IR 05000388/1985013
| ML17156A317 | |
| Person / Time | |
|---|---|
| Site: | Susquehanna |
| Issue date: | 05/28/1985 |
| From: | Bettenhausen L, Florek D NRC OFFICE OF INSPECTION & ENFORCEMENT (IE REGION I) |
| To: | |
| Shared Package | |
| ML17156A316 | List: |
| References | |
| 50-388-85-13, NUDOCS 8506070568 | |
| Download: ML17156A317 (11) | |
Text
U.S.
NUCLEAR REGULATORY COMMISSION
REGION I
~ Report No.
50-388/85-13 Docket No.
50-388 License No.
NPF-22 Priority Category C<
Licensee:
Penns lvania Power and Li ht Com an 2 North Ninth Street Allentown Penns lvania 18101 Facility Name:
Sus uehanna Steam Electric Station Unit 2 Inspection At:
Salem Townshi Penns lvania Inspection Conduct
A ril 23-26 1985 Inspectors:
D. Florek, Lead Reactor Engineer gP II Da e
Approved by.
L.
ettenhausen, C ief, Operations Branch, DRS Dat Ins ection Summar
Ins ection on A ril 23-26 50-388/85-13 1985 Re ort Number Areas Ins ected:
Routine unannounced inspection of licensee action on previous inspection findings resulting from the July 26, 1984 loss of AC power event, QA/QC interfaces and tours of the facility.
The ipspection involved 29 hours3.356481e-4 days <br />0.00806 hours <br />4.794974e-5 weeks <br />1.10345e-5 months <br /> onsite by one region based inspector.
Results:
No violations were identified.
aSOE070SiS eSOSS0 PDR ADOCK 05000388
PDR ~~
II
DETAILS 1.0 Persons Contacted Penns lvania Power and Li ht Com an G. Butler, Instrument and Control Supervisor J. Everett, Power Production Engineer
- J.
Graham, Senior Compliance Engineer H. Keiser, Plant Superintendent G. Kuczenski, Maintenance Planning and Schedule Supervisor R. Paley, Compliance Engineer R. Peale, Nuclear Operations Training Supervisor
R. Prego, Operations guality Assurance Supervisor D. Thompson, Assistant Plant Superintendent 2.0 U.S. Nuclear Re ulator Commission R. Jacobs, Senior Resident Inspector
L. Plisco, Resident Inspector The inspector also contacted several other licensee personnel in the course of the inspection including shift supervisors, reactor operators and members of the technical staff.
- Denotes those present at the exit meeting held on April 26, 1985.
Licensee action on revious ins ection findin s Closed Violation 388/84-34-01 Previous corrective actions werenot effective in preventing an operator from opening the incorrect knife switch on July 26, 1984.
The inspector reviewed the licensee response in PLA-2389 dated January 17, 1985.
The inspector verified the licensee corrective actions in the manner indicated below.
The inspector verified by review of WA-S42335 and WA-S42215 and inspection of selected 13.8 KV and 4160 V
ESS breaker cubicles that new labels have been installed on the breaker and bus DC control power switches.
Warning signs were installed on knife switches which disable the ESS bus and associated generator as an immedi-ate response to the event as described in inspection report 50-388/84-34 and were observed as still installed in this inspection.
The inspector's review of training records, lesson plan SY017 M-7 dated August 29, 1984 and interview with the training supervisor verified that training wa's pro-vided to the operators in breaker rackout procedures.
Operating Instruc-tion OI-AD-036, "Racking Breakers",
dated April 25, 1985 was reviewed.
The revised labeling for knife switches was included in this instructio Non routine training corrective actions were verified by review of OI-TR-004 "Non-Routine Training", revision 1 dated October 3, 1984,'eview of the shift non-routine training books for non-routine training irj process, and review of completed non-routine training.
By review of the shift non-routine training books, the inspector noted that training that was[required prior to assuming shift duties had been provided.
There was, however, an example of training that was required to be provided during the shift cycle that had not yet been provided to an individual of "B" shift in Mar'ch 1984 even though he participated in other shift training in April 1984.
I, This was brought to the licensee attention.
In addition, the inspector noted that the day shift operating crew on April 26, 1985 had outstandingl signa-tures in the training records of non-routine training to be provide'd during their current shift cycle.
