IR 05000395/2019010
| ML19354A673 | |
| Person / Time | |
|---|---|
| Site: | Summer |
| Issue date: | 12/20/2019 |
| From: | James Baptist NRC/RGN-II/DRS/EB1 |
| To: | Stoddard D South Carolina Electric & Gas Co |
| Su TC RGN-II/DRS | |
| References | |
| IR 2019010 | |
| Download: ML19354A673 (13) | |
Text
December 20, 2019
SUBJECT:
VIRGIL C. SUMMER NUCLEAR STATION, UNIT 1 - TRIENNIAL INSPECTION OF EVALUATION OF CHANGES, TESTS AND EXPERIMENTS BASELINE INSPECTION REPORT 05000395/2019010
Dear Mr. Stoddard:
On November 7, 2019, the U.S. Nuclear Regulatory Commission (NRC) completed an inspection at Virgil C. Summer Nuclear Station, Unit 1. On December 12, 2019, the NRC inspectors discussed the results of this inspection with Mr. George Lippard and other members of your staff. The results of this inspection are documented in the enclosed report.
One Severity Level IV violation without an associated finding is documented in this report. We are treating this violation as a non-cited violation (NCV) consistent with Section 2.3.2 of the Enforcement Policy.
No NRC-identified or self-revealing findings were identified during this inspection.
If you contest the violation or the significance or severity of the violation documented in this inspection report, you should provide a response within 30 days of the date of this inspection report, with the basis for your denial, to the U.S. Nuclear Regulatory Commission, ATTN:
Document Control Desk, Washington, DC 20555-0001; with copies to the Regional Administrator, Region II; the Director, Office of Enforcement; and the NRC Resident Inspector at Virgil C. Summer Nuclear Station, Unit 1.
This letter, its enclosure, and your response (if any) will be made available for public inspection and copying at http://www.nrc.gov/reading-rm/adams.html and at the NRC Public Document Room in accordance with Title 10 of the Code of Federal Regulations 2.390, Public Inspections, Exemptions, Requests for Withholding.
Sincerely,
/RA Brian R. Bonser for/
James B. Baptist, Chief Engineering Branch 1 Division of Reactor Safety
Docket No. 05000395 License No. NPF-12
Enclosure:
As stated
Inspection Report
Docket Number:
05000395
License Number:
Report Number:
Enterprise Identifier:
I-2019-010-0032
Licensee:
South Carolina Electric & Gas Company (SCE&G)
Facility:
Virgil C. Summer Nuclear Station, Unit 1
Location:
Jenkinsville, SC
Inspection Dates:
November 04, 2019 to November 07, 2019
Inspectors:
M. Donithan, Operations Engineer
G. Ottenberg, Senior Reactor Inspector
M. Schwieg, Reactor Inspector
T. Su, Reactor Inspector
Approved By:
James B. Baptist, Chief
Engineering Branch 1
Division of Reactor Safety
SUMMARY
The U.S. Nuclear Regulatory Commission (NRC) continued monitoring the licensees performance by conducting a triennial inspection of evaluation of changes, tests and experiments baseline inspection at Virgil C. Summer Nuclear Station, Unit 1, in accordance with the Reactor Oversight Process. The Reactor Oversight Process is the NRCs program for overseeing the safe operation of commercial nuclear power reactors. Refer to https://www.nrc.gov/reactors/operating/oversight.html for more information.
List of Findings and Violations
Failure to Obtain License Amendment Regarding Containment Isolation Valve Technical Specification Guidance Cornerstone Significance Cross-Cutting Aspect Report Section Not Applicable NCV 05000395/2019010-01 Open/Closed Not Applicable 71111.17T The inspectors identified a Severity Level IV Non-cited Violation (NCV) of Section 59 of Part 50 of Title 10 of the Code of Federal Regulations (10 CFR 50.59) for the licensee's failure to obtain Commission approval prior to making a procedure change that involved a change to Technical Specification (TS) 3.6.4, Containment Isolation Valves.
Additional Tracking Items
None.
INSPECTION SCOPES
Inspections were conducted using the appropriate portions of the inspection procedures (IPs) in effect at the beginning of the inspection unless otherwise noted. Currently approved IPs with their attached revision histories are located on the public website at http://www.nrc.gov/reading-rm/doc-collections/insp-manual/inspection-procedure/index.html. Samples were declared complete when the IP requirements most appropriate to the inspection activity were met consistent with Inspection Manual Chapter (IMC) 2515, Light-Water Reactor Inspection Program - Operations Phase. The inspectors reviewed selected procedures and records, observed activities, and interviewed personnel to assess licensee performance and compliance with Commission rules and regulations, license conditions, site procedures, and standards.
