IR 05000390/2014612

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IR 05000391/2014612, on 12/19/2014, Watts Bar Nuclear Plant, Unit 2, Construction Fire Protection Program Inspection
ML15034A211
Person / Time
Site: Watts Bar Tennessee Valley Authority icon.png
Issue date: 02/02/2015
From: Shaeffer S M
NRC/RGN-II/DRS/EB2
To: Skaggs M D
Tennessee Valley Authority
References
IR 2014612
Download: ML15034A211 (43)


Text

February 2, 2015

Mr. MichaelSenior Vice President Nuclear Generation Development and Construction Tennessee Valley Authority 6A Lookout Place 1101 Market Street Chattanooga, TN 37402-2801

SUBJECT: WATTS BAR NUCLEAR PLANT UNIT 2 CONSTRUCTION FIRE PROTECTION PROGRAM INSPECTION, NRC INSPECTION REPORT NO. 05000391/2014612

Dear Mr. Skaggs:

On December 19, 2014, the U.S. Nuclear Regulatory Commission (NRC) completed an inspection of construction activities at your Watts Bar Unit 2 reactor facility. The enclosed inspection report documents the inspection results, which were discussed on December 19, 2014, with you and other members of your staff.

This inspection examined the licensee's readiness in the area of fire protection, fire safe shutdown procedures, and operator manual actions to support future licensing. The majority of the items reviewed were not currently required under the existing Watts Bar Unit 2 construction permit. Items identified and described in this report which the NRC determined as not meeting the Unit 1/Unit 2 As-Constructed Fire Protection Report require corrective actions. The NRC staff will evaluate your resolution for these items during subsequent inspections. Based on the results of this inspection, no findings were identified during this inspection. In accordance with 10 Code of Federal Regulations (CFR) 2.390 of the NRC's "Rules of Practice," a copy of this letter, its enclosure, and your response (if any) will be available electronically for public inspection in the NRC Public Document Room or from the PubliclyAvailable Records (PARS) component of NRC's document system (ADAMS). ADAMS is accessible from the NRC Web site at http://www.nrc.gov/reading-rm/adams.html (the Public Electronic Reading Room).

Should you have questions concerning this letter, please contact us.

Sincerely,/RA/ Scott M. Shaeffer, Chief Engineering Branch 2 Division of Reactor Safety

Docket No. 50-391 Construction Permit No: CPPR-92

Enclosure:

Inspection Report 05000391/2014612 w/Attachment

cc w/encl: (See next page)

SUMMARY

This team inspection included aspects of engineering and construction activities performed by

TVA associated with the Watts Bar Nuclear (WBN) Plant Unit construction project. This report covered a three-week period of inspections in the areas of operational readiness activities (Fire Protection), and follow-up of other activities. The inspection program for Unit construction activities is described in Nuclear Regulatory Commission (NRC) Inspection Manual Chapter (IMC) 2517, "Watts Bar Unit Construction Inspection Program." Information regarding the WBN Unit Construction Project and NRC inspections can be found at http://www.nrc.gov/info-finder/reactor/wb/watts-bar.html. Inspection Results

  • No findings were identified in the fire protection area. However, the inspectors were unable to accomplish all the inspection objectives due to observations identified regarding feasibility and reliability of operator manual actions; validation of technical basis for fire safe shutdown procedures; lack of surveillance procedures for some fire protection features; degraded fire penetrations; and completion of work related to the installation of Unit Containment fire protection features, emergency lights, and emergency communication equipment. Items identified and described in this report which the NRC determined as not meeting the Unit 1/Unit As-Constructed Fire Protection Report require corrective actions. The NRC staff will evaluate your resolution for these items during subsequent inspections.
  • The inspectors concluded that issues pertaining to several open items, including two Bulletins, one Generic Letter, and one construction deficiency report have been appropriately addressed for WBN Unit 2. These items are closed.

REPORT DETAILS

Summary of Plant Status

During the inspection period covered by this report, Tennessee Valley Authority (TVA) performed construction completion and preoperational testing activities on safety-related systems and continued engineering design activities of the Watts Bar Nuclear (WBN) Plant, Unit 2 (U2).

III. OPERATIONAL READINESS ACTIVITIES

F. 1 Fire Protection This inspection was conducted in accordance with applicable portions of Inspection Procedures (IPs) 64704 - Fire Protection Program; 64100 - Post-fire Safe Shutdown, Emergency Lighting and Oil Collection Capability at Operating and Near-Term Operating Reactor Facilities; and 71111.05T - Fire Protection (Triennial) as a guidance document. The objective of the inspection was to review a sample of fire risk-significant fire areas (FAs) to evaluate implementation of the fire protection program (FPP) as described in the Watts Bar Nuclear Plant Unit 1/Unit 2 As-Constructed Fire Protection Report (FPR). The FAs were selected based on a review of available risk information as analyzed by a senior reactor analyst from Region II, a review of previous inspection results, plant walkdowns of FAs, consideration of relational characteristics of combustible material to targets, and location of equipment needed to achieve and maintain safe shutdown (SSD) of the reactor. The FAs chosen were identified as follows:

  • FA 29, Room 757.0-A22, 125-V Vital Battery Board Room IV (Analysis Volume (AV) -055)
  • FA 31, Room 757.0-A24, 6.9 KV & 480-V Shutdown Board Room B (AV-057)
  • FA 48, Room 692.0-C9, Communications Room (AV-076 & AV-076A)
  • FA 60, Room 711.IPS - Electrical Board Room, 480-V Board Room (AV-089)
  • FA 42, Room 772.0-A12, 480-V Transformer Room 2A (AV-069) In addition, the inspection included a review of fire protection features added for Unit 2 operation to verify that installation was in compliance with the As-Constructed FPR and applicable National Fire Protection Association (NFPA) Codes. F.1.1 Postfire Safe Shutdown, Emergency Lighting and Oil Collection Capability at Operating and Near-Term Operating Reactor Facilities (IP 64100) 02.01 Section III.G.2, Redundant Train Safe Shutdown Capability 1. Protection of Redundant Train Safe Shutdown Capability

a. Inspection Scope

The inspectors reviewed the piping and instrumentation diagrams, safe shutdown analysis, and safe shutdown equipment list to verify that the shutdown methodology had properly identified the components and systems necessary to achieve and maintain safe shutdown conditions for equipment in the fire areas/analysis volumes selected for review. For each of the selected fire areas/analysis volumes, the inspectors reviewed 4 the adequacy of separation and protection provided for the redundant train of cables and equipment required to achieve and maintain hot shutdown conditions.

On a sample basis, the inspectors verified that the systems and equipment identified by the licensee as being required to achieve and maintain hot shutdown conditions would remain free of fire damage in the event of a fire in the selected fire areas/ analysis volumes. Specifically, the inspectors evaluated the adequacy of electrical independence, physical separation, and fire protection features provided for cables and equipment needed to assure the operation of systems that were relied on to achieve and maintain hot shutdown conditions in the event of a fire. The evaluation included a review of cable routing data for a sample of components. The specific components selected for review are listed in the attachment.

b. Observations and Findings

No findings were identified.

c. Conclusions

The inspectors concluded that protection of redundant train safe shutdown capability was ready for implementation as described in the As-Constructed FPR. 2. Protection from Damage from Fire Suppression Activities

a. Inspection Scope

The inspectors verified that redundant trains of systems required for hot shutdown, including dual unit shutdown, which were located in the same fire area, were not subject to damage from fire suppression activities or from the rupture or inadvertent operation of fire suppression systems. The inspectors evaluated whether manual water-based firefighting activities from fires within the selected FAs could adversely affect equipment credited for SSD, inhibit access to alternate shutdown equipment, or adversely affect local operator actions required for SSD. The inspectors reviewed calculations of suppression system discharge, drainage capacity of floor drains and estimated water accumulations relative to the submergence of electrical equipment. Fire Strategies (pre-fire plans); fire brigade training procedures, and abnormal procedures for fire events were also reviewed to verify that inter-area migration of water would not adversely affect SSD equipment or the performance of operator manual actions. Walkdowns of the selected FAs were performed to confirm that drains were open and free of debris and that electrical equipment was curbed or elevated where submergence was possible.

b. Observations and Findings

The inspectors noted that pre-fire plans for the selected FAs did not address strategies for managing water runoff during and after fire events to ensure that fire SSD equipment was not adversely impacted. The licensee entered this condition in their corrective action program as PER 969435.

No findings were identified.

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c. Conclusions

The inspectors concluded that equipment necessary for SSD would not be subject to damage from fire suppression activities or from the rupture or inadvertent operation of fire suppression systems. 3. Circuit Analyses

a. Inspection Scope

The inspectors reviewed the licensee's post-fire safe shutdown analysis and the As-Constructed FPR to verify that the licensee had identified both required and associated circuits that may impact SSD. On a sample basis, the inspectors verified that the cables of equipment required for achieving and maintaining safe shutdown conditions, in the event of fire in the selected FAs, had been properly identified. In addition, the inspectors verified that these cables had either been adequately protected from the potentially adverse effects of fire damage, mitigated with approved manual operator actions, or analyzed to show that fire-induced faults (e.g., hot shorts, open circuits, and shorts to ground) would not prevent SSD. In order to accomplish this, the inspectors reviewed electrical schematics and cable routing data for power and control cables associated with each of the selected components. In addition, on a sample basis, the adequacy of circuit protective coordination for the safe shutdown systems' electrical power and instrumentation busses were evaluated. A review of the licensee's fuse replacement procedure was conducted to determine if adequate administrative controls exist to prevent the inadvertent substitution of incorrectly sized fuses in critical circuits. Additionally, a review was conducted of cable routing information for the motor drive fire pumps. The components reviewed are listed in the attachment.

The inspectors also reviewed logic diagrams and circuitries of the diesel generators to verify that postulated spurious signals would not prevent the diesels from performing their function if needed to safely shutdown the plant.

b. Observations and Findings

No findings were identified.

c. Conclusions

Based upon the review of protection of circuit required for safe shutdown, the inspectors concluded that the reviewed activities were ready for implementation as described in the As-Constructed FPR. 4. Cold Shutdown Repairs

a. Inspection Scope

The inspectors sought to review the licensee procedures, equipment, and materials credited for repairing components required for cold shutdown. The inspectors sought to review and verify that repair equipment, components, tools, and materials (e.g., pre-cut cable connectors with prepared attachment lugs) were available and accessible on site to plant personnel.

b. Observations and findings No findings were identified.

c. Conclusions

At the time of the inspection, the licensee had not developed procedures to incorporate cold shutdown repairs. This inspection item will remain open until inspection activities are conducted to verify adequacy of cold shutdown repairs procedures. 5. Manual actions as compensatory measures for SSD

a. Inspection Scope

For the selected FAs, the inspectors reviewed the applicable attachments specified in Procedure 0-AOI 30.2, Fire Safe Shutdown, Rev. 0 to assess the applicable information to relevant design requirements specified in calculations, the As-Constructed FPR, training material, and other applicable reference materials. The inspectors reviewed applicable job performance measures (JPM) to assess the training aspects of operators. The inspectors verified a subset of operator manual actions (OMAs) to determine if these were feasible and reliable. To assess the feasibility and reliability of the OMAs, the inspectors used the guidance provided in IP 71111.05T, paragraph 02.02.j.2, and NUREG/CR 1852, "Demonstrating the Feasibility and Reliability of Operator Manual Actions in Response to Fire."

b. Observations and Findings

The inspectors identified multiple observations with the reviewed procedures regarding lack of technical basis for procedure steps, verification and validation of analysis assumptions, and inadequate flow down of design requirements to the procedures. The identified observations included:

  • Calculation EPMSMC110292, Section 4.0, Assumptions, stated in part the basis for establishing natural circulation cooldown from hot standby to cold shutdown. The calculation specified a cooldown rate of 17 degrees Fahrenheit per hour yet procedure 0-AOI-30.2 C28, Step 26.2.2 specified a rate of 25 degrees Fahrenheit.

The inspectors identified that this inconsistency did not have a technical basis. The licensee captured this condition in the corrective action program as PER 970586.

