IR 05000334/2015008

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Problem Identification and Resolution Inspection Report 05000334/2015008 and 05000412/2015008
ML15201A478
Person / Time
Site: Beaver Valley  FirstEnergy icon.png
Issue date: 07/20/2015
From: Silas Kennedy
NRC/RGN-I/DRP/PB6
To: Emily Larson
FirstEnergy Nuclear Operating Co
KENNEDY, SR
References
IR 2015008
Download: ML15201A478 (18)


Text

UNITED STATES NUCLEAR REGULATORY COMMISSION

REGION I

2100 RENAISSANCE BLVD., SUITE 100 KING OF PRUSSIA, PA 19406-2713 July 20, 2015 Mr. Eric Larson Site Vice President FirstEnergy Nuclear Operating Company Beaver Valley Power Station P.O. Box 4 Shippingport, PA 15077-0004 SUBJECT: BEAVER VALLEY POWER STATION - PROBLEM IDENTIFICATION AND RESOLUTION INSPECTION REPORT 05000334/2015008 AND 05000412/2015008

Dear Mr. Larson:

On June 25, 2015, the United States Nuclear Regulatory Commission (NRC) completed an inspection at your Beaver Valley Power Station, Units 1 and 2. The enclosed report documents the inspection results, which were discussed on June 25, 2015, with you, and other members of your staff.

This inspection examined activities conducted under your license as they relate to identification and resolution of problems and compliance with the Commissions rules and regulations and conditions of your license. Within these areas, the inspection involved examination of selected procedures and representative records, observations of activities, and interviews with personnel.

Based on the samples selected for review, the inspectors concluded that FirstEnergy Nuclear Operating Company (FENOC) was generally effective in identifying, evaluating, and resolving problems. FENOC personnel identified problems and entered them into the corrective action program at a low threshold. FENOC prioritized and evaluated issues commensurate with the safety significance of the problems and corrective actions were generally implemented in a timely manner.

If you disagree with the cross-cutting aspect assigned to the finding in this report, you should provide a response, within 30 days of the date of this inspection report, with the basis for your disagreement, to the Regional Administrator, Region I, and the NRC Resident Inspector at Beaver Valley Power Station. In accordance with 10 CFR 2.390 of the NRCs Rules of Practice, a copy of this letter, its enclosure, and your response (if any) will be available electronically for public inspection in the NRC Public Document Room or from the Publicly Available Records (PARS) component of the NRCs document system (ADAMS). ADAMS is accessible from the NRC website at http://www.nrc.gov/reading-rm/adams.html (the Public Electronic Reading Room).

Sincerely,

/RA/

Silas R. Kennedy, Chief Reactor Projects Branch 6 Division of Reactor Projects Docket Nos. 50-334, 50-412 License Nos. DPR-66, NPF-73

Enclosure:

Inspection Report 05000334/2015008 and 05000412/2015008 w/Attachment: Supplementary Information

REGION I==

Docket Nos.: 50-334, 50-412 License Nos.: DPR-66, NPF-73 Report Nos.: 05000334/2015008 and 05000412/2015008 Licensee: FirstEnergy Nuclear Operating Company (FENOC)

Facility: Beaver Valley Power Station Units 1 and 2 Location: Shippingport, PA 15077 Dates: June 8, 2015 to June 25, 2015 Team Leader: S. Shaffer, Senior Project Engineer Inspectors: B. Reyes, Resident Inspector B. Pinson, Project Engineer S. Horvitz, Project Engineer Approved by: Silas R. Kennedy, Chief Reactor Projects Branch 6 Division of Reactor Projects Enclosure

SUMMARY

IR 05000334/2015008 and 05000412/2015008; June 8 to 25, 2015, Beaver Valley Power

Station Units 1 and 2, Biennial Baseline Inspection of Problem Identification and Resolution.

The inspectors identified one finding in the area of effectiveness of problem identification.