REACTOR SAFETY
71111.17T - Evaluations of Changes, Tests, and Experiments Sample Selection (IP Section 02.01)
The inspectors reviewed the following evaluations, screenings, and/or applicability determinations for 10 CFR 50.59 from November 4 through November 7, 2019.
(1)50.59 Screening for AOP-304.4, Rev. 4, "ARG-4, Loss of All ESF AC Power While on RHR" (2)50.59 Evaluation for ECR-50846K, Weld Repair Contingency for RV Head Inspection (3)50.59 Evaluation for ECR-50585U, A-Chiller Replacement (4)50.59 Evaluation for ECR-50884E, OPC Strategy for the GDC-17 Offsite Power Sources (5)50.59 Screening for ECR-50890, External Flooding Protection (6)50.59 Screening for ECR-50906, KWH Meter Replacement (7)50.59 Screening for ECR-72470, Replacement of D.G. OBrien Hermetic Connector with EGS Quick Disconnect (8)50.59 Screening for ECR-50753M, OCA Perimeter Upgrades - Radar Systems (9)50.59 Evaluation for ECR-50695E, EFW Flow Margin Improvement (10)50.59 Evaluation for Bases Revision Notice BRN-17-002 TS Bases 3/4 7.1.2 Change of EFW Combined Flow of 380 Gallons (11)50.59 Evaluation for ECR-71781, RMA2 Guidance (12)50.59 Screening for ECR-50912, Modification to Platform SWP-1 (13)50.59 Screening for ECR-50900, New Enclosure on Control Building Roof (14)50.59 Screening for EOP-1.0, Rev. 30, E-0, "Reactor Trip or Safety Injection" (15)50.59 Screening for EOP-1.1, Rev. 22, ES-0.1, "Reactor Trip Response" (16)50.59 Screening for ECR 50909A, RCP Oil Lift Pump Enclosure (17)50.59 Screening for ECR 70436, Control Room Differential Pressure Switches (18)50.59 Applicability Determination for ARP-045-XPN-2050, "Industrial Chiller Heat Tracing Control Panel" (19)50.59 Applicability Determination for VCS-SAP-0705, "Site Switchyard Coordinator Responsibilities" (20)50.59 Screening for AOP-112.1, Rev. 7, "ARG-2, Shutdown LOCA" (21)50.59 Evaluation ECR-50897 Replace Reactor Service Structure - Integrated Head Assembly, 2017-001 (22)50.59 Evaluation for GTP-302 Rev. 7A Change and CR 18-01032 and CR 19-02562 (23)50.59 Screening BRN 17-001, The Basis 3/4.7.6 Is Being Revised to Clarify Which Revisions or RG 1.196 and CEI 99-03 Is Applicable (24)50.59 Screening for ECR 70814, Revise Set Point for ITB00451 and ITB00452 (25)50.59 Screening for ECR 50874V, Major Revision fpr RB Cooling Permanent Power (26)50.59 Screening for ECR 50905, Boron Concentration System Monitoring Sys Elimination (27)50.59 Screening for ECR 72012, RWST Empty Alarm Set-point Change (28)50.59 Applicability Determination for ARP-016-XCP-6210-LCB1, Annunciator Response Procedure
INSPECTION RESULTS
Failure to Obtain License Amendment Regarding Containment Isolation Valve Technical Specification Guidance Cornerstone Severity Cross-Cutting Aspect Report Section Not Applicable Severity Level IV NCV 05000395/2019010-01 Open/Closed
Not Applicable 71111.17T The inspectors identified a Severity Level IV Non-cited Violation (NCV) of Section 59 of Part 50 of Title 10 of the Code of Federal Regulations (10 CFR 50.59) for the licensee's failure to obtain Commission approval prior to making a procedure change that involved a change to Technical Specification (TS) 3.6.4, Containment Isolation Valves.
Description:
In 1992, V.C. Summer requested a TS amendment from the NRC to remove Table 3.6-1 from TS in accordance with the guidance in NRC Generic Letter (GL) 91-08, "Removal of Component Lists from Technical Specifications," and the request was granted by the NRC. After the amendment was granted, the licensee relocated the table to station procedure GTP-302, Inservice Testing of Valves, revision 6A, dated March 29, 1993, and also included other valves in the list in accordance with the guidance in GL 91-08. Prior to the licensee's implementation of the procedure change as a result of the amendment, Table 3.6-1 was located in TS 3/4.6.4 and it identified the containment isolation valves (CIVs) to which the TS applied. The guidance in GL 91-08 included the following description:
"The list of containment isolation valves in the TS may not include all valves that are classified as containment isolation valves by the plant licensing basis. Generally, the FSAR identifies those valves that are classified as containment isolation valves. With this TS change, the LCO, remedial actions, and surveillance requirements will apply for all valves that are classified as containment isolation valves by the plant licensing basis."