  • Job performance measure, 3-OT-JPMA047C006023847, Operate Steam Generator (S/G) #1 AND #2 TD AFW LCVS (Locally With N2) Per SOI- 3.02, Performance Step: [2.6], directed the performer to check pressure indicator, 1-PI 400D and to verify that pressure was within 85 to 95 psig. This JPM supported the auxiliary feedwater system description, WBN-SDD-N3-3B-4002. The reviewed procedure did not provide clear actions to throttle the level control valves (LCVs) associated with auxiliary feedwater. System description WBN-SDD-N3-3B-4002 stated that the operator must go to one of the emergency control stations just outside the South Main Steam Valve Room and manually align the high pressure nitrogen bottles and associated piping to take local manual control of the LCVs.

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  • Procedure 0-AOI-30.2 C.30, Step 13.4 required the operator to control S/G flow to S/Gs #1 and #2 using 0-LIC 164 and 0-LIC 156. The procedure did not provide steps to take local manual control of the LCVs. The licensee captured these conditions in the corrective action program as PER 914685.
  • Calculation EDQ00099920090016, Rev 2, Appendix R - Units 1 & 2 Manual Action Requirements, Section B.21, stated in part that the Watts Bar Appendix R analysis did not support liquid letdown through the pressurizer power operated relieve valves (PORVs) since adequate pressure control for maintaining subcooling margin for natural circulation cooldown was difficult. The calculation further stated that the head vents should be used for reactor coolant system (RCS) letdown and the pressurizer PORVs should be used for RCS pressure control only. The inspectors identified the following:
  • Procedure 0-AOI-30.2 C.30, Step 22 directed operators to use the A train pressurizer PORV to control pressure for Unit 1 and Unit 2. However, 0-AOI-30.2 C.30, Step 23 and Step 24 allowed operators to use either A or B head vents or A train pressurizer PORVs for RCS letdown control.
  • Procedure 0-AOI-30.2 C28, Step 27 directed operators to use the A train pressurizer PORV to control RCS pressure for Unit 1 and Unit 2. However, 0-AOI-30.2 C28, Step 28.2 gave the operator the option to use the PORV for RCS letdown. The licensee captured these conditions in the corrective action program as PER 960956.
  • The licensee did not provide suitable procedural guidance for operating the emergency raw cooling water (ERCW) system during fire events at the Intake Pumping Station. The inspectors determined that Procedure 0-AOI-30.2, C.62, did not provide specific guidance on which ERCW pumps to operate. The additional guidance was required because pumps on both trains would be unavailable because of postulated fire damage. The licensee captured this condition in the corrective action program as PER 960916. No findings were identified.

c. Conclusions

The inspectors concluded that manual actions as compensatory measures for SSD were not ready for implementation as described in the As-Constructed FPR. Additional inspection activities are required to verify adequacy of corrective actions and extent of condition reviews conducted by the licensee.

02.02 Sections III.G.3 and III.L, Alternate and Dedicated Shutdown 1. Alternate Shutdown Capability

a. Inspection Scope

The inspectors verified that WBN Dual Unit's alternative shutdown methodology had properly identified the systems and components necessary to achieve and maintain SSD. The inspectors reviewed the As-Constructed FPR, FHA, the licensee's plant procedures, system flow diagrams, electrical drawings, and other supporting documents for postulated fires in the Control Building. The inspectors also conducted a walkdown of the Auxiliary Control Room (ACR) and interviewed the licensee about the differences between Unit 1 and Unit 2 ACRs. The review included assessing whether hot shutdown from outside the main control room (MCR) could be implemented, and that transfer of control from the MCR to the ACR could be accomplished. The inspectors also verified that electrical isolation was provided for the ACR from the MCR. In addition, the inspectors evaluated the effect of fires to the new digital control system for pressurizer level control and charging / letdown controls.

b. Observations and Findings

No findings were identified.

c. Conclusions

Based upon the review of alternate shutdown capability, the inspectors concluded that the reviewed activities were ready for implementation as described in the As-Constructed FPR.

2. Cold Shutdown Repairs

a. Inspection Scope

and Findings The inspectors sought to review the licensee procedures, equipment, and materials credited for repairing components required for cold shutdown. The inspectors sought to review and verify that repair equipment, components, tools, and materials (e.g., pre-cut cable connectors with prepared attachment lugs) were available and accessible on site to plant personnel.

b. Conclusions

At the time of the inspection, the licensee had not developed procedures to incorporate cold shutdown repairs. This inspection item will remain open until inspection activities are conducted to verify adequacy of cold shutdown repairs procedures.

3. Manual actions as compensatory measures for SSD

a. Inspection Scope

For the selected FAs, the inspectors reviewed Procedure 0-AOI-30.1, Plant Fires, Rev. 0 and the applicable attachments specified in Procedure 0-AOI 30.2, Fire Safe Shutdown, Rev. 0 to assess the applicable information to relevant design requirements specified in calculations, the As-Constructed FPR, training material, and other applicable reference materials. The inspectors selected a subset of OMAs to determine if these were feasible and reliable. To assess the feasibility and reliability of the OMAs, the inspector used the guidance provided in IP 71111.05T, paragraph 02.02.j.2, and NUREG/CR 1852,

"Demonstrating the Feasibility and Reliability of Operator Manual Actions in Response to Fire."

b. Observations and Findings

The licensee developed a new series of abnormal operating instructions (AOIs) to achieve safe shutdown conditions for Units 1 and 2 during fire events. The AOIs included required performance times for specified operator actions; the licensee determined the performance times in Calculation EDQ00099920090016, "Appendix R -

Units 1 & 2 Manual Action Requirements," Rev. 3. The inspectors identified the following observations that were associated with the fire AOIs and Calculation EDQ00099920090016:

  • The procedural guidance provided to recall Auxiliary Unit Operators (AUOs) to the MCR during fire events would not provide reasonable assurance that the AUOs would be promptly recalled to MCR. Specifically, the inspectors determined that the "fire verification" methodology as described in the As-Constructed FPR was not effectively translated into procedure 0-AOI-30.1, "Plant Fires." The licensee submitted a correction to this observation in a revision to the As-Constructed FPR (ADAMS Accession No. ML15010A054.)
  • The licensee incorrectly calculated a parameter associated with the cold leg accumulators. The inspectors determined that the licensee did not consider instrument uncertainty when determining the minimum pressure for isolating the cold leg accumulators. The non-conservative value was translated into Procedure 0-AOI-30.2, Appendix D, Rev. 0. The licensee captured this condition in the corrective action program as PER 967401.
  • The guidance in Procedure AOI 30.2, C.69 would not assure that main feedwater isolation and bypass valves would be closed within the calculated time when evacuating the main control room during a fire event. The licensee captured this condition in the corrective action program as PER 967896.
  • The licensee did not provide suitable guidance for reducing RCS inventory in the fire procedures. The procedures allowed RCS inventory letdown via the pressurizer PORV which was different from the design output in Calculation EDQ00099920090016. The licensee captured this condition in the corrective action program as PER 962419.
  • The cooldown criteria in the AOIs were different than the criteria stated in Calculation EDQ00099920090016. The licensee captured this condition in the corrective action program as PER 970586.
  • The procedural guidance provided to control RCS pressure would not ensure that the pressure would be greater than the shut-off head of the safety injection pumps for one hour. The inspectors noted that Calculation EDQ00099920090016 assumed that plant cool down and depressurization would not be initiated prior to 60 minutes.
  • The licensee did not provide suitable procedural guidance for maintaining sub-cooling margin. The inspectors determined that that the magnitude of the required sub-cooling margin that was listed in the fire procedures - combined with the lack of detailed guidance for achieving plant cooldown and depressurization - would result in many of the Calculation EDQ00099920090016 computations being invalidated. The licensee captured this condition in the corrective action program as PER 969421.
  • The licensee incorrectly calculated in Calculation EDQ00099920090016 an operator action performance time associated with preventing SG overfill. The inspectors determined that the license did not account for steam generator water level instrument uncertainty and incorrectly assumed a constant steam flow from the SG safety relief valve. The licensee captured this condition in the corrective action program as PER 972134.
  • The licensee did not provide suitable procedural guidance for cold overpressure protection system when abandoning the main control room. The inspectors noted that Procedure C.69 included a note that stated that the cold overpressure mitigation system would not be available from the auxiliary control room. The licensee did not include any alternative guidance or compensatory measures in the procedure for the loss of the system. The licensee captured this condition in the corrective action program as PERs 972066 and 970587.
  • The licensee did not state the time requirement for an action associated with starting and loading the emergency diesel generators in procedure C. 69. The inspectors noted that a 340 seconds time critical action (WBN-SDD-N3 4002, Standby Diesel Generator System, Rev. 17) was not translated into the fire procedure.

Additionally, a supporting calculation that determined the 340 seconds requirement must be re-performed because it could not be located by the licensee. The licensee captured this condition in the corrective action program as PER 824165.

  • The licensee did not provide suitable procedural guidance for solid plant operations when abandoning the main control room. The inspectors determined that guidance in the fire procedure conflicted with other design requirements. During the inspection, the licensee noted that the safe shutdown analysis did not rely on solid plant operations; and plans to remove solid plant operations from the procedure.

The licensee captured this condition in the corrective action program as PER 972060.

  • The licensee did not provide suitable procedural guidance for operating the reactor vessel vent throttle valves. The inspectors noted that document WBN-SDD-N3 11 4001, Reactor Coolant System, Rev. 31, stated that reactor vessel vent throttle valves shall be opened slowly such that it takes a minimum of five (5) seconds for the valve opening stroke to be completed. The inspectors determined that this guidance was not translated into the fire AOIs. The licensee captured this condition in the corrective action program as PER 969430.

No findings were identified.

c. Conclusions

The inspectors concluded that manual actions as compensatory measures for SSD were not ready for implementation as described in the As-Constructed FPR. Additional inspection activities are required to verify adequacy of corrective actions and extent of condition reviews conducted by the licensee. 02.03 Section III.J, Emergency Lighting

a. Inspection Scope

The As-Constructed FPR, Part II, Section 12.7 states that in accordance with the requirements of 10 CFR 50 Appendix R, Section III.J, eight-hour emergency battery pack lighting is provided in areas required for manual operation of safe shutdown equipment and in the access/egress routes to these areas. Additionally, the FPR states that operators carry an alternate battery lighting (portable hand held lantern) when they are directed to perform a required OMA based upon the fire effects.

The inspectors sought to review installation, design aspects, and maintenance of the fixed 8-hour battery pack emergency lighting units required by 10 CFR 50 Appendix R, Section III.J and the As-Constructed FPR. The inspectors walked down steps of the post-fire SSD procedures for the selected FAs to observe the placement and coverage area of the lights required to illuminate operator access and egress pathways, and any equipment requiring local operation and/or instrumentation monitoring for post-fire SSD.

b. Observations and Findings

The inspectors were informed by the licensee that Watts Bar Unit 2 has numerous areas in which the battery powered emergency lights are either missing or inadequate. The licensee is currently in the process of installing new eight - hour emergency lighting units. The installation is being done under DCN-54871.

No findings were identified.

c. Conclusions

At the time of the inspection, the licensee had not completed the installation of required emergency lighting units required for Dual Unit operations. This inspection item will remain open until inspection activities are conducted to verify the installation and adequacy of emergency lighting units and as part of the follow-up inspection for CDR 83-61.

02.04 Section III.O, Oil Collection Systems for Reactor Coolant Pumps (RCP)

a. Inspection Scope

The inspectors sought to verify that the design and installation of the RCPs oil collection system was in compliance with Section III.O of Appendix R.

b. Observations and Findings

The licensee informed the inspectors that the RCPs oil collection system was currently being installed and tested to ensure compliance with Section III.O of Appendix R. The work is being done as part of the corrective actions for CDR 81-88 and CDR 84-32.