During the inspection, the outstanding signa-tures were obtained prior to the completion of the shift cycle.
The in-spector identified these items and expressed concern at the exit meeting on the implementation of operating instruction OI-TR-004.
The licensee acknowledged the inspector's concern.
Training for event evaluators was provided by a three day course on event analysis by EGKG and a one week course provided by INPO on the Human Performance Evaluation System on sel,ected compliance group event evaluators.
Addit'ional training isI,planned.
The implementation of the Human Performance Evaluation System (HPES)
has been verified based on the review of AD-gA-121 "Human Performance Evalua-tion System",
Revision 0, dated March 5, 1985 and the review of "trial use" HPES Report 84-001.
Feedback on the report was provided by INPO on~~January 17, 1985 and February 6,
1985.
Based on the above review, the inspector verified the licensee's corrective actions and had no further questions.
This item is closed.
Closed Violation 388/84-34-02 Training was inadequate in the breaker rackout, emergency diesel generator reset of alarms, breaker light i,'ndi-cations and restoration of suppression pool monitoring instrumentation.
The inspector reviewed the licensee response to the violation in PLA-2389 dated January 17, 1985.
The corrective actions were reviewed and verified to be satisfactory in the following manner.
The training of operators prior to restart was reviewed in inspection report SO-388/84-34.
Proce-
.
dures issued to assure proper breaker rackout operation included OI-AD-36 as discussed in the response to violation 388/84-34-01.
This procedure also discussed breaker light indication.
ON-024-001,
"Diesel Generator Trip", Revision 0, dated July 30, 1984 discussed reset of diesel gen'erator trips and ON-117 and ON-217 discussed SPOTMOS restoration as described in inspection report SO-388/85-10.
The operator training tracking system is discussed in the response to violation 388/84-34-01.
Based on interviews with the Nuclear Operator Training Supervisors non-licensed operators were interviewed by training simulator instructors for deficiencies in the training program and these deficiencies were factored into the training program.
Specific deficiencies included electrical line up and breaker
operation.
These items are being included in retraining.
A job analysis of non-licensed operators and auxiliary system operators, dated July 26, 1984, was reviewed.
Deficiencies were identified and catego-rized.
Four training modules of "operating practices" were developed.
The inspector reviewed three training modules on 1)
Preventing Opera-tional Problems, 2)
Gathering and Giving Information, and 3)
Cari'ng for Equipment.
Based on the inspector's review of licensee completed a'nd in-process activities, the inspector had no further questions'his item is closed.
Closed Unresolved item 388/84-34-05 Replace labels for knife switches and fuses as required, establish fuse control policy, revise appropriate procedures.
Work authorizations (WA)
S42335, S42203, S41194 and S42215 revised labels for 13.8KV, 4160V and 480V, equipment.
OI-AD-037 "Fuse Control", Revision 0, dated August 27, 1984 was reviewed to verify estab-lishment of a fuse control policy.
OP-203-001 "Electrical Plant Lineup",
Revision 4, dated January 22, 1985 and OP-205-001
"480V AC System",
Re-vision 3, dated February 5, 1985 were observed to have consistent termi-nology with respect to labels.
The inspector also noted the licensee does have a program in place to assure consistency of procedures and labels as each procedure is required to be revised.
The inspector's review of OP-264-001, Revision 4, revealed references to the old label description.
The licensee's representative indicated that the procedure was an individual system/component procedure which has not been revised to 're-flect the new labels.
This procedure is being revised for label consis-tency as part of the in process labeling/procedure consistency progr'am.
The inspector had no further questions at this time.
This item is closed.
~/- -8 E
detect loss of control and trip DC power.
The inspector noted that 'the licensee has a program to assure consistency of labels and procedures as each procedure is required to be revised.
OI-AD-036 contains breaker rackout procedures.
PLA-2419, dated March 7, 1985, describes modifications to be installed on both Unit 1 and 2 to provide control room indication of availability of 4160 DC switchgear.
Pending installation of the
,
modifications, this item will remain open.
Closed Unresolved.Item 388/84-34-11 Conduct operator training.
, The inspector reviewed licensee scram recovery action item file 2-84-04-17.