Because they were not previously included in Table 3.6-1, the licensee added the steam generator power operated relief valves (SG PORVs) to the table which was now being maintained in GTP-302. The SG PORVs function as closed system isolation valves designed to meet the requirements of General Design Criterion (GDC) 57 in 10 CFR 50, Appendix A.
The licensee later updated GTP-302 in revision 7A, dated June 18, 1993, to include the following 'Note (2)' which was applicable to the SG PORVs:
"(2) Should this valve be found to be incapable of meeting its containment isolation requirements, i.e., inoperable per Technical Specification 3/4.6.4, action statement 3.6.4.c may be satisfied by verifying that the connected closed system is intact inside the Reactor Building."
TS 3.6.4 required that "Each Containment Isolation Valve Shall be OPERABLE.*" The TS Actions (which included action statement 3.6.4.c) stated the following:
"With one or more of the isolation valve(s) inoperable, maintain at least one isolation valve OPERABLE in each affected penetration that is open, and either:
- a. Restore the inoperable valve(s) to OPERABLE status within 4 hours4.62963e-5 days <br />0.00111 hours <br />6.613757e-6 weeks <br />1.522e-6 months <br />, or
- b. Isolate each affected penetration within 4 hours4.62963e-5 days <br />0.00111 hours <br />6.613757e-6 weeks <br />1.522e-6 months <br /> by use of at least one deactivated automatic valve secured in the isolation position, or
- c. Isolate each affected penetration within 4 hours4.62963e-5 days <br />0.00111 hours <br />6.613757e-6 weeks <br />1.522e-6 months <br /> by use of at least one closed manual valve or blind flange, or
- d. Be in at least HOT STANDBY within the next 6 hours6.944444e-5 days <br />0.00167 hours <br />9.920635e-6 weeks <br />2.283e-6 months <br /> and in COLD SHUTDOWN within the following 30 hours3.472222e-4 days <br />0.00833 hours <br />4.960317e-5 weeks <br />1.1415e-5 months <br />."
The inspectors observed that the as-approved TS action statements in TS 3/4.6.4, Containment Isolation Valves did not contain an explicit provision in action statement 3.6.4.c that allowed consideration of the closed system as being equivalent to a closed manual valve or a blind flange in order to satisfy the action statement, and that Note
- (2) was intended to provide appropriate action if that type of containment isolation valve was found to be inoperable. Although the closed system would function as a passive containment barrier similar to a closed manual valve or blind flange, the provision for its credit as such did not exist in the approved TS. The inspectors discovered that Note
- (2) was added to GTP-302 in revision 7A, and due to a revision process error did not receive a review in accordance with 10 CFR 50.59 to determine whether or not an amendment to technical specifications was required. The inspectors determined that the licensee should have obtained Commission approval prior to implementing the change in revision 7A to GTP-302 that included Note (2),because it involved a change in the TS incorporated into the license for the V.C. Summer station.
The inspectors further observed that licensee event report (LER) 2019-002-00, "Condition Prohibited by Technical Specification 3.6.4" was submitted to the NRC on October 9, 2019, regarding a failed SG PORV. The inspectors also noted that, prior to concluding an LER was required, the licensee utilized the guidance contained in GTP-302, "Inservice Testing of Valves" when they performed a past-operability review of the valve failure under action number 14 to condition report (CR) CR-18-01032, and initially inappropriately concluded that the failure did not constitute a condition prohibited by Technical Specifications (TS) because the procedure allowed action statement 3.6.4.c to be considered satisfied if the closed system inside containment was intact. Although operation of the station while the licensee may consider action statement 3.6.4.c to be met would represent an alignment not previously explicitly allowable by TS, the consequence of the licensee's failure to correctly consider the change and request an amendment prior to implementing the change was considered to be minor because the current alternate source term assumptions for radioactive release for the events where the closed system inside containment is compromised bound the presumed containment isolation valve failure because immediate release of the fission products with no mitigation is assumed.
Corrective Actions: Upon discovery, the licensee entered the issue into their corrective action program and indicated that Note
- (2) was not to be used to satisfy the action statement in TS 3.6.4.c.
Corrective Action References: CR-19-04328
Performance Assessment:
The inspectors determined this violation was associated with a minor performance deficiency. The licensee failed to perform a correct 50.59 screening and safety evaluation when considering the changes to procedure GTP-302, done in 1993. Specifically, the addition of Note
- (2) was not originally considered within the 50.59 process when the procedure was revised, and had it been considered, the licensee should have concluded that a TS amendment was required because it allowed an application of a TS action statement that was not stated in the TS. The consequence of the licensee's implementation of the change without receiving prior Commission review and approval was considered minor because the alternate source term assumptions for radioactive release for the events where the closed system inside containment is compromised bound the presumed containment isolation valve failure because immediate release of the fission products with no mitigation is assumed.
Enforcement:
The ROPs significance determination process does not specifically consider the regulatory process impact in its assessment of licensee performance. Therefore, it is necessary to address this violation which impedes the NRCs ability to regulate using traditional enforcement to adequately deter non-compliance.
Severity: The NRC's Enforcement Policy dated May 28, 2019, section 6.1.d. stated in part, SL IV violations involve, for example: Violations of 10 CFR 50.59 result in conditions evaluated as having very low safety significance (i.e., green) by the SDP." Further, the NRC's Enforcement Manual, dated October 1, 2019, Part II, section 2.1.3, "Enforcement of 10 CFR 50.59 and Related FSAR Violations," subsection D.5 stated in part, "a. Violations of 10 CFR 50.59 will be considered more than minor and categorized at Severity Level IV if: the activity or change
- (1) required prior Commission review and approval, and the licensee failed to obtain Commission approval;
- (2) the consequence of the activity or change evaluated by the SDP is minor, or of very low safety significance (i.e., Green); and
- (3) the NRC would have likely approved the change." The inspectors determined that the change required prior NRC review and approval, which was not obtained prior to implementing the change; the consequence of the change evaluated by the SDP was minor; and the NRC would have likely approved the change, if requested.
Violation: Section 59 of Part 50 of Title 10 of the Code of Federal Regulations (10 CFR 50.59) required, in part, that The holder of a license authorizing operation of a production or utilization facility may
- (i) make changes in the facility as described in the safety analysis report,
- (ii) make changes in the procedures as described in the safety analysis report, and (iii)conduct tests or experiments not described in the safety analysis report, without prior Commission approval, unless the proposed change, test or experiment involves a change in the technical specifications incorporated in the license or an unreviewed safety question." Further, 10 CFR 50.59(c) required "The holder of a license authorizing operation of a production or utilization facility who desires
- (1) a change in technical specifications or (2)to make a change in the facility or the procedures described in the safety analysis report or to conduct tests or experiments not described in the safety analysis report, which involve an unreviewed safety question or a change in technical specifications, shall submit an application for amendment of his license pursuant to 50.90." Contrary to the above, in 1993, the licensee made a change to a station procedure that involved a change in the technical specifications incorporated in the license and did not submit an application for an amendment of the license pursuant to 50.90, as required by 10 CFR 50.59(c). Specifically, the addition of Note
- (2) to procedure GTP-302, Inservice Testing of Valves changed the interpretation of the TS as written but did not change the wording of the TS to match the intended usage of Note (2).
Enforcement Action: This violation is being treated as a non-cited violation, consistent with Section 2.3.2 of the Enforcement Policy.
EXIT MEETINGS AND DEBRIEFS
The inspectors verified no proprietary information was retained or documented in this report.
- On December 12, 2019, the inspectors presented the triennial inspection of evaluation of changes, tests and experiments baseline inspection results to Mr. George Lippard and other members of the licensee staff.
- On November 7, 2019, the inspectors presented the On site debrief inspection results to Mr. George Lippard and other members of the licensee staff.
DOCUMENTS REVIEWED
Inspection
Procedure
Type
Designation
Description or Title
Revision or
Date
71111.17T Calculations
DC03290-007
Rev. 0
DC03290-008
Evaluation of Foam Seal, Drain Pipe Plugs, and Floor Mats
for External Flooding Event
Rev. 0
DC03690-005
Evaluation for SWPH Pipe Rupture/Flooding Effects
Rev. 2
Corrective Action
Documents
CR-18-01032
While performing STP-121.002A, B PORV failed to open
Dated
3/8/2018
CR-19-02562
Reportability of B SG PORV failing to open
Dated
07/17/2019
Corrective Action
Documents
Resulting from
Inspection
CR-19-03964
ARP-016-XCP-6210-LCB1 Applicability Determination Check
Boxes Were Checked
Dated
11/06/2019
CR-19-03972
GTP-302 May Not Be the Right Place for Note 2
Dated
11/07/2019
CR-19-03973
Exceptions to Reg. Guide 1.75 Not Specified
Dated
11/07/2019
CR-19-03974
50.59 Screening Question 3 Did Not Cover Adverse Effect of
Direct Trip to Feederer Breakers
Dated:
11/07/2019
CR-19-04328
GTP-302 Addition of Note Without Licensee Amendment
Request
Dated
2/05/2019
Engineering
Changes
ECR 50897
Replacement Reactor Service Structure-Integrated Head
Assembly
Dated
2/01/2017
ECR 50905
Boron Concentration Monitoring System Elimination
Dated
06/11/2018
ECR 70814
Revise Set-Point For ITB00451 and ITB00452
Dated
08/09/2019
ECR 72012
RWST Empty Alarm Setpoint Change
Dated
2/16/2017
ECR-50585
A-Chiller Replacement
Rev. U
ECR-50695
EFW Flow Margin Improvement
Rev. E
ECR-50753
OCA Perimeter Upgrades - Radar Systems
Rev. M
ECR-50884
OPC Strategy for the GDC-17 Offsite Power Sources
Rev. E
ECR-50890
External Flooding Protection
Rev. 0
ECR-50900
New Enclosure on Control Building Roof
Rev. 0
Inspection
Procedure
Type
Designation
Description or Title
Revision or
Date
ECR-50906
KWH Meter Replacement
Rev. 0
ECR-71781
RMA2 Guidance
Rev. 0
ECR-72470
Replacement of D.G. OBrien Hermetic Connector with EGS
Quick Disconnect
Rev. 0
Engineering
Evaluations
DC0295A-006
Qualification of CB Roof Enclosure
Rev. 3
Miscellaneous
50.59 Evaluation
Report Log
Number 2016-
0001
ECR50695E, EFW Flow Margin Improvement
Rev. 0
Bases Revision
Notice
BRN No.17-002
Dated
05/23/2017
CGE-15-70
Transmittal of LTR-PL-15-66, V.C. Summer Emergency
Feedwater (EFW) Flow Margin Increase Engineering Impact
Results Summary
Dated
11/03/2015
D2018024
Incidental Submergence of Rosemount 3152N Pressure
Transmitter with Curtiss-Wright Generation 1 EGS QDC
Rev. A
EGS-TR-913601-
Nuclear Environmental Qualification Report of EGS 3/4 Inch
Quick Disconnect Electrical Connector
Rev. B
Evaluation 14-10
EFW Mod ECR50695E Reliability
Dated
05/09/16
FATR-079-
351025399-01
Factory Acceptance Test Report for NLI HVAC Chiller
Rev. 1
GTP-302
In-service Testing of Valves
Rev. 7 Chg.
A
ICES # 434234
During the SG PORV Operability Test Header Power Relief
Valve
Dated
04/03/2018
Procedure
Development
Form
GTP-302 Rev 7A Inservice Testing of Valves
Dated
06/18/93
QR-0798582-2
Qualification Report for 4" Ball Valve with Beck Actuator
Model 11-288-119306-04
Rev. 0
RN 12-030
FSAR Revision Notice ECR50695B/C/E/G
Dated
11/08/2017
Inspection
Procedure
Type
Designation
Description or Title
Revision or
Date
RN 18-008
To Eliminate Boron Concentration Monitoring (BCMS)
Dated
10/17/2019
RN No.16-030
Correcting Mislabeled Fire Damper
Dated
03/09/2017
USA 50.59 Resource Manual
Rev. 3
Technical
Specifications
Change Request
Removal of Table 3.6-1 Per Generic Letter 91-08 (TSP
20003-0)
dated
09/23/1992
TSP 920003
Proposed Technical Specification Change
Dated
09/23/1992
An Evaluation of Solid State Logic Reactor Protection in
Anticipated Transients
Dated
07/1971
Procedures
ARP-016-XCP-
210-LCB1
Annunciator Response Procedure
Rev. 2
ECR 50874
Major Revision for RB Cooling Upgrade
Dated
01/08/2015
GTP-302
Inservice Testing of Valves
Revs. 6A, 7,
7A, and 17
OAP-109.1
Guidelines for Severe Weather
Rev. 5
Document Review and Approval Process
Rev. 38
VCS-ERP-0119
ERU Flooding Response
Rev. 1