This NRC team inspection was performed by three regional inspectors and one resident inspector. The inspectors identified one finding of very low safety significance (Green) during this inspection. The significance of most findings is indicated by their color (i.e., greater than Green, or Green, White, Yellow, Red) and determined using Inspection Manual Chapter (IMC)0609, Significance Determination Process, dated June 2, 2011. Cross-cutting aspects are determined using IMC 0310, Components Within Cross-Cutting Areas, dated December 4, 2014. All violations of NRC requirements are dispositioned in accordance with the NRCs Enforcement Policy, dated June 7, 2012. The NRCs program for overseeing the safe operation of commercial nuclear power reactors is described in NUREG-1649, Reactor Oversight Process, Revision 5.

Problem Identification and Resolution The inspectors concluded that FENOC was generally effective in identifying, evaluating, and resolving problems. FENOC personnel identified problems, entered them into the corrective action program at a low threshold, and prioritized issues commensurate with their safety significance. In most cases, FENOC appropriately screened issues for operability and reportability, and performed causal analyses that appropriately considered extent of condition, generic issues, and previous occurrences. The inspectors also determined that FENOC typically implemented corrective actions to address the problems identified in the corrective action program in a timely manner.

The inspectors concluded that, in general, FENOC adequately identified, reviewed, and applied relevant industry operating experience to Beaver Valley Power Station operations. In addition, based on those items selected for review, the inspectors determined that FENOCs self-assessments and audits were thorough.

Based on the interviews the inspectors conducted over the course of the inspection, observations of plant activities; and reviews of individual corrective action program and employee concerns program issues; the inspectors did not identify any indications that site personnel were unwilling to raise safety issues nor did they identify any conditions that could have had a negative impact on the sites safety conscious work environment.

Cornerstone: Initiating Events

Green.

A Green self-revealing finding of NOP-LP-2001, Corrective Action Program, was identified after FENOC failed to generate a condition report for a condition adverse to quality. Specifically, FENOC did not initiate a condition report when a lifted lead was identified during preventative maintenance and installation of the Unit 1 main transformer.

As a result, corrective actions were not taken and this led to an unplanned downpower from 100 percent to 15 percent reactor power on January 31, 2014.

The performance deficiency was more-than-minor because it was associated with the Equipment Performance attribute of the Initiating Events cornerstone, and adversely affected the cornerstone objective of limiting the likelihood of events that upset plant stability and challenge critical safety functions during shutdown as well as power operations. This finding was determined to be of very low safety significance (Green), because it did not cause a reactor trip and the loss of mitigation equipment. This finding has a cross-cutting aspect in the area of Human Performance, Field Presence, because FENOC failed to ensure supervisory and management oversight of work activities, including contractors and supplemental personnel [H.2]. (Section 4OA2)

REPORT DETAILS

OTHER ACTIVITIES (OA)

4OA2 Problem Identification and Resolution

This inspection constitutes one biennial sample of problem identification and resolution as defined by Inspection Procedure 71152. All documents reviewed during this inspection are listed in the Attachment to this report.

.1 Assessment of Corrective Action Program Effectiveness

a. Inspection Scope

The inspectors reviewed the procedures that described FENOCs corrective action program at Beaver Valley Power Station. To assess the effectiveness of the corrective action program, the inspectors reviewed performance in three primary areas: problem identification, prioritization and evaluation of issues, and corrective action implementation. The inspectors compared performance in these areas to the requirements and standards contained in 10 CFR 50, Appendix B, Criterion XVI, Corrective Action, and FENOC procedure NOP-LP-2001, Corrective Action Program, Revision 35. For each of these areas, the inspectors considered risk insights from the stations risk analysis and reviewed condition reports selected across the seven cornerstones of safety in the NRCs Reactor Oversight Process. Additionally, the inspectors attended multiple Management Ownership and Alignment meetings; Management Review Committee meetings; and Corrective Action Review Board meetings. The inspectors selected items from the following functional areas for review:

engineering, operations, maintenance, emergency preparedness, radiation protection, chemistry, physical security, and oversight programs.

