IR 05000324/1978030
| ML19263B463 | |
| Person / Time | |
|---|---|
| Site: | Brunswick |
| Issue date: | 12/05/1978 |
| From: | Dance H, Riley B, Taylor P NRC OFFICE OF INSPECTION & ENFORCEMENT (IE REGION II) |
| To: | |
| Shared Package | |
| ML19263B442 | List: |
| References | |
| 50-324-78-30, 50-325-78-30, NUDOCS 7901180277 | |
| Download: ML19263B463 (4) | |
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pnstaGo UNITED STATES N'1 CLEAR REGULATORY COMMISSION
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Report Nos. : 50-325/78-30 and 50-324/78-30 Docket Nos. : 50-325 and 50-324 License Nos. : DPR-71 and DPR-62
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Licensee: Carolina Power and Light Company 336 Fayetteville Street Raleigh, North Carolina 27602 Facility Name: Brunswick I and 2 Inspection at: Southport, North Carolina Inspection conducted: November 15-17, 1978 Inspectors:
B. W. Riley P.
Taylor Approved by:
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H. C. Dance, Chief Date Reactor Projects Section No. 1 Reactor Operations and Nuclear Support Branch Inspection Summary Inspection on November 15-17, 1978 (Report Nos. 50-325/78-30 and 50-324/78-3 Areas Inspected:
Routine, unannounced inspection of plant operations, follow-up on IE Bulletins and Circulars, review implementation of recent Technical Specification changes, inspection of new spent fuel racks, observe temporary liquid radwaste processing set up and plant tour. The inspection involved 38 inspector hours on-site by two NRC inspectors.
Results: Of the six areas inspectel., no items of noncompliance or deviations were found in five areas; one apparent item of noncompliance was found in one area (infraction - failure to promptly and effectively correct conditions adverse to quality (325/78-30-01, 324/78-30-01)).
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RII Report Nos. 50-325/78-30 and 50-324/78-30 I-1 DETAILS I Prepared by:
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. / 2.[f[g B.' W. Riley7 Reactor Wspector
/ Date Reactor Projects Section No. 1 Reactor Operations and Nuclear Su port Branch
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P. A. Taylof, Reactor Inspector Date Nuclear Support Section No. 2 Reactor Operations and Nuclear Support Branch Dates of Inspectio : Noverper 15-17, 1978 Reviewed by:
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H. ' C. Dance, Chief Dtte '
Reactor Projects Section No.1 Reactor Operations and Nuclear Support Branch 1.
Persons Contacted
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C. Tollison, Jr., Plant Manager
- W. M. Tucker, Superintendent, Technical and Administration
- S. E. Thorndyke, Operating Supervisor W. L. Triplett, Engineering Supervisor
- L. A. Rogers, Regulatory Coordinator
- J. L. Kiser, Radiation Control Engineer
- J. Cribb, Quality Assurance Specialist R. Porterfield, Engineer L. Trip, Radiation Control and Test Supervisor Several Shif t Specialists, Shif t Foreman, and Control Operators
- Denotes those present at the Exit Interview.
2.
Licensee Action on Previous Inspection Findings Not Inspected.
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Unresolved Items No new unresolved items were identified during this inspectio.
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RII Report Nos. 50-325/78-30 and 50-324/78-30 I-2 4.
Exit Interview The inspector met with licensee representatives (denoted in paragraph 1)
at the conclusion of the inspection on November 17, 1978. The inspectors summarized the purpose and scope of the inspection and the findings.
With regard to the noncompliance item concerning corrective action on conditions adverse to quality, the inspector identified this item as an apparent item of noncompliance but did not indicate a caterory level. On November 29, 1978 by telephone the inspector informed the Acting Plant Manager that this was an item of noncompliance and had been catergorized as an infraction.
5.
Plant Operations The inspector reviewed a recent Technical Specification change concern-ing Torus to reactor building vacuum relief vent lines, to verify adequate implementation.
The affected operating equipmeat had been promptly realigned and appropriate plant procedure changes were properly made. The inspector suggested and the licensee agreed in future to accomplish procedure changes in a more timely manner. The inspector reviewed and discussed with operating and management personnel the arrangements of temporary equipment to process liquid radwaste. The inspector determined that the licensee had reviewed and evaluated the potential paths for liquid leakage and had taken certain preventative acasures. The inspector suggested and the licensee agreed that further considerations be given to increased locatione and frequencies of survey points for and of potential radwaste.iquid leakage paths associated with the temporary process setup.
The inspector discussed with plant manage. t the recent history of reactor coolant chemistry conductivity an both units and problems and corrective programs underway involving reactor water cleanup pumps and main turbine condenser leakage.
The inspector reviewed recent history of liquid leakage within Unit 1
} rimary containment and noted no unexplained adverse changes had cecurred.
Within the areas of plant operations noted above, no items of noncom-pliance or deviations were identified.
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IE Circular and Bulletin Follow Up The inspector reviewed the status of outstanding circulars and bulletins and reviewed the licensee actions. As a result of these reviews the following two circulars are considered closed item.'
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t RII Report Nos. 50-325/78-30 and 50-324/78-30 I-3 IEC 78-07 Damaged Components of a Bergen-Patterson Series 25000 Hydraulic Test Stand IEC 78-15 Tilting Disc Check Valves Fail to Close with Gravity in Vertical Positon.
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Spent Fuel Storage Modification The inspector reviewed on a sample basis procurement and receipt inspection documents on new spent fuel racks to verify consistency with licensee comritments.
No items of noncompliance were identified.
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Plant Tour The inspectors toured various areas of the plant and yard to inspect general conditions.
Extensive modification work was observed in progress thoughout the plant concerning security systems and additions to fire detection and protection systems.
The diesel generator, radwaste, control room, and auxiliary heating boiler buildings of both units were toured.
In touring the outside yard area of plant the inspectors observed storage of spent fuel baskets in an unprotected manner.
Further investigations and discussion with licensee personnel, revealed the unprotected manner of storage had been identified by the plant Quality Assurance surveillance reports on three separate occasions, (January, Hay, and July 1978) but no response from plant occurred until August 15, 1978.
On September 23, 1978 a Corporate Quality Assurance audit report recognized that spent fuel baskets had not been protected in storage and that three separate plant QA reports cited this. The adverse conditions of storage continued until November 16, 1978 when licensee action moved the baskets indoors. The history which occurred indicates a failure to comply with regulatory and licensee requirements (Criterion XVI, Appendix B, 10 CFR 50; Section 11.2.11, Part 2 of Carolina Power and Light Corporate Quality Assurance Program; and purchase specification 952-028-216-1) to establish and carry out seasures to promptly and effectively correct conditions adverse to quality. This failure is an item of noncompliance and is classified as an inf raction (325/78-30-01, 324/78-30-01).