HVAC and Emergency Recirculation System; Revision 7

71111.05AQFire Protection Annual/Quarterly

- CR 2018-04395; NRC Identified: Incomplete Secondary Search during Unannounced Fire

Brigade Drill; May 10, 2018

- CR 2018-04561; NRC Identified: Transient Combustibles in a Combustible Control Zone;

May 16, 2018

- CR 2018-04568; Combustible Control Zone on Aux Building 574 Elevation Exceeded

PAP- 910 Quantities; May 16, 2018

- FENOC Plant Access Training; Revision 10

- FP-0CC; Control Complex; Revision 10

- FPI-0FH; Fuel Handling Building; Revision 5

- FPI-0IB; Intermediate Building; Revision 9

- FPI-1AB; Auxiliary Building Unit 1; Revision 3

- FPI-1DG; Diesel Generator Building; Revision 8

- FPI-A-A01; Preparation, Review, and Approval of Pre-Fire Plan and Fire Protection

Instructions; Revision 5

- FPI-A-B02; Fire Drill Assessment; May 10, 2018

- FPI-A-B02; Fire Drill Critique; May 10, 2018

- FPI-A-B02; Fire Drill Planning Guide; Scenario FDBU-1125-051018; May 10, 2018

- FPI-A-B02; Fire Drill Record; May 10, 2018

71111.11Licensed Operator Requalification Program and Licensed Operator Performance

- OTLC-30582018-07; PY-SGC1 Evaluated Simulator Scenario; Revision 0

- eSOMS Plant Narrative Logs; April 12, 2018

- eSOMS Plant Narrative Logs; April 23, 2018

71111.12Maintenance Effectiveness

- CR 2018-04484; Replacement Elbow for HPCS Could not be Located; May 14, 2018

- NOP-LP-2020-01; Quality Control Receiving Inspection Report for 90 Degree Elbow, 4,

Long Radius, SA234 Grade WPB, Schedule 120, ANSI B16.9; May 15, 2018

- NOP-MS-4001; Warehousing; Revision 11

- WO 200737508; High Pressure Core Spray Through Wall Leak in Minimum Flow Piping

Elbow; June 12, 2018

71111.13Maintenance Risk Assessments and Emergent Work Control

- EOP-03; Secondary Containment Control and Radioactive Release Control; Revision 7

- eSOMS Plant Narrative Logs; April 8 and 11, 2018

- eSOMS Plant Narrative Logs; May 16, 2018

- NOP-LP-2601; Procedure/Work Instruction Use and Adherence; Revision 6

- NOP-OP-1007; Risk Management; Revision 25

- NOP-OP-1007-01; De-Energized Inspection/Energized Testing of HPCS Pump Motor

(4 yr PM); April 18, 2018

- NOP-OP-1007-01; Division 3 4.16KV Bus EH13 Degraded Voltage Channel Functional Test;

April 18, 2018

- NOP-OP-1007-01; Risk Management Plan for Calibration/Replacement of A APRM Power

Supply Monitor Card; April 6, 2018

- NOP-OP-1007-01; Risk Management Plan for Replacement of Reactor Recirculation

Hydraulic Power Unit 'b' subloop 1 Servo Valve Amphenol Connector Cable; April 20, 2018

- NOP-OP-1007-01; Risk Management Plan for Shuffling Fuel in Support of 1R17;

April 18, 2018

- ONI-J11-2; Fuel Handling Accidents; Revision 16

- ONI-SPI E-1; Containment/Fuel Handling Building Closure; Revision 0

- ONI-ZZZ-7; Contingency Plans; Revision 8

- SOI-F11; Fuel Handling Platform; Revision 19

- SOI-F11; Fuel Handling Platform; Revision 20

- SVI-M40-T5340; Fuel Handling Building Integrity to Handle Irradiated Fuel; Revision 3

- WO 200747618; Simple Troubleshooting Plan - Reactor Recirculation Loop B HPU Subloop

B1; April 27, 2018

- WO 200747619; Replace Servo Control Valve 1B33F0601B Connector Cable; April 27, 2018

71111.15Operability Determinations and Functionality Assessments

- CR 2018-03124; Division 2 Diesel Generator RTD Found Broken during Repairs;

April 4, 2018

- CR 2018-04676; Identified Potential Requirement to Perform SVI-E22-T2680 Following