(1) Effectiveness of Problem Identification In addition to the items described above, the inspectors reviewed system health reports, a sample of completed corrective and preventative maintenance work orders; completed surveillance test procedures; operator logs; and periodic trend reports. The inspectors also completed field walkdowns of various systems on site, such as the intake structure, emergency diesel generator, and auxiliary building. Additionally, the inspectors reviewed a sample of condition reports written to document issues identified through internal self-assessments, audits, emergency preparedness drills, and the operating experience program. The inspectors completed this review to verify that FENOC entered conditions adverse to quality into their corrective action program as appropriate.
(2) Effectiveness of Prioritization and Evaluation of Issues The inspectors reviewed the evaluation and prioritization of a sample of condition reports issued since the last NRC biennial Problem Identification and Resolution inspection completed in December 2013. The inspectors also reviewed condition reports that were assigned lower levels of significance that did not include formal cause evaluations to ensure that they were properly classified. The inspectors review included the appropriateness of the assigned significance, the scope and depth of the causal analysis, and the timeliness of resolution. The inspectors assessed whether the evaluations identified likely causes for the issues and developed appropriate corrective actions to address the identified causes. Further, the inspectors reviewed equipment operability determinations, reportability assessments, and extent-of-condition reviews for selected problems to verify these processes adequately addressed equipment operability, reporting of issues to the NRC, and the extent of the issues.
(3) Effectiveness of Corrective Actions The inspectors reviewed FENOCs completed corrective actions through documentation review and, in some cases, field walkdowns to determine whether the actions addressed the identified causes of the problems. The inspectors also reviewed condition reports for adverse trends and repetitive problems to determine whether corrective actions were effective in addressing the broader issues. The inspectors reviewed FENOCs timeliness in implementing corrective actions and effectiveness in precluding recurrence for significant conditions adverse to quality. The inspectors also reviewed a sample of condition reports associated with selected non-cited violations and findings to verify that FENOC personnel properly evaluated and resolved these issues. In addition, the inspectors expanded the corrective action review to five years to evaluate FENOC actions related to the main transformer and switchyard.

b.

Assessment

(1) Effectiveness of Problem Identification Based on the selected samples, plant walkdowns, and interviews of site personnel in multiple functional areas, the inspectors determined that FENOC identified problems and entered them into the corrective action program at a low threshold. FENOC staff at Beaver Valley Power Station initiated approximately 10,000 condition reports between January 2013 and May 2015. The inspectors observed supervisors at the Management Ownership and Alignment meetings; Management Review Committee meetings; and Corrective Action Review Board meetings appropriately questioning and challenging condition reports to ensure clarification of the issues. Based on the samples reviewed, the inspectors determined that FENOC trended equipment and programmatic issues, and appropriately identified problems in condition reports. The inspectors verified that conditions adverse to quality identified through this review were entered into the corrective action program as appropriate. Additionally, inspectors concluded that personnel were identifying trends at low levels. In general, inspectors did not identify any issues or concerns that had not been appropriately entered into the corrective action program for evaluation and resolution. In response to several questions and minor equipment observations identified by the inspectors during plant walkdowns, FENOC personnel promptly initiated condition reports and/or took immediate action to address the issues.

Additionally, the inspectors identified one example of more than minor significance where FENOC personnel were not effective in identifying problems. This finding is documented in Section 4OA2.1.c.

(2) Effectiveness of Prioritization and Evaluation of Issues The inspectors determined that, in general, FENOC appropriately prioritized and evaluated issues commensurate with the safety significance of the identified problem.

FENOC screened condition reports for operability and reportability, categorized the condition reports by significance, and assigned actions to the appropriate department for evaluation and resolution. The condition report screening process considered human performance issues, radiological safety concerns, repetitiveness, adverse trends, and potential impact on the safety conscious work environment.

Based on the sample of condition reports reviewed, the inspectors noted that the guidance provided by FENOC corrective action program implementing procedures appeared sufficient to ensure consistency in categorization of issues. Operability and reportability determinations were generally performed when conditions warranted and in most cases, the evaluations supported the conclusion. Causal analyses appropriately considered the extent of condition or problem, generic issues, and previous occurrences of the issue.

(3) Effectiveness of Corrective Actions The inspectors concluded that corrective actions for identified deficiencies were generally timely and adequately implemented. For significant conditions adverse to quality, FENOC identified actions to prevent recurrence. The inspectors concluded that corrective actions to address the sample of NRC non-cited violations and findings since the last problem identification and resolution inspection were timely and effective.

c. Findings

Introduction.

A Green self-revealing finding of NOP-LP-2001, Corrective Action Program, was identified after FENOC failed to generate a condition report (CR) for a condition adverse to quality. Specifically, FENOC did not initiate a condition report when a lifted lead was identified during preventative maintenance and installation of the Unit 1 main transformer. As a result, corrective actions were not taken and this led to an unplanned downpower from 100 percent to 15 percent reactor power.

Description.

On January 30, 2014, while performing a startup following a forced outage, Unit 1 received annunciators Main Transformer Cooling Trouble or DC Preferred Source Loss and Main Transformer Oil Flow Low and dispatched operators to investigate. FENOCs troubleshooting efforts revealed that main transformer temperature control winding temperature was out-of-service due to a suspected wiring issue. Operations discussed taking manual control of transformer cooling if established limits were reached and implemented a temporary log to monitor transformer temperatures more frequently. On January 31, 2014, Unit 1 was operating at 100 percent power when an engineer performing a field walkdown discovered that the main transformer temperature controller (TTC), which provides control for transformer cooling stages, was not functioning as expected. The TTC outer display was reading zero amps, which indicates that it is not receiving power, and transformer oil and winding temperatures were not being calculated. Stage 3 cooling, which relies solely on winding temperature, will not automatically start if there is no power going to the TTC. Further inspection revealed that current transformer high voltage A phase #5 (CT-HA.5), which provides power to the TTC, had a lifted lead (wire W/305) on the secondary circuit and was therefore open-circuited and unavailable. After troubleshooting, FENOC made the decision to downpower Unit 1 to 15 percent reactor power to remove the main generator from service and land wire W/305 on the main transformer.

Current transformers (CTs) are instrument transformers that are used to supply a reduced value of current to meters, protective relays, and other instruments. CTs provide isolation from the high voltage primary, permit grounding of the secondary for safety, and step-down the magnitude of the measured current to a value that can be safely handled by the instruments. The transformer CT lead connections are made in the transformer control panel on shorting terminal blocks. When current is passed through the primary of a CT, an electromagnetic field (EMF) is induced in the CTs secondary winding causing current to flow. When the CT secondary circuit is open-circuited, no current flows and the EMF builds to a very high level. When this occurs the CT acts as a step-up transformer resulting in a high voltage being developed across the secondary winding of the CT. This high secondary voltage could lead to significant damage to the panel or the transformer.

The inspectors reviewed FENOCs root cause analysis of this event and determined that FENOC missed several opportunities to generate a condition report for the lifted wire W/305 and enter this issue into their corrective action program (CAP). Wire W/305 was observed lifted on two occasions during preventative maintenance in work orders 200395819 and 200518671, which were worked on August 23, 2011, and August 25, 2013, respectively. In both cases no CR was initiated and station transformer drawings were not updated to reflect the as-found field configuration. General Electric (GE) was contracted to perform inspections and testing while ASEA Brown Boveri (ABB) was to provide technical support and quality control during installation of the main transformer on Unit 1. On January 22, 2014, while performing CT ratio and polarity checks, a GE contractor identified wire W/305 was lifted. The GE contractor notified a FENOC electrician that wire W/305 was lifted; however, a CR was not generated. An ABB contractor also identified that wire W/305 was not landed while performing a warranty inspection on January 29, 2014; however, the contractor assumed that the wire would be landed and therefore did not inform FENOC. In each of these instances, no attempt was made to restore the wire to its proper configuration. Consequently, the main transformer was installed with wire W/305 lifted, which resulted in a CT open secondary circuit; stage 3 transformer cooling being unavailable due to the TTC not having power; and ultimately, an unplanned downpower to prevent transformer damage.

The inspectors reviewed the requirements of NOP-LP-2001, Corrective Action Program. NOP-LP-2001, step 4.1.1.1 states, contractors working under the FENOC quality program shall initiate CRs in accordance with this procedure. Additionally, step 4.1.2 states that all adverse conditions shall be entered in the CR process. Step 3.1 defines an adverse condition as any event, defect, characteristic, state or activity that prohibits or detracts from safe, efficient nuclear plant operation or a condition that could credibly impact nuclear safety, personnel safety, plant reliability or compliance with federal, state, or local regulations. The inspectors determined that FENOC failed to meet the requirements of NOP-LP-2001 when a CR was not initiated upon identifying that wire W/305 was lifted during preventative maintenance and installation of the main transformer.

Analysis.

The inspectors determined that failure to initiate a CR upon identification of an adverse condition, in accordance with NOP-LP-2001, was a performance deficiency that was within the ability of FENOC to foresee and correct, and therefore should have been prevented. The performance deficiency was more-than-minor because it was associated with the Equipment Performance attribute of the Initiating Events cornerstone, and adversely affected the cornerstone objective of limiting the likelihood of events that upset plant stability and challenge critical safety functions during shutdown as well as power operations. Specifically, FENOC failed to initiate a CR upon identification of a lifted lead on the Unit 1 main transformer during preventative maintenance and installation. This led to an unplanned downpower from 100 percent to 15 percent reactor power, thus upsetting plant stability.

The inspectors evaluated this finding using IMC 0609, Attachment 4, Initial Characterization of Findings, issued June 19, 2012, and IMC 0609, Appendix A, The Significance Determination Process (SDP) for Findings At-Power, issued June 19, 2012. Using IMC 0609, Appendix A, Exhibit 1, Initiating Events Screening Questions, this finding was determined to be of very low safety significance (Green), because it did not cause a reactor trip and the loss of mitigation equipment.

This finding has a cross-cutting aspect in the area of Human Performance, Field Presence, because FENOC failed to ensure supervisory and management oversight of work activities, including contractors and supplemental personnel. Specifically, FENOC did not ensure that supervisory and management oversight of contractors during the Unit 1 main transformer installation was adequate, and as a result, corrective actions were not taken when an adverse condition was identified, which led to an unplanned downpower. [H.2]

Enforcement.

This finding is against NOP-LP-2001 for FENOCs failure to initiate a CR when an adverse condition was identified during preventative maintenance and installation of the Unit 1 main transformer. NOP-LP-2001 is not a procedure recommended by Regulatory Guide 1.33, Quality Assurance Program Requirements (Operation), Revision 2, and the work being performed was not on a safety-related system. Therefore, this finding does not involve enforcement action because no violation of a regulatory requirement was identified. The issue was entered into FENOCs CAP as CR 2015-08947. Because this finding did not involve a violation and was of very low safety significance (Green), it is identified as a FIN. (FIN 05000334/2015008-01, Failure to Initiate a Condition Report for an Adverse Condition)

.2 Assessment of the Use of Operating Experience

a. Inspection Scope

The inspectors reviewed a sample of condition reports associated with review of industry operating experience to determine whether FENOC appropriately evaluated the operating experience information for applicability to Beaver Valley Power Station and had taken appropriate actions, when warranted. The inspectors also reviewed evaluations of operating experience documents associated with a sample of NRC generic communications to ensure that FENOC adequately considered the underlying problems associated with the issues for resolution via their corrective action program.

In addition, the inspectors observed various plant activities to determine if the station considered industry operating experience during the performance of routine and infrequently performed activities.

b. Assessment The inspectors determined that FENOC appropriately considered industry operating experience information for applicability, and used the information for corrective and preventive actions to identify and prevent similar issues when appropriate. The inspectors determined that operating experience was appropriately applied and lessons learned were communicated and incorporated into plant operations and procedures when applicable. The inspectors also observed that industry operating experience was routinely discussed and considered during the conduct of Management Ownership and Alignment meetings and pre-job briefs.

c. Findings

No findings were identified.

.3 Assessment of Self-Assessments and Audits

a. Inspection Scope

The inspectors reviewed a sample of audits, including the most recent audit of the corrective action program, departmental self-assessments, and assessments performed by independent organizations. Inspectors performed these reviews to determine if FENOC entered problems identified through these assessments into the corrective action program, when appropriate, and whether FENOC initiated corrective actions to address identified deficiencies. The inspectors evaluated the effectiveness of the audits and assessments by comparing audit and assessment results against self-revealing and NRC-identified observations made during the inspection.

b. Assessment The inspectors concluded that self-assessments, audits, and other internal FENOC assessments were generally critical, thorough, and effective in identifying issues. The inspectors observed that FENOC personnel knowledgeable in the subject completed these audits and self-assessments in a methodical manner. FENOC completed these audits and self-assessments to a sufficient depth to identify issues which were then entered into the corrective action program for evaluation. In general, the station implemented corrective actions associated with the identified issues commensurate with their safety significance.

c. Findings

No findings were identified.

.4 Assessment of Safety Conscious Work Environment

a. Inspection Scope

During interviews with station personnel, the inspectors assessed the safety conscious work environment at Beaver Valley Power Station. Specifically, the inspectors interviewed personnel to determine whether they were hesitant to raise safety concerns to their management and/or the NRC. The inspectors also interviewed the station Employee Concerns Program coordinator to determine what actions are implemented to ensure employees were aware of the program and its availability with regards to raising safety concerns. The inspectors reviewed the Employee Concerns Program files to ensure that FENOC entered issues into the corrective action program when appropriate.

b. Assessment During interviews, Beaver Valley Power Station staff expressed a willingness to use the corrective action program to identify plant issues and deficiencies and stated that they were willing to raise safety issues. The inspectors noted that no one interviewed stated that they personally experienced or were aware of a situation in which an individual had been retaliated against for raising a safety issue. All persons interviewed demonstrated an adequate knowledge of the corrective action program and the Employee Concerns Program. Based on these limited interviews, the inspectors concluded that there was no evidence of an unacceptable safety conscious work environment and no significant challenges to the free flow of information.

c. Findings

No findings were identified.

4OA6 Meetings, Including Exit

On June 25, 2015, the inspectors presented the inspection results to Mr. Eric Larson, Site Vice President and other members of the Beaver Valley Power Station staff. The inspectors verified that no proprietary information was retained by the inspectors or documented in this report.

ATTACHMENT:

SUPPLEMENTARY INFORMATION

KEY POINTS OF CONTACT

Licensee Personnel

E. Larson, Site Vice President
C. McFeaters, Director of Site Operations
S. Baldwin, Mechanical Maintenance Supervisor
D. Batina, Employee Concerns Program
C. Battistone, Oversight Assessor
W. Cohen, Regulatory Compliance Manager
A. Crotty, Electrical System Engineering Supervisor
T. Delmonico, Mechanical Maintenance Supervisor
J. Fontaine, RP Supervisor of ALARA
J. Gibbs, Mechanical Maintenance Supervisor
B. Haney, Supervisor
R. Hepp, Nuclear Engineer
D. Huff, Site Maintenance Manager
M. Jansto, System Engineer
D. Jones, In-Service Testing Coordinator
E. Loehlein, Site Operations Manager
M. Mayer, Configuration Control Engineering Specialist
T. Migdal, Operations Support Superintendent
A. Ray, Field Operations Supervisor
D. Salera, Manager Site Chemistry
S. Sawtschenko, Emergency Response Manager
B. Sepelak, Compliance Supervisor
J. Sharpless, Security Support Supervisor
K. Sloan, Shift Manager
T. Steed, Director Performance Improvement
M. Testa, Consulting Engineer
E. Thomas, Compliance Supervisor
D. Wacker, Regulatory Compliance Engineer
D. Wilson, Air-Operated Valve Engineer
B. Winters, Staff Nuclear Specialist

LIST OF ITEMS OPENED, CLOSED, DISCUSSED, AND UPDATED

Opened and Closed

05000334/2015008-01 FIN Failure to Initiate a Condition Report for an Adverse Condition

LIST OF DOCUMENTS REVIEWED