The review of the training records and lesson plan S-Y017 M-7 dated August 29, 1984, indicated that training was provided to operating shift personnel.
This item is closed.
Closed Unresolved Item 388/84-34-12 Evaluate adequacy of written tag out direction.
The inspector reviewed licensee scram recovery action item file 2-84-04-19.
The inspector reviewed PCAF 1-84-1198, PCAF 1-84-1199 and PCAF 1-84-1200 to procedures AD-QA-302, AD-QA-306 and AD-QA-307.
No unacceptable conditions were noted.
This item is close Closed Unresolved Item 388/84-34-13 Evaluate the necessity of diesel enerator emer enc start ca abilit from the control room other than th g
g Y
p Y
e methods currently available.
The inspector reviewed licensee scram re-covery action item file 2-84-04-20.
The inspector reviewed PLI-36852 dated November 29, 1984, which concluded that no change is required con-sidering:
(1)
the unusual plant lineup caused by the conduct of the loss of offsite power test, (2)
the safety analysis describing the time periods available prior to the need to restore AC power during a plant blackout, (3)
the availability of signals which cause diesel generator automatic operation, (4)
and the other methods available to improve diesel generator availability.
Availability improvement methods include installation of new generator overvoltage relays, currently planned for July 1985, and installation of the air dryers for the fuel rack air~ supply which have been completed.
The licensee is monitoring diesel generator performance for availability improvement.
Based on the above, the [in-spector had no further questions.
This item is closed.
0 en Unresolved Item 388/85-34-14 Evaluate diesel generator
"A" frequency oscillations.
The inspector reviewed the licensee scram re-covery file for action, item 2-84-04-21.
The licensee had completed) the assessment of past diesel generator performance regarding frequency) oscil-lation.
The licensee's corporate office recommended additional testing of diesel generators in PLI-37643 dated January 14, 198S.
The site staff is currently evaluating the recommendations in PLI-37643.
Pending final disposition of the testing recommendations, this item will remain open.
Closed Unresolved Item 388/85-34-1S Assure non-routine training is conducted.
The inspector reviewed the licensee's scram recovery action item file 2-84-04-22.
OI-AD-036 describes methods to assure proper)
rackout of breakers; OI-TR-004 describes methods for assuring non-routine training is conducted.
See additional discussion in item 388/84-34-~01.
This item is closed.
Closed Unresolved Item 388/84-34-19 Evaluate power transfer swi',tches
~
The inspector reviewed the licensee's scram action item file 2-84-04-29.
PLI-37719 dated January 17, 1985, listed all power transfer switches, and PCAF-1-84-1148, 1149, 1150, 1151 incorporated the switches into appr'opri-ate procedures is as described in item (388/84-34-OS).
The inspector had no further questions.
This item is closed.
0 en Unresolved Item 388/84-34-20 Evaluate loss of AC instrument indication.
The inspector reviewed the licensee's scram recovery action item file 2-84-04-30.
The inspector reviewed PLI-35438 dated Sep-tember 13, 1984, PLI-36S61 dated November 13, 1984 and PLA-2419 dated Harch 1985.
Based on the above documents, the licensee plans to evaluate control room instrument availability to be completed by the third quarter of 1985.
Pending completion of the evaluation and implementation of[the recommendations, this item will remain open.
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Closed Unresolved Item 388/84-34-21 Develop an independent verifi-cation policy.
The inspector reviewed the station policy 6-84 on ["Control and Verification of Operating Sections".
See additional discussion on item (388/84-34-30).
This item is closed.
Closed Unresolved Item 388/84-34-22 Review of standard electrical operating practices.
The inspector reviewed the licensee s scram recovery I
action item file 2-84-04-32.
A poll of operators on station practices was completed on November 26, 1984.
During the polling process, the following station policies were issued.
These policies were reviewed by the inspector.
2-84
"Need for Procedures" dated October 9, 1984 3-84
"Need for Special Briefing" dated October 9, 1984 4-84
"Operation of Electrical Isolation Devices for Protective Permit and Tag Blocking" dated October 9, 1984 5-84
"Operation of Electric Isolation Devices" dated October 9, 1984 6-84
"Control and Verification of Operating Actions" dated October 9, 1984 Based on review of the above documents, the inspector had no further question.
This item is closed.