Adjustments Made during Division 3 Diesel Generator Run; May 19, 2018

- CR 2018-04905; Control Rod Drive Pump A Aux Oil Pump Degraded; May 28, 2018

- CR 2018-05504; ESW A Through-Wall Pipe Leak at RHR A HX Outlet Piping Aux 574 E;

June 13, 2018

- eSOMS Plant Narrative Log; May 20, 2018

- NOP-OP-1009-01; Prompt Operability Determination for CR 2018-05504; Revision 0

71111.18Plant Modifications

- ECP 18-0095-000; Design Change to Implement and Restore a Temporary Modification to

Isolate the Automatic Trip Contacts for the Exciter Field Breaker, 1N41S0002, to Eliminate

Indicated Ground on Non-Safety DC Bus D-1-B; April 24, 2018

71111.19Post Maintenance Testing

- CR 2018-04676; Identified Potential Requirement to Perform SVI-E22-T2680 Following

Adjustments Made during Div 3 Diesel Generator Run; May 19, 2018

- ICI-C-51-4; Average Power Range Monitor (APRM) Component Calibrations (C-C51-4);

April 23, 2018

- IMI-E3-0023; Division 3 Diesel Generator Woodward Governor Maintenance; Revision 10

- PMI-0001; Preventive Maintenance of Vane Axial Fans; Revision 10

- SVI-C51-T0027A; APRM A Channel Functional For 1C51-K605A; April 23, 2018

- SVI-C71-T5232; RPS - Electrical Power Monitoring Calibration/Functional for 1C71-S003B

and 1C71-S003D; May 9, 2018

- SVI-E22-T1329; Division 3 HPCS Diesel Generator Functional Test; Revision 12

- SVI-E22-T2680; HPCS ECCS Integrated Test; May 20, 2018

- SVI-E22-T2680; HPCS ECCS Integrated Test; Revision 9

- WO 200516061; HPCS DG Governor Maintenance; May 20, 2018

- WO 200516196; Exercise and Service Breaker L2001; May 9, 2018

- WO 200516652; Reactor Protection System RPS MG Set B De-Energized and Energized

Motor Analysis; May 10, 2018

- WO 200517529; Perform Breaker L2003 Overhaul; May 11, 2018

- WO 200589327; Calibration Check, Power Supply Monitor Card; April 23, 2018

- WO 200591777; Verify Structural Integrity of the Diesel Generator Building Ventilation Supply

Fan 2A; June 27, 2018

- WO 200679210; Replace Fullers Earth Filter/B33 HPU B SL-1; April 27, 2018

- WO 200690610; Clean, Inspect, Lube B RPS MG; May 8, 2018

- WO 200693315; Inspect Fittings and Replace Hoses on the Division 3 Governor;

May 20, 2018

- WO 200736994; Reactor Protection System, Replace Logic Control Boards 1C71S0003B and

1C71S0003D; May 10, 2018

- WO 200737508; High Pressure Core Spray Through Wall Leak in Minimum Flow Piping

Elbow; June 12, 2018

71111.22Surveillance Testing

- SVI-B21-T0369-E; SRV And Low-Low Set Pressure Actuation Channel Functional For

1B21-N668E; May 24, 2018

- SVI-C41-T2001-A; Standby Liquid Control A Pump and Valve Operability Test;

June 27, 2018

- SVI-C51-T0030A; APRM A Channel Calibration for 1C51-K605A; April 23, 2018

- SVI-E22-T1319; Diesel Generator Start and Load Division 3; May 11, 2018

- SVI-G41-T2001; Fuel Pool Cooling and Cleanup System Pump and Valve Operability Test;

June 20, 2018

- WO 200682915; (184D) APRM A Channel Calibration for 1C51-K605A; April 23, 2018

- WO 200703535; (31D) Diesel Generator Start and Load Division 3 Functional Testing;

May 11, 2018

- WO 200718820; (92D) Fuel Pool Cooling and Cleanup System Pump and Valve Operability

Test; June 21, 2018

- WO 200719638; (92D) SRV Pressure Actuation Channel E Functional for 1B21-N668E;

May 24, 2018

71114.06Drill Evaluation

- Perry ERO Drill Scenario Guide; June 6, 2018; Revision 0

71124.03In-Plant Airborne Radioactivity Control and Mitigation

- A Fuel Handling Building Ventilation Charcoal Absorber Operability Test and Plenum

Inspection; December 11, 2016

- Bauer Air Compressor Maintenance Record; December 2017

- CR-2017-07426; Self Contained Breathing Apparatus (SCBA) Back Pack Fails Functional

Test; July 14, 2017

- CR-2017-08937; MS-C-17-08-03 Respirator Inspection Administrative Issues;

August 29, 2017

- CR-2017-12228; PDM Mask could not be Located during Monthly SCBA Inspections;

December 14, 2017

- CR-2018-00114; SCBA Back Pack Fails Functional Test; January 5, 2018

- FHB Ventilation Exhaust Flow and Filter Operability Test-A; December 12, 2016

- Firehawk M7 SCBA Annual Inspection and Flow Test Records; 2017

- Firehawk M7 SCBA Inspection Records; First Quarter 2018

- Grade D Air Quality Records; 2017-2018

- HPI-G0007; Maintenance of Respiratory Protective Equipment and Operation of the

Respiratory Cleaning/Issue Facilities; Revision 24

- NOP-OP-4301; Respiratory Protection Program; Revision 10

- NOP-OP-4310; Firehawk M7 SCBA; Revision 7

- Respiratory Protection Program Fit Test Records; Various Records

- Respiratory Protection Program Medical Qualification Records; Various Records

- Respiratory Protection Program Training Records; Various Records

- Self-Assessment; Pre-NRC Inspection, In-Plant Rad Controls and Mitigation and Occupational

Dose Assessment; February 2018

71124.04Occupational Dose Assessment

- 2017 External Dosimetry Data and Electronic Dosimeter Data; January 1 through

April 30, 2017

- CR-2016-13555; TLD Recorded a High Shallow Dose Reading; November 18, 2016

- CR-2017-042441; Discrepancy Found in Annual Dose Report to NRC; April 14, 2017

- CR-2018-00662; TLD Recorded Higher than Normal Shallow Dose Reading;

January 25, 2018

- Declared Pregnant Worker Records; Various Records

- Dosimetry Investigation/Dose Assessment; November 29, 2016

- Email from Mirion to Perry; April 25, 2018

- External Dosimetry Anomalous Record Reports; Various 2017 Records

- External Dosimetry Records; Various 2017 Records

- Generic Radiation Worker Training Lesson Plan; Revision 11

- Internal Dose Assessment Records; Various 2017 Records

- Mirion NVLAP Certification; June 30, 2017, to July 1, 2018

- Neutron Radiation Exposure Tracking Forms; April 24, 2018

- Neutron Radiological Surveys; Various Records

- NOP-OP-4202; Declared Pregnant Workers; Revision 1

- NOP-OP-4204; Special External Exposure Monitoring; Revision 10

- Personal Contamination Monitor Internal Sensitivity Test; July 26, 2016

- Portal Monitor Internal Sensitivity Test; April 5, 2016

- TLD to ED Comparison Data; Various 2017 Records

71151Performance Indicator Verification

- CR 2018-04054; NRC PI Indicator for Safety System Functional Failures exceeds the 50%

Green/White threshold; May 1, 2018

- NEI 99-02; Regulatory Assessment Performance Indicator Guideline; Revision 7

- NOBP-LP-4012; NRC Performance Indicators; Revision 6

- NOBP-LP-401204, Revision 3; Mitigating Systems Performance Index (MSPI) Unavailability

Index (UAI) & Unreliability Index (URI) for Emergency AC Power Systems; April, 2017

through March, 2018

- NOBP-LP-4012-05, Revision 2; Mitigating Systems Performance Index (MSPI) Unavailability

Index (UAI) & Unreliability Index (URI) for High Pressure Injection System (HPCS) & High

Pressure Emergency Diesel Generator (EDG); April, 2017 through March, 2018

- NOBP-LP-4012-08, Revision 2; Safety System Functional Failure; April, 2017 through

March, 2018

71153Follow-Up of Events and Notices of Enforcement Discretion

- CR 2018-03357; ONI-C51 Entered for Unplanned Change in Reactor Power; May 3, 2018

- SOI-B33; Reactor Recirculation System; Revision 37

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