No findings were identified.

c. Conclusions

At the time of the inspection, the licensee had not completed the installation of the oil collection system for the reactor coolant pumps. This inspection item will remain open until inspection activities are conducted to verify the installation of the reactor coolant pumps oil collection system units. F.1.2 Fire Protection Program (IP 64704) 02.02/03 Procedures to Implement the Entire Fire Protection Program 1. Combustible Material Control, Housekeeping, and Fire Hazard Reduction

a. Inspection Scope

The inspectors verified that the control of transient combustibles program was revised to incorporate Dual Unit operations. The inspectors conducted tours of numerous plant areas that were important to reactor safety, including the selected FAs, to verify the licensee's implementation of FPP requirements as described in the As-Constructed FPR, and Procedures NPG-SPP-18.4.7, Control of Transient Combustibles, Rev. 5 and TI-211, Fire Protection, Rev. 6. For the selected FAs, the inspectors evaluated generic fire protection training; fire event history; the potential for fires or explosions; the combustible fire load characteristics; and the potential exposure fire severity to determine if adequate controls were in place to maintain general housekeeping consistent with the As-Constructed FPR and administrative procedures. The inspectors observed the licensee perform an inspection of transient combustibles in the Auxiliary Building in accordance with TI-211. The inspectors also reviewed a sample of transient combustible permits for Unit 2 activities to verify adequate implementation of the program.

b. Observations and Findings

No findings were identified.

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c. Conclusions

The inspectors concluded that the combustible control program was ready for implementation as describe in the As-Constructed FPR. 2. Administration / Fire Control Capabilities

a. Inspection Scope

The inspectors verified that fire protection equipment added for Unit 2 operation was included in the operating requirements (ORs) described in Part II of the As-Constructed FPR. The inspectors reviewed the administrative controls for out-of-service, degraded and/or inoperable fire protection features (e.g. detection and suppression systems, and passive fire barriers) to verify that short-term compensatory measures were adequate for the degraded function or feature until appropriate corrective actions could be taken. The inspectors reviewed NPG-SPP-18.4.6, Control of Fire Protection Impairments, Rev 5 to verify that the impairment program was revised to incorporate Dual Unit operations.

The inspectors reviewed a sample of impairment permits for Unit 2 to verify adequate implementation of the program and to evaluate the adequacy of compensatory measures. The inspectors also reviewed impairment and compensatory measures forms for fire watches tours to confirm they were being performed within the allowable time frames. Hourly and roving fire watch personnel were interviewed to ascertain that their duties and responsibilities were properly understood.

b. Observations and Findings

The inspectors noted that the licensee did not prescribe appropriate compensatory measures for all fire areas adversely affected by the unavailability of the diesel driven fire pump. The licensee determined in the FHA that several fire areas would have inadequate fire suppression capability with the diesel fire pump out-of-service. As a result, the As-Constructed FPR prescribed compensatory measures for these fire areas.

The inspectors determined that the licensee did not identify a fire in the Control Building as an area that also required compensatory measures. The As-Constructed FPR stated that all motor driven fire pumps would be adversely affected in a Control Building fire. The As-Constructed FPR, Part II, 14.2.1 did not list the Control Building as an area that required enhanced compensatory measures.

The licensee entered this issue in their corrective action program as PER 966670. The licensee committed to revise the appropriate 0-AOI-30.1 and 30.2 procedures to ensure the electric fire pumps remain running or are restarted as appropriate once the transfer switches are placed in the AUX position. The licensee stated that the electric fire pumps could be made available by operation of the transfer switches and associated start switches in the 480V Shutdown boards located in the Auxiliary Building. In addition, the licensee stated that the As-Constructed FPR needed be revised to address the availability of the motor driven fire pumps after transfer switch operation. Through the review of electrical and block diagrams, the inspectors validated that the motor driven fire pumps could be started from the respective 480V Shutdown boards located in the Auxiliary Building.

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c. Conclusions

Based upon the review of the fire impairment program, the inspectors concluded that the program needed to be revised to address the availability of the motor driven fire pumps for fires in the Control Building. This inspection item will remain open until the corrective actions related to PER 966670 are implemented. 3. Fire Risk Maintenance Evolutions

a. Inspection Scope

The inspectors reviewed Procedure NPG-SPP-18.4.8, Control of Ignition Sources (Hot Work), Rev. 3 and the As-Constructed FPR to verify that the hot work program was revised to incorporate Dual Unit operations. The inspectors also reviewed Procedure FPT013.000, Fire Protection Training, Rev.1 and associated attachments. The inspectors observed on going hot work activities for Unit 2 and reviewed a sample of hot work permits for Unit 2 to verify adequate implementation of the program.

b. Observations and Findings

No findings were identified.

c. Conclusions

The inspectors determined that the hot work program was ready for implementation as described in the As-Constructed FPR.

4. Ventilation

a. Inspection Scope

The inspectors reviewed firefighting pre-plan strategies; fire brigade training procedures; fire damper locations; HVAC drawings; and fire response procedures to verify that inter-area migration of hot gases and smoke was addressed and accessed that it did not have an adverse impact on safe shutdown equipment and OMAs. Field walk-downs of selected dampers were performed to verify their installation was performed in accordance with manufacturer's requirements and that the dampers were in proper operating condition.

b. Observations and Findings

The inspectors noted that Part II, Section 8.3.62 of the As-Constructed FPR stated that OMA 1016 was feasible and reliable because the licensee demonstrated that there was adequate time available (margin) for the AUO to reliably perform this action. The licensee also stated that there were not any environmental factors that could adversely impact the OMA; and that local indication for monitoring nitrogen cylinder pressure and regulator adjustment were available. The action involved the operation of the SG PORV to control secondary pressure and to provide a controlled means of removing decay 15 heat. The licensee also determined that the action must be initiated at 60 minutes after the reactor is tripped.

The OMA is required for a fire in the 6.9KV & 480V Shutdown BD RM B (757.0-A24) and performed in the 480V Shutdown BD RM 2A (757.0-A21), which is adjacent to room 757.0A-24. These two rooms are located in different fire areas. During plant walkdowns, the inspectors noted that two fire dampers were installed in the wall separating both rooms and that they were installed very close to the floor (~1 foot from the floor). The inspectors performed fire modeling to determine if the dampers would close quick enough to prevent fire propagation and smoke migration from 757.0-A24 to 757.0-A21. The inspectors noted that it would require a significant fire for the dampers to close, but there was reasonable assurance that they will close to prevent fire propagation to the adjacent room. However, the inspectors noted that a significant amount of smoke will migrate through the dampers. The inspectors determined that smoke and the reduced visibility could prevent accessing the necessary equipment and hinder successful performance of the OMA.

The licensee acknowledged that they did not account for smoke migration in their analysis to ensure that it will not affect performance of the OMA. The licensee's review indicated that the demonstration of 100% margin bounded uncertainties related to smoke migration and other unknowns (e.g. increased noise levels from the fire, the operation of suppression equipment, and from personnel shouting instructions; water on the floor possibly delaying personnel movements; obstruction from charged fire hoses; increased heat and humidity resulting from fire-induced loss of heating, ventilation, and air conditioning (heat stress); or too many people getting in each other's' way). In addition, Part V, Section 2.1 of the As-Constructed FPR, stated that a robust defense-in-depth fire prevention/protection program provided additional assurance that OMAs were both feasible and reliable. The inspectors determined that the licensee could not take credit for a robust defense-in-depth fire prevention/protection program because the location of the dampers will allow smoke migration that could prevent performance of the OMA. The licensee did not consider all of the applicable environmental factors that could adversely impact the performance of the OMA. Additionally, the licensee did not recognize that they needed to implement the acceptance criteria related to environmental factors as described in Section 2.1.2.2.b of Part V. Section 2.1.2.2.b stated, in part, "The 100% time margin or performance time plus uncertainty allowances from paragraph 1.a and 1.b above ensures adequate time to reach the control location and perform the action. Additional time margin must be included for OMAs required for a fire in an area lacking robust defense-in-depth fire prevention/protection." Based on the above information, the inspectors determined that OMA 1016 was not feasible and reliable. The licensee entered this issue in their corrective action program as PER 967466 and committed to perform an extent of condition review to determine if there were other OMAs that could be adversely impacted by smoke migration.

No findings were identified.

c. Conclusions

Based on the inspection activities related to the above section, the inspectors determined that OMA 1016 was not ready for implementation as described in the As-16 Constructed FPR. Additional inspection activities are required to verify corrective actions related to PER 967466 and to review the extent of condition analysis. 5. Emergency Communications

a. Inspection Scope

The guidelines established by BTP CMEB 9.5-1, Section D.5. "Lighting and Communication," requires that a communications system should be provided for use by the fire brigade and other operations personnel required to achieve safe plant shutdown. Also fixed repeaters installed to permit use of portable radio communication units should be protected from exposure fire damage. The As-Constructed FPR, Part II, Section 12.8 states that the in-plant radio signal will be the primary means of communication for performing manual actions and for the fire brigade use. Additionally, an alternate (emergency) communication system (sound powered phones with headsets) is provided.

The inspectors sought to verify that communication capabilities were adequate to support plant personnel in the performance of OMAs to achieve and maintain SSD, and the fire brigade. The inspectors sought to perform walkdowns to assess the credited method of communications used to complete safe shutdown actions as specified in post-fire SSD procedures for the selected FAs. The inspectors also sought to verify that the design and location of communications equipment, such as repeaters and transmitters, would not cause a loss of communications during a fire.

b. Observations and Findings

During the inspection, the inspectors observed a fire drill involving the Control Building 24v/48v Battery Room. The inspectors observed that the radio communication equipment between fire brigade members was intermittent and affected brigade response. The licensee entered this issue in their corrective action program as PER969442. The licensee informed the inspectors that the communication system on Unit 2 was currently being installed and tested to support dual unit shutdown. The work is being done under DCN-60384-A.

No findings were identified.

c. Conclusions

At the time of the inspection, the licensee had not completed the installation of the new communication system. This inspection item will remain open until inspection activities are conducted to verify the installation and adequacy of the communication system per DCN 60384-A. 02.04 Installation, Operability, and Maintenance of Fire Protection Systems and Equipment 1. Passive Fire Protection

a. Inspection Scope

The inspectors walked down the selected FAs to evaluate the adequacy of the fire resistance of barrier enclosure walls, ceilings, and floors. This evaluation also included 17 fire barrier reinforced concrete, penetration seals, fire doors, fire dampers, and the Thermo-Lag electrical raceway fire barrier systems to ensure that at least one train of SSD equipment would be maintained free of fire damage. Construction detail drawings were reviewed as necessary to verify the fire barriers met the requirements and licensee commitments. Where applicable, the inspectors observed the installed barrier assemblies and compared the as-built configurations to the approved construction details; supporting fire endurance test data; As-Constructed FPR; and standard industry practices.

b. Observations and Findings

During the walkdowns of Unit 2 only areas, the inspectors noted three penetrations (A0006AM, A1405AM, A0220AM) in the safety injection pump room 2B-B that were degraded and in need of repair. The inspectors also could not verify that fire door A-130 (Unit 2 Ventilation and Purge Air Room) was a 3 - hour rated door as required by the As-Constructed FPR, because the door did not have a fire rating label attached. The licensee stated that prior to turning over any Unit 2 areas for operation, TI-338, Unit 2 Area Turnover Supporting Operational Readiness, Rev. 11 will be performed. The purpose of TI -338 is to provide assurance that the Unit 2 areas ready to be turned over to operations will support plant operational requirements. As part of the TI, the licensee will perform visual inspections to verify that Unit 2 areas comply with fire protection requirements and fire protection features are in compliance with the FPP.

The inspectors reviewed surveillance procedures implementing Testing and Inspection Requirements (TIR) described in Part II of the As-Constructed FPR to verify that passive fire protection equipment added for Unit 2 operations was included in the TIRs. The inspectors noted that surveillance procedure 0-SOI-13.01, Fire Detection System, Rev.

0, did not include some of the fire dampers added for Unit 2 operations. The licensee acknowledged the observation and entered the issue in their corrective action program as PER 960445.

No findings were identified.

c. Conclusions

The inspectors determined that passive fire protection features were not ready for implementation as described in the As-Constructed FPR. Additional inspection activities are required to verify corrective actions related to PER 967466 and observations related to Unit 2 fire barriers. 2. Active Fire Protection

a. Inspection Scope

The inspectors compared the fire detection and fire suppression systems for the selected FAs to the applicable NFPA Standard(s) by reviewing design documents and observing their as-installed configurations during in-plant walkdowns. The inspectors reviewed selected fire protection vendor equipment specifications, drawings, and engineering calculations to determine whether the fire detection and suppression methods were appropriate for the types of fire hazards that existed in the selected FAs.

18 During plant walkdowns, the inspectors observed the placement of the fire hose stations, fire extinguishers, fire hose nozzle types, and fire hose lengths, as designated in the firefighting pre-plan strategies, to verify that they were accessible and that adequate reach and coverage was provided. The inspectors reviewed completed periodic surveillance testing and maintenance program procedures for the fire detection and suppression systems and compared them to the operability, testing, and compensatory measures. This review was to assess whether the test program was sufficient to validate proper operation of the fire detection and suppression systems in accordance with their design requirements.

b. Observations and Findings

The inspectors reviewed surveillance procedures implementing TIRs described in Part II of the As-Constructed FPR to verify that active fire protection equipment added for Unit 2 operations were included in the TIRs. The inspectors identified that the surveillance procedures for fire alarm panels: -623, -625, -628, and -629 were not updated to include the additional detectors required for Dual Unit operation. The licensee acknowledged the observations and entered the issue in their corrective action program as PER 954084. At the time of the inspection, work related to the installation of fire protection features in the Unit 2 Reactor Building Annulus was not completed. The following EDCRs still need to be completed in order to close the inspection activities related to active fire suppression:

  • 54655 - Install fire detectors, additional sprinklers in the U2 Rx Bldg Annulus. Install flame detectors on the RCPs
  • 53587 - Relocate hose station 2-SPV 1207 and delete hose station 2-SPV 1203. Replace sprinkler heads in the Annulus previously plugged No findings were identified.

c. Conclusions

The inspectors determined that active fire protection features were not ready for implementation as described in the As-Constructed FPR. Additional inspection activities are required to verify corrective actions related to PER 967466 and verify adequate completion of EDCRs 54655 and 53587.

02.05 Readiness of the Licensee's Personnel to Fight Fires

a. Inspection Scope

Aspects of fire brigade readiness, training, qualifications, and responsibilities were reviewed, including but not limited to, the fire brigade's personal protective equipment, self-contained breathing apparatuses, portable communications equipment, and other fire brigade equipment to determine accessibility, material condition, and operational readiness of equipment.

During plant walkdowns, the inspectors compared firefighting pre-plan strategies to existing plant layout and equipment configurations and to fire response AOIs for the selected FAs. This was done to verify that firefighting pre-fire plan strategies and 19 drawings were consistent with the fire protection features and potential fire conditions within the area. The inspectors also verify that appropriate information was provided to fire brigade members to facilitate suppression of an exposure fire that could impact the SSD strategy.

An operating shift of the fire brigade was randomly selected to confirm that all members were currently designated and qualified with regard to their medical and fire brigade training records. Current mutual aid agreements with local outside fire departments were also reviewed. Additionally, an announced fire drill involving the Control Building 24v/48v Battery Room was observed.

b. Observations and Findings

No findings were identified.

c. Conclusions

The inspectors concluded that the reviewed activities related to the above section were ready for implementation as described in the As-Constructed FPR. 02.06 Adequacy of the Licensee's System for Conducting Programmatic Changes Necessitated by Quality Assurance (QA) Audit Results, Generic Deficiencies, or Licensee Events 1. Review and Documentation of FPP Changes

a. Inspection Scope

The inspectors verified that changes made to the FPP related to Unit 2 were performed in accordance with applicable regulations; did not constitute an adverse effect on the ability to safely shutdown Unit 1; and did not decrease the effectiveness of the overall FPP. Specifically, the inspectors verify that reviewed changes to the FPP did not adversely affect the ability to achieve and, maintain safe shutdown in the event of a fire and the changes comply with applicable codes and standards.

The inspectors reviewed a sample of design change documents, system flow diagrams, calculations, and interviewed the licensee to determine if the changes to the FPP were appropriately implemented. The modifications reviewed are listed in the attachment.

b. Observations and Findings

No findings were identified.

c. Conclusions

The inspectors concluded that the reviewed activities related to the above section of the inspection procedure conformed to the applicable regulatory requirements.

20 2. Audits, Inspections, and Assessments

a. Inspection Scope

The inspectors reviewed a sample of licensee independent audits, self- assessments, and system/program health report for thoroughness, completeness and conformance to the FPP requirements.

b. Observations and Findings

No findings were identified.

c. Conclusions

The inspectors concluded that the reviewed activities related to the above section of the inspection procedure conformed to the applicable regulatory requirements.

02.07 Effectiveness of Licensee Controls - Identification and Resolution of Problems

a. Inspection Scope

The inspectors verified that the licensee was identifying issues related to fire protection at an appropriate threshold and entering the issues in the corrective action program. For a sample of selected issues documented in the corrective action program, the team verified that the corrective actions were appropriate. The inspectors assessed the attributes of timeliness and cause determination to ensure that proposed corrective actions addressed the apparent cause, reportability, and operability determination. The inspectors reviewed operating experience from various sources to assess the licensee's response consistent with program procedures.

b. Observations and Findings

No findings were identified.

c. Conclusions

The inspectors concluded that the reviewed activities related to the above section of the inspection procedure conformed to the applicable regulatory requirements. IV. OTHER ACTIVITES OA.1.1 (Closed) Bulletin No. 1992-01: Failure of Thermo-Lag 330 Fire Barrier System to Maintain Cabling in Wide Cable Trays and Small Conduits Free from Fire Damage; Bulletin No. 1992-01 (Supplement 1): Failure of Thermo-Lag 330 Fire Barrier System to Perform Its Specified Fire Endurance Function; Generic Letter 1992-08:

Thermo-Lag 330-1 Fire Barriers (IP 35007)

a. Inspection Scope

Background: GL 92-08 informed licensees of failures in fire barrier system endurance and ampacity derating tests, installation procedures, and as-built configuration 21 discrepancies associated with the Thermal Science, Incorporated (TSI), St. Louis, Missouri, Thermo-Lag 330-1 electrical raceway fire barrier system (ERFBS) that was installed to protect safe shutdown capability. The NRC initiated a series of small scale fires test for a sample of ERFBS and issued the results of the TU Electric and NRC fires tests in Bulletins 92-01, "Failure of Thermo-Lag 330 Fire Barrier System to Maintain Cabling in Wide Cable Trays and Small Conduits Free form Fire Damage," June 24, 1992, and 92-01 Supplement 1, "Failure of Thermo-Lag 330-1 Fire Barrier system to Perform its Specified Fire Endurance Function," August 28, 1992. NRC Inspection Reports 05000391/2013609 (ADAMS Accession No. ML13353A599), 050003912013615 (ADAMS Accession No. ML13310A820), and 050003912014607 (ADAMS Accession No. ML14274A076) describes additional background information, Unit 1 and Unit 2 corrective actions, and additional NRC inspection activities for Unit 2.

Inspection Activities: The inspectors reviewed the work procedures of the ERFBS thermo-lag 330-1 material installations for conduits 1B1049F, OMC557A, and 2PLC5369A to verify that the installation activities were completed in accordance with G-98, "Installation, Modification, and Maintenance of Electrical Raceway Fire Barrier Systems," revision 9 and the approved drawings. The inspectors also reviewed ampacity de-rating, and combustible loading calculations to verify that the addition of the Thermo-lag material to the conduits were included in the revised design analysis, were adequate and completed in accordance with the approved procedures. In addition, the inspectors reviewed the Thermo-lag 330-1 material test reports to verify the material density and shear strength test results were in compliance with the design requirements.

Documents reviewed for this inspection are listed in the attachment.

b. Observations and Findings

No findings were identified. c. Conclusion Bulletin No. 1992-01, Bulletin No. 1992-01 (Supplement 1), and Generic Letter 1992-08 are closed. Thermo-Lag material installations are ongoing to meet the requirements of the approved Fire Protection Report for Unit 2. The Thermo-Lag fire barrier material installations were installed in accordance with the approved procedures and design controls were in place to address the original historical ERFBS material and installation issues.

OA.1.2 (Closed) CDR 391/84-32: Inadequate Separation of Redundant Cables Near Floor Openings (IP 35007)

a. Inspection Scope

Background: The deficiency was initially reported to the NRC on July 20, 1984, as NCR WBN MEB 8430 in accordance with 10 CFR 50.55(e). The issue was documented as CDR 390/84-36 for Unit 1 and CDR 391/84-32 for Unit 2.

The deficiency concerned the auxiliary building floor openings that were not provided with adequate protection features to meet 10 CFR 50, Appendix R, Section III.G.2, separation and fire protection requirements for redundant safe shutdown components.

The specific areas of concern in the auxiliary building were: 1) open stairwells 5 and 6 22 connecting auxiliary building elevations 692.0 ft., 713.0 ft., and 737.0 ft. at columns A4-A5/S-T and A11-A12/S-T; 2) the 10 ft. by 12 ft. steel equipment hatch (normally closed)in the hoist way between auxiliary building elevations 757.0 ft. and 772.0 ft. at columns A12-A13/S-T; and 3) three unprotected ventilation duct penetrations through the two hour-rated reinforced concrete floor between auxiliary building elevations 692.0 ft., 713.0 ft., and 737.0 ft.

The concern was that, if the nonconforming condition was not corrected, a single exposure fire from an affected redundant cable or an intervening combustible in one area could produce effects that could adversely affect another redundant cable of a safe shutdown system in another area. This could adversely affect the ability to achieve and maintain safe shutdown of the plant.

In a letter from TVA to the NRC, dated September 19, 1984, the applicant stated: "TVA will install water curtains designed in accordance with NFPA Standard 13-1983, Section 4-4.8.2, around the affected stairwell and hatch openings. Fire dampers rated at 1-1/2 hours will be installed in the affected duct penetrations." The applicant also noted: "All Unit 1 redesign and construction modifications will be accomplished per ECN 5087."

To address the corrective actions for both Unit 1 and Unit 2, the applicant installed fire dampers in the auxiliary building in the following locations: 1-ISD 3995 (elevation 713.0 ft. at column A6/S), 1-ISD 3996 (elevation 737.0 ft. at column A5/S), and 2-ISD 3988 (elevation 713.0 ft. at column A10/S). Also, the applicant installed water curtains in the following locations: 1) open stairwell 3 connecting auxiliary building elevations 692.0 ft., 713.0 ft., and 737.0 ft. at column A8/U-V; 2) the 8 ft. by 16 ft. equipment hatch openings located below elevations 713.0 ft., 737.0 ft., and 757.0 ft. at column A8/U-W; 3) the 10 ft. by 12 ft. steel equipment hatch (normally closed) in the hoist way between auxiliary building elevations 757.0 ft. and 772.0 ft. at columns A12-A3/S-T, and 4) at the auxiliary building elevator door openings located below elevations 713.0 ft., 737.0 ft., and 757.0 ft. at column A8/T. All of the water curtains are listed in the Fire Protection Report, Part VII - Deviations and Evaluations, Section 2.6.3.1.

For Unit 1 the NRC closed CDR 390/84-36 in IR 50-390/85-09 (ADAMS Accession No.

ML082190704), noting that the applicant's final report was dated September 19, 1984, with the supplemental report dated February 6, 1985. During the time period from February 19 - 22, 1985, the inspectors reviewed the installation of the auxiliary building water curtains and three new fire dampers: 1-ISD 3995 (elevation 713.0 ft. at column A6/S), 1-ISD 3996 (elevation 737.0 ft. at column A5/S), and 2-ISD 3988 (elevation 713.0 ft. at column A10/S).

Inspection Activities: The NRC documented the review of Unit 2 inspection actions in IR 50-391/2013-604 (ML13179A079). The inspection report stated that remaining actions to close this item were to implement the corrective actions associated with PER 726637 to clarify the applicable code for water curtain installations identified by NCR WBN MEB 8430 and verify the as-built condition meets the approved NFPA code of record.

The inspectors verified that the corrective action associated with PER 726637 was implemented. As a corrective action, procedure G-73, Installation, Modification, and Maintenance of the Fire Protection Systems and Features was revised to clarify that the code of record is the standard as documented in the approved FPR. In addition, the revision included that any new installation or modification not installed in accordance to 23 the code of record will be installed in accordance with the most recent edition of the Code at the time the work is performed. The inspectors also verified that the as-built water curtains met NFPA 13 Standard -1975 edition as described in the As-Constructed Fire Protection Report.

b. Observations and Findings

No findings were identified. c. Conclusion This item is closed. V. MANAGEMENT MEETINGS X1 Exit Meeting Summary An exit meeting was conducted on December 19, 2014, to present inspection results to Mr. Skaggs and other members of his staff. The inspectors identified that no proprietary information had been received during the inspection and none would be used in the inspection report. The applicant acknowledged the observations, and provided no dissenting comments.

SUPPLEMENTAL INFORMATION

KEY POINTS OF CONTACT

Applicant personnel

M. Skaggs, TVA - Senior Vice President
J. Sterchi, Fire Marshall
C. Brush, Appendix R Consultant
J. Ricks, WBN Design Engineer - Electrical
E. Haston, WBN Design Engineer - Fire Protection
J. O'Dell, WBN Licensing
T. Morgan, WBN Licensing
H. Baldner, WBN Licensing
J. Bushnell, WBN Licensing
B. Crouch, WBN Engineering
H. Baldner, TVA - Regulatory Compliance
M. Marinac, WBN Operations

INSPECTION PROCEDURES USED IP 35007 Quality Assurance Program Implementation During Construction and Pre-Construction Activities IP 64100 Postfire Safe Shutdown, Emergency Lighting and Oil Collection Capability at Operating and Near-Term Operating Reactor Facilities IP 64704 Fire Protection Program

LIST OF ITEMS OPENED, CLOSED, AND DISCUSSED

Opened

None

Closed

1992-01 BL Failure of Thermo-Lag 330 Fire Barrier System to Maintain Cabling in Wide Cable Trays and Small
Conduits Free from Fire Damage (Section OA.1.1) 1992-01 (Supplement 1) BL Failure of Thermo-Lag 330 Fire Barrier System to Perform Its Specified Fire Endurance Function (Section OA.1.1) 1992-08 GL Thermo-Lag 330-1 Fire Barriers (Section OA.1.1) 391/84-32 CDR Inadequate Separation of Redundant Cables Near Floor Openings (Section OA.1.2)

Discussed

64100 IP Postfire Safe Shutdown, Emergency Lighting and Oil Collection Capability at

Operating and Near-Term Operating Reactor Facilities (Section F.1.1) 64704 IP Fire Protection Program (Section F.1.2)

LIST OF FIRE BARRIER FEATURES INSPECTED (Refer Report Section F.1.2) Fire Barriers Floors/Walls/Ceiling Identification Description Barrier Description/Identification Fire Areas Reinforced Concrete Walls, Floors & Ceiling * FA 29, 125-V Vital Battery BD RM IV * FA 31, 6.9 KV & 480-V Shutdwn BD RM B * FA 48, Communications Room * FA 60, IPS Electrical BD RM * FA 42, 80-V Transformer RM 2A Fire Door Identification Description Door Number Room 1 Room 2 A169 757.0-A22 757.0-A24 A190 772.0-A11 772.0-A12 A45 692.0-A25 692.0-A24 A76 713.0-A19 713.0-A20 A130 737.0-A9 737.0-A10 A192 737.0-A9 737.0-A14 A43 692.0-A23 692.0-A1 A46 692.0-A26 692.0-A1 A42 692.0-A22 692.0-A1 A39 692.0-A19 692.0-A1 A40 692.0-A20 692.0-A1 A77 713.0-A19 713.0-A21 Fire Damper Identification Description Damper Number Room 1 Room 2 0-ISD-31-2785 757.0-A22 757.0-A24 0-ISD-31-4622 757.0-A22 757.0-A21 0-ISD-31-2780 757.0-A23 757.0-A24 0-ISD-31-2782 757.0-A23 757.0-A24 0-ISD-31-2785 757.0-A22 757.0-A24 0-ISD-31-4623 757.0-A24 757.0-A21 0-ISD-31-4624 757.0-A24 757.0-A21 0-ISD-31-4625 757.0-A24 757.0-A21 2-ISD-31-2500 757.0-A17 772.0-A10 2-ISD-31-3884 757.0-A17 757.0-A16 0-ISD-31-2772 757.0-A1 757.0-A24 2-ISD-31-2930 692.0-A24 692.0-A25 2-ISD-31-3929 692.0-A25 713.0-A19 2-ISD-31-3927 713.0-A19 713.0-A29 0-ISD-31-2771 757.0-A1 757.0-A24 Pen Seals, ERFBS, Thermo Lag Description Rooms of Fire Areas PS69D, PS118, PS120, PS121 480 V Shutdn Brd Transformer RM A0006AM, A1405AM, A0220AM SI Pump Room 2B-B Cable 2PP675A ERFBS Cable 1B13F ERFBS Cable 1B18F ERFBS Cable 2PP687A ERFBS Cable 2PL5392A ERFBS

Cable 2PL5394A ERFBS 6.9V Shutdn Brd RM A 480 V Shutdn Brd RM A 480 V Shutdn Brd RM A 6.9V Shutdn Brd RM A

6.9V Shutdn Brd RM A

6.9V Shutdn Brd RM A

LIST OF COMPONENTS REVIEWED (Refer to Report Section F.1.1) Component No. Description 0-BD-236-4-G 125V Vital Battery Board IV 1-BD-211-A-A 6900V Shutdown Board 1A-A

1-DG-82-A-A Unit 1 Train A Diesel Generator

1-DG-82-B-B Unit 1 Train B Diesel Generator 1-FCV-67-66-A Emerg DSL H/X 1A1 & 1A2 Supp FM HDR 1A 1-FCV-67-67-B Emerg DSL H/X 1B1 & 1B2 Supp FM HDR 1A

1-FCV-72-21B Unit 1 RWST to CS Pump 1B-B Suction

1-FCV-72-22A Unit 1 RWST to CS Pump 1A-A Suction

1-FCV-74-21B Unit 1 RHR Pump 1B-B Suction 1-FCV-74-3-A Unit 1 RHR Pump 1A-A Suction 1-HTR -68-341A Unit 1 Pressurizer Heater Backup Group 1A-A

1-LCV-62-132A Unit 1 VCT Outlet Isolation Valve

1-LI-68-320F Unit 1 Pressurizer Level Indicator

1-LI-68-339A Unit 1 Pressurizer Level Indicator 1-MTR-62-108A Charging Pump 1A-A 1-PCV-68-340-A Unit 1 Train A Pressurizer PORV

2-BD-211-B-B 6.9 kV Shutdown Board 2B-B 2-BD-212-A1-A 480V Shutdown Board 2A1-A

2-BD-212-A2-A 480V Shutdown Board 2A2-A

2-DG-82-A-A Unit 2 Train A Diesel Generator 2-DG-82-B-B Unit 2 Train B Diesel Generator 2-FCV-1-17A Unit 2 Steam Flow Aux FWP Isolation Valve

2-FCV-1-18B Unit 2 Steam Flow Aux FWP Isolation Valve

2-FCV-67-66-A Emerg DSL H/X 2A1 & 2A2 Supp FM HDR 1A

2-FCV-67-67-B Emerg DSL H/X 2B1 & 2B2 Supp FM HDR 1A 2-HTR-68-341A Unit 2 Pressurizer Heater Backup Group 1A-A 2-LCV-62-133B Unit 2 VCT Outlet Isolation Valve

2-LI-3-39 Unit 2 SG Level (Loop1)

2-LI-3-52 Unit 2 SG Level (Loop 2)

2-LI-63-50 Unit 2 RWST Level Indicator

2-LI-68-320F Unit 2 Pressurizer Level Indicator 2-LI-68-339A Unit 2 Pressurizer Level Indicator 2-LIC-3-156-A Unit 2 SG #2 Level Indicator Controller

2-LIC-3-164-A Unit 2 SG #1 Level Indicator Controller

2-MCC-213-A1-A Reactor MOV BD 2A1-A

2-MCC-213-A2-A Reactor MOV BD 2A2-A 2-MTR-3-118-A Unit 2 Motor Driven AFW Pump A-A 2-MTR-62-104B Charging Pump 2B-B

2-PCV-68-334B Unit 2 Train B Pressurizer PORV

2-PCV-68-340-A Unit 2 Train A Pressurizer PORV

HS-68-333A PORV 340A Block Valve

LI-3-164C S/G level indicator O-XS-26-1-A Fire Pump 1A-A (motor driven)

LIST OF DOCUMENTS REVIEWED

Procedures

0-AOI-30.2 C.13, Fire Safe Shutdown Room 772-A12, Rev. 0 0-AOI-30.2 C.28, Fire Safe Shutdown Room 757-A17 or 757-A24, Rev. 0
0-AOI-30.2 C.30, Fire Safe Shutdown Room 757-A22, Rev. 0
0-AOI-30.2 C.31, Fire Safe Shutdown Room - 757-A17 or 757-A24, Rev. 0
0-AOI-30.2 C.6, Fire Safe Shutdown Room - 772-A4, Rev. 0
0-AOI-30.2 C.61, Fire Safe Shutdown Room -
IPS-C West, Rev. 0 0-AOI-30.2 C.62, "Fire Safe Shutdown Room
IPS-B (B Train Strainer R,, B Train ERCW Pump Rm, B Train HPFP & Screen Wash Pump Rm), IPS - C East,
IPS-C Middle, and IPS Duct Bank
B", Rev 0000
0-AOI-30.2 C.62, Fire Safe Shutdown Room -
IPS-C East,
IPS-C Middle, Rev. 0
0-AOI-30.2 C.69, "Fire Safe Shutdown Room Control Building", Rev 0000 0-AOI-30.2 C.69, Fire Safe Shutdown Room - Control Building, Rev. 0 0-AOI-30.2, Appendix D, Fire Safe Shutdown - Long Term Actions, Rev. 0
0-FOR-228-1A, Quarterly Inspection and Testing of Emergency Light Battery Packs, Diesel Generator and Control Buildings Common and Train A Areas, Rev. 41
0-FOR-228-1B, Quarterly Inspection and Testing of Emergency Light Battery Packs, Diesel Generator and Control Buildings Common and Train B Areas, Rev. 33 0-FOR-228-2A, Quarterly Inspection and Testing of Emergency Light Battery Packs, Auxiliary Building Elevations 692 and 713, Rev. 52
0-FOR-228-2B, Quarterly Inspection and Testing of Emergency Light Battery Packs, Auxiliary Building Elevations 692, 729, and 737
0-FOR-228-3A, Quarterly Inspection and Testing of Emergency Light Battery Packs, Auxiliary Building Elevation above 737 A Train and Common Areas, Rev. 45 0-FOR-228-3B, Quarterly Inspection and Testing of Emergency Light Battery Packs, Auxiliary building Elevation above 737 B Train and Common Areas, Rev. 42
0-IMI-200, Periodic Calibration of Plant Instrumentation and Control Equipment, Rev 0
0-MI-56.007, Westinghouse Safety Related DS Circuit Breaker Overhaul Maintenance Inspection and Testing, Rev. 1 0-MI-57.002, Westinghouse DS Circuit Breaker Routine Maintenance, Inspection, and Testing, Rev. 7
0-MI-57.007, Non 1E DS Circuit Breaker Overhaul Maintenance, Inspection, and Testing, Rev. 2
0-MI-57.027, Initial Testing of Molded Case Circuit Breakers, Rev. 0
0-MI-57.250, 18 Month Periodic Testing of 1E Molded Case Circuit Breakers with 1E Loads, Rev. 0 0-SOI-13.01, Fire Detection System, Rev. 0
0-SOI-26.01, High Pressure Fire Protection System, Rev. 0
0-TI-12.19, Control of Time Critical Operator Actions, Rev. 1
0-TI-2018, Appendix R Demonstration of Operations Actions Required
0-TRI-0-1, 18 Month Periodic Testing of Molded Case Circuit Breakers Protecting 1E Busses from Non-1E Loads and Associated Circuits, Rev. 20
0-TRI-0-2, 18 Month Periodic Testing of 480V Circuit Breakers Protecting 1E Busses from Non-
1E Loads, Rev. 5
1-AOI-30.1, Plant Fires, Rev. 2
1-AOI-30.1, Plant Fires, Rev. 2 1-AOI-30.2 C13, Fire Safe Shutdown Room 772-A12, Rev. 1 1-AOI-30.2 C20, Fire Safe Shutdown Room 757-A2 or 757-A9, Rev. 2
1-AOI-30.2, App. E, Fire Safe Shutdown Energizing Credited Equipment and Instrumentation,
1-AOI-30.2, Appendix B Fire Safe Shutdown Elevation Diagrams, Rev. 0
1-AOI-30.2, Fire Safe Shutdown Elevation Diagrams, Rev. 0 1-AOI-30.2, Fire Safe Shutdown, Rev. 2 1-E-0, Reactor Trip or Safety Injection, Rev. 0
1-E-3, Steam Generator Tube Rupture, Rev. 0
1-ES-0.2, Natural Circulation Cooldown, Rev. 0 1-FOR-228-1, Refueling Replacement and Inspection and Testing of Emergency Light Battery Packs Reactor Building, Rev. 7
1-SI-0-8, Monitoring Component Cyclic or Transient Limits, Rev. 8
1-SOI-236.02, 125 VDC Vital Batter Board II, Rev. 29
2-ARI-88-94, Reactor Coolant System, Rev. 001U2
AOI-21.01, Loss of 125 VDC Vital Battery Bd I, Rev. 25
AOI-21.02, Loss of 125 VDC Vital Battery Bd II, Rev. 22
AOI-21.02, Loss of 125 VDC Vital Battery Bd II, Rev. 23
AOI-21.03, Loss of 125 VDC Vital Battery Bd III, Rev. 21
AOI-21.04, Loss of 125 VDC Vital Battery Bd IV, Rev. 20
AOI-35, Loss of Offsite Power, Rev. 39 Following a Fire, Rev. 0
FPDP-4, Fire Emergency Response, Rev. 3
FPDP-5, Development and Evaluation of Fire Drills, Rev. 5
FPI-0131, Smoke Removal, Rev. 3
FPT013.000, Fire Protection Training, Rev.1
GO-6, Unit Shutdown from Hot Standby To Cold Shutdown, Revision 0052
NC-PP-1, Watts Bar Nuclear Plant Unit2 Procedure Control, Rev. 8
NC-PP-32, Watts Bar Nuclear Plant Unit 2 Development and Issue of Operating and Technical Instructions, Rev. 05
NPG-SPP-03.9, NRC Inspection Preparation and Support, Rev. 01
NPG-SPP-10.3, Verification Program, Rev. 0
NPG-SPP-17.3, Fleet Fire Brigade Training
TPD-FBT, Rev. 2
NPG-SPP-18.4.5, Fire Protection Quality Assurance (Q07), Rev. 0
NPG-SPP-18.4.6, Control of Fire Protection Impairments, Rev. 5
NPG-SPP-18.4.7, Control of Transient Combustibles, Rev. 5
NPG-SPP-18.4.8, Control of Ignition Sources (Ho Work), Rev. 3
NPG-SPP-2.3, Operating Experience Program, Rev. 5
NPG-SPP-22.500, Operating Experience Program, Rev. 0
NPG-SPP-3.6, Fire Protection Program Change Regulatory Reviewers, Rev. 3
OPDP-1, Conduct of Operations, Rev. 24
OPDP-7 Fuse Control, Rev. 5
P1976-000-002, Post-Fire Safe Shutdown Cable Selection, Rev. 0 P1976-000-002, Post-Fire Safe Shutdown Cable Selection, Rev. 0
TI-12.04, User's Guide for Abnormal and Emergency Operating Instructions, Rev. 17
TI-12.06, Writer's Guide for Abnormal and Emergency Operating Instructions, Rev. 6
TI-211, Fire Protection, Rev. 6
TI-338, Unit 2 Area Turnover Supporting Operational Readiness, Rev. 11 TPD- ISFW, Ignition Source Fire Watch Training, Revision 0 WBN
TI-291, Combustible Control Zones and Sensitive Areas, Rev. 2
WBN-DCD-40-51, Fire Protection of Safe Shutdown Capability, Rev. 6
WG-1.0, Procedure Writer's Guide, Rev. 2
WG-1.1, Organization and Standard Procedure Modules, Rev. 0
WG-1.2, Procedure Outlines, Rev. 0
WG-1.2-004, Standard Structure for Single Column Abnormal Operating Instructions, Rev. 0
WG-1.2-005, Standard Structure for Safe Shutdown Instructions and Sub-Instructions, Rev. 0
Calculations, Evaluations, & Specifications
EDN00299920080005, Load Flow, Voltage Drop, Short Circuit, Cable Ampacity in Conduits &
Trays and Protection/Coordination for Unit 2 BOP Circuits, Rev. 35
EDN00299920080007, Unit 2 480V BOP Protection, Coordination and Thermal Overload Heater Sizing Calculation, Rev. 13
EDQ00099920090012, Unit 1 and 2 Appendix R Safe Shutdown Analysis, Rev. 2 EDQ00099920090012, Unit 1 and 2 Appendix R Safe Shutdown Analysis, Rev. 3 EDQ00099920090013, Appendix R - Unit 2 SSD Cables Required Following a Fire, Rev. 2
EDQ00099920090013, Appendix R - Unit 2 SSD Cables Required Following a Fire, Rev. 3
EDQ00099920090016, Appendix R - Units 1 & 2 Manual Action Requirements, Rev 2
EDQ00099920090016, Appendix R - Units 1 & 2 Manual Action Requirements, Rev. 3
EDQ00299920080004, Unit 2 480V 1E Protection, Coordination and Thermal Overload Heater Calculation, Rev. 25 EDQ00299920080016, Unit 2 6.9 KV Protection and Coordination Calculation, Rev. 9
EDQ00299920090013, Appendix R- Unit 2 Cables Required for Safe Shutdown Following A
Fire, Rev. 2
EDQ00299920090013, Appendix R- Unit 2 Cables Required for Safe Shutdown Following A Fire, Rev. 3 EDQ00299920090021, Appendix R - Fire Protection Suppression Effects Evaluation, Rev. 0
EPM-AST-031895, HPFP System Water Supply to the Auxiliary Building Preaction Sprinkler System, Rev.4
EPMDOM012990, Combustible Loading Data, Rev. 84
EPM-HAM-060192, Design Pressure and Flow for Control Building HPFP Preaction Sprinkler Systems, Rev. 1
EPM-HAM-081392, Hydraulic Analysis of the Intake Pumping Stating Sprinkler System, Rev. 2
EPM-RAC-032392, Evaluation of Suppression System Discharge, Rev.01
EPM-RJW-042992, Design Flow and Pressure for the Auxiliary Building HPFP Sprinkler Systems, Rev.3 EPMSMC110292, Backup Nitrogen Supply for Auxiliary Feedwater LCVs and Main Steam
G-73, Installation, Modification, and Maintenance of Fire Protection Systems And Features, Rev. 6
MDN-000-067-2008-0130, WBN Probabilistic Risk Assessment - Essential Raw Cooling Water
MDQ00299920110381, Appendix R - Operator Manual Action Evaluations, Rev. 0 N3-26-4002, High Pressure Fire Protection System, Rev. 13 PORVs, Rev. 8
R-1976-20-001, "Unit 2 Multiple Spurious Operation Evaluation", Rev. 3
R1976-20-01, Multiple Spurious Operation Evaluation, Rev. 3
System, Rev. 5
TIECS96, 10CFR50, Appendix R, Heating, Ventilating, and Air Conditioning Review, Rev. 17 UFSAR, Section 8.0, Electric Power, Rev. 18
Watts Bar Nuclear Plant (WBN) Unit 2, As-Constructed Fire Protection Report (FPR), Dated September 18, 2014
WB-DC-30-13, 10
CFR 50, Appendix R, Type I, II, and III Circuits - Unit 1 / Unit 2, Rev. 10
WB-DC-30-22, Electrical Raceways, Rev. 8
WB-DC-30-28, "Low and Medium Voltage Power Systems (Unit 1/ Unit 2)", Rev. 22
WB-DC-30-4, Separation/Isolation, Rev. 43
WB-DC-30-5, Power, Control, and Signal Cables For Use In Category 1 Structures - (Unit 1 /
WB-DC-40-62, Fire Protection, Rev. 5
WB-DC-40-62, Fire Protection, Rev. 5
WBNAPS2-065, Appendix R post-fire Coolant System Cooldown and Depressurization, Rev. 5
WBN-DCD-40-36, "The Classification of Piping, Pumps, Valves, and Vessels (Unit 1/ Unit 2)," Rev. 20
WBN-DCD-40-51, Fire Protection of Safe Shutdown Capability (Unit 1 / Unit 2), Rev. 6
WBN-DCD-40-51, Fire Protection of Safe Shutdown Capability (Unit 1 / Unit 2), Rev. 6 WBNEEBMSTI070018, 120V AC Protection, Coordination, and Short Circuit Study, Rev. 90 WBNEEBMSTI1070005, 125V DC Protection and Coordination Calculation, Rev. 72
WBN-IPE-002 U2, Unit 2 IPEEE Ignition Source Data Report, Rev. 0
WBN-IPE-003 U2, Determination of Fire Scenario Safe Shutdown Path Unavailability Watts Bar Nuclear Plant Unit 2, Rev. 0
WBN-IPE-004 U2, Unit 2 IPEEE Zone of Influence, Rev. 0
WBN-IPE-005 U2, Individual Plant Examination for External Events - Fires (IPEEE - Fires), Rev. 0
WBPEVAR8909010, Cable Ampacity Calculation Report, Rev. 85
WBPEVAR9004001, Appendix R - Cables Required For Safe Shutdown Following A Fire, Rev.
WBPEVAR9004001, Appendix R- Cables Required for Safe Shutdown Following a Fire, Rev. 44
WCG-1-1876, Architectural Doors, Doors, Fire Doors, 6/10/99 Work Orders and Completed Surveillance Records WO #113502197, RHR Heat Exchanger Outlet Flow, 2/11/2013
WO 08-810638-000, 0-FOR-304-3, Fire Damper (Internal) Visual Inspection-Auxiliary, Control and Diesel Generator Building, Rev. 14
WO 10-813607-000, 0-FOR-304-1, Fire Bar/Mech, Conduit, Cable Tray, Damper (EXT) Pent Visual Inspect - AB, CB-, DG, IPS, Rev.10
WO 112054707, 0-FOR-304-1, Fire Bar/Mech, Conduit, Cable Tray, Damper (EXT) Pent Visual Inspect - AB, CB-, DG, IPS, Rev.12
WO 112411930,CCM EDCR52882, System 030 Flexible Connections, 3/27/2012
WO 112461853,CCM EDCR52882,
PER 369701 System 030 Flexible Connections, 3/26/2012
WO 112859577, Type
DS 206 Breaker Overhaul Perform
MI-56.007, dated 3/22/14
WO 112941188, 480 V Breaker Inspection Perform
MI-57.002 7/21/12
WO 113215486, 0-FOR-304-3, Fire Damper (Internal) Visual Inspection-Auxiliary, Control and Diesel Generator Building, Rev. 16
WO 113447366, 0-FOR-26-2, 3 Year High Pressure Fire Protection Hydraulic Performance Verification, Rev 18
WO 113966171, Type
DS 206 Breaker Overhaul Perform
MI-57.007, dated 2/20/14
WO 114043972, 0-For-26-8-A, 18 Month Test of High Pressure Fire Protection Pump 2A-A, Rev. 13
WO 114082435,
WBN-0-FPs-777-EQUIP, Fire Equipment Located in Cages Inspect PPE, 4/22/2013
WO 114210514, 18 Month 10% MCCB Testing, dated 4/12/14
WO 114411690, 0-FOR-304-3, Fire Damper (Internal) Visual Inspection-Auxiliary, Control and Diesel Generator Building, Rev. 16
WO 114435382 &
WO 115122667, 0-FOR-13-613, 6 Month Fire Detection Test Panel L613, Rev. 8
WO 114435715, 0-FOR-26-3, 18 Month Inspection of HPFP Sprinkler Systems in Accessible Safety Related Areas, Rev. 06, 12/10/13
WO 114503545,
WBN-0-FPS-510-SCBA, Clean, Maintain, Inspect, Inventory and Storage Inspection of SCBAs, 9/20/2013
WO 114625188 &
WO 115123823, 0-FOR-13-606, 6 Month Fire Detection Test Panel L606, Rev. 6
WO 114625315, 0-FOR-13-637 18 Month Fire Detection and Suppression Test for Panel L637, Rev. 8
WO 114625610, 0-FOR-26-25, 18 Month Diesel Driven Pump Capability Test, Rev. 24
WO 114692887, 0-For-26-7-A, 18 Month Test of High Pressure Fire Protection Pump 1A-A, Rev. 12
WO 114693198 &
WO 115253580, 0-FOR-13-612, 6 Month Fire Detection Test Panel L612, Rev. 10
WO 114846181, 0-For-26-7-B, 18 Month Test of High Pressure Fire Protection Pump 1B-B, Rev. 10
WO 114846183, 0-For-26-8-B, 18 Month Test of High Pressure Fire Protection Pump 2B-B, Rev. 12
WO 114846281 &
WO 115540534, 0-FOR-13-618, 6 Month Fire Detection Test Panel L618, Rev. 8
WO 115015542,
WBN-0-FPS-777-EQUIP, Fire Protection Personal Protective Garment Inspection PMUG 0539W, 4/21/2014
WO 115123822 &
WO 114625186, 0-FOR-13-604, 6 Month Fire Detection Test Panel L604, Rev. 7
WO 115253474, 0-FOR-13-636 18 Month Fire Detection and Suppression Test for Panel L636, Rev. 10
WO 115435434, Installation of Thermolag for Conduit 0MC557A
WO 115438197, Installation of Thermolag for Conduit 2PLC5369A
WO 115540531, 0-FOR-304-1, Fire Bar/Mech, Conduit, Cable Tray, Damper (EXT) Pent Visual Inspect - AB, CB-, DG, IPS, Rev.13
WO 115575458,
WBN-0-FPS-510-SCBA, Clean, Maintain, Inspect, Inventory and Storage Inspection of SCBAs, 8/25/2014
WO 115586761, 18 Month Periodic Testing of 480V Circuit Breakers Protecting 1E Busses From Non-1E Loads, dated 7/21/14
WO 115590393, 0-FOR-410-1, 31 Day Fire Door Inspection, Rev 11
WO 115601742,
WBN-0-FPS-510-SCBA, Clean, Maintain, Inspect, Inventory and Storage Inspection of SCBAs, 8/29/2014

Drawings

0296-004, TVA Watts Bar Contract #84K71-834574, Rev. A 1-15E500-1, Key Diagram Station Aux Power System, R37
1-15E500-2, Key Diagram Station Aux Power System, R49
1-45B1769-2E, Wiring Diagrams 480V Reactor MOV Board 1B2-B Connection Diagram- Compt 2E, Rev. 10L 1-45W600-57-4, Wiring Diagram Separation & Miscellaneous Auxiliary Relays Schematic Diagrams, rev. 17
1-45W700-1, Key Diagram 12V & 125V DC Vital Plant Control Power System, Rev. 35
1-45W721-1A, Wiring Diagram 6900V Unit Bds 2A, & 2B Single Line
SH-1, R10 1-45W721-2A, Wiring Diagram 6900V Unit Bds 2C, & 2D Single Line
SH-2A, R9 1-45W724-1, Wiring Diagram 6900V Shutdown Board 2B-B Single Line, R28
1-45W724-3, Wiring Diagram 6900V Shutdown Board 2A-A Single Line, R26
1-45W724-4, Wiring Diagram 6900V Shutdown Board 2B-B Single Line, R24
1-45W749-2, Wiring Diagrams 480V Shutdown BD 1A2-A Single Line
1-45W760-1-2, Wiring Diagram Main Steam System Schematic Diagrams, Rev. 11 1-45W760-201-1, Wiring Diagram 6900V Unit Boards Transfer Schematic Diagrams, R15 1-45W760-201-2, Wiring Diagram 6900V Unit Board Schematic Diagram, R11
1-45W760-211-20, Wiring Diagram 6900V Shutdown Power Schematic Diagram, R7
1-45W760-211-3, Wiring Diagram 6900V Shutdown Power Schematic Diagram, R8
1-45W760-26-1, Wiring Diagram High Pressure Fire Protection System Schematic Diagrams, Rev. 27 1-45W760-62-6, Wiring Diagrams Chemical & Volume Control Systems Schematic Diagrams, Rev. 16
1-45W760-62-7, Wiring Diagrams Chemical & Volume Control System Schematic Diagrams, Rev. 15
1-47W200-3, Equipment Plan El 757.0 & 755.0, Rev. 16 1-47W200-6, Equipment Plan El 692.0 & 685.5, Rev. 12 1-47W32-1, Flow Diagram Raw Service Water & Fire Protection System, Rev. 40
1-47W610-62-3, Electrical Control Diagram Chemical & Volume Control System, Rev. 30
1-47W611-62-4, Electrical Logic Diagram Chemical & Volume Control System, Rev. 14
1-47W809-2, Flow Diagram Chemical & Volume Control System, Rev. 25 1-47W832-2 Flow Diagram Raw Service Water & Fire Protection System, Rev. 36 1-47W832-3 Flow Diagram Raw Service Water & Fire Protection System, Rev. 14
1-47W850-2, Flow Diagram Fire Protection Raw Service Water, Rev. 37 1-47W850-5, Flow Diagram Fire Protection, Rev. 27
1-47W866-3, Flow Diagram Heating Ventilation & Air Cond Air Flow, Rev. 39 1-47W866-4 Flow Diagram Heating Ventilating and Air Conditioning Air Flow, Rev. 43 1-75W503, Wiring Diagram Main Single Line 161kV Transformers, R8
2-45B2766-8B, Wiring Diagrams 480V Reactor MOV Board 2A1-A Connection Drawing- Compt
8B, Rev. 10
2-45B2768-8A, Wiring Diagrams 480V Reactor MOV Board 2B1-B Connection Diagram-Compt
8A, Rev. 10 2-45B2769-2E, Wiring Diagrams 480V Reactor MOV Board 2B2 Connection Diagram-Compt 2E, Rev. 7
2-45B2769-2E, Wiring Diagrams 480V Reactor MOV Board 2B2-B Connection Diagram- Compt
2e, Rev. 0
2-45N2638-8, Wiring Diagrams Auxiliary Control Board Panel 2-L-IIA Connection Diagram Sheet 8, Rev. 15 2-45N2638-8, Wiring Diagrams Auxiliary Control Board-Panel 2-L-IIA Connection Diagram Sheet 8, Rev. 15
2-45N2639-8, Wiring Diagrams Auxiliary Control Board-Panel 2-L-IIB Connection Diagram Sheet 8, Rev. 13 2-45W2766-2, Wiring Diagrams 480V reactor MOV Board 2AI-A Connection Diagram, Rev. 20 2-45W2768-3, Wiring Diagrams 480V Reactor MOV Board 2B1-B Connection Diagram, Rev. 20
2-45W2768-6, Wiring Diagrams 480V Reactor MOV Board 2B1-B Connection Diagram, Rev. 10
2-45W2769-4, Wiring Diagrams 480V Reactor MOV Board 2B2-B Connection Diagram, Rev. 21
2-45W2769-5, Wiring Diagrams 480V Reactor MOV Board 2B2-B, Rev. 8
2-45W600, Wiring Diagram Reactor Coolant System Schematic Diagrams, Rev. 12 2-45W760-1-2, Wiring Diagram Main Steam System Schematic Diagram, Rev. 5 2-45W760-1-2, Wiring Diagram Main Steam System Schematic Diagrams, Rev. 5 2-45W760-1-2, Wiring Diagrams Main Steam System Schematic Diagrams, Rev. 5
2-45W760-62-1, Wiring Diagrams Chemical & Volume Control System Schematic Diagram, Rev. 8 2-45W760-62-6, Wiring Diagrams Chemical &Volume Control System Schematic Diagrams, Rev. 6
2-47W240-4, Fire Protection Compartmentation - Fire Cell Plan El. 755.0 & 757.0, Rev. 2
2-47W240-4, Fire Protection Compartmentation- Fire Cell Plan Elevation 755.0 & 757.0, Rev. 2
2-47W240-4, Fire Protection Compartmentation-Fire Cell Plan El 755.0 & 757.0, Rev. 2
2-47W240-9, Fire Protection Compartmentation-Fire Cells Plan El 726.0 & 728.0, Rev. 3 2-47W803-2, Flow Diagram Auxiliary Feedwater System, Rev. 18 2-47W809-1, Flow Diagram Chemical & Volume Control System, Rev. 33
2-47W810-1, Flow Diagram Residual Heat Removal System, Rev. 21
2-47W811-1, Flow Diagram Safety Injection System, Rev. 36
2-47W812-1, Flow Diagram Containment Spray System, Rev. 25 2-47W813-1, Flow Diagram Reactor Coolant System, Rev. 29 2-47W813-1-FAC-SNM, Flow Diagram Feedwater System, Rev. 0
2-47W850-1, Flow Diagram Fire Protection & Raw Service Water, Rev. 3
2-47W859-1, Flow Diagram Component Coolant System, Rev. 17
31N220-1, Concrete General Outline Features Sheet 1, Rev. 3
35W800-5, Intake Pumping Station Units 1 & 2 Conduit &Grounding Details, Rev. 22 35W800-6, Intake Pumping Station Units 1 & 2 Conduit &Grounding Details, Rev. 19 35W800-8, Units 1 & 2 Conduit &Grounding Details Fire Detection, Rev. 07
37-W206-13, Mechanical Intake Pumping Station Piping & Equipment, Rev. 9
37W206-13, Mechanical Intake Pumping Station Piping and Equipment Sprinklers, Rev. 9
37W206-13, Mechanical Intake Pumping Station Piping and Equipment Sprinklers, Rev. 9 37W900-1, Mechanical Heating and Ventilating, Rev. 3 41N321-1, Concrete
EL 757.0 Floor Outline, Rev. 5
41N321-2, Concrete
EL 757.0 Floor Outline, Rev. 7 45A883-17, Fire Rated Penetration Typical Detail N4-1, Rev. 4
45A883-39, Fire Rated Penetration Typical Detail M4, Rev. 4 45B2767-2E, Wiring Diagram- 480V Reactor MOV BD 2A2-A Connection Diagram- Compt 2E, Rev. 7
45N1642-1, Unit 1 Wiring Diagrams Unit Control Board Panel 1-M-3 Connection Diagrams Sheet, Rev. 22
45N2639-3, Wiring Diagrams Auxiliary Control Board Panel 2-L-IIB Connection Diagram Sheet 3, Rev 2. 45N2644-6, Wiring Diagrams Unit Control Boards Panel 2-M-5 Connection Diagram Sheet 6 45N280-1, Electrical Equipment Trans Room Layout -
EL 772.0Plan & Section, Rev. 7
45N706-4, Wiring Diagram 120 V AC Vital Instrument Power Boards 1-IV & 2-IV Connection Diagram Sheet 4, Rev. 18
45N708-7, Wiring Diagram 120V AC TSC Power Board 1 Connection Diagram, Rev. Z 45W2724-1, Wiring Diagrams 6900 Shutdown Board 2A-A & 2B-B Connection Diagram, Rev. 4 45W2766-2, Wiring Diagram 480V Reactor MOV Board 2AI-A Connection Diagram, Rev. 20
45W2767-2, Wiring Diagram- 480V Reactor MOV Board 2A2-A Connection Diagram, Rev 18
45W2767-5, Wiring Diagrams- 480 V Reactor MOV Board 2A2-A Connection Diagram, Rev. 12
45W703-8, Wiring Diagrams 125V Vital Battery Board IV Panel 4 Connection Diagram Sheet 5, Rev. 20 45W703-8, Wiring Diagrams 125V Vital battery Board IV Panel 4 Connection Diagram Sheet 8, Rev. 20
45W810-6, Conduit & Grounding
EL 692.0, COLS C1-C7, N-Q Details- Fire Protection, Rev. 8
45W810-7, Conduit & Grounding
EL 692.0, COLS C7-C13, N-Q Details-Fire Protection, Rev. 9
45W828-25, Conduit & Grounding
EL 757.0 Fire Protection, Rev. 5 45W830-9, Conduit & Grounding
EL 772.0 Fire Protection, Rev. 2 47W200-3, Equipment Plan- Elevation 757.0 & 755.0, Rev. 16
47W200-6, Equipment Plan- Elevation 692.0 & 685.5, Rev. 12
47W491-83, Mechanical Fire Protection, Rev. 1
47-W491-87, Mechanical Fire Protection High Pressure Fire Protection, Rev. 1 47W600-245, Electrical Instruments and Controls, Rev. 5 47-W600-246, Electrical Instruments and Controls, Rev. 9
47-W600-253, Electrical Instruments & Controls, Rev. 5
47W920-8, Mechanical Heating, Ventilating and Air Conditioning, Rev. 41
47W920-9, Mechanical Heating, Ventilating and Air Conditioning, Rev. 29
47W930-1, Mechanical Heating, Ventilating & Air Conditioning, Rev. 60 75K52-86100-1, Door Schedule, sheets 1 to 3, 1/19/75 75K52-86100-1, Door Schedule, sheets 1 to 3, 1/19/75
E-3620E, Wiring Diagram Panel 2 Termination Board 6900V Shutdown Board 2BB Logic Relay Panel Sheet 6 Sheet 6, Rev 911
GE-0126D4499, Metal Clad Switchgear Interconnection Diagram Sheet 6, Rev. 915 ICC0483032, Fire Test for Penetration Detail M4, Rev. 1 ICC0985011, Fire Test for Penetration Detail M4, Rev. 1
ICC1088024, Fire Test for Penetration Detail N4-1, Rev. 1
ICS0879002, Fire Test for Penetration Detail N4-1, Rev. 1
WBN Plant Electrical Distribution System, 480V - 500KV, Rev. 0 Plant Modifications and Engineering Changes
DCN 35983-A, Install a Fire Damper & Replace a Fire Damper, Dated 10/25/95
DCN 53413, Physical Work in the component cooling system, Rev. A
DCN 54871, Install/modify Emergency Lighting Required for Two Unit Operation to Comply with 10CFR50 Appendix R Requirements, Rev. A
DCN 55050 - MEQ Change Supplement, Refurbishment of Several Air Operated Flow Control Valves in the Incore Instrument Room A/C, Rev. 0
DCN 55523, Install Fire Rated Protective Wrap on Electrical Raceway as Required by Unit 2 Appendix R Analysis, Rev. A
DCN 64512, Bellow Expansion Joint Replacement, Rev. A
DCN-60384-A, Changes to Radio Power Supplies, Rev. A ECN, Modify Smoke Actuated Fire Dampers per Nonconforming Condition Reports, W-210-P, W-220-P, and WBNMEB8510, Dated 03/05/85
EDCR 52849, Work Scope 3 (System 31) - Install Two Fusible Links for Certain Fire Dampers to Meet Single Failure Criteria, Rev. A
EDCR 53293, Replace safety Related, Class 1E MCC Buckets, Feeders Breakers, and Internal Wiring in the Existing Compartments of the Safety Related 480V REAC MOV BD 2B2-B, Rev. A EDCR 54924, Work Scope 38, (System 30)-Install Fire Rated Fabric Over Expansion Joints
DCN 58383, EDG Emergency Stop, Rev. B
Fire Fighting Preplan Strategies
AUX-0-757-02, Auxiliary Building Elevation 757, Rev. 3
AUX-0-772-02, Auxiliary Building Elevations 772 and 782, Rev. 2
CON-0-692-01, Control Building Elevation 692, Rev. 1
IPS-0-711-01, Intake Pumping Station Elevations 711.0 and 722.0, Rev. 2
WBN Pre-fire Plan, Con-0-692-02, Rev. 2
Applicable Codes & Standards
ASTM D-4057-95, Standard Practice for Manual Sampling of Petroleum and Petroleum Products
NFPA 13, Automatic Sprinkler Systems, 1975
NFPA 14, Standpipe and Hose Systems, 1974 NFPA 20, Centrifugal Fire Pumps, 1973 NFPA 24, Outside Protection, 1973
NFPA 72D, Proprietary Protective Signaling Systems, 1975
NFPA 72E, Automatic Fire Detectors, 1974
NFPA 80, Fire Doors and Windows, 1975
Technical Manuals and Vendor Information Ruskin Manufacturing Company Contract 84K71-834574 Fusible Links Letter of Certification, dated July 27, 1983
Viking, Technical Data, 4" Deluge Valve Model D-5 Trim Chart, December 1974
Viking, Design Data, Single Interlocked Preaction. July 6, 1989 Viking, Technical Data, Pressure Operated Relief Valve (PORV), January 25, 1989 Dow Corning 561 Silicone Transformer Liquid, Technical Manual Audits & Self-Assessments
WBN-OPS-F-13-001, Watts Bar Nuclear Fire Protection Program and 10CFR50 Appendix R, Entire Program Self-Assessment, Dated March 31, 2013
QA-CH-13-002, Fire Protection Non-Audit Year Performance, Dated 01/17/14
License Basis Documents
TVA-NQA-PLN89-A, Nuclear Quality Assurance Plan, Rev. 30 Watts Bar Nuclear Plant Unit 1/Unit 2 As-Constructed Fire Protection Report, dated September 18, 2014 Watts Bar Nuclear Plant Unit 2 FSAR

Other Documents

00076090, TVA NPG Fire Drill Evaluation Report,
EL 757 Unit 2, 10/30/2014
00082402, TVA NPG Fire Drill Evaluation Report, Turbine Building
EL 729 Unit 1 EHC pump, 6/11/2013
0-AOI-30.2 C1 App. R QA Package Rev. 4 3-OT-AOI-18, Malfunction of Pressurizer Pressure Control System, Rev. 9
3-OT-AOI-20, Malfunction of Pressurizer Level Control, Rev. 11 3-OT-AOI-30.1, Plant Fires/Fire Safe Shutdown 3-OT-AOI-38, Main Steam or Feedwater Line Break, Rev. 12
3-OT-AOI3000, Plant Fires, Rev. 12
3-OT-JPMA011, Bypassing of 1-FCV-62-89, Charging Flow Control Valve, For The Purpose of
3-OT-JPMA015A, Local Operation of Turbine Driven AFW Pump Per
SOI-3.02, Rev. 5
3-OT-JPMA047C, Operate S/G #1 and #2 TD AFW LCVs (Loc. With N2) Per
SOI-3.02, Rev. 33-OT-MSC-142, Distributed Controls System (DCS) Process Controls Modification Package
3-OT-MSC146G, Unit 2 Electrical and Fire Protection Differences, Rev. 0
3-OT-SYS032A, Control Air System, Rev 10
3-OT-SYS068E, Reactor Vessel Head Vent System, Rev. 8
3-OT-SYS-082I, Diesel Generator Electrical, Rev. 9 3-OT-SYS201B, Blackout and Load Shed Logic Relays, Rev. 10 3-OT-SYS203A, 480V Boards, Rev 9
3-OT-SYS203A, Plant 480V AC Systems, Rev. 9
3-OT-SYS235A, 120V AC Distribution, Rev. 15
90NNB-75723A, Watts Bar Nuclear Plant Units 11 and 2 Fire Dampers for Auxiliary Building, Vital Battery Board Rooms, and Backdraft Damper for Control Building Auxiliary Instrument Room, Dated 08/30/90
Contract No. 5031, Amendment 1, Contract for Fire Protection Services at Watts Bar Nuclear Plant, Dated March 12, 2014.
Engineering Procedure No. E-511, Installation Instructions - NIBD23 Curtain Type Fire Damper/Door, Rev. 0 Engineering Procedure No/ E-512, Operation and Maintenance of NIBD23 Curtain Type Fire Damper/Doors, Rev. 0
IEEE Standard 279-1971, Criteria for Protection systems for Nuclear Power Generating Stations Local Control Per
SOI-62.01, Rev. 6
LOR 3-OT-MSC-142 R 42 Attachment 5, DCNs 56905 and 52853, Distributed Control System Process Controls N3-1-4002, Main Steam System, Rev. 16
N3-74-4001, Residual Heat Removal System, Rev. 14
NCO080008046, IP&S 199 -
GL 1989-19 Overview, Rev. 42
PO0637768-7-14-23, Acceptance lab test report for Thermo-Lag-330-1, Batch F13-12005,Rev.0
PO585153, Acceptance lab test report for Thermo-Lag-330-1, Batch F13-06003, Rev. 0 PO606798ITEM17, Acceptance lab test report for Thermo-Lag-330-1, Batch F13-10004, Rev. 1 PO637768ITEM1, Acceptance lab test report for Thermo-Lag-330-1, Batch F13-12002, Rev. 0
SQEEI-99001, Sequoyah Electrical Engineering Instruction, dated 4/2/99
TVA Fire Brigade leader's Incident Report, Unit 2 South Valve Room
EL 729, 10/21/2014
USNRC, Generic Letter 90-06, Resolution of Generic Issue 70 and Generic Issue 94 WB2CCP Engineering Desktop Procedure for Disposition of Failed LittleFuse Flas-5 Fuses, dated 11/25/13
WB2CCP PreOp Startup Desktop Instruction for Disposition of Failed LittleFuse Flas-5 Fuses
Memorandum of Understanding-MOU-031, dated 11/23/13
WBNP-QCP-4.27, Damper Inspection, Damper 2-ISD-31-3855
WBN-SDD-N3-15-4002, Steam Generator Blowdown System, Rev. 16
WBN-SDD-N3-3B-4002, Auxiliary Feedwater System, Rev. 17
WBN-SDD-N3-63-4001, Safety Injection System, Rev. 27
WBN-SDD-N3-67-4002, Essential Raw Cooling Water System, Rev. 26
WBN-SDD-N3-68-4001, Reactor Coolant System, Rev. 31
WBN-SDD-N3-82-4002, Standby Diesel Generator System, Rev. 17Westinghouse Letter,
LTR-TA-14-31, Appendix R CVCS Malfunction Studies for WBN Units 1 & 2, dated 06/03/2014
Westinghouse Letter, TVA WBN Unit 1, Loss of Offsite Power / Loss of Normal Feedwater Analysis, dated 11/30/2001
White Paper -
IPS 199, Fire Safe Shutdown Analysis of Steam Generator Overfill
List of Corrective Action Documents Reviewed During Inspection
PERs
110690,
867408,
744636,
730980,
726637,
948615,
824165,
857207
List of Service Requests and Problem Evaluation Reports Generated as a Result of this Inspection
PERs
824165,
950465,
945241,
952778,
954082,
954084,
955650,
959691,
960445,
959183,
960916,
960956,
962419,
966270,
967466,
966670,
967896,
967401,
969421,
969430,
969432,
969435,
969442,
970586,
972066,
972060,
972134, 970587

LIST OF ACRONYMS

ACR Auxiliary Control Room

ADAMS Agencywide Documents Access and Management System AOI Abnormal Operating Instruction

AUO Auxiliary Unit Operator

AV Analysis Volume
CDR Construction Deficiency Report
ERCW Emergency Raw Cooling Water
ERF [[]]

BS Electrical Raceway Fire Barrier System

FA Fire Area

FHA Fire Hazard Analysis
FPP Fire Protection Program
FPR Fire Protection Report
IP Inspection Procedure (

NRC)

JPM Job Performance Measure

LCV Level Control Valve
MCR Main Control Room

NFPA National Fire Protection Association OMA Operator Manual Action

OR Operating Requirement
PO [[]]

RV Power Operated Relief Valve

RCP Reactor Coolant Pump
RCS Reactor Coolant System S/G Steam Generator

SSD Safe Shutdown

TIR Testing and Inspections Requirements

TVA Tennessee Valley Authority

U2 Unit

2 WBN Watts Bar Nuclear Plant