(Open) Unresolved Item (388/84-34-23)
Review of Labeling blackout instru-mentation.
The inspector reviewed the licensee's scram recovery action item file 2-84-04-33.
The inspector reviewed WA-V48336, T46273, T46274, T46275 and T46163 which labeled the instruments, provided with DC power, with purple labels and verified label color changes in the control room.
The inspector's review of EO-200-030 revealed that the RCIC turbine speed was listed as a
DC supplied instrument.
The label, however, had not been changed to purple.
Further investigation by the licensee indicated Ithat it should be a purple label.
Pending revision of the RCIC Turbine Speed label from black to purple and inclusion of RCIC turbine speed instrument number and range in EO-200-030.
This item will remain open.
Closed Unresolved Item 388/84-34-26 Review RHR and core spray circuit breaker response for various combination of motive and control power availability.
The inspector reviewed the licensee'
scram recovery action item file 2-84-04-36.
The licensee evaluated the breaker response and concluded that breakers would not close on loss of DC control power due to no power to the 44 AX relay.
This is comparable to results de-scribed in inspection report 50-388/84-34.
Training on this item was provided to the operators in lesson plan SY017 M-7 dated August 29, 1984.
This item is close.0 Closed Violation 388/84-34-30 Independent verification activities did not prevent the wrong knife switch from being operated on July 26, 1984.
The inspector reviewed licensee response to the violation in PLA-2389 dated January 17, 1985.
The inspector reviewed Policy "Letter 6-84, Revision 0, dated October 9, 1984; Revision 1, dated January'~18, 1985; and d~aft Revision 2, dated April 25, 1985.
The revi sions reflect feedback experience from the work groups in the implementation of the station policy.
Verification activities are required for defined a'ctiv-ities with three types of verification established:
verification, ~inde-pendent verification and system test verification.
The inspector verified that Operations, Maintenance and Instrumentation and Control work groups have translated the station policies into procedures.
The inspector re-viewed the following documents and interviewed individuals from each group and verified the station policies have been translated into procedu'res:
AD-QA-300 "Conduct of Ope} ations",
Revision 5, dated February 22, 1985; OP-250-001
"RCIC System",
Revision 4, draft copy; AD-QA-500 "Conduct of Maintenance",
Revision 5, dated January 28, 1985; AD-QA-502 "Work Authorization System",
Revision 6, dated January 14, 1985; MI-PS-001 "
"Maintenance Work Planners Guide", Revision 8, dated November 16, 1984; WA-V41455 planning verification included; WA-S51030 completed verification activity; Instrument and Control Instruction IC-IS-01 "Control and Veri-fication of Operating Actions";
IBC correlation of new station policy on verification to IKC procedures not yet revised which is attached to~tall unchanged procedures; SI-161-301 draft copy of change to reflect new policy.
Based on review of the documents above and interviews, thei,sta-tion policy is being translated into procedures.
Feedback in the imple-mentation of the policy has resulted in revisions to the policy.
This is principally in feedback from 18C personnel in the verification of removal of equipment from service.
Independent verification is required when activities affect equipment from more than one division.
Independent verification requires the verifier not to accompany the individual per-forming the activity but must conduct his verification at a time after the activity is completed.
Based on the above, the inspector had no fur~'ther questions.
This item is closed.
tLI/
The inspector reviewed Quality Assurance Surveillance Reports QASR-850-033 dated April 17, 1985,84-087 dated August 16, 1984 and 84-098 dated (,
August 30, 1984 reflecting surveil lances conducted on the implementation of the action items from the July 26, 1984 loss of AC power event.
QASR-85-033 identified item 85-33-1 which identified that I@C had not properly complied with the station verification policy 6-84.
This finding led to revisions of the station policy.
No unacceptable conditions were noted.
I(
4.0 Plant Tours The inspector made several tours of the facility during the course of the inspection including the reactor building, turbine building, control structure and control room.
No unacceptable conditions were noted(
5.0 Exit Interview An exit meeting was held on April 26, 1985 to di scuss the inspection findings as detailed in this report (see paragraph one for attendee's).
At no time during the inspection did the inspector provide written t
inspection findings to the licensee.
At the exit, the licensee didl not identify any proprietary material that, was contained within the scope of the